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Category:CORRESPONDENCE-LETTERS
MONTHYEARML17241A5001999-10-21021 October 1999 Forwards Rev 3 to Emergency Response Data Sys (ERDS) Data Point Library for St Lucie Unit 1.Rev Provides Replacement Pages & Follows Format Recommended by NUREG 1394, ERDS Implementation, Rev 1,App C ML17309A9981999-10-19019 October 1999 Forwards Revised Epips,Including Rev 3 to EPIP-10 & Rev 25 to HP-202.EPIP-10 Added Onsite Monitoring Points,Made Administrative Changes & Incorporated New Attachments & HP-202 Added Red Team Survey Points ML20217F6171999-10-0808 October 1999 Forwards Insp Repts 50-335/99-11 & 50-389/99-11 on 990827 & 990907-09.No Violations Identified.Matl Encl Contained Safeguards Info as Defined by 10CFR73.21 & Disclosed to Unauthorized Individuals Prohibited by Section 147 of AEA ML17241A4811999-10-0101 October 1999 Reports Number of Tubes Plugged During Unit 1 Refueling Outage SL1-16,per TS 4.4.5.5.a ML20212M1601999-09-28028 September 1999 Refers to 990908 Engineering Meeting Conducted at NRC Region II to Discuss Engineering Issues at Lucie & Turkey Point Facilities.List of Attendees & Copy of Presentation Handout Encl ML17241A4701999-09-25025 September 1999 Forwards Info Requested by NRC Staff During 990916 Telcon to Complete Staff Review of Request for risk-informed Extension of Action Completion/Aot Specified for Inoperable Train of LPSI Sys at Plant ML17241A4721999-09-24024 September 1999 Forwards Rev 1 to Plant Change/Mod (PCM) 99016 to St Lucie Unit 1,Cycle 16 COLR, IAW TS 6.9.1.11.d.Refueling Overhaul Activities Are Currently in Progress & Reactor Operations for Cycle 16 Are Scheduled to Commence in Oct 1999 ML17241A4681999-09-22022 September 1999 Requests Restriction Be Added to Senior Operator License SOP-21093 for TE Bolander.Nrc Forms 369,encl.Encl Withheld Per 10CFR2.790(a)(6) ML17241A4671999-09-20020 September 1999 Forwards Completed NRC Form 536, Operator Licensing Exam Data, for St Lucie Units 1 & 2,as Requested in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams. ML17241A4581999-09-13013 September 1999 Forwards Info Requested by NRC Staff During 990630 & 0816 Telcons,To Complete Review of Proposed License Amend for Fuel Reload Process Improvement Program ML17241A4531999-08-31031 August 1999 Informs That No Candidates from St Lucie Plant Will Be Participating in PWR Gfes Being Administered on 991006 ML17241A4521999-08-31031 August 1999 Withdraws Relief Request 16 & Suppl Relief Request 15 with Info Requested During 990526 Telephone Conference Re ISI Insp Plan,Third 10-yr Interval ML17241A4501999-08-26026 August 1999 Informs That FPL Has Reviewed Reactor Vessel Integrity Database,Called RVID2,re Closure of GL 92-01,rev 1,suppl 1. Requested Corrections & Marked Up Pages from Rvid 2 Database Summary Repts That Correspond to Comments,Attached ML17241A4371999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data for six- Month Period Ending 990630,per 10CFR26.71(d) ML17241A4461999-08-11011 August 1999 Requests That W Rept Entitled, Evaluation of Turbine Missile Ejection Probability Resulting from Extending Test Interval of Interceptor & Reheat Stop Valves at St Lucie Units 1 & 2, Be Withheld from Public Disclosure L-99-171, Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3)1999-07-29029 July 1999 Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3) ML17309A9911999-07-26026 July 1999 Forwards Revised EPIPs & Revised Procedures That Implement Emergency Plan as Listed.Procedures Provides Instruction for Operational Support Ctr (OSC) Chemistry Supervisor to Establish Remote Labs at Locations Specified ML17241A4471999-07-22022 July 1999 Requests That Rev 1 to WCAP-14732 & Rev 1,Add 1 to WCAP-14732 Be Withheld from Public Disclosure ML17241A4221999-07-22022 July 1999 Forwards List of Proposed Licensing Actions for St Lucie Units 1 & 2,planned During Fys 2000 & 2001,in Response to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates. ML17241A4151999-07-22022 July 1999 Forwards Revised Relief Request 25 for Second 10-yr ISI Interval for Unit 2 ML17241A4101999-07-16016 July 1999 Forwards FP&L Supplemental Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants ML17309A9881999-07-0707 July 1999 Forwards Rev 5 to EPIP-03, Emergency Response Organization Notification/Staff Augmentation. Rev 5 to EPIP-03 Was Revised to Transfer EP Responsibilities from Training Manager to Protection Svcs Manager ML20209F1541999-07-0606 July 1999 Informs That NRC in Process of Conducting Operational Safeguards Response Evaluations at Nuclear Power Reactors. Plant Chosen for Such Review Scheduled for Wk of 990823-26 ML17241A4011999-06-30030 June 1999 Forwards Info Copy of Florida Wastewater Permit (FL0002208) (Formerly NPDES Permit) Mod,Which Was Issued by Florida Dept of Environ Protection on 990604 ML17241A3971999-06-30030 June 1999 Forwards Suppl Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs, as Requested in 990317 Ltr ML17355A3661999-06-30030 June 1999 Forwards Florida Power & Light Topical QA Rept, Dtd June 1999.Encl I Includes Summary of Changes Made to Topical QA Rept Since 1998 ML17241A3951999-06-29029 June 1999 Provides Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants, Requested Response on Status of Facility Y2K Readiness by 990701.Disclosure Encl ML17241A3731999-06-17017 June 1999 Supplements Relief Requests 4,11 & 13 for Third ten-year ISI Interval with Info Requested During 990526 Telcon.Expedited Review Is Requested by 990730 to Avoid Negatively Impacting Upcoming St Lucie Unit 1 Refueling Outage (SL1-16) ML17241A3641999-06-14014 June 1999 Submits Supplement to Relief Request 24 with Info Requested by Nrc.In Addition Relief Request 24 Is Identical to St Lucie Unit 1 Relief Request 4 for Third ISI Interval Being Supplemented by FPL Ltr L-99-139 ML20195F3871999-06-11011 June 1999 Final Response to FOIA Request for Documents.App a Records Being Withheld in Entirety (Ref FOIA Exemption 5) IA-99-247, Final Response to FOIA Request for Documents.App a Records Being Withheld in Entirety (Ref FOIA Exemption 5)1999-06-11011 June 1999 Final Response to FOIA Request for Documents.App a Records Being Withheld in Entirety (Ref FOIA Exemption 5) L-99-129, Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3)1999-06-0909 June 1999 Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3) ML17241A3561999-06-0707 June 1999 Forwards Rept Containing Brief Description & Summary of SEs for Changes,Tests & Experiments Which Were Approved for Unit 3 During Period of 970526-981209 ML17241A3601999-06-0707 June 1999 Forwards Correction to Annual Radiological Environ Operating Rept for CY98.Util Has Identified Transcription Error on Last Page of Attachment C of Rept,Results from Interlaboratory Comparison Program 1998 ML20195F3941999-05-27027 May 1999 FOIA Request That Memo from J Calvo to Fl Lebdon Re TIA - St Lucie,Unit 1 Environ Qualification of Woodward Governor Controls Be Placed in PDR ML17241A3461999-05-24024 May 1999 Forwards Revised Relief Request 22 to Clarify Several Areas of Relief.Nrc Action Is Requested to Be Complete by Aug 1999 to Support Planning for Spring 2000 Unit 2 Refueling Outage ML17241A3391999-05-20020 May 1999 Forwards Notification of Change to Small Break LOCA ECCS Evaluation Model Used for St Lucie Unit 1.Anomaly Was Discovered & Corrected That Resulted in Reducing Calculated PCT for Limiting SBLOCA by More than 50 F ML17241A3371999-05-20020 May 1999 Forwards Util Suppl to GL 95-07 Response Re pressure-locking & Thermal Binding of safety-related power-operated Gate Valves,In Response to NRC Second RAI Dtd 990225 ML20207C7531999-05-17017 May 1999 Discusses Issue Identified by FPL in Feb 1998 Involving Potential for Fire to Cause Breach of Rc Sys High/Low Pressure Interface Boundary & NRC Decision for Exercise of Enforcement Discretion ML17241A3301999-05-17017 May 1999 Forwards LER 99-004-00 Re as Found Cycle 10 Psv Setpoints Outside TS Limits,Which Occurred on 990415.Root Cause Determination Not Yet Complete.Suppl to Include Root Cause & Corrective Actions Will Be Submitted ML17309A9821999-05-10010 May 1999 Forwards Rev 36 to St Lucie Emergency Plan, Per 10CFR50.54(q).Executive Summary & Summary of Changes Incorporated by Rev,Encl IR 05000335/19980141999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated ML17241A3221999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated ML17229B1071999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept for St Lucie Unit 2. Rept Includes Discussions of 5-inch Barrier Net Maint & Taprogge Condenser Tube Cleaning Sys Ball Loss,As Agreed at First Biennial Sea Turtle Meeting Held on 980120 ML17229B1051999-04-22022 April 1999 Requests That Listed Individuals Be Placed on Official Serve List for Nuclear Matl Safety & Safeguards Info Notices ML17229B1061999-04-21021 April 1999 Notifies NRC of Change in Medical Status of Licensed Operator Pf Farnsworth (Docket 55-21285,license SOP-21094). NRC Form 3996, Medical Exam Certification, Encl.Encl Withheld Per 10CFR2.790(a)(6) ML17309A9851999-04-15015 April 1999 Requests That NRC Review Denial of Appeal from Assessment of Fees Assessed in 981101 Invoice RS0062-99 & Assessment of Fees in Invoice RS0182-99 Which Was Also Denied in 990305 Ltr.Both Invoices Are for Fees Re Inspector GG Warnick ML20205M0431999-04-13013 April 1999 Eighth Partial Response to FOIA Request for Records.App Q & R Records Encl & Being Made Available in PDR ML17229B0951999-04-0808 April 1999 Requests Approval of Encl Revised Relief Request 6,in Response to 990322 Telcon with NRC & 10CFR55.55a(a)(3). Request States That Visual VT-3 Exams Will Be Conducted IAW IWA-2213 & Repairs Will Be IAW Util ASME Section IX Program ML17229B0821999-04-0707 April 1999 Requests Approval of Interim Relief Request 26 Re Repair Requirements for Class 2 ECCS Piping,Per 10CFR50.55a(a)(3) & 50.55a(g)(iii).Alternative Actions Apply Guidance of GLs 91-18 & 90-05 & ASME Code Case N-513.Evaluation,encl 1999-09-28
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17241A5001999-10-21021 October 1999 Forwards Rev 3 to Emergency Response Data Sys (ERDS) Data Point Library for St Lucie Unit 1.Rev Provides Replacement Pages & Follows Format Recommended by NUREG 1394, ERDS Implementation, Rev 1,App C ML17309A9981999-10-19019 October 1999 Forwards Revised Epips,Including Rev 3 to EPIP-10 & Rev 25 to HP-202.EPIP-10 Added Onsite Monitoring Points,Made Administrative Changes & Incorporated New Attachments & HP-202 Added Red Team Survey Points ML17241A4811999-10-0101 October 1999 Reports Number of Tubes Plugged During Unit 1 Refueling Outage SL1-16,per TS 4.4.5.5.a ML17241A4701999-09-25025 September 1999 Forwards Info Requested by NRC Staff During 990916 Telcon to Complete Staff Review of Request for risk-informed Extension of Action Completion/Aot Specified for Inoperable Train of LPSI Sys at Plant ML17241A4721999-09-24024 September 1999 Forwards Rev 1 to Plant Change/Mod (PCM) 99016 to St Lucie Unit 1,Cycle 16 COLR, IAW TS 6.9.1.11.d.Refueling Overhaul Activities Are Currently in Progress & Reactor Operations for Cycle 16 Are Scheduled to Commence in Oct 1999 ML17241A4681999-09-22022 September 1999 Requests Restriction Be Added to Senior Operator License SOP-21093 for TE Bolander.Nrc Forms 369,encl.Encl Withheld Per 10CFR2.790(a)(6) ML17241A4671999-09-20020 September 1999 Forwards Completed NRC Form 536, Operator Licensing Exam Data, for St Lucie Units 1 & 2,as Requested in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams. ML17241A4581999-09-13013 September 1999 Forwards Info Requested by NRC Staff During 990630 & 0816 Telcons,To Complete Review of Proposed License Amend for Fuel Reload Process Improvement Program ML17241A4531999-08-31031 August 1999 Informs That No Candidates from St Lucie Plant Will Be Participating in PWR Gfes Being Administered on 991006 ML17241A4521999-08-31031 August 1999 Withdraws Relief Request 16 & Suppl Relief Request 15 with Info Requested During 990526 Telephone Conference Re ISI Insp Plan,Third 10-yr Interval ML17241A4501999-08-26026 August 1999 Informs That FPL Has Reviewed Reactor Vessel Integrity Database,Called RVID2,re Closure of GL 92-01,rev 1,suppl 1. Requested Corrections & Marked Up Pages from Rvid 2 Database Summary Repts That Correspond to Comments,Attached ML17241A4371999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data for six- Month Period Ending 990630,per 10CFR26.71(d) ML17241A4461999-08-11011 August 1999 Requests That W Rept Entitled, Evaluation of Turbine Missile Ejection Probability Resulting from Extending Test Interval of Interceptor & Reheat Stop Valves at St Lucie Units 1 & 2, Be Withheld from Public Disclosure L-99-171, Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3)1999-07-29029 July 1999 Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3) ML17309A9911999-07-26026 July 1999 Forwards Revised EPIPs & Revised Procedures That Implement Emergency Plan as Listed.Procedures Provides Instruction for Operational Support Ctr (OSC) Chemistry Supervisor to Establish Remote Labs at Locations Specified ML17241A4221999-07-22022 July 1999 Forwards List of Proposed Licensing Actions for St Lucie Units 1 & 2,planned During Fys 2000 & 2001,in Response to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates. ML17241A4471999-07-22022 July 1999 Requests That Rev 1 to WCAP-14732 & Rev 1,Add 1 to WCAP-14732 Be Withheld from Public Disclosure ML17241A4151999-07-22022 July 1999 Forwards Revised Relief Request 25 for Second 10-yr ISI Interval for Unit 2 ML17241A4101999-07-16016 July 1999 Forwards FP&L Supplemental Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants ML17309A9881999-07-0707 July 1999 Forwards Rev 5 to EPIP-03, Emergency Response Organization Notification/Staff Augmentation. Rev 5 to EPIP-03 Was Revised to Transfer EP Responsibilities from Training Manager to Protection Svcs Manager ML17241A4011999-06-30030 June 1999 Forwards Info Copy of Florida Wastewater Permit (FL0002208) (Formerly NPDES Permit) Mod,Which Was Issued by Florida Dept of Environ Protection on 990604 ML17241A3971999-06-30030 June 1999 Forwards Suppl Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs, as Requested in 990317 Ltr ML17355A3661999-06-30030 June 1999 Forwards Florida Power & Light Topical QA Rept, Dtd June 1999.Encl I Includes Summary of Changes Made to Topical QA Rept Since 1998 ML17241A3951999-06-29029 June 1999 Provides Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants, Requested Response on Status of Facility Y2K Readiness by 990701.Disclosure Encl ML17241A3731999-06-17017 June 1999 Supplements Relief Requests 4,11 & 13 for Third ten-year ISI Interval with Info Requested During 990526 Telcon.Expedited Review Is Requested by 990730 to Avoid Negatively Impacting Upcoming St Lucie Unit 1 Refueling Outage (SL1-16) ML17241A3641999-06-14014 June 1999 Submits Supplement to Relief Request 24 with Info Requested by Nrc.In Addition Relief Request 24 Is Identical to St Lucie Unit 1 Relief Request 4 for Third ISI Interval Being Supplemented by FPL Ltr L-99-139 L-99-129, Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3)1999-06-0909 June 1999 Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3) ML17241A3601999-06-0707 June 1999 Forwards Correction to Annual Radiological Environ Operating Rept for CY98.Util Has Identified Transcription Error on Last Page of Attachment C of Rept,Results from Interlaboratory Comparison Program 1998 ML17241A3561999-06-0707 June 1999 Forwards Rept Containing Brief Description & Summary of SEs for Changes,Tests & Experiments Which Were Approved for Unit 3 During Period of 970526-981209 ML20195F3941999-05-27027 May 1999 FOIA Request That Memo from J Calvo to Fl Lebdon Re TIA - St Lucie,Unit 1 Environ Qualification of Woodward Governor Controls Be Placed in PDR ML17241A3461999-05-24024 May 1999 Forwards Revised Relief Request 22 to Clarify Several Areas of Relief.Nrc Action Is Requested to Be Complete by Aug 1999 to Support Planning for Spring 2000 Unit 2 Refueling Outage ML17241A3371999-05-20020 May 1999 Forwards Util Suppl to GL 95-07 Response Re pressure-locking & Thermal Binding of safety-related power-operated Gate Valves,In Response to NRC Second RAI Dtd 990225 ML17241A3391999-05-20020 May 1999 Forwards Notification of Change to Small Break LOCA ECCS Evaluation Model Used for St Lucie Unit 1.Anomaly Was Discovered & Corrected That Resulted in Reducing Calculated PCT for Limiting SBLOCA by More than 50 F ML17241A3301999-05-17017 May 1999 Forwards LER 99-004-00 Re as Found Cycle 10 Psv Setpoints Outside TS Limits,Which Occurred on 990415.Root Cause Determination Not Yet Complete.Suppl to Include Root Cause & Corrective Actions Will Be Submitted ML17309A9821999-05-10010 May 1999 Forwards Rev 36 to St Lucie Emergency Plan, Per 10CFR50.54(q).Executive Summary & Summary of Changes Incorporated by Rev,Encl ML17241A3221999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated IR 05000335/19980141999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated ML17229B1071999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept for St Lucie Unit 2. Rept Includes Discussions of 5-inch Barrier Net Maint & Taprogge Condenser Tube Cleaning Sys Ball Loss,As Agreed at First Biennial Sea Turtle Meeting Held on 980120 ML17229B1051999-04-22022 April 1999 Requests That Listed Individuals Be Placed on Official Serve List for Nuclear Matl Safety & Safeguards Info Notices ML17229B1061999-04-21021 April 1999 Notifies NRC of Change in Medical Status of Licensed Operator Pf Farnsworth (Docket 55-21285,license SOP-21094). NRC Form 3996, Medical Exam Certification, Encl.Encl Withheld Per 10CFR2.790(a)(6) ML17309A9851999-04-15015 April 1999 Requests That NRC Review Denial of Appeal from Assessment of Fees Assessed in 981101 Invoice RS0062-99 & Assessment of Fees in Invoice RS0182-99 Which Was Also Denied in 990305 Ltr.Both Invoices Are for Fees Re Inspector GG Warnick ML17229B0951999-04-0808 April 1999 Requests Approval of Encl Revised Relief Request 6,in Response to 990322 Telcon with NRC & 10CFR55.55a(a)(3). Request States That Visual VT-3 Exams Will Be Conducted IAW IWA-2213 & Repairs Will Be IAW Util ASME Section IX Program ML17229B0821999-04-0707 April 1999 Requests Approval of Interim Relief Request 26 Re Repair Requirements for Class 2 ECCS Piping,Per 10CFR50.55a(a)(3) & 50.55a(g)(iii).Alternative Actions Apply Guidance of GLs 91-18 & 90-05 & ASME Code Case N-513.Evaluation,encl ML17229B0851999-04-0505 April 1999 Requests Approval of Encl Relief Request 25 Which Proposes to Use Alternative Requirements of ASME Code Case N-613 in Lieu of Requirements of ASME Section XI Figures IWB-2500-7(a) & IWB-2500-7(b).Action Requested by Aug 1999 ML17309A9791999-03-31031 March 1999 Forwards Revised EPIPs Including Rev 2 to EPIP-00,rev 2 to EPIP-09,rev 2 to EPIP-10 & Rev 10 to HP-207.Summary of Revs Listed ML17309A9761999-03-23023 March 1999 Forwards Revised Epips,Including Rev 4 to EPIP-03, Er Organization Notification/Staff Augmentation, Rev 3 to EPIP-05, Activation & Operation of OSC & Rev 14 to HP-200, HP Emergency Organization. Changes to Epips,Discussed ML17229B0691999-03-19019 March 1999 Transmits TS Pages Requested by NRC for Use in Issuance of Proposed License Amend Re SFP Storage Capacity,Per Soluble Boron Credit ML17229B0721999-03-16016 March 1999 Requests Approval of Enclosed Relief Requests 23 & 24 Re ISI Plan for Second ten-year Interval.Nrc Action Is Requested to Be Complete by Aug 1999 to Support Planning for Spring 2000 Unit 2 Refueling Outage ML17355A2631999-03-12012 March 1999 Forwards FPL Decommissioning Fund Status Repts for St Lucie, Units 1 & 2 & Turkey Point,Units 3 & 4.Rept for St Lucie, Unit 2 Provides Status of Decommissioning Funds for All Three Owners of That Unit ML17229B0481999-03-10010 March 1999 Informs That Util Delivered Matls Requested in Encl 1 of NRC Ltr by Hand on 990308,as Requested by NRC Ltr Dtd 990218 1999-09-25
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CATEGORY 1 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9801140201 DOC.DATE: 98/01/02
~ ~ NOTARIZED: YES DOCKET FACIL:50-335 St. Lucie Plant, Unit 1, Florida Power Ec Light Co.
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05000335 389 St. Lucie Plant, Unit 2, Florida Power & Light Co. 05000389 AUTH.NAME AUTHOR AFFILIATION PLUNKETT,T.F. ~ Florida
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Power t Light Co.
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RECZP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Responds to violations noted in insp rept 50-335/97-15 &
50-389/97-15.Corrective actions:completed temporary sys alteration that reversed two of three power leads to low speed winding of fan motor at motor control center.
DISTRIBUTION CODE: IE01D COPIES RECEIVED:LTR ENCL SIZE:
TITLE: General (50 Dkt)-Insp Rept/Notice of Violation Response E NOTES:
RECIPIENT COPIES RECIPIENT COPIES ZD CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 PD 1 1 WIENS,L. 1 1 2 2 AEOD/SPD/RAB 1 1 1 1 DEDRO 1 1 1 1 NRR/DRCH/HHFB 1 1 NRR/DRPM/PECB 1 1 NRR/DRPM/PERB 1 1 NUDOCS-ABSTRACT 1 1 OE DIR 1 1 OGC/HDS3 1 1 RGN2 FILE 01 1 1 XTERNAL: LITCO BRYCE,Q' 1 1 NOAC 1 1 D NRC PDR 1 1 NUDOCS FULLTEXT 1 1 0
U NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 19 ENCL 19
Florida Power 5 Light Company. 6351 S. Ocean Drive, Jensen Beach, FL 34957 January 2, 1998 L-97-322 10 CFR $ 2.201 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 Re: St. Lucie Units 1 and 2 Docket Nos. 50-335 and 50-389 Reply to a Notice of Violation NR ecial Ins ection Re ort 97-15 Florida Power and Light Company (FPL) has reviewed the subject Notice of Violation and, pursuant to 10 CFR $ 2.201, the responses to the violations are attached.
FPL acknowledges that the cited violations related to the inoperable containment fan coolers are of significant regulatory concern. As described in the violation response, FPL has taken comprehensive corrective actions to resolve the identified condition, and has reviewed the event for generic implications. In this context, FPL appreciates NRC's recognition of the questioning attitude exhibited by St. Lucie personnel in the identification of the inoperable containment fan cooler and the timely and comprehensive corrective actions taken. FPL is optimistic that the behavior demonstrated by the personnel that identified the fan cooler testing deficiency is indicative of the cultural changes encouraged by St. Lucie management.
Please contact us with questions on the enclosed violation responses.
Very truly yours, Thomas F. Plunkett President Nuclear Division TFP/JAS/EJW Attachment cc: Regional Administrator, USNRC, Region II Senior Resident Inspector, USNRC, St. Lucie Plant 980%140201 980102 PDR ADOCK OS00033S PDR IIIIIIIIIIIII/IIIIIII IIIIIIIII/IIIIIII an FPL Group company
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St. Lucie Units 1 and 2
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Docket Nos. 50-335 and 50-389 L-97-322 Page 2 STATE OF FLORIDA )
) ss.
COUNTY OF PALM BEACH )
Thomas F. Plunkett being first duly sworn, deposes and says:
That he is President, Nuclear Division, of Florida Power & Light Company, the Licensee herein; That he has executed the foregoing document; that the statements made in this document are true and correct to the best of his knowledge, information and belief, and that he is authorized to execute the document on behalf of said Licensee.
Thomas F. Plunkett STATE OF FLORIDA COUNTY OF Sworn to and subscribed before me this' day of by Thomas F. Plunk6tt, who is
/~~M, 1997 rsonally known to me.
+go~~
Name orida pIIY PO i&F'CiALtiOTARY SEAL Oi ~C Oc":nNICn M GALINIS
)l~ i)( 0 OOuueaON RuuOSR IXI COidMSSION EXPIRES Oi: RP SFPT 10,2001 Print, type or stamp Commissioned Name of Notary Public)
L-97-322 Attachment P~g 1
~Viola i o A Technical Specification 3.6.2.1 states that two containment spray trains and two containment cooling trains shall be OPERABLE.
Contrary to the above, between May 16, 1997 and October 8, 1997, while operating in Modes 1, 2, and 3, one Unit 2 containment cooling train was inoperable.
R~g~ny
- 1. FPL concurs with the violation.
- 2. REASON FOR VIOLATION This violation was caused by both: a) personnel error during post maintenance testing activities associated with containment cooling fan 2-HVS-1D; and, b) an inadequate 31 day Technical Specification surveillance procedure. These deficiencies contributed to returning containment cooling fan unit 2-HVS-1D to service when it was unable to perform its emergency mode of operation due to reverse slow speed operation. Causes and corrective actions associated with the above are discussed in FPL's responses to violations B and C, respectively.
The low flow alarm for 2-HVS-1D was not documented during the periodic 18 month test of the engineered safety features because the containment fan cooler unit was out of service during the test. Although the procedural requirements for documenting actions to be taken to resolve annunciators received during the performance of safeguards testing were weak, this test was not a missed opportunity for discovering that 2-HVS-1D was inoperable during the emergency mode of operation.
- 3. CORRECTIVE STEPS TAKEN AND THE RESULTS ACHIEVED FPL entered the applicable Technical Specification ACTION statements when the low flow alarms were received during initial and subsequent containment fan cooler slow speed testing on October 6 and October 7, 1997. The reverse slow speed operation was corrected by implementing a temporary system alteration that reversed two of the three power leads to the low speed winding of the fan motor at the motor control center. This action was completed within the allowed outage time for inoperable containment fan cooler(s). Containment fan cooler unit 2-HVS-1D was returned to service on October 9, 1997, after proper operation of the unit was verified.
L-97-322 Attachment P~ae 2
- 4. CORRECTIVE STEPS TO AVOID FURTHER VIOLATIONS FPL revised surveillance operating procedure 1-0400050, "Periodic Test of the Engineered Safety Features," to enhance the disposition of annunciators that are received during the performance of the Integrated Safeguards Test. This revision includes a new appendix used to track and disposition annunciators that occur during the test. This revision to the Unit 1 procedure was completed on November 18, 1997.
B. The Unit 2 Safeguards procedure, 2-0400050, will be revised to include the new annunciator response appendix prior to performing safeguards testing during the Unit 2 1998 refueling outage (SL2-11).
Full compliance was achieved on October 9, 1997, when containment fan cooler unit 2-HVS-ID was returned to service.
L-97-322 Attachment P~ae 3 VIolation 8 10 CFR 50, Appendix B, Criterion V, Instructions, Procedures and Drawings, requires, in part, that activities affecting quality shall be prescribed by documented procedures of a type appropriate to the circumstances and shall be accomplished in accordance with those procedures.
Maintenance Procedure (MP) 2-0950173, Revision 9, "The Overhaul of Containment Fan Coolers Motors 2HVS-lA, 1B, 1C, 1D (EQ Motors)," Section 9.9, implements the post maintenance checks of the containment fan cooler motors after maintenance. MP 2-0950173 requires the fan to be started in slow and fast speed to verify proper blade rotation in each speed.
Contrary to the above, on May 16, 1997, the licensee failed to perform Section 9.9 of Maintenance Procedure 2-0950173 properly in that containment fan cooler 2-HVS-1D was not started in slow speed and proper blade rotation was not verified.
~Rea on e
- 1. FPL concurs with the violation.
REASON FOR VIOLATION The cause for the violation was personnel error that occurred during the execution of post maintenance testing performed during the last Unit 2 refueling outage. This error resulted in reverse rotation of containment fan cooler 2-HVS-1D. The root cause evaluation concluded that the improper test execution on May 16, 1997, was caused by faulty communications between the maintenance personnel assessing fan rotation inside containment and the control room operator who started the fan. FPL reviewed the completed documentation for the May 16, 1997, post maintenance test and compared it against the May 16, 1997, Unit 2 control room sequence of events recorder (SER). The SER showed that 2-HVS-1D was started twice during the post maintenance testing; however, both the slow and fast speed rotational checks were performed with the motor operating in fast speed. The fact that two motor starts were done implies that maintenance personnel were correctly following the test procedure steps. The proper use of three way communications, as required by both the Conduct of Maintenance and Conduct of Operations policies, would have prevented the faulty communication which led to the unsatisfactory execution of the post maintenance test.
L-97-322 Attachment P~ae 4
- 3. CORRECTIVE STEPS TAKEN AND THE RESULTS ACHIEVED A. Procedure MP-2-0950173, "The Overhaul of Containment Fan Cooler Motors 2-HVS-lA, 1B, 1C, 1D (EQ Motors)," was revised to require the following:
- 1) verification signatures for both fast and slow speed motor rotation testing;
- 2) a caution statement to ensure that both windings are energized to verify proper motor rotation subsequent to electrically reconnecting the motor;
- 3) an addendum sheet that will be used by the control room operators to follow the performance of the motor rotation checks; and,
- 4) a requirement to perform a functional test of the containment fan cooler in both fast and slow speed prior to returning the unit to service (i.e., no low flow alarms present during rotation checks).
The procedure revisions were completed on November 28, 1997. Additional editorial clarifications were subsequently added and approved on December 17, 1997.
- 4. CORRECTIVE STEPS TO AVOID FURTHER VIOLATIONS A. This specific event, including the importance of accurate communications and the use of three way communications, was included in a Maintenance training bulletin that was issued on November 22, 1997.
B. Procedure ADM-78.01, "Post Maintenance Testing," will be revised to add a caution note about testing multiple speed or multiple winding motors by January 31, 1998.
- 5. Full compliance was achieved on November 28, 1997, when the procedure revisions to MP-2-0950173, "The Overhaul of Containment Fan Cooler Motors 2-HVS-1A, 1B, 1C, 1D (EQ Motors)," were completed.
L-97-322 Attachment P~s 5 Violation C 10 CFR 50, Appendix B, Criterion XI, Test Control, requires, in part, that a test program shall be established to assure that all testing required to demonstrate that components will perform satisfactorily in service is identified and performed in accordance with written test procedure which incorporate the requirements and acceptance limits contained in the applicable design documents.
Final Safety Analysis Report Section 6.2.2.2.2 states that the fan coolers operate at a reduced flow of 39,600 cubic feet per minute each, with low speed motor operation during accident operation.
Normal Operating Procedure, NOP-2-2000020, Revision 2, "Containment Cooling System Operation," which implements monthly surveillance testing of the containment fan coolers, requires that each cooling train fan unit be started from the control room and verified that each unit operates for at least 15 minutes, at least once per 31 days.
Contrary to the above, as of October 6, 1997, the licensee failed to assure that all testing required to demonstrate that components will perform satisfactorily in service, in accordance with the requirements and acceptance limits contained in the applicable design documents, was identified and performed. Specifically, NOP-2-2000020, did not require the containment cooler fans to be tested in slow speed, which is the alignment required during emergency operation. This procedural inadequacy had existed since initial plant operation.
R~es ense
- 1. FPL concurs with the violation.
- 2. REASON FOR VIOLATION The cause for the violation was non-cognitive personnel error during the development of surveillance procedure NOP 2-2000020, "Containment Cooling System Operation," that resulted in the surveillance procedure deficiency. The procedure, as it was written, did not meet the intent of the Technical Specification surveillance requirements because it required testing of the containment cooler fans only in the fast speed, and did not require verification of the post-accident safety related function of the fans in slow speed.
L-97-322 Attachment P~ae 6
- 3. CORRECTIVE STEPS TAKEN AND THE RESULTS ACHIEVED Procedure NOP 2-2000020, "Containment Cooling System Operation," was revised and issued on October 13, 1997. The revision clearly requires that all fans must be started and run in slow speed. Once all four fans have been shifted to slow speed, the absence of any low flow alarms throughout the 15 minute run time constitutes satisfactory completion of the surveillance test. The procedure also requires satisfactory fast speed operation of the containment fan coolers.
B.. FPL investigated the generic implications of this event to determine what other equipment types may be subject to inadequate surveillances. The review revealed that, with the exception of heating, ventilating, and air conditioning (HVAC) equipment, additional requirements (e.g., ISUIST requirements and industry standards) exist which enhance the development of surveillance procedures. All HVAC procedures used to perform Technical Specification sur veillances were reviewed to ensure the intent of the Technical Specification surveillance were met.
This review was completed on November 24, 1997.
- 4. CORRECTIVE STEPS TO AVOID FURTHER VIOLATIONS FPL Quality Instruction (QI) QI-S-PSL-1, "Preparation, Revision, Review/Approval of Procedures," Section 5.5 requires that site procedures be periodically reviewed. This QI was revised to require a qualified independent review of procedures that aFect surveillances or tests to ensure that the procedure adequately implements the intent of Updated Final Safety Analysis Report (UFSAR) surveillance descriptions and Technical Specification surveillance requirements when procedure periodic reviews are conducted.
This revision was approved on November 28, 1997.
- 5. Full compliance was achieved on October 13, 1997, when the revision to procedure NOP 2-2000020, "Containment Cooling System Operation," was approved.