ML17228B324
| ML17228B324 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 10/16/1995 |
| From: | Landis K, Prevatte R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17228B322 | List: |
| References | |
| 50-335-95-15, 50-389-95-15, NUDOCS 9511140316 | |
| Download: ML17228B324 (54) | |
See also: IR 05000335/1995015
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETTASTREET, N.W., SUITE 2900
ATLANTA,GEORGIA 303234199
Licensee:
Florida Power
& Light Co
9250 West Flagler Street
Miami,
FL
33102
gp,It
Robot
Report Nos.:
50-335/95-15
and 50-389/95-15
Docket Nos.:
50-335
and 50-389
Facility Name:
St.
Lucie
1 and
2
License Nos.:
and
Inspection
Conducted:
July 30
Lead Inspector:
revatte,
Inspector
through September
16,
1995
nidor
es1
ent
at
S)gne
Approved by:
M. Miller, Resident
Inspector
R. Aiel o,
'nse
Examiner
a
ls,
1e
Reactor Projects
Branch
3
Division of Reactor Projects
SUMMARY
e
gne
Scope:
This routine resident
inspection
was conducted onsite in the 'areas
of plant operations
review, maintenance
observations,
surveillance
observations,
engineering
support,
plant support,
and other areas.
Inspections
were performed during normal
and backshift hours
and
on
weekends.
Results:
Plant Operations
area:
Operator
performance
declined during this assessment
period.
However,
the inspector
observed
control
room activities during the
RCS draindown to reduced
inventory conditions
and found that
operators
controlled the evolution well.
Six violations were identified in the operat'ions
area.
The first
five violations involved
a failure to follow procedures
which
resulted
in incorrect safety
system alignments,
damaging reactor
coolant
pump seals,
an inadvertent
main steam isolation signal
actuation,
the failure to document
a deficiency,
and inadequate
operations
logs.
The sixth violation resulted
in
a spraydown of the
Unit
1 containment.
A Non-Cited Violation involving logkeeping
was
also identified.
Fiv'e weaknesses
were identified:
a hydrogen
9511140316
951016
ADOCK 05000335
8
overpressurization
of the main generator,
a Unit
2 downpower from a
heater drain
pump trip, the extension of a forced outage
due to poor
work screening
and planning,
inadequate
control
room logs,
and the
inappropriate delegation of line management
functions to guality
Control.
Maintenance
and Surveillance
area:
Performance
in this area
was found to be acceptable.
A violation,
which indicated that maintenance
personnel
were not signing off
procedural
steps
as they were completed,
was identified.
A similar
occurrence
had
been previously identified 'in IR 95-10.
A procedural
weakness
involving the
amount of supervisory oversight required for
unqualified workers
was also identified.
During the Unit
1 outage,
that started
on August
1,
a large
amount of maintenance
work
occurred.
Several
of these
maintenance
activities were
on
components
that
had
been overhauled
during the last refueling
outage.
Engineering
area:
The support of diesel
generator
maintenance
and root cause
evaluation
was found to be timely and helpful.
Plant Support area:
Plant support
by health physics
and radiation during the Unit
1
outage
was good.
Unit
1 was decontaminated
to pre-outage
conditions
after the inadvertent
spraydown.
Overall, the Unit
1 outage
was very challenging
and demanding,
but the
licensee's
response
to each
issue
was acceptable.
Within the areas
inspected,
the following violations
and unresolved
items
were identified:.
VIO 335/95-15-01,
"Failure to Follow Procedures
and Block MSIS
Actuation,"
paragraph
3.b.
VIO 335/95-15-02,
Two examples of "Failure to Follow Procedures
during
RCP Seal restaging,"
paragraph
3.b.
VIO 335/95-15-03,
"Failure to Follow Procedure
and
Document
abnormal
valve position in the Valve Switch Deviation Log,"
paragraph
3.b.
VIO 335/95-15-04,
"Failure to Follow Procedures
during Alignment of
Shutdown Cooling System,"
paragraph
3.b.
VIO 335/95-15-05,
"Failure to Follow Procedure
and
Document
a
deficiency
on Containment
Spray Valve Surveillance
Test Procedure,"
.paragraph
3.b.
VIO 335/95-15-06,
"Failure to Initial Maintenance
Procedure
Steps
as
work was completed,"
paragraph
3.b.
VIO 335/95-15-07,
"Failure to Follow Procedures
during venting of
ECCS System resulted
in Containment
Spraydown,"
paragraph
3.b.
NCV 335/95-15-08,
"Failure to Follow Logkeeping Procedures,"
paragraph
3.b.
REPORT
DETAILS
1.
Persons
Contacted
Licensee
Employees
- R. Ball, Mechanical
Maintenance
Supervisor
- W. Bladow, Site guality Manager
- L. Bossinger,
Electrical
Maintenance
Supervisor
H. Buchanan,
Health Physics
Supervisor
C. Burton, Site Services
Manager
- ,*R.
Dawson,
Licensing Manager
- ,*D. Denver, Site Engineering
Manager
J.. Dyer, Maintenance guality Control Supervisor
H. Fagley,
Construction
Services
Manager
P. Fincher, Training Manager
R. Frechette,
Chemistry Supervisor
'.
Fulford, Operations
Support
and Testing Supervisor
K. Heffelfinger, Protection
Services
Supervisor
- J. Harchese,
Maintenance
Hanager
- R. Olson,
Instrument
and Control Maintenance
Supervisor
W. Parks,
Reactor
Engineering
Supervisor
- C. Pell,
Outage
Manager
L. Rogers,
System
and Component
Engineering
Manager
- J
- ,*D. Sager,
St.
Lucie Plant Vice President
. Scarola,
St.
Lucie Plant General
Manager
- J.
West,
Operations
Manager
- C.
Wood, Operations
Supervisor
W. White, Security Supervisor
Other licensee
employees
contacted
included engineers,
technicians,
operators,
mechanics,
security force members,
and office personnel.
NRC Personnel
- M. Hiller, Resident
Inspector
- ,*R. Prevatte,
Senior Resident
Inspector
R. Aiello, License
Examiner
S. Sandin,
- Attended
September
15,
1995 exit interview
- Attended October
11,
1995 exit interview
last paragraph.
and initialisms used throughout this report are 1'
d 'h
is
e
>n
e
2.
Plant Status
and Activities
a
~
result of a se
'nit
1
was
shutdown
on August
1
as
a result of Hurricane
E
'
ries of equipment
problems
and personnel
errors,
the
rin.
s
a
Unit remained
shutdown for'the remainder of th
>nspec
>on period.
b.
c
~
Unit 2 was also
shutdown
on August
1
as
a result of Hurricane Erin.
The Unit was restarted
August
4 and achieved full power on August 5.
On August 17, high condenser
back pressure
resulted
in reducing
power.
The Unit operated
at power levels of 50 to 90 percent while
the condenser
water boxes
were cleaned,
modifications were performed
on the heater drain
pump electrical controls,
and other equipment
problems
were corrected.
The Unit returned to full power on
August 29.
Power
was reduced
again
on September 15,'or condenser
waterbox cleaning.
NRC Activity
R.
F. Aiello, an Operator
License
Examiner from NRC Region II, was
on site
on August 14-18.
His activities involved augmenting
the
resident
inspection effort and his inspection results
are contained
in this report.
3.
Plant Operations
'a
~
Plant Tours
(71707)
The inspectors periodically conducted
plant tours to verify that
monitoring equipment
was. recording
as required,
equipment
was
properly tagged,
operations
personnel
were
aware of plant
conditions,
and plant housekeeping
efforts were adequate.
The
inspectors
also determined that appropriate radiation controls were
properly established,
critical clean
areas
were being controlled in
accordance
with procedures,
excess
equipment
or material
was stored
properly,
and combustible materials
and debris were disposed of
expeditiously.
During tours,
the inspectors
looked for the
existence
of unusual fluid leaks,
piping vibrations,
pipe hanger
and
seismic restraint settings,
various valve
and breaker positions,
equipment
caution
and danger tags,
component positions,
adequacy of
fire fighting equipment,
and instrument calibration dates.
Some
tours were. conducted
on backshifts.
The frequency of plant tours
and control
room visits by site management
was noted.
During
a tour of the Unit
1 control
room, conducted
on September
12,
the inspector
noted that the FI-3312, flow indicator for 1A2 LPSI
flow, was indicating
50 gpm.
As the unit was not employing
SDC, the
indicator should
have indicated
0 gpm.
The inspector
brought this
to the attention of the
RCO.
was generated
to
correct the condition.
The inspectors
routinely conducted
main flow path walkdowns of ESF,
ECCS,
and support
systems.
Valve, breaker,
and switch lineups
as
well
as equipment conditions were randomly verified both locally and
in the control
room.
The following accessible-area
ESF system
and
area
walkdowns were
made to verify that system lineups
were in
accordance
with licensee
requirements
for operability and equipment
material conditions
were satisfactory:
e
~
Unit
1 Containment Building
~
Unit 2 Containment
Spray Trains
A and "8
The inspector verified that major flowpath valves
were
correctly positioned,
that indicated
pump oil levels were
appropriate
and that control
room indications
were
satisfactory.
The following minor deficiencies
were
identified:
~
PI-07-6A, the
A train hydazine
pump discharge
pressure
gage indicated
15 psig.
PI-07-6B, the
B train hydrazine
pump discharge
pressure
gage indicated
10 psig.
The
inspector
informed the
ANPS of the conditions
and
a
PWO
.was generated
to verify gage calibrations.
~
HV-07-3 and HY-07-4 local valve position indicators
indicated that the valves
were
90 per cent open.
Control
board lights indicated that the valves were fully open.
The inspector
informed the
ANPS,
who initiated
a
PWO.
b.
Plant Operations
Review (71707,
62703,
37551,
40500,
93702)
The inspectors periodically reviewed shift logs
and operations
records,
including data sheets,
instrument traces,
and records of
equipment malfunctions.
This review included control
room logs,
auxiliary logs, operating orders,
standing orders,
jumper logs,
and
equipment tagout records,
The inspectors
routinely observed
operator alertness
and demeanor
during plant tours.
They observed
and evaluated
control
room staffing, control
room access,
and
operator
performance
during routine operations.
The inspectors
conducted
random off-hours inspections
to ensure that operations'nd
security performance
remained
at acceptable
levels.
Shift turnovers
were observed to'erify that they were conducted
in accordance
with
approved
licensee
procedures.
Control
room annunciator
status
was
verified.
Except
as noted
below,
no deficiencies
were observed.
1)
Hurricane Erin
On July 31, at 11:28 a.m,,
an Unusual
Event
was declared
due to
a hurricane warning (Hurricane Erin) for the East coast of
Florida in the vicinity of the St.
Lucie Plant.
At that time
both Units were at
100 percent
power,
In the afternoon,
the
NRC dispatched
a van with emergency
radio equipment
from
Atlanta to provide assistance
to the Florida plants
as
needed.
In the late afternoon additional
members of the
NRC staff were
dispatched
from Atlanta to provide assistance
as
needed
to
Florida plants,
The resident
inspector
was onsite
and monitored the licensees
preparation for severe
weather
as required
by AP 0005753,
Rev
13,
"Severe
Weather Preparations."
These preparations
were
verified to be completed
on the morning of August
1;
At 8:05 a.m.,
on August
1, the licensee
commenced
a shutdown of
both nuclear units.
The Senior Resident
Inspector returned
from the RII office and the resident staff monitored the
shutdown of both units to hot standby
and other licensee
preparations
for the approach
of Hurricane Erin.
At
approximately 3:00 p.m., the
NRC, van with emergency
communications
equipment,
arrived
on site.
All.equipment
was
tested
and placed
in storm protected
areas.
The licensee
established
and maintained
continuous
communications with the
NRC and corporate
EOF at approximately
9:00 p.m.
The hurricane
made landfall about midnight on August
1, approximately
20 miles north of the plant with winds in that
area of approximately
70 mph.
Actual winds at the plant
averaged
about
40
mph with periods of heavy rain.
The plant sustained
no significant damage
due to the wind or
rain.
At 5:00 a.m.,
on August 2, Erin was downgraded to
a
tropical storm and the Unusual
Event
was terminated at 5:42
a.m.
Plant preparation,
staffing, planning,
and response
to'rin
was excellent.
It was later discovered that during hurricane preparations
the
licensee
had tested
Room floor drain valves
HCV-21-1
through HCV-21-7.
During testing
conducted
by control
room
operators,
some of the valves
had failed to stroke properly.
As
a result,
the valves
were left closed for troubleshooting
and were not reopened.
OP 1-0010123,* Rev 99, "Administrative
Control of Valves,
Locks,
and Switches," required,
in step
8. 1.6, that "All valve or switch position deviations or lock
openings
shall
be documented
in Appendix C, Valve Switch
Deviation Log..."
The inspector
reviewed archived'ppendix
C
logs completed
in Ju'ly and August
and control
room open
Appendix
C logs
and found
no evidence that HCV-25-1 through
7
were logged
as being out of position.
The failure to enter the
valves'losed
status
into the valve deviation log's
a
violation (VIO 335/95-15-03,
"Failure to Follow Procedure
and
Document
abnormal
valve position in the Valve Switch Deviation
Log". This ultimately led to flooding of this space
when
a
Relief Valve lifted and did not reseat
(IR 95-20).
STAR 950917
was initiated to develop
a
PH for verifying that floor drains
were
unclogged'nit
2 was restarted
on August
4 and returned to full power
operation
on August 5.
The inspector
reviewed
and verified the
unit's readiness
for restart.
The restart
was achieved without
experiencing significa'nt problems.
Unit
1 remained
shutdown
for the remainder of the inspection period.
5
Unit
1 Forced
Outage
After Hurricane Erin, the plant scheduled
a restart of Unit
1
for August 2.
A failed
RCP seal
resulted
in placing the unit
in cold shutdown.
A series of personnel
errors
and equipment
failures resulted
in the unit being
shutdown to perform repairs
and correct deficiencies.
The following major work activities
were accomplished
during this outage:
~
RCP IAI and
1A2 seal
replacement
~
Replaced
and adjusted
SDC relief, valve 3439
~
Replaced
jumpered cell
43 on
B safety related battery
~
Repair/replace
1402
and
1404
~
Cleanup
and decontamination
of containment
as
a result of
spraydown
~
Inspection of containment
equipment
~
Repair of containment
spray valve FCV-07-1A
~
PCN on
DG 1A/B to improve trip solenoids
and temperature
monitors
~
Inspection
and repair of damaged
182
~
Replacement
and setpoint
changes
for eight safety related
relief valves
Work on the
above
items
was monitored
as it occurred.
Several
of the above
items are discussed
in detail in this report.
This unplanned
outage
became
a challenge
to the licensee
because
as
each
item was repaired
another event or equipment
failure occurred that lengthened
the outage duration.
After the restart
was delayed,
the licensee
added to the work
scope.
During this time span,
the inadvertent
spraydown of
containment
brought other operator-work-arounds
"into question.
After questions
about the number of open
STARS, Caution Tags,
J/LLs,
and OWAs'y the
NRC, the licensee
conducted
a review of
all open
STARs, Caution Tags,
PWOs, J/LLs,
PCNs,
OWAs,
and
Equipment
Out Of Service
on Unit 1.
Based
on this review,
approximately
80 of these
items were also
added to and
completed during the forced outage.
The inspector
noted that several
of the components
that were
worked
on had also
been
worked
on during, the last Unit
1
refueling outage.
The licensee
plans to evaluate this item and
determine if they have
a repetitive failure or rework issue.
In addition to the equipment
problems,
several
management
changes
occurred that
may have affected
the outage duration.
Vendor support
was obtained
as
needed
during the outage
and
site
and corporate
engineering
provided assistance
as
needed
to
resolve
issues
as they occurred.
Overall, the Unit
1 outage
was very challenging
and demanding,
but the licensee's
response
to each
issue
was acceptable.
0
6
As
a result of several
events that
have occurred during the
Unit
1 outage,
the
NRC requested
that
FPL management
discuss
these
issues
and their actions
being taken.
A meeting
was held
in the Region II office in Atlanta on August
29 on this item.
At that meeting the licensee
covered the events that
had
occurred
and their planned
and corrective actions
completed.
They also noted that they had formed
an inspection
team
composed primarily of three senior managers
from two utilities
'and
a sister plant to assess
these
recent
events
and provide
recommendations
for improvement.
This team
was
composed
of a Unit Manager
from ANO, the
Operations
Manager
from North Anna,
and the Assistant to the
Vice President
from Turkey Point.
This team was.assisted
by a
Plant
gA Supervisor to provide knowledge
on plant procedures
and interface.
The team arrived
on site September
5, completed their
assessment,
and'exited
on September
9.
The inspector
noted
that the team
members
observed
operations
in the control
room
on various shifts,
conducted
interviews with a large
number of
personnel
and worked long days to complete the assessment.
The
inspector
attended
the exit on September
9 and noted that the
majority of the teams findings closely paralleled
previous
NRC
identified deficiencies.
The licensee
submitted
the results of this team inspection
and
an action plan to the
NRC on September
15.
The unit again
atte'mpted
a restart during the week of September
10.
After achieving
532'F
and approximately
1700 psia,
a leak
at the flange of pressurizer
safety valve 1201,resulted
in
returning the plant to cold shutdown to repair this item.
A
review by the licensee
found that this deficiency
had
been
identified on August 3, but had not been
adequately
evaluated
to determine
the
need for rework prior to plant restart.
As
a
result of this, the unit was still shutdown at the
end of the
inspection period.
This item is identified as
a weakness
in
the work screening
and planning process.
RCP Seal
Failure
Background
St.
Lucie employed
Byron-Jackson
and seal
packages.
The
packages
consisted
of 3 primary seals
and
a fourth vapor seal.
The primary seals
acted
to break
down
RCS pressure
in'
equal
stages
of approximately
750 psid.
The seal'stages
segregated
the seal
package
into
4 cavities,
the lower (below the lower
seal),
the middle (between
the lower and middle seals),
the
upper
(between
the middle
and upper seals),
and the controlled
bleedoff (between
the upper
and vapor'seals).
Each seal
was
rated for full RCS pressure.
The pressure
breakdown
process
resulted
in a controlled bleedoff flow to the
VCT of
approximately
1
gpm per
pump.
Seal injection into the lower
seal cavity was possible via the
CVCS system,
however,
the
licensee
discontinued routine
use of seal
injection in 1993
(via safety evaluation
JPN-PSL-SENJ-93-001)
following
indications that the cooler injection water led to damage of
RCP shafts.
The seals
were cooled
and lubricated
by controlled
bleedoff flow which was cooled
by
a combination of the thermal
barrier heat
exchanger
(below the seal
package)
and
a seal
water heat exchanger
(which cooled flow rising from the
casing driven by an auxiliary impeller affixed to the
pump
shaft).
Seal
Failure-
On August 2, while performing
a Unit
1 heatup following
Hurricane Erin, operators
noted that the middle seal cavity of
the
1A2
RCP indicated
a pressure
which approximated
pressure,
indicating
a failure of the lower seal of the
package.
Operators
subsequently
entered
ONOP 1-0120034,
Rev 34,
Pump," which required,
upon
identification of a failed seal,
that seal
parameter
data
be
recorded
every 30 minutes to ensure that additional
seal
stages
were not degrading.
Throughout the day,
the licensee
considered
the option of
"restaging" the seal
package.
The process
involved opening
vents associated
with each
seal cavity in an effort to increase
the differential pressure
across
each
seal
stage
which, in
principle, would force moving and stationary
seal
faces
together
more tightly, thus reestablishing
the seal.
The
evolution was describeg
in
OP 1-0120020,
Rev 72, "Filling and
Venting the
RCS," Appendix
E, "Restaging
Pump
Seals."
According to various personnel
in the licensee's
Operations
organization,
the process
had
been successfully
applied several
times in the past.
The licensee
opted to perform the
procedure,
and informed the inspector of their intentions.
The
inspector
was not familiar with the process;
however,
in
discussions
with the licensee,
the inspector
was informed that
the process
had
been
performed satisfactorily in the past, that
a procedure
existed for the process,
and that experienced
ANPSs,
who had performed
the procedure
in the past,
were being
assigned
to the task.
At 5: 17 p.m.
on the
same
day,
the licensee
be'gan
the restaging
process.
Plant conditions at the time were
Node 3,
1450 psia,
370'F, with RCPs in operation. 'er the governing procedure,
the controlled bleedoff cavity was vented,
followed by the
upper
and middle cavities.
At this point, flow out the vents
was expected
to decrease
as the lower seal
stage
restaged;
however,
flow did not diminish and, after approximately I
minute, black material
was noted to be in suspension
in the
vented reactor coolant
from the middle cavity.
Additionally,
the water temperature
was noted to increase
rapidly.
Operators
closed the middle cavity vent valve
and noted that,
almost
immediately,
black, hot, water issued
from the upper seal
cavity vent, indicating
a middle seal failure.
Operators
immediately closed the vent valves associated
with the upper
seal cavity and the controlled bleedoff cavity.
At 5:50 p.m., control
room differential pressure
indications
were received
which confirmed that both the lower and middle
seal
stages
had failed.
Controlled bleedoff flow iricreased to
greater
than 3.5 gpm.,
which indicated degradation
of the upper
seal.
At 6: 10 p.m.,
a cooldown
and depressurization
of the
unit commenced.
At 6:40 p.m.,
the
1A2
RCP was secured
and
lower seal cavity temperatures
were noted to increase
to 300'F
due to the increased
leak rate through the seal
package
and the
lack of auxiliary impeller-driven cooling
(as
a result of
securing the pump).
A.
NSIS Actuation
As the cooldown proceeded,
SG pressure
decreased
and,
at
approximately
700 psig,
9-18 and g-20,
"HSIS
Actuation Channels
A/B Block Permissive,"
illuminated.
These
were expected
alarms,
as cooldowns naturally result
in
SG pressure
decreases
below the HSIS setpoint.
HSIS
block keys were provided for this eventuality to prevent
NSIS actuations
under non-accident
related conditi'ons of
low SG pressure.
The desk
RCO,
who was performing cooldown-related
duties
at the subject
area of the control panels,
acknowledged
the annunciators
and later reported
observing that the
MSIVs and NFIVs were in their post-NSIS positions
as
a
function of the cooldown.
Consequently,
the
RCO elected
not to insert the
MSIS block and returned to
VCT degassing
operations.
The
RCO was then questioned
by an
STA as to
the failure to block the MSIS.
The
RCO responded
that,
as
the NSIVs and
MFIVs were in their post-trip positions,
the
actuation
would not present
a problem.
The board
RCO (the
second of the two
RCOs performing the cooldown)
became
involved and directed that the
NSIS be blocked.
Before
the keys could
be inserted
to block the signals,
pressure fell below the actuation setpoint
and
an HSIS was
received.
The signal
was later blocked
and reset.
The inspector
reviewed
HPES '95-07,
Rev 2, the licensee's
review of the event.
In it, the licensee
determined that,
in "Summary of Factors that Influenced
Human Performance,"
the event
was the result of a lack of knowledge
on the
part of the desk
RCO that
an HSIS was reportable
to the
NRC whether or not components
changed
state.
Under
'"Summary of Causes,"
the licensee cited the following
causal
factors:
~
Training/gualification:
The licensee
determined that training had not
educated
operators
as to the reportable
nature of ESF
actuations,
whether or not components
changed state.
~
Supervisory
Hethods - Progress/Status
of Task not
Adequately Tracked:
The licensee
determined that the
ANPS and
NPS were
too involved in the diagnosis of the
RCP seal
failures
and were not observing the overall
cooldown
in progress
at the time.
~
Work Practices
- Pertinent
Information not
Transmitted:
The licensee
determined that the desk
RCO did not
announce
to the rest of the control
room that the
had
been received;
thus,
ANPS/NPS
involvement to establish
the
NSIS block was not
obtained.
~
Work Practices - Document
Use Practices
Documents
not Followed Correctly:
The licensee
determined that
OP 1-0030127,
Rev 68,
"Reactor
Plant
Cooldown
Hot Standby to Cold
Shutdown," contained
a step requiring the operator to
block the
MSIS when the permissive
was received;
however,
the step
was contained further into the
procedure
than the operator
had proceeded.
Additionally, the licensee
determined that the
operator
had failed to refer to the annunciator
response
procedure,
which directed that the block
keys
be inserted.
The licensee's
proposed
corrective actions for this event
included:
~
Re'vising operator training to include "the necessity
to block
and other reportable, actuations
when
they alarm...The plant's operating
philosophy of
keeping
Licensee
Event Reports to
a minimum should
also
be included
and stressed."
10
~
Including the event in Licensed Operator
Requalification Training.
~
Emphasizing that control
room management
should
maintain
a "big picture" view of plant evolutions,
that formal crew communications
should
be employed,
and that procedures
are followed.
The inspector
concluded that the licensee's
investigation
was weak in that:
~
The operator's
knowledge of procedural
requirements
prior to the event
was not reported (i.e. did the
operator
know that the
OP 1-0030127 required that the
HSIS
be blocked?).
~
The conclusion that the operator's
lack of knowledge
of the reportability of the HSIS actuation
was
a
principle contributor to his actions
appeared
to
place
more importance
on avoiding
an administrative
burden
and the visibility of reporting actuations
to
the
NRC, than it did on knowledge of,
and adherence
to, procedural
requirements.
The inspector discussed
the subject report with the
licensee.
Operations
management
stated that the operator
in question
reported
being confused
at the time and that
it was their expectation that,
under
such circumstances,
operators
would refer to the annunciator
response
procedures
provided for each annunciator
panel.
Management further stated that it was not their
expectation that
RCOs would be familiar with NRC reporting
requirements
(reportability knowledge
was said to be the
responsibility of ANPS/NPSs
and
STAs)
and that operator
actions
should
be based
upon procedure
requirements,
as
opposed
to reportability.
The inspector
reviewed
OP 1-0030127
and found that step
8.21 directed that "At 700 psia
S/G pressure,
g-18 and g-20,
HSIS Actuation Channels
A/B Block
Permissive, will alarm.
Block HSIS by placing HSIS block .
key switch to
BLOCK position."
Additionally,
ONOP 1-
0030131,
Rev 60, "Plant Annunciator Summary," specified
that,
upon valid receipt of annunciators
g-18 and g-20,
operators
were to immediately block MSIS channels
A and
B,
respectively.
The inspector
concluded that the failure of
the
Desk
RCO to perform step 8,21 of OP 1-0030127 is
a
violation (VIO 335/95-15-01,
"Failure to Follow Procedures
and Block MSIS Actuation".
Following the HSIS, the cooldown
was temporarily suspended.
At
approximately 8: 18 p'.m.,
an annunciator
was received indicating
11
that reactor cavity leakage
exceeded
1 gpm.
Operators verified
that control
room instruments
indicated
an increased
leak rate
from approximately
.25
gpm to approximately
2 gpm.
The leakage
was identified as being related to the
1A2
RCP vapor barrier.
Operators
entered
ONOP 1-0120031,
Rev 23,
"Excessive
Reactor
Coolant
System
Leakage,"
at 8:24 p.m.
At 8:44 p.m., safety
function status
checks
were completed satisfactorily.
At 9:25
p.m., the licensee
declared
an Unusual
Event based
upon
occurrences
that warrant increased
awareness,
specifically,
due
to concerns
over further
RCP seal
degradation.
At 6:30 a.m.
on
August 3, the Unusual
Event was terminated
based
upon the
reduction in
RCS leakage
through the
1A2
RCP seal
(due to
depressurization)
and
on stability of plant conditions.
The licensee
performed
a cooldown/depressurization
of Unit
1
and replaced
the subject
seal
package.
The failed package
was
then disassembled
in an attempt to determine
the root cause for
=the failures.
At the close of the inspection period,
the
licensee
had not concluded its root cause investigation..
The
inspector
discussed
the effort with the licensee,
The most
probable root causes
for the noted conditions
were described
as
follows:
~
The most probable root cause for the indicated failure of
the lower seal
was destaging.
Upon restaging,
the carbon
face of the lower seal
was believed to have
been forced,
rapidly, against its mating seal
face, resulting in
fracture.
The most probable
cause for the middle seal failure and
degradation
of the remaining seals
was stated to be
a
reduction in cooling
and lubricating flow though the seal
as
a result of the venting of the seal cavities.
The
subsequent
imposed
due to pump rotation without
lubrication, fractured the middle seal rotating face.
Following the failure of the
1A2
RCP seal
package,
the
PGM
initiated
STAR 950849 to perform
a self-assessment
of the
decision
making process
that led to the restaging of the seal.
The conclusions
reached
in the self-assessment
were that the
one-on-one
nature of the decision
making process
precluded
a
"synergistic environment."
The study went
on to state that,
while several
individuals expressed
concern
over the prospects
for success,
no specific technical
issue
was raised.
The
licensee
determined that the existing Nuclear Policy 105
process,
which required multidisciplinary review of proposed
abnormal activities,
should
be expanded
such that it is
employed
when questions
of procedure applicability are raised.
The insp'ector
reviewed available
information regarding
seals
and restaging.
The following was noted:
12
~
OP 1-0120020,
Rev 72, "Filling and Venting the
RCS,"
contained,
in the
base
procedure,
precaution
4.2 which
stated
"Do not attempt to vent if the
RCS temperature
is
above 200'F."
Initial conditions specified in the
base'rocedure
were consistent
with the Cold Shutdown
mode of
operation.
~
OP 1-0120020,
Rev 72, "Filling and Venting the
RCS,"
Appendix E, "Restaging
Pump Seals,"
included only two statements
that could
be construed
as'nitial
conditions or'recautions.
One
was in the form of
a note
and the other in the form of a caution.
The note
stated
"Ensure
seal
injection is aligned
and in service."
The caution stated
"If RCS is greater
than 200'F,
Then
use
caution
when venting."
~
FSAR section 5.5.5.2 stated
that the vapor seal
was
designed
to withstand
RCS operating
pressure
when the
were idle.
~
The restaging
process
described
in Appendix
E of OP 1-
0120020
was substantially
the
same
as the seal
package
venting procedure
described
in the vendor technical
manual
for the
RCP.
However,
the venting procedure
in the
technical
manual directed that the venting
be performed at
approximately
200 psi with an idle pump.
Safety Evaluation JPN-PSL-SENJ-93-001,
Rev 1, "Deletion of
RCP Seal Injection," included,
by reference,
FPL letter L-
81-107 to the
NRC reporting test results for RCP seals
in
postulated
station blackout conditions.
The results of
the tests
were that,
under simulated
Hot Standby
conditions,
a maximum of 16, 1 gph was recorded after 50
hours without cooling water flow to the seal
package.
~
The vendor
recommended
a maximum seal
package
temperature
of 250'F based
upon the rubber components
in the seal
package.
Safety evaluation
JPN-PSL-SENJ-93-001
provided
analyses
to increase
the temperature limit to 300'F.
~
The licensee
produced
a Byron-Jackson letter,
dated
November
16,
1990,
which reported
a review of St. Lucie's
proposed
restaging
process.
The letter stated that the
proposed
process
was acceptable.
The letter also stated
that application of the process
sh'ould consider initial
seal
condition
and
age in determining whether to apply the
process.
The inspector
concluded that the licensee
had reason
to believe
that restaging
the
1A2
RCP seal
package
would correct the
identified condition.
Vendor information and
knowledge of
previous successful
restagings
tended to support the evolution.
13
However, 'the inspector
found that the procedure
appendix which
directed
the evolution did not require initial conditions
sufficient to ensure that seal
package
temperature
limitations
would be observed.
In fact, the "Caution" statement
of the
Appendix (advising caution if RCS temperature
exceeded
200'F)
ran counter to precaution
4.2 of the base
procedure
(precluding
venting if RCS temperature
exceeded
200'F).
Absent
any
modifying information in Appendix
E, the inspector concluded
that the initial conditions specified in the base
procedure
applied to the procedure
and its appendices.
Consequently,
the
failure of the licensee
to adhere to the initial conditions
specified in
OP 1-0120020 is the first example of a violation
of failure to follow procedure
during
RCP Seal
restaging
(VIO
335/95-15-02,
"Failure to Follow Procedures
during
RCP Seal
restaging").
The inspector
noted that control
room logs did not reflect 'the
alignment of seal injection, while the note of Appendix
E of OP
1-0120020 required
seal
injection.
When questioned,
the
licensee
stated that seal
injection was not aligned
due to
concerns
for the affect it might have
on the
RCP shaft.
When
asked
why a
TC had not been
made to the Appendix, the licensee
had
no explanation.
The licensee's. failure to align seal
injection to the
1A2
RCP prior to restaging
the pump's
seal
is
the
second
example of a violation of failure to follow
procedure
during
RCP Seal
restaging
(VIO 335/95-15-02,
"Failure to Follow Procedures
during
RCP Seal restaging").
The inspector
reviewed
ONOP 1-0120034,
Rev 34,
Pump,"
and found that, while actions
were described for the
failure of one
RCP seal
(30 minute readings
to ensure
degradation
is not'ccurring - step 7.2.8.C),
and more than
one
RCP seal
(unit shutdown,
secure
RCP when
TCBs open
step
7.2.8.0),
no actions
were specified for the instance
when
3
seals,had
failed.
As stated
above,
the fourth, vapor,
seal
was
only designed
to contain
system pressure
when
an
RCP is idle.
The failure of ONOP 1-0120034 to direct the securing of an
when
3 seals
have failed was found to be in contradiction to
the design
parameters
of the
RCP.
The inspector
brought this
to the attention of the licensee.
The licensee
reviewed the
issue
and stated that
PCRs would be prepared for the
RCP off-
normal
procedures
for each unit, adding
a requirement
to trip
the unit and secure
the affected
RCP should third stage
seal
failure occur.
In conclusion,
the inspector
found that the activities relating
to the failure of the lower seal of the
lA2 RCP were poorly
considered
in that the restaging
process
was 'applied in
inappropriate plant conditions.
The failure to establish
proper initial conditions 'for the restaging
was found to
exacerbate
the seal's
already
degraded
condition.
The
inspector further concluded that two examples of procedural
14
noncompliance
were associated
with the seal
restaging effort
and that one example of procedural
noncompliance
was associated
with the HSIS actuation.
The licensee's
evaluation of the HSIS
actuation
was found to be inappropriately
focused
on event
reportability,
as
opposed
to procedure
compliance.
The
licensee's
self-assessment
of the decision
making process
that
led to the restaging of the
1A2
RCP was found to be
commendable.
OP 1-0120034
was found to include inconsistencies
between
the base
procedure limitations and those
found in
Appendix
E of the
same
procedure.
A'weakness
was identified in
ONOP 1-0120034,
in that design limits of the
RCP seal
package
vapor seal
were not properly incorporated
into the procedure.
4)
Reduced
Inventory for RCP Seal
Replacements
On August 5, Unit
1 entered
a reduced
RCS inventory condition
to support
RCP seal
replacement
work.
The following items were
observed
during this evolution:
~
Containment
Closure Capability
Containment
was
established
and maintained during the evolution.
The
equipment
hatch
had
been
open prior to draindown,
but it
was replaced,
and the personnel
hatch closed,
once
equipment required for the
RCP maintenance
was in
containment,
RCS Temperature
Indication - Normal
mode
1
CETs were
available for indication,
I
RCS Level Indication
-. Independent
RCS level indications
were available.
A Tygon tube level indicating standpipe,
in the containment
was
manned during the draindown
and
was
displayed,
via closed-circuit televisi'on,
in the control
room.
The inspector walked
down the tygon standpipe
and
verified it to be correctly aligned
and free of obvious
kinks which would adversely affect its operation.
Additionally,
a wide range pressurizer
level transmitter
provided level
and trend indications
in the control
room.
RCS Level Perturbations
- When
RCS level
was altered,
additional operational
controls were invoked,
At plant
daily meetings,
operations
took actions to ensure that
maintenance
did not consider performing work that might
effect
RCS level or shut
down cooling.
RCS Inventory Volume Addition Capability
Three charging
pumps
and
a HPSI
pump were availqble for RCS addition.
RCS Nozzle
Dams - Due to the type of outage,
the nozzle
dams
were not installed this time.
15
Vital Electrical
Bus Availability Operations
would not
release
busses
or alternate
power sources
for work during
this evolution.
Both
as were all
offsite power sources.
I
Pressurizer
Vent Path
The manway atop the pressurizer
has
been
removed to provide
a vent path.
The inspector
observed
control
room activities during the
draindown to reduced
inventory conditions.
The'volution was
performed in accordance
with OP 1-0410022,
Rev 21,
"Shutdown
Cooling," Appendix A,
" Instructions for Operation at Reduced
Inventory or Hid-Loop Conditions,"
and
OP 1-0120021,
Rev 38,
"Draining the Reactor Coolant System."
The inspector verified
that specified conditions
were met prior to the evolution.
The
inspector
found that operators
controlled the evolution well,
that appropriate
cross
checking
between level indications were
performed,
and that procedural
requirements
for waiting periods
between draining stages
were met.
The licensee
exited reduced
inventory conditions following the
RCP seal
replacements
on
August 7.
5)
Containment
Spraydown
A.
Background
The St.
Lucie Unit
1
and
CS systems
are
shown in
Figure
1.
The two systems
are interrelated
in that they
share
the
SDC heat exchangers.
In an accident
mode,
the
SDC heat
exchangers
serve to cool water drawn from the
containment
sump prior to delivery to the containment
environment via the containment
spray headers.
Referring
to Figure
1, the accident
mode flowpath for CS, train A,
involves water traveling into the
A CS
pump,
through the
SDC heat exchanger,
and to the
In a
SDC mode,
the
SDC heat exchangers,
in conjunction
with the
LPSI pumps,
serve to remove heat
from reactor
coolant.
The flowpath in this
mode (again, for the
A
train) involves water flowing from the
RCS hot leg and
through the
A LPSI
pump.
The fluid flow is then split at
FCV-3306, with some water passed
through the valve
and the
balance diverted through the
SDC heat exchangers,
through
NV-3456 and/or HV-3457,
and returned to the
LPSI system
for delivery to the
RCS cold legs.
During power operations,
the two systems. are isolated
from
one another
and
each is aligned to perform its safety
function.
In the case of the
CS system,'his
alignment
involves
an
open flowpath from the
RWT, through. the
pumps,
and
up to FCV-07-1A and
FCV-07-1B, normally closed
AOVs which receive
open signals
in response
to
a
CSAS.
'
0
0
16
LPS'I System Venting
In February,
the licensee
experienced
a waterhammer
event
in the Unit
1
LPSI system while placing
SDC in service
(see
IR 95-04),
The licensee
determined
that
one of the
potential contributors to the event
was air, trapped
in
system piping.
At approximately the
same,
the licensee
identified
a Unit
2 LPSI
pump in an air bo'und condition
during
a surveillance
run of the
pump.
In response
to
these
events,
the licensee
developed
aggressive
venting
programs for the systems.
As
a part of the effort,
OP 1-
0420060,
"Venting of the
Emergency
Core Cooling and
Containment
Spray Systems,"
was developed.
The procedure
required,
in part, that venting
be performed following SDC
system operation.
The procedure
was approved
on August
13.
As
a part of the venting procedure,
the licensee
pressurized
the lines leading to the
SDC heat
exchanger
via the
pumps
and systematically
di.rected flow to the
RWT in an effort to sweep air from the system.
The
boundary of this venting process
included the
CS lines
up
to the
FCV-07-1A Inoperability
On August
11,
CS flow control valve FCV-07-IA failed
a
stroke time test
and
was declared
OOS.
As shown
on Figure
1, the valve isolated
the
from the
CS system
outside containment.
The valve was designed
to open
on
a
and
was
a fail-open
AOV.
The valve was required
by
AP 1-0010125A,
Rev 39, "Surveillance
Data Sheets,"
Data
Sheet
8A, "Valve Cycle Test
Non-Check Valves," to stroke
in less
than
8 seconds.
In the failed test,
the stroke"
was recorded
as 20.3 seconds.
As
a result of the failed surveillance test,
STAR 950869
was generated.
The stroke time failure was documented
and
the
STAR was assigned
to Engineering for disposition.
Engineering
proposed
placing the valve in its safeguards
position
(open)
and prepared
SE JPN-PSL-SENS-95-016,
Rev
0, "Alternative Valve Position for Spray Header Isolation
Valve 1-FCV-07-1A."
The inspector
reviewed the subject
SE.
The purpose of the
valve
and its relationship to containment isolation
and
containment
boundary integrity were found to be
appropriately considered.
The
SE concluded that
no
unreviewed safety question
was introduced
by placing the
valve in an open position.
The
SE went
on to provide
3
"required/recommended"
actions:
0
0
17,
~
Administrative controls,
consisting of caution tags
and the installation of plastic covers
over switches,
were required to be implemented locally and at the
pump
1A to prevent inadvertent
operation
of the
pump.
~
Operators
were to be informed of the
new valve
alignment with emphasis
given to
pump
surveillances
and
A SDC train operation.
~
Procedures
were to be reviewed for impact.
The
stated that,
in lieu of procedure
changes,
administrative controls
may
be used while the valve
was open.
The
SE was
approved
by the
FRG on August
12.
Upon
completion of the evaluation,
the
STAR was turned over to
Mechanical
Maintenance with a required action of restoring
the valve to original design
and to perform
a root cause
investigation into the failure.
The inspector
noted that
the subject
STAR included
no indication that the required
actions listed
above
had
been
completed prior to
Engineering releasing
the
STAR to Mechanical
Maintenance
and prior to Operations
repositioning
FCV-07-1A.
The
inspector questioned
the
STAR coordinator
as to who was
responsible
for ensuring that the SE's required actions
were complete
and
was informed that Engineering,
as the
organization
responsible
for the resolution,
was
responsible.
The
same question
was
posed to the
Engineering Chief Site Engineer,
who stated that the
responsibility for completing the action belonged to
.Operations.
The inspector
reviewed
OI 16-.PR/PSL-2,
Rev 1,
"St. Lucie Action Report
(STAR) Program,"
and found that
the pr'ocedure
was unclear
as to who was responsible for
ensuring
the activities were completed.
As
a result the
inspector
concluded that
a weakness
existed
in the
program with regard to ensuring that required corrective
actions
were documented
and completed.
On August 15,
a Night Order was issued
which informed
operators
that the unit would be operated
with FCV-07-1A
open.
The Night Order went on to state
"See attached
Engineering evaluation
which includes actions to be taken
to avoid
an accidental
spraydown of containment."
The
limited its consideration for the potential of inadvertent
spraydown to inadvertent
pump starts,
except
as
provided in the
second
required action
summarized
above.
On August
16, caution tags
were
hung
and the valve was
taken to
an
open position.
Containment
Spraydown
J
0
18
On August
18, venting of the
A train was
commenced
per
OP 1-0420060,
Rev 0, "Venting of the
Emergency
Core
Cooling and Containment
Spray Systems."
When the
A train
was pressurized
through the
SDC heat exchangers,
the open
flow path created
to the
through FCV-07-IA
allowed water to be drawn from the
RWT and
passed
into the
containment
atmosphere
via the spray header.
Operators
were alerted to the event
by an annunciator
indicating high reactor cavity inleakage. 'ndicated
flow
into the cavity was increasing rapidly and operators
entered
ONOP 1-0120031,
Rev 23,
"Excessive
System
Leakage."
Approximately one minute after the
'nnunciator
was received,
operators
identified the
flowpath leading to the
spraydown
and secured
the
A LPSI
pump.
The spraydown resulted
in
a slight decrease
in
containment
temperature
and pressure.
The licensee
noted
that
90 percent of containment
smoke detectors
alarmed or
faulted
and
an electrical
ground developed
in the lA2 SIT
sample valve
as
a result of the event.
Impact
on Unit
1
The licensee
determined that approximately
10,000 gallons
of water from the
RWT was transferred
to containment
during the event.
The water
was borated
at approximately
2200
ppm.
The spray resulted
in an increase
in
contamination fevels inside containment,
with levels
exceeding
Ix10
dpm/100
cm
in many areas.
Following the event,
the licensee
placed
a hold on all
work on Unit 1.
The unit was maintained
stable in Mode
3
and
management
announced
that it would conduct
a series of
meetings with all plant personnel
to discuss
the recent
events
on Unit
1
and to reiterate
management 'expectations
for worker performance.
Meetings
were held
on August
18
in which the Division President,
the Site Vice President,
and the Plant General
Manager stressed
the
need for worker
vigilance, procedural
compliance,
and
a questioning
attitude
on the part of all plant personnel.
Additionally, plant management
made plans to cool
down
Unit
1 to allow for a decontamination
of containment,
a
repair of FCV-07-1A,
and
a number of other work items
prior to returning the unit to service.
The licensee's initial plans for containment
cleanup did
not bring the contamination levels to pre-event
conditions.
After discussions
with management,
a decision
was
made to expand
the
scope of this cleanup
and
decontamination
to reduce
the
need for additional
cleanup
during the next refueling outage.
0
19
The inspector toured the containment
on August
19.
briefings prior to entry indicated that the majority of
the contamination
was in
a smearable
form.
Containment
cleanup
had
begun,
and guidelines
had
been
developed
and
promulgated
under
LOI-HP-23, "Oecontamination
Following
Inadvertent
Spraydown of the Unit
1 RCB."
The inspector
noted that the
62 ft. elevation of containment
had
been
separated
into quadrants
for initial decontamination.
While light water spotting
was noted
on the outer surfaces
of some equipment,
no obvious
boron deposits
were
identified.
Water was observed
to be puddled in upturned
I-beams supporting floor grating,
but floor surfaces
were
dry.
The licensee
evaluated
the event in Engineering
Evaluation
JPN-PSL-SENS-95-017,
"Assessment
of Inadvertent
Containment
Spray Event."
Items considered
in the
evaluation
included:
~
Boric acid corrosion of carbon steel
components,
potential effects
on
EQ and
non-EQ instrumentation
and electrical
equipment.
~
Potential effects
on cranes
and supports
~
Potential effects
on snubbers
~
Potential
effects
on containment
Corrective actions resulting
from the evaluation
included
a comprehensive
inspection of components
inside
containment.
Included were visual inspections
of all
inside containment
following containment
washdown
for decontamination.
The inspection list compiled by
engineering
included
items to be inspected
by tag number,
the type of inspection to be performed,
acceptance
criteria,'and
actions to be performed if acceptance
criteria was not met.
In all, approximately
1000
individual inspections
were performed.
Of the items
inspected,
only minor deficiencies
were identified.
Evaluation of the Licensee's Activities
The inspectors
concluded that the root cause of the
containment
spraydown
event
was
a failure of OP 1-0430060,
Rev 0, "Venting of the
Emergency
Core Cooling and
Containment
Spray Systems,"
to require
a verification of
initial conditions.
Specifically, the procedure failed to
verify that the
CS system
was in an alignment which was
appropriate for the evolution being conducted.
The
procedure
was revised to remove the subject portion,
leaving only static venting,
on September
1.
The licensee
20,
reached
a similar conclusion
in LER 335/95-007,
and
added
that contributing factors included operators failing to
realize that plant conditions at the time of the evolution
would result in the event.
Additionally, the licensee
identified that the decision to defer the repair of FCV-
07-1A contributed to the event.
The failure to include
appropriate initial conditions in OP 1-0430060 constitutes
a violation (VIO 335/95-15-08,
"Inadequate
Procedural
Initial Conditions" ).
The inspectors
reviewed the licensee's
corrective actions
as they related to containment
inspections
following the
event.
The inspectors
found that the licensee's
evaluation of the event
and the inspection
scope resulting
.from the evaluation
was in agreement
with the
NRC position
on the subject
(as described
in the
NRR DST Safety
Evaluation
on the subject,
transmitted to regional offices
via letter from T.E. Murley on March 13,
1991).
The
licensee's
inspection
was determined
to be comprehensive
in scope
and detail
and adequate
to ensure future
component reliability.
6)
Primary Water Storage
Tank Overfill
On August 19, at approximately 5:30 p.m., the Unit
1
RCO
directed the
SNPO
and
ANPO to fill the
PWST.
At approximately
7:45 p.m., the "Primary Water Tank Level High/Low" alarm
annunciated
in the control
room.
The
RCO directed the
SNPO to
have the
ANPO secure
the fill valve to the
PWST while making
his rounds.
The decision to delay securing
the valve was based
on the
RCO using
a tank strapping table in the control
room
which. showed
a margin of approximately
1.5 feet, from the high
level alarm to tank overflow.
At 8:30 p.m.,
a call
was
received
from the Unit
1 containment
ramp that the
PWST was
overflowing.
At that time the
ANPO and
SNPO were directed to
immediately secure
from filling the
PWST.
The fill valves were
then closed.
It was estimated
that about eleven
thousand
gallons overflowed form the tank.
Chemistry
samples
found that
no release
limit's were exceeded
as
a result this event.
The cause of this event
appeared
to be inappropriate
and
untimely operator
response
to an alarm coupled with an existing
operator work around
on the level control
system for the
PWST.
The
PWST level control valve LCV15-6 had
a history of
unreliability.
Because of this unreliability, the operator
had
been manipulating
V15106 or V15105 which are in series with
LCV15-,6. If this condition had
been correcte'd,
the system
would have
been able to automatically maintain
PWST level.
7)
2A Heater Drain
Pump Trip
21
At 8:20 a.m.,
on August 23, the
"LP Heater
2-4A Level Hi/Lo"
alarmed
in Unit 2 control
room.
The operator
observed that
2A condenser
back pressure
had increased
from 4.5
to 4.9 inches
Hg.
Immediately thereafter,
the
2A heater drain
pump tripped.
The control
room operator
immediately entered
ONOP 2-0610031,
Rev
13,
Loss of Condenser
Vacuum,
and
began
reducing
power to maintain condenser
back pressure
to less
than
4,0 in Hg.
Power
was reduced
and the unit was stabilized at 82
percent.
The inspector
responded
to the control
room and
observed this power reduction.
An investigation of the event
by the licensee
found that relay
63X-4A (a
HGA relay),
common to both the
4A alternate
and
5A
normal heater drain valves
had failed.
This failure caused
the
4A alternate
drain valve solenoid to de-energize
and the val've
to fail open.
It also caused
the
5A normal drain valve to fail
closed.
These failures resulted
in a rapid decrease
in level
in the
4A heater
and tripped the
4A heater drain
pump.
The inspector
found that operators
response
to the event
was
timely and correct.
The failed relay was subsequently
replaced.
An investigation
by the licensee
determined that the
relay failure was
due to aging.
A review of other applicable
uses of this type relay by the licensee
found and replaced
several
other
HGA relays in the heater drain system.
The inspector
noted that at least eight other heater drain
pump
trips had occurred
over the past
two years.
None of these
trips were the result of a
HGA relay failure.
The
licensees'eview
of this
and other recent
HDP trips led them to install
a
PC/N in the heater drain
pump protection cir cuiting during this
outage that should result in
a reduction of these
and similar
HDP trips.
The inspector
found that the licensee's
corrective action for
this event
was detailed
and thorough.
However, taking into
consideration
the previous
number of HDP trips that
had
occurred
and the licensee's
knowledge of this problem
and the
needed
changes
clearly indicate that corrective action
on this
item was not timely.
This item is identified as
a weakness
in
corrective action.
Control
Room Logs
On August 24, during
a review of the Unit 2 control
room
RCO
log, the inspector
noted
an entry which stated that
28
EDG had
erratic load swings during the performance of the monthly
surveillance tests.
Further review of the lo'g indicated that
the
EDG was taken out of service to replace
an air start
and then tested
and returned to service.
The
RCO,
on the shift after this item occurred,
was questioned
on
the entry involving the erratic load swings
and
was not aware
0
22
of the cause
or any corrective action taken
on this potential
deficiency.
This item was discussed
in detail with the system
engineer
who was able to satisfactorily address
this item.
AP 0010120,
Rev 74,
"Conduct of Operations,"
section 2.A.3,
requires that problems
associated
with major equipment
be
logged,
The inspector
noted that the control
room log should
have contained
adequate
information to allow the operator
on
a
succeeding shift to clearly understand
this potential
problem
and
know if it had
been
adequately
addressed
to ensure
operability of this
ESF component.
In addition to the above,
on September
1,
a review of the Unit
1 00S log found that containment
purge valve FCV-25-4 had
PWOs
95013857
and
95004327
and
STAR 94110479
issued
against it.
The
valve had
been
placed in the failed closed position but had not
been
entered
in the
OOS log.
OP 0010129,
Rev 24,
"Equipment
Out of Service," section 3.2, required that inoperable
TS
equipment that is out of service
be logged.
Upon
identification by the inspector this item was entered
in the
00S log.
On September
2, the inspector
noted that clearance
1-95-009-011
had
been
issued to deenergize
1B
EDG fuel oil transfer
pump to
permit work on
a local switch.
A review of the
OOS log and
control
room log also found that this had not been entered
in
either
as required
by the clearance
procedure
OP 0010122 step
5.6.5.
A discussion
with the
RCO revealed that
he did not
think this entry was necessary
since the
EDG was out of service
for other maintenance
activities.
This item was discussed
with
the
ANPS who directed that the appropriate
log entries
be made.
The inspector
noted that all of the
above
items were in a safe
condition
and did not affect system operability.
These
items
do indicate
a weakness
in logkeeping that could result in
operating
the plant with equipment out of service that could be
required for that operational
mode.
This item is identified as
a weakness
in logkeeping
and
a failure to follow procedures.
The licensee
response
to this item has led to significant
improvements
in the
amount of detail provided in control
room
logs.
They also plan to implement computerized
control
room
logs.
Since this item has minimal safety
importance
and
corrective action is underway to prevent recurrence
and the
licensee efforts meet the criteria specified in section VII of
the
NRC Enforcement Policy, it will not be cited.
It will be
identified as
a Non-Cited Violation (NCV 335/95-15-08 "Failure
to Follow Logkeeping
Procedures" ).
Operation of 1B LPSI
Pump with the Suction'Valve
Closed
On August 29, Unit
1 was in mode
5 with both trains of SDC in
operation.
At 2:20 p.m., the
B train of SDC was placed in
23
standby to allow a
SDC hot leg suction valve leak test to be
performed
as specified
in data
sheet
25 of AP 1-0010125A.
Step
6.5.4.B of this test left one hot leg suction valve
V3651 open
and the'ther
hot leg injection valve closed at the completion
of the test.
The
SDC normal operating
procedure
OP 1-0410022,
section 8.3,
was then
used to return the
B train of SDC to
service.
Instead of using the procedure,
the
RCO transposed
the procedural
steps of section 8.3 to
a separate
piece of
paper
and
used this to perform the procedural
steps.
Using
this guidance
he failed to open
and lock open
B hot leg suction
valve V3652 as required
by procedure
step 8.3.7.
The
1B LPSI
pump was then started
by the board
RCO who noted
the starting
surge
on the
pump ammeter
and that the
amperes
had
subsequently
declined
and steadied
out at about
15 amperes.
The
ANPS opened
the
LPSI discharge
valve at the
CRAG panel
to
re-establish
flow in the
B LPSI loop,
The board
RCO did not
recognize that
pump
B amperes
were lower than anticipated.
The board
RCO then went to the
CRAC panel
to initiate flow to
B
At about 4:45 p.m., the
NPS identified that
pump amperes
were lower than anticipated.
At the
same time the desk
RCO
found that the hot leg suction valve V3652 was shut.
The
1B
LPSI was secured
and the
1B
SDC train was returned to the
standby lineup.
A subsequent
inspection of the
pump determined
that
no apparent
damage
had occurred during the short period of
pump operation.
After an inspection
and evaluation the
pump
was returned to'service
and all parameters
were normal.
An
ASNE Section
XI test
was subsequently
performed satisfactorily.
The failure of the operator to follow OP 1-0410022 is
a
violation (VIO 335/95-15-04,
"Failure to Follow Procedures
during Alignment of Shutdown Cooling System" ).
This failure
could have resulted
in the failure of the
1B LPSI
pump
and
subsequent
loss of one loop of SDC.
1B Emergency
Diesel
Generator
Failure
On August 31, the
1B
EDG tripped due to high crankcase
pressure
in the
12 cylinder engine during the performance of the monthly
surveillance test,
OP 1-2200050B,
"1B
EDG Periodic Test
and
General
Operating Instructions."
Licensee
personnel
found that
the engine coolant expansion
tank had drained
and the engine
oil
sump level
had increased
approximately eight inches
above
normal.
Inspection
by licensee
personnel
revealed that the number nine
power pack crown
and cylinder head
had sustained
severe
damage,
apparently
due to separation
of the northeast
exhaust
valve
head
from its stem.
The failed valve head
became
loose within
the combustion
chamber
and during numerous
strokes
punctured
24
the piston crown
and cylinder,
The engine coolant then'eaked
through the cylinder head
and piston into the oil and entered
the engine
sump,
The source of the high crankcase
pressure
trip was
a combination of intake air and exhaust
gases
escaping
through the failed piston into the crankcase.
The licensee
developed
a root cause
investigation
team
composed
oF personnel
from mechanical
maintenance,
technical staff, site
and corporate
engineering,
and
an engine
vendor representative.
This team performed
a detailed investigation
over several
days
which concluded that the most probable root cause
was:
Cylinder number
9 lash adjuster lock nut loosened.
The
screw
was then able to back out of position
due to normal operational
vibration.
As the lash adjuster
screw loosened,
the hydraulic lifters
initially compensated
for the increased
height of the
valve bridge assembly.
Eventually the increased
height of
the valve bridge resulted
in impact loading at the locking
ring in the lower spring seat.
The locking ring is
normally unloaded
during operation.
The impact loading eventually
caused
the bridge guide to
fail.
This allowed further bridge movement
and loss of
"zero lash" in the valve train.
The increased
clearances
resulted
in impact loads
being transmitted to the valves
themselves.
The bridge guide failure also increased
wear
on the guide's
lower spring seat.
The impact loading caused
the lock grooves of both east
valve spring
stems to deform due to fretting wear from the
valve spring seat .locks.
The northeast
val've spring seat
eventually failed due to hoop stresses
induced
by the
wedging action of the seat locks.
The failed spring seat
was retained
by the helical spring
coil which initially prevented 'valve stem detachment.
The
additional
clearances
provided
by the failed spring seat
allowed the seat
locks to progressively fail due to
wedging
and point loads until they finally released
the
valve and allowed it to drop into the engine cylinder.
The valve head
separated
from the
stem due to impact
loading
by the piston.
The separated
valve head
was then
loose in the cylinder and punctured
the piston crown and
the cylinder head
when the piston rose.
Engine tripped
on high crankcase
pressure
due to flow of
turbocharged inlet air and exhaust
gases
through the
piston into crankcase.
Water from broken cylinder head
water passages
flowed through the piston into the
25
crankcase
to drain the expansion
tank.
Smaller particles
from the piston
and cylinder head
were blown into the
exhaust ducting.
The inspector
conducted daily meetings with the manager of'the
root cause
team
and discussed
the status of their investigation
and findings.
He also observed
numerous
facets of the licensee
investigation,
inspections,
and repairs to the affected diesel
engine.
The initial plans called for replacement
of the number
9 power
pack (cylinder and piston)
and inspection of all shaft
bearings.
After inspections
found several
metal parts
from the
damaged
number. 9 cylinder in the exhaust
ports of other
cylinders
and
on the engine
exhaust
intake
screens,
the engine inspection
was
expanded
to include all
cylinders,
exhaust
and bearings.
This inspection
found
some rust in number
12 cylinder and led to replacing that
power pack also.
The inspection of the remaining cylinders
also led to replacing
number
3
and
4 cylinder heads
due to
leaking
valves.'fter
the above repairs
and bearing
inspect'ions,
the engine
was
reassembled
and flushed with new lubricating oil and all
filters were replaced.
As
a result of the root cause
investigation
the lash adjuster locking nuts were torqued to
a
50 ft-lbf value given by the
EDG service
company (this value
had not been previously specified in the vendor manual
or
licensee
maintenance
procedures).
This torquing
was
accomplished
on all cylinders for both the
1A and
1B Unit
1
diesel
engines.
After a series of maintenance
runs
and
adjustments
on September
5 and 6, the
1B
EDG successfully
completed its surveillance test
and
was declared
on
September
6.
The inspector
found the root causes
investigation
team to be
composed of well-qualified individuals.
They pursued
the
issues
associated
with the failure in
a diligent manner
and
worked well with the personnel
performing engine repairs.
The
inspector noted that the licensee's
service
vendor plans to
also perform
a root cause
investigation of this failure.
The inspector
was very impressed
with the teams that worked the
engine repairs
around
the clock.
Their detailed investigation
resulted
in expanding
the scope of inspection
and repair to
cover the entire engine.
The overall repair effort was
strongly supported
by site
and corporate
engineering
and
resulted
in timely completion of the
repairs.'nit
2 Hain Generator
Hydrogen Overpressurization
26
On September
7, at approximately I:30 a.m.,
a
NPO noted that
the hydrogen
pressure
on Unit
2 generator
was at
58 psig.
This
pressure
is normally maintained
at
57 to 60 psig,
The
contact'ed
the
RCO and notified him that
he would be bringing
the pressure
up to approximately
60 psig,
When the hydrogen
supply header
was aligned to the generator,
control
room
"H2 Nanf Sply Press
Hi/Lo" alarmed
as expected
due
to low header
pressure
and remained illuminated.
The
NPO left the area to continue his rounds.
At approximately
2:00 a.m.,
the control
room requested
the
NPO come to the
control
room and assist
in a digital electro hydraulic loss of
load test.
This test
was completed
at about 2:24 a.m.
The
then completed his round
and returned
to his office area.
At about 3:20 a.m.,
the
ANPS noticed that the
"H2 Hanf Sply
Press
Hi/Lo" annunciator
was illuminated.
The
RCO checked
the
hydrogen pressure
and found it to be 80 psig.
The
RCO then
directed the
NPO to secure
the hydrogen
and reduce
the
generator
gas pressure
to 60 psig.
Licensee investigation of this event determined that the
and control
room operators
did not apply sufficient detail to
the progress
of this evolution.
The
NPO allowed himself to be
assigned
to another
task
and lost control of the status of the
evolution.
The generator
hydrogen filling evolution was not
adequately
tracked
by the
RCO and
ANPS.
They also permitted
the
"H2 Hanf Sply Press
Hi/Lo" annunciator
to stay illuminated
for about two hours
when the filling evolution should
have
taken approximately
30 minutes.
The licensee
also found that
a
generator
high gas pressure
alarm should
have
sounded
and
actuated
an annunciator
in the control
room.
The local alarms
were found to be inoperable with existing
PWOs that required
work.
This event pointed out
a failure of the
NPO and
RCO to maintain
status while adding hydrogen to the main generator
and the
failure to reset
a control
room alarm.
It also
showed that
an
operator
must stay
aware of the status of alarms
on equipment
and take compensatory
actions if normal
are not
available.
This item is identified as
a weakness.
A subsequent
inspection
and evaluation
by the equipment
vendor
determined that the generator
had not been
damaged
as
a result
of this event.
Plant Housekeeping
(71707)
Storage of material
and components,
and cleanliness
conditions of
various
areas
throughout
the facility were observed
and
no safety
and/or fire hazards
were identified.
I
J
0
27
d.
Clearances
(71707)
During this inspection period,
the inspectors
reviewed the following
tagouts
(clearances):
~
1-95-009-011 - on
1B fuel oil transfer
pump.
The inspector
found the clearance
tag in place
and the breaker
in the off
position
as required.
~
2-95-09-002
control valve V-3661 for SIT outlet drain valve
to
RDT.
The inspector
found the valve in the closed position
with fuses
removed
from RTGB-206.
No deficiencies
were identified.
e.
Technical Specification
Compliance
(71707)
Licensee
compliance with selected
TS
LCOs was verified. -This
included the review of selected
surveillance test results.
These
verifications were accomplished
by direct observation of monitoring
instrumentation,
valve positions,
and switch positions,
and
by
review of completed
logs
and records.
Instrumentation
and recorder
traces
were observed for abnormalities..
The licensee's
compliance
with LCO action statements
was reviewed
on selected
occurrences
as
they happened.
The inspectors verified that related plant
procedures
in use
were adequate,
complete,
and included the most
recent revisions.
f.
Effectiveness
of Licensee
Controls in Identifying, Resolving,
and
Preventing
Problems
(40500)
1)
Licensee Self Assessment
The inspector
reviewed
a special
gC assessment
of decisions
'hat
led to the inadvertent
spraydown of Unit
1 containment.
This assessment
was requested
by the
FPL Nuclear Division Vice
President
and focused
on the plant's decision to operate
Unit
1
with FCV 07-1A in the open position
and the development
and
execution of new procedure
OP 1-0420060,
"Venting of Emergency
.
Core Cooling and Containment
Spray System."
This review found
that operating
the
CS system in an abnormal
lineup
and
executing
a new procedure
under this condition,
coupled with
operator error resulted
in spraydown of Unit
1 containment.
The assessment
also noted that schedule
pressure
may have
prevented timely repair of. the
CS valve
FCV 07-1A.
The
inspector
noted that the assessment
was detailed
and provided
some
recommendations
for improvement.
The inspector
also noted that the assessment
identified that
the quarterly surveillance test directed that
FCV 07-lA be
lubricated
immediately prior to the performance of its
scheduled
surveillance.
The inspector questioned this practice
0
28
since prelubricating the valve prior to performance of the
surveillance test would not result in testing the valve's
ability to provide the required
response
time during
an
actuation.
The licensee
agreed with this
and changed .the
procedure
to delete
the prelubrication
under
TCN 2-95-177
on
September
7,
1995.
The inspector also questioned
why
QA had not documented this
deficiency under the
STAR program
as required
by QI 16-PR/PSL-
2,
Rev
1, "St. Lucie Action Report
(STAR) Program," Section
5. 1, "Initiation of a
STAR Form."
As
a result of the question,
a
STAR was generated
on September
6.
The failure to document
the subject finding via the
STAR process
is
a violation (VIO
335/95-15-05,
"Failure to Follow Procedure
and
Document
a
deficiency
on Containment
Spray Valve Surveillance
Test
Procedure" ).
g.
Unit
1 Restart Activities
The inspector
accompanied
maintenance
QC on
a walkdown of the Unit
1
containment prior to unit restart.
This inspection
by
QC was
conducted after departmental. heads
had completed their final
inspection,
as specified in AP 0010728.
It was noted that these
department
tours
had
been
completed
and signed off (with a few
exceptions
for items that would be
as
a part of unit restart).
The
inspector
and
QC identified approximately
40 deficiencies that
needed
to be corrected prior to unit restart.
These
included:
Burned out lights
Hissing covers
on electrical outlets
and components
Electrical
box and panel
covers that
had not been tightened
Areas that needed
additional cleaning
Some small trash
and debris
on top of components
A scaffold that
had not been
removed
Hissing screws
and bolts in various
components
Hissing conduit covers
The inspector
noted that the majority of the deficiencies
were the
responsibility of Electrical Haintenance.
A meeting
was
hei.d with
the Haintenance
Hanager to discuss
the items after the inspection
was complete..
He indicated that these
items would be corrected
prior to restart and,that
responsible
managers
would be counseled
on
this item.
The inspector
found that the
QC walkdown was very thorough.
Discussions
with
QC found that
QC had conducted
several
inspections
prior to this final closeout
inspection to .verify that containment
was being prepared for closeout.
IR 94-24 noted that at the
completion of the Unit
1 refueling outage
in November
1994 the
NRC
also
accompanied
QC on the final closeout
inspection
and identified
similar conditions to that found in this inspection.
That
IR also
identified that heavy management
reliance
was placed
on
QC to verify
\\
0
29
the readiness
of containment
closure.
Although containment
was
returned to
a final satisfactory condition it appears
tliat licensee
management
is employing
gC in a line function rather than quality
verification role.
This item is identified as
a management
weakness.
4.
Haintenance
and Surveillance
'a ~
Haintenance
Observations
(62703)
Station maintenance activities involving selected
safety-related
systems
and components
were observed/reviewed
to ascertain
that they
were conducted
in accordance
with requirements.
The following items
were considered
during this review:
LCOs were met; activities were
accomplished
using
approved
procedures;
functional tests
and/or
calibrations
were performed prior to returning components
or systems
to service; quality control records
were maintained; activities were
accomplished
by qualified personnel;
parts
and materials
used
were
properly certified;
and radiological controls were
implemented
as
required.
Work requests
were reviewed to determine
the status of
outstanding
jobs
and to ensure that priority was assigned
to safety-
related
equipment.
Portions of the following maintenance
activities
were observed:
1)
PWO 61/5570
and
PWO 61/5571
Remove
1402
and
1404 from
pressurizer,
repair
as necessary
and reinstall.
The valves
had
been identified as inoperable
and the
above
PWOs
were generated
to remove the valves,
determine
the cause of
failure and correct.
The valves
were
removed
and worked using
HP 1-H-0037,
Rev 6,
"Power-Operated
Relief Valve Haintenance."
The inspector
observed
selected
portions of the valve
disassembly
and troubleshooting
to determine
the cause of
failure.
These efforts involved several
shifts over several
days.
This work was accomplished
in a contaminated
work area
in Unit 2 RAB.
The inspector
noted that
HP coverage
was
provided
and that
a vendor representative
assisted
maintenance
in this effort.
The inspector
also noted that continuous
supervisory oversight
and engineering
support
were present
in
the field to provide for a timely repair of these
components.
These
items were worked around the clock since they delayed
plant restart.
The inspector also noted that calibrated tools
were being
used
and that
gC provided coverage of this job.
The
inspector
found that work procedures
and
PWO were in the field
and being used.
At the completion of the
above work, the inspector
reviewed the
completed
work package
documentation
and
found that
TC had
been
implemented for requir'ed
procedure
changes,
repair parts,
and
work was correctly documented,
and other support documentation
was properly filled out.
30
Overall,'he
personnel
performing this task were adequately
qualified and
used the appropriate
procedures.
The overall
work effort resulted
in identifying, correcting the problem
and
returning the
PORVs to service.
Adequate supervisory,
engineering,
and vendor support
was provided to successfully
complete the task in
a timely manner.
See
IR 95-16 for a
detailed description of the root cause of the noted
inoperability.
PWO 1230/65 Perform
PCH 11-195
on
DG IA/1B,
The inspector,
while conducting routine plant inspections,
observed that work on this modification was in progress
on
18.
Two electricians
were completing the work activities
associated
with installing new splice
boxes for the trip
solenoids
on the
12
and
16 cylinder engines for DG 1B.
The
inspector
reviewed the
PWO and procedure that the technicians
were using.
He noted that the work was nearly complete
on the
12 cylinder engine,
but only the first few steps of the
procedure
had
been
signed off.
He questioned
the electrician
as to what work had
been
completed
and the electrician stated
that
he had terminated
the wiring, torqued the connections,
and
applied several
layers of different types of tape in the
sequence
indicated
by the
PC/H.
Noting that only a few steps
of the
PC/H had
been
signed off, the inspector
asked specific
questions
as to the wiring identification, torquing
requirements,
and
sequence
and type of tapes
used.
The electrician
was unable to locate the guidance
provided for
wiring identification for correct termination
and admitted
that,
although
he
had torqued the connection
to the correct
value,
he did not'ocument this in the work package
when the
step
was accomplished.
He also stated that
he
had taken over
this job from another
individual
and
had only scanned
through
the work package
instructions
and details.
Further review of
his work activity and the work package
by the inspector
determined that the connections
had
been correctly made
and the
correct torque value
had
been
used.
The circuitry was tested
on the night of August
31
and
performed satisfactorily.
The inspector discussed
this item in
detail with the Maintenance
Manager
and noted that. not filling
out procedural
steps
as they are accomplished,
doing only
a
cursory review of a work package,
and not being knowledgeable
of all aspects
of the job can lead to serious errors or
mistakes
in the performance of maintenance activities.
The
Maintenance
Manager stated that
he agreed with the inspector's
observations
and that corrective action would be taken in this
concern.
ADM-08.02,
Rev 7,
"Conduct of Maintenance,"
Appendix 5, Step
5,
required that procedures
be present
during work and that
31,
individual steps
be initialed once performed.
The noted
failure of the electrician to initial procedural
steps
on an
as-completed
basis
is
a violation (VIO 335/95-15-06,
"Failure
to Initial Haintenance
Procedure
Steps
as work was completed" ).
A deficiency very similar to this
had
been identified by the
NRC to Maintenance
in IR 95-10,
3)
PWO 95-02-4066
Remove Cylinder Head
No, 9, Inspect for Damage.
This
PWO was later expanded
to perform repairs.
The inspector
conducted periodic inspections
of these activities
as they
occurred over
a period of approximately
one week.
Additional
details
and evaluation of this work is contained
in paragraph
3.b.11).
Surveillance
Observations
(61726)
Various plant operations
were verified to comply with selected
TS
requirements.
Typical of these
were confirmation of TS compliance
for reactor coolant chemistry,
RWT conditions,
containment
pressure,
control
room ventilation,
and
AC and
DC electrical
sources.
The
inspectors verified that testing
was performed in accordance
with
adequate
procedures,
test instrumentation
was calibrated,
LCOs were
met,
removal
and restoration of the affected
components
were
accomplished
properly, test results
met requirements
and were
reviewed
by personnel
other than the individual directing the test,
and that any deficiencies identified during the testing
were
properly reviewed
and resolved
by appropriate
management
personnel.
The following surveillance test
was observed:
1)
OP 1-220050A,
1A
EDG Periodic Test
and Operational
Inspection.
The inspector
observed this special
test that was done
as
a
result of identified oscillations in
EDG frequency
and voltage.
This test
was modified to permit operation
unloaded for one
hour followed by
a one hour full load test.
The unloaded test
was completed satisfactorily.
Near the
end of the
one hour
loaded run,
a ground
was identified in the
DG control
system.
The ground
was located in the wiring from the engine control
panel
to the governor
on the
16 cylinder engine.
This faulty
wire was replaced
and the engine retested
satisfactory.
The
system engineers
vigorous pursuit of the ground led to timely
identification and repair.
Overall the performance of this
test
was satisfactory.
ILC Training and Qualification (41500)
The purpose of this inspection
was to conduct
a review of the
qualifications
and training of IKC personnel.
This inspection
was
conducted
in accordance
with the requirements
of 10 CFR 50
F 120.
The
inspector
reviewed the scope
and content of IEC maintenance
training
under the guidance of Inspection
Procedure'.41500,
"Training and
32
gualification Effectiveness"
and
NUREG-1220, "Training Review
Criteria and Procedures."
The inspector
examined
the facility's procedures
and administrative
controls with respect
to
I&C training, the self evaluation report,
the Maintenance Training Instructional Materials
Upgrade Project
Report,
a selection of student
feedback
forms, the
ILC lesson
plans'tructure
and format,
and all of the
I&C examination results.
The
inspector
also interviewed personnel
regarding
the nuclear
training program for Journeymen
and Specialist.
I&C Technicians
were interviewed using the
Incumbent protocols in NUREG 1220,
Rev l.
The inspector identified no strengths
or weaknesses
in the training
and qualification arena.
However
a weakness
was identified in the administrative
procedures.
It was not clear to the inspector that proper job supervision
(as
directed
by ADH-08.02,
"Conduct of Maintenance"
and
AP 0010432,
"Nuclear Plant
Work Orders" ),
was being maintained during the
conduct of safety related
work by unqualified
I&C journeymen
(see
details
below).
This issue currently has
low safety si'gnificance
since the work that was performed
(see
PWO 93033900 description
below)
had
no adverse
affect
on safety related
equipment or the
health
and safety of the public.
The inspector
concluded that the
I&C training program incorporated
a Systems
Approach to Training.
The inspector identified no violations or deviations
in the area of
I&C training.
In February,
1994,
two
PSL Journeymen
were tasked
to calibrate Unit
2
RCS Pressurizer
Pressure
Loop Transmitter,
PT-1102D
(PWO
93033900).
The licensee
was unable to prove through documentation
that the two Journeymen
were qualified to do the task.
However,
one
of the two
PSL Journeymen
had
been previously
a qualified
supervisor
at Turkey Point.
That Journeyman
appeared
to be well
qualified to perform this calibration,
however
he had not completed.
the required
I&C training for basic qualifications at St Lucie.
The inspector
reviewed
how the licensee
addressed
maintenance
to be
performed
by
I&C Journeymen
that
had not completed
basic
qualifications at St Lucie.
Administrative Procedure
ADH-08.02,
Conduct of Maintenance,
which states
that
"If personnel
not
possessing
the required training or qualification are assigned
to
a
work activity, increased
instruction detail or "on the job"
supervision
is required."
Administrative Procedure
0010432,
Nuclear Plant Work Orders,
contains
a caution which states, if the assigned
i.ndividual is not
on the qualification list for that component,
the following
additional
steps
must
be taken:
1)
Must have additional
supervisory oversight or specific
procedural
guidance.
33
2)
Must have greater detail in the
NPWO work description.
ADH-08.02 states
that the supervisor
must
be "on the job" which
implies continuous
supervision.
AP 0010432 states
that the
supervisor
must provide "supervisory oversight."
The facility
contends
that "supervisory oversight"
does
NOT insinuate
continuous
supervision.
The facility stated that additional oversight
was provided
by the
IKC supervisor.
The inspector
reviewed the work order
and
.interviewed the two journeymen
who conducted
the maintenance.
The
journeymen
stated that additional oversight
(out of the ordinary)
was not provided.
Additional oversight
was neither requested
by the
facility nor identified by the inspector
on the work order,
The inspector's
review of the calibration data revealed that the
instrument
was in calibration
and
had received
supervisory review.
Therefore, this issue
had low safety significance
since the work
that
was performed
had
no adverse affect
on safety related
equipment
or the health
and safety of the public.
However,
a procedure
inconsistency
existed
in which the facility had committed to resolve
via Temporary
Change
Request
TC-95-213
and
a procedure
change
request
to
ADM 08.02.
The licensee
plans to change
ADM 08.02 to
reflect
AP 0010432 thus requiring additional supervisory oversight
in lieu of on the job supervision.
The inspector
concluded that the
statements
in both procedures
regarding
journeyman qualifications
were weak.
5.
Engineering
Support
(37551)
A concern involving the lack of prompt corrective action
on
a plant
generic
problem associated
with relief valves
was identified and will be
discussed
in IR 95-20.
A concern involving the assumptions
used in engineering
evaluation
JPN-
PSL-SEMP-95-101,
which evaluated
the impact of V3439 setpoint
and
blowdown on plant operations,
was identified,
The licensee
is currently
reviewing the issue.
Engineering
support of diesel
generator
repairs
and root cause
evaluation
of the diesel failure and pressurizer
power operated refief was found to
be effective.
6,
Plant Support
(71750)
a.
Fire Protection
During the course of their normal tours,
the inspectors
routinely
examined
facets of the Fire Protection
Program.
The inspectors
reviewed transient fire loads,
flammable materials
storage,
34.
b.
housekeeping,
control
hazardous
chemicals,
ignition source/fire risk
reduction'fforts, fire protection training, fire protection
system
surveillance
program, fire barriers, fire brigade qualifications,
and
gA reviews of the program.
No deficiencies
were identified.
Physical
Protection
During this inspection,
the inspector toured the protected
area
and
noted'hat
the perimeter
fence
was intact
and not compromised
by
erosion or disrepair.
The fence fabric was secured
and barbed wire
was angled
as required
by the licensee's
Physical
Security Plan.
Isolation zones
were maintained
on both sides of the barrier
and
were free of objects
which could shield or conceal
an individual.
The inspector
observed
personnel
and packages
entering the protected
area
were searched
either by special
purpose detectors
or by
a
physical
patdown for firearms,
explosives
and contraband.
The
processing
and escorting of visitors was observed.
Vehicles were
searched,
escorted,
and secured
as described
in the
PSP.
Lighting
of the perimeter
and of the protected
area
met the 0.2 foot-candle
criteria,
C.
In conclusion,
selected
functions
and equipment of the security
program were inspected
and found to comply with the
requirements.
Radiological
Protection
Program
Radiation protection control activities were observed
to verify that
these activities were in'onformance with the facility policies
and
procedures,
and in compliance with regulatory requirements.
These
observations
included:
Entry to and exit from contaminated
areas,
including step-off
pad conditions
and disposal
of contaminated
clothing;
Area postings
and controls;
Work activity within radiation,
high radiation,
and
contaminated
areas;
Radiation Control Area
(RCA) exiting practices;
and,
Proper wearing of personnel
monitoring equipment,
protective
clothing,
and respiratory
equipment.
7.
Other Areas
The following plant organizational
changes
were
made during the report
period:
J. Scarola. was reassigned
from Manager of Operations
to Plant
General
Manager.
J.
West
was reassigned
from Manager of Site Services
to Manager of
Operations.
35
~
C. Burton was reassigned
form Plant General
Manager to Manager of
Site Services.
~
L. Rogers
was reassigned
from Instrument
and Control Maintenance
Supervisor to Manager of System
and
Component
Engineering.
~
P. Fulford was assigned
as Operations
Support
and Testing
Supervisor,
a new position in Operations
that will be responsible
for inservice,
surveillance,
predictive,
and post maintenance
testing.
~
R. Olson
was promoted to Instrument
and Control Maintenance
Supervisor.
8.
Exit =Interview
The inspection
scope
and findings were
summarized
on September
15 and
October
11,
1995, with those
persons
indicated in paragraph
1 above.
The
inspector described
the areas
inspected
and discussed
in detail the
inspection results listed below.
Proprietary material is not contained
in this report.
Dissenting
comments
were not received
from the licensee.
Plant
management
was
aware of the large
number of issues
that were being
discussed
at the exit and expanded
the normal
attendance
to include
a
large
number of supervisors,
operators,
maintenance,
and plant support
personnel.
They appeared
to desire that the exit information be
disseminated
to as
many plant personnel
as possible.
The exit appeared
to be well received
by plant management
and staff.
At the exit
conclusion,
the site vice president
and plant general
manager
commented
on:
Plant performance
not
up to past standards.
Need for improvement.
Need to set
new standards.
Personal
accountability.
Identifying and fixing problems.
~T
e
Item Number
50-335/95-15-01
Open
"Failure to Follow
Procedures
and Block MSIS
Actuation,"
paragraph
3.b.
50-335/95-15-02
Open
Two Examples of "Failure to
Follow Procedures
during
Seal
restaging,"
paragraph
3.b.
50-335/95-15-03
Open
"Failure to Follow Procedure
and
Document
abnormal
valve
36
position in the Valve Switch
Deviation Log,"
paragraph
3.b.
50-335/95-15-04
50-335/95-15-05
50-335/95-15-06
50-335/95-15-07
Open
Open
Open
Open
"Failure to Follow
Procedures
during Alignment
of Shutdown Cooling System,"
paragraph
3.b.
"Failure to Follow Procedure
and
Document
a deficiency
on
Containment
Spray Valve
Surveillance
Test
Procedure,"
paragraph
3.b.
"Failure to Initial
Maintenance
Procedure
Steps
as work was completed,"
paragraph
3.b.
"Failure to Follow
Procedures
during venting of
System resulted
in
Containment
Spraydown,"
paragraph
3,b.
50-335/95-15-08
Closed
"Failure to Follow
Logkeeping Procedures,"
paragraph
3b.
9.
Abbreviations,
and Initialisms
ADM
Administrative Procedure
Nuclear
One
ANPO
,
Auxiliary Nuclear Plant [unlicensed]
Operator
ANPS
Assistant
Nuclear Plant Supervisor
Air Operated
Valve
Administrative Procedure
ASME Code American Society of Mechanical
Engineers
Boiler and Pressure
Vessel
Code
Component
Cooling Water
CFR
Code of Federal, Regulations
cm
Centimeter
CRAC
Control
Room Auxiliary Control
(panel)
Containment
Spray
(system)
Containment
Spray Actuation System
Chemical
8 Volume Control
System
Diesel
Generator
dpm
Disintegration
Per Minute
Demonstration
Power Reactor
(A type of operating license)
DST
Division of Systems
Technology
EDT
ESDE
F
FI
FR
FRG
gph
gpm
HDP
Hg
HPES
HUT
IR
J/LL
JPN
lbf
LCO
LER
MFIV
MV
No.
NPF
NPWO
NRC
Emergency
Core Cooling System
Emergency
Diesel
Generator
Equipment Drain Tank
Engineering
Package
Environmentally Qualified
Excessive
Steam
Demand
Event
Engineered
Safety Feature
Engineered
Safety Feature Actuation System
Fahrenheit
Flow Control Valve
Flow Indicator
The Florida Power
5 Light Company
Federal
Regulation
Facility Review Group
Final Safety Analysis Report
General
Electric Company
Gallon(s)
Per Hour (flow rate)
Gallon(s)
Per Minute (flow rate)
Hydraulic Control Valve
Heater Drain
Pump
A GE relay designation
Mercury (element)
Health Physics
Human Performance
Enhancement
Systems
High Pressure
Safety Injection (system)
Holdup Tank
Heat
Exchanger
.
Instrumentation
and Control
[NRC] Inspection
Report
Jumper/Lifted
(Juno
Beach)
Nuclear Engineering
Pounds
Force
TS Limiting Condition for Operation
Level Control Valve
Licensee
Event Report
Loss of Coolant Accident
Letter of Instruction
Low Pressure
Low Pressure
Safety Injection (system)
Main Feed Isolation Valve
Main Steam Isolation Signal
Motorized Valve
Number
Nuclear Production Facility (a type of operating license)
Nuclear Plant Operator
Nuclear Plant Supervisor
Nuclear Plant
Work Order
Nuclear Regulatory
Commission
NRC Office of Nuclear Reactor Regulation
Nuclear Regulatory
(NRC Headquarters
Publication)
NWE
ONOP
OP
PC/M
PGM
ppm
psia
psld
pslg
PSL
PWO
PWST
QI
RCB
RCO
RDT
Rev
RII
SNPO
St.
TCB
TCN
TS
VIA
38
Nuclear Watch Engineer
Off Normal Operating
Procedure
Out Of Service
Operating
Procedure
Operator
Work Around
Plant Change/Modification
PerCent Milli (0.00001)
Procedure
Change
Request
NRC Public Document
Room
Plant General
Manager
Power Operated Relief Valve
Part(s)
per Million
Pounds
per square
inch (absolute)
Pounds
per square
inch (differential)
Pounds
per square
inch (gage)
Plant St.
Lucie
Physical
Security Plan
Plant
Work Order
Primary Water Storage
Tank
Quality Assurance
Quality Control
Quality Instruction
.
Reactor Auxiliary Building
Reactor
Containment Building
Reactor Control Operator
Pump
System
Reactor Drain Tank
Revision
Region II - Atlanta, Georgia
(NRC)
Reactor Turbine Generator
Board
Refueling Water Tank
Shut
Down Cooling
Safety Evaluation
Tube Rupture
Senior Nuclear Plant [unlicensed]
Operator
Saint
St.
Lucie Action Request
Temporary
Change
Trip Circuit Breaker
Temporary
Change Notice
Technical Specification(s)
[NRC] Unresolved
Item
Volume Control
Tank
By Way Of
Violation (of NRC requirements)
i V
I
0