ML17227A455

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Insp Repts 50-335/92-07 & 50-389/92-07 on 920324-0502. Violations Noted.Major Areas Inspected:Plant Operations Review,Maint Observations,Surveillance Observations,Fire Protection Review & Preparation for Refueling
ML17227A455
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 05/29/1992
From: Elrod S, Landis K, Schin R, Michael Scott
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17227A453 List:
References
50-335-92-07, 50-335-92-7, 50-389-92-07, 50-389-92-7, NUDOCS 9206150031
Download: ML17227A455 (33)


See also: IR 05000335/1992007

Text

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++*++

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W.

ATLANTA,GEORGIA 30323

Report Nos.:

50-335/92-07

and 50-389/92-07

Licensee:

Florida Power

5 Light Company

9250 West Flagler Street

Miami, FL

33102

Docket Nos.:

50-335

and 50-389

License Nos.:

DPR-67

and

NPF-16

Facility Name:

St. Lucie

1 and

2

Inspection

Conducted:

arch

24 - May 2,

1992

Inspectors:

S.

.

o , Sensor

Ress

ent

nspector

Date

lgne

. A. Scott,

Re

ent Inspector

Dat

Sig ed

Approved by:

R.

. Sch n,

roj t Engineer

ls

ection

le

Division of Reactor Projects

D te Si

ne

at

lgne

SUMMARY

Scope:

This routine resident inspection

was conducted onsite in the areas of plant

operations

review, maintenance

observations,

surveillance observations,

evaluation of licensee

self-assessment

capability, fire protection review,

preparation for refueling, review of special reports,

review of nonroutine

events,

followup of previous inspection findings,

and followup of regional

requests.

Results:

This inspection

found Unit 1 continuing to operate in a routine manner with an

obvious regard for safety.

Unit 2 set

a light water reactor world record of

502 days of continuous

power operation

when it shut

down on April 20 for

refueling.

During the Unit 2 shutdown,

the turbine did not trip automatically

or manually when the operators

tripped the reactor.

Immediate operator

response

was excellent

and subsequent

root cause investigation

has

been

vigorous.

Preparation

and control of entry into reduced inventory were quite

well controlled.

A number of surveillances

and maintenance activities were

well performed.

One procedure violation was 'observed while setting

steam

generator safety valves.

Another violation of technical specifications

was

observed

involving isolation of a containment

pressure

transmitter sensing

line.

920615003k

920529

PDR

ADOCK 05000335'PR

Within the areas

inspected,

the following violations were identified:

VIO 389/92-07-03;- Isolation of Containment

Pressure

Sensing

Line Without

Placing Effected Instrumentation

Channels

in Trip or Bypass

as Required,

paragraph

2a.

VIO 389/92-07-04,

Failure to Follow Procedure for Setting

Steam Generator

Safety Valves, paragraph

5k.

Within the areas

inspected,

the following non-cited violations were identified

associated

with events

reported

by the licensee:

NCV 335/92-07-01,

Fuel Handling Building Ventilation Radiation Monitor

Out of Service

Due to Personnel

Error, paragraph

9a.

NCV 335/92-07-02,

Containment

Atmosphere Particulate

and

Gaseous

Radioactivity Monitors Out of Service

Due to Personnel

Error, paragraph

9b.

REPORT DETAILS

Persons

Contacted

Licensee

Employees

D. Sager,

St. Lucie Plant Vice President

G. Boissy, Plant General

Manager

J. Barrow, Fire/Safety Coordinator

H. Buchanan,

Health Physics

Supervisor

C.--Burton, Operations

Manager

R. Church,

Independent

Safety Engineering

Group Chairman

R. Dawson, Maintenance

Manager

R. Englmeier,

Nuclear Assurance

Manager

R. Frechette,

Chemistry Supervisor

J. Holt, Plant Licensing Engineer

C. Leppla, Instrument

and Control Supervisor

L. McLaughlin, Licensing Manager

G. Madden, Plant Licensing Engineer

A. Menocal, Mechanical

Supervisor

T. Roberts, Site Engineering

Manager

L. Rogers, Electrical Supervisor

N. Roos, Services

Manager

C. Scott,

Outage

Manager

M. Shepherd,

Operations Training Super visor

D. West, Technical

Manager

J. West, Operations

Supervisor

W. White, Security Supervisor

D. Wolf, Site Engineering Supervisor

E. Wunderlich, Reactor Engineering Supervisor

Other licensee

employees

contacted

included engineers,

technicians,

operator s, mechanics,

security force members,

and office personnel.

NRC Employees

  • S. Elrod, Senior Resident

Inspector,

St. Lucie Site

  • M. Scott, Resident Inspector,

St. Lucie Site

R. Schin, Project Engineer,

Division of Reactor Projects

  • Attended- exit interview

2.

Acronyms=and=. ini:tial.-isms- used-throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707)

Unit-1 began

and ended the inspection period at power - day

131 of

continuous

power- operation-.-

Unit 2 began the inspection period at power and then shut

down on April 20

for a normal refueling outage.

The outage

was scheduled

to last until

June '27.

Unit 2 set

a light water reactor world record for continuous

power operation during this just completed

run of 502 days.

E

Plant Tours

The inspectors periodically conducted plant tours to verify that

monitoring equipment

was recording

as required,

equipment

was

properly tagged,

operations

personnel

were'ware of plant conditions,

and plant housekeeping

efforts were adequate.

The inspectors

also

determined that appropriate radiation controls were, properly

established,

critical clean areas

were being controlled in accordance

with procedures,

excess

equipment or material

was stored properly,

and combustible materials

and debris

were disposed of expeditiously.

During tours,

the inspectors

looked for the existence

of unusual

fluid leaks, piping vibrations, pipe hanger

and seismic restraint

settings,

various valve and.breaker.

positions,

equipment caution

and

danger tags,

component positions,

adequacy of fire fighting

equipment,

and instrument calibration dates.

Some tours were

conducted

on backshifts.

The frequency of plant tours

and control

room visits by site management

was noted to be adequate. "

'he

inspectors routinely conducted partial

walkdowns of ESF,

ECCS,

and support systems.

Valve, breaker,

and switch lineups

as well as

equipment conditions were randomly verified both locally and in the

control

room.

The following accessible-area

ESF system

and area

walkdowns were made to verify that system lineups were in accordance

with licensee

requirements

for operability and equipment material

conditions were satisfactory:

Unit 2

CCW platform,

Unit 1 AFW trestle

space,

Unit 1 mechanical

penetration

room,

and

Unit 2

ICW pump area.

On April 29, during

a tour of the Unit 2 containment,

the inspectors

observed

an instrument sensing line penetrating

the containment at

penetration

58.

The penetration

was labeled to indicate that.its

function involved differential pressure

between the containment

and

RAB.

The sensing line was capped.

Subsequent

pressure test

confirmed the sensing line to have indeed

been isolated.

Drawing

2998-8-231,

sheet

P136,

Instrumentation Installation Details Unit 2,

Rev 1, showed that this line served safety-related

PT-07-2C,

channel

"C" containment

pressure

transmitter.

This transmitter provided one

of four containment

pressure

signals for several

safety functions-

reactor trip, containment isolation actuation,

containment

spray

actuation,

and safety injection actuation.

When found, this sensing

line and associated

transmitter,

one of four, was not available to

perform its safety function for either the

RPS or ESFAS.

The

pressure

transmitter would behave

as if the channel

were in "bypass."

Three conditions contributed to the probability of this occurrence:

(2)

(3)

The licensee

did not ensure

the sensing lines were open in

conjunction with equipment calibration or at the beginning of

operating cycles.

The licensee calibrated

containment

pressure

sensing

instrumentation

on

a refueling outage

basis

per

TS 4.3.1. 1 and

associated

table 4.3-1, Reactor Protective Instrumentation

Surveillance

Requirements,

and

TS 4.3.2. 1 and associated

table

4.3-2,

Engineered

Safety Features

Actuation System

Instrumentation Surveillance

Requirements,

which was

implemented

in part by ILC procedure

2-1400153C,

Reactor Protection System-

Engineered

Safeguards

System

Loop Instrumentation Calibration

for Containment Pressure..

This procedure

al,lowed test equipment

hookup near the pressure

transmitter in the

RAB, isolated

by

closing

a valve between

the test point and the containment

sensing point.

The sensing lines from the containment to the

pressure

transmitter were not specifically tested.

At the

conclusion of the

1989 refueling outage,

based

on an

NRC concern

that blockage of open-ended

sensing lines could exist yet be

undetected,

the licensee

blew down the sensing lines

and

verified air flow per plant work order 7826/62.

The licensee

did not subsequently

test the lines during the 1990 refueling

outage.

Drawings, procedures,

and labels did not clearly show the

function of sensing lines and differentiate between active

and

spare lines.

Two of the penetrations

involved had four lines in each.

Three

of the four lines were capped

and one

had

an open-ended

90

degree

male thread adaptor attached.

The other two penetrations

had

one line each with the open-ended

90 degree

male thread

adaptor attached.

One of these single lines

was the

one found

isolated.

Containment pressure

instrumentation

sensing

tubing

.and fittings penetrating

into the containment

were described

on

drawing 2998-B-231, sheet

P136.

Neither the drawing, nor

labels,

nor other reasonably

available information visually

showed which of the'ultiple lines were in service

and which

were the spares.

They all looked alike except for the end

fittings threaded

onto the pipes.

Drawings, procedures,

and labels did not clearly show the

acceptable

tubing and end-fitting configuration of sensing lines

inside containment.

Containment pressure

instrumentation

sensing tubing and fittings

penetrating into the containment

were described

on drawing

2998-B-231, sheet

P136.

Neither the drawing, nor labels,

nor

other reasonably

available information visually showed the

acceptable

tubing and end fitting configuration.

The bill of

material listed items that apparently

would result in an

open-ended

l'ine with an exposed

male tubing fitting thread at

the end.

In contrast,

the drawing did show, outside containment

in the

RAB, a 3/8 inch mud dauber

cap (item 70A) on the

transmitter high-side reference

sensing .line.. This. device was .-

intended to prevent blockage of the reference

sensing line by

for eign material

such

as

an insect.

The device also 'provided

a

finished appearance

.to the installation.

The inspector judged

that exposed

tubing threads

on the end of a line penetrating

containment,

coupled with poor labeling, would certainly invite

someone

to install

a cap during

a pre-startup

inspection.

Unit 2 TS addressed

this equipment in several

places

because

the

pressure

transmitter,

served: multiple safety. functions:.

~ 1

II

Unit 2 TS 3.3.2

and included Table,3.3-3 required that

ESFAS

instrumentation

be

OPERABLE for the Containment

Spray function

in Operational'odes

1, 2, or'3; including a minimum of three of

the four channels

of Containment

Pressure - High-High.

Action

Statement-

17 required that, with three of the four channels

OPERABLE, the inoperable

channel

must be placed in the tripped

condition within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

Action Statement

17 further stated

that-one additional

channel

may be bypassed for up to two hours

for surveillance testing.

Unit 2 TS 3.3.2 and included Table 3.3-3 also required that

ESFAS instrumentation

be

OPERABLE for the Safety Injection,

Containment Isolation,

and. Main Steam Line Isolation functions

in operational

Modes 1, 2, or. 3; including a minimum of three of

the four channels

of Containment

Pressure - High.

Action

Statement

13 required that, with three of the four channels

OPERABLE, power operation

may continue provided that the

inoperable

channel is placed in the bypassed

or tripped

condition within one hour.

Action Statement

14 required that,

with two of the four channels

inoperable,

power operation

may

continue provided that one of the inoperable

channels

has

been

bypassed

and the other inoperable

channel

is placed in the

tripped condition within one hour.

Unit" 2 TS; 3.3..1

and .included--Table 3.3-1 required that

RPS

instrumentation

be

OPERABLE. in operational

Nodes

1 or 2,

including

a- minimum of three of the four channels of Containment

Pressure - High.

Action Statement

2.a required that, with three

of the four channels. OPERABLE, power operation

may continue

provided that. the inoperable.'channel

is placed

on the tripped or

bypassed- condition within one hour.

Action Statement

2.b

required that, with two of the four channels

OPERABLE, power

operation

may continue provided that one of the inoperable

channels

has

been

bypassed

and the other inoperable

channel

is

placed in the tripped condition within one hour.

Containment Pressure

Channel

C (High and High-High) was actually

inoperable during the previous operating cycle from about at least

December,

1990, to April 22, .1992,

and possibly from April 13,.1989,

when the sensing line was last blown out,

because its instrument

sensing line inside containment

was capped,

and Containment

Pressure

Channel

C was not placed in the tripped or bypassed

condition as

required.

During most of this time, St. Lucie Unit 2 was operated

in

Mode

1 or 2.

Additionally, between

December,

1990 and April 22,

1992, with Containment

Pressure

Channel

C inoperable,

another

channel

of containment

pressure

was placed in bypass

on April 19,

1992, for

three hours while the unit was operated

in Mode

1 or 2.

Between

April 13,

1989 and April 22,

1992, with Containment

Pressure

Channel

C inoperable,

another

channel of containment

pressure

was placed in

bypass

on six different occasions, for a total of approximately

97

hours, while the unit was operated

in Mode

1 or 2.

This is identified as

VIO 389/92-07-03,

Isolation of Containment

Pressure

Sensing

Line Without Placing Effected Instrumentation

Channels

in Trip or Bypass

as Required.

Subsequent

to discovery of the capped

sensing line, the licensee

has

expeditiously evaluated

the potential root causes

and consequences

of

the condition.

Activities included:

(1)

Analysis of maintenance

and operating history to:

(a)

Bound the inoperability of containment

pressure

channel

C.

The Unit 2 sensing

lines were blown out on

19 April, 1989-

two outages

ago.

(b)

Correlate other

equipment

outages

due to maintenance

or

test.

(2)

Engineering analysis of the potential

accident

consequences

of

this channel

being inoperable.

The analysis

assumed .the entire

containment

spray system

was inoperable.

The licensee's

analysis

concluded that no containment

breach nor additional

core

damage

would occur.

(3)

Development of a technique to use

on an operating plant to check

Unit 1 and Unit 2 to ensure that the

same conditions

were not

present

elsewhere.

The inspector

observed

these tests

per

NPWOs

7340/63 (Unit 1) and 7452/64 (Unit 2).

The test consisted of

blowing air from a hand-carried

low pressure

storage

tank

through the sensing lines from a test connection

near the

transmitter.

The pressure

gage would indicate while air was

flowing but would immediately drop to zero when the tank's

discharge ball valve was shut, thus

showing

a clear flow path.

All four sensing lines for each of Unit 1 and Unit 2 were clear.

(4)

Search of operating

records

from previous reactor plant heatups

to determine if the isolated pressure

sensing line could have

been detected

during startup;

The licensee

concluded that the

lack of indication .was reasonable

based .on the containment

volume of'about 2.5 million cubic feet*and the small

amount of

heatup due.to containment cooling in operation.

(5)

Probabilistic Risk Assessment

PSL-2JFR-92-004

dated

Hay 7,

1992

and evaluating the risk input to St. Lucie Unit 2 due to the

isolation of PT-07-2C.

It concluded that the loss of that

channel

represented

a 3.9E-8 per reactor year increase

in CDF

over having all channels

operable.

The frequency calculated

was

1.23E-7 per reactor. year.. This was

compared .to NRC.criteria

listed in GL 88-20:.-

It was less

than the 1.0E-6 screening

value;

A St. Lucie total

CDF has not been determined.

Even if it

were as low as

1.0E-5 per reactor year, the 1.27E-7

contribution would be less

than the

5X of total

CDF

screening

value referenced

in GL 88-20.

Even if the evaluated

sequence

were conservatively

assumed

to result in core

damage

and containment failure, the

estimated

CDF was still less

than the 1.0E-6 screening

value.

Loss of the spray function did not constitute

a containment

bypass function.

The 1.2E-7 per reactor year sequence

would not therefore

be

considered potentially important.

(6)

Physical

and procedural

changes

were being pursued to identify

sensing lines opening into the containment or annulus

and to

ensure

the required status

would be easily understood.

Identification tags to indicate the purpose

and required

condition of these

sensing lines.

Changes

to procedures

for surveillance

and plant startup to

verify that the lines are clear.

Drawing revisions

as necessary

to capture

the required line

status

and to install end covers

(mud dauber screens)

on

the ends of the'lines.

The inspector

had

no further questions at the time.

Plant Operations

Review

The inspectors periodically reviewed shift logs and operations

.

records,

including data sheets,

instrument =traces,.

and records of

equipment malfunctions.

This review included control

room logs

and

auxiliary logs, operating orders,

standing orders,

jumper logs,

and

equipment tagout records.

The -inspectors routinely observed

operator

alertness

and demeanor

during plant tours.

They observed

and

evaluated

control

room staffing, control

room access,

and operator

performance

during routine operations.

The inspectors

conducted

random off-hours inspections

to assure that operations

and security

performance

remained at acceptable

levels.

Shift turnovers

were

observed to verify that they were conducted in accordance

with

approved

licensee

procedures.

Control

room annunciator

status

was

verified.

Except as noted below,

no deficiencies

were observed.

During this inspection period, the inspectors

reviewed the following

tagouts

(clearances):

2-3-104

2B

EDG [12 cylinder diesel

fan shaft repair],

2-3-35

HVE 10B Motor Replacement

[routine maintenance],

2-4-9

2A HPSI

pump breaker repair (see the maintenance

paragraph),

2-4-24

2B1 circulating water

pump out for water box

cleaning,

and

2-4-222

HVE 6B Heater Control Inspection.

Unit 2 commenced

a shut

down for refueling

on April 20.

Since this

was the first Unit 2 shutdown in 502 days,

both the licensee

and

inspector

showed additional interest in operating staff performance

and equipment reliability.

The operating staff performed well during

both routine evolutions

and unexpected

occurrences.

The licensee

treated

the shutdown

as

an infrequently performed evolution per

AP

0010020,

Rev 1, Conduct of Infrequently Performed Tests or Evolutions

at St. Lucie Plant,

and focused additional

management attention.

Pre-evolution briefings were held by the operations

supervisors

and

the procedures

were talked through at length

by the on-shift licensed

operators

during the shift prior to commencement.

Copies of needed

procedures

were -tabbed

and conveniently -placed in notebooks within

arm reach of the reactor control station.

The quality assurance

staff also provided extensive

coverage.

The licensee

performed initial power reduction per

OP 2-0030125,

Rev

14, Turbine Shutdown - Full Load to Zero Load.

Procedure

adherence

was excellent.

Reactor

plant and steam plant equipment generally

worked very well, with a few exceptions.

Prior to commencing

shutdown, the 2A train 6.9

KV circuit breaker

from the generator

auxiliary transformer would not open from the control

room to

transfer the switchgear

feed to the startup transformer.

The

shutdown

was delayed until the circuit breaker

was returned to

service in about

two hours.

During the power reduction,

the B-train

low-flow feedwater controller-level input failed, so an operator

manually controlled

2B

SG level from the control

room console.

At low power and late in core life, the licensee

found that axial

shape

index was difficult to keep within limits using the

CEA

controls allowed by TS.

The operators

had previously decided that,

if three of four pretrip alarms initiated, they would trip the

reactor manually rather than continue attempting

a manual

shutdown.

When these

alarms indicated at 2:38 a.m.

on April 21, the reactor

operator tripped the reactor from 12 percent

power and initiated

standard

post trip actions

per 2-EOP-01,

Rev 6, Standard

Post Trip

Actions.

Though the reactor trip itself was.uneventful .with reactor plant

safety equipment subsequently

performing as designed,

the turbine

trip function did not perform as designed.

The turbine did not trip

either automatically or,manually from the control board.

Operators

immediately carried out compensatory

actions,

including shutting the

main steam isolation valves, tripping the generator output circuit

breaker,

stopping the turbine control

DEH pumps,

and tripping the

turbine using the local manual control at the turbine front standard.

After the safety functions of 2-EOP-01 were met, the licensee

initiated 2-EOP-02,

Rev 5, Reactor Trip Recovery.

The licensee

subsequently initiated a root cause investigation

and maintained Unit

2 at normal no-load temperature for over 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

pending initial

investigation,

removal of certain

key components for dissection,

and

determination that no critical evidence

would be destroyed.

The licensee started reactor cooldown

on April 22 per

OP 2-0030127,

Rev 43, Reactor Plant Cooldown - Hot Standby to Cold Shutdown.

The

cooldown of about

35 degrees

per hour was plotted

as required using

data sheets

1, 2, and 3.

Unit 2 entered

operational

modes

4 and

5

later. that day.

During the inspection period, Unit 1 entered

a reduced

RCS inventory

condition to install

SG nozzle

dams.

The following items were

observed prior to or during this evolution:

Containment Closure Capability - Instructions were issued to

accomplish this; personnel

and tools were on station.

RCS Temperature

Indication - Four normal

mode

1 CETs were

available for indication.

Two were from train A and two from

train B.

RCS Level Indication - Independent

RCS wide and narrow range

level. instruments

which indicate in the control

room were

operable.

An additional

Tygon tube loop level in the

containment

was

manned during level changes

and checked

every

two hours during static conditions.

.

RCS Level Perturbations

When

RCS level

was altered, additional:

operational

controls were invoked.

At plant daily meetings,

operations

took actions to ensure that maintenance

did not

consider performing work that might effect

RCS level or shutdown,

cooling.

RCS Inventory Volume Addition Capability - Nominally one (of

three)

charging

pumps

and

a HPSI

pump were available for RCS

addition.

RCS Nozzle

Dams - Procedural

control

was via MMP-01.05,

Rev 0,

Steam Generator. Primary Side Maintenance.

This required the

pressurizer:manway

be removed prior to installation:of"nozzle

dams, that hot leg manways

be opened'rior to cold leg manways,

and that cold leg dams

be installed prior to hot leg dams.

The

removal of these

items is in the reverse

order.

Vital Electrical

Bus Availability - Both trains of vital power

were available.

Operations

would not release

busses

or

alternate

power sources for work.

Draindown was held

up pending

completion of emergent

work in the switchyard.

Overall, operational

controls were well planned

and executed.

The

off-normal Unit 2 turbine shutdown

was well handled.

c.

Technical Specification

Compliance

Licensee

compliance with selected

TS LCOs was verified. This included

the review of selected

surveillance test results.

These

verifications were accomplished

by direct observation of monitoring

instrumentation,

valve positions,

and switch positions,

and by review

of completed

logs and records.

Instrumentation

and recorder traces

were observed for abnormalities.

The licensee's

compliance with LCO

action statements

was reviewed

on selected

occurrences

as they

happened.

The inspectors verified that related plant procedures

in

use were adequate,

complete,

and included the most recent revisions.

d.

Physical Protection

The inspectors verified by-observation

during routine activities that

security program plans were being implemented

as evidenced

by: proper

display of picture badges;

searching of packages

and personnel

at the

plant entrance;

and vital area portals being locked and alarmed.

e.

Jumpers

and Lifted Leads

The inspectors

reviewed the Jumper/Lifted

Lead

book in each unit and

AP 0010124,

Control

and

Use of Jumpers

and Disconnected

Leads,

Rev.

10

25.

Each approved jumper/lifted lead request

had received extensive

review and approval, including technical

review by an STA, 50.59

review when appropriate,

approval

by an

NPS or

ANPS; and

FRG review

and Plant Manager approval

when appropriate.

Both electrical

and

mechanical

jumpers/lifted leads

were included.

Tags were

hung at the

location of the jumper/lifted lead (the inspectors verified two tags

located inside

an electrical cabinet).

The inspectors

noted that

a

total of about nine

RTGB annunciators

in the two units were affected

by jumpers/lifted leads.

One or all of the inputs to these

annunciators

were disabled.

However, this was not readily apparent

for operators.

There were

no sticker s

on the annunciators

or entries

in the related annunciator

panel status

books to ensure

operator

awareness.

This was identified .to the .licensee for review.

Jumpers/lifted

leads are temporary modifications*to the plant.

Several jumpers/lifted leads

had been in place for over two years.

The inspectors verified that these

were periodically reviewed

by the

licensee to ensure that permanent modifications were being pursued.

f.

Facility Review Group

The inspectors

attended

two

FRG meetings;

reviewed

FRG records;

reviewed

TS 6.5. 1, Facility Review Group;

and reviewed

AP 0010520,

- Rev. 21, Facility Review Group.

During the two meetings,

the

FRG

reviewed and approved four PCMs,

10 permanent

Procedure

Changes,

three Temporary

Changes

to procedures,

two Contractor

Procedures,

one

Instruction Manual

change,

two Jumper/Lifted

Lead requests,

one

NPWO,

and

one Work Process

Sheet.

The

FRG reviewed

items that

TS required

them to review and also many others,

such

as non-safety-related

procedure

changes.

A copy of each item to be reviewed

was present at

the

FRG meeting, with proposed

procedure

changes written clearly in

red to facilitate quick review.

A representative

from the sponsoring

department

was present

to describe the changes

and answer questions

.

as

needed.

If any

FRG member

was not satisfied with an item, it was

sent

back to the sponsoring

department for further answers

or

revisions to be presented

at

a future

FRG meeting.

The review of

each

item was

done quickly and efficiently.

The inspector verified that requirements for minimum

FRG meeting

quorum,

FRG member training, and appointment of alternate

members

were met.

TS requirements

were implemented

by AP 0010520.

FRG

member training records

and meeting minutes

were well organized.

The

inspector noted that the required written appointment of each

alternate

'member

was accomplished

by inclusion in the minutes of an

FRG meeting,

and that there

was

no approved list of alternate

members.

This was identified to the

FRG Chairman (Plant Manager) for

review.

As

FRG review of an item was completed,

the

FRG chairman ensured that

no member had any objections to approval,

then signed the item with

Plant Manager approval.

At one of the

FRG meetings,

the Plant

Manager

was the

FRG Chairman.

In the other

FRG meeting,

the Plant

Manager was not present

and the Operations

Superintendent

was

alternate

FRG Chairman.. The inspector

found. that it was.common

practice for an alternate

FRG chairman to sign

a required Plant

Manager approval

on documents.

However,

'AP 0010520 did not authorize

an alternate

FRG chairman to sign for required Plant Manager

approval.

This was identified to the Plant Manager, for..review.

Licensee Control of Important Equipment Not Included in Technical

Specifications.

During the inspection period,

as

a response

to IN 92-06, Reliability

of ATWS Mitigation System

and Other

NRC Required

Equipment Not

Controlled by Plant TS, the inspectors

reviewed implementation

aspects

of the

ATWS rule (10 CFR 50.62).

-The

IN addressed

perceived

problems at other utilities..in keeping the

ATWS equipment

in. service.

Notices of Violation against the'ule itself had

been

issued at other

sites

even

though

no TS had

been issued in the area.

ATWS equipment provides

an alternate

means for emergency insertion of

CEAs [rodsj to terminate nuclear power generation.

ATWS equipment

was not required to be safety-related.

At this site, the equipment

was bought as safety-related,

but was not addressed

as

safety-related.

Both units at this site have the

ATWS equipment installed

and

operational.

Routine plant tours of the control

rooms

and

RABs have

not indicated

problems with this utility maintaining their

ATWS

equipment.

Daily and weekly tours

have found the equipment in

service

and functional.

Actuation circuitry and initiation

components

have

been found to be configured properly.

Procedures

existed that calibrated the

ATWS equipment

and checked its

functionality on

a routine b'asis.

Different features of the system

have been

checked

and calibrated

as required

on

a monthly, six month,

or outage basis.

Inspector analysis of the administrative features

surrounding the

ATWS equipment revealed that additional controls

may be necessary.

The rationale for the additional controls are discussed

below:

(1)

Unit 1 AP 1-0010123,

Rev 82,,Administrative Control of Valves,

.Locks and Switches,

provided control methods for selected

components.

At the time the

ATWS was

added,

the keys that

contr ol

ATWS bypass

features

were added to procedure

Appendix

"A", Key Locker Index.

This got the

ATWS keys accounted for on

a quarterly basis,

and the keys were required to be checked in

and out of the controlled key locker when used.

12

Procedure

section 7.3 discussed

the "Valve, Switch Deviation

Log".

The log was

used to maintain

a record of

other-than-normal

equipment configuration.

The

ATMS bypass

locks and associated

circuitry were physically

located in the

ESFAS cabinets,

which contained

many locks for

safety-related

channels,

and

had locked doors.

Section 8.11 of

the above procedure listed the

ESFAS cabinet lock and door keys

but neither it, nor other instructional sections

of the

procedure, listed or dealt with ATWS keys.

This omission meant

that the keys were not required to be entered in the "Valve,

Switch Deviation Log".

The equivalent Unit 2 procedure

required

ATWS bypass

key usage

be logged in the above mentioned

log for that unit for-

configurational. purposes;

'The

ATWS bypass

keys were-also

.

discussed

in the Unit 2 procedure's

instructional text.

The

operators

on both units, out of force of habit from the in-use

proceduralized

methodology for controlled

keys in general,

would

have utilized the log for the subject

keys in any case.

The licensee

agreed to change Unit 1 AP 1-0010123 to match the

Unit 2 procedure

regarding

ATMS bypass

key configuration

controls.

On both units, the placing of an actuation circuit in bypass

with a key would remove the

ATWS trip feature from one

CEA MG

set.

Since the

ATMS trip must open the output of both

CEA MG

sets to be effective, the probability of the

ATWS logic circuit

producing

a reactor trip would go to zero - essentially

placing

the

ATWS system out-of<<service.

Although the other

ATMS

actuation cir cuit would still be available for tripping the

second

MG set,

power from the first MG set would maintain the

CEAs'ositions

unless

the primary safety-related trip feature

(RPS)

had deenergized

the

CEAs.

This situation

was

a departure

from the logic change

associated

with the bypassing of a

RPS

trip channel

in that the

RPS trip logic changed

and the

proximity to trip was increased.

The above fact was not general

knowledge to the licensee staff.

There was

no general

information available/apparent

to the

operations staff.

INC personnel

were aware of the facts.

Operations

has

agreed to place plastic tags

on the

ATWS

actuation circuit bypass

keys stating to the effect that bypass

of the circuit would place the

ATMS system out of service.

Further, the licensee

was considering

changing both

units'dministrative

control of valves, locks,

and switches

procedures

to indicate this information.

13

The above licensee

interactions

indicated

a positive commitment to

improvement.

Plant controls

and response

to events during various:evolutions

were

excellent.

One violation was identified .in this area concerning

a capped

containment

pressure

transmitter sensing line.

The inspector

had no-

further questions

at this time.

3.

Surveillance Observations

(61726)

Yarious plant operations

were verified to comply with selected

TS

requirements.

Typical of these

were confirmation of TS compliance for

reactor coolant chemistry,

RWT conditions,

containment. pressure,

control

room ventilation,

and

AC. and

DC electrical

sources.

The inspectors

verified that testing

was performed in accordance with adequate

procedures,

test instrumentation was::calibrated,'.COs

were met,'emoval

and restoration of the affected

components

were accomplished

properly,

test results

met requirements

and were reviewed

by personnel

other than

the individual directing the test,

and that any deficiencies identified

during the testing were properly reviewed

and resolved

by appropriate

management

personnel.

The following surveillance tests

were observed:

a.

OP 1-0640020,

Rev 33,

ICW System Operation

[1B ICW pump]

b.

OP 1-2200050,

Rev 61,

Emergency Diesel Generator Periodic Test

and

General

Operating Instructions

[1B EDG, three separate

tests]

On April 3, the inspector

observed

the 20th weekly idle start test of

1B

EDG per OP-1-2200050B,

1B Emergency Diesel

Generator

Periodic Test

and General

Operating Instructions.

This test

was to be the last in

a series of 20 weekly starts to meet

TS Table 4.8-1 requirements-

based

on the previous failure history.

The

EDG started

and ran

properly at idle speed

and at rated

speed,

however following EDG

warmup, the control

room operator

was unable to close the

EDG output

circuit breaker.

The licensee

aborted the test

and subsequently

stopped

the

EDG per the procedure.

The inspector

had

no further

questions

concerning

these actions.

Troubleshooting at the

EDG control cabinet per

NPWO 5139/65 found the

"frequency relay" K49 not functional.

This relay's function was to

prohibit

EDG output breaker closure until an

EDG frequency near

60 Hz

(above

54 Hz) is reached.

The failed relay was subsequently

found to

function'properly in the shop.

Since the relay failure mode would

require detailed investigation,

a replacement

relay, identical but

not dedicated for the proper quality level, was tested for

installation.

The inspector

observed that the new relay performed

identically to the old one.

Relay test performance is further

discussed

below.

Following relay installation, the licensee's

successful

idle start retest

was also observed

by the inspector.

Following the

EDG retest,

the licensee

continued to declare the

EDG

"out of service" but functional

pending completion of the

new relay's

dedication

package.

During the shop testing of the

new K49 .relay, the inspector

observed

that the

new relay performed identically to the .old one (i.e., the

contacts

were closed at low.frequency

and opened at about 62.5 Hz).

Neither relay functioned in the manner the inspector

expected (i.e.,

relay contacts

would remain

open until a predetermined

frequency

was

reached - then close to enable the

EDG output circuit breaker to

close).

The inspector requested

the licensee to evaluate this

observation.

The existing relays were Westinghouse

style

177C717G03

60 Hz/120

V

over-frequency relays.

Westinghouse

instruction sheet

I,.L. 14443

described

a 1-2 Hz .differential between

open

and close functions, but

was ambiguous

concerning whether or not the contacts

open or close

on

increasing

frequency.

Also, the relay specified in the

EDG vendor

manual,

on drawing 8770-2421,

was Westinghouse

relay style

117C717G03,

not 177C717G06.

The licensee

confirmed with

Westinghouse,

Morrison-Knutson,

and

EBASCO that:

The vendor manual

number was

a typographical error,

Westinghouse

relay style

177C717G03

was intended to be

an

over-frequency

relay whose contacts

would be open above the

setpoint.

The design basis,

as described

in FSAR section 8.3.1.1.7.d.

and

Figure 8.3-5 was for the relay contacts to be open below the

setpoint to prohibit EDG output circuit breaker closure until

the

EDG reached at least

90 percent of rated voltage

and

frequency.

The relays,

as installed, failed to perform this function.

The

installation,

as installed, deviated from a written comoitment in the

FSAR.

Specification of improper relays

was considered

to be

a

generic design issue.

The

NRC vendor branch

and industry

organizations

were notified.

Further enforcement action was not

considered

because of the licensee's

extremely prompt and effective

corrective action and because

the existing installation's

actual

performance

met safety requirements.

The licensee-found=that

the

EDG frequency permissive function was

performed

on St. Lucie Unit 2 and at Turkey Point by a different.

relay,

a WILMAR ELECTRONICS model

20-050 relay.

That relay was also

qualified for safety-related

service.

The licensee

prepared

PCM

116-192M, procured

and tested

the relays,

and installed them on both

1A and

1B EDGs on April 4 per the

PCM and

NPWO 5141/65.

The

EDGs

were subsequently

tested

per the

PCM package

and temporarily changed

versions of OP 1-2200050A and B.

Since the

EDGs were not fast start

tested,

the last fast start times were evaluated

as still bounding

by

15

adding

an increased

relay actuation time to the previous strip chart

data.

The licensee's

response

upon discovering this design error

was

notably swift and thorough,.involving coordination .of a number of

departments

and vendors.

1A EDG retest

on April 26 following replacement of the

16 cylinder

radiator fan idler shaft.

The fan belt appeared

loose

and flapped

excessively,

about two inches deflection

on each of the short spans.

The vibration analysis

crew measured

about

70 mils vibration.

The

EDG remained out of service for further corrective action.

OP 1-0700050,

Rev .37,:Auxiliary Feedwater

Periodic .Test

[1C AFW

pump].

I&C 2-1130050,

Rev 7, Loose Parts Monitoring System Periodic Test.

MP 2-0950184,

Rev 1, Fast

Dead

Bus Transfer Surveillance Test.

This

test

was properly aborted

when the B-train 4

KV circuit breaker for

the generator auxiliary transformer failed to close.

Subsequent

troubleshooting

per the recently written large breaker

troubleshooting

procedure

MP-0920069,

Rev 0, proved that the circuit

breaker

was satisfactory but the synchronizing switch in the control

room had failed.

A piece of trash

had gotten inside and jazzed the

switch action.

The inspector

observed

periodic- testing of the Main, Startup,

and

Auxiliary transformer control circuits and alarms per

OP 1-0910051,

Rev 8, Hain Transformer Periodic Test,

OP 1-0910050,

Rev 12, Startup

Transformer Periodic Test,

and

OP 1-0910052,

Rev 7, Auxiliary

Transformer Periodic Test; respectively.

During the test of 1A main transformer,

the operator closed

a wrong

switch by mistake but recognized

the error and corrected it.

There

were

no bad results

from- this error.

Review of the procedure

and

work site showed

a

human factors shortcoming in the procedure.

Procedure. section 8.6 listed switches

numbered

TS-2 through TS-15,

but the-procedure

step

numbers

were one number off [step

1 through

14], and easily mistaken for the switch number.

The switches

themselves

had adjacent

small text label plates but were numbered

on

the panel

face in pencil with incomplete nomenclature [just a

number].

- The numbers

resembled

the procedure

step

number more than

the switch number.

Step 8.7 then stated

"Place TS-7, 8, 9, 10, 11,

12 in TEST position." The operator placed TS-8, 9, 10, ll, 12,

and

13

in TEST..

Switch TS-13 involved a different function.

After reading

the label text, the operator

stopped

and corrected

the switch

alignment.

This was identified to the site procedures

group for

correction.

16

The

1A main transformer control cabinet contained

a number of devices

that had

a green colored

ooze

on the wire terminals.

.Examples

included undervoltage

relays

1 through 6, current transformers

1

through 6,

and relays

TR-1 and TR-2.

The green color came from

corrosion

caused

by breakdown of aging

PVC wire insulation found in

certain lots of such wire manufactured

about

20 years

ago.

The

insulation gives off a liquid that turns corrosive in air.

The

nonsafety-related

main transformer controls are serviced

by the

utility s system protection division.

This condition was identified

to the plant maintenance staff for'oordination of future repair.

During the test of the

2B startup transformer controls,

a large relay

hung up, causing

unexpected

indications.

The relay ultimately

started

smoking.

The operator recognized

the unusual

response

and

promptly summoned supervisory-aid.'hat

circuit was deenergized

pending repair.

The inspector

had

no further comments

on this surveillance.

The inspector

observed

the performance of OP 2-0400050,

Rev 12,

Periodic Integrated Test of the Engineered

Safety Features,

from the

control

room and

2B

EDG room.

This test

had

a number of sections

that were performed independently,

however the main body of the test

simulated

a loss of offsite power concurrent with a LOCA.

This

forced

EDGs to fast start

and automatically feed the safety busses,

and all the safety-related

pumps

and equipment to start.

EDG 2A

output circuit breaker

closed in 8.54 seconds

and

EDG 2B output

circuit breaker

closed in 9.86 seconds.

The standard

was

10 seconds.

Equipment not working during the test included:

2B Containment

Spray

Pump Automatic Actuation [The pump started

manuallyj,

2B1

RCP Oil Lift Pump [the circuit breaker

was faultyj, and

MFIV 09-1B operated

when tested with the AFAS test,

but failed

to fully close during the subsequent

MSIS test.

A sticky limit

switch limited valve closure to 90 per cent open.

The

1B

ICW pump was returned to service at the beginning of the

inspection period after being modified with a self lubricating

alteration.

PCM 281-189

removed the existing need for support

equipment to process

and to supply

pump discharge

water to lubricate

the water bearings

and

pump packing area.

The

1B pump became

the

third and final Unit 1'ump to be modified.

Post-modification

pump

surveillance

per

OP 1-01010020 established

new pump baseline

data

per

ASME Code Section XI.

AP 1-0010125,

Rev 87, Schedule of Periodic Tests,

Checks,

and

Inspections,

Check Sheet

6, Test Shield Building Ventilation System,

B-train.

This was

a 10-hour test run of the system

by plant

I

17

operators.

During the test,

the inspector

observed that the

6B fan

discharge

damper counterweight

arm was installed at

a different angle

than the equivalent item on the

6A fan,

and that it had

14 weights

while the

6A fan damper

had

2 weights.

After,,the surveillance

run

was complete,

the inspector

observed that the

6B damper would not

quite close,

though free,

because

of the amount of counterweight.

In

contrast,

the

6A fan damper required significant effort to open.

Both ventilation trains

have routinely demonstrated

that they would

perform their safety function in spite of the dampers.

The licensee

group developing

damper

PMs reviewed the situation, relocated

the

6A

counterweight

arm to match the

6B arm and adjusted

the weight on both

dampers.

Both dampers

now function well.

During this period the conduct of surveillance:activities

and response

to

unexpected

findings was excellent.

4.

Evaluation of Licensee

Self-Assessment

Capability (40500)

The inspector s. evaluated

the licensee's

self-assessment

programs to

determine whether they contributed to the prevention of problems

by

monitoring and evaluating plant performance,

providing assessments

and

findings,

and communicating

and following up on corrective action

recommendations.

'Portions of this evaluation

were accomplished

throughout the

SALP period

[November 1,

1990 to May 2, 1992] by various inspectors

and the results

are found in multiple IRs,

as follows:

IR 335.389/91-01,

paragraph

6 discussed

licensee

audit and reviews of

the Emergency Plan;

IR 335,389/91-03,

paragraph

1 and Appendix A (finding 91-03-09)

discussed

licensee self-audits prior to an EDSFI;

IR 335,389/91-04,

paragraph

2.b discussed

gA audit reviews in

performance monitoring, refueling activities,

and breaker

modification;

IR 335,389/91-09,

paragraph

7 discussed

10 CFR Part 21 closeouts

under the licensee's

Corrective Action Report program;

IR 335,389/91-10,

paragraph

2.b discussed

licensee

audits of

. operations;

and paragraph.7-discussed

CNRB review of plant

performance;

IR 335,389/91-16,

paragraph

9 discussed

management efforts in work

control programs;

IR 335, 389/91-18,

paragraph

3 discussed

the licensee

assessment

of

the

MOV program at the plant;

18

IR 335,389/91-201,

paragraph

2.5 discussed

licensee

audit findings in

the area of service water system;

IR 335,389/92-02,

paragraph

3 discussed

audit in the areas of offsite

dose,

process control,

and the. radiological environmental

program;

IR 335,389/92-03,

paragraph

2 discussed

implementation of changes

within the

ISEG program;

and,

IR 335,389/92-04,

paragraph

2.b discussed

licensee

audits in

surveillance,

gA program,

and performance monitoring.

The above

documents

reported

on diverse areas. under various

programs at

the site.

They noted that several-areas,

such

as the operations,

instrument

and control, electrical,

and chemistry were improving or

continuing to take positive .actions.--Two

team 'inspections

however

indicated areas

where improvement

was

needed

or weakness

was apparent.

The

NOV program was found to be in the early phases

of implementation

addressing

most generic letter

recommendations

but there were

some

concerns

about potential deviations

from the subject letters

and there

was

a lack of detail in some

NOV program aspects.

The service water team

found insufficient depth in certain areas of assessment.

In contrast,

an

EDSFI team inspection. considered

the licensee's

preparations

to be so

significant that they constituted

a safety

improvement.

Ouring the

day- to day inspections,

the licensee

had several

notable events

to which they. responded well. 'Unit 1 NSIV air control [support] solenoid

valves

had

a moisture entry problem that was resolved in a proper manner.

Engineering

and the electrical

department

had overall excellent corrective

action

on an, HFA relay latch manufacturing

problem that arose during the

Unit 1 refueling outage. and

a. diesel

generator

underfrequency

relay

problem that was identified in .1992 after the Unit 1 outage.

Although

they were slow- to. realize

a diesel fuel oil contamination

problem

initially, the licensee

responded

well with an extremely solid response.

On the whole, the licensee's

approach

to plant operations

during this

SALP

evaluation period was--very conservative

and demonstrated

continued

critical self assessment-.-.

Previous

inspection reports

have discussed electric motor failures at this

site in both safety

and non-safety related applications.

The failures

were- as follows:

Unit 1

1A ICW pump motor in Nay,

1990 (failed megger);

Unit 1

1A heater drain pump motor in April, 1990;

and Unit 1

1C

CCW pump

motor in February,

1991.

In response

to these failures to G.E. motors of

different model types, the licensee

has performed several

evaluations

and

developed

a methodology for rewinding these

motors utilizing a vendor,

their own electrical

department,

and site

gA personnel

to qualify the

rewind process

under-the extensive

EPRI guidance

documents.

To date,

the

above motors

and two additional

G.E. motors

have

been

rewound.

A suomary

of the. site's

analysis--and

planned activities inclusive of the Unit 2

~

~

lans are discussed

in FPL letter

JPN/ESI-92-086

dated

February 28,

1992

from A.R. Hall to W.N. Dean].

To date, the corrective actions

and

19

planned actions

have

been well thought out and well enacted.

The actions

have

been conservative

in maintaining plant reliability and demonstrate

excellent self assessment

at both the maintenance

and engineering levels.

The inspectors

conclude that the licensee

management

strongly supports

self identification of problems

and that the utility has

demonstrated

a

continuous pattern of success

in recognizing

and addressing

problems.

Individual exceptions

do not destroy this pattern.

5.

Maintenance

Observation

(62703)

Station maintenance activities involving selected

safety-related

systems

and components

were observed/reviewed

to ascertain

that they were

conducted in accordance

with requirements.

The following.items were

considered

during this review:

LCOs were.met; activities were

accomplished

using approved

procedures;

functional tests

and/or'alibrations

were performed prior to returning

components

or systems

to

service; quality control records

were maintained; activities were

accomplished

by qualified personnel;

parts

and materials

used were

properly certified; and radiological controls were implemented

as

required.

Work requests

were reviewed to determine the status of

outstanding

jobs and to assure

that priority was assigned

to

safety-related

equipment.

Portions of the following maintenance

activities were observed:

a.

NPWO 4883/66 - HVE 10B Fan Motor Replacement

(MP 0940062C,

R11,

The

Overhaul of Motors).

b.

NPWO 8361/62 - Sequence

of Events

Recorder

Repair

and

Troubleshooting.

c.

NPWO 7254/63 -

CEDM NO. 8 Control Element Drive Coil Power Supply

Troubleshooting.

d.

NPWO 0962/62 - 2B

EDG 12 Cylinder Diesel

Fan Shaft Replacement.

This

job was inefficient in that the procedure did not specifically

require all three fan belt drive hubs to be aligned following the

job, and shop personnel

ignored the driving hub by aligning only the

idler hub and the fan hub.

The procedure

also did not specify where

to measure belt tension.

In short, at the post-work test,

the belt

was loose

and misaligned, requiring further work.

The workmanship

was corrected prior to returning the

EDG to service.

The work

.documents

were identified to maintenance

shop engineers for generic

correction.

e.

NPWO 4633/66 - 2A LPSI

Pump Breaker

Change

Out [nine year cyclical

overhaul].

f.

NPWO 4953/66 - MOV 3517,

2A LPSI to

SDC Heat Exchanger Isolation

Valve,'Spring

Pack Replacement.

20

g.

h.'.

NPWO 4960/66 - 2A HPSI Breaker Anti-pumping "Y" Relay Replacement.

NPWO 5117/65 (Unit 1) and 4936/66

(Uni.t 2) - Inspection of

Latching-Type

HFA Relays.

The inspector,

observed testing

and

inspection of 14 of 16 Unit 1 relays

and

4 of 6 Unit 2 relays.

All

latched properly.

The remaining relays

had

been recently inspected

under other

NPWOs.

These relays

had

been previously inspected

during

the Fall

1991 refueling outage

and

some

had

been replaced

or

adjusted.

The potential for drift was considered

small but was

an

unknown factor.

This present

inspection

confirmed that the relays

. had not changed characteristics.

NPWO 7146/63 - Test Engineered

Safeguards

Cabinet

Power Supplies for

Voltage and Ripple - Replace.-Bad

Power, Supplies.

This work was

further corrective action for"a failed instrument

power supply

'erving

channel

MD MSIS'for 'lA SG.

The acceptance

criteria for

voltage

was per the component specification.

The ripple criterion of

200 mv peak-to-peak

was conservatively specified

by the shop

engineer.

Five of 24 power supplies failed and were replaced.

The

licensee

was considering

a possible replacement,

which would include

improved electrical

lead connections,

through their engineering

division.

This work was additionally controlled by AP 0010142,

Rev

8, Unit Reliability - Manipulation of Sensitive

systems.

The

inspector found that field activities were well performed

and

documented.

NPWO 7202/64 - Calibrate

ICW Flow Instruments

FIS-21-9A and

9B.

The specialist

also found

a broken face plate screw and

a rusted

terminal board, which he annotated

on the

NPWO.

Work request 92003451

was subsequently

generated

to initiate repair.

NPWO 1114/62 - Test Both A and

B Train Low Range

Main Steam Safety

Valves.

Each

SG had 8 safety valves under the cognizance of TS

3/4.7.1.

The TS required,

by specifying individual valve numbers,

that

4. safety valves per

SG be verified to be set at 1000 psia +/-

1

percent

[10 psi], and that the other 4 be verified to be set at 1040

psia +/- 1 percent.

This

NPWO addressed

the 8 total valves with the

1000 psia setpoint.

The

NPWO specified the controlling procedure to

be GMP-0705,

Rev 17, Main Steam Safety Valve Maintenance

and

Setpressure

Testing.

The cover

page boldly announced

the procedure

had

been recently been rewritten and should

be read completely - a

good practice.

The procedure

included well marked

gC hold points.

The inspector

observed test performance

on April 21.

The licensee

was using two test gages,

a 1500 psig gage

and

a 200 psig gage.

These were relatively small

gages with 4 1/2 inch diameter faces that

stated

on the face that they had 1/4 of 1 percent accuracy.

Though

1500 psig gage

M-195 had 5-psi divisions, implying that it could be

read to 2 1/2 psi or half a division, it had

a large label

on the

side stating that it had been calibrated to only 1 percent

accuracy

[+ - 15 psi7.

200 psig gage

M-201 also

had

a large

1 percent

21

calibration [+ - 2 psig] label

on its side.

Procedure

GMP-0705

'ection

8.0, Material

and Equipment Required, plainly-specified that

all test

gages shall

have

an accuracy of 0.5'i of full scale.

Worksite review of the of these gages'alibration

sheets

showed that

1500 psig gage

M-195 was actually calibrat'ed

much closer than

1

ercent,

but 200 psig gage

M-201 was actually varying over

a 2 psig

1%j range.

The test crew stopped work, obtained

another

200 psig

gage that met the requirements,

and retested

three valves previously

set using the out-of-specification

gage.

They also verified that the

Unit 1 safety valves set in the Fall of 1991, were in fact properly

set.

Failure to follow (implement)

GMP-0705,

Rev 17, Main Steam Safety

Valve Maintenance

and. Setpressure

Testing,.was

a violation of TS 6.8.l.c. which required procedures for safety. related activities

be

established,

implemented,

and maintained for surveillance

and test

activities of safety-related

equipment.

This is identified as

VIO

389/92-07-04; Failure to Follow Procedure for Setting

Steam Generator

Safety Valves.

As a result of this occurrence,

the licensee

also planned to review

several relief and safety relief valve setting procedures

regarding

gage size,

range,

and type;

gage calibration range

and technique;

and

procedural verification of essential

parameters

at the time of the

test.

On April 3, during an attempt to fill a SIT, the

2A HPSI

pump failed

to start.

The pump's

4160 Volt breaker failed to close.

Operations

generated

NPWO 4960/66 for its repair.

Electrical maintenance

evaluated

the condition via the administrative

constraints

of above

NPWO and newly-generated

maintenance

procedure

MP 0920069,

Rev 0, Troubleshooting

4 KY/6.9 KV Breaker Failures.

The

procedure

was very useful in identifying the breaker

problem.

The

breaker

was repaired within hours of the failure, greatly limiting

the amount of time the component/train

was in an

LCO situation.

Referring to Unit 2 drawing 2998-327 for the

2A HPSI

pump breaker

2A3-1 cubicle, the Westinghouse

50-DHP-250 4160 Volt breaker for the

pump had

a failed "Y" anti-pumping relay.

With the failure of this

relay, the breaker would not close.

The relay had four contacts,

two

of which were not used.

One of the unused

contacts

had loosened in

the relay,

moved within the-relay,

and blocked further relay

operation.

A new relay was installed

and successfully

tested

(pump

started).

Electrical maintenance

and the operational

s'taff are reviewing the

situation for root cause.

Several factors

such

as breaker

use

and

breaker overhaul period were being considered.

The HPSI

pump was

being routinely used to fill two weeping SITs

on

a once to twice

daily basis.

The filling, which was

due to slow leaking valves,

had

22

been effect for most of the fuel cycle.

The breaker

was scheduled

for its nine year overhaul this upcoming (April 20) maintenance

and

refueling outage.

The electrical staff ..was planning to tear

down the

"Y" relay for investigation.

Most activities observed,

particularly the

HPSI circuit breaker

troubleshooting,

were acceptable

and conservative.

The licensee

promptly

initiated corrective action

on observations

d and

k above,

where

shop

performance

elements

were weak.

Receipt

and Handling of New Fuel (Unit 2)(60705)

During this period, the inspectors

observed

the receipt

and handling of

new fuel for Unit 2.

The review included .observation of truck unloading;

shipping cask operations;

fuel unpacking

and lifting into dry storage,

including crane operations;

repacking the empty containers;

and

cleanliness

inspection of dry storage.

The licensee's

reactor engineering

group had preplanned

and supervised

the receipt.

The operators

and

maintenance

crew handled

the shipping containers

and the fuel properly

with due care

and efficiency.

A vendor representative

and

a health

physics technician

were present

during the several

observations.

The

containers

inspected

were in good shape,

well preserved,

and properly

packed

by the vendor.

Records

being generated

at the time were

satisfactory.

Documents

reviewed at the worksite included:

OP 1610020,

Rev 8, Receipt

and Handling of New Fuel

and

CEAs, and

ONOP 2-1600030,

Rev 5, Accidents Involving New or Spent Fuel.

The licensee's

new fuel receipt process

was well polished.

The inspectors

had

no further questions

concerning the recei.pt of new fuel.

Fire Protection

Review (64704)

During the course of normal tours, the inspectors

routinely examined

facets of the Fire Protection

Program.

The inspectors

reviewed transient

fire loads,

flammable materials storage,

housekeeping,

control of

hazardous

chemicals, ignition source/fire risk reduction efforts,

and fire

barriers.

Fire protection program implementation

was apparent.

Review of Periodic 'and -Special

Reports

(90713)

The inspector reviewed spe'cial

report L-92-117 dated April 28,

1992.

It

was issued

per TS 4.8.1.1.3

and 6.9.2,

and addressed

a failure of the

1B

EDG to load on April 3.

This subject is discussed

in paragraph

3.b. of

this report.

The inspector

had

no further comment concerning the special

report.

This item is closed.

23

The inspector

reviewed

a

10 CFR Part 21 initial notification dated April

1, 1992.

The formal written notification was forwarded in letter L-92-119

dated April 28.

It addressed

crack-like indications found in a

3-inch-diameter

Monel 400 tee fitting supplied

by Tioga Pipe Supply Co.

The material did not meet requirements of'he

ASME SB564.specification.

Of the seven

items received,

one was analyzed in the laboratory

and six

were returned to the vender.

The inspector

had

no further questions

in

this area.

This item is closed.

9.

Onsite Followup of Written Nonroutine Event Reports

(Unit 1) (92700)

The following LERs were reviewed for potential

generic impact, to detect

trends,

and to determine whether corrective actions

appeared

appropriate.

The

LERs were reviewed in accordance

with the current

NRC Enforcement

Policy.

a.

(Closed)

LER 335-92-001,

Fuel Handling Building Ventilation Radiation

Monitor Out of Service

Due to Personnel

Error.

This

LER discussed

a

licensee-identified violation of TS 3.3.3.10,

Radioactive

Gaseous

Effluent Monitoring Instrumentation.

The fuel handling building

ventilation radiation monitor was required to be operable at all

times but was removed from service for about

23 hours2.662037e-4 days <br />0.00639 hours <br />3.80291e-5 weeks <br />8.7515e-6 months <br />

by a series of

personnel

errors

and without knowledge of the control

room operators.

The licensee's

event analysis

and resultant corrective action plans

appear to be thorough

and consistent with corrections for LER

335-92-003

below.

This violation will not be subject to enforcement action because

the

licensee's

efforts in identifying and correcting the violation meet

the criteria specified in Section VII.B of the Enforcement Policy.

It is identified as

NCV 335/92-07-01,

Fuel Handling Building

Ventilation Radiation Monitor Out of Service

Due to Personnel

Error.

b.

(Closed)

LER 335-92-003,

Containment

Atmosphere Particulate

and

Gaseous

Radioactivity Monitors Out of Service

Due to Personnel

Error.

This

LER discussed

a licensee-identified violation of TS 3.3.3.1,

Radiation Monitoring Instrumentation

Channels,

and 3.4.6.1,

RCS

Leakage Detection Systems.

Containment isolation valves were

inadvertently left closed following periodic valve stroke testing.

The licensee

found several

contributing factors, including no

independent verification of restoration,

a burned out light bulb,

and

weakness

in reviewing the details of radiation monitor readings.

Corrective actions"addressed

all safety-related

valve stroke time

procedures,

including independent verification of post test

restoration.

Corrective actions also included

a significant upgrade

of the radiation monitor log sheets

to require checks of instrument

trends.

This violation will not be subject to enforcement

action because

the

licensee's

efforts in identifying and correcting the violation meet

the criteria specified in Section VII.B of the Enforcement Policy.

24

It is identified as

NCV 335/92-07-02,

Containment

Atmosphere

Particulate

and Gaseous

Radioactivity Monitors Out of Service

Due to

Personnel

Error.

The licensee

has taken extensive corrective action for these

two problems.

10.

Onsite Followup of Events

(Units

1 and 2)(93702)

A nonroutine plant event

was reviewed to determine

the

need for further or

continued

NRC response,

to determine whether corrective actions

appeared

appropriate,

and to determine that

TS were being met and that the public

health

and safety received primary consideration.

Potential

generic

impact and trend detection

were also considered.

On April 21, at 2:38 a.m., the reactor operator manually tripped Unit 2

from 12 percent

power during

a planned shutdown'or refueling.

The

turbine did not trip from remote signals

from the reactor trip switchgear

nor from the control board pushbutton.

The Nuclear Watch Engineer

manually tripped the turbine locally at the turbine stand.

This is

discussed

further in paragraph

2b.

The operators'esponse

to this unexpected

event

was excellent.

ll.

Followup (Units

1 and 2) (92701)

a. 'ollowup of Unresolved

Items

(Closed - Units

1 and 2) URI 335,389/92-03-01,

Evaluate Operability

of Containment Cooling System Relief Dampers.

This item concerned

an

ISEG surveillance finding in March, 1990, that

a number of Unit 1 containment ventilation pressure relief dampers

were painted shut.

The record did not indicate that the dampers

had

been determined to be operable during the time they were painted

.over..

FPL engineering

subsequently

performed engineering

evaluation

JPN-PSL-SEMS-92-002,

REV 0, assessing

the containment fan cooler

relief dampers'istorical

operability.

This study found that, at

design pressure,

the force to open

each relief damper would be about

55 pounds - far greater

than the force 'actually exerted

by the person

who opened

the dampers.

This study also found that, of the eight

damper assemblies

installed, if only one damper

assembly

opened,

the

ventilation system would not experience

excessive differential

pressure.

The computer

program used for the analysis

would not work

if all damper assemblies

were assumed failed closed,

so that more

extreme analysis

was not completed.

The inspector

had

no further

questions.

This URI is closed.

(Closed - Units

1 and 2)

URI 335,389/91-05-01,

Drug Testing Program

Elements.

f

25

I

This St. Lucie item concerned

weekend

and holiday drug testing.

During an inspection at the Turkey Point facility', the cognizant

security inspector determined that the item was satisfactory

throughout the corporate structure,

including both Turkey Point and

St. Lucie.

This is discussed

in IR 250, 251/91-40.

This URI is

closed.

b.

Followup of Regional

Requests

During this period, the inspectors

conducted

two surveys

per Region

II directions

and returned

the results to regional contacts:

Identification of present or past waste

dumps at reactor sites,

and

Completion of a licensee staffing matrix.

12.

Exit Interview

The inspection

scope

and findings were summarized

on May 8, 1990, with

those

persons

indicated in paragraph

1 above.

The inspector

described

the

areas

inspected

and discussed

in detail the inspection findings listed

below.

Proprietary material is not contained in this report.

Dissenting

comments

were not received from the licensee.

Item Number

Status

Description and Reference

335,389/91-05-01,

closed

URI - Drug Testing

Program Elements,

paragraph lla.

335,389/92-03-01

closed

URI - Evaluate Operability of Containment

Cooling System Relief Dampers,

paragraph lla.

335/92-07-01

closed

NCV - Fuel Handling Building Ventilation

Radiation Monitor Out of Service

Due

to Personnel

Error, paragraph

9a.

335/92-07-02

closed

NCV - Containment

Atmosphere Particulate

and Gaseous

Radioactivity Monitors

Out of Service

Due to Personnel

Error, paragraph

9b.

389/92-07-03

open

VIO - Isolation of Containment

Pressure

Sensing

Line Mithout Placing Effected

Instrumentation

Channels

in Trip or

Bypass

as Required,

paragraph

2a.

389/92-07-04

open

VIO - Failure to Follow Procedure for

Setting

Steam Generator

Safety

Valves, paragraph

5k.

26

Abbreviations,

Acronyms,

and Initialisms

AFAS

AFW

ANPS

.AP

ASME Code

ATTN

ATWS

CC

CCW

CDF

CEA-

CEDM

CET

CFR

CNRB

DEH

DPR

ECCS

EDG

EDSFI

EOP

EPRI

ESF

ESFAS

FIS

FPL

FRG

FSAR

GL

GMP

HFA

HPSI

HVE

Hz

I&C

ICW

IR

ISEG

JPN

KV

LCO

LER

LOCA

LPSI

'MFIV

MG

Auxiliary Feedwater Actuation System

Auxiliary Feedwater

(system)

Assistant Nuclear Plant Supervisor

Administrative Procedure

American Society of Mechanical

Engineers Boiler and Pressure

Vessel

Code

Attention

Anticipated Transient Without Scram

Cubic Centimeter

Component Cooling Water

Core

Damage

Frequency

Control

Element Assembly:

Control Element Drive Mechanism

Core Exit Thermocouple

Code of Federal

Regulations

Company Nuclear Review Board

Digital Electro-Hydraulic (turbine control system)

Demonstration

Power Reactor

(A type of operating license)

Emergency

Core Cooling System

Emergency

Diesel Generator

Electrical Distribution System Functional

Inspection

Emergency Operating

Procedure

Electric Power Research Institute

Engineered

Safety Feature

Engineered

Safety Feature Actuation System

Flow Indicator/Switch

The Florida Power

& Light Company

Facility Review Group

Final Safety Analysis Report

[NRC] Generic Letter

General

Maintenance

Procedure

A GE relay designation

High Pressure

Safety Injection (system)

Heating

and Ventilating Exhaust (fan, system, etc.)

Hertz (cycle per second)

Instrumentation

and Control

Intake Cooling Water

[NRC] Inspection Report

Independent

Safety Engineering

Group

.(Juno Beach)-Nuclear

Engineering

KiloVolt(s)

TS Limiting Condition for Operation

Licensee

Event Report

Loss of Coolant Accident

Low Pressure

Safety Injection '(system)

Main Feed Isolation Valve

Motor Generator

27

MHP

NOV

MP

NSIS

NSIV

mv

NCV

NPF

NPS

NPWO

NRC

ONOP

OP

PCN

PN

PSI

PSIA

PSL

PT

Pub

PVC

gA

gI

RAB

RCP

RCS

Rev

RPS

RTGB

RWT

SALP

SB

SDC

SG

SIT

St.

STA

TgR

TR

TS

URI

VIO

Mechanical

Maintenance

Procedure

Motor Operated

Valve

Maintenance

Procedure

Main Steam Isolation Signal

Main Steam Isolation Valve

millivolt

Non-Cited Violation (of NRC requ

Nuclear Production Facility (a t

Nuclear Plant Supervisor

Nuclear Plant Work Order

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Operating

Procedure

Plant Change/Modification

Preventive Maintenapce

Pounds

Per Square

Inch

Pounds

Per Square

Inch Absolute

Plant St. Lucie

Pressure

Transmitter

Publication

PolyVinylChloride

guality Assurance

guality Instruction

Reactor Auxiliary Building

Reactor Coolant

Pump

Reactor Coolant System

Revision

Reactor Protection

System

Reactor Turbine Generator

Board

Refueling Water Tank

Systematic

Assessment

of License

Safety Train

B

Shut

Down Cooling

Steam Generator

.Safety Injection Tank

Saint

Shift Technical Advisor

Topical guality Requirement

Temperature

Recorder

Technical Specification(s)

I NRC] Unresolved

Item

Violation (of NRC requirements)

irements)

ype of operating license)

e Performance