ML17223A317

From kanterella
Jump to navigation Jump to search
Resident Insp Repts 50-335/89-20 & 50-389/89-20 on 890711-0814.Violations Noted:Emergency Diesel Generator 1B Fuel Transfer Sys Inoperable & Containment Cooler Temporary Filter Media Installed During Plant Operation
ML17223A317
Person / Time
Site: Saint Lucie  
Issue date: 08/29/1989
From: Crlenjak R, Elrod S, Michael Scott
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17223A316 List:
References
50-335-89-20, 50-389-89-20, NUDOCS 8909140149
Download: ML17223A317 (17)


See also: IR 05000335/1989020

Text

0

~

gp,$\\ REGS

C~

+

0

Cy

C

p

p

Yg

Cy

~o

<<<<*++

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTAST., N.W.

ATLANTA,GEORGIA 30323

Report

Nos:

50-335/89-20

AND 50-389/89-20

Licensee:

Florida Power

8 Light Co

9250 West Flagler Street

Miami,

FL

33102

Docket Nos.:

50-335

and 50-389

Facility Name:

St. Lucie

1 and

2

License Nos.:

DPR-67

and

NPF-16

Inspection

Conduct

-:

11 August 14,

1989

Inspect

S. A.

ro

o

Resident Inspector

at

Signed

M. A. Sco

, Res'n

In pecto

Approved By:

R.

V. Crlenjak,

ection Chief

Division of Reactor Projects

Date Signed

D te

Soigne

.SUMMARY

Scope:

This routine resident .inspection

was

conducted

onsite in the

areas

of plant

operations

review, maintenance

observations,

surveillance

observations,

safety

system inspection,

and followup of previous inspection findings.

Results:

Three previously identified unresolved

items

have

been identified as violations

and

are

being

considered

for potential

escalated

enforcement

action.

Additionally, one other

new unresolved

item * was identified.

Within the

areas

inspected,

the following violations were identified and are

being considered for escalated

enforcement:

EDG

1B fuel oil transfer

system inoperable,

paragraph

7.

Containment

cooler

temporary -filter media

installed

during

plant

operation,

paragraph

2.a.

Containment

cooler

access

doors

not properly sealed

in required

modes,

paragraph

7.

Within the areas

inspected,

the following *URI was'dentified:

Unexplained plant modification, paragraph

2a.

  • Unresolved

items

are matters

about

which

more

information is required

to

determine

whether they are acceptable

or may involve violations or deviations.

890&i40i49 890831

PDR

ADOCK 050003::5

REPORT

DETAILS

Persons

Contacted

Licensee

Employees

"D. Sager,

St. Lucie-Site Vice President

  • G. Boissy, Plant Manager
  • A. Bailey, guality Assurance

Super visor

'*J. Barrow, Operations

Superintendent

  • J. Barrow, Fire Prevention Coordinator
  • S. Brain,

Independent

Safety Evaluation

Group

'*H. Buchanan,

Health Physics

Supervisor

  • C. Crider, Outage Supervisor
  • D. Culpepper,

Site Juno Engineering

Manager

  • R. Dawson, Maintenance

Superintendent

  • C. Leppla,

IKC Supervisor

  • L. McLaughlin, Plant licensing Supervisor
  • L. Rogers, Electrical Maintenance

Supervisor

  • N. Roos,

equality Control Supervisor

  • R. Sipos,

Service

Manager

  • D. West,

Technical Staff Supervisor

  • E. Wunderlich, Reactor Engineering Supervisor

Other

licensee

employees

contacted

included

engineers,

technicians,

operators,

mechanics,

security force members

and office personnel.

NRC Employees

  • P. Madden,

Region II Project Engineer

  • M. Scott, Resident Inspector
  • Attended exit interview

Acronyms

and initialisms used

throughout this report are listed in the

last paragraph.

Review of Plant Operations

(71707).

Unit

1

began

the inspection

period

in day

12 of an

outage to replug

certain

SG tubes.

On July 17th, at 3:00

am, the unit tripped from 15

percent

power during. restart

from the outage.

'Power operation

was

resumed

by early the 18th.

During the

SG replugging,

44 'A'G hot leg,tube

ends

where

replugged

and

19 'B'G hot leg tube

ends

were replugged.

The

licensee

intends

to replug

the

cold leg

tube

ends

during

the

next

refueling outage.

The unit ended

the period at

100 percent

power.

Unit 2 began

the inspection

period at power.

The

2A heater drain cooler

expansion joint began to leak

on August 14.

The unit ended

the period at

approximately

80

percent

power

while the

leaking joint was

being

evaluated.

On July 18,

1989,

the

SALP presentation

was given by the

NRC at the site.

The presentation

Was well received

by the licensee

and

NRC management

toured the facility prior to and after the presentation.

The

SALP ratings

for licensee

were considered

to

be above

average

in most categories;

the

SALP report

was issued

as

IR 50-335,389/89-13.

a.

Plant Tours (Units

1 and 2).

The

inspectors

perio'dically conducted

plant tours to verify that

monitoring

equipment

was

recording

as

required,

equipment

was

properly tagged,

operations

personnel

were aware of plant conditions,

and plant housekeeping

efforts were adequate.

The inspectors

also

determined

that

appropriate

radiation

controls

were

properly

established,

critical clean areas

were being controlled in accordance

with procedures,

excess

equipment or material

was stored properly and

combustible

materials

and

debris

were

disposed

of expeditiously.

During tours,

the inspectors

looked for the existence

of unusual

fluid leaks,

piping vibrations,

pipe hanger

and seismic restraint

settings,

various valve

and breaker positions,

equipment caution

and

danger

tags,

component

positions,

adequacy

of fire fighting

equipment,

and

instrument

calibration

dates.

Some

tours

were

conducted

on backshifts.

The frequency of plant tours

and control

room visits by site management

was noted to be adequate.

The inspectors routinely conducted. partial walkdowns of ECCS systems.

Valve,

breaker,

and

switch lineups

and

equipment

conditions

were

randomly verified

both locally

and

in the control

room.

The

following accessible-area

ECCS system

walkdowns

were

made to verify

that system lineups

were in accordance

with licensee

requirements

for

operability and equipment material conditions

were satisfactory:

The

1A LPSI

room piping was

inspected this period in detail.

The walkdown indicated that the piping

was in accordance

with

procedure

OP 1-0410020,

Rev. 24,

HPSI/LPSI - Normal Operation,

and

drawing

8770-G-078,

sheet

130,

Rev 5, Safety Injection

System.

During a tour of the Unit 1

ECCS space,

the inspector

noted that

1B

HPSI

pump

discharge

vent

valve

V3920

was

leaking

approximately

3 to

5 cc/minute.

When attempts to vent and shut

.the valve failed to reduce

the leakage,

the valve

was repaired

within a few days

under

a

PWO.

The inspectors

performed

walkdown of the piping around the Unit

1

CST.

The

valve

lineup

was

in accordance

with drawing

8770-G-080,

sheet

3,

Rev.

26,

and

procedure

OP 1-0700022,

Rev

21, Auxiliary Feedwater

- Normal Operation.

Walkdown of the

major safety related

components

was satisfactory.

During the

above

walkdown,

two inch valve

V28145,

Condensate

Recovery

to

CST Isolation,

was

noted to be suspended

from the

3

side of the tank

on

a

25 foot vertical length of pipe.

This

line was

shown

on drawing 8770-B-124,

isometric

number

CR-23,

Condensate

Recovery,

Rev. 3.

The piping

down to the valve was

covered with metal

insulation to just above

the valve and the

line ended

approximately five inches

below the valve in an open

ended nipple.

There were

no hangers

on the line or the valve.

The condensate

recovery drawing indicates

other piping attached

to the existing piping as

a continuous

pipe run.

This other

pipe

no longer existed.

The drawing, issued

on March 20, 1978,

did not indicate

any modification that might have deleted

the

missing piping run.

The licensee

was researching their records

to determine

whether or not this piping configuration

had

been

'valuated

by their staff.

Additionally, the

site

was

determining if a plant modification existed to explain what had

happened

to the

removed

condensate

recovery piping and hangers.

,Corporate

and site procedures

which are consistent with license

and

regulatory

requirements

require

that

modifications

be

documented

and analyzed.

This is identified

as

URI 335/89-20-04,

Unexplained

Plant

Modification, until this situation is clarified by the licensee.

During

a Unit

1 containment

tour on July 15,

1989, with Unit 1

shut

down

for

SG

tube

replugging, filter media

(blue

loosely-woven fibrous material)

was found covering the coils of

all four containment

fan coolers.

The filter media,

which was

covered

by

a matted dirt film, had

been

installed

during

a

previous refueling outage

as is commonly done to maintain'coil

cleanliness

during

the

outage.

There

was

no

procedure

to

install or remove the media for this unit.

However, there

was

a

procedure

for Unit 2,

which

was verified to

have

no media

installed.

The licensee

immediately

removed

the filter media

from the coils.

At. the

end of the reporting period,

the

licensee

was performing

an engineering

evaluation of coil/fan

cooler

performance

and previous operability with the media in

place.

The evaluation

was not yet available.

The licensee

had

also initiated

a

LER on the event.

Unit

1

TS 3.6.2.3

requires

containment

fan coolers

to

be

operable for modes

1, 2, and 3.

With one containment

fan cooler

inoperable, it must

be

. restored

within

30

days if both

containment

spray

pumps

are operable,

or within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> with

one

containment

spray

system

inoperable,

or the reactor unit

must

be placed in hot shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

Between

February

1987

and July

15,

1989, all four Unit

1

containment- coolers

were potentially inoperable

due to temporary

filter media not being

removed following the last two refueling

outages.

This is identified as violation 50-335,389/89-20-02,

Containment

Cooler Temporary Filter Media Installed During Plant Operations.

b.

Plant Operations

Review (Units

1 and 2)

The

inspectors

periodically

reviewed shift logs

and

operations

records,

including data

sheets,

instrument traces,

and records of

equipment malfunctions.

This review included control

room logs

and

auxiliary logs, operating

orders,

standing

orders,

jumper logs

and

equipment tagout records.

The inspectors

routinely observed

operator

alertness

and

demeanor

during

plant

tours.

During routine

operations,

control

room staffing, control

room access

and operator

performance

and

response

actions

were

observed

and evaluated.

The

inspectors

conducted

random off-hours

inspections

to assure

that

operations

and .security

remained

at

an acceptable

level.

Shift

turnovers

were

observed

to verify that they

were

conducted

in

accordance

with

approved

licensee

procedures.

Control

room

annunciator status

was verified.

The

inspectors

performed

an

in-depth

review of the

following

safety-related

tagouts

(clearances):

1-7-221-1

1-8-404-76

HVE-10B inlet damper breaker ¹40508

181 SIT outlet MV-3634 breaker

¹42113

The above clearances

were satisfactory.

8-118

Unit

1 Nitrogen to Condenser

(PWO 6122)

,9-13

Unit.1

SAS Point, TE,1121Y -

1

(PWO 6627/61)

Drawing 8770-B-327,

sheet

1506,

associated

with tag

9-13,

contained

an

erroneous

electrical

cabinet

number.

A I&C foreman

was able, with difficulty, to

determine

the

appropriate

cabinet.

The

personnel

involved notified an

I&C foreman

who leads

a QIP team

in

human

factors

concerns

related

to electrical

drawings.

This particular problem will be resolved

via the

IP team.

Q

8-127

. Unit

1 TR-22-1, Point 2, terminals

G-3, G-4

(PWO

6372)

The

inspector

examined

the following jumper

log tags

(circuit

alteration tags):

The

above

jumpers

were in accordance

with procedure

AP 0010124,

Rev.

20, Control

and

Use of Jumpers

and Disconnected

Leads.

Reactor Trip

At about 3:00

am on July 17, while operators

were preparing to roll

the main turbine during

a startup,

Unit 1'ripped from approximately

15 percent

power.

The trip resulted

from low level in 18

SG.

The

RCO at the

SG level station

was shifting

SG feed from AFW flow to

main

feed.

The

RCO noticed

the

SG levels

decreasing

and

took

corrective

action but

SG level

continued

to drop until the trip.

Causal factors for the trip included:

Main feedwater line block valves

NV-09-7 and'V-09-8

were shut

and

main feed

water

could not get to the

SGs.

The startup

procedure

did not require

these

valves to

be

opened prior to

power ascension.

Previously,

RCOs

had automatically

checked

valve status,

located at a different control panel.

The audible

alarm accompanying

the pretrip annunciator

did not

alarm

when the

SG reached pretrip level.

This alarm was stated

to be used

by the operators

as

a warning,of the impending trip.

Corrective action included halting the startup until the annunciator

audible

alarm

was repaired.

Prior to restart,

a temporary startup

procedure

change,

which required

the block valves to'be checked

open

prior to main feed initiation, was

issued.

A permanent

procedure

change

was being processed

at the time of the restart.

The inspector

arrived

on site to review this event shortly after it occurred

and

determined that the licensee's

actions

in response

to this event were

satisfactory.

Unit 2 Turbine Load Runback

On July 22, Unit 2

Sigma

gauge

PIS 22-36,

which reads

out turbine

first stage

pressure,

began

to deteriorate.

The

gauge

provides

. feedback

to the turbine control circuits concerning

the

amount of

runback that

has

occurred.

The gauge

was reading artificially low

and, if left unrepaired,

could eventually

cause

a turbine runback.

The inspector discussed

the problem with the

NPS on shift.

The load-threatening

repair was planned for day shift on July 25 when

..support

would be available.

Operators

were briefed

on the intended

, repair

and possible operator actions

were discussed

should the repair

cause

generator

load problems.

During the repair, the

18C technician

shorted

the gauge

in such

a manner that

a runback with a zero-load

end

point

was initiated.

Due to the briefing and appropriate

operator

actions,

the

runback

was

limited to approximately

200

NW.

The

minimal reactor

response

was

as expected;

Tavg rose from 573 degrees

to

579 degrees,

pressurizer

pressure

rose

from 2250 psig to 2320

psig,

and

pressurizer

level

rose

from

65% to

73%.

Parameters

returned

to

normal

when

the electrical

load

was

restored.

The

licensee's

operations

staff

handled

the

transient

well.

The

inspector

arrived

in the control

room within minutes after the

runback

and

assessed

the

reactor

conditions

with the onshift

operations

staff.

The inspector

also reviewed the

PWO C31592

work

package

and

found

no

problems.

The

gauge

repair

was

completed

successfully.

c.

Technical Specification

Compliance (Units

1 and 2)

Licensee

compliance with selected

TS

LCOs was verified. This included

the

review

of

selected

surveillance

test

results.

These

verifications

were

accomplished

by direct observation of monitoring

instrumentation,

valve positions,

and switch positions,

and by review

of completed

logs

and records.

The licensee's

compliance with LCO

action

statements

was

reviewed

on selected

occurrences

as

they

happened.

The inspectors

verified that plant procedures

involved

were adequate,

complete, the correct revision and instrumentation

and

recorder traces

were observed for abnormalities.

No violations or deviations

were identified.

d.

Physical

Protection

(Units 1 and 2)

The inspectors verified by observation

during routine activities that

security program plans

were being implemented

as evidenced

by: proper

display of picture badges;

searching of packages

and personnel

at the

plant entrance;

and vital area portals

being locked and alarmed.

Backshift security patrols

were

observed

during the observation

of

surveillances

such

as the fire protection item discussed

in paragraph

3.

No violations or deviations

were identified.

3.

.Surveillance

Observations

(61726)

Various

plant

operations

were verified to

comply with selected

TS

requirements.

Typical of 'these

were confirmation of TS compliance for

reactor

coolant chemistry,

RWT conditions,

containment

pressure,

control

room ventilation

and

AC

and

DC electrical

sources.

The

inspectors

verified

that

testing

was

performed

in

accordance

with

adequate

procedures,

test

instrumentation

was calibrated,

LCOs were met,

removal

and restoration

of the affected

components

were

accomplished

properly,

test results

met requirements

and

were reviewed

by personnel

other than

the individual directing the test,

and that any deficiencies identified

during the testing

were properly

reviewed .and

resolved

by appropriate

management

personnel.

The

performance

of monthly fire prevention

surveillance

OP

1800050,

Rev.

27,

Monthly Fire

Valves,

Fire

Pumps

Surveillance

and

Wet

Pipe

Sprinkler Systems

Test,

was observed.

The ANPO-required actions

were the

principal

area

observed.

Multiple valves that were checked

were missing

the metal identification tags that

had

been

hung during construction

and

the painted-on

valve identifiers

had not been verified to be correct.

The

valves

had to be identified by the

system

drawing.

Several

of the

ANPO

valves

were listed

on the

SNPO list and vice versa.

This created

some

confusion.

The

procedure

sketch

which

showed

some of the

remote

valve

locations

was not very legible.

The last

two items mentioned

were minor

human factor problems

but should

be corrected

by a procedure

change.

The

inspector also

noted that the fire pump miniflow recirculation line had

a

minor through wall leak at

a weld joint and required

a

PWO for its repair.

The inspector's

concerns

were identified to the licensee.

The

performance

of

OP

1-0110050,

Rev.

18,

Control

Element

Assembly

Periodic Exercise,

was observed.

CEA 23 would -not operate in the outward

direction.

One of the four upper electrical limit switches

was found to

be stuck shut.

This indicaged

to. the control circuit that the-control

element

was fully withdrawn, resulting in no out motion.

The switch was

disconnected

.from the circuit 'and

CEA 23 control

was

restored;

The

inspector

observed

operator,

supervisor

and

I&C repair activities during

this troubleshooting evolution and

had no further questions.

The performance

of

OP 1-0410050,

Rev.

27,

HPSI/LPSI Periodic Test,

was

observed for the Vnit 1, train A, pumps.

This monthly surveillance test

involved flow path valve lineup,

pump operation,

check valve operation

verification,

recording

ASME

pump

and

valve

program data,

and visual

inspection of the systems

in the

pump area.

The procedure

did not line up

the

pump recirculation

flow path,

however

those

valves

were lined

up

weekly by procedure

AP 1-00100125A,

Surveillance

Data Sheets,

Data

Sheet

36F,

and

checked

monthly per

AP 0010123,

Rev.

63, Administrative Control

of Valves,

Locks,

and Switches.

The test data

was properly obtained

and

recorded.

Several

small boric acid leaks

were observed

by the operator

and reported for repair.

The inspector

had

no further questions.

No violations or deviations

were identified

Maintenance

Observation

(62703)

Station maintenance

activities involving selected

safety-related

systems

and

components

were

observed/reviewed

to ascertain

that

they

were

conducted

in accordance

with requirements.

The following items

were

considered

during this review:

ICOs were met; activities were accomplished

using

approved

procedures;

functional

tests

and/or calibrations

were

performed prior to returning

components

or systems

to service; quality

control .records

were maintained; activities were accomplished

by qualified

personnel;

parts

and

materials

used

were

properly certified;

and

radiological

controls

were

implemented

as required.

Work requests

were

reviewed to determine

the status

of outstanding

jobs

and to assure

that

priority was

assigned

to safety-rela'ted

equipment.

Portions

of the

following maintenance activities were observed:

(PWO C31592,

Maintenance

on Gauge

PIS 22-36) is discussed

in paragraph

2.b.

above.

(PWOs 1768/61, Air Filter, and 1802/61 Valve Replacement)

relating to

maintenance

on the

18 instrument air compressor

were

observed

in

part.

The compressors

are

approximately

one year old Atlas

Copco

models.

The suction

and discharge

valves

were removed for inspection

and,

though very little wear

was evident,

the licensee

replaced

the

valves.

In order to determine

and

document

the level of wear,

the

valves

were dimensionally

inspected

and

examined *by various site

personnel.

The licensee

has

plans to expand

the written instructions

regarding air. compressor

tear

down based

on the experience

gained

,duri.ng this evolution.

Work detai,ls

such

as

torque

val.ues

for

fasteners

were

discussed

with the

vendor

and

implemented.

The

inspector

found the licensee'.s

ma'intenance

activity 'in this area to

be .satisfactory.

.(PWO

5184/61)

The electrical

.department

repaired circuit breaker

40508 for safety-related

fan

HVE lOB, the main

RAB exhaust fan.

The

packaged

replacement

assembly

that is

changed

out during breaker

overhaul

had

been previously replaced

on this breaker during the last

outage.

That previous replacement

package

was missing

a part causing

the breaker to not trip as designed while being manually racked out.

This condition had

no direct nuclear safety impact (i.e., the breaker

would have

performed normally in-service),

but could have

a personnel

safety

impact.

This current

work activity installed the missing

part.

The work was

performed without a supporting

procedure.

The

electricians

had

been trained

by the breaker

vendor

and did have the

technical

manual at hand.

The technical

manual.did not list detailed

work instructions

but listed

parts

and their function.

Per

discussions

with the electricians,

the vendor

had not discussed

the

particulars of the off-normal evolution which had occurred.

The work

proceeded

with difficulty but

was

completed

satisfactorily.

Subsequent

testing of the breaker

proved the item to be functionally

acceptable.

The department

was considering

procedural

changes.

At

the time of this work- observation,

the details of the missing part

problem

had not been relayed to the electrical

'department

management.

Once

alerted,

similar

breakers

were

inspected,

affected

breakers

identified,

and repair

work scheduled.

The missing part

problem

affected

3 of 9 recently-received

breakers.

The licensee is is aware

of the potentially-generic

nature of this

issue

and is discussing

this information with the breaker distributor.

During the

past

several

months,

the

inspectors

'had

observed

the

licensee

attempting repair of a seal

around

a safety related

pipe in

'-- the lA LPSI-room.

These seals

provide several

types of protection to

-- the

ECCS envelope.

The seal

material

in question

was

a putty- like

material that weighs

147 .to

177

pounds

per cubic foot; the material

stays in place

due to primarily surface friction between the material

and

the surrounding

(steel)

envelope.

The problems with the seals

were

generally

known to engineering

via

a

nonconformance

report

written in January

1989;

the fire protection

group

had written the

report based

on potential fire protection

boundary implications.

The

repairs initially involved forcing the existing

seal

back into its

position in the

room ceiling.

Subsequently,

engineering

generated

a

modification which included additional angle'iron"supports."

'NRC and

licensee

inspection

has identified additional

seals for repair.

The

licensee

was continuing to evaluate

the seals.

These

seals

which

were originally installed

by Tech-Sil, Inc.,

are

believed

to

be

installed at other utilities.

The licensee

and the

NRC are following

the evaluation for potential

informational release

as appropriate.

On June

28,

1989, the lower (most interior) of four seals failed in

the 2Bl RCP shaft seal

package.

This date

was also associated

with a

reactor trip.

During this

inspection

period,

the

seal

package

condition

has

not continued

to degrade.

The licensee

has

been

monitoring

the

seal

package

condition

using

control

room

instrumentation.

The last

time

a

RCP seal

package

had

a similar

failure, the package

did not exhibit any additional

degradation

and

remained fully functional until the unit was shutdown for refueling.

5.

Safety System Inspection

(71710)

During the

1A LPSI

room piping walkdown,

discussed

in paragraph

2.a,

portions of the

CCW piping which provides cooling flow to

ECCS equipment

inside the LPSI

room were also

walked down.

The walkdown indicated that

the

CCW piping inside this room was in accordance

with drawing 8770-G-083,

Rev.

22,

Component Cooling System.

The walkdown and inspection of the

CCW

system will be completed during subsequent

NRC inspections.

No violations or deviations

were identified.

6.

Onsite Followup of Written Nonroutine Event Reports

(Unit 1) (92700)

(Open)

LER 89-02, Misaligned Valve Caused

Inoperability of the

1B Diesel

Fuel Oil System

Due to Personnel

Error,

was issued

on July 14, 1989.

The

event

was

discussed

in

a

previous

inspection

report

as

URI

335,389/89-18-01

and in this report in paragraph

7.

The

LER remains

open.

7.

Followup of Unresolved

Items (Units

1 and'2)

(92701)

(Closed)

URI 335,389/89-18-01,

Mispositioned

1B Diesel

Fuel Transfer

Pump

Discharge

Valve.

Unit 1

TS 3.8.1.1

requires that, for modes 1,2,3,

and

4 as

a minimum, two

separate

and independent

diesel

generator

sets

be operable,

each with: an

engine

mounted fuel tank containing

a minimum of 152 gallons of fuel,

a

separate

fuel storage

system

containing

a

minimum of 16,450

gallons of

fuel,

and

a separate

fuel transfer

pump.

With

a diesel

generator

set

inoperable,

operability of the remaining

AC sources

must

be demonstrated

within one

hour and at least

once

per eight hours thereafter.

At least

two offsite circuits

and

two diesel

generator

sets

must

be restored

to

operable

status

within 72

hours

or the unit must

be in at least

hot

standby within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

On June

14,

1989, for a period of approximately

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />,

the fuel oil

transfer

pump discharge

valve for-the

1B

EDG was not in the required

open

10

position

and

the

remaining

AC sources

were

not demonstrated

operable

within one

hour.

The

EDG would have automatically started

and

run if

needed

but the automatic

fuel makeup to the engine

mounted

tank would not

function.

The tank does

have

a level alarm to warn of low level.

Failure

to

have

an

operable

fuel

transfer

system

is

violation

50-335/89-20-03.

-

URI -335,389/89-18-01

is administratively

closed

and

replaced

by this violation.

-'(Closed)

URI 335,389/89-10-05,"

Operability Requirements. for Containment

Coolers.

Containment

cooler doors

were discussed

in Inspection

Reports

335,389/89-10

and 89-16.

-: Unit

1

TS 3.6.2.3 requires

containment

fan .coolers to,be

operable, for

modes 1, 2, and 3.

With one containment fan cooler inoperable, it must

be

restored within 30 days if both containment

spray

pumps

are operable,

or

within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> with one containment

spray system inoperable,

or be in hot

shutdown within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

Unit 2 TS 3.6.2.3 requires that containment fan coolers shall

be operable

for modes

1, 2,

and

3.

With one containment

fan cooler inoperable, it

must

be restored within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or be in hot shutdown within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />.

8.

For Unit 1,

between

August

28,

1988

and April 12, .1989, all four

containment, coolers

were potentially inoperable

due to cooler access

doors

not being properly dogged after the last refueling outage.

Also, for Unit

2, the fan coolers

were potentially inoperable

from 1:56

am, April 14,

1989,

when the unit entered

Mode

3 with multiple access

doors improperly

dogged, until the dogs were adjusted

on April 15.

URI

335,389/89-10-05

is

- administratively

closed

and

replaced

with

violation 335,389/89-20-01,

Containment

Cooler Access

Doors not Properly

Sealed

in Required

Modes.

Exit Interview (30703).

The inspection

scope

and findings were summarized

on August 15,1989, with

those

persons

indicated in paragraph

1 above.

The inspector described

the

areas

inspected

and discussed

in detail

the inspection

findings listed

below.

Proprietary

material is not contained

in this report.

Dissenting

comments

were not received

from the licensee.

Item Number

Status

"

Descri tion and Reference

335,389/89-20-01

open

VIO--Containment Cooler Access

Doors

not Properly

Sealed

in Required

Modes,

paragraph

7

335/89-20-02

open

VIO--Containment Cooler Temporary

Filter

Media

Installed

During

Plant Operation,"paragraph

2.a

11

I tern Number

335/89-20-03

'35/89-20-04

Status

open

open

Descri tion and Reference

VIO

EDG 18 Fuel Oil Transfer

System

Inoperable,

paragraph

7

URIUnexplained

Plant Modification,

. paragraph

2.a

335,381/89-10-05

closed

URI--Operability Requirements

for

Containment

Coolers

335/89-18-01

closed

URI Nispositioned

1B Diesel

Fuel

Transfer

Pump Discharge

Valve and

Effects

on .EDG Operability

Abbreviations,

Acronyms,

and Initialisms

AC

AFM

ALARA

ANPO

ANSI

AP

ATWS

BQAP

CCW

CEA

CFR

CIS

CST

DC

DDPS

DEY

ECCS

EDG

FIS

FPL

FSAR

GDC

GL

HP

HPSI

HVE

HX

IFI

IN

I&C

ICW

INPO

IR

ISI

JPE

Alternating Current

Auxiliary Feed Mater (system)

As Low as Reasonably

Achievable (radiation exposure)

Auxiliary Nuclear Plant

I unlicensedj

Operator

American National

Standards

Institute

Administrative Procedure

Anticipated Transient Without Scram

Backfit Quality Assurance

Procedure

(EBASCO Services

Inc.)

Component Cooling Water

Control Element Assembly

Code of Federal

Regulations

Containment Isolation System

Condensate

Storage

Tank

Direct Current

Digital Data Processing

System

Deviation (from Codes,

Standards,

Commitments, etc.)

Emergency

Core Cooling System

Emergency Diesel

Generator

Flow Indication Sensor

The Florida Power

& Light Company

Final Safety Analysis Report

General

Design Criteria (from 10CFR 50, Appendix A)

NRC Generic Letter

" Health Physics

High Pressure

Safety Injection (system)

Heating

and Ventilating Exhaust (fan, system, etc.)

Heat Exchanger

NRC Inspector

Follow-up Item

NRC Information Notice

Instrumentation

and Control

Intake Cooling Water

Institute for Nuclear

Power Operations

Inspection Report

(NRC)

InService Inspection

(program)

(Juno

Beach)

Power Plant Engineering

12

JPN

LTOP

LCO

LER

LPSI

MFIV

MFP

MSIV

MV

'MW

NCV

NPO

NPS

NRC

ONOP

OP

PCM

PIS

PORV

psi 9

ppm

PT

PWO

QA

QC

QI

RAB

RCB

RCO

RCP

RCPB

RCS

Rev

RG

RO

RWT

SALP

~

SAS

SDC

SDCS

SG

SIT

SNPO

SRO

Tavg

TCW

TE

TMI

TR

TS

(Juno

Beach)

Nuclear Engineering

Low Temperature

Overpressure

Protection

(system)

TS Limiting Condition for Operation

Licensee

Event Report

Low Pressure

Safety Injection (system)

Main Feed Isolation Valve

Main Feed

Pump

Main Steam Isolation Valve

Motorized Valve

'Megawatt(s)

Non-Cited Violation (of NRC requirements)

Nuclear Plant Operator

Nuclear Plant Supervisor

Nuclear Regulatory

Commission

Off Normal Operating

Procedure

Operating

Procedure

Plant Change/Modification

Pressure

Indicator/Switch

Power Operated Relief Valve

Pounds

per square

inch (gage)

Part(s)

per Million

Pressure

Transmitter

Plant Work Order

Quality Assurance

Quality Control

Quality Instruction

Reactor Auxiliary Building

Reactor

Containment Building

Reactor Control Operator

Reactor

Coolant

Pump

Reactor Coolant Pressure

Boundary

Reactor Coolant System

Revision

[NRC] Regulatory Guide

Reactor [licensed] Operator

Refueling Water Tank

Systematic

Assessment

of Licensee

Performance

Safety Assessment

System

Shut

Down Cooling

Shut

Down Cooling System

~ : Steam Generator

Safety Injection,Tank

Senior Nuclear Plant [unlicensed] Operator

Senior Reactor [licensed] Operator

Reactor

average

temperature

Turbine Cooling Water

Temperature

Element

Three Mile Island

Temperature

Recorder

Technical Specification(s)

13

URI

NRC Unresolved

Item

VIO 'iolation (of NRC requirements)