ML17209B156

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Forwards LER 81-021/03L-0
ML17209B156
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 05/26/1981
From: Schmidt A
FLORIDA POWER & LIGHT CO.
To: James O'Reilly
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17209B157 List:
References
335-81-21, NUDOCS 8106080296
Download: ML17209B156 (2)


Text

P.O. BOX 529100hllAfvll, FL 33152 0

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May 26, 1981 PRN-LI-81-252 Mr. James P. O'Reilly, Director, Region II Office of Inspection and Enforcement U.S. Nuclear Regulatory Commission 101 Marietta Street, Suite 3100 Atlanta, Georgia 30303

Dear Mr. O'Keilly:

REPORTABLE OCCURRENCE 335-81-21 ST. LUCIE UNIT 1 DATE OF OCCURRENCE: APRIL 24, 1981 TECHNICAL SPECIFICATION 3.3.1.1 FAILURE OF "B" CONTAINMENT PRESSURE DETECTOR

'The attached Licensee Event Report is being submitted in accordance with Technical Specification 6.9 to provide 30 day notification of the subject occurrence.

Very truly yours, A. . Schmid Vice President Power Resources PLP/cab Attachment cc: Director, Office of Inspection and Enforcement (30)

Harold F. Reis, Esquire File 933.1 SL 8XO6OSO ~~~

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