/03L-0 on 780902:during Short Maint Shutdown, Charging Pump 1A Was Found to Have Cracked Pump Casing, Probably Due to Suction cavitation.1Apump Casing Will Be Replaced & Damping Device Installed on Pump Suction Line| ML17206A475 |
| Person / Time |
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| Site: |
Saint Lucie  |
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| Issue date: |
10/02/1978 |
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| From: |
Schoppman M FLORIDA POWER & LIGHT CO. |
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| To: |
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| Shared Package |
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| ML17206A474 |
List: |
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| References |
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| LER-78-034-03L, LER-78-34-3L, NUDOCS 7810120051 |
| Download: ML17206A475 (2) |
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LER-1978-034, /03L-0 on 780902:during Short Maint Shutdown, Charging Pump 1A Was Found to Have Cracked Pump Casing, Probably Due to Suction cavitation.1Apump Casing Will Be Replaced & Damping Device Installed on Pump Suction Line |
| Event date: |
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| Report date: |
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| 3351978034R03 - NRC Website |
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text
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$3 EVENTCATE REPORT QA> 3 30 EVENTOESCRIPTION A>40 PROBABL= CCNScCU i'4CcS ~IQ During a short maintenance
- shutdown, charging pump "1A" was found to have a cracked pump casing.
The pump was stopped and placed out of 4
service.
The water leakage through the crack was minor and it was contained by the radioactive waste management system.
Due to design redundanc the two char in um s remainin in service are capable of plmlping the required design capacity of the CVCS system, and fully meet
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This is the first occurrence of this type.
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The cause has not been confirmed.
- However, a previous engineering
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The "lA" pump casing will be replaced and a a
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damping device (accumulator) will be installed on the pump suction line.
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REPORTABLE OCCURRENCE 335-78-34 LXCENSEE EVENT REPORT PAGE T["TO Additional Cause Descri tion The engineering evaluation of system operation and vibration suggests that suction cavitation, primarily due to piping configuration, may be the cause.
Although the other two pumps are much less subject to this problem due to signi-ficant differences in the suction piping configuration, we plan to install damping devices (accumulators) on the suctions 'of all three (3) charging pumps.
&le are already in 'the procurement stage of this project which will be pursued on an expedited basi's.
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| 05000250/LER-1978-017-03, /03L-0:on 780514,improper Switching at Pratt & Whitney Substation & Incorrect Wiring of Protective Relays at Midway Substation Led to de-energization.Offsite Power Lost.Incorrect Wiring Corrected | /03L-0:on 780514,improper Switching at Pratt & Whitney Substation & Incorrect Wiring of Protective Relays at Midway Substation Led to de-energization.Offsite Power Lost.Incorrect Wiring Corrected | | | 05000250/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000335/LER-1978-025-03, /03L-0 Update on 780905:2 Damper Motors in Suction Line for HVE-9B Blew Fuses in Control Circuits, Causing B Train to Be Oper, Rather than Inoper as Previously Reported.Condition Is Not Reportable Per Tech Specs | /03L-0 Update on 780905:2 Damper Motors in Suction Line for HVE-9B Blew Fuses in Control Circuits, Causing B Train to Be Oper, Rather than Inoper as Previously Reported.Condition Is Not Reportable Per Tech Specs | | | 05000335/LER-1978-033-03, /03L-0 on 780901:During Plant Startup from Short Maint Shutdown, the Dose Equivalent of Iodine Exceeded Tech Spec Due to Plant Shutdown & Subsequent Startup Transients | /03L-0 on 780901:During Plant Startup from Short Maint Shutdown, the Dose Equivalent of Iodine Exceeded Tech Spec Due to Plant Shutdown & Subsequent Startup Transients | | | 05000335/LER-1978-033, Forwards LER 78-033/03L-0 | Forwards LER 78-033/03L-0 | | | 05000335/LER-1978-034-03, /03L-0 on 780902:during Short Maint Shutdown, Charging Pump 1A Was Found to Have Cracked Pump Casing, Probably Due to Suction cavitation.1Apump Casing Will Be Replaced & Damping Device Installed on Pump Suction Line | /03L-0 on 780902:during Short Maint Shutdown, Charging Pump 1A Was Found to Have Cracked Pump Casing, Probably Due to Suction cavitation.1Apump Casing Will Be Replaced & Damping Device Installed on Pump Suction Line | | | 05000335/LER-1978-034, Forwards LER 78-034/03L-0 | Forwards LER 78-034/03L-0 | | | 05000335/LER-1978-035-03, /03L-0 on 780905:During Full Pwr Oper 2 Damper Motors in the Suction Line for ECCS Area Exhaust Fan HVE-9B Blew Control Circuit Fuses,Caused by Loss of Insulating Fluid Thru Leaking Gasket in One Motor,Shorting Both Out | /03L-0 on 780905:During Full Pwr Oper 2 Damper Motors in the Suction Line for ECCS Area Exhaust Fan HVE-9B Blew Control Circuit Fuses,Caused by Loss of Insulating Fluid Thru Leaking Gasket in One Motor,Shorting Both Out | | | 05000335/LER-1978-035, Forwards LER 78-035/03L-0 | Forwards LER 78-035/03L-0 | | | 05000335/LER-1978-036-03, /03l-0 on 780905:during Monthly Surveillance on a Diesel Generator the 4160V Tie Breaker to Its Emergency Bus Would Not Close Remotely from Control Room Due to Dirty Contacts on Oper Relay | /03l-0 on 780905:during Monthly Surveillance on a Diesel Generator the 4160V Tie Breaker to Its Emergency Bus Would Not Close Remotely from Control Room Due to Dirty Contacts on Oper Relay | | | 05000335/LER-1978-036, Forwards LER 78-036/03l-0 | Forwards LER 78-036/03l-0 | | | 05000335/LER-1978-037, Forwards LER 78-037/01T-1 | Forwards LER 78-037/01T-1 | | | 05000335/LER-1978-037-01, /01T-1 on 780919:during Sys Insp,Class I Longitudinal Braces on Auxiliary Bldg Ventilation Ducts Were Found Missing.Caused by Unique Combination of Personnel Errors | /01T-1 on 780919:during Sys Insp,Class I Longitudinal Braces on Auxiliary Bldg Ventilation Ducts Were Found Missing.Caused by Unique Combination of Personnel Errors | | | 05000335/LER-1978-038-01, /01T-0 on 780925,input Error Made to ECCS Analysis Re Containment Spray Flow.Caused by Ambiguous Data Supplied by Ae.Amend to Cycle 2 ECCS Analysis Will Be Issued Shortly | /01T-0 on 780925,input Error Made to ECCS Analysis Re Containment Spray Flow.Caused by Ambiguous Data Supplied by Ae.Amend to Cycle 2 ECCS Analysis Will Be Issued Shortly | | | 05000335/LER-1978-038, Forwards LER 78-038/01T-0 | Forwards LER 78-038/01T-0 | | | 05000335/LER-1978-039-03, /03L-0:on 780930,during Power Operation,Digital Processing Sys Malfunctioned.Caused by Momentary Memory Failure.Sys Repaired & Placed Back in Svc in 70 Minutes | /03L-0:on 780930,during Power Operation,Digital Processing Sys Malfunctioned.Caused by Momentary Memory Failure.Sys Repaired & Placed Back in Svc in 70 Minutes | | | 05000335/LER-1978-039, Forwards LER 78-039/03L-0 | Forwards LER 78-039/03L-0 | | | 05000335/LER-1978-040, Forwards LER 78-040/03L-0 | Forwards LER 78-040/03L-0 | | | 05000335/LER-1978-040-03, /03L-0 on 781002:During Pwr oper,1B Charging Pump Failed to Start While Only 1C Pump Was operable.Cause:1B Suction Pressure Gage Waspegged Highdue to Leaking Valve. Valve Repaired,Gage Vented & Pump Returned to Svc | /03L-0 on 781002:During Pwr oper,1B Charging Pump Failed to Start While Only 1C Pump Was operable.Cause:1B Suction Pressure Gage Waspegged Highdue to Leaking Valve. Valve Repaired,Gage Vented & Pump Returned to Svc | | | 05000335/LER-1978-041, Forwards LER 78-041/01T-0 | Forwards LER 78-041/01T-0 | | | 05000335/LER-1978-041-01, /01T-0 on 781103:water from Reactor Coolant Sys Injected Through a Containment Spray Header.Caused by Improper Clearance Removal Instructions & 2 Isolation Valves Opened Between Spray Sys & Shutdown Cooling Sys by Operator | /01T-0 on 781103:water from Reactor Coolant Sys Injected Through a Containment Spray Header.Caused by Improper Clearance Removal Instructions & 2 Isolation Valves Opened Between Spray Sys & Shutdown Cooling Sys by Operator | | | 05000335/LER-1978-042-01, /01T-0 on 781111:4 Solenoid Operated Naoh Addition Sys Valves Found de-energized Due to Failure to Replace Fuses for Valves SE07-1A,1B,2A & 2B During Plant Heatup & Following Outage | /01T-0 on 781111:4 Solenoid Operated Naoh Addition Sys Valves Found de-energized Due to Failure to Replace Fuses for Valves SE07-1A,1B,2A & 2B During Plant Heatup & Following Outage | | | 05000335/LER-1978-042, Forwards LER 78-042/01T-0 | Forwards LER 78-042/01T-0 | | | 05000335/LER-1978-043-03, /03L-1 on 781120:during Power Operation Cambridge Electron Accelerator 62 Slipped 13 Inches a Second Time to Point 43 Inches Below Original Position.Personnel Misinterpreted Tech Specs | /03L-1 on 781120:during Power Operation Cambridge Electron Accelerator 62 Slipped 13 Inches a Second Time to Point 43 Inches Below Original Position.Personnel Misinterpreted Tech Specs | | | 05000335/LER-1978-043, Forwards LER 78-043/03L-0 | Forwards LER 78-043/03L-0 | | | 05000335/LER-1978-044, Forwards LER 78-044/03L-0 | Forwards LER 78-044/03L-0 | | | 05000335/LER-1978-044-03, /03L-0 on 781121:motor Operated Valve Mv 07-13 Failed to Open Electrically Following Closure Due to Faulty Torque Switch on Valve Operator.Switch Replaced & Valve Checked | /03L-0 on 781121:motor Operated Valve Mv 07-13 Failed to Open Electrically Following Closure Due to Faulty Torque Switch on Valve Operator.Switch Replaced & Valve Checked | | | 05000335/LER-1978-045-03, /03L-1 on 790305:during Power Operation,Digital Data Processing Sys Malfunctioned.Caused by Error in Program Installed by Licensee in June 1978.Program Error Corrected | /03L-1 on 790305:during Power Operation,Digital Data Processing Sys Malfunctioned.Caused by Error in Program Installed by Licensee in June 1978.Program Error Corrected | | | 05000335/LER-1978-045, Forwards LER 78-045/03L-1 | Forwards LER 78-045/03L-1 | | | 05000335/LER-1978-046-03, /03L-0 on 781207:during Power Operation,Control Element Assembly 59 Dropped as It Was Manually Inserted to 100 in Position for Moderator Temp Coefficient Test.Cause Unknown | /03L-0 on 781207:during Power Operation,Control Element Assembly 59 Dropped as It Was Manually Inserted to 100 in Position for Moderator Temp Coefficient Test.Cause Unknown | | | 05000335/LER-1978-046, Forwards LER 78-046/03L-0 | Forwards LER 78-046/03L-0 | | | 05000333/LER-1978-089, Forwards LER 78-089/03L-0 | Forwards LER 78-089/03L-0 | |
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