ML17179A925

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Insp Repts 50-237/93-12 & 50-249/93-12 on 930316-0505. Violations Noted.Major Areas Inspected:Operational Safety Verification & ESF Sys Walkdown & Summary of Operations & Maint & Surveillance Observations
ML17179A925
Person / Time
Site: Dresden  
Issue date: 05/25/1993
From: Hiland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17179A923 List:
References
50-237-93-12, 50-249-93-12, NUDOCS 9306080184
Download: ML17179A925 (17)


See also: IR 05000237/1993012

Text

U.S. NUCLEAR REGULATORY COMMISSION

. REGION II I

Report Nos. 50-237/93012(DRP); 50-249/93012(DRP)

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Licensee:

Commonwealth Edison Company

Opus West III

1400 Opus Place - Suite 300

Downers Grove, IL

60515

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Ir.specticn At:

Morris, IL

Inspection Conducted:

March 16 through May 5, 1993

Inspectors:

Approved By:

Inspection Summary

M. Peck

A. M. Stone

C. Gill

D. Hills

D. Liao

C. Zelig

R. Zuffa, .Illinois/9epartment

/OcJ_ /JLrd_

P. L. Hiland, Chief

Reactor Projects Section lB

Inspection from March 16 through May 5, 1993

(Report Nos. 50-237/93012(DRP); 50-249/93012(DRP))

Date

Areas Inspected: Routine, unannounced inspection by resident inspectors,

regional inspectors, and an Illinois Department of Nuclear Safety inspector.

The inspection included followup of licensee action on previous inspection

findings; temporary instructions; summary of operations; operational safety

verification and engineered safety feature (ESF) system walkdown; maintenance

and surveillance observations; engineering and technical support observations;

safety assessment and quality verification; licensee event reports (LERs);

refueling activities, report review, and management meetings.

Results:

Of the ten areas inspected, no violations were identified in eight

areas.

One violation concerning an inadequate work instruction was identified

in paragraph 5.b.

An additional example of a previous violation, 237/93011-

01, concerning the failure to follow out-of-service procedures, was identified

in paragraph 5.b. A non-cited violation concerning the failure to adequately

maintain critical drawings control was identified in paragraph 6.

An

unresolved item associated with inspector concerns related to the fire

protection system was described in paragraph 6.

9306080184 930526

PDR

ADOCK 05000237

G

PDR

Assessment of Plant Operations

Operations personnel conducted themselves in a professional manher.

Control

room demeanor was good.

Fuel handling operation~ during the Unit 2 reload was

good.

A decision associated with the main control room habitability system

was non-conservative. Housekeeping was poor during the inspection period.

Assessment of Maintenance and Surveillance

The performance of maintenance and surveillance activities was good.

A

violation for a poor work package and examples of poor foreign material

exclusion practices were identified.

Ari out-of-service error by contractor

personnel resulted in the flooding of an emergency core cooling system corner

room.

The conduct of the Unit 2 refueling outage was significantly better

than previous outages.

Assessment of Engineering and Technical Support

Engineering and technical support was considered weak.

Concerns were

identified during review of a fire protection safety evaluation, control of

critical control room drawings, and a contractor prepared hydraulic analysis.

Assessment of Radiological Controls

Work practices were good as evidenced by the low.dose received by workers

associated with the remova.l of a source range monitor .

2

DETAILS

1.

, Persons Contacted

C.

~chroeder, Manager, Dresden Station

_

  • D. Booth, Electrical Maintenance Department Master
  • E~ Carroll, Chemistry Supervisor
  • A D'Antonio, Site Quality Verification Supervisor
  • R. Flahive, Technical Superintendent

.

  • B. Gurley, NRC Coordinator, Regulatory Assurance
  • M. Hayworth, *Lead Heal th Physicist-Operator
  • R. Janecek, Independent Review Group Member
  • R. Johnson, OPEX Administrator

F. Kanwischer, Services Superintendent

M. Korchynsky,' Senior Operating Engineer

  • J. Kotowski, Manager of Operations

S. Lawson, Operating Engineer

T. Mohr, Operating Engineer

  • T. O'Connor, Assistant Superintendent, Maintenance
  • R. Radtke, Executive Assistant to Sit~ Vice- President

J. Shields, Regulatory Assurance Supervisor

R. Stobert, Operating Engineer

M. Strait, Technical Staff Supervisor

  • B. Viehl, Engineering Supervisor
  • Indicates p~rsons present at the exit interview on May 5, 1993.
  • The inspectors al so contacted other licensee personnel fnc l ud i ng members

of the operating, maintenance, security, and engineering staff.

2.

Licensee Actions on Previous Inspection Findings (92701, 92702)

Violations

(Closed) Vi6lation (237/92009-0JfDRP)):_ inoperability of a low press~re

coolant injection sYstem due to ~n jmproperly set torque switch on a

reactor recirculation valve (2-202-SA}~ On August 7, 1991, operations

personnel were unable to.close the 2-202-5A valve against system

differential pressure during the recirculation pump start sequence.

The

failure was due to a misinterpretation of the VOTES trace data and

subsequent incorrect closing thrust value.

The licensee's corrective

actions included:

The station motor operated valve (MOV} coordinators w~re trained

  • to use an e_nhanced diagnostic software package by the VOTES

vendor.

A commitment to involve corporate engineering personnel for the

proper disposition should any uncertainty in data interpretation

exist in the future.

3

Dresden Maintenance Proced_ure 40-10,

11VOTES System Operating

Procedure," was enhanced to require independent review of the

valve thrust windows.

All corrective actions were complete. This viQlation is closed.

{Closed} Violation {249/92023-03{DRPll:

Failure to perform a techni~al

specifi~ation (TS) required reactor water sample.

Th~ licensee

implemented a computer tracking system for chemistry related TS

surveillances. All corrective actions were complete. This violation is

closed.

Unresolved Items

(Closed) Unresolved Item (237/92005-06(DRP)):

Degraded containment

cooling service water system flow and incorrect low pre~sure coolant

injection system heat exchanger duties. This unresolved item- was the

subject of Special Inspection Report_50-237/92034(DRP).

This item is

closed.

Inspector Followup Items

{Closed} Inspector Followup Item (249/92002-0l{DRPll:

Corrective

actions prior to the Unit 2 refuel outage.

The inspectors reviewed the

licensee's corrective actions in the areas of fuel handling, procedural

-upgrades, equipment upgrades, and training enhancements.

The corrective

actions were complete. This item is closed.

Temporary Instructions (Tl)

(Closed} TI 2515/119:

Water Level Instrumentation Errors During and

After Depressurization Trarisients (Generic Letter 92-04).

The TI

focused on the licensee's response to water level instrumentation

anomalies resulting from non-condensible gases evolving in level

reference legs during rapid reactor depressurization events.

The

inspector's reviewed licensee action in response to Generic Letter 92-0~

and noted the following:

Licensed operators were found knowledgeable and capable of

executing the g~idance provided by Boiling Water Reactor Owners

Group (BWROG) Emergency Procedures Committee (EPC) '.

All licensed operators received classroom training on BWROG

guidance.

Operations personnel had not received specifit simulator trainin~

on the phenomenon.

However, during the inspection period the

plant simulator software was modified to model the anomalies.

The

inspectors observed an operating crew correctl~ responded to a

transient using the modified software.

4

The Emergency Operating Procedures were consistent with the BWROG

guidance.

-

The licensee did not routinely inspect the reference legs for

indications of leakage to minimize the likelihood of level

indicating errors.

The licensee had not reviewed past depressurization events to

determine if the instrument anomaly occurred at the station.

No violations or deviations were identified.

3.

Summary of Operations

Unit 2

The unit was maintained in cold shutdown condition durin~ the

inspection period for refueling and modifications.

Unit 3

The unit was restarted on April 28 following a 60-day forced outage to.

facilitate repair of the main high pressure turbine.

No violations or deviations were identified.

4. -

Plant Operations (71707 & 93702)

Tours of accessible areas of the plant were conducted to observe plant

equipment conditions including potential fire hazards, fluid leaks and

excessive vibration, and to verify that equipment discrepancies were

noted and being resolved by the licensee .

On a sampling basis the inspectors observed control room staffing and

coordination of plant activities; observed operator aqherence to

procedures and technical specifications; monitored control room

indications for abnormalities; verified that electrical power was

available and observed the frequency of plant and control room visits by

- station managers.

The inspectors also monitored various administrative

and operating records.

The specific areas observed were:

Engineered Safety Features (ESF) Systems

Accessible portions of ESF systems and associated support

components were inspected to verify operability through

observation of instrumentation and proper valve and electrical

power alignment.

The inspectors visually inspected components for

material conditions.

The following systems were inspected by

direct field observations:

5

Unit 2

Control Rod Drive* (CRD) *

Standby Liquid Control

Containment Cooling Service Water (CCSW)

Unit 3

Low Pressure Coolant Injection (LPCI)

Isolation Condenser (IC)

High Pressure Coolant Injection Turbine and Support Compo~ents

4.lKV and 480V Electrical Distribution Systems

Radiation Protection Controls

The inspectors ~erified that workers were following health physics

procedures and randomly examined radiation protectfon

instrumentation for.operability and calibration.

The Unit 3 source range monitor 24 was remtived using a special

procedure and equipment on April 20. *The llcensee ~sed a shielded

bucket method de~eloped at Duane Arnold Energy Center.

Thi~

method was used because of the radiation hazards involved and the

high activation of the detector cable and tubing.

Special

equipment was obtained from the Duane Arnold Energy Center for the

removal.

Personnel from Duane Arnold were present to assist

during the evolution.

The licensees' ~slow as*reasonably

.

achievable (ALARA) planning resulted in no personal contaminations

and a dose exposure to workers of less than 570 millirem.

Security

During the inspection period, the inspectors monitored the

licensee's security program to ensure that observed actions were

being implemented according to the licensee~s approved security

pl an.

Housekeeping and Plant Cleanliness

The inspectors monitored the status of housekeeping and plant

cleanliness for fire protection and protection of safety-related

~equipment from intrusion of foreign matter.

Housekeeping during the inspection period was poor.

Examples

included the following:

Seventeen non-secured trunks and several piles of fencing

material, trash, and scaffold1ng stored in .the Unit 3

isolation condenser room.

Trash and tools stored in the Unit 3 480-volt reactor

building board room .

6

Grout chips left on equipment and on the floor of the Unit 2

high pressure coolant injection room.

Debris taken out of

the room was left piled in the doorway.

Improperly Stored Compressed Gas Cylinders

Multiple examples of improperly stored compressed gas cylinders

were observed by the inspector. This included unsecured

cylinders, flammable gas cylinders stored next to oxygen

cylinders, and cylinders restrained by chains around valves.

The

licensee promptly corrected the conditions. Also, the Plant

Safety Advisor requested all department supervisors review the

compressed gas cylinder safety policy for use and storage, ensure

all employees and contractors understand and follow the policy,

and to inspect work areas to confirm compliance.

Shutdown Safety Management Signs

The inspector identified a Shutdown Safety Management Protected

Pathway component sign lying on the Unit 2 drywell grating.

The

sign indicated the electromagnetic relief valves (EMV) were a

"protected component."

However, the sign was not attached to the

EMVs or related components.

The inspector previously identified

an unattached Protected Pathway sign in the drywell on March 10,

1993, as documented in Inspection Report Nos. 50-237/249-

93011 (DRP).

Failure to adequately control the placement and removal of the

Protected Pathway signs was considered a weakness in the

implementation of the shutdown safety program.

The signs

prevented inadvertent operation of components that could

potentially affect reactor vessel inventory.

The signs were used

during periods when shutdown risk activities were in progress.

This is considered an Inspector Followup Item (50-237/93012-01)

pending review of the licensee's corrective actions.

Foreign Material Exclusion

Prior to Unit 3 startup the inspectors found a metal air hose

coupling and a spray nozzle attachment lying in a main generator

potential current transformer (PCT) pull-out drawer.

The coupling

could have resulted in a failure of the main generator due to its

proximity to the PCT wiring and fuse terminal blocks.

The licensee's foreign material exclusion (FME) program was

described in Dresden Administrative Procedure (OAP) 3-23, "Foreign

Material Exclusion Program," and OAP 7-35, "Foreign Material

  • Exclusion Program for the Unit 2/3 Refueling Floor."

However,

electrical cubicles and compartments were not included in the

licensee's FME program.

7

The inspectors observed FME measures during maintenance on the

Unit 2 reactor feed pumps.

The casings of two pumps were removed

in preparation for*machining the stationary vanes.

Numerous

visible gaps existed between the synthetic fabric FME barrier and

the pump casing surfaces. Undetected debris could have entered

the pump discharge piping and be fl us_hed into the feed.water

system.

The observations noted above were discussed with cognizant

licensee personnel as examples where the FME program could be

strengthened.

a.

Operational Events

The Unit 2/3 emergency diesel generator (EOG) automatically

started when operations personnel transferred plant loads

from the rese_rve auxiliary transformer to the station

auxiliary transformer on April 28.

The ESF actuation was

the result of a broken auxiliary contact on one of the

feeder breakers to bus 33.

This event will be further

reviewed in a subsequent report.

A Unit 3 Group V isolation occur~ed on April 21.

The

isolation occurred during valve operator diagnostic testing

on the isolation condenser condensate return valve to the

reactor (MOV 3-1301-3).

The isolation signal resulted from

flow induced vibrations when the valve ~as man~ally opened_

from the fully closed position. This event will be further

reviewed in a subsequent report.

The Unit 2 EOG output breaker failed to close during an

undervoltage test on April 18.

The failure resulted from a

misaligned linkage. to an auxiliary contact on an alternate

bus feed breaker. This event will be further reviewed i~ a

subsequent report.

A standby gas treatment system automatic start and a partial

Unit 2 group II isolation occurred following a blown fuse on

.April 6.

The fus~ blew after engineering and construction_

personnel caused an electrical short circuit while working

on the drywell floor drain sump isolation valves

(2-2001-105 and 106). This event will be further reviewed

in a subsequent report.

-

An unexpected Unit 2 partial Group II isolation occurred on

March 30.

The isolation occurred when electrical

maintenance personnel lifted the neutral lead from the relay

coil for the drywel l equipment sumps (2-2001-106Xl). This

event will be further reviewed in a subseq~ent report.

8

5.

b.

Observations of Plant Operations

Control room operators generally performed licensed dutfes well.

The inspectors observed good procedural adherence, communications,

and use of repeat-backs.

However, the in~pectors observed

examples of poor attention to control room panels {looking toward

center-desk for long periods) and lengthy discussions on n6n-work

related,subjects during the Unit 3 startup by the on-shift crew.

One example of horseplay in.the control room involving a licensed

operator was noted by a quality assurance inspector. The licensee

took disciplinary action against the individual involved.

An example of a non-conservative operational decision was noted

during the inspection period. The licensee proceeded with Unit 2

core alterations and the restart of Unit 3 with an inoperable main

control room emergency ventilation system.

As discussed in

Inspection Report 50-237/93011, both trains of the qualified

service water supply were intentionally removed from service in

January for scheduling considerations.

The decision to allow the

Unit 2 fuel reload and the start-up of Unit 3, although permitted

by technical specification, with the degraded main control ro.om

emergency ventilation system was non-conservative.

No violaticins or deviations were identified.

One inspector followup

  • tern was identified regarding the shutdown safety program.

Monthly Maintenance and Surveillance (62703 and 61726)

Routinely, station maintenance and surveillance activities were,observed

or reviewed to astert~in that they were conducted in accordance with

approved procedures, regulatory guides and industry codes or standards,

and in conformance with technical specifications.

The following items we~e also considered during this revjew: approvals

were bbtained prior to initiating the work and testing and that

operability requirements were met during such activities; functional

testing and calibrations were performed prior to declari~g the component

operable; discrepancies identified during the activities were resolved

prior to' returning the component to service; quality control records

were maintained; and activities were accomplished by qualified

personnel ..

a.

  • Maintenance and Surveillance Related Activities

Unit 2

Removal and Overhaul of the 2C LPCI Pump Motor

Rebuild of 28 and 2C CCSW Pumps

Replacement of Unit 2 CCSW Flow Orifice

CRD Return Line Capping

Rebuild of the Condensate and Condensate Booster Pump

MSIV Pilot Operator Replacement

Fue 1 Grapp'l e Repair

9

-.

Source Range Monitor 21 Repair and Replacement

Feedwater Nozzle Repair

_

Core Spray Penetration Bellows (X-149A) Replacement

Rebuild Isolation Condenser Steam Supply Inboard Isolation Valve

Unit* 3

Main Turbine High.Pressure Turbine Repair

. Rebuild of the* 3C Reactor Feed Pump

3B LPCI Pump Impeller Balancing

Electrical Disconnection_ of MOV-3-2301-6 (HPCI).

SRM 24 Replacement

3D LPCI Pump Vibration Testing and Analy~is

The inspectors witnessed portions of the following test activities

Unit 2

DIS 1500-05, LPCI Logic Testihg

DOS 6600-06, Bus Undervoltage and ECCS Integrated Functional Test

for the Unit 2/3 Diesel Generator

Unit 3

DOS 1500-02, Quarterly CCSW Pump.Test

DOS 1500-06, LPCI System Pump Operability Test

DOS 1500710, LPCI Quarterly Pump fn Service Test

DOS 1400-01, Core Spray System Pump Test

DOS 2300-03, HPCI Operability Verification

DOS 2300-01, HPCI Valve Ops

.

DOS 1600-05, Unit 3.Quarterly Valve Timing

DTS 8138, Nuclear Instrumentation Overlap Verifications for IRMs

DOS 1600-14, Oxyg~n Analyzer and Sampling System Calibration and.

Functional Test

DTS 8135, Source Range Monitor Performance

DOS 2300-03, HPCI *system Operability Veri fi cation

DOS 2300-08, HPCI Pump Discharge Line Temperature Monitoring

b.

Maintenance and Surveillance Observations

Unit 2 HPCI Turbine Repair

The inspectors reviewed the installation of the Unit 2 high

pressure coolant injection turbine exhaust piping.

The bolts used

to secure the t~rbine top flange were ultrasonically tested prior

to installation. A temporary Garlock gasket was used on the

.

turbine exhaust flange to provide a ~attern for the permanent

gasket. A Flexitallic ga~ket was subsequently installed on the

flange prior to completion of the work.

Th~ inspectors observed

both contract and station craftsmen review work packages and

discussed with those individuals available methods to report

problems.

-

10

Incorrect Breaker Installed in Unit 2 Cubicle

On March 10, 1993, the main feed breaker for motor control center

29-5/6 failed to open during the performance of Dresden Instrument

Surveillance (DIS) 1400-01, "Core Spray L~gic Testing on B Core

Spray System."

The breaker failed to open because the *shunt trip

device, as specified on drawing 12E-2374, was not installed ..

The breaker was modified, per M12-2-91-25, in Decemb~r 1991 to

included the shunt trip device.

The modification ensured adequate*

voltage for the diesel generator cooling water pump by providing

load shed of the non-essential condensate storage tank heater

during a loss of coolant accident.

On October 12, 1992, the

breaker was removed for preventative maintenance.

The breaker

cubicle remained empty until February 4, 1993, when a different

refurbished manual breaker was installed. However, the work

package failed to specify a manual breaker with a shunt trip

device.

The work package preparer did not know a shunt trip

device was required on the breaker.

The safety significance of this event was minimal because the

error was identified before startup. However, the potential

. existed for an inoperable diesel under different plant conditions.

Corrective actions included:

Installation of the shunt trip device and retesting,

Review of other breakers for speci~l characteristics and

feature_s, and

Revision to the work analysts' breaker removal and

installation instructions.

Failure to install a shunt trip device on the 29-5/6 feed breaker,

in accordance with Drawing 12E-2374, revision AA, is a Violation

of 10 -CFR 50, Appendix B, Criterion V (50-231/93012-02).

However,

the corrective actions were reviewed by the inspectors prior to

the close of the inspection perind and were found adequate.

Therefore, no response to this_ violati6n was required.

Unit 2 West ECCS Corner Room Flooding Due to Personnel Error

Approxima'tely 9,500 gallons of service water sprayed into an

emergency core cooling system (ECCS) corner room on April 1.

The water level in the room rose to about 18 inches. Operatlons

p~r~onnel, in the ar~a at the time of event, quickly responded to

isolate the service water line upstream of the breach.

The

licensee entered the appropriate emergency procedures and verified

redundant safety system operability.

The licensee inspected

instrumentation, junction boxes and conduits for water intrusion

and meggered the affected ECCS pumps.

11

6.

The flooding occurred when contractor maintenance pe~sonnel

disconnected a flange on the service water piping upstream of an

out-of-service boundary.

The event was caused by mis-

communication and failure to properly review the work package.

Contributing to the event was a generic misunders~anding of out-

of-service boundaries by the contractors and inadequate

communication of the foreman's expectations.

Corrective actions

included:

Stopping all contractor work to reinforce procedure and out-

of-service boundary adherence.

Termination of employment for the individuals involved.

Revision of the pre-job briefing checklist to include a

required check list for each work request.

Reinforced the self check program and personnel safety

practices during pre-shift briefings.

Dresden Administrative Procedure (OAP) 03-05, "Out-Of-Service and

Personnel Protection Cards,

11 controlled the out-of-service program

with regards to equipment and personnel protection.

Disconnection

of the flange up-stream of an out-of-service boundary was contrary

to OAP 03-05 and was considered another example of Violation 50-

237/93011-0l(DRP).

The licensee established a team to investigate

the root cause and develop corrective action for this and other

out-of-service errors.

The results of that investigation will be

reviewed in a subsequent inspection.

One violation and an example of a previous violation were identified .

Engineering and Technical Support (37700)

The inspectors evaluated the extent to which engineering principles and

evaluations were integrated into daily plant activities. This was

accomplished by assessing the technical staff involvement in non-routine

events, outage-related activities, and assigned TS surveillances;

observing on-going maintenance work and troubleshooting; and reviewing

deviation investigations and root cause determinations.

Fire Protection System Concerns

The inspectors reviewed the ability of the fire protection system to

provide makeup water to the isolation condenser during fire suppression.

The inspectors were concerned about the adequacy of the safe shutdown

and surveillance procedures *to ensure adequate inventory was available

for the isolation condenser.

The inspector's concerns included:

The cross-tie valve between the lA Condensate Storage Tank (CST)

and 2/3A and 2/3B CSTs was closed since April 1988.

The safe

shutdown procedures did not provide instructions to the operators

12

to open the cross-tie valve to ensure water in the lA CST would be

made available to the isolation condenser during safe shutdown

6perations.

The licensee took credit for the water in all three

CSTs to satisfy the 260,000 gallonrequirement.

The 260,000

gallons ensured adequate makeup water to the isolation condensers

and proper operation of th~ high pressure.coolant injection (HPCI)

system.

The Fire Hazard Analysis (January 1986).assumed administrative

controls were in place to ensure adetjuate make-up was available

for the isolation cohdenser and the reactor pressure vessel (RPV).

Prior to August 1989, the licensee did not have surveillance

mechanisms to ensure the necessary amount of water was maintained

in the CSTs.

The licensee used an unqualified local instrument to verify IA CST

level.

The licensee failed to compensate for the head differences between

the CST level instruments and the piping leading to the isolation

condenser during level surveillances.

As a result,*the indicated

CST volume was non-conservative.

The licensee did not perform an adequate safety evaluation for

reactor operation with the lA CST cross-tie valve closed. The

licensee also failed to evaluate the effect on the makeup

capability to the isolation condenser.

Professional Loss Control, Inc. (PLC) performed a hydraulic study of the

fire protection system in February 1985.

The study concluded the

limiting case scenario existed when th~ most critical section of piping

was out of service. The limiting case prevented the system from meeting

design requirements; therefore, the licensee modified the fire*

protection system. A new limiting case was createp i.e. 2/3 diesel fire

pump out of service. Since other scenarios were not evaluated after the

modification, assurance that a new limiting case had not been created

was not proVided.

These concerns ~ere discussed with the licensee and are considered an

Unresolved Item (50-237/93012~03(DRP)) pending furthe~ NRC review.

Inspection of Recirculation Manifold Cross .Tie Valve

A through wall circumferential crack, located at the weld connecting the

equalizing line to the recirculation manifold cross-tie valve, was

identified at the Quad Cities facility on April 2.

Sirice the Dresden

piping configuration was similar to Quad Cities, the licensee also

inspected the Dresden equalizing line.

No problems were identified .

13

Control of Critical Control Room Drawings

The inspector identified several discrepancies with the critical control

room drawings.

The licensee performed a self assessment which

identified additional deficiencies with thirty three percent of the 484

critical drawings.

The problems found included~

Outstanding design change requests were not marked on drawings.

Inaccuracies between identical critical drawings stored at

different locations.

Numerous temporary alterations not reflected on drawing.

The licensee promptly corrected all identified problems.

Long term

corrective actions included revision of the critical drawing procedure

and review of all outstanding temporary alterations prior to Unit 3

start-up.

Dresden Administrative Procedure (OAP) 02-09, "Control of Critical

Orawings,

11 outlined the method required to ensure accuracy of field

installations and plant drawings.

Technical Specification (TS) 6.2.A

required that written procedures listed in Appendix A of Regulatory

Guide 1.33, Revision 2, February 1978 shall be established, implemented

and maintained.

The failure to follow OAP 02-09 was considered a

Violation of TS 6.2.A.l.

However, the licensee identified a majority

of the violation examples and implemented prompt corrective actioni.

Therefore, a violation is not being cited because the criteria specified

in

10 CFR 2, Appendix C, part VII.B were satisfied.

One unresolved item and one non-cited violation were identified.

No

deviations were identified.

7.

Safety Assessment and Quality Verification (40500)

The effectiveness of management controls, verification and oversight

activities in the conduct of jobs observed during this inspection.were

evaluated.

Management and supervisory meetings involving plant status

were attended to observe the coordination between departments.

The

results of licensee corrective action programs were routinely monitored

by attendance at meetings, discussion with the plant staff, review of

deviation reports, and root cause evaluation reports.

No violations or deviations were identified.

8.

Licensee Event Reports (LERs) Followup (92700)

Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to

determine that reportability requirements were fulfilled, immediate

corrective action was accomplished, and corrective action to prevent

14

recurrence had been accomplished in accordance with technical

specifications.

The LERs listed below are considered closed:

UNIT 2

(Closed) LER 237/91-028:. Violation of Technical Specification Limits on

Torus Bulk Water Temperatuie. This item was the subject of Violation

50-237/91035-0l(DRP).

(Closed) LER 237/92-024:

HPCI Declared Inoperable Due to Turning Gear

Motor Failure.

(Closed) LER 237/92-027-01:

Failure to Sample Reactor Water Due to

Personnel Error and Programmatic Weakness.

The missed sample discussed

in the LER was considered a Violation of Technical Specification *4.6.C.2

{249/92023~03(DRP)). *This supplemental LER addressed the inspector's

concerns documented in Inspection Report 50-237/92023.

UNIT. 3

(Closed) LER.249/89-005:

HPCI Declared Inoperable Due to.Cable Terminal

Blocks Not Environmentally Qualified.

{Closed) LER 249/92-015:

Low Pressure Coolant Injection Pump Minimum

Flow Auto~atic Closure During Valve Operational Test.

The inspectors reviewed the licensee's problem. identification forms

(PIFs) generated during the inspection period. This was done to monitor

the conditions re1ated to plant or personnel perfor~ance and potential

trend: Tha results of the investigations were also reviewed to ensure*

that PIFs were generated appropriately and dispositioned in a manrier

consistent with the applicable procedures and the quality assurance

manual.

No violations or deviations were identified.

9.

Refueling Activities (60710)

The inspector verified that refueling activities were conducted and

controlled as required by technical specifications and approved

procedures. This was done on a sampling basis through direct

observation of activities and equipment, tours of the facility,

interviews and discussions with licensee personnel, and independent

verification of safety system status and limiting conditions for

operation (LCOs) action requirements.

The inspector observed fuel

movement during the D2Rl3 core reload and verified core alterations were

performed in a safe manner.

Fuel handling personnel displayed a positive application of. the "Self-

Chetk" process during. the Unit 2 fuel reload.

Fuel handling was

suspended several times to collectively verify previous actions and

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procedure compliance ..

An aggressive questioning attitude by the fuel

handling personnel led to a completed Unit 2 core reload without

significant error.

No violations or deviations were identified in this area. *

10.

Report Review (90713)

During the inspection period, the inspector reviewed the licensee's

Monthly Performance Reports for January, February and March 1993.

The

inspector confirmed that the information provided met the requirements

of Technical Specification 6.6.A.3 and Regulatory Guide 1.16.

~o violations or deviations were identified.

11.

Management Meetings (30703)

A management meeting was conducted at the Dresden station on March 30,

1993.

Mr. J. A. Zwolinski, Assistant Director for Region III Reactors,

Office of NRR, was in attendance.

Monthly Dresden Plant Information meetings were held at the Region III

office on March 31 and at the Dresden site on April 30.

The Region III

Regional Administrator, A. B. Davis, attended both meetings.

The

meetings discussed the resolution of technical issues, outage dose,

outage schedule, and self assessment.

NRC Commissioner J. R. Curtiss met with several licensee management

personnel on April 9.

The meeting focused on the current status of the

facility and improvement initiatives.

12.

Inspector Followup Items

Inspector followup items are matters which have been discussed with the

licensee which will be reviewed further by the inspector and which

involve some action on the part of the NRC or licensee or both.

One

inspector followup item disclosed during this inspection is discussed in

paragraph 4.

13.

Unresolved Items

Unresolved items are matters about which more information is iequired in

order to ascertain whether they are acceptable items, items of

noncompliance or deviations.

One unresolved Item disclosed during this

inspection was discussed in paragraph 6.

14.

Licensee Identified Violations

The NRC uses the Notice of Violation as a standard method for

formalizing the existence of a violation of a legally binding

requirement.

However, because the NRC wants to encourage and support

licensee's initiatives for self-identification and correction of

16

problems, the NRC will not generally issue a Notice of Violition for a

violation that meets the tests of 10 CFR 2, Appendix C, Section VII.B.

These tests are:

t

It was not a violation that could reasonably be expected to have

been prevented by the licensee's corrective action for a.previous

violation.

t

The violation was or will be corrected, including measures to

prevent recurrence, within a reasonable time; and

t

It was not a willful violation.

One violation of regulatory requirements identified during this

inspection for which a Notice of Violation will not be issued was

discussed in Paragraph 6.

15.

Exit Interview (30703)

The inspectors met with licensee representatives (denoted in

-Paragraph 1) throughout the inspection period and at the conclusion of

the inspection on May 5, 1993, to summarize the scope and findings of

the inspection activities. The licensee acknowledged the inspectors'

comments.

The inspectors also discussed the likely informational

content of the inspection report with regard to documents or processes

reviewed by the inspectors during the inspection. The licensee did not

identify any such documents or processes as proprietary.

17