ML16342D435

From kanterella
Jump to navigation Jump to search
Insp Repts 50-275/96-16 & 50-323/96-16 on 960707-0803. Violations Noted.Major Areas Inspected:Operations,Maint & Engineering
ML16342D435
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 09/12/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D434 List:
References
50-275-96-16, 50-323-96-16, NUDOCS 9609230043
Download: ML16342D435 (96)


See also: IR 05000275/1996016

Text

ENCLOSURE 2

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:'nspectors:

50-275,

50-323

DPR-80,

DPR-82

50-275/96016.

50-323/96016

Pacific Gas

and Electri'c Company

Diablo Canyon Nuclear

Power Plant.

Units

1 and

2

7 1/2 miles

NW of Avila Beach

Avila Beach, California

July 7 through August 17,

1996

M. Tschiltz, Senior Resident

Inspector

S.

Boynton. Resident

Inspector

C. Paulk, Division of Reactor Safety,

Region

IV

B. Olson, Project Inspector,

Region

IV

P. Goldberg, Division of Reactor Safety,

Region

IV

D. Corporandy,

Project Inspector,

Region

IV

Approved By:

R. Huey, Acting Chief, Branch

E

Division of Reactor Projects

ATTACHMENTS:

ATTACHMENT 1:

ATTACHMENT 2:

ATTACHMENT 3:

ATTACHMENT 4:

Partial List of Persons

Contacted

List oi Inspection

Procedures

Used

List of Items Opened.

Closed,

and Discussed

List of Acronyms

List of Attendees

at the July 1,

1996.

Predecisional

Enforcement

Conference

Apparent Violations as Originally Proposed for the

Predecisional

Enforcement

Conference

Licensee Presentation

Slides for the Predecisional

Enforcement

Conference

960'7230043

960'Vi2

PDR

ADOCK 05000275

8

PDR

EXECUTIVE SUMMARY

Diablo Canyon Nuclear

Power Plant, Units

1 and

2

NRC Inspection Report 50-275/96016;

50-323/96016

~0erations

~

Following the loss of instrumentation

on the primary and secondary

meteorological

towers,

the shift supervisor

and regulatory services

staff failed to recognize the requirement to report the event in

accordance

with plant procedures

and

10 CFR 50.72.

A noncited violation

was identified (Section 01.2).

~

Both Units

1 and

2 operators

were challenged

by equipment

problems

following the dual unit trip caused

by a power grid disturbance.

Operator

response

to reduce

steam pressure

below the main steam safety

valve

(MSSV) lift pressure

on both units

and restore Unit 2 reactor

.coolant

pump

(RCP) seal injection flow was prompt and effective,

and

prevented additional complications

(Section 01.3).

~

Both the Unit 1 Control Operator

and Senior Control Operator

(SCO) were

observed escorting visitors while on watch.

The practice of allowing

the operator at the controls

and the

SCO to be assigned

the duties of

visitor escort creates

the potential to distract the operators

attention

from assigned

duties

and is considered to have

been

a weakness

in shift

management

oversight of'perator activities (Section 08.1).

~

Operators failed to properly position containment

fan cooler unit (CFCU)

2-3 and 2-4 speed selector

switches following surveillance testing which

resulted in the associated

high speed

breakers tripping following a bus

transf'er to startup

power due to a power

system grid disturbance.

A

noncited violation was identified (Section 01.3).

Maintenance'he

lift pressures

of three of'he five HSSVs associated

with Steam

Gener ator

(SG) 1-1 were improperly set .when personnel

performing. the

maintenance

inadvertently uti ized the valve-specific correction factors

for the

MSSVs associated

with SG 2-1 (Section E1.2).

Maintenance

personnel

did not adequately self-verify and review work

activities which resulted in one train of reactor trip permissive

P-4

being inoperable for a period of over 2 months.

A noncited violation

was identified (Section Hl.2).

Improper restoration

from maintenance

resulted in the failure to

maintain the TS required

number of Unit 1 reactor coolant leakage

detection

systems

in service.

A noncited violation was identified

(Section M8.1).

Licensee

management

was adequately tracking the backlog of corrective

maintenance:

however.

there were no organizational

goals set for

0

-2-

reducing the number of existing corrective maintenance

items

(Section, M6.1) .

~E

~

Engineers failed to perform

a prompt operability assessment

(POA) for

a

period of ten days after discovering

an emergency diesel

generator

(EDG)

voltage regulator with scorched resistor

and circuit board

and circuitry

different from that specified in the design

document.

A violation was

identified (Section E1.1).

Summar

of Plant Status

Re ort Details

Unit 1 began the period at

100 percent

power.

On July 12,

power

was reduced

to 50 percent to facilitate cleaning of the circulating water

Pump 1-2 tunnel.

The unit was returned to full power on July 15.

On July 19, Unit

1 was

curtailed to 48 percent

power to make repai rs on the main feedwater

Pump 1-1

control oil system.

Repairs

were completed

and the'nit returned to

100 percent

power on July 20.

On August 10, Unit 1 tripped on

12 kV bus

under voltage due to a significant grid disturbance

on, the Pacific Inter-tie.

The unit returned to Mode

1 on August

16 and reached

100 percent

on August 17.

Unit 2 began the period at 100 percent

power.

On August 1, the unit entered

Mode 2 and secured

the main turbine due to a nonisolable

leak on the turbine

electrohydraulic control oil system.

The unit returned to full power on

August 3.

On August 10, Unit 2 tripped due to loss of all four RCPs.

The

RCP

breakers

opened

due to an undervoltage condition on the

12 kV auxiliary and

startup

busses

caused

by

a significant grid disturbance

on the Pacific

Inter-tie.

The unit returned to Mode

1 on August

15 and was at 90 percent

power at the end of the inspection period.

I. 0 erations

Ol

Conduct of Operations

Ol. 1

General

Comments

71707

Using Inspection

Procedure

71707. the inspectors

conducted

frequent

reviews of ongoing plant operations.

In general,

the conduct of

operations

was professional

and safety-conscious.

01.2'oss

of Primar

. and Secondar

Meteorolo ical Instrumentation

a.

Ins ecti on Sco

e

71707

On July 27, the secondary

meteorological

tower instrumentation

was

damaged

as

a result of'

lightning strike to the tower.

The primary

meteorological

tower was concurrently out of service for extensive

maintenance.

The inspector

reviewed the licensee's

actions in response

to this event

and Procedure XIl.I02, Revision 3A, "Regulatory Reporting

Requirements

and Reporting Process."

b.

Observations

and Findin s

In response to the loss of the secondary

meteorological

instrumentation.

the licensee

established

a communication data link with the National

Weather Service Point Bouchon Station

and

made available

an onsite

portable meteorological station for local indications of weather

conditions.

Subsequently,

the licensee set

up several

additional

meteorological

instruments that could be polled from the control

room.

The secondary

meteorological

tower was returned to service

on July 30.

0

Procedure

XI1. ID2 provides specific guidelines for determining the

reporting requirement of various events.

In accordance

with

Attachment 8.6 of Procedure

XI1.ID2, a total loss of primary and

secondary

meteorological

tower indications requires

a 1-hour

nonemergency

report to the

NRC as directed

by 10 CFR 50.72(b)(1)(v).

On

July 28, the inspectors

discus'sed

the loss of the meteorological

instrumentation with the shift supervisor

(SS)

and questioned

the need

for reporting the event to the

NRC.

The

SS determined that the event

was reportable in accordance

with Procedure

XI1. ID2.

A 1-hour

nonemergency

report was subsequently

made later that evening.

The

primary and secondary

meteorological

indications

had been unavailable

for 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />

when the condition was reported.

Conclusions

The failure of the licensee to notify the

NRC within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> of the loss

of the secondary

meteorological

instrumentation

was not in accordance

with the licensee's

own regulatory reporting procedural

requirements

and

was also

a violation of 10 CFR 50.72.

However. since the licensee

promptly initiated actions to re-establish

meteorological

assessment

capabilities following the loss of the secondary

meteorological

tower

this violation is considered to be minor and is being treated

as

a

noncited violation. consistent with Section VII.B.1 of the

NRC

Enforcement Policy

(NCV 50-275/96016-01;

50-323/96016-01).

Res

onse to the Dual Unit Tri

Followin

a

Ma or Grid Disturbance

Ins ection Sco

e

71707

Inspectors

responded to the site following notification of the dual unit

trip and observed control

room indications,

discussed

the event with

operators

and reviewed alarm summaries

and plant process

computer

recorded

parameter

data.

Observations

and Findin s

On August 10; at approximately 3:49 p.m.,

PDT,

a major grid disturbance,

which included the loss of the Pacific inter-tie,

caused

both Diablo

Canyon Units

1 and

2 reactors to trip.

Unit 1 tripped as

a result of

12 kV bus undervoltage,

while Unit 2 tripped due to the loss of RCPs

on

undervoltage trips.

Unit

1

RCPs

remained in operation following the

transfer to startup

power.

Startup

power (230 kV) remained available following the trip and

provided offsite power to the site until restoration of the auxiliary

power

(500 kV) system.

After 500

kV power was restored'perators

realigned Units

1 and

2 electrical

systems to backfeed offsite power

from the 500

kV system.

Following the realignment.

Unit

1 busses

autotransferred

back to 230 kV power due to a ground in the protective

n

0

relay circuitry.

Auxiliary power to Unit

1 was declared

inoperable

until the problem was isolated

and corrected.

Following the grid disturbance

the licensee

reported that

100 of 135

offsite early warning sirens

were without power.

Within several

hours

the licensee

restored

power to all sirens within the

10 mile emergency

planning zone.

Following the trip of the units, several

anomalies

were noted:

Unit 1:

MSSV RV-7 lifted following the trip at approximately

50 to

60 psig below its lift setpoint.

Operators

responded

by lowering steam

pressure to approximately

1000 psig using the atmospheric

dump valves at

which point the

MSSVs reseated

(details of MSSV testing are provided in

Section El.2).

Unit 2:

Operators

shut the main steam isolation valves to limit

cooldown.

MSSVs RV-4 and

RV-8 lifted approximately 50-60 psig below

thei r set lift pressure.

Operators

responded

by lowering steam pressure

to 1000 psig at which point the valves reseated.

RCP seal injection

flow decreased

to approximately

2 gpm per

pump apparently

due to

blockage of seal injection needle valves.

Operators

responded

by fully

opening

and then rethrottling the needle valves which restored

normal

seal injection flow.

CFCUs 2-3 and 2-4 breakers

tripped on overcurrent.

CFCUs 2-3 and 2-4 were, later determined to have

been selected to high

speed

and tripped as

a result of attempting to start directly in high

speed following the bus transfer.

Operators

had incorrectly left the

switches selected to high speed following the completion of surveillance

testing.

The licensee

concluded that the surveillance

procedure

was

adequate,

although it did not provide specific restoration

requirements.

Operating

Procedure

(OP) H-2: I, Revision 13,

"Containment

Fan Cooler

'nits

- Place in Service," the governing procedure for operation of

CFCUs, Section

6. 11, contains specific requirements

to reset

CFCU

selector

switches to slow speed after starting

a

CFCU in high speed.

It

was later verified by review of the associated

control schematics

that

CFCUs 2-3 and 2-4 would have started

and run in slow speed

as required

upon receipt of an engineered

safety feature

(ESF) start signal with the

selector

switches selected to the high speed position.

The fai lure of

the operators to properly restore the selector switches for CFCU 2-3 and

2-4 to the position required by OP H-2:I is

a violation of TS 6.8. 1.,

which requires that procedures

be established'mplemented

and

maintained covering the startup,

operation

and shutdown of the

containment cooling system.

Since this violation was self-revealing, of

minor safety consequence

and corrective actions to prevent recurrence

are being implemented

by the licensee, it is being treated

as

a noncited

violation, consistent with Section VII,B.1 of the

NRC Enforcement Policy

(NCV 50-323/96016-02).

-4-

08

08.1

b.

Conclusions

Operator

response

to the dual unit trip was good.

Both units were

quickly stabilized in Hode 3 despite

several

equipment

problems that

occurred which complicated operator

response

following the trips.

Improper restoration

from CFCU surveillance testing caused

CFCU 2-3 and

2-4 high speed

breakers to trip when the

CFCUs attempted to start

directly in high speed following an automatic

bus transfer.

Hiscellaneous

Operations

Issues

Control

Room Observations

Durin

Surveillance Testin

Ins ection Sco

e

71707

The inspector s observed

the normal conduct of routine evolutions in the

control

room during the performance of Rod Drop Surveillance testing.

Observations

and Findin s

During control

room observations

the inspector

noted that both the

CO

and the

SCO were escorting visitors.

The appropriateness

was questioned

and the Operations

Hanager

determined that it was inappropriate for

control

room operators to be assigned

the additional duty of escorting

visitors and directed that the visitor escort duties

be assigned to

another individual.

The guidance of OP1.DC10.

"General Authorities and

Responsibilities

of Operating Shift Personnel,"

specified that the

operator at the controls

must give full attention to the condition of

the plant at all times.

The guidance did not specifically address

the

performance of escort duties while on shift.

This procedure

incorporated the guidance of'egulatory Guide 1. 114,

"Guidance to

Operators

at the Controls

and Senior

Operators

in the Control

Room of a

Nuclear

Power Unit."

Conclusions

The practice of allowing the operator at the controls

and the

SCO to be

assigned

the additional duty of escorting visitors has the potential to

distract the operator

from assigned

duties

and was considered

a weakness

in shift management

oversight of operator acti vities.

Conduct of Maintenance

Maintenance

Observations

Ins ection Sco

e

62707

II. Maintenance

The inspectors

observed all or portions of the following work

activities:

~

CO 145794:

Replacement

of EDG 1-3 exhaust

bellows locknuts

Observations

and Findin s

The inspectors

found the work performed

under these activities to be

professional

and thorough.

All work observed

was performed with the

work package

present

and in active use.

Technicians

were experienced - .

and knowledgeable of their assigned

tasks.

The inspectors

observed

system engineers

monitoring job progress

and that quality control

personnel

were present

when required

by the procedure.

When'pplicable,

appropriate radiation control measures

were in place.

In addition, selected

maintenance

observations

are discussed

below.

Im ro er Material Utilized for Auxiliar Salt Water

ASW

Pum

Shaft

Ke

Ins ection Sco

e

62707

On August 3, during refurbishment of the Unit 2 ASW pump that had been

replaced

during 2R7, the licensee

discovered

one of the

pump shaft

couplings

was missing one of its two torsion keys.

The inspector

reviewed the licensee's

actions taken to determine the root cause of the

missing key and the licensee's

evaluation of the condition of the

installed

ASW pumps.

Observations

and Findin s

fach of the

ASW pumps are vertically mounted wet pit pumps with the

impeller coupled to the

pump motor through

a three-piece

extended shaft

arrangement.

The three

segments

of the

pump shaft are coupled by means

of a thrust ring and two torsion keys fitted into a coupling sleeve.

As

these coupling arrangements

are normally exposed to a saltwater

environment,

a corrosion resistant

stainless

steel alloy, trade

name

Hastelloy, is used in their fabrication.

The licensee

evaluated

the as-found condition of the

pump shaft

and

determined that

a key had been installed in the coupling;

howevers

the

key installed

was most likely fabricated

from carbon steel.

During the

time the

pump was installed in the system,

the key had dissolved in the

0

0

-6-

corrosive saltwater environment.

As

a consequence,

the

pump shaft was

allowed to rotate inside the coupling sleeve before galling between the

two components

caused

them to fuse together.

The licensee

had not

completed its evaluation of the impact of the as-found condition on past

operabi lity of the

pump at the end of this inspection period.

In evaluating'the

root cause of installing

a key of the wrong material.

the licensee

looked at (1) the key configuration of the entire

ASW

pump-motor

assembly,

(2) previous work packages

associated

with the

refurbishment of each of the

ASW pumps,

including procurement of any

replacement

keys,

(3) work practices

during pump refurbishment,

including material accountability,

and (4) warehouse

stocking of the

different keys.

The licensee

did not identify any process

inadequacies

in 'these

areas

and concluded that this was

an isolated event

and it was unlikely that

an improper key was

used in any of the currently installed

ASW pumps.

The licensee

supported their conclusion

by showing that the key

configuration of the

ASW pump shaft does not allow for interchanging the

various keys.

Thus, the improper key had been installed

as

a

replacement.

A survey of the warehouse

found that the carbon steel

keys

and Hastelloy keys are in separate

locations.

Additionally,

a magnet

test found that there were no carbon steel

keys inadvertently stored in

the bin for the nonmagnetic Hastelloy key.

The licensee

found that

three carbon steel

keys

had been pulled from stock for refurbishment of

the

ASW pumps

and was confident that the keys

had been installed in the

motor-to-shaft couplings.

Conclusions

The licensee

took reasonable

steps to determine whether or not

a

degraded

condition exists in the currently installed

ASW pumps.

However,

a definitive conclusion

on the current configuration could not

be made without visual observation of the

pump shaft keys.

Therefore,

the licensee's

past operability evaluation

and long-term corrective

actions will be examined

as

an inspection followup item

(IFI 50-275/96016-03:50-323/96016-03).

Ino erable Reactor Tri

Permissive

P-4

Ins ection

Sco

e

92902

The inspectors

reviewed the work order and maintenance

procedure

utilized for the replacement of solenoid valve (SV)-171. the applicable

TS and operator

emergency

procedures.

Observations

and Findin s

On August 2.

a maintenance

technician

found

a lifted lead associated

with Train 8 of Unit 2 reactor trip Permissive

P-4.

The lifted lead

0

K

would have precluded

a Train 8 turbine trip upon opening of the Train 8

reactor trip breakers.

The licensee

determined that the lead

had not

been landed after restoration

from maintenance activities on May 22,

1996.

As

a result. the

TS requiring two operable trains of the reactor

trip permissive

had not been

met when Unit 2 entered

Hode

1 on May 24

and during subsequent

plant operation.

The licensee

reviewed the work order for the work performed

'on Hay 22

and identified that Step 8.6.26.f. 'of Procedure

HP I-1.36-1,

"Main

Turbine Control Integrated

Functional Test," to land the lifted leads

had not been initialed as completed.

The licensee's

root cause

determination

indicated that inadequate self-verification during the

activity and inadequate

postwork review contributed to the event.

Proposed corrective actions

included revising the maintenance

procedure

to enter

the

TS action statement

when the lead is lifted. training

maintenance

personnel

on the event,

and counseling

those involved.

Train A of reactor trip permissive

P-4 had been inhibited for

surveillance testing while Train 8 was inoperable.

The longest period

when both trains were inoperable

was approximately

50 minutes,

occurring

on June

6; however, diverse methods of tripping the turbine were

available while reactor trip permissive

P-4 was inoperable.

The methods

included operator initiated trips and automatic trips as

a result of a

safety injection signal, electrical faults, or overspeed.

The licensee

performed simulator scenarios

and confirmed that the turbine would trip

approximately

15 seconds

following a reactor trip if P-4 was disabled

and no operator actions

were performed.

The inspector confirmed that

licensee

procedures

di rect operator s to verify or initiate a turbine

trip following a reactor trip.

The inspector

noted that

an October 27,

1987.

Westinghouse

evaluation

concluded that failure of the turbine to

trip 'following a reactor trip was not likely, gi ven the diverse

means of

tripping the turbine.

Conclusions

The safety impact of this event

was not significant.

The licensee

identified and corrected the violation and. therefore, this occurrence

is being treated

as

a noncited violation, consistent with

Section VII.B.1 of the

NRC Enforcement Policy

(NCV 50-323/96016-04).

Surveillance Observations

Ins ection Sco

e

61726

Selected

surveillance tests

required to be performed

by the

TS were

reviewed

on

a sampling basis to verify that:

(1) the surveillance tests

were correctly included on the facility schedule.

(2)

a technically

adequate

procedure existed for the performance of the surveillance

tests,

(3) the surveillance tests

had been performed at

a frequency

l

0

0

-8-

M6

N6.1

specified in the TS,

and (4) test results satisfied

acceptance criteria

or were properly dispositioned.

The inspectors

observed all or portions of the following surveillance:

~

STP R-2B1. Revision 6.

"PPC Operator

Heat Balance," Unit 2

~

STP R-1B, Revision 16,

"Rod Drop Measurement,"

Unit I

~

STP I-38-B.l. Revision 2,

"SSPS Train

B Actuation Logic test in

Modes l. 2, 3, or 4," Unit 1

Observations

and Findin s

The inspectors

found that the survei llances

reviewed and/or observed

'were being scheduled

and performed at the requi red frequency.

The

procedures

governing the surveillance tests

were technically adequate

and personnel

performing the surveillance

demonstrated

an adequate

level

of knowledge.

The inspectors

also noted that test results

were

appropriately dispositioned.

Maintenance Organization

and Administration

Mana ement of Maintenance

Backlo

Ins ection Sco

e

62707

The inspectors

reviewed the licensee's

maintenance

backlog reports,

nonoutage priority 4 action requests

(ARs) and Interdepartmental

Administrative Procedure

OM7. ID1. Revision 6,

"Problem Identification

and Resolution."

Observations

and Findin s

The maintenance

backlog reports indicated

an overall decreasing

number

of maintenance

backlog items at Diablo Canyon during the past year.

Although there

was no formal procedure for reporting or monitoring

backlog,

maintenance

managers

routinely received reports that indicated

the backlog of corrective maintenance

in their respective

areas.

The

reports

were focused primari ly on the higher priority corrective

maintenance

items;

however,

lower priority (priority 4) issues

were also

being separately

tracked.

The work loads at the work. planner

and

maintenance

group assigned to perform the work appeared

to be the

largest contributors to the backlog.

The licensee

was evaluating what

actions were necessary

to reduce the backlog at the work planning stage.

These

items were noted to be in large part lower priority work items.

Action requests

are prioritized by assigning

a priority level of 1

through 4,

4 being the lowest priority maintenance

issue.

Until

recently,

the

AR initiator determined its priority.

The licensee

has

0

I

I

<I

-9-

M8

M8.1

changed the process

by establishing

a review panel that meets

on

a daily

basis,

in part, to ensure that

ARs are assigned

the correct priority.

The licensee also groups

ARs into nonoutage

and outage categories.

The

focus of the licensee

maintenance

organization

was to reduce the

nonoutage

maintenance

backlog.

As

a result, the total backlog

number

was not readily available but was later determined to be approximately

1400 items.

Several initiatives had recently been started in an effort

to reduce the backlog.

The most significant of these efforts was the

establishment

of a "fixit now" team to perf'orm minor maintenance.

Control

room deficiencies

were not being tracked separately.

Although

the licensee

had previously established

a program for tracking control

room deficiencies,

the decision

was

made that the deficiencies

had been

reduced to the number that was easily manageable.

The licensee is

determining the number of outstanding control

room deficiencies

and is

r'eevaluating the need to track control

room deficiencies

separately

from

other corrective maintenance

items.

Discussions with the Maintenance

Hanager indicated that there were no

organizational

goals for the reduction of the backlog.

In addition,

a

number of priority 4 ARs had been written greater

than

1 year ago,

and

several that had been written close to 3 years

ago without having been

corrected.

Concerns

were raised during the inspection regarding the

potential

worsening of equipment conditions that when first noted were

categorized

as priority 4.

The licensee

had not conducted

reviews of

priority 4 ARs that had been in existence for long periods of time

(e.g.

minor oil leaks,

seal

leaks

and valve packing leaks) to determine

if degradation

from the initially reported condition had occurred which

in turn warranted raising the priority of the maintenance

item.

Conclusion

The licensee

appeared to be effectively tracking and managing the

backlog of corrective maintenance.

Several

areas of potential

improvement were noted including:

establishing

goals for the reduction

of the backlog, periodic reviews

and reassessment

of priorties of

equipment deficiencies that have existed for a period of time without

being corrected,

and the separate

tracking of control

room deficiencies.

Miscellaneous

Maintenance

Issues

(92902)

Closed

Licensee

Event

Re ort

LER

50-275/95-005-00.:

TS 3.4.6. 1 not

met with the reactor coolant leakage detection

systems

inoperable

due to

personnel

error.

The

LER was issued

due to the TS requirements

for

containment

atmosphere

radiation monitoring systems

not being met.

TS

Re uirements f'r Containment

Atmos here Radiation Monitor in

S stems

TS 3.4.6. 1 requires that three different reactor coolant system

(RCS)

leakage detection

systems

be operable in Modes

1, 2,

3 and 4. If only

two systems

are operable.

operation

can continue for up to 30 days

-10-

provided grab samples of containment

atmosphere

are obtained

and

analyzed

once per 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The

TS requires if less than two of the

leakage detection

systems

are operable that the unit be in HOT STANDBY

within the next

6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />,

and in COLD SHUTDOWN within the following 30

hours.

The licensee failed to meet

TS 3.4.6.1 in that only one of the

three

RCS leakage detection

systems

was operable for an estimated

time

period of approximately

1 day.

Upon discovery operators

placed the

containment

fan cooler collection monitoring system in service

and

entered the .TS action statement.

Licensee

Investi ative and Corrective Actions:

The licensee's

investigation of the incident revealed that

on June 22,

1995,

maintenance

was performed which removed the containment

atmospheric

particulate monitoring system

(RH-11) and the containment

atmosphere

gaseous

radioactivity monitoring system

(RH-12) from service.

During the

maintenance

on RH-11 and RH-12,

TS 3.4.6.1

requirements

were satisfied

by having two reactor

coolant leakage detection

systems

available

and by

entering the action statement,

which required the analysis of grab

samples

every 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The licensee

determined that after completion of the maintenance,

contrary to procedure

guidance,

the technicians incorrectly left the

RH-ll and

RH-12 sample selector switch in the purge position which

prevented

the sampling of containment

atmosphere.

Both RH-11 and

RH-12

use

a

common sample path.

The improper alignment

was noted

by control

room operators

during routine shift checks.

After discovering the

problem operators

placed the

CFCU collection monitoring system into

service

and entered the

TS 3.4.6.1 action statement.

The licensee

noted

in the

LER that during the time period when only one reactor coolant

leakage detection

system

was in service

a grab sample of containment

atmosphere

was taken

and,RCS

1'eak rate calculations

were being performed

as required.

Corrective actions initiated in response to this event included:

revision of the surveillance

procedure to verify that the sample path

alignment is correct prior to placing

RH-11 and

RH-12 back into service,

review of other procedures

for similar concerns

and training of

operators

and

18C technicians

on the importance of self-verification.

These actions

appeared to address

the problem appropriately.

Conclusion

The fai lure to maintain the required

number of reactor

coolant leakage

detection

systems

in service is

a violation of TS 3.4.6. 1.

Based

upon

the details noted above, this failure constitutes

a violation of minor

safety signif'icance

and is being treated

as

a noncited violation

consistent with Section

IV of the

NRC

ENFORCEHENT POLICY

(NCV 50-275/96016-05)

-11-

M8.2

k

El

El. 1

Closed

LER 50-275/95-008-00

01

and 02:

control

room ventilation

system

(CRVS) outside design basis

due to a programmatic deficiency in

the operation

and maintenance of the HEPA filter and charcoal

absorber

system.

On August 11,

1995, the licensee

determined that the

CRVS had

been outside its design basis

on four occasions

when charcoal

absorbers

were replaced,

and isolation was not provided to separate

the

ventilation trains.

The licensee

determined that

a design basis

accident would have introduced unfiltered air into the control

room.

and

initial calculations

showed that postaccident

exposure limits would have

been

exceeded for control

room operators.

The licensee

subsequently

performed detailed calculations

which showed

that exposure limits would not be exceeded if the open ventilation train

was isolated within 5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after

a design basis accident.

The licensee

concluded that operator action after receiving control

room radiation

alarms would result in train isolation within approximately

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and

20 minutes after-the event.

The licensee ultimately concluded that

a

condition outside of the design basis

had not existed.

Additionally.,TS

had not been

exceeded

because

the charcoal filter replacement

took

approximately

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> out of an allowed outage time of 7 days.

As corrective actions,

the licensee

placed signs

on the ventilation

filter units to warn personnel

to not perform work unless the units were

isolated.

The licensee

also changed

maintenance

and surveillance

procedures

to install

a blank filter isolation when work was performed.

The inspector

reviewed the licensee's

dose calculations for this issue

and the changes

made to licensee

procedures.

The inspector

concluded

that the licensee's

corrective actions

were adequate.

III. En ineerin

Conduct of Engineering

EDG Volta e

Re ulator Circuit Board Deficiencies

Ins ection Sco

e

37551

The inspectors

reviewed the licensee's

actions taken in response to the

identification of concerns

associated

with the

EDG voltage regulator

ci rcuit cards identified in ARs A0399437,

A0399596,

and A0401207

~

and

Quality Evaluation

(QE) Q0011867.

The inspectors

also interviewed

engineers

associated

with the licensee's

investigation.

Observations

and Findin s

The inspectors

developed

a time line for the licensee's

actions after

identification of six concerns

documented

on AR A0399437

on April 17,

1996.

The inspectors

noted that the

AR identified

a potential

concern

that printed circuit cards in the voltage regulators for the six EDGs

were not in accordance

with design drawings.

The inspectors

noted that

-12-

the licensee initiated

a second

AR (A0399596)

on July 18 to address

only

the first two issues identified on AR A0399437.

On July 19, the

licensee

determined that the issues

were such that validation was needed

to determine the impact on operability.

The inspectors

noted that

Inter-Departmental

Administrative Procedure

OH7. ID8,

"Oper ability

Evaluation," Revision 2, allowed the licensee

30 days to determine if a

degraded

condition existed;

however,

a

POA was requi red to be completed

within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of determining that

a degraded

condition existed.

A

degraded

condition, in accordance

with Procedure

ON7. ID8, is any

"[p]hysical or documentation

evidence

(including design,

analysis,

licensing

or qualification) of deg'radation of the ability of a

structure,

system,

and component to perform its Specified Safety

Function(s)."

On April 22, the system engineer

documented that the printed circuit

boards in EDGs 1-1. 1-3,

and 2-1,

had undergone

a number of tests,

including the

18 month surveillance tests,

without experiencing

any

problems related to not having

a capacitor

in the field voltage feedback

circuit.

The inspectors

noted that Procedure

OH7.108 stated that ".

.

.

performance of surveillance

requirements

alone

may not be sufficient to

determine Operability

.

. ."

The inspectors

observed that the system

engineer

provided

a replacement

schedule for the affected circuit

boards.

The inspectors

found that the conclusion of the system engineer

that the

EDGs were operable

on the basis of their passing the tests

was

not substantiated

by additional evaluation,

which could have

analytically demonstrated

that the testing accounted for the degraded

condition.

On April 22. the supervisor for procurement

engineering

rejected the

initial AR (A0399437)

and transferred all actions, to the second

AR (A0399596).

The licensee

determined that the sixth issue identified

on the initial AR was not valid.

The sixth issue alleged that the

printed ci rcuit boards

had been

upgraded for safety-related

use.

The

inspectors

agreed with the evaluation that the subject printed circuit

boards

had not been

upgraded,

but had been

purchased

as safety-related

in 1978 in accordance

with the regulations

in effect at that time.

The

licensee

determined that the root cause of the configuration control

problem was that the incorrect circuit boards

had been supplied

by the

vendor.

At the time the circuit boards

were procured the vendor did not

identify any differences

between the typical schematic of the voltage

regulator

and the printed circuit boards that were supplied to the

licensee.

On April 24, the licensee

issued

Work Order C0144207 to replace the

affected voltage regulator printed ci rcuit board in

EDG 2-2.

The

inspectors

considered that this action confirmed that the licensee

had

determined that

EDG 2-2 was in a degraded

condition:

however,

no

POA was

documented,

as required

by Procedure

OM7. ID8.

0

-13-

On April 27,

a vendor representative

informed the licensee that the

proper configuration of the printed circuit boards

requi red two

resistors

in parallel in a filter circuit to minimize the effects of the

firing of the silicon-controlled recti fiers on the field voltage

circuit.

Also, the vendor representative

stated that if only one

resistor

was in the circuit. the single resistor would overheat

and

cause

scorching.

In addition to the two resistors.

the vendor

representative

stated that there were differences

between the installed

circuit b'oards

and the design in the feedback ci rcuit.

These

differences affected

a capacitor

and two additional resistors.

The

licensee

determined that the subject printed circuit boards in the

voltage regulators for EDGs 1-2, 1-3, 2-2,

and 2-3 did not conform to

the design drawing and should have

been replaced.

The inspectors

found

that this information was sufficient for the licensee to determine that

.a degraded condition existed;

however, the licensee failed to promptly

document

an operability assessment

as required

by Procedure

ON7. IDB.

On Nay 2, the system engineer,

along with the senior

resident inspector.

found that the single resistor

on the subject circuit board in the

voltage regulator for EDG 1-3 had visible signs of scorching.

The

system engineer

concluded that the

EDG was operable

because

".

.

. there

was

no immediate danger that the board would fail

.

. ."; however, the

system engineer

recommended

that the board

be replaced

as

soon

as

possible.

The inspectors

found that the scorched resistor

was yet

another indication of a degraded condition;

however, the licensee failed

to document

a

POA as required

by Procedure

ON7. IDB.

On May 7.

a system engineering

supervisor

documented that on the basis

of "previous successful

surveillance testing,

discussions

and

observations

described [in AR A0401207] and engineering

judgement, it

[was] expected that

EDG 1-3 voltage regulator operate correctly and i s

in no immediate

danger of fai ling."

Also on May 7, licensee

management

determined that

a

POA was required.

The inspectors

noted that the

system engineering

supervisor

documented

the

POA, in accordance

with

Procedure

ON7. IDB, later

on May 7,

and that the Director of

Instrumentation

and Controls Engineering concurred.

The inspectors

found that the licensee

had at least

four opportunities

to appropriately declare

a degraded

condition for four of the six EDGs.

At each opportunity, the licensee

was aware that. either the installed

configuration did not match the design

(physical

and documentation

evidence)

or the resistors

were scorched

(physical evidence).

In

addition. the vendor representative

informed the licensee that the

installed configuration did not match the design.

The inspectors

determined that the licensee failed to appropriately identify a degraded

condition and failed to properly perform

a

POA in accordance

with

Procedure

ON7. ID8, Revision 2.

The failure to comply with

Procedure

OM7. IDB was

a violation of Criterion

V of Appendix

B to 10 CFR Part 50.

This was identified as violation (VIO 50-275/96016-96:

50-323/96016-06).

0

-14-

E1.2

Conclusions

The fai lure to promptly identify a degraded

condition and perform

a

POA

in accordance

with procedural

requirements

was identified as

a violation

of Criterion

V of Appendix

B to 10 CFR Part 50.

Ins ection of Premature

MSSV Lifts

Ins ection Sco

e

92903

On August 10.

1996, following reactor trips on Diablo Canyon Units

1 and

2.

one

HSSV on Unit 1 and two MSSVs on Unit 2 lifted at pressures

below

their requi red set pressure.

The inspectors

reviewed the licensee's

actions in response

to this event.

Observations

and Findin s

Following a dual unit trip, one

HSSV (RV-7) on Unit

1 and two HSSVs

(RV-4 and RV-8) on Unit 2 lifted prematurely.

Prior to the trip, on

August 7-8,

1996, the licensee

had tested the Unit 2 valves in place

using the AVK hydraulic assist

device.

The licensee

performed the

testing

as part of their augmented test program to determine the reason

for the

MSSV high initial lifts and set pressure drift previously

experienced.

Both Unit 2 valves which lifted prematurely

had their set

pressure

adjusted during this test series.

The valve set pressure

is

adjusted

by turning the adjusting bolt and either compressing

or

relaxing the spring.

The number of flats turned

on the adjusting bolt

indicates

how much

a valve was required to be adjusted.

Each flat on

the adjusting bolt typically corresponds

to a change in the set pressure

of approximately

5 to 20 psi.

The Unit

1

HSSV had its set pressure

adjusted during testing

on

April ll, 1996.

The inspectors

reviewed the licensee's

test data

from

April ll, 1996,

and found that .the Unit 1 Valve,

RV-7, had

an "as-left"

set pressure of 1065 psig.

During online testing the

MSSV adjusting

bolt had been adjusted

a total of -4.5 flats from the valve setting

on

live steam at the Westinghouse test facility.

The -4.5 flats adjustment

caused

a decrease

in the MSSV's set pressure.

During the plant trip,

the

MSSV lifted at 1014 psig.

A review of the Unit 2 test results of

August 7-8,

1996 found that

RV-4 had

an

AVK "as-left" set pressure of

1086 psig with a total adjustment of'5.0 flats of the adjusting bolt

from the valve setting

on live steam at the test facility.

Valve RV-8

had

an "as-left" set pressure of 1083 psig with a total adjustment of

the set pressure

adjusting bolt of -4.0 flats from the valve setting

on

live steam at the test facility.

During the plant trip, RV-4 had opened

at 1020 psig and RV-8 at 1014 psig.

After the three valves

had lifted low. the licensee

retested

the valves

using the AVK device.

AVK test results indicated that the set pressures

were approximately the

same

as the "as-left" values prior to the plant

0

0

trips.

The AVK test results did not reflect the low set points recorded

by the plant process

computer

.

Following the

AVK tests,

the licensee

performed additional testing using Trevitest equipment

on eight of the

forty MSSVs and establish

set pressures

independent of AVK testing

and

the plant process

computer.

The inspectors

reviewed the Trevitest test

data

and found that the "as-found" set pressures

were

1035 psig for

RV-7,

1055 psig for RV-4, and

1032 psig for RV-8.

The Trevitest results

correlated closer to the results

recorded

by the plant process

computer

than the

AVK results did.

After the licensee

reviewed the test data for

the eight valves,

they proceeded

to test the remaining valves

on both

units with the Trevitest device

arid reset

them according to the

Trevitest results.

During the last outages for Units

1 and 2, the licensee

developed

individual valve correction factors to be used

when testing the valves

in place using the AVK test apparatus.

These individual valve

correction factors were developed

by comparing

AVK test results with

steam test results.

The licensee

applied correction factors

by changing

the valve seat

area utilized to calculate lift pressure.

These

correction factors resulted in the effective seat

area of individual

valves ranging from 20.18 square

inches to 24.27 square

inches.

The

manufacturer of the AVK device

recommended

using

a 22.46 square

inch

mean seat

area.

The manufacture

of the Trevitest device

recommended

using

a mean seat

area of 23.046 square

inches.

When

a hydraulic lift

assist

device is used,

the valve set pressure

is determined

by adding

the valve inlet pressure to the load cell force divided by the mean seat

area.'

low mean seat

area would cause the hydraulic lift device

contribution to the set pressure to be proportionately too high.

Therefore,

the valve would be set too low resulting in the valve lifting

at

a lower than expected

pressure.

The three valves that opened at low

pressures

had been adjusted

using low mean seat

areas.

A review of the

AVK and Trevitest test data

found that when tested with

the

AVK device,

the valves which had a, low mean seat

area

had the

largest

number of flats adjusted to decrease

the set pressure after

having been set

on steam at the Westinghouse

Test Facility. It was also

noted that,

when tested with the Trevitest device,

the

same valves with

the low AVK mean seat

areas

were found to have low set points

and had to

be adjusted

by increasing the set pressure.

These adjustments

were

approximately equal

but opposite to the adjustments

made when tested,,

with the

AVK device.

The inspectors

found that the Trevitest results

correlated

more closely with the steam test results

than the AVK results

with valves with low mean seat

areas.

The inspectors

reviewed Operability Evaluation. 96-06, "Operability of

Main Steam Safety Valves," Revision 0.

The purpose of the operability

evaluation

was to document the operability of the

MSSVs for Units

1 and

2.

The li'censee

concluded that the TS required

number of MSSVs were

operable while the plant was in Mode 3 and that Unit 2 could increase

power up to 87 percent before the remaining

MSSVs had to be tested.

The

0

-16-

licensee

concluded that the incorrect correction factors

(mean seat

areas)

could have contributed to the

MSSVs lifting low and the cause of

the valves lifting low was primarily due to the low set points

established

using AVK.

In addition, the licensee stated that the

continuing formal augmented test program for the

HSSVs to determine the

reason for the high initial lifts and set pressure drift would be

revised to reflect the recent testing experience.

The licensee stated

that the program would be ready for Plant Staff Review Committee

approval

by August 30.

1996.

On August 10,

1996, the licensee

was performing surveillance tests

on

the Unit

1 Lead

1

MSSVs using the

AVK device prior to the plant trip.

During the surveillance tests

the licensee incorrectly used the Unit 2

Lead

1 individual valve mean seat

areas

on the Unit

1 valves.

AR A410913410913

dated August 10.

1996,

was written to document the failure

to use the correct

mean seat

areas

and to document the fact that three

of the five HSSVs were outside of the

TS as-left set point +1 percent

tolerance but within the +3 percent tolerance.

As discussed

above,

the

valves were retested

and adjusted,

as necessary.

using the Trevitest

lift assist

device.

The testing

was performed prior to Unit 1

reentering

Hode 2.

The failure to use the correct

mean seat

areas

was

identi fied as

a violation of Procedure

HP M-4. 18, Revision 14,

"Verification of Lift Point Using Ultra Star Assist Device for the Main

Steam Safety Valves."

Procedure

No. OPl.DC17, Revision 2A, "Control of Equipment Required

by

the Plant TS."

requires that whenever

TS equipment is declared

inoperable,

a

TS sheet

should

be initiated.

The licensee

determined

that three of the Unit 1

HSSVs were outside of their "as-left" set point

tolerance

on August 10.

1996,

when they identified that the Unit 2 mean

seat

areas

had been

used

on the Unit 1 valves.

The licensee did not

'nitiate the

TS sheets until August 12,

1996.

Although the TS action

statement" requirements

were followed and. therefore.

no violation

occurred.

the inspectors

considered this to be

a weakness.

Conclusions

E2

During surveillance testing of Unit

1 Lead

1 MSSVs, the licensee

used

incorrect

mean seat

areas

which caused three of the five valves to be

outside of the "as-left" set pressure

tolerance of +1 percent.

This

issue is being considered

as

an unresolved

item since further inspection

is requi red to determine whether the licensee

complied with the

requirements of the maintenance

rule (URI 50-275/96016-07).

Engineering

Support of Facilities and Equipment

Review of U dated Final Safet

Anal sis

UFSAR

Commitments

A recent discovery of a licensee operating their facility in a manner

contrary to the

UFSAR description highlighted the need for a special

0

-17-

focused review that compares

plant practices,

procedures.

and/or

parameters

to the

UFSAR description.

During the inspection period, the

inspectors

reviewed the applicable sections of the

UFSAR that related to

the inspection

areas

discussed

in this report.

There were no

inconsistencies

noted between the wording of the

UFSAR and the plant

practices,

procedures,

and/or parameters

observed

by the inspectors.

E8

Hiscellaneous

Engineering

Issues

l

f8.1

Closed

LER 50-275/95-011-00:

Unit 1 Hain Steam

System outside of

design basis

due to high initial HSSV lift points.

Testing to identify

the cause

and to resolve problems associated

with high initial MSSV lift

points is ongoing.

LER 1-96-003

has

been

opened to report the results

of continued testing,

investigation,

and corrective actions for the

HSSVs in Units

1 and 2.

No further inspection

on

LER 50-275/95-011,

Revision

00 is necessary,

since the issue is being tracked

under

LER 1-96-003.

X1

Exit Meeting Summary

V. Mana ement Meetin s

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on August 22.

1996.

The

licensee

acknowledged

the findings presented.

The .inspectors

asked the licensee

whether

any materials

examined during the

inspection should

be considered

proprietary.

No proprietary information was

identified.

X2

Predecisional

Enforcement

Conference

Summary

On July 1,

1996,

a predecisional

enforcement. conference,

open to public

observation,

was conducted at the Region

IV office in Arlington, Texas.

The

purpose of this meeting

was to discuss

the April 1996 augmented testing of the

Diablo Canyon Unit

1 HSSVs

and subsequent

actions

as described in NRC Special

Inspection Report 50-275/96-12;

50-323/96-12.

Meeting attendees

are listed in

Attachment 2.

The apparent violations as originally proposed

and discussed

at

the meeting are presented

in Attachment 3,

and the licensee's

presentation

is

provided in Attachment 4.

The action taken

by the

NRC following the

inspection

and predecisional

enforcement

conference

was documented

in a letter

dated July 10,

1996.

0

ATTACHMENT 1

Licensee

PARTIAL LIST OF

PERSONS

CONTACTED

M. J.

Angus,

Manager,

Regulatory

and Design Services

J.

R. Becker, Director, Operations

J.

E. Bonkonsky,

General

Foreman,

Technical

Maintenance

D. F. Brosnan,

Director, Regulatory Services

W.

G. Crockett,

Manager,

Nuclear Quality Services

S.

R. Fridley, Manager of Outage Services

C.

R. Groff, Director, Nuclear Secondary

Systems

J .

R. Hinds, Director, Quality Control. Nuclear Quality Services

T. L. McKnight, Engineer,

Regulatory Services

D.

B. Miklush, Manager,

Engineering Services

E.

P. Nelson, Materials Supervisor.

Procurement

Engineering

D. A. Vosburg, Director, Nuclear Steam Supply Systems

Engineering

l,

-2-

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 92700:

IP 92902:

IP 92903:

INSPECTION

PROCEDURES

USED

Onsite Engineering

Surveillance Observations

Maintenance

Observations

Plant Operations

Onsite

LER Review

Followup - Maintenance

Followup - Engineering

~oened

50-275/96016-01

50-323/96016-01

50-323/96016-02

50-275/96016-03

50-323/96016-03

50-323/96016-04

50-275/96016-05

50-275/96016-06

50-323/96016-06

50-275/96016-07

Closed

50-275/96016-01

50-323/96016-01

50-323/96016-02

50-323/96016-04

50-275/96016-05

50-275/95-005-00

50-275/95-011-00

ITEMS OPENED,

CLOSED,

AND DISCUSSED

NCV

Failure to follow 10 CFR 50.72 Reporting

Requirements

NCV

Failure to follow CFCU operating

procedure

IFI

Installation of Improper

ASW Pump Shaft

Key

NCV

Inoperable Reactor Trip Permissive

P-4

NCV

Violation of TS 3.4.6. 1

VIO

Failure to take prompt and adequate

corrective actions following identification of

a degraded

condition

URI

Unit

1 Lead

1 MSSVs'Set~ Using Unit 2 Lead

1

. Correction Factors

NCV

Failure to follow 10 CFR 50.72 Reporting

Requirements

NCV

Failure to follow CFCU operating

procedure

NCV

Inoperable

Reactor Trip Permissive

P-4

NCV

Violation'of TS 3.4.6. 1

LER

Technical Specification 3.4.6.1

Not Met with the

Reactor Coolant

Leakage Detection Systems

Inoperable

Due, to Personnel

Error

LER

Main Steam

System Outside of Design Basis

Due to

High Initial MSSV Lift Points

I4

-3-

50-275/95008-00.

LER

Control

Room Ventilation System Outside Design

Basis

Due to

a 01,

and

02 Programmatic

Deficiency in the Operation

and Maintenance of

the

HEPA Filter and Charcoal

Absorber System

AR

ASM

CFCU

CRVS

EDG

kv

LER

MSSV

OP

POA

PDR

RCP

RCS

s~co

TS

UFSAR

LIST OF ACRONYMS USED

action request

auxiliary saltwater

containment

fan cooler unit

control

room ventilation system

emergency diesel

generator

kilo-volt

licensee

event report

main steam safety valve

operating

procedure

prompt operability assessment

public document

room

reactor coolant

pump

reactor coolant system

radiation monitor

senior control operator

shift supervisor

Technical Specification

Updated Final Safety Analysis Report

ATTACHMENT 2

LIST OF ATTENDEES

PREDEC ISIONAL ENFORCEMENT CONFERENCE

Licensee/Facility:

Pacific Gas

and Electric Company/

Diablo Canyon Unit 1

Date/Time:

SUBJECT:

July 1,

1996,

2:30 p.m.

APRIL 1996

AUGMENTED TESTING OF DIABLO CANYON UNIT 1 MAIN

STEAM SAFETY VALVES AND SUBSEQUENT ACTIONS AS DESCRIBED IN

NRC SPECIAL INSPECTION

REPORT

50-275/96-12;

50-323/96-12

Licensee Attendees

S. Allen, Senior

Engineer,

Valve Engineering

J. Alviso. Engineer Assistant,

NRC Interface

M. Angus.

Manager.

Regulatory

and Design Services

P.

Beckham.

Senior Consultant

D. Brosnan.

Director, Regulatory Services

B. Coley, Engineer.

Regulatory Services

C. Groff, Director, Engineering Services

R. Locke, Attorney

D. Miklush, Manager,

Engineering Services

G.

Rueger

~ Senior Vice President,

Nuclear

Power Generation

L. Womack,

Vice Presidents

Nuclear Technical Services

NRC Attendees

W. Bateman,

Project Director

S.

Bloom. Project

Manager

S.

Boynton, Resident

Inspector

K. Brockman,

Deputy Director, Division of Reactor Safety

S. Collins, Deputy Regional Administrator

D. Corporandy,

Project Engineer

P. Goldberg,

Reactor inspector

B. Henderson'ublic Affairs Officer

K. Perkins,

Director. Walnut Creek Field Office

G. Sanborn,

Enforcement Officer

M. Tschi ltz, Senior Resident

Inspector*

H.

Wong, Chief, Reactor Project

Branch

E

  • By telephone

ATTACHMENT 3

APPARENT VIOLATIONS AS ORIGINALLY PROPOSED

DIABLO CANYON

APPARENT VIOLATION j.

10 CFR Part 50, Appendix B, Criterion XVI, "Corrective Action," requires that

measures

shall

be established

to assure that conditions adverse to quality,

such

as failures, deficiencies,

and deviations,

are promptly identified and

corrected.

Contrary to the above.

between April 2,

1996,

and April 14,

1996,

a condition

adverse to quality (out of tolerance

main steam safety valves

(MSSVs)) existed

that was not promptly identified or corrected.

Specifically,

on April 2,

1996

~

the licensee identified by testing that the pressure liftsetpoints

on three of

five MSSVs on Unit

1 main steam lead

1 exceeded

allowable Technical

Specification tolerances.

The licensee did not take prompt corrective action

to identify. and correct the out-of-tolerance deficiencies

on the remaining

MSSVs.

The

MSSVs on main steam

lead were not tested until April 11,

1996,

when

three of the five MSSVs were found to be out-'of-tolerance.

The

MSSVs on main

steam

leads

3 and 4 were not tested until April 14,

1996,

when six of ten

MSSVs

were found to be out-of-tolerance.

This apparent violation is subject to change

based

upon discussion.

0

-2-

DIABLO CANYON

APPARENT VIOLATION 2

CFR Part 50, Appendix 8, Criterion V, states,

in part, that activities

affecting quality shall

be prescribed

by documented

instructions,

procedures.

or drawings

.

.

.

and shall

be accomplished

in accordance

with these

instructions,

procedures,

or drawings.

Diablo Canyon Procedure

ON7. ID8, Revision 2, Subsection

2.2.3,

requires

that:

"For Degraded Conditions impacting Structure.

System

and Component

operability identified by physical

evidence at

DCPP. the

POA (Prompt

Operability Assessment)

should

be completed

and documented

during the

operating shift in which the physical

evidence

was identified.

In all

cases'he

POA shall

be completed

and documented within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

following identification of a Degraded Condition."

Contrary to the above.

as of May 14,

1996,

NRC inspector s identified that

the licensee

had not documented

a

POA of a degraded

condition

(n'amely

three of five HSSVs out-of-tolerance).

On April 2,

1996, licensee test

engineers

identified three of five HSSVs on steam

lead

1 ot Unit

1 to be

5

out-of'-tolerance

(high).

b.

Diablo Canyon Procedure

ON7. 108, Revision 2, Subsection

4.1,

requi res

that "The individual and his/her group supervisor

identifying a Degraded

Condition or an Issue

Needing Validation is responsible for:

Immediately

0

-3-

noti fying the Shi ft Foreman,

if the condition is an observed

physical

Degraded Condition at the plant that could adversely affect the

Operability of a Structure,

System,

and Component."

Contrary to the above,

on April 2,

1996,

licensee test engineers

identified three of five IISSVs on steam

Lead

1 of Unit

1 to be out-of-

tolerance

(high), but did not notify the Shift Foreman.-

This apparent violation is subject to change

based

upon discussion.

0

ATTACHMENT 4

LICENSEE PRESENTATION SLIDES

FOR PREDECISIONAL ENFORCEMENT

CONFERENCE

0

LICENSEE'

PRESENTATION

~ DCPP Main Steam Safety Valves (SV)

Background

~ Inspection Report Issues

Unit 1 Correction Factors

Formality and Conduct of Augmented Test

Program

SV Operability Evaluation and Timeliness

~ Safety Significance

~ Concluding Remarks

Ã!

OCF'F'NAIN STEAM SAFETY

VAL.VE BACKGROUNQ

~ DCPP SV Type, Purpose, and Design Basis

~ SV Testing History

~ Program to Resolve Issues

~ Findings To-Date

~ Future Program Activities

Pageos

0

hi

SAFETY VALVETYPE

~ Dresser Model 3707R

~ 20 installed on each unit and 3 spares

~ 5 SVs per steam lead

~ Setpoints 1065, 1078, 1090, 1103, and 1115 psig

~ Common SV, used at other plants

NIfll

SV PURPQSE 8 DESIGN BASIS

~Ori inst

Present

/-1%

+/-3% (1 065 +3/-2%)

/-1%

/-1%

- As-left

- Test frequency each refueling outage.

(ASME Code would

allow 5 years for 20 valves)

t

Prevents Steam Generator (SG) pressure from rising above

110% of design pressure.

Limiting event is:

Turbine trip without a reactor trip (MFW maintained)

Maintain minimum AFW flow, 410 gpm (upper setpoint limits)

Prevent SG overfill (lower setpoint limits)

Technical Specifications

As-found

'"5 3

Page 2

SV TESTING HISTORY

~ Trevitest instrumentation historically used at DCPP and

much of the industry for SV surveillance testing and

setpoint adjustment

~ Maintaining SVs within+/-1% of setpoint has been a

problem since QCPP startup

~ SV out-of-tolerance (OOT) performance an industry

issue per NRC document AEOD 4/92

~ Trevitest validity brought into question (NRC IN 94-56)

~ 1994: To resolve SV issues, PGKE took the initiative to

pursue a comprehensive research and corrective

actions program

"63

PROGRAM TQ RESOLVE ISSUES

~ Obtain improved test instrumentation

~ Reanalyze basis for+/-1% TS setpoint tolerance to

support a wider band of acceptability

~ Develop a comprehensive understanding of SV

operating, testing, and maintenance characteristics

~ Ifresearch findings dictate, redesign/refurbish SVs to

resolve setpoint problems

Pll

Page 3

FINQiNGS TO DATE

~ AVKtest instrumentation selected and purchased

AVKresults repeatable within an acceptable

distribution

AVKand PG8E test data substantiates

AVK

mean seat area (MSA) adequate for on-line

SV setting

~ Re-analysis allows change in TS limits

Design basis supported with +/- 3% {+3/-2%

for 1065 SVs)

LAR approved on 10/1/95 with augmented

test program on Unit 1

Pl

AL.TERNATIVE TES T/NG

METHODS COlNPARISON

Page 4

0

FINDiNGS TO DATE (cont'd)

~ SV setpoint distribution considered during setpoint

adjustments

~ SVs exhibit initial high lifts

Believed to be due to thermal bonding which arises

from seating surface galling during thermal cycle

differential expansion

Thermal bonding not observed at beginning of cycle

Thermal bonding present 120+ days into cycle

'inimal

thermal bonding once SVs lifted "hot"

Seat refurbishment and materials appear to increase

" likelihood of bonding

~ SV liftvariation

Torque differences, installation vs test stand (Theory)

SVs spring hysteresis (Theory)

I4

TRENDS!N INITIALLIFTS

8FI

Page 5

0

FUTURE PROGRAM AC T!VlTIES

~ AVKtest methodology validation

Complete uncertainty analysis

~ Initial high lifts

Complete seating materials replacement

evaluations

'

Test all SVs on return to power from Mode 5

outages

3% accumulation on "sticking" SVs can be

eliminated for operability and safety analysis

~ Setpoint variation

SV-specific performance evaluation

Potential SV parts improvement program

~ Monitor industry SV experience

Eall

!NSPEC TION REPORT ISSUES

~ Unit 1 Correction Factors

~ Formality and Conduct of Augmented Test

Program

~ SV Operability Evaluation and Timeline'ss

~ For each issue PG8 E willcover:

Events Chronology

Key Conclusions

Corrective Actions

twirl

Page 6

0

CORRFCT/ON FACTQRS

CHRONOLOGY

~ 9/23/95, U2 Trip, 3 SVs lifted low, AVKvs steam

correction factor evaluation considered necessary

~ 9/30/95, LAR 95-06 submitted requesting setpoint

tolerance relaxation

~ 10/1/95, NRC LA 108 and 107 issued, requiring

augmented test program

~ 10/8 - 18/95, Unit 1 SVs sent to Westinghouse

Western Service Center (WSC) for testing/adjustment

on steam

Set all SVs on steam for normal TS testing

Collected AVKCF data for all SVs

o

Data for 10 SVs subsequently determined to

be invalid

o

Data*for 1 SV lost

/~II

CORRECTION FACTORS

CHROWOLOGV conm

~ 11/1/95, DCL-95-241 described formal augmented test

program and indicated that SV-specific CF testing would be

obtained during 1R7 and 2R7. Regulatory Services failed

to document Unit 1 CF commitment on t'racking AR.

~

11/1 5/95, Engineering verbally informs NRC Resident of

installation of 11 SVs without CFs and agreed this is not a

restart issue.

Regulatory Services notinformed by

Engineering.

~

11/15/95, Action Request (AR}written outlining an

alternative process to obtain AVKCF data on-line.

Subsequent

PSRC discussion questions validity of this

approach.

As a result, further testing was not pursued

~ 11/27/95, Unit 1 restart.

Commitment tracking omission

results in a missed opportunity to identifyneed forwritten

NRC notification

Page 7

0

CORRFC TION FACTORS

CHRONOLOGY conf'd

~ 4/1 5-26/96, Unit 2 SVs sent to WSC for testing and

adjustment on steam.

Set all SVs on steam for normal TS testing

Collected AVKCF data for all SVs

Unit 2 results substantiate both Unit 1 data and

AVKMSA

~ 5/3/96, OE 94-02, Rev 5 updated to include Unit 1

Augmented Testing experience.

~ 6/26/96, OE 94-02, Rev 6 concluded that CFs of the

remaining SVs were not required since the

overpressure

and AFW design basis was met with

worst case as-left setting using Vendor supplied MSA

"53

CF CONCLUSIONS AND

LESSONS LEARNED

~ AVKand PG8 E test data substantiates

that use of

AVKMSA is adequate for on-line SV setting of all

valves

~ Communications were inadequate between

Regulatory Services and the responsible Engineering

organization doing the testing

~ Commitment tracking AR not written for Unit 1 CFs.

Cognizant personnel failed to promptly inform NRC

and PG8 E management

~ PG8 E should have communicated with NRC in a

more complete and formal manner regarding the

decision to restart without all Unit 1 CFs.

NB

li'r5 3

Page 8

0

CF CQRRECTlVE ACTIONS

~ Updated OE 94-02 to address CFs (ref Rev 6)

~ Commitment tracking process reviewed relative

to observed problems.

Existing process deemed

adequate

but ineffective in this circumstance due

to personnel error

~ Management expectations regarding licensing

commitment implementation and communications

(both internal PG8 E and NRC) re-emphasized

with responsible personnel

~ Technical Staff training to review appropriate

licensing commitment implementation and NRC

communication requirements

s agr

~ NRC required an augmented testing program as

part of TS limitchanges

~ PG8 E letter of 11/1/95, detailed planned program

PGB E viewed program as an augmentation,

not a TS test for sample expansion

This understanding

is acknowledged

in NRC

Safety Evaluation Report of 12/26/95

Augmented testing for Unit 1 only

~ Initiated to evaluate the potential time

dependency of seat bonding

~ Finding high initial lifts during the augmented test

program was expected

Fl

Page 9

AUGMENTED TES T PROGRAM

PLAN

~ Testing requested

on an Action Request (AR);

documented on Work Order; performed under

Maintenance Procedure MP M-4.18

~ Originally, augmented testing program to be

performed on Unit 1 SVs only

~ Testing performed on one header on a staggered

basis to preserve time dependency

~ Valves outside +/-1% will be reset

~ If a liftoutside +/-3% occurs, test expansion to be

discussed with NRC per augmented test program

agreement

~ TS testing to occur as normally scheduled prior to

2R7 and 1R8

Pl

AUGMENTED TEST PROGRAM

RATIONALE

~ TS provided operability requirements

~ OE 94-02, Rev 4 provided operability basis for high

initiallifts

~ DCPP practice, even under TS surveillance, was not to

project test results from one SV to another while in

testing activities unless an equipment concern existed

regarding the adequacy of last setpoints established

~ Regular TS surveillance requires automatic expansion

for unsatisfactory results

~ Augmented testing program expansion was not

automatic; consultation with the NRC was required to

determine the extent of expansion

Page 10

0

AUGMENTED TES T PROGRAM

LOOP 7 CHRONOLOGY

~ 4/2/96,

Loop

1 SVs tested (3 of 5 OOT high) and

returned to +/-1%

The degree of OOT not unusual

Operations aware of testing and that all SVs

returned to within TS requirements

~ 4/3/96, Shift Foreman informed of Loop 1 test

r suits (approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> after tests)

'5$

AUGMENTED TES T PROGRAM

LOOP I CHRONOLOGY cont'd)

~ 4/3/96, Reviewed data to assess

operability

Existing OE 94-02, Rev 4 bounded test

results

OE considered AFWflow, although could

have been more clear

~ 4/4/96, Analysis results received for Loop 1 test

results

~ 4/8/96, PG&E/NRC conference call

Loop 1 testing results discussed

Potential expansion explored

PGRE and NRC agreed to test 5 more SVs

under the augmented test program'!

Page

11

AUGMENTED TEST PROGRAM

LOOP 2,3,4 CHRONQLOGY

~ 4/10-11/96, Loop 2 SVs tested (3 of 5 OOT high) and

returned to +/-1% except RV-223

The degree of OOT raised concern

Work orders requested to test Loops 3 and 4

RV-223 left at+1.4% since no CF was available and

steam setting was considered more accurate

~ 4/12/96, PG&E/NRC call at 1000 PDT.

PG&E informed NRC that Loops 3 and 4 would be

tested on 4/14/96

SVs < 1.5% without CFs would not be reset since live

steam was considered more accurate

Operable since OOT SVs reset and existing OE

applicable

Expeditious testing of Loops 3 and 4 planned

'53

AUGMENTED TEST PROGRAM

LOOP 2,3,4 CHRONOLOGY(conf'd)

~ 4/12/96, Operations made 10 CFR 50.72 report to NRC at

approximately 1730 PDT on SG 1-2 outside design limits

~ 4/12/96, 2130 PDT, NRC called requesting clarification on

1-hour report and conditions of Loops 3 and 4 ifprojection

of Loop 2 results was made to Loops 3 and 4

PG&E does not believe projection is appropriate, but

responded that Loops 3 and 4 would be operable

PG8 E's conclusion was based on incorrect

understanding of the analysis model

'3

Page 12

0

AUGMENTED TEST PROGRAM

LOOP 2,3,4 CHRONOLOGY(cont'd)

~ 4/13/96, PG8 E reviewed the validity of previous evening

response to NRC

Original basis found to be incorrect

Loops 3 8 4 were still considered operable based on

availability of 10% ADVs

NRC not immediately notified of change in reason

behind operability statement

~ 4/14/96, Loops 3 (5 of 5OOT) and 4 (1 of 5OOT) tested

and reset to +/-1% except RV-14

RV-14 left at+1.2% since no CF was available and

steam setting was considered more accurate

~ 4/16/96, PG&E/ NRC call on Loops 3 and 4 test results

and proposed Unit 2 testing.

NRC informed of PG8 E

miscommunication on 4/12 regarding basis of operability

statement

AUGMENTED TEST PROGRAM

LOOP 2,3,4 CHRONOLOGY (cont'd)

~ 4/19/96, PG8 E/NRC call

Agreed to test Unit 2 SVs in Mode 3

Expand the augmented test program to Unit 2 for

cycle 8

NRC stated that Unit 2 SVs must be returned to+/-1%

~ 4/21/96, PG&E initiated actions to ensure all Unit 1 SVs

returned to +/-1%

RV-14 was adjusted

RV-223 was tested and required no adjustment

~ 5/3/96, OE 94-02, Rev 5 approved to encompass

recent

test results

~ as

~

Page 13

0

CONDUCT OF TEST PROGRAM

CONCLUSIONS

~ Formality of the test program was adequate

Work was performed under an approved Work

Order and in accordance with MP 4.18

PG8 E decided not to use STP M-77. This

decision was consistent with our 11/1/95 letter

and the NRC's understanding noted in the SER

dated 12/26/95

The test program was carried out as planned.

Automatic expansion was not called for prior to

discussion of results with the NRC

PG8 E agrees that the Shift Foreman should

have been informed of results earlier, but it is

believed that doing so would not have resulted

in accelerated

testing of SVs

'3

CONDUCT OF TEST PROGRAM

CONCLUSIONS cont'6

~ Formality of the test results evaluation was not

adequate

PGKE should have anticipated and planned

appropriately given the range of results

obtained in prior SV testing

Information exchange requirements (type and

timeliness) with the NRC should have been

specified in the testing plan

Once it was known that valve specific CFs

were not available for 11 SVs, the effect on

results evaluation and SV reset action should

have been clearly analyzed and incorporated

in the testing plan

5FI

Page 14

CONDUCT QF TEST PROGRAM

CORRECTIVE ACTIONS

~ Immediately reset all Unit 1 SVs initiallyleft outside

+I- 1% tolerance

~ Tested SVs on Unit 2 in Mode 3 and at full power (to

check for thermal bonding)

~ Included Unit 2 in augmented testing program

~ SV augmented test plan has been revised to include

test scope expansion and reset criteria

~ Technical Staff training willreview this event focusing

on technical data evaluation, formal communication

and compliance with commitments

~ Engineering personnel involved with the evaluation of

test data have been counseled regarding the need to

provide formal documentation

P'll

SV OF'ERABILITYEVALUATION4

TIMELINESS CONCLUSIONS

~ Based on analysis of Loop 1 results, there was no

immediate operability issue, affording time to

communicate and plan additional testing

~ Given the nature of the Loop 1 results, PG8 E's actions

not to project results for operability determinations was

believed appropriate and consistent with past practice

All Unit 1 SVs were set on steam during 1R7, thus

pre 1R7 results should not be "projected" to post

1R7 testing

~ OE 94-02, Rev 4, was judged to bound Loop 1 test

results and therefore a POA was not required

Pll

Page 15

SV OPERABILITYEVALUATION8

TIMELINESS CONCLUSIONS (cont'd)

~ Though judged adequate

at the time, OE needed

clarification forAFW(revised 5/3/96)

~ The reasoning behind the adequacy of OE

should have been documented

~ PGB E initial communication with the NRC after

Loop 1 testing should have been more timely and

more complete

~ The implications of not resetting SVs steam set

without specific CFs and found less than 1.5%

OOT, though discussed with the NRC, should

have been communicated more fully and formally

SV OPERABILITYEVALUAT!ON4

TIMELINESS CONCLUSIONS (cont'd)

~ PG8 E should have notified the NRC on April 13,

1996 of the discovery that the "Operability under

projection" statement on April 12, 1996 was

based on erroneous assumptions

~ OE 94-02, Rev 5 and 6, should have been

updated in a more timely fashion

Page 16

SV OF'ERABILITYEVALUATIONE

TIMELINESS CORRECTIVE ACTIONS

~ Management expectations re-emphasized

with

'esponsible

Engineering personnel regarding:

Formal documentation of operability

Formality of special test programs

~ Technical staff training on operability

determination procedures (on-going)

~ Lessons Learned to be communicated at

technical staff sessions (future)

Emphasis on established schedules for

Operability Evaluation updates

Pl

SAFETY SIGNIFICANCE,

~ Though the analysis for Loops 2 and 3 shows that the

design basis pressure for the SG would have been

exceeded,

the system remained operable and would have

performed its event function because:

40% steam dump valves available

Atmospheric steam dump valves available

Reactor trip from turbine trip functional

~ SGs were hydro tested to 125% and designed for 5 hydro

tests at this pressure

~ AFW flows exceeded minimum 410 gpm requirement

T

~ AFW flownot affected by high initial lifts since credit not

assumed until 60 seconds following event initiation and

subsequent

lifts tend to return to nominal setpoint range

I I g

~

Page 17

SAFETY SIGNIFICANCE (conf'd)

~ Conclusions

No increased risk to public health

and safety

Safety significance is low

O'I

Page 18

&

0

DIABLOCANYON UNIT 1

TREVITEST

AVK

Range

(%)

<3%

3% <<5%

> 5%

1R1

- 2.2 to+

5.2

18

1R2

-4.1 to

+ 9.2

15

1R3

-2.6 to

+ 10.2

15

1R4

-1.5 to

+ 3.1

19

1R5

-1.6 to

+ &.7

16

1R6

- 1.7 to

+ 9.1

13

1R7

+ 0.4 to

+ 9.3

Mode 1

(Apr-96)

- 1.9 to

+ 9.3

10

TREVITEST

DIABLOCANYON UNIT 2

STEAM

MISC

AVK

2R1

2R2

2R3

2R4

2R5

2R6

Mid-

Cycle

2R7

Mode 3

May-96

Mode 1

Jttn-96'ange(%)

s3%

3% -5%

) 5%

- 0.5 to

+ 5.5

16

3v'

1.8 to

+ 3.4

-1.8 to

+ 2.7

20

-0.9 to

+ 8.3

17

-1.4 to

+ 8.8

- 1.7 to

+ 3.6

18

-0.9 to

+ 8.7

13

- 1.3 to

+ 4.5

18

-1.5 to

+ 5.0

17

- 1.2 to

+ 4.5

Qnty '10 Valves were tested

10

0

ALTERNAT/VE TES T/MG

ME7 HQQS CQMPAR/8QM

Test Method

LiftSensor

TREVlTEST

(In-Situ)

H. E."

Processor

Load Cell

None

Hydraulic with

Gripper (Man.)

Line Pressure

Heise Gauge

AVK

(In-Situ)

Acoustic

Transducer

Micro

Hydraulic with

Gripper (Auto.)

STEAM

(Test Stand)

H.

E.'eise Gauge

None

None

Correction

Factors

MSA

MSA/CF

NIA

  • H. E.- Human Ear

Y"

r

~fl

0