ML16342A694

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Insp Repts 50-275/98-20 & 50-323/98-20 on 981206-990123. Violations Noted.Major Areas Inspected:Opearations,Maint, Engineering & Plant Support
ML16342A694
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 02/19/1999
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342A693 List:
References
50-275-98-20, 50-323-98-20, NUDOCS 9902250315
Download: ML16342A694 (52)


See also: IR 05000275/1998020

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

Report No.:

Licensee:

Facility:

Location:

Dates:

Inspectors:

'pproved

By:

50-275

50-323

DPR-80

DPR-82

50-275/98-20

50-323/98-20

Pacific Gas and Electric Company

Diablo Canyon Nuclear Power Plant, Units 1 and 2

7 ~/~ miles NW of Avila Beach

Avila Beach, California

December 6, 1998, through January 23, 1999

D. L. Proulx, Senior Resident Inspector

D. G. Acker, Resident Inspector

I. A: Barnes, Technical Assistant, Division of Reactor Safety (DRS)

C. A. Clark, Reactor Inspector, Engineering and Maintenance Branch,

DRS

L. J. Smith, Acting Chief, Project Branch E

ATTACHMENT:

Supplemental Information

99022503i5 9902i9

PDR

ADQCK 05000275

8

PDR

0

EXECUTIVE SUMMARY

'iablo

Canyon Nu'clear Power Plant, Units 1 and 2

NRC Inspection Report 50-275/98-20; 50-323/98-20

This inspection included aspects of licensee operations, maintenance,

engineering and plant

support.

The report covers a 7-week period of resident inspection.

~Oerations

The inspectors monitored portions of each reactor startup and power ascension and

determined that operators manipulated both units in a careful manner in accordance

with procedures (Section 01.1).

Operator identification of increasing Unit 1 unidentified leakage and shut down of Unit 1

was an example of good attention to detail and conservative decision making. The root

cause analysis, repairs, and retesting of a leaking threaded joint on Reactor Coolant

Pump (RCP) 1-3 were performed well (Section 01.2).

Overall, Unit 1 operators responded well to two failures of expansion joints. However,

operators initiallycross-connected

intake cooling system trains upon rupture of an

expansion joint that could have resulted in loss of both Unit 1 circulating water pumps.

Operators recognized and corrected this error before any adverse impact occurred

(Section 01.3)

Maintenance

With the exception of corroded instrument lines associated with the outside tanks, the

external condition of plant components observed during tours was good (Section 02:2).

Routine maintenance and surveillance tasks observed were performed satisfactorily

(Sections M1.1 and M1.2).

The inspectors concluded that vendor information provided to ensure acceptable

installation arid maintenance of elastomeric expansion joints was not properly

implemented into the maintenance program. The licensee's failure to replace expansion

joints in a timely manner led to failure of two joints and caused partial flooding of the

intake structure and loss of a circulating water pump. These failures required operators

to quickly reduce power to preclude a reactor trip. The operability assessment

supporting the operability of the safety-related expansion joints failed to reference

vendor recommendations

on replacement frequency and seismic interactions.

As

a'esult,

the licensee did not identify an inoperable elastomeric joint, until challenged by

the inspector.

Further NRC review of the licensee's evaluation of this degraded

condition and application of the Maintenance Rule program to expansion joints is

required (Section. M2.1).

0

'I

Encnineering

The prompt operability assessment

associated with the Unit 1 condensate

storage tank

leak was an example of good engineering support for operations (Section E2.1).

The licensee had implemented comprehensive actions in both units to increase tubing

stress corrosion resistance and minimize steam generator tube degradation

(Section E8.3).

Housekeeping

in the Unit 1 containment building was excellent in that the area near the

containment recirculation sumps was clear, the containment building was free of loose

work material and debris, and only minor leaks existed in pump and valve packing

(Section 02.1).

~

A noncited violation of 10 CFR 20.1902(b), consistent with Section VII.B.1 of the

Enforcement Policy,'was identified for failure to properly post a high radiation area.

Radiation protection personnel failed to post a back entrance to Residual Heat Removal

Pump Room 1-2. Although the root cause analysis was inconclusive, corrective actions

were satisfactory (Section R1.1).

The inspectors noted that the licensee had inappropriately stored compressed

gas

cylinders in the auxiliary building. Contrary to plant procedures,

personnel had not

obtained a transient combustible permit, as required for storing flammable material,

which resulted in a violation of Technical Specification 6.8.1.h. The licensee

demonstrated that this instance involved low likelihood of a fire involving hydrogen gas.

. The licensee determined the cause of the violation, identified other examples, and took

appropriate corrective actions; therefore, no response was required (Section F1.1).

0

Re ort Details

Summa

of Plant Status

Unit 1 began this inspection period at 100 percent power.

On December 17, 1998, Unit 1 was

shut down because of a weld leak on the component cooling water side of the RCP 1-3 lube oil

cooler.

Following replacement of the lube oil cooler and resolution of boric acid wastage

concerns on RCP 1-3 carbon steel bolts, operators increased Unit 1 power on December 24.

Operators synchronized the plant to the grid on December 25 and returned power to

100 percent on December 26. Unit 1 continued to operate at essentially 100 percent power

until the end of this inspection period.

Unit 2 began this inspection period at 8 percent power, with power ascension

in progress

following a forced outage.

Unit 2 was synchronized to the grid on December 8 and achieved

100 percent power on December 9. Unit 2 continued to operate at essentially 100 percent

power until the end of this inspection period.

I. ~Oerattons

01

Conduct of Operations

01.1

General Comments

71707

The inspectors visited the control room and toured the plant on a frequent basis when

on site, including periodic backshift inspections.

In general, the performance of plant

operators reflected a focus on safety, evidenced by self- and peer-checking.

The

utilization of three-way communications continued to improve, and operator responses

to alarms were observed to be prompt and appropriate to the circumstances.

The inspectors monitored portions of each reactor startup and power ascension and

determined that operators manipulated both units in a careful manner in accordance

with procedures.

In addition, on December 17, the inspectors witnessed portions of the

Unit 1 reactor shutdown and determined that operators manipulated Unit 1 in a careful

manner in accordance

with procedures.

01.2

Shutdown of Unit 1 because

of Weld Leak

a.

Ins ection Sco

e 92901

93702

The inspectors evaluated the response to an increase in unidentified leakage and

subsequent

reactor shutdown.

Observations and Findin s

On December 16, 1998, during daily sump calculations, operators detected an increase

in unidentified leakage in Unit 1. The unidentified leakage rate had increased from

essentially 0 to 0.21 gpm over the previous 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

Because 'of the high radiation

0

-2-

levels, operators reduced Unit 1 power to 50 percent to allow entry into the RCP 1-3

area.

Upon examination, the licensee identified a weld leak on the component cooling

water side of the RCP 1-3 upper bearing lube oil cooler.

The licensee replaced the cooler with a spare from the warehouse and performed an

operational pressure test to ensure th'e leakage was corrected.

The failure analysis of

the weld failure revealed that vibration induced high cycle fatigue caused the failure.

The licensee identified that the vibration of the lube oil cooler for RCP 1-3 was

significantly higher than the other three Unit 1 RCPs.

t

On December 18, during routine inspections of the RCP 1-3 work area, a buildup of

boric acid on the pump was identified. The licensee determined that the leakage was

reactor coolant system pressure boundary leakage from a RCP 1-3 lower radial bearing

resistance temperature detector thermowell. Consequently, the licensee cooled down

the plant and entered Cold Shutdown on December 19, as required by the Technical

Specifications.

Mechanics repaired the leak by replacing the threaded resistance

temperature detector on December 20.

Following the leak repair, the licensee consulted with the vendor as to the effects of the

boric acid on RCP 1-3. The vendor noted previous problems with Westinghouse plants

associated

with boric acid wastage of the RCP motor stand base bolts. The licensee

inspected these bolts on December 20 and noted that 6 of 24 bolts exhibited significant

wastage.

The licensee examined all of the motor stand bolts associated

with RCP 1-3

to determine if further action was required.

Based on these inspections, the licensee

replaced all of the RCP 1-3 motor stand bolts. No other significant boric acid wastage

was identified on the other RCPs.

The inspectors visually confirmed that the licensee

properly assessed

the condition of RCP 1-3.

The licensee determined the root cause of the leak to be incorrect thread engagement

of Thermowell TE-168. The inspectors found the root cause assessment

satisfactory.

Conclusions

Operator identification of increasing Unit 1 unidentified leakage and shut down of Unit 1

was an example of good attention to detail and conservative decision making. The root

cause analysis, repairs, and retesting of a leaking threaded joint on RCP 1-3 were

performed well.

0 erator Res

onse to Ex ansion Joint Failures

Ins ection Sco

e 92901

93702

The inspectors evaluated operator response to two failures of expansion joints in the

intake structure.

This inspection included observation of operator response and review

of licensee evaluations.

-3-

Observations and Findin s

On December 1, 1998, with Unit 1 at 50 percent power and Unit 2 in Hot Shutdown, an

expansion joint failed that partially flooded the intake structure.

Approximately 3 feet of

water accumulated

in the area near the Units 1 and 2 circulating water pumps. This

expansion joint was associated with the cross-connect

line between the Unit 1 screen

wash header and the Unit 2 service cooling system.

Upon notification, operators

ramped Unit 1 reactor power in a controlled manner to 40 percent, in anticipation of

having to secure the operating circulating water pump if the flooding worsened.

Once

the source of the leak was identified, operators terminated the power decrease

and

isolated the cross-connect

line.'quipment

damage was limited to intake structure sump pumps and light fixtures. The

licensee pumped the excess water out of the intake structure and inspected the area for

further damage.

No safety-related equipment was affected.

The inspectors responded to the control room, witnessed the operator response to this

event, and determined that operators carefully manipulated Unit 1 and took prompt

action to mitigate the event.

In addition, the inspectors examined the flooded areas and

concurred with the assessment

of the impact of flooding. The root cause of the

expansion joint failure is discussed

in Section M2.1 of this report.

On December 2, with Unit 1 at 97 percent power, the Unit 1 intake cooling system

(which cooled the pump motor windings) expansion joint for Circulating Water Pump 1-2

began leaking. Operators noted that the leakage was minor and intake cooling head

tank level could be maintained by the makeup system.

As the shift progressed,

the leak

through this expansion joint worsened, and operators could no longer maintain head

tank level. Also, mechanics were unable to affect temporary repairs to mitigate the leak

. from the expansion joint.

Subsequently,

the failure of the expansion joint progressed to the point that a low

pressure alarm occurred in the intake cooling system header for Circulating Water

Pump 1-2.

Because this low pressure condition initiated a timer that automatically trips

the circulating pump after 5 minutes, operators decreased

Unit 1 power to 50 percent,

then secured Circulating Water Pump 1-2.

One of the initial actions had the operators open the two cross-connect valves between

the intake cooling headers for Circulating Water Pumps 1-2 and 1-1. This action

propagated the expansion joint failure leakage to the other intake cooling system and

could have resulted in a similar low pressure condition and subsequent

trip of Circulating

Water Pump 1-1. Shortly after taking this action, operators recognized the

inappropriateness

of the action, closed the cross-connect valves between the two intake

cooling headers,

and isolated the fault. The leakage was contained in the small vault

associated

with the expansion joint and no other equipment was affected by the

presence of the standing water.

Procedure AR PK13-12, "[Circulating Water Pump] CWP 1-2 Cooling Water Low

Pressure," Revision 5, provided direction for operator response to a low pressure

-4-

condition for the intake cooling header.

Step 5.1 of Procedure AR PK13-12 required

operators to open cross-connect valves as an initial action to determine if the condition

clears.

Step 5.3 stated that, if the low pressure alarm does not clear and there is a

subsequent

tow head tank level alarm, ~sus

ect a rupture and reclose the cross-connect

valves.

On December 2, the operators knew that an expansion joint rupture and low

intake cooling head tank level condition existed prior to the receipt of the low header

pressure alarm, yet took procedural actions contrary to this knowledge.

The inspectors responded to the control room and witnessed operator recovery of the

leak. The inspectors concluded that operator response was satisfactory with the

exception of initiallycross-connecting

the intake cooling headers.

In addition, the

inspectors examined the area of the expansion joint failure and noted that no other

equipment was affected.

The root cause of failure of the expansion joint is discussed

in

Section M1.2 of this report.

The Operations Director obtained personnel statements with respect to the operator

response.

The licensee concurred that operator response was satisfactory with the

exception of the initial cross-connecting

of the intake cooling system headers.

The

licensee briefed the shift foreman on thoroughly understanding the consequences

of

taking actions prior to proceeding.

In addition, the licensee stated that they would

evaluate the need to enhance Procedure AR PK13-12.

c.

Conclusions

Overall, Unit 1 operators responded well to two failures of expansion joints. However,

operators initiallycross-connected

intake cooling system trains upon rupture of an

expansion joint that could have resulted in loss of both Unit 1 circulating water pumps.

Operators recognized and corrected this error before any adverse impact occurred.

02

Operational Status of Facilities and Equipment

02.1

Unit 1 Containment Tour

a.

General Comments

71707

On December 21, 1998, during a forced outage of Unit 1, the inspectors toured the

containment to assess

readiness for restart.

The inspectors noted that the area near

the containment recirculation sumps was clear, the containment building was free of

loose work material and debris, and only minor pump and valve packing leaks existed.

The inspectors concluded that the licensee had satisfactorily restored the Unit 1

containment materiel condition such that the plant was ready for restart.

-5-

02.2

Plant Materiel Condition

a.

General Comments

71707

The inspectors toured both units on a frequent basis to assess

the materiel condition of

safety-related areas.

The inspectors identified minor housekeeping

items, such as

loose tools and unattended ladders, that were brought to the attention of the shift

supervisor and immediately corrected.

With the exception of corroded outside tank

instrument lines {refer to Section E1.1), the external condition of components observed

during plant tours was good.

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments on Maintenance Activities

a.

Ins ection Sco

e 62707

The inspectors observed portions of work activities covered by the following work orders

and procedures:

R0187104, "Lubricate [AuxiliaryFeedwater] Turbine Over speed Trip Linkages"

(Unit 1)

~

MP M.3.7A, "Terry Turbine Throttle Trip Valve Preventive Maintenance,"

Revision

1 (Unit 1)

~

R0133000, "MS-1-RV-57 [AuxiliaryFeedwater Turbine Casing Relief Valve],

Test, Stage, and Replace" (Unit 1)

The inspectors concluded that each of these routine work activities were performed

satisfactorily.

M1.2

Surveillance Observations

a.

Ins ection Sco

e 61726

The inspectors observed performance of all or portions of the following procedures and

reviewed completed data.

Procedure R-3A, "Use of Flux Mapping Equipment," Revision OA (Unit 2)

Procedure STP R-3D, "Routine Monthly Flux Map," Revision 18 {Unit2)

Procedure STP R-27A, "Monthly Incore Thermocouple Evaluation," Revision 3

(Unit 2)

0

-6-

Procedure STP R-13B, "Nuclear Power Range Incore/Excore Single-Point

Calibration Data," Revision 2 (Unit 2)

~

Procedure STP M-81A, "Diesel Engine Generator Inspection (Every Refueling

Outage)," Revision 13 (Unit 1)

b.

Observations and Findin s

The surveillance tests were satisfactorily performed.

For the procedures related to

incore/excore detector calibration, the data indicated no abnormal axial offset. For

Procedure STP M-81A, the licensee performed an engine analysis on Diesel Engine

Generator 1-2. The procedure allowed this analysis to be performed prior to the outage,

which is scheduled to start February 7, 1999. The inspectors reviewed the licensee's

justification for performing this task on-line and determined that it was satisfactory.

Conclusions

The inspectors concluded that surveillances observed during this inspection period were

performed satisfactorily.

M2

Maintenance and Materiel Condition of Facilities and Equipment

~

~

~

~

M2.1

Failure to lm lement Vendor Instructions for Elastomeric Ex ansion Joints

Ins ection Sco

e 37551

62707

The inspectors reviewed the circumstances surrounding two recent failures of flexible

rubber/elastomeric expansion joints. An elastomeric expansion joint was a specially

designed section of pipe inserted within a rigid piping system to provide flexibility. The

inspectors reviewed action requests (AR) and work packages and interviewed system

engineers,

maintenance personnel, nondestructive examination personnel, and

management.

The inspectors observed licensee corrective actions in response

to the

recent expansion joint failures.

b.

Observations and Findin s

Two recent expansion joint failures are discussed below:

On December

1, 1998, as noted in AR A0472252, the screen wash auxiliary

header expansion joint failed, resulting in flooding at the intake structure.

The

expansion joint was 24-inch inside diameter by 12-inch long.

On December 2, the Circulating Water Pump 1-2 motor cooling inlet-outside

housing flexible elastomeric expansion joint (SW-1-EJ21) failed. The expansion

joint inside diameter was 6 inches and it was 6 inches long.

-7-

b.1

Vendor Information

The inspectors were informed by the system engineers that Uniroyal had provided the

original elastomeric expansion joints installed at Diablo Canyon.

1Nhen Uniroyal

stopped manufacturing elastomeric expansion joints, replacement elastomeric

expansion joints were obtained from Goodall, RM-Holz Rubber Company, Proco,

Uniflex, and Garlock.

The two expansion joints that failed were manufactured in 1972 by Uniroyal and had

been installed for approximately 26 years.

The replacement expansion joints were

manufactured by Garlock.

The inspectors reviewed the equipment specification and vendor documents for the

various expansion joints installed. These documents provided detailed expansion joint

information related to installation, disassembly, shelf life, and replacement schedule.

The documents reviewed included:

Vendor Manual DC 663323-19-2, "Gartock Expansion Joints, Installation &

Maintenance," Revision 4, dated September 1995.

Vendor Manual DC 663323-11-1, "RM-HolzTechnical Handbook - Fifth Edition,"

Revision 1, dated October 1980.

Vendor Manual DC 663323-29-1, "How to Install a Garlock Expansion Joint,"

dated 1995.

Specification 8725, "Furnishing and Delivery of Elastomeric Expansion Joints for

Units 1 and 2 Diablo Canyon Site - Uniroyal Inc.," dated December 22, 1971.

An April 7, 1994, Garlock supplier (Pacific Mechanical) letter referenced

P.O. 42932.

The vendor manuals provided detailed instructions to disassemble

the expansion joints,.

including critical measurements;

to install the expansion joints, such as measuring the

bolt tightness

1 week after installation and periodically thereafter; and to install control

units. Other vendor manual information included the life expectancy of the elastomeric

joints. The documents clearly established a life expectancy of 5 years for service

conditions that were not severe, which included no misalignment and proper installation

and storage.

The documents indicated that the elastomeric expansion joints had a

5-year shelf life from the date of manufacture and that the elastomeric joints should be

replaced every 5 years.

Manual DC 663323-19-2 specifically states, "If no

physical/visible signs of distress are present, the expansion joint should be replaced

every 5 years.

The strength of the expansion joint is in the internal structuring of its

layers - deterioration of these strengthening joints is not always apparent."

Other

information indicated that, although the service life was 5 years, inspections should take

place on a yearly basis to check for signs of fatigue or wear.

0

-8-

b.2

Followup on Other Uses of Elastomeric Expansion Joints

System engineers identified approximately 120 elastomeric expansion joints installed in

both units and that 13 elastomeric expansion joints were safety-related.

On

December 8, the inspectors toured various areas of the plant to evaluate elastomeric

expansion joint installations in various systems and identified the following:

Five Uniroyal elastomeric expansion joints had each accumulated approximately

26 years of service.

The other elastomeric expansion joints had been in service

for 10 years or more.

A nonsafety-related elastomeric expansion joint on the discharge of Screen

Refuse Pump 0-1 was incorrectly installed. Some of the expansion joint flange

bolts were installed backwards (the bolt was in contact with the rubber arch

section of the joint) and half of the triangular plates of the control units were

installed on the wrong side of the expansion joint flanges. The system engineer

documented the inspector's observations

in AR A0472743 and implemented

corrective actions for the installed expansion joint.

Three as-found elastom'eric expansion joints that might have had piping

misalignments in excess of the vendor's recommendations for maximum

allowable piping misalignment.

Two of the expansion joint installations (motor

cooling lines for the Unit 1 circulating water pumps) identified with possible piping

misalignment problems had similar configurations to the failure of Expansion

Joint SW-1-EJ21.

The inspectors noted that vendors recommended that, whenever excessive

piping misalignment existed prior to installing an expansion joint, either the piping

had to be realigned or a special offset expansion joint had to be supplied by the

vendor. The inspectors noted that acceptable piping alignment is critical to

ensure elastomeric expansion joints have freedom of movement within specified

design limits. The system engineer informed the inspectors that engineering

personnel were reviewing all existing elastomeric expansion joint installations as

part of the corrective actions implemented for the expansion. joint failures.

After replacing failed Expansion Joint SW-O-EJ2, the flange on the east side of

the expansion joint had a crack, which leaked approximately 10 gallons per hour.

The crack extended from the edge of a flange bolt hole into the flange neck

area.

The licensee documented this deficiency in AR A0472629. The licensee

determined that the leak resulted from a flaw in the flange, not from maintenance

activities.

b.3

Generic Letter 89-13 Commitments

The inspectors reviewed the licensee's November 25, 1991, response to Generic Letter 89-13, "Service Water System Problems Affecting Safety-Related Equipment."

The licensee had established a routine inspection and maintenance program to ensure

that auxiliary saltwater system performance was not adversely impaired. The inspectors

-9-

reviewed AR A0043296 and noted that it identified 13 safety-related expansion joints

that were to be inspected every 24 months to satisfy the commitment to Generic Letter 89-13. These expansion joint inspections were performed in accordance with

various recurring task activity work orders under the preventive maintenance program.

During these inspections engineering personnel performed a visual inspection of

expansion joints for cracks, bulges, leaks, or visible indications of past leakage.

The

inspectors concluded that the licensee's actions met the Generic Letter 89-13

commitments with respect to elastomeric joints.

b.4

Preventive Maintenance Program Adequacy for Elastomeric Joints

At the completion of the inspection, the licensee had not determined whether the initial

two failures were maintenance preventable functional failures or completed their plans

for upgrading the preventive maintenance program.

The inspectors reviewed various vendor documents supplied to the licensee, work

orders, ARs, and expansion joint installations and, after conducting discussions with

maintenance and system engineering personnel, the inspectors noted that as of

January 6, 1999:

Approximately 10 of the 13 safety-related elastomeric expansion joints currently

installed in the plant had been manufactured by Garlock, and some of these

expansion joints had been in service in excess of 5 years.

While Garlock vendor information identified that the typical service life

expectancy of an elastomeric expansion joint was 5 years and that preventive

maintenance schedules should be enacted accordingly, the licensee had not

implemented this information into the applicable maintenance programs or

schedules or provided the technical basis for not accomplishing this

recommendation.

Engineering personnel had not identified the service life expectancy for the

various other nonsafety-related

elastomeric expansion joints currently installed in

the plant.

The inspectors determined that existing maintenance procedures and work

documents did not include various vendor recommendations for elastomeric

expansion joint installations, which included:

(1) Retighten the expansion joint

flange bolts after 7 days of system operation; (2) recheck bolts for tightness

periodically, or every 6 months, after placing the system into service; and

(3) check bolts for tightness after any extended system outage.

Vendor documentation also stated that, prior to replacing an existing expansion

joint, dimensions must be verified. As a result of settlement, misalignment, or

improper design, many elastomeric expansion joints may be overstressed

beyond their performance limitations. It is critical, therefore, that all

measurements

(overall flange-to-flange, lateral, torsional, and angular

misalignment) be checked against original specifications/drawings.

-10-

The inspectors noted that these measurements

were not documented for the

replacement of the two failed joints and, based on a sample review, had not been

documented during replacement of other expansion joints over the last 2 years.

b.5

Engineering personnel implemented actions to have vendor representatives

(Garlock)

perform onsite evaluations of the condition of all installed expansion joints and perform

onsite elastomeric expansion joint training for plant personnel the week of January 11.

The vendor representatives

informed the inspectors that they would be providing the

licensee with a trip report and recommended actions.

The licensee representatives

stated that they would evaluate the vendor information for any needed changes in their

maintenance

program.

The licensee representatives

also stated that the vendor

identified two other nonsafety-related

expansion joints that showed indications of

potential failure. The licensee initiated actions to replace these expansion joints.

Operability Assessment of Safety-Related Expansion Joints

During review of the safety-related expansion joints, the licensee identified three

expansion joints in the auxiliary saltwater system that had been in service longer than

15 years.

The licensee determined that two expansion joints had been installed for 15

years and that one expansion joint had been installed for over 26 years (same

manufacturer and age as the failed expansion joints). The licensee concluded by

engineering judgement that these expansion joints remained acceptable for use until the

Unit 2 outage in September 1999. The licensee based this decision on: (1) external

visual inspections of all three expansion joints; (2) internal inspections of the oldest

Uniroyal expansion joint; and (3) an analysis that indicated that these joints, located at

the high point in the system, were subject to very little differential pressure.

Because the licensee had not thoroughly consulted the vendor manual with respect to

expansion joints, the licensee wrote a prompt operability assessment

in AR A0472506

that had questionable reasoning.

The assessment

stated that the expansion joints had

only slightly exceeded their service life of 15 years, even though the vendor manual

recommended

replacement every 5.years.

In addition, the assessment

stated that

external visual inspections were satisfactory.

However, the vendor manual indicated

that external inspections did not provide useful information because the integrity of the

expansion joint was based on the material condition of the internals.

The licensee

correctly noted that the aging expansion joints in the auxiliary saltwater system were

subjected to pressures

substantially less than the design pressure

(3 versus 100 psig).

The inspectors visually inspected the external surface of the three older auxiliary

saltwater expansion joints and did not note any damage.

In addition, the inspectors

inspected the internal surface of the 26-year old expansion joint during routine

component cooling water heat exchanger cleaning and did not note any degradation.

However, the inspectors noted that Garlock technical information indicated that visual

inspections did not always indicate impending failure. In addition, the inspectors

determined that the licensee had not yet addressed

the potential common-mode failure

of both Unit 2 component coolin'g water heat exchangers

because

of age hardening

failure of the auxiliary saltwater expansion joints during a seismic event.

S

-11-

Subsequently,

the licensee calculated the magnitude of the displacement of the

safety-related expansion joints during a seismic event.

Calculations revealed that total

displacement (including thermal expansion) of the Component Cooling Water Heat

Exchanger 2-1 inlet expansion joint was approximately 0.75 inches.

The licensee

contacted the vendor with this information. The vendor representative stated that

operability of this expansion joint could not be assured given the age-related hardening

and maximum displacement.

On January 28, 1999, the licensee declared Expansion

Joint SW-2-EJ3 inoperable and replaced it immediately. The vendor evaluated the other

.

two questionable auxiliary saltwater expansion joints and determined that they would

remain operable because of considerably less displacement during a seismic event.

The inspectors concluded that the licensee's operability determination of the oldest

safety-related expansion joints was weak, because

it failed to accurately reference

vendor recommendations

on replacement frequency and had not considered seismic

interactions.

Further NRC review of compliance with 10 CFR 50.65, "Requirements

for Monitoring the Effectiveness of Maintenance at Nuclear Power Plants,"

(Maintenance Rule) in regard to expansion joints is required, pending completion of the

licensee's maintenance preventable functional failure evaluation.

This issue is

unresolved (50-275; 323/98020-01).

Conclusions

The inspectors concluded that vendor information provided to ensure acceptable

installation and maintenance of elastomeric expansion joints was not properly

implemented into the maintenance program. The licensee's failure to replace expansion

joints in a timely manner led to failure of two joints and caused partial flooding of the

intake structure and loss of a circulating water pump. These failures required operators

to quickly reduce power to preclude a reactor trip. The assessment

that supported the

operability of the safety-related expansion joints failed to reference vendor

recommendations

on replacement frequency and seismic interactions.

As a result, the

licensee did not identify an inoperable elastomeric joint; until challenged by the

inspector.

Further NRC review of the licensee's evaluation of this degraded condition

and application of the Maintenance Rule program to expansion joints is required.

MS

Miscellaneous Maintenance Issues (92903)

M8.1

Closed

Violation 50-275 323/96021-04:

failure to establish appropriate performance

criteria for the main steam safety valves (MSSVs)

This violation reported that the licensee had set system level performance criteria for the

MSSVs at too high a threshold to provide a true indication of component reliability.

Although a number of MSSVs had failed to meet the Technical Specification criteria, the

licensee had not considered any of these failures to be maintenance preventable

functional failures.

As corrective action, the licensee also performed an audit of Maintenance Rule

compliance and found other program deficiencies.

However, the licensee did not

-12-

resolve these program deficiencies in a timely manner, which resulted in Violation 50-

275; 323/97004-01 as documented in the NRC Maintenance Rule baseline inspection.

Because the programmatic corrective actions were subject to review during the

Maintenance Rule baseline inspection, the inspectors reviewed the corrective actions

specifically associated with the MSSVs.

The inspectors determined that the Maintenance Rule program included specific

performance criteria for the MSSVs, including meeting the Technical Specifications

requirements.

The inspectors reviewed recent MSSV testing and determined that most

valves had met the Technical Specifications criteria during the most recent testing even

though the MSSVs were still in 10 CFR 50.65 (a) (1), goal setting. The inspectors also

determined that recent individual failures to meet the Technical Specifications criteria

were properly considered to be maintenance preventable functional failures and that the

testing program included performance of additional testing, if any one valve failed to

meet the Technical Specifications criteria.

Closed

Violation 50-275 323/96023-02:

failure to take corrective action to preclude

failure of first level undervoltage relay to meet Technical Specification requirements.

This violation resulted because 8 of 18 surveillance tests of first level undervoltage

relays had failed to meet Technical Specifications requirements.

They had not

determined the root cause or taken actions to preclude recurrence.

The licensee later

determined that many of these failures resulted from personnel error in setting the

relays different than recommended by the manufacturer.

During observations of secondary level undervoltage relay testing, discussed

in NRC

Inspection Report 50-275; 323/98-16, the inspectors reviewed recent first level

underyoltage relay data and determined that the performance had improved.

In

addition, the licensee had submitted Licensee Amendment Request 98-08 to obtain

NRC approval to change the specific model of the relay and slightly modify the relay

setpoints.

The inspectors considered that the licensee corrective actions to resolve this

violation were appropriate.

Closed

Violation 50-323/96023-03:

failure to properly restore a temporary

modification.

The inspectors identified that, following removal of a temporary pressure gage from the

Unit 2 chemical and volume control system, maintenance personnel failed to remove the

jumper tag and correct the control room drawings, which violated procedures.

For corrective actions the licensee:

(1) removed the information tag; (2) corrected the

control room drawing; (3) discussed the violation with the personnel involved

and'rovided

shift orders to the operating crews to emphasize operator responsibilities with

respect to lifted leads and jumpers; (4) revised Procedure CF4.ID7, "Temporary

Modifications - Plant Jumpers and M&TE"to provide added tracking mechanisms for

closure of lifted lead and jumper entries; and (5) performed a review of the jumper logs

to ensure that no other discrepancies

existed.

-13-

The inspectors reviewed licensee documentation that demonstrated

that these items

were completed and concluded that the documentation was satisfactory.

M8.4

Closed

Licensee Event Re ort50-275 323/96-018-01:

4kV bus undervoltage

protection relays out of specification because of personnel error.

This LER revision is closed as discussed

in Section M8.2.

E1

Conduct of Engineering

E1.1

Condensate

Stora

e Tank CST Leaka

e

Ins ection Sco

e 37551

The inspectors evaluated the engineering response to leakage from the Unit 1 CST, in

accordance with AR A0474556.

Observations and Findin s

On January 11, 1999, the licensee noted water leaking from the area of the Unit 1 CST.

Inspection revealed that the leak was from a 1-inch instrument line for Level

Transmitter LT-40 that penetrated the side wall near the bottom of the CST. Level

Transmitter LT-40 provided level indication at the hot shutdown panel for the CST. This

carbon steel line had corroded because of rainwater seepage

into the area, resulting in

the through-wall leak. The licensee declared Level Transmitter LT-40 inoperable and

initiated an AR to enter this item into the corrective action program.

Because of the through-wall leak, the licensee determined that the seismic qualifications

of the instrument line could not be justified. Consequently, the licensee postulated a

complete failure of the instrument line and initiated a prompt operability assessment.

'The licensee evaluated whether the CST had adequate capacity to support auxiliary

feedwater operation for the required 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> in hot shutdown, with the additional water

loss from the 1-inch instrument line break and assumed that the CST was 83 percent

full. The licensee used guillotine breaks of the single 12-inch and four 4-inch Class 2

lines'and calculated the amount of time it took for the CST to drain below these

penetrations.

Using this methodology, the licensee determined that the CST remained

operable.

The inspectors reviewed the licensee calculations and agreed with the

conclusions.

For a temporary repair, divers entered the CST and installed an expandable plug in the

affected penetration for the instrument line. Technical Specifications require Level

Transmitter LT-40 to be returned to service within 30 days or place the unit in hot

shutdown.

However, since this leak was discovered 26 days before Refueling

Outage 1R9, the licensee delayed the permanent repair of the instrument until the

outage.

-14-

The inspectors questioned the generic implications of this issue.

The Unit 1 CST had

two other safety-related instrument lines. The licensee inspected these lines and noted

some degradation of the wall thickness but no through-wall leakage.

In addition, the

licensee inspected similar penetrations on Unit 2 and identified no additional concerns.

The inspectors also examined these areas and concurred with the conclusions.

The

licensee stated that they had also planned to inspect the penetrations associated with

the other outside storage tanks (refueling water storage tanks, primary water storage

tanks, and fire water storage tank). The inspectors considered the scope of the

inspections satisfactory.

The inspectors questioned the licensee as to why the maintenance

rule program for

periodically examining safety-related structures had not identified this issue.

The

licensee stated that the outside tanks and associated

penetrations were in the scope of

the inspections but had not yet been scheduled.

The inspectors willperform further

review of the adequacy of the maintenance

rule program for assessing

structures.

This

issue will be tracked as an inspection followup item (50-275; 323/98020-02)

~

Conclusions

The prompt operability assessment

associated with the Unit 1 CST leak was an example

of good engineering support for operations.

Review of the adequacy of the

maintenance

rule program to assess

safety-related structures required further review.

Miscellaneous Engineering Issues (92700, 92903)

Closed

Licensee Event Re ort 50-275 323/96-014-00:

Steam Generator primary

coolant tubes were locked in tube support plates.

This licensee event report is administratively closed based on issuance of Revision 1.

Closed

Violation 50-275 323/96024-02:

Design criteria memoranda revised without

proper evaluation.

The inspectors identified that Design Criteria Memorandum S-9, "Safety Injection

System," was revised without evaluating the changes

in accordance

with

Procedure CF3.ID2, "Design Criteria Memoranda," Revision 2, which required changes

to the design criteria memoranda to be evaluated for impact on the plant licensing basis.

For corrective actions the licensee:

(1) incorporated the proper calculation into Design

Criteria Memorandum S-9, (2) discussed the improper changes with the personnel

involved, (3) performed a separate

calculation to verify that the proper amount of water

existed in the refueling water stowage tank, and (4) performed additional reviews of other

design criteria memoranda.

The inspectors performed a review of documentation supporting completion of the

corrective actions and concluded that the licensee actions were satisfactory.

-15-

E8.3

Closed

Licensee Event Re orts 50-275/97-007-00and50-323/98-002-00:

greaterthan

1 percent steam generator tubes defective.

In accordance with Technical Specification 4.4.5.5c, the licensee reported that greater

than

1 percent of the tubes inspected in Steam Generators

1-1 and 1-2 during Refueling

Outage 1R8 and Steam Generator 2-2 during Refueling Outage 2R8 were defective.

The inspectors ascertained from review of the Refueling Outage 1R8 examination history

that the number of tubes found to contain defects in Steam Generators 1-1, 1-2, 1-3,

and 1-4 were, respectively, 46, 125, 10, and 18. Alldefective tubes were removed from

service by plugging. The defective tube totals for Steam Generators

1-1 and 1-2

represented,

respectively, 1.36 percent and 3.69 percent of the 3388 tube population in

an individual steam generator.

The most significant tube degradation mechanism was

primary water stress corrosion cracking at hot-leg side dented tube support plate

intersections, which resulted in a total of 128 tubes being removed from service in the

four steam generators.

The second greatest detected tube degradation mechanism was

. outside diameter stress corrosion cracking at nondented tube support intersections,

which resulted in the removal of 45 tubes from service in the four steam generators.

Actions taken by the licensee to increase tubing stress corrosion resistance and minimize

steam generator tube degradation were reviewed during a 1995 steam generator tube

integrity inspection (NRC Inspection Report 50-275; 323/95-10).

Specific initiatives

implemented by the licensee included the following:

Thermal stress relief of Rows

1 and 2 low radius U-bends to minimize the tubing

susceptibility to primary water stress corrosion cracking; implement boric acid

additions to the secondary side to arrest tube denting and limitinitiation of outside

.diameter stress corrosion cracking; and replace copper alloy tubes in the

feedwater heaters with stainless steel, in order to eliminate copper transport to

the steam generators and minimize its contribution to,development of outside

diameter stress corrosion cracking and pitting in the steam generator tubes;

Shot peening the inside diameter surface of the tubes in the tube sheet region to

minimize development of primary water stress corrosion cracking at this tubing

location;

Adopting Electric Power Research

Institute secondary water chemistry

recommendations

to increase hydrazine additions to 100 parts per billion, in order

to reduce electrochemical potential in the steam generators and thereby minimize

development of outside diameter stress corrosion cracking;

Initiating the use of ethanolamine (for pH control) to reduce iron transport to the

steam generators, which minimizes its contribution to development of outside

diameter stress corrosion cracking;

Adopting Electric Power Research

Institute secondary water chemistry-

recommendations

for use of molar ratio control (using ammonium chloride

(I

-16-

injection), as a means of eliminating alkaline crevice chemistry conditions that

promote initiation of outside.diameter stress corrosion cracking;

, Using eddy current examination practices that are consistent with the latest

guidance contained in Electric Power Research institute Document "PWR Steam

Generator Examination Guidelines" and the WEXTEXowners group guidelines;

Adopting a policy of maintaining steam generator blowdown at 1 percent of the

'ain

steaming rate, in order to minimize steam generator contaminate levels.

In June 1998, the licensee initiated injection of zinc acetate into the Unit 1 reactor coolant

system to maintain a zinc concentration of 35-40 ppb.

Ionic zinc has been found by

laboratory testing and analytical programs to reduce general corrosion of primary system

materials and to partially inhibit primary water stress corrosion cracking of Inconel 600.

The inspectors ascertained from review of the Refueling Outage 2R8 examination history

that the number of tubes found by eddy current examination to contain defects in Steam

Generators 2-1, 2-2, 2-3, and 2-4 were, respectively, 8, 34, 26, and 23. Allof the

defective tubes were plugged.

These totals reflected the initial use by the licensee of

voltage-based

alternate repair criteria for outside diameter stress corrosion cracking at

tube support plates.

Use of the voltage-based

alternate repair criteria for Unit 2 steam

generators was approved by the issuance of License Amendment 122. Without the

voltage-based

alternate repair criteria, the respective plugging totals for Steam

Generators 2-1, 2-2, 2-3, and 2-4 would have been 29, 48, 33, and 99 tubes.

Accordingly, the use of voltage-based alternate repair criteria made only Steam

Generator 2-2 reportable in accordance with Technical Specification 4.4.5.5c, with

slightly over

1 percent of the tubes being plugged.

R1

Radiological Protection and Chemistry Controls

R1.1

Inade

uate Hi h Radiation Area Postin

a.

Ins ection Sco

e 71750

The inspectors evaluated the licensee's response to AR A0473925, which described an

inadequate high radiation posting.

b.

Observations and Findin s

On December 23, 1998, during a routine radiation protection tour of the facility, radiation

protection personnel identified that the Residual Heat Removal Pump Room 1-2

recirculation chamber door was posted as a radiation area while the main double-door

entry into the room was posted as a high radiation area.

Radiation protection personnel

corrected this posting error immediately and initiated an AR. A high radiation area sign

and yellow and magenta rope were found staged near the improper posting.

e

-17-

Licensee investigation revealed that, on December 18, high radiation area signs and rope

were staged at all entrances to both Unit 1 residual heat removal rooms. This was done

in anticipation of initiating the residual heat removal system to cool down the plant for

repairs of a primary pressure boundary leak. On December 20, radiation protection

technicians performed surveys that established that the residual heat removal pump

rooms required upgrading to high radiation area postings.

A radiation protection

technician stated that he properly posted each room at this time. No other surveys of the

room were performed subsequently, and no other personnel in the area could recall the

area being reposted as a radiation area.

Therefore, the licensee concluded that the root

cause was indeterminate.

Although the licensee did not identify a definitive root cause, the licensee recommended

several corrective actions.

Corrective actions included:

(1) properly posting Residual

Heat Removal Pump Room 1-2, (2) initiating an expectation that changes

in postings be

documented on the survey forms and that personnel reviewing surveys check the

postings, (3) recommending that radiation protection foremen walk down areas that have

changes to postings, and (4) discussing this event with all radiation protection technicians

and foremen.

The inspectors considered the corrective actions to be satisfactory.

Failure to properly post an area containing radiation doses in excess of 100 millirem per

hour as a high radiation area is a violation of 10 CFR 20.1902(b).

However, this

nonrepetitive, licensee-identified and corrected violation is being treated as a noncited

violation, consistent with Section VII.B.Iof the Enforcement Policy

(50-275; 323/98020-03).

'onclusions

A noncited violation of 10 CFR 20.1902(b), consistent with Section VII.B.Iof the

Enforcement Policy, was identified for failure to properly post a high radiation area.

Radiation protection personnel failed to post a back entrance to Residual Heat Removal

Pump Room 1-2. Although the root cause analysis was inconclusive, corrective actions

were satisfactory.

Conduct of Security and Safeguards Activities

General Comments

71750

During routine tours, the inspectors noted that the security officers were alert at their

posts, security boundaries were being maintained properly, and screening processes

at

the Primary Access Point were performed well. During backshift inspections, the

inspectors noted that the protected area was properly illuminated, especially in areas

where temporary equipment was brought in.

I

18-

Control of Fire Protection Activities .

Control of Combustibles

Units 1 and 2

Ins ection Sco

e 71750

The inspectors toured safety-related areas to ensure that licensee procedures

concerning the control of combustibles were implemented.

Observations and Findin s

On October 20, 1998, the inspectors identified that 2 hydrogen compressed

gas cylinders

were located on the 85-foot elevation of the auxiliary building. These cylinders were

sized to contain 7.1 cubic feet of 10 percent hydrogen at 2200 psig. The inspectors

expressed

concern because

hydrogen is flammable. -Further, the fire protection program

required a permit to bring combustible materials into vital areas, including the power

block. Subsequently,

the licensee removed the cylinders from the power block and

initiated AR A0470209 to enter this item into the corrective action program.

On

October 29, the licensee performed walkdowns of both units and noted 5 other

compressed

gas cylinders of similar size that were improperly stored, and which

contained flammable gasses.

These items were also removed from the power block.

Licensee investigation revealed that maintenance personnel had brought these

compressed

gas cylinders into these vital areas.

Compressed

gas cylinders containing

argon were approved for use in the power block on the 85-foot elevation of the auxiliary

building in accordance with Design Change Notice DCN-EM-39613. Personnel believed

that this document allowed compressed

gas cylinders in the area without regard to

content. This misconception was discussed with maintenance personnel because the

design change did not exempt the licensee from fire protection requirements.

The.

licensee evaluation further revealed that this issue was of low potential safety

significance.

Although hydrogen, a flammable gas, was introduced into areas containing

safety-related equipment, a scenario involving a fire associated

with the hydrogen gas

was considered unlikely.

In addition, the licensee performed calculations that revealed

that, because

of the size of the space, if all of the gas was released to the 85 foot

elevation, a combustible mixture would not result.

Procedure OM8.ID4, "Control of Flammable and Combustible Materials," Revision 7,

Section 4.2.3, required issuance of a transient combustible permit when flammable

materials were brought into the power block. Therefore, the introduction of compressed

gas cylinders containing hydrogen without a transient combustible permit is a violation of

Technical Specification 6.8.1.h.

However, because the licensee took satisfactory

corrective actions in AR A0470209 in response to this issue, no response was required

(50-275; 323/98020-04).

0

0

c.

Conclusions

-19-

The inspectors noted that the licensee had inappropriately stored compressed

gas

cylinders in the auxiliary building. Contrary to plant procedures, personnel had not

obtained a transient combustible permit, as required for storing flammable material,

which resulted in a violation of Technical Specification 6.8.1.h. The licensee

demonstrated that this instance involved low likelihood of a fire involving hydrogen gas.

The licensee determined the cause of the violation, identified other examples, and took

appropriate corrective actions; therefore, no response was required.

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at the

conclusion of the inspection on January 30, 1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection should

be considered proprietary.

No proprietary information was identified.

T

A%IACHMENT

SUPPLEMENTAL INFORMATION

PARTIALLIST OF PERSONS CONTACTED

Licensee

J. R. Becker, Manager, Maintenance Services

W. G. Crockett, Manager, Nuclear Quality Services

R. D. Gray, Director, Radiation Protection

T. L. Grebel, Director, Regulatory Services

D. B. Miklush, Manager, Engineering Services

J. E. Molden, Manager, Operations Services

D. H. Oatley, Vice President and Plant Manager

L. F. Womack, Vice President, Nuclear Technical Services

IP 37551

IP 61726"

IP 62707

IP 71707

IP 71750

IP 92700

IP 92901

IP 92902

IP 92903

IP 93702

INSPECTION PROCEDURES (IP) USED

Onsite Engineering

Surveillance Observations

Maintenance Observation

- Plant Operations

Plant Support Activities

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup - Operations

Followup - Maintenance

Followup - Engineering

Prompt Onsite Response

to Events at Operating Power Reactors

ITEMS OPENED AND CLOSED

~Oened

50-275; 323/

98020-01

50-275;323/

98020-02

URI,

Evaluate adequacy of maintenance

rule program for

expansion joints (Section M2.1)

IFI

Evaluate adequacy of maintenance

rule monitoring of

outside tanks (Section E1.1)

0

0

-2-

Closed

50-275; 323/

96021-04

50-275; 323/

96023-02

50-275; 323/

96023-03

VIO

VIO

VIO

Failure to establish appropriate performance criteria for

MSSVs (Section M8.1)

Failure to take corrective actions to preclude first level

undervoltage relay failures to meet Technical Specifications

requirements (Section M8.2)

Failure to restore a temporary modification (Section M8.3)

50-275; 323/

96-018-01

LER

4kV bus undervoltage protection relays out of specification

because of personnel error (Section M8.4)

50-275; 323/

96024-02

VIO

Design criteria memoranda revised without proper

evaluation (Section E8.1)

50-275; 323/

96-014-00

50-275/97-007-00

50-323/98-002-00

LER

Steam generator primary coolant tubes were locked in tube

support plates (Section E8.2)

LER

Greater than

1 percent steam generator tubes defective

(Section E8.3)

LER

Greater than

1 percent steam generator tubes defective

(Section E8.3)

0 ened and Closed

50-275; 323/

98020-03

50-275; 323/

98020-04

NCV

Failure to properly post a high radiation area (Section R1.1)

VIO

Failure to obtain transient combustible permit for

compressed

gas cylinders containing hydrogen

(Section F1.1)

-3-

Procedure

LIST OF LICENSEE DOCUMENTS REVIEWED

MA1 ~ID17

"Maintenance Rule Monitoring Program," Revision 5

S ecification

8725

"Furnishing and Delivery of Elastomeric Expansion Joints for Units 1 and 2 Diablo

Canyon Site - Uniroyal Inc" dated December 22, 1971

Vendor Manuals

DC 663323-10-2

DC 663323-11-1

DC 663323-19-2

DC 663323-29-1

Action Re uests

"Expansion Joints and Vibration Dampeners Installation Instructions Unit

One &Two,"Revision 2

"RM-HolzTechnical Handbook - Fifth Edition", Revision

1

"Garlock Expansion Joints, Installation 5 Maintenance," Revision

4'How

to Install a Garlock Expansion Joint," dated 1995

A0043296

A0336216

A0472252

A0472458

A0472506

A0472629

A0472743

Q~i

A0472288

Nonconformance Re ort

N0002079

Work Orders.

C0140103

C0143142

C01 59711

C0159751

R0078760

R0078800

R0165894

R01 65917

t

-4-

LIST OF ACRONYMS USED

AR

CFR

CST

CWP

IP

LER

MSSV

NCV

NRC

PDR

RCP

jo

STP

URI

VIO

Action Request

Code of Federal Regulations

Condensate

Storage Tank

Circulating Water Pump

Inspection Procedure

licensee event report

Main Steam Safety Valve

Noncited Violation

Nuclear Regulatory Commission

Public Document Room

Reactor Coolant Pump

Surveillance Test Procedure

Unresolved Item

Violation

e