ML16341F655

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Insp Repts 50-275/90-01 & 50-323/90-01 on 900108-12 & 0122- 0202.Violations Noted.Major Areas Inspected:Effectiveness of Corrective Actions Program,Sys Engineering Program,Safety Oversight Groups & Corporate Engineering Activities
ML16341F655
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 03/28/1989
From: Huey F, Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341F654 List:
References
50-275-90-01, 50-275-90-1, 50-323-90-01, 50-323-90-1, NUDOCS 9004200461
Download: ML16341F655 (80)


See also: IR 05000275/1990001

Text

'

U. S.

NUCL'EAR REGULATORY CONSaISSION

REGION

V

Report Nos.:

30-275/90-01,

50-.323/90-01

Docket Nos.:

License Nos.:

Licensee:

.

Facility Name:

Inspection at:

50-272,

.50-323-

DPR-BO, 3PR-82

'

Pacific

Gas

and Electric

Company

'77 Beale Street,

Room 1451

San Francisco,

California

94106

Diablo Canyon Units

1 and

2

Diablo Canyon Site,

San Luis Obispo, California

PG8E Corporate Offices,

San Francisco,

California

Inspection

Conducted:

January

S - 12 and January

22 - February 2,

1990

Inspectors:

Z zg(qc

nson,

rogect

ection

se

ate

cygne

am Leader

P.

N. gualls,

Resident

Inspector

Assistant

Team Leader

J.

F. Burdoin, Reactor Inspector

R.

G. Gilbert, Program Assistant

R. L. Prevatte,

Senior Resident

Inspector

J.

F. Ringwald, Resident

Inspector

R. S. Hodor, Systems

Engineering Consultant

K. Sullivan, Electrical Engineering Consultant

Approved by:

~F

.

Hu

,

ref,

nglneer)ng

Sect>on

~Summar:

ate

sgne

Ins ection

on Januar

1 - 12 and Januar

22 - Februar

2

1990

Re ort Nos.

50-275/90-0

an

50-323/90-01

~Al

1:

A

p i1,

1

i

p

effectiveness

of the licensee's

corrective actions

program.

The system engi-

neerina

program, safety oversight groups, corporate

engineer ing activities,

emergency lighting, and plant housekeeping

conditions were also inspected.

Portions of inspection

procedures

30703,

35702,

40500,

40702, 40703,

40704,

62705,

64704,

71707,

92701

92709,

and

92720 were utilized during this

inspection.

0

n 04bi

~

" a7>

9004~

gCK 0>

DR

AD

6

-2-

Results:

General

Conclusions- and

S ecific"Findin s:

1.

Inadequate

control-was provided for .temporary

changes to surveil-

lance procedures.

Other weaknesses

were also observed

in the

.preparation

and implementation of surveillance

procedures.

(Paragraph

3.c(6));

2.

3.

5.

6.

7.

8.

The corrective actions

program

w'as effective in initiating

corrective actions- and in accomplishing timely corrective actions

for safety-significant

issues.

However, several

issues

of lesser

individual significance

had been

open for several

months to'

few

years.

(Paragraphs

3.b and 3.c)

While the initiation of corrective actions

was effective

(and

actively encouraged

by management),

no person or group within the

licensee's

organization

was responsible for driving the clos'ure or

resolution of action items.

Trending reports

prepared

by the

licensee

showed that the

number of open action requests

was contin-

uing to increase.

(Paragraph

3.e)

Weaknesses

were noted in some aspects

of the System Engineer

and

Design

System Engineer

programs.

(Paragraph

5)

The backlog of Nuclear Engineering

and Construction Services

(NECS)

engineering

work was sizeable'nd

was growing slowly, although it

appeared

to be managed effectively.

(Paragraph

6)

Plant housekeeping

was found to be in need of improvement.

(Paragraph

7)

Emer gency lighting systems

were found to be adequate for safe shut-

down in the event of a station blackout.

(Paragraph

8)

While applicable

requirements

were being met, the General Office

Nuclear Plant Review and Advisory Committee

(GONPRAC) was providing

minimal ongoing guidance

and oversight regarding the conduct of

audits

performed

under its cognizance.

(Paragraph

3.d)

Significant Safet

Natters:

None.

Summar

of Violations:

Three violations were identified:

(I) failure to take effective correc-

tive action (paragraph 3.c(4)), (2) failure to obtain approval of tempo-

rary changes. to approved surveillance

procedures

(paragraph 3.c(6)),

and

(3) improper housekeeping

practices

(paragraph

7).

0

'

DETAILS

1.

Persons

Contacted

Principal Staff:

  • J. D.
  • J. D.
  • W. H.
  • J. A.
  • R. C.
  • J. B.

Yi. J.

  • D

B.

W.

Shiffer

Townsend

Wallace

Sexton

Anderson

Hoch

Angus

Miklush

Giffin

Senior Vice 'President,

Nuclear

Power Generation

Yice 'President,

Diablo Canyon Operations

,-Yice:President,

Engineering

Manager, guality Assurance

Manager,

Nuclear Engineering

and Construction

Services

Manager,

Nuclear Safety

and Regulatory Affairs

Assistant

Plant Manager,

Technical

Services

Assistant Plant Manager,

Oper'ations

Services

.Assistant

Plant Manager,

Yiaintenance

Additional staff members

contacted

during the inspection

are listed in

Attachment A.

  • Attended exit meeting at

DCPP

on February 2, 1990.

2.

Ins ection

Ob 'ectives

The overall objective of this inspection

was to assess

the effectiveness

of the licensee's

corrective actions

program.

This included

an assess-

ment of the following principal elements

of the program:

Effective definition of the program.

Proper initiation of appropriate corrective actions.

Effective and timely completion of corrective actions.

The effectiveness

of each of the principal quality oversight groups

involved in the corrective actions

program.

As part of'his assessment,

team members

were assiqned

to review and

walk down various plant systems.

Specific issues

related to these

systems

were identified for use in assessing

the effectiveness

of the

corrective actions

program.

The inspection

team also sought to assess

the effectiveness

of the

licensee's

System Engineer

(SE)

and Design System Engineer

(DSE)

programs (initiated, in part,

as corrective action for previously

identified weakness

in plant/corporate

interface).

Although outside the intended

scope of the team inspection,

one team

member also conducted

an inspection of emergency lighting systems.

'

3.

Corrective Actions Pro ram

The licensee's training staff provided the team a'brief introduction to

the computer-based

corrective action program.

The"team also reviewed

relevant directives,

interviewed members of the licensee's staff,

examined selected facility records,

and conducted

system

walkdowns in

order to assess

<he functioning of the corrective action program.

The

findings from .this effort are discussed

below.

a4

Pro ram Definition

The corrective action program at Diablo Canyon

Power Plant

(DCPP)

is defined .in Nuclear Plant Administrative Procedure

(NPAP) C-12,

Identification and Resolution of Problems

and Non-Conformances,

Revision

19.

The program is managed

through the Plant Information

Management

System

(PIMS),

a computer database

system.

This system

requires that the identifier of a problem (regardless

of the

quality classification)

or a nonconformance,

or suspicion that

a

nonconformance exists, initiate an Action Request

(AR) and report

the problem to his immediate supervisor.

The

AR is entered

into

the

PIMS system.

If access

to the

PIMS is not available,

the

individual should report the problem to his immediate supervisor

who will insure that an

AR is issued to address

the identified

problem.

Each

AR entered into the

PIMS system is sequentially

assigned

a

unique

number (this is done automatically

by the computer program)

as it is created.

Once entered,

the

AR is

a permanent plant record

and cannot

be deleted.

This system gives

a complete record of the

actions

taken, status,

and resolution for every problem entered

into the system.

Plant workers at the technician level are

required to have their supervisor enter

ARs into the system for the

problems they identified.

Employees

above the technician level

enter

ARs into the system themselves,

with supervisory review of

the

AR after it is entered.

Each

AR, once initiated, is classified

as either

a corrective main-

tenance

(CM) or administrative task

(AT) prior to implementation of

corrective action.

Once entered into the system,

each

AR is

reviewed for guality Assurance

(gA) program applicability and plant

operations

impact,

and is assigned

a priority based

on these

factor s. If a safety-related

system is involved, the

AR is

reviewed to determine if a nonconformance

report

(NCR) is required,

or whether

a quality evaluation

(gE) must be performed.

If the

problem requires evaluation for nonconformance,

significant event

investigation, root cause determination, reportability, or

justification for continued operation,

the

AR may require

additional

processing

using the steps

provided in the Decision Tree

for Problem Resolution,

Appendix 7.6 of NPAP C-12.

If an

NCR is

required,

then

a plant Technical

Review Group

(TRG) evaluates

the

NCR to determine

the root cause

and corrective actions.

The program appeared

to the inspectors to be

a broad-based

problem

reporting system,

and the actions required

by various personnel

involved with identifying and resolving problems

were adequately

delineated in procedure

NPAP C-12.

The

AR reporting program

began

onsite at DCPP in tune

1985

and

was

implemented in the

San Francisco offices in October

1988.

At the inception:of the

AP program, training was conducted for all

plant employees.

Training also

has

been provided periodically for

new employees.

Although no periodic refresher

training was

provided, plant personnel

interviewed appeared

knowledgeable

about;

='he

use of the

AR system.

One difficulty noted with the system

was

the difficulty in readily determining

component identification

( ID)

numbers,

in that an on-screen

index

was not provided by the

PIt15

program.

This problem appeared

to the inspectors

to at times

restrict the

use of the

PINS program.

This appeared

to be of

lesser

concern for CN ARs, since the

ID can

be added during review

by the Work Planning group.

However, since

AT type

ARs are not

normally routed to Work Planning,

determination of the

ID for these

ARs must

be done

by the originator or his/her supervisor.

b.

Initiation of Corrective Action

The team conducted

numerous

interviews,

reviewed

a wide selection

of plant records,

and walked

down several

plant systems

to identify

issues

requiring corrective actions.

It is considered

noteworthy

that this effort did not result in the identification of any items

deserving corrective action for which an action request

(AR) had

not been initiated.

Persons

contacted

and records

reviewed during the inspection

are

identified in Attachments

A and

C, respectively, to this inspection

report.

Inspection effort involved with system reviews

and walk-

downs is discussed

in paragraph

4 of this report.

Additional

reviews to determine

whether

appropriate

actions

had been identi-

fied were conducted

as follows:

(1)

Engineering Support

Discussions

and interviews were conducted with various

corporate

and plant staff members.

Corporate interviews

included the President's

Nuclear Advisory Committee

(PNAC)

Executive Secretary;

the Chairman

and Secretary of the General

Office Nuclear Plant Review and Audit Committee

(GONPRAC); the

Director of guality Assurance

(gA); one

gA engineer;

one

gA.

consultant;

one

gA supervisor;

and one

gA senior engineer.

In

the Operating

Experience

Assessment

area,

the group supervisor

and two engineers

were interviewed.

In the Engineering area,

two supervisors,

four group leaders

and approximately ten

other en'gineers

were interviewed.

Interviews were also

conducted with the cognizant

system engineers

and

some of the

design

system engineers

for the various

systems

reviewed,

as

discussed

in paragraph

4 of this report.

The results of these

(2)

interviews revealed .that, overall, personnel

were knowledge-

able of their jobs

and in the initiation of corrective action

requests.

'Plant Operations

Interviews conducted in this area

included the Assistant Plant

Manager for Operations

and Maintenance;

the Managers of

Operations,

Maintenance,

and Engineering;

two supervisory

and

two non-supervisory

engineers;

a shift supervisor;

a shift-

foreman;

two auxiliary operators;

an electrical,

an instrument

and controls

( IKC) and

a mechanical

maintenance

foreman;

a

machinist;

an electrician;

and an

ISC technician.

Each of

these

persons

appeared

to be knowledgeable

on the corrective

action program and their part in insuring its success.

All of

the above, with the exception of the electrician

and

machinist,

expressed

confidence

in their ability to input ARs

into the computer

and to use

PIMS.

These

two persons

stated

that deficiencies

or problems

are reported to their respective

foremen,

who input the problems into PIMS.

An auxiliary operator

expressed

a concern

about remaining

current with computer software

changes

as they occur.

An

inquiry into this matter revealed that

a telephone

HELP line

is available during normal working hours,

and

a refresher

course is offered by computer engineering

when sufficient

persons

to establish

a class

have requested

this training.

It

was stated that this training program was recently initiated

and

one class

was conducted

in January

1990.

The inspectors

attended shift crew briefings four times,

maintenance

supervisory morning meetings

three times,

and the

shift supervisor's

8:30 a.m.

work planning meeting

on four

different occasions.

On each occasion all of the meetings

were attended

on the

same

day to determine if the plant

problems

were communicated

through each of these

groups.

The

meetings

appeared

to be timely with significant events or

problems

being well covered.

On two 'occasions,

AR's discussed

in these

meetings

were verified to be on PINS.

The inspector

accompanied

an auxiliary operator

on his

required shift rounds

and observed

his performance of equip-

ment checks.

During these

rounds

a deficiency was identified

involving a leaking air regulator

and

a sticking gauge

needle

on the air supply to the spent fuel pool transfer

canal

gate.

The inspector verified that this item was documented

on

AR

A0176728, initiated by the operator.

During the above rounds,

the inspector observed

AR tag Nos.

A0174079, A0174082,

A0079363

and A0176432 hanging

on various

equipment in the auxiliary building.

The operator

was able to

enter

PIMS and verify the current status of these

items.

Discussions

with this operator revealed that he was capable of

documenting deficiencies

in his area.

0

(3)

During the above

rounds it was also noted that lighting in

some of the auxiliary building areas

was marginally adequate

and not conducive to the identification of equipment

and space

problems.

Other

problems

noted

on these

rounds, such'as

oil'tanding

under equipment

and water

on 'the floor, were dis-

cussed with the operator.

His explanation, that this problem

would be reported if it persisted after initial cleanup,

was

considered

reasonable.

I

The inspector

observed

control

room activities and held

discussions

with shift personnel

on three separate

occasions.

The discussion

centered

around their part in the review of ARs

reported

by operators

under their supervision,

and their

identification and reporting of self-identified problems.

These

personnel

were very knowledgeable

on the computer,

the

AR system

and existing problems.

Plant Maintenance

The inspector monitored selected

portions of the mechanical

maintenance activities associated

with a failure of the Unit 1

positive displacement

charging

pump which occurred during'he

inspection.

This item was identified by operations

and

documented

on

AR A0176837

on January

23,

1990 at 7:00 a.m.

At

9:00 a.m., mechanical

maintenance

conducted

a test

run and

isolated

the source of the problem to a crack in the

pump

suction casing.

The system engineer,

maintenance

engineer

and

work planner

were actively involved in determining the scope

and depth of repairs

needed.

The knowledge

and coordination

efforts of the mechanical

maintenance

engineer

and the

assigned

machinist were timely and impressive.

The repairs to

this

pump were tracked for the duration of the inspection.

Selected

portions of the compressed air system were walked

down with the system engineers

on three different occasions

during the inspection

(review of the compressed air system is

discussed

further in paragraph 4.f).

Extensive discussions

were conducted

focusing

on past system

and component

problems,

in-process

work and corrective maintenance,

and other work

activities

on this system.

The general office design engineer

participated in one of these meetings.

These

persons

were

very aware of past

system

problems

and activities in process

or planned.

No significant deficiencies

were identified

during these

walkdowns that had not been previously documented

in the corrective action system.

Timeliness

and Effectiveness

of Corrective Actions

The various interviews, walkdowns,

and record reviews discussed

in

paragraph

3.b resulted in review by the inspectors of many active

and completed action requests

(ARs).

These

reviews indicated that

the priority system

used for classifying

ARs was effective, in that

problems

which had safety significanc'e or another

reason for-

expeditious

resolution

had

been

addressed

in

a timely manner.

However, these

reviews also identified,several

items of lesser

individual significance which had

been

open for,extended

periods,

and which 'indicated that additional attention

needed to be given to

the closure of ARs.

These long-standing

active

ARs are discussed

below.

(1)

Auxiliary Feedwater

Pump

(AFW) Governor Cooling Water Flow

During walkdown of the Unit 1

AFW .system,

the inspecto~'oted

a tag for AR No. A0085279 attached

to flow indicator FI-12 in

the cooling water line to the turbine-driven

AFW pump gover-

nor.

This tag stated

"no flow indicated."

Review of the

AR

indicated that it was

an administrative

task

(AT) type AR-

which had

been initiated in November,

1987.

The history of

the concern traced

back through several

ARs and work orders

(for Units

1 and 2) to AR No. A0000974, initiated in July

1985.

The licensee

determined early in the process

that the

indication of no flow to the governor oil heat exchanger

did

not affect operability of the

AFW pump.

Various steps of the

review had also determined that (1) there

was

no physical

blockage of the cooling water lines

and (2) the flapper in the

Unit

1 FI-12 was about twice as thick as in Unit 2.

(2)

Resolution of the no-flow indication focused for some time on

impr'oper operation of FI-12, and Engineering

recommended

in

October

1989 that it be replaced with a

new indicator of the

same type.

This recommendation

was not accepted

by the system

engineer,

and the

AR was reassigned

for furthe'r evaluation.

In November

1989, after testing

showed that FI-12 did indicate

flow introduced

from a test source

(hose connection), it was

concluded that the problem was actually one of flow balancing

(i.e., two bearing

heat exchangers

in parallel with the gover-

nor oil heat exchanger

were carrying almost all of the flow,

and flow through FI-12 was actuall

low).

At the time of the

inspection, further testing

was

p armed to try balancing the

flow so that FI-12 would indicate flow through the governor

oil heat exchanger.

The total time to resolve the concern

.. with FI-12 (in both units) appeared

to be excessive,

with more

than four years elapsing before it was concluded that the

indication was valid and that actual

low flow was the reason.

Overgreasing

of Electrical Motors

NRC Information Notice 88-12, Overgreasing of Electric h1otor

Bearings,

was reviewed

by the Operating Experience

Assessment

(OEA) group,

and recommendations

were sent to the Plant Staff

Review Committee

(PSRC)

on 6/13/88.

The

PSRC agreed to the

recommendations

on 9/29/88 and issued

an Action Request

(A/R).

The completion date

was revised to 4/1/89 and then to

10/31/89.

As of 1/10/90, the action

was still not complete

because

resources

for this project had

been shifted to other

activities.

Plant maintenance

personnel

stated that over-

greasing

had not been

a problem at Diablo Canyon,

and that the

issue

was being addressed

cautiously to ensure that corrective

(3)

action to address

the issue did cot result in undergreasing

of

motors.

Nevertheless,

the inspector

concluded tttat the time

to complete

these

PSRC-approved

actions

to .address

recognized

industry concerns

was excessive.;

Blind Flange

on Condensate

Storage

Tank

(CST) Overflow Line

C

A licensee-conducted

Safety System Functional Audit and Review

(SSFAR) of the

AFW system determined in July 1989 that

a blind

flange (with a 2-inch hose connection)

was installed

on the

14-inch overflow line for the Unit 2 CST.

The

SSFAR raised

several

questions,

including why the flange

was in place

and

whether possible overpressurization

of the

CST had occurred.

The inspectors

noted that

a work order

(WO) was written and

the flange was

removed

from the overflow'ine on the day of

discovery.

The absence

of a flange on the Unit

1

CST was also

verified.

Examination

by the inspectors

identified two ARs,

two quality evaluations

(gEs), three action evaluations'(AEs),

and the one

WO (referenced

above) dealing with this issue,

and

making numerous

references

to one another.

Although this

made

it tedious to determine

the actual status of related actions,

it was determined that little action, other than removal of

the flange (along with consideration of security concerns

and

confirmation that other tanks

were not affected),

had

been

accomplished.

In particular, the following actions called for

by the

SSFAR were still incomplete:

Correction of system flow diagram.

Engineering evaluation to determine

whether the

CST could

have

been overpressurized

(an 'initial evaluation

by

Engineering that this was indeterminate,

and therefore

not

a concern,

was rejected

by gA).

Determination of reportability.

Determination of root cause.

(4)

While these actions

were being tracked

by the licensee's

AR

program for eventual

completion, the amount of time to address

them (particularly the question of reportability) appeared

to

be excessive.

Steam Generator

(SG)

Slowdown Monitor

While observing control

room activities

and discuss'ing

correc-

tive actions

on problems identified by operations,

the

inspector determined that Operations

had experienced

recurring

problems with Technical Specification (TS) 3.3.3. 10.

The

concern

was with the radioactive

gaseous

effluent monitoring

instrumentation for the steam generator

blowdown tank vent

gross radioactivity monitor (RN-27).

The steam generator,

blowdown system at

DCPP is, designed to

maintain

steam generator

water chemistry within specified

limits.

The .'blowdown of approximately

20 - 30

gpm

per'enerator

flows to the .blowdown tank

and discharges .to'he

circulating water discharge

tunnel.

To conserve water;

a

second

blowdown system .recycles the flow through

a treatment

and recovery system to 'the main condenser.

Each of the above

systems

has

a capacity of approximately .150

gpm.

Each unit is

equipped with the above systems.

The steam generator

blowdown flow to the blowdown tank is

continuously monitored for radioactivity by the blowdown

radiation liquid sample monitor RN-19. If this system detects

a high concentration of activity in the blowdown flow, the

blowdown isolation valves

and the blowdown tank effluent

valves will be automatically closed.

Approximately 35 percent of the blowdown flow flashes to steam

inside the tank and is vented to the atmosphere.

The

remaining

65 percent, is condensed

in the blowdown tank.

This

condensed

portion is monitored

by radiation monitor RN-23

prior to discharge.

The steam

vented to atmosphere

is

monitored for gross activity by radiation monitor

RN-27.

This

monitoring system takes

a sample

from the steam being vented,

passes it through

a sample cooler to condense

the steam to

water,

and routes

the condensed

sample through the monitor.

Past experience

has revealed that the

RN-27 sample cooler

becomes

air-bound during startup

and when the blowdown flow

rates

are changed.

This problem was documented

on AR's

A0021200

and A0029247 in 1986.

Design

changes

DCP-J-35910

and

36910 were issued in November

1986 to modify the sample lines

and correct this problem.

The modifications were accomplished

in September

1987, but did not correct the problem.

Since

that time, operators

have

been required to verify proper

system flow each

12-hour shift'uring their rounds

and also to

recheck

the system if blowdown flow changes.

Discussions

with operations

management

and the system engineer

for this system revealed that the licensee

was concurrently

pursuing

two plans in an attempt to resolve this problem.

One

proposed

plan would replace

RN-27"and provide

a positive flow

to this monitor as part

a planned

upgrade of the plant

radiation monitoring system.

This project was in the planning

stage

and was listed under the

FY-90 budget

as

Budget Line

Items (BLI) 63

A and

63 B. If approved

and implemented, this

project could be completed in 1992.

The other plan involved

a

proposed

TS change

removing the requirement for RN-27 and

permitting removal of the monitor.

Based

on the above, it appeared

that management

had

been

aware

of this problem for over three years,

but had not taken appro-

priate action to correct the problem.

At the time of the

inspection,

operator

action

was required

each shift to verify

that the monitor .-was operational

Under conditions

and

procedures in effect at that time, RM-27,

a TS-required

component,

could .be inoperable for up to

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br />.

This

indicated

a failure of management

to take appropriate

corrective action

and resolve this

known deficiency,

and was

considered

by the team to constitute

a violation of 10 CFR 50,

Appendix;B, Criterion XVI..

(Enforcement

item 275/90-01-01)

(5)

Calibration Ratios for Measuring

and Test Equipment

(METE)

NCR DC0-87-gA-N001, Measuring

E Test 'Equipment

(MSTE) Calibra-

tion Accuracy Ratios,

was issued in September

1987.

The Tech-

nical

Review Group

{TRG) met initially in October

1987

and then

twice more before

a

new TRG Chairman

was

named

on January

15,

1988.

The Plant Manager requested

a

new direction

on February

10,

1988.

On February 25,

1988,

gA Audit 88804T resulted in

an Instrument

and Controls

( ISC) Stop Work Order.

The next

TRG meeting did not occur until April 30,

1988.

Department

action plans

were not due until February

17, 1989,

and were

submitted

by that date except for the Maintenance

Department,

which did not submit theirs until August 16,

1989.

The

inspector

reviewed the activities associated

with this

NCR and

concluded that the time to develop action plans

was excessive.

The inspector further concluded that, while the action plan

development

time was excessive,

the impact

on nuclear safety

was minimal once the problem was fully understood

in that

ISC

stopped calibrating their own test equipment

and utilized gA-

approved calibration vendors,

including General

Construction,

. until they had completed

the actions

indicated

by this

NCR.

(6)

Surveillance

Procedure

Weaknesses

During a review of five surveillance tests

conducted

on the

Unit

1 safety injection system during the fall 1987 outage,

the inspector

noted the following discrepancies:

After step 8.3.1 of STP.V-4A, Functional Test of ECCS

Check Valises, Revision 3,

per formed on November 14,

1987,

an additional step

was

added directing the operator to

"close 1128,

112C [ ]."

Also, step 8.2.26 of this proce-

dure stated,

"Record flow on FI-9718," and included

acceptance

criteria of greater

than or equal to 3976

GPM.

A measurement

of 2380

GPM was recorded for FI-971B.

A

notation at this step specified that the procedure

was in

error and that the flows of FI-9718 and FI-970B should

be

summed to give the required data for this step.

The

surveillance test result was accepted

based

upon this

notation.

No On-The- Spot

Change

{OTSC) was written.

Step 7.4 of STP.V-SC,

ECCS Hot Leg Check Valve Test,

Revision 2, Performed

on December 4,

1989 stated,

"Verify

10

current calibration of the following plant instruments,"

"

and listed SI Test Line Flow, FI-928A and FI-928B.

These

.

instruments

cannot

be cal'ibrated.

Test engineers

noted

that these instruments

were not calibrated

and continued

with .performance of the procedure.

No OTSC was written.

On step 8:16.25 of STP.V-5C,

ECCS Hot Leg Check Valve

Test, Revision 2, performed

on December 4, 1989,

a

requirement

was handwritten in to "Cap" valve SI-41.

No

OTSC was written.

Step 7.5 of STP.V-5A,

ECCS

Check Valve Leak Test,

Post-Refueling

Maintenance,

Rev. 5, performed

on

December

1,

1989 required that the current calibration of

SI test line flow indicators,

FI-928A and FI-928B,

be

verified.

Although these

instruments

cannot

be

calibrated,

no

OTSC was

made to the procedure

to change

these

requirements.

Technical Specification (TS) 6.8. 1 requires that written pro-

cedures

be implemented including the procedures

recommended

in

Appendix

A of Regulatory

Guide 1.33.

Appendix

A of Regulatory

Guide 1.33, Section B.b, states

that "... procedures

are

required for each surveillance test,

inspection ... listed in

the technical specifications."

TS 6.8.3 specifies

approval

requirements

for temporary

changes

to the procedures

of TS 6.8. 1.

Plant Administrative Procedure,

AP E-454,

Issuance

and

Approval of On-The-Spot

Changes

to Procedures,

Revision

15 (in

effect during this time period), Section 2.1, states, "It is

necessary

tn issue

an On-The-Spot

change

(OTSC) if ...The

procedure

cannot

be followed as written".

The above

examples

constitute

a violation of Technical Specifications 6.8.3.

(Enforcement

Item 275/90-01-02)

Licensee Audits 88831T,

performed September

30 - November

14,

1988; 88833T,

performed

November 21,

1988 - February

17,

1989;

and

SSFAR 89800T,

issued

May 31, 1989,

documented

similar

findings wherein

OTSCs were not issued prior to performance of

surveillance

procedure

changes.

The continuing recurrence of

this problem indicates

a failure by the licensee to take

effective corrective action to address

this concern.

Other items noted during

a review of these

procedures

appeared

to the inspector to indicate

a lack of rigor in procedural

adherence.

These included:

On STP.V-15, 8.4.3.b, neither block LCV112B nor LCV112C

was checked to indicate which valve was closed;

On Step

8.4.14,

"Close

CVCS 8106 and/or HCV-142," nothing

indicates

which was done;

on Step 8.4.6,

"Open or Bypass

HCV-142," nothing indicates

which activity was performed;

.11

%he shift-manager did*not check "yes" or "no", regarding

concurrence

with Step 9.6.a;

and

on Attachment 11.3,

D,

WWST level, no;check

was entered to .indicate which level

indicator"was .used.

On STP.V-4A, Step 9.3.1,

"Are all valves tested. deter-

"

mined to be

OPERABLE?",

a check to indicate-."yes" or "no"

was not made

by the shift foreman.

Other observations

noted during the review of these procedures..

included:

Step 8.4 of STP.V-5C recorded

Psat

as

124.4 psig.

Step

8.7.8, required adjustment of pressure

until it is

,slightly above Psat.

A reading'of

150 psig was recorded

in this step.

The gage accuracy of the indicator used,

PI-942 is +60psi, leaving the actual

pressure

as possibly,.

less

than Psat.

A similar action

was observed

in STP.-

V-5A.

Step 8.10. 1 recorded saturation

pressure

(Psat) at

121 psig.

Step 8.12.4 recorded actual

pressure

P) at

100 psig; since

P was less

than Psat,

no additional.

actions

were required.

Using the +60 psi

gage accuracy

correction,

actual

pressure

could Eave

been greater

than

Psat,

requiring additional

procedure

steps

to be

performed.

Additional information provided to the

inspector

subsequent

to the inspection

showed that this

accuracy

was technically adequate for performance of

these tests,

although the issue indicated insufficient

rigor in the application of instrument error to test

readings.

STP.V-5A and

V-5C contained

steps

which stated "... if a

steam void is suspected,

the line can

be repressurized

from the

RHR System

by opening

8885A or 8885B.

If a

valve is opened to repressurize,

ensure that it is

reclosed".

The procedure

also stated "If the pressure

on

PI-942 is greater

than Psat,

close 8963,

open 8961,

then

carefully throttle open 8963 until pressure

is reduced to

approximately Psat.

Close 8963"

(No guidance

was pro-

vided to reclose

8961).

Each of these

steps

contained

several

valve manipulations

and

a variety of actions

which could lead to operator confusion

and error.

Due to a valve misalignment in November

1989 during perfor-

mance of STP.P-4B,

"Routine Surveillance Test of Containment

Spray Pumps", the licensee

ran

a containment

spray

pump with

the outlet valve closed.

Licensee corrective actions for that

event included changing the plant Engineering Writer's Guide

to include increased

signoffs.

During discussion of the above

findings with the licensee,

management

also recognized

the

inadequacy

in the quality of procedures

and stated that

corrective actions

would be taken.

32

Battery Charger Firing Nodules

To evaluate

the timeliness

and effectiveness

of corrective

actions initiated by the plant and design electrical engineer-

ing staffs for the vital

125V

DC system,

the inspector

reviewed

18 ARs initiated for this system during calendar year

1989.

Except for battery charger problems, this review did

-not identify any significant areas of concern.

The vital

125V

DC systems

at the Diablo .Canyon

Power Plant

(DCPP) Units 152 incorporate

a total of ten Class

1E battery

chargers

(five per, unit).

The chargers

were manufactured

by

.Exide Power Systems

Division (Nodel

UPC, Three

Phase)

and are

approaching

20 years old.

Located within each

charger are six

firing module circuit boards.

Basically, the firing modules

form part of the control circuitry necessary for regulating

and balancing the output current developed

by each of six

associated

solid state, silicon controlled rectifier (SCR)

devices.

Upon an identified failure of a firing module, the plant's

practice for repair of the affected battery charger

has

been

to replace

the affected circuit board

as

an entire unit.

Following replacement,

the failed circuit boards

have

been

discarded.

The licensee

has not performed troubleshooting of

such circuit board failures to the component level.

Action Request

(AR) No. A0161585, dated

September

21,

1989,

was found to have

been initiated by the Plant System Engineer

to document

and track his finding that the battery charger

manufacturer,

Exide, is

no longer producing or stockin9

replacement firing module circuit boards for the type of

chargers

currently in use at

DCPP.

During discussions

with

members of the

PGSE Plant and Design Electrical Engineering

staff, it was learned that the

125V

OC Battery Chargers

are

experiencing

a relatively high rate of firing module circuit

board failures.

In addition, the engineering staff indicated

" that the vast majority of such failures

have

been detected

during the performance of a specific section of preventive

maintenance

tests

which requires

the load current developed

by

each of the six SCRs

be balanced

to within +5%.

At DCPP,

such

testing is performed at approximately

18-month intervals in

accordance

with electrical

maintenance

procedure

NP E-55.2,

Routine Preventive

Naintenance

'Of Station Battery Chargers.

The licensee

was not maintaining

a formal method for tracking

equipment failures at the sub-component

level.

Therefore,

an

accurate

estimate of the firing module failure rate was diffi-

cult to determine.

Consequently,

somewhat differing failure

rate estimates

were reported to the inspection

team.

For

example,

the electrical

design engineering

group leader stated

that

4 card failures

had occurred during the previous

18

months, while a

memo dated

December

12, 1989, from the design

~

'

13

system engineer to the p'1ant system'engineer

indicated

a

failure rate of 4 board failures .every

12 months.

It should be noted that sub-component failure information of

this type is, at best, difficult;to retrieve using the present

Plant Information Management

System

(PINS) configuration.

While the fai lure of a specific piece of equipment (e.g.

battery charger)

would be expected

to generate

a.separate

AR,

that is entered into the

PINS tracking system,.the identifi-

cation of specific sub-component(s)

replaced

during subsequent

corrective maintenance activities

was typically being docu-

mented only on the corrective maintenance

work order(s).

Therefore, finding .the exact

number of failures of a specific

type of sub-component

(such

as the firing modules)

would

require

a manual

review of all corrective maintenance

work

orders written against

each piece of equipment that uses that

sub-component (i.e. the

10 battery chargers).

An estimate of firing module failure rate

was also attempted

through

a review of the Institute of Nuclear

Power Operation

( INPO) Nuclear Plant Reliability Data System

(NPRDS) data

base.

This review, however, did not identify any firing

module circuit board failures reported

by DCPP.

Based

on

discussions

with the licensee's

NPRDS coordinator, it appeared

that the failure of equipment to meet preventive maintenance

test specifications

is classified

by

INPO as

an "incipient"

type of failure.

Since

such failures are typically detected

prior to the occurrence

of an actual

equipment operability

problem, their. reportability under existing

INPO guidelines is

optional.

Corrective actions

taken

by the licensee

to resolve the firing

module failure rate vs. availability concern

include locating

a source for the purchase

of 29 replacement circuit boards

and

evaluating

the feasibility of relaxing the current preventive

maintenance

acceptance

test criteria.

These criteria require

balancing

load current developed

in each leg of the charger

from +5% at 200 Amps (half-load) to +lOX at 300

Amps (3/4

load) . The adjustment of individual ECR load cur rent balance

is currently specified in PGSE electrical

maintenance test

procedure

number

MP E-55.2, Routine Preventive

Maintenance of

Station Battery Chargers.

Step

Number

15 of this procedure

was found to specify

a +5% tolerance in load balance

between

individual

SCRs

and instructed the technician to adjust the

firing modules to obtain the desired values.

The inspector.

reviewed the manufacturer's

instruction book for the Exide

Model

UPC Battery Chargers

(PGSE Instruction Book Number

DC-663344-34-l).

Based

on this review, specific manufacturer-

recommended

tolerance

values for such adjustments

of the

Firing Nodules were not clear.

During a subsequent

interview,

the System Engineer stated that

a plan to revise this test

requirement

to a 'less restrictive test criterion (i.e. 10Ã),

was

based

on his telephone

conversations

with the manufacturer

and is in accordance

with the manufacturer's

recommendations.

0

14

Although such corrective

actions,.may mitigate 'this concern in

the short term, they do not appear to provide,a long-term

solution.

The licensee

had not performed

a root:cause

analysis

to determine

the exact nature'f the. circuit,board

fai lures that have occurred.

Such an;assessment

would provide

valuable troubleshooting

information which may identify

recurring failures of a particular circuit board component.

In addition, since the existing preventive maintenance failure

data

do not indicate

how far out of tolerance the firing

module circuit boards

have

been found during previous

fai lures, it is not clear .that relaxing, the existing testing

criteria would significantly reduce

the observed failure rate.

In addition, it should

be noted that the

29 replacement

boards

have not as yet been

purchased

and that approximately

6 boards

remain in spare stock.

d.

Performance of Safet

Oversi ht Grou

s

The team also assessed

the performance of the various safety

oversight

groups in the licensee's

organization, particularly with

regard to their involvement in the corrective actions

program.

This review included the following oversight groups:

On-Site Review Group

(OSRG)

Plant Staff Review Committee

(PSRC)

Plant guality Assurance

(gA)

Plant guality Control

(gC)

General Office Nuclear Plant Review

8 Advisory Committee

(GONPRAC)

President's

Nuclear Advisory Committee

(PNAC)

Corporate guality Assurance

(Technical Auditing and

Program

Auditing)

Nuclear Operations

Support

(NOS)

Operations

Events

Assessment

(OEA)

Although time limitations did not permit the team to perform an

extensive

review of the performance of each of the above groups,

.

the level of review performed indicated

each of the groups to be

participating effectively in support of the corrective action

program.

An observation

was

made regarding

GONPRAC.

Overall, this was

considered

to be an effective and insightful group with significant

industry experience.

An inspector's

attendance

at one meeting

showed little hesitancy

by the

GONPRAC to probe

and address

~

'

significant issues.

However, regarding their responsibility 'for

audits required

(by the'Technical

Specifications) to be conducted

"under the cognizance" of the'ONPRAC, the Committee's

review was

not extensive.

The review did confirm that audits

were conducted

by gA in the proper scope

and frequency,

but little input was

provided to gA regarding

issues of current industry emphasis

or of

specific concern to the Committee members.

GONPRAC also did not

normally review the resulting audit reports, but,reviewed

those

significant issues

brought'o their attention

by the

gA auditors.

'I

The review of industry experiences,

including

NRC Information

Notices,

by

NOS was found by the

team to be effective.

However, it

'ppeared

to the team that clear responsibility for review and

feedback of DCPP operating experience

was not defined.

Licensee

representatives

stated that Training and other groups

performed

portions of this function.

Licensee

management

stated that this

responsibility would be considered for assignment

to a

new

organizational

group which was still being evaluated

(see followup

item in paragraph 3.e).

Conclusions

Overall, the inspection

team considered

the licensee's

corrective

action program to be functioning with reasonable

effectiveness.

In

view of the records

reviewed

and interviews conducted, it is

noteworthy that

no issues

indicating

a need for corrective action

were identified which had not been entered into the

PINS corrective

action program.

The team also did not identify any problems

or

issues of safety significance which were not corrected

in an appro-

priate

and timely manner.

However,

as discussed

in paragraph

3.c

of this report, several

items of lesser individual significance

were determined to have

been

open for extended

periods,

and it was

not apparent

that the licensee

had addressed

the collective

significance of these

long-standing

issues.

The team was not able

to determine

how many other such

items were still open in the

corrective actions

system.

The team noted that. each organizational

group was responsible for

acting

on action requests

(ARs) assigned

to it (until completed or

reassigned

to another group).

However,

no group or person

appeared

to feel responsibility or "ownership" for managing

the overall

system,

or for shepherding

individual

ARs to completion.

In addi-

tion, trend analyses

performed

by the licensee

showed the total

number of ARs to be increasing with time.

This was partly due to

a

management

policy, considered

a noteworthy strength,

which

encouraged

licensee

personnel

to maintain

a low threshold for the

initiation of ARs.

However, there

was

an apparent

need for someone

to more actively encourage

the closure of ARs.

Management

was

similarly concerned with the number

and average

age of quality

evaluations

(gEs)

and nonconformance

reports

(NCRs).

Plant

management

stated at the end of the team inspection that,

based

on

an assessment

previously in progress,

a

new organizational

group

was being established

to provide oversight of the corrective,

16

actions,

root:cause, <rip reduction,

and other similar programs,

and 'to provide feedback to <he plant staff-on

DCPP operating

experiences.

The licensee'.s

plans in this regard will be evaluated

during future inspections.

(Followup Item 275/90-01-03)

~5R

Selected plant systems

were assigned to members of the inspection

team

for emphasis

during the inspection.

This emphasis

included walkdown of

the system,

examination of corrective actions

and other records associ-

ated with the system,

and interview of the system engineer.

Recent

history or problems

were also reviewed where appropriate.

Inspection

findings on the various systems

reviewed are discussed

below.

a.

Safet

In'ection

S stem

SIS

From a list of outstanding

ARs for the system,

the inspector

selected

35 for a detailed review of the status.

Although some

ARs

appeared

to be untimely in completion,

adequate justification was

documented

regarding

why the items were still open.

The inspector selected

35 closed

ARs and reviewed the closure of

each.

The inspector

concluded that in each

case

proper evaluations

and corrective actions

had

been taken.

The inspector

performed

a walkdown of the SIS for each of the

DCPP

units.

Discrepant conditions,

such

as small leaks evidenced

by

boric acid buildup, were noted;

however, all conditions

observed

by

the inspector

had

been

recorded

on an AR.

The inspector interviewed the SIS system engineer

and judged

him to

be well qualified and knowledgeable

about the system.

The

inspector also reviewed the last two quarterly system reviews

and

noted that they appeared

to be well documented with items of

concern clearly identified.

b.

Auxiliar

Feedwater

AFW

S stem

Approximately 64 ARs were issued for the

AFW system

between July

1

and December

31,

1989.

The inspectors

selected

10 of these for

detailed review, including examination of the identified problem,

its proposed resolution,

and documentation of a guality Evaluation

(gE).

The

gEs normally include the immediate corrective actions,

root cause

analyses,

and corrective actions to preclude repetition.

The problems

were found to be clearly identified, with corrective

actions properly articulated in the documents.

Although no

safety-related

issues

were found to have received

improper or

untimely attention, the inspectors identified two problems of

lesser significance which had required excessive

time for

completion of corrective actions

(see

paragraphs 3.c(l) and (3)).

A walkdown of accessible

portions of the Unit 1

AFW system did not

identify any discrepant

conditions which were not documented

in the

~

'

17

Plant Information Management

System

(PINS) corrective action-data

base.

Numerous

adverse

housekeeping

items were noted,

as discussed

further in paragraph

7.

Discussions

with the system engineer

showed

him to be familiar with the

AFW system

and knowledgeable

of

its performance history.

The 'i~spectors

reviewed the results of the recently concluded

,Safety System Functional Audit and Review (SSFAR), report 89808T,

issued

November

17, 1989.

This

PGSE internal audit assessed

the

operational

readiness

of 'the

AFM system

and its associated

components.

The inspectors

noted that, although the audit was

performed

under the auspices

of the guality Assurance

Manager,

staffing of the audit team relied heavily on contractor support.

Licensee

management

noted that this

had

been

done in order to

provide the technical

background

needed

by the audit team.

The

inspectors

acknowledged this objective, noting that the licensee

should also provide sufficient involvement of PGSE employees

in the

audit and in the resolution of identified corrective actions to

ensure that substantial

corporate

memory from the effort remains

with the

PGSE staff.

Licensee

management

agreed with this concern

and stated that it was being considered

in the staffing of audits.

The

SSFAR identified 21 concerns

and

17 recommendations

requiring

followup.

These

were grouped

as

6 Nonconformance

Reports

(NCRs),

15 gE-AFRs (audit finding reports),

and

17 ARs.

The inspectors

verified that each of the concerns

and recommendations

identified

in the report

had

been properly tracked to an

NCP gE-AFR or AR.

The

SSFAR report established

target dates for staff responses

to

gE-AFRs

and ARs.

These target dates

allowed 30 days for a gE-AFR

and 45 days for an AR.

The inspectors

noted that in most cases

the

response

goals established

by gA had

been met; however, in about

one-third of the cases it appeared

that

a response

had yet been

made.

Licensee

gA representatives

stated that followup on these

issues

was in progress.

A representative

of Technical Auditing, in a telephone

interview,

stated that management

recognized

a slippage

in timely responses

to

the action items

and was taking steps

to address

the matter.

Effective February 5, 1990,

a two-man team

was to conduct followup

on action items

and ensure that corrective actions

were properly

handled.

The

SSFAR team leader

was to lead the followup team.

As

part of management's

incentive goals for 1990, the team would be

responsible for a detailed review of each

item and would complete

the process

by May 1990.

Additionally, periodic memoranda

would be

issued to management

covering the status of corrective actions

and

highlighting areas

in need of management

attention to ensure

the

completion of timely action.

Emer enc

Diesel

Generators

The emergency diesel

generating

(EDG) system

(System

21) was

inspected for the timeliness

and effectiveness

of corrective

~

'

18

.actions necessary

to maintain <he five emergency

diesel

generatino'units

at .Diablo Canyon in reliable operating condition.

This wa~

.achieved

by examining

a wide variety of records

and documents,

including 40 action requests,

17 maintenance

history records,

8 surveillance Nests,

.6 nonconformance

reports,

12 work orders,

2 .-

,design

change

packages,

11 system procedures

(operating,

mainten-

ance, etc.),

2 system status

reports,

and various piping and

instrument drawings (flow diagrams).

These

documents

applied to

-the engine

and generator,

as well as the fuel oil storage

and'ransfer

systems.

The recurring records

reviewed, in most cases,

were those

generated

during the past six to seven months.

The

system

was also discussed

and reviewed with the staff members

who

are directly involved with the system,

including the system

engineer,

design

system engineer,

plant engineer,

and plant

operators.

System

21 was also discussed

and reviewed with the

guality Support Manager,

Onsite guality Audit Supervisor,

Acting

guality Control Supervisor,

and various other staff members.

The

EDG system consists of five 2600

KW diesel

generating units.

Two are installed per Unit, with the fifth unit installed

as

a

"swing" unit, available to either Unit

1 or Unit 2.

Three of the

EDG units are located in the reactor plant Unit

1 area of the

turbine building, and two are located in the Unit 2 area of the

turbine building.

A sixth (new) diesel

generator of the

same

capacity is schedule

to be installed in Unit 2 area of the turbine

building during 1992.

This modification will provide three

dedicated

EDGs each for Units

1 and 2, eliminating the

need for a

swing

EOG unit.

The five emergency diesel

generator units were inspected

in the

field several

times during the inspection period to follow up on

corrective maintenance

work and surveillance in progress

during

this period.

The two redundant fuel oil storage

and transfer

systems

were also walked

down to confirm modifications completed

on

the systems

during the inspection period.

Several

housekeeping

problems

were noted during these

walkdowns of the

EOG system,

as

discussed

in paragraph

7 of this report.

A modification made to each of the redundant fuel oil storage

and

transfer

systems

was completed during this inspection period.

This

modification consisted of installing

a pressure

control valve

(PCV)

in the fuel oil transfer

pump bypass line (piping).

The

PCV

operates

to prevent the transfer

pump from cycling on and off to

replenish

the five EDG fuel oil day tanks

when all

EDG units are in

service during and following an accident.

Continuous operation of

the transfer

pumps is considered

a safer

mode of operation than-

frequently cycling the transfer

pump on and off as the level

controls for each

day tank call for for the addition of fuel.

However, in making the modification, two valves were relocated in a

manner which inhibits the transfer of diesel fuel oil between

storage

tanks without compromising the intended separation

of the

two storage

and transfer systems.

The transfer of fuel oil between

19

storage tanks is

a monthly operation,

required under Surveillance

Test Procedure

(STP) N-25A, Leak Rate Test for Underground

Fuel

Oi1

storage

Tanks.

Procedure

N-25A was in the process of being revised

.during the inspection period to accomp1ish

the transfer using

a

.portable .pump.

A review of the processing

of the 'DCP for this'modification

revealed that Operations

was not afforded sufficient time to review

the design pursuant to procedure 3.6, Operating Nuclear

Power 'Plant

Design

Changes,

prior to the advance

design coordination meeting.

Operations indicated that,

had they been given sufficient time to

review the initial design for the modification, they would have

identified the prospective inability to transfer fuel oil between

storage tanks

(using the installed transfer

pumps)

as

an Operations

concern.

This was identified as

a licensee failure to fully follow

the established

procedure 3.6,

and constituted

a violation of

'0

CFR 50, Appendix 8, Criterion V.

Before completion of the

inspection, the vmspector

determined that the licensee

had

recognized this concernand taken appropriate corrective actions.

Consistent with the

NRC Enfoncement Policy,

1D CFR 2, Appendix Z,

this item was sot included in the Notic~ of Violation Mich

accompanies

this inspection repoM.

(Non-cited violation

275/90-01-04)

Generally, it was concluded

from the inspection of the

EDG system

that corrective actions

had been properly initiated where appro-

priate,

and that the timeliness

and effectiveness

of corrective

actions for the system were adequate.

It also appeared

that

licensee

personnel

were familiar with and were effectively using

the PINS and

AR systems

to initiate cormctive action on identified

problems

and deficiencies.

Vital 125V

DC S

tern

(1)

Backgr ound

The vital DC system provides continuous

power to such loads

as

circuiX4reaker control

and protection, diesel engine

generator control and ln otection, reactor coolant system

control valves, annunciators

and 9G-to-AC voltage inverters

for nuclear instrumentation.

At Diab1o Canyon',

redundant, safety-related

{Class ZE) loads

are supplied from three physically separate and electrically

independent

125V

DC switchgear

buses for each unit. Each of.

.the three

125V

DC switchgear buses is supplied power from a

dedicated battery and

a dedicated battery charger.

In

addition,

one backup battery charger is shared

between

two

125V,DC buses

and

a dedicated

backup battery charger is

provided for the third 125V DC bus (i.e., UniM 2 and

2 each

have five battery chargera).

(2)

(3)

Corrective Actions'Related

To The Vital 125V DC'ystem

e

The assessment

of corrective action activities associated

~with

the vital 125V

DC system concentrated

on a review of selected

problem tracking 'documents,

which included Action Requests

(ARs), guality Evaluation - Audit Finding Reports

(gE-AFRs),

and Corrective llaintenance

Work Orders

(CM WOs)'that were

initiated during calendar year

1989.

In addition, interviews

were conducted with p'lant and design engineering staff members

involved in the evaluation

and resolution of problems

asso-

ciated with this system.

Except for the fo'llowing issues that

are discussed

in detail in other sections

of this report,

these

reviews did not identify any significant areas

of

concern with the licensee's

corrective action program.

Battery charger firing module failure rate vs.-

replacement availability concern

(Paragraph

3.c(7))

Training of Design System Engineers

(Paragraph

5)

Housekeeping

deficiencies

observed

during the system

walkdown (paragraph

7)

System

Ralkdown

On Wednesday,

January

31,

1990 the inspector participated

in a

walkdown of the

DCPP Unit

1 and

2 vital 125Y

DC system

and the

4160V switchgear.

Licensee

representatives

present

during the

walkdown included the Plant

and Design System Engineers for

the

125V

DC system,

the Electrical Maintenance

Engineer,

and

the Nuclear Engineering

and Construction

Services

(NECS)

Electrical Engineering

Design

Group Leader.

Overall, the systems

appeared

to be well maintained with no

obvious signs of material

degradation

or poor quality repairs.

The inspector

performed

a visual inspection of the internal

areas of a selected vital 125V

DC battery charger

and

a 4160

switchgear circuit breaker cabinet.

This visual inspection

did not identify any issues of concern.

The cabinet internal

areas

were free of debris,

and electrical

connections

and the

physical configuration of components

appeared

to be

acceptable.

e.

480/4160V

AC

S stems

Background

The 480 and 4160 Volt AC systems

have presented

the licensee

with few difficulties during the past few years.

Since these

systems

were not included in the system engineering

program

when it was initially instituted, there

was

no formal site

System Engineer,

and there

had

been

no joint walkdowns with

the Site and Design System Engineers,

and no quarterly system

reports.

A station electrical

maintenance

engineer

was acting

~

'

21

(2)

(3)

f.

Com

as the site System Engineer for these

systems

(as discussed

.ir,

paragraph

5, the corporate

Design System

Engineer

was not

aware of .this when he was. interviewed

by the inspector).

Corrective Actions Related to the 480/4160;VAC Systems

A detailed review of approximately

50% of all the

94 gEs, on

PINS and approximately

20K of the 256 ARs issued

during .1989

revealed

no unusual

concerns,

no chronic problems,

and

no

indications of corrective actions

which had not received

appropriate

levels of attention.

The inspector

noted that that switchgear associated

with a

given piping system were usually entered into PINS under the

system

number of the piping system rather than under the

system

number for the switchgear.

While many examples of this

were noted, there were

some exceptions

which indicated

some

inconsistency

in this area.

The inspector

had

no additional

concerns

with the 480/4160

VAC systems

beyond those described

under

system walkdown.

System

Walkdown

A walkdown conducted

on January

31,

1990 revealed

systems

which appeared

to be operable

and in good physical condition.

However,

two adverse

conditions

were noted.

One was the

absence

of relay calibration cards in Unit 2 for the 4160

VAC

"F" Bus, for two overcurrent relays for safety injection

pump

circuit breaker ¹21,

and for auxiliary salt water

pump circuit

breaker ¹21.

A second

adverse

condition was

a Unit 2

4160

VAC "G" Bus differential relay which had not been cali-

brated since July 21,

1983.

These conditions

were being

addressed

by cognizant personnel,'nd

calibration of the "G"

Bus relay was scheduled for the

1990 refueling outage.

A number of housekeeping

deficiencies

were noted in these

rooms, including two which had the potential to impact

operability.

One was

a beverage

can

on top of a 480

VAC

transformer;

the second

was

a missing section of fire barrier

foam between

the Unit 2 4160

VAC "H" and

"G" cable spreading

rooms.

This reduction in foam thickness

might have permitted

a fire in the "H" room to spread to the "G" room under certain

circumstances.

These

concerns

are discussed

further in

paragraph

7 of this report.

ressed Air S stem

Background

and History

The compressed air system at the Diablo Canyon

Power Plant

(DCPP)

was designed

and installed

as

a shared

system for units

1 and 2, and provides the service

and instrument air for both

units.

Air enters

the system through

a filter on the air

compressor

The compressed air passes

through

an aftercooler,

22

where the heat of compression is removed,"then through a.

pre-filter and the air dryer before it is stored inChe

,receiver Vor system

use.

Afterfilters further clean the air

before delivery to the various .systems

requiring

compressed'ir.

The compressed

air system at

DCPP is non-safety grade,-

as is the case for most U.S. plants;

however, it does

serve-

a

function of mitigating complications of plant .transients

and

~

challenges

to safety systems. ".

Operating experience

with the compressed air system

has

been

marred

by numerous

and persistent

operating

problems,

including the following:

System underdesign for all of the plant's air needs

r

System contamination consisting of grit, rust, scale

and

water intrusion

(2)

Numerous air system leaks that contribute to the system's

volume requirements

Component failures, including compressors,

dryers,

valves, regulators,

and instrumentation.

A contributor to the compressed air system

problems

was the

inadequacy of preventive maintenance.

Corrective actions

Inspector guidance for the air systems

portion of the

inspection

was provided

by Operating

Experience

Feedback

Report,

NUREG-1275;

NRC Information Notice 87-'8; the Region

V

maintenance

team inspection

conducted

on July ll - 22,

1988

(Report 0275/88-15

5 323/88-14);

and the licensee

responses

to

the enforcement

items identified in that inspection report.

Over the past several

years,

in response

to the numerous

operational

problems involving the compressed air system,

the

licensee

has

embarked

on

a major upgrading of the system.

Changes

to the system,

including those in place, currently

being installed,

and future enhancements,

were reviewed

and

evaluated

by the inspection

team.

As part of the evaluation,

the piping and instrument drawings

(PSIDs) were reviewed,

along with applicable

design

change notices

(DCN's)

and

actions

requests

(AR's).

Replacement

of air cooled rotary compressors,

nos.

5 and 6,

with new water cooled rotary type compressors

(DCP-J-43374)

was in process

at the time of the inspection.

The root cause

of the high maintenance

and operational

problems for the

original air compressors

was identified as

a higher ambient

operating temperature

than that for which the units were

designed.

The replacement

water cooled compressors

were

on

~

'

23

site at the time of the inspection,

but had not been

installed.

Installation work was being performed

on one

100

percent'apacity

cooling water booster

pump, capable'of serving both

compressors.

A backup cooling water pump, also being

installed, will auto-start if the operating

pump. trips .from

power failure.

A solenoid-operated

auto bypass is provided

around

each

compressor

to assure

minimum pump cooling water

flow.

The plant fire water system

serves

as

an additional

backup

source of cooling water should the service cooling

water system fail.

The two compressors,

currently powered from a unit

1 non-vital

480V bus, will be powered from different unit busses,

along

'ith

the

new cooling water pumps.

The rebuilding of the compressed air system also includes

installation of a new larger capacity air dryer unit along

with resized

pre- and afterfilters

ahead of the receivers.

An ongoing major cleanup of the instrument air system

was in

progress

at the time of the inspection to free it of sand,

rust, pipe scale,

and water found in the system during 1988.

This was expected

to be completed during the next refueling

outage of unit 2 (spring of 1990).

The instrument air system

was being supplied with air by a

temporary air compressor

located in the yard on the west side

of the turbine building.

The plant's rotary air compressors

Nos.

05 and 06 were aligned to supplement

the instrument air

system if demand

should

exceed

the capacity of the temporary

air compressor.

The four installed reciprocating air compres-

sors

were aligned

as

a third source of instrument air if

needed.

The licensee's

plans,

pursuant to AR A0150078

and design

change

DCP-J-43374,

to replace

the presently installed air

cooled compressors

with modern water-cooled

compressors will

be accomplished

in phases,

since the air system is always

required

when either or both nuclear units are in operation.

The anticipated

completion date for the replacement of

compressors

05 and 06 is early 1991.

Procedural

changes

have

been

implemented for system operating

procedure

OPK-1, Compressed Air System,

Revision 4.

The

changes

were

needed to meet the

demands

of the air system

under the temporary configuration necessary

to accomplish

the

installation of the

new compressors.

Air system leaks at

DCPP have

been

a problem,

and

seem to be

more prevalent

than in other U.S. plants.

A number of action

requests

{ARs) from the second six months of 1989, involving

24

"

C

compressed air system leaks,

were .reviewed

and, discussed. with

the system engineer

and the system design engineer.

Implemer>-

tation of corrective action specified

on these

AR's was found

to be timely except for leaks requiring repair during

a 'system

outage..

The system engineer for, the compressed air system

was

unable to verify'whether the plant

had

a program:to evaluate

the various root causes

of compressed air system',.leaks

and

implement corrective action in appropriate

cases.

The

APs

reviewed did not request

a quality evaluation

(gE) be

performed.

The compressed air system

has experienced

problems with two of

its monitoring instruments,.the

air flow meter

and the

moisture analyzer.

ARs have

been written for each instrument;

however,

progress

has

been slow in resolution of the problems.

In discussions

with the systems, engineer,

he indicated that

final resolution of system

problems is often sought prior to

testing of the complete

system.

Based

on review of the proposed

and completed modifications to

the compressed

air systems

at

DCPP, including walkdowns

.of

selected

portions of the system

and interviews with the system

engineers,

the inspection,team's

conclusion

was that the

licensee

has

taken appropriate

measures

to enhance

the

reliability and maintainability of the system.

The team's

review included interviews

and discussions

with the system

engineer

and the system design engineer

assigned

to the

compressed air system.

Both engineers

were found to be

aggressively

following system operation

and modifications,

and

they were found to be technically competent

in their areas

of

responsibility.

5.

S stem

En ineer

Pro

ram

PGSE issued letter No. DCL-89-206, dated August 4,

1989 in response

to

NRC Enforcement Action No. 89-85.

As part of the actions

accomplished

by the licensee

in response

to the

NRC concerns

which prompted the

enforcement letter, the licensee's

response

discussed

implementation of

a plant System Engineer

(SE) Program,

increased

involvement of Nuclear

Engineering

and Construction Services

(NECS) engineers

in plant

operations,

and actions to strengthen

the interface

between

NECS System

Design Engineers

(SDEs)

and the plant staff.

Specific reference

was

made to "... the emphasis

placed

on coordination of design

and

operations activities between

the plant System Engineers

and

NECS System

Design Engineers."

One of the inspection

team's objectives during this inspection

w'as to

assess

the effectiveness

of the

SE and

DSE programs

and their working

relationships.

This was accomplished

through interviews, review of

governing procedures,

examination of quarterly system status

reports,

and interface with SEs

and (in some cases)

DSEs

as part of the system

reviews discussed

in paragraph

4.

~

'

25

The team's

observations

and findings regarding the System

Engimeer

and

Design System Engineer

proarams

are discussed

in the following

paragraphs.

A

'

a.

Plant

S stem

En ineers

The plant System

Engineer'-Program

was defined in 'Administrative

Procedure

(AP) A-350, System Engineering

Program, Revision 1.

This

procedure

appeared

to have

been generally effective in establishing

the program, but provided insufficient guidance

in some areas.

For

example:

Vhile minimum initial quali'fications were established for

assignment

of an individual as System Engineer,

no specific

training requirements

were identified as prerequisite to

assignment.

AP A-350 indicated...that

"the concept of

on-the-job training is the core of the qualification and

training program."

The

AP also stated that within two years

of initial assignment,

the System

Engineer

should

be assigned

to participate

in the Technical Staff Training Program.

Successful

completion of this program

was stated to be

a

prerequisite

to continued

assignment

as

a System Engineer.

Paragraph

4. 1.10 of AP A-350 stated that the System Engineer

"... should provide

a Readiness

For Restart Evaluation for

his/her system

when requested

or following significant outages

However, the

AP did not indicate

how or to whom this

report should

be provided.

Requests

for documentation

(e.g.,

compressed air system)

and discussions

with System Engineers

indicated that this was not routinely accomplished.

During

discussion

of this question,

Technical

Services

management

stated that System Engineers

do not report accomplishment of

this task to anyone -- they just do it.

Nuclear Plant Administrative Procedure

C-26, Root Cause

Analysis, Revision

0 (in Step 5.2.1) stated that the System

Engineer should perform an investigation of events for root

cause.

AP A-350 did not indicate this or state that the

System Engineer would be assigned

to the root cause investi-

gating team.

However, discussion with System Engineers

indicated that they have actively participated in the

investigation of events

and problems associated

with their

assigned

systems.

AP A-350 did not provide sufficient guidance

on the conduct

'nd

documentation of quarterly system walkdowns; e.g.,

the

type of information which should

be included in the quarterly

reports.

As

a result,

some of the quarterly system status

reports

were more complete

than others,

and

some did not

appear

to provide

a complete

and accurate

status of the

system.

For example,

the compressed air system 3rd and 4th

quarter reports did not provide estimates

of when requested

~

'

.work. on design

changes. would 'be accomplished

on the .system.

'They did not address

specific";problems

or delays in getting

Casks

accomplished

that may need -management;assistance

or

attention.

The trending

and recommendations. section of this

report only, stated that system performance

was improving and

.provided ~o basis for'this solution.

The report did not

,provide

a status of design

changes

or modifications in

progress.

The

AP stated that System Engineers

should

do trending of

system

performance,

but-gave little guidance

on what informa-

tion should

be trended,

or how.

Plant management

stated

during discussion of the above

issues

that

a revision to AP A-350 was planned to address

the inspector's

observations

and to incorporate other improvements

based

upon

experience

to date with the System Engineering

Program.

Interviews

and interface with the plant System Engineers

during the

course of the inspection

indicated that most were well qualified,

knowledgeable,

and actively involved in issues

dealing with their

assigned

systems.

Staffing weaknesses still existed in some areas

for example,

the 480/4160

VAC systems

did not have

a System

Engineer assigned,

although

an electrical

maintenance

engineer

was

fulfillingthis function very effectively.

Some

20 System

Engineers

had completed

the 20-week Technical Staff Training

Program, with six to eight more scheduled

to participate in the

next course to be given this year.

This course

includes

approximately

10 weeks

devoted to study of various plant systems,

and also includes

80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />

on the plant simulator.

The plant systems

engineering

supervisor

was developing

an intro-

ductory training curriculum for new persons

coming into the systems

engineering

program.

This was expected to be completed

by the end

of the second quarter of 1990.

He was also developing qualifica-

tion standards

for each

System Engineer assignment

which were

expected to be completed

by mid-summer

1990.

Initially, when

PGSE

changed

to the System Engineer

program from the surveillance test

(ST) engineer

program,

the test engineers

stayed with the system

they had under the

ST engineer

program.

At the time of this

changeover,

only one

new person

was brought into the System

Engineer

program.

He came from the general office design group.

He had completed the training program which included plant systems

and time on the simulator;

and

he was given on-the-job training for

his system

by his supervisor.

Consequently,

no introductory

program

was provided at that time.

Overall, the team concluded that the System Engineering

Program

was

working reasonably

well at Diablo Canyon,

and was making positive

contributions to improved interface with NECS.

System Engineers

with whom the team interfaced

were generally well qualified.

Some

weaknesses

were noted in the program,

as discussed

above.

~

'

27

Desi

n S stem 'En ineers

~ ~

The 'NECS Design 'Design .Emgineer

program

was addressed

in Engineer-

ing:Procedure'No.

3.14, 'PGIIE System Engineer

Program.

This

provided for a Design System Engineer to be assigned

to principal

plant systems.'ections

3.4 and 4.3 of this procedure,

along with

DCPP

AP A-350., provided for the plant System Engineer

and the

Design 'System.-Engineer

Co jointly conduct the quarterly system

walkdown and prepare the quarterly System Status

Report which is to

be submitted to the

DCPP Plant Manager.

These

references

also

indicated that the System Engineer

and Design System Engineer are

to consult

as necessary

on issues

involving their assigned

systems.

The team's

review of the Design

System Engineer program, including

interviews

and discussions

with several

persons

involved, indicated

that it was not as fully implemented

as the plant System

Engi'neer

program.

Strengths

were noted in some

areas -- the Design

System

Engineer for the compressed air system, for example,

was very

involved with his System Engineer counterpart in planning signifi-

cant modifications to the plant's

compressed

air system.

Evidence

was observed of meaningful

involvement by Design System

Engineers

in many of the quarterly system walkdowns

and in other issues.

On

the other hand,

weaknesses

in the program were observed

as follows:

As with the plant System Engineers,

specific training require-

ments for Design System Engineers

had not been established.

One electrical

Design System

Engineer

who had

been assigned

for about two months,

although experienced

in the electrical

engineering discipline with PGIIE, had

no prior nuclear

experience.

During an interview,

he stated that

he

had not

received

any training specifically related to his system,

and

was not aware of any training planned for the near future.

He

also stated that while he had met with his plant System

Engineer counterpart,

they had not performed

a joint walkdown

of their assigned

system or formally discussed

the status of

current issues.

This electrical

Design System

Engineer

had

been assigned

for only about

two months,

and

had difficultywalking the

inspector through

a one-line diagram of his system.

Based

on

the inspector's

review of the System Status

Report prepared

for the fourth quarter of 1989, which had

a cover sheet

showing the Design System Engineer's

name, it appeared

that

the Design

System Engineer for this system

had participated

in

the system walkdown and contributed to the report.

During

'iscussions

with the Design System Engineer

(DSE) at the time

of the inspection,

however, it was learned that the

DSE had,

in fact, not participated in the system walkdown or contri-

buted to the report.

The

DSE stated that the cover sheet of

the report was signed for him by the System Engineer without

his specific knowledge or instruction.

During followup dis-

cussions,

the plant System Engineer stated that his signing of

the quarterly cover sheet for the

DSE was

an oversight

on his

part -- in that

he had

been previously responsible for prepar-

0'

'

28

'i~g the quarterly status report, since

a Design System'Engineer

had onlv recently

been assigned.

Some

'NECS design engineering 'groups

used contract engineers

'or

a significant portion of %heir Design System Engineers.

-This was"notably true Sor the electrical distribution group,

although

some of the 'contract engineers

had

been working with

PGIWE for .several

years..

A weakness

noted

was that one contract

engineer

assigned

as

an electrical

DSE did not

know who his

plant SE:counterpart

was.

The licensee

stated that the use of

contract .personnel

was necessary

to staff the group with

qualified engineers

in the time frames established.

The team

noted that for the long term, however,

management

must

consider the balance of contract

and

PGIIE staff personnel

which will give the flexibility needed while ensuring that

corporate

knowledge about important plant systems

is retained.

A check of ten engineers

assigned

to one electrical engineer-

ing group indicated that five did not have

a site badge,

and

that only one. was

badged for protected

area entry.

The

'icensee

noted that badging for some others in this group was

in progress.

Other observations

indicated

a need for some

Design System

Engineers

to work more closely with their System Engineer

counterparts.

For example,

one electrical

DSE did not

know

that

a maintenance

engineer

was acting

as plant System

Engineer for his system.

One

DSE Group Leader also indicated

that

he did not get

a copy of quarterly system status

reports,

although Engineering

procedure

3.14 indicates that

he should

receive

and review

a copy.

c.

Conclusions

Overall, the System'ngineer

and Design

System Engineer

programs

appeared

to have

been established.

The Design

System Engineer

program

was not as fully implemented

as the System Engineer

program.

Both programs

showed

room for additional

improvement in

program definition, establishment

of training,

and the effective-

ness of the interface

between

them.

6.

En ineerin

Activities

A brief review of engineering activities was conducted

to ascertain

the

staffing and workload experienced

by the Nuclear Engineering

and

Con-

struction Services

(NECS) engineering staff.

The organization

had about

1250 open engineering

work items, with the backlog appearing

to be

growing slowly.

NECS management

planning estimates

indicated

a total of

approximately 973,000 engineering

and drafting work-hours, including

design basis

data

update activities.

This estimate

also included all

capital

improvements

authorized for 1990 and

1991 (representing

about

25K of the total), plus existing Operations

and Maintenance

(08M)

engin'eering

support work.

This represented

approximately

one and

one

quarter years of engineering effort for the approximately

400 engineers

20

"

{PGSE and .contractor)

who compr'ise the corporate engineering staff

.available to work on

DCPP,.

NECS management

considered

the engineering

workload <o be under control,

and appeared to have

an effective priori-

tization system.

The team noted that the level of DIEM work appeared to

be growing.slowly, however.

The licensee

was

aware of this

and appeared

committed,to ensuring that the

08M growth remains controlled.

'No violations or deviations

were identified.

7. ~kk

Plant conditions

and material/equipment

storage

were assessed

during the

inspection to determine the general

state of cleanliness

and housekeep-

ing.

During plant tours, inspectors

were alert for debris, potential

hazards, oil and water leakage,

and equipment conditions; e.g.,

bearing

oil levels,

and the configuration

and cleanliness

of electrical

connections.

'During wa1kdowns of selected

areas

in the plant by the various

team

inspectors

the following housekeeping

discrepancies

were identified:

Damaged fire barrier seal

in 4KV vital cable spreading

room (on.

north wall, separating

rooms

"G" and "H").

A piece of foam fire

barrier material

6" x 2" x 1" deep

was missing

on the

H side of the

fire stop, with an ear plug container stuffed into the opening;

on

the

G side,

a cigarette butt (apparently snuffed out in the fire

stop material)

was protruding from the fire stop.

Debris in the bottom of panel

1PM247 (by Unit

1 oil-water separator

room,

85 foot level)

Beverage

can

on top of transformer

"G" and plastic water cup on

floor, Unit

1 480V switchgear

room "G"

Cigarette butt in safety

panel

RNPIC,

Rack No. 3; Unit 2, cable

spreading

room

Masking tape

and cardboard

tag in Unit 2 remote

shutdown

panel

White plastic bottles

and debris

on floor at 85-foot level, Unit 2

containment penetration

area

Black duct tape

and miscellaneous

debris (bolts/nuts)

on floor at

100-foot level, Unit

1 near auxiliary feedwater

(AFW

valves, north

side of containment

Tools,,parts,

and other debris in instrument cabinets Panels

1-PM-82, 2-PM-72, air compressor

control

panel

PM-150 (also

had

broken handle)

Oil and grease

under air compressors

5 and

6

Portable vent fan, air sampler,

and extension

cords (not is use)

near

AFW .valves

on 100 foot level

~

a

30

Buildup. of boric acid crystals

noted in various locations

(packing

on safety injection (5I) pumps

1-1 and 1-2 and several

valves in

penetration

area)

Diesel

Generator

(DG) rooms looked poor during the week of January

8, and the inspector informed the Plant

and System Engineers.

The,

rooms were not cleaned

up until the inspector again

commented to

the System Engineer during the week of January

22

Cardboard cartons, etc., stored

on top of computer,

Unit 1 Plant

Computer

Room

The team concluded that housekeeping

was generally poor, considering

that both units

had

been operating routinely since completion of the

Unit I refueling outage

about

two months earlier.

The examples

above

demonstrated

a failure by the licensee

to meet the requirements

of

established

housekeeping

procedures

and were considered

to be

an

apparent violation of 10 CFR Part 50, Appendix B.

(Enforcement

Item

273/90-01-05)

Emer enc

Li htin

62705,

64704

The plant's

emergency lighting was

examined to assess

its availability

for necessary

response

to emergency conditions.

The emergency lighting

consists of three

systems:

DC emergency lighting, AC emergency light-

ing, and battery operated lights (BOLs).

The

DC emergency lighting is

supplied at

125V from the non-vital station batteries.

It is located

principally in electrical

equipment

rooms, stairways, exits

and

entrances,

corridors,

passageways,

and at lower levels in all other

areas.

The

AC emergency lighting is supplied from two of the three vital 480V

buses

through dry type, single-phase

transformers,

and is limited to 100

KW of power.

It is located throughout the plant to provide minimum

lighting.

Emergency battery operated lights are provided in engineered

safety feature

(ESF) equipment

areas

and various

access

routes thereto.

This lighting system consists of individual battery

power pack lights

capable of providing eight hours of illumination if normal

DC emergency

and

AC emergency lighting is lost.

The battery

power

pack built-in

charger maintains

a continuous

charge

on the battery.

The

AC emergency lighting circuits are routed in separate

conduits

from

the normal

AC lighting on the secondary

transformer sides to panels

and

fixtures.

On the primary side, the

AC power from the vital 480V buses

is run in separate

conduits or in respective vital routes.

The

DC

circuits are in separate

conduits in vital operating

areas of the plant.

The lighting fixture supports for the three

emergency lighting systems

are installed to seismic requirements.

After the diesel

generators

start

and the single-phase

AC emergency

transformers

receive

power, the

DC emergency lights are automatically

turned off.

The average

period of operation of the

DC lights is

15

seconds.

31

'A walkdown of selected

areas

was made to evaluate

%he coverage 'of

emergency lighting in those

areas

required for remote shutdown'of the

Units.

The walkdown started at the control

room and 'proceeded "to the

access

-route

(main stairway

No.

1) to the following remote

shutdown

areas:

battery switchgear

rooms,

4160Y switchgear

rooms,

480V

switchgear areas,

remote

shutdown

panel

areas,

and emergency

diesel

'enerator

rooms.

The three plant emergency lighting 'systems

described

.

above were found in all of these areas.

The

DC emergency lighting:

fixtures were identified with a yellow circular label while the

AC

emergency lighting fixtures were identified with a red circular label.

The battery operated lights were readily recognizable.

It was concluded

that the em'ergency lighting coverage

in those

areas

surveyed

was

adequate.

'To evaluate

the licensee's

testing

and ma'intenance

programs for the

three

emergency lighting systems,

the inspector

examined.,the

following

surveillance test

and preventive maintenance

procedures:

STP M-17Bl, Functional Test of Emergency

DC Lighting System (six months

frequency).

STP N-1782, Functional Test of Emergency

DC Lighting System Inside

Containment'during

outage).

STP M-17C1, Functional Test of the Emergency Battery Operated Lighting

(BOL) System (six months frequency).

STP M-17C2, Discharge Test of the Emergency Battery Operating Lighting

(BOL) System (twelve months frequency).

STP H-17C3,

Check of the

Emergency

AC Lighting System for Safe

Shutdown

Route Il'lumination (six months frequency).

HP E-55.5, Maintenance of Battery Pack

Emergency Lights (two months

frequency).

AP C-81, Standard

Plant Prior ity Assignment

Scheme.

The inspector

assessed

the thoroughness

of the above surveillance tests

and preventive maintenance

tasks

and the frequency at which they were

being performed.

This was

done by reviewing the computer readout list-

ing the dates

when the

STPs

and

PN tasks

were accomplished

during the

past

two to three years.

Fifteen work orders

under which the above

listed surveillance tests

and preventive maintenance

task were performed

were reviewed.

The inspector concluded that the timeliness

and

thoroughness

of the surveillance tests

and preventive maintenance

tasks

were acceptable.

The inspector

evaluated

the corrective maintenance

(CM) program for

repairing

and returning to service battery operated lighting units by

examining

a sample of twenty action requests

(ARs) which initiated

corrective maintenance for BOLs.

Many of the

ARs resulted

from the

performance of STP M-17C1.

The priorities assigned for completing the

~

'

32

'

work appeared

to conform to administrative procedures

C-81.

Priorities

1 and

2 are normally assigned

to corrective maintenance

for BOLs

required for safe shutdown of %he plant.

These corrective maintenance

jobs were usually completed

in 48 to 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

In those

instances

where

maintenance

could not

be performed within,a,reasonable

time, the

BOL was

usually changed

out with a spare

BOL from the warehouse until the

maintenance

was completed.

The corrective maintenance

program for BOLs

appeared

to function as prescribed with the

CH work .orders. being

accomplished

in a timely manner.

The inspector also examined three

ARs which dealt with FSAR reviews

related to Appendix

R emergency lighting.

Based

on the facts that the

emergency lighting systems

at the Diablo Canyon .Plant are well

distributed throughout the plant, overlap

one another,

are periodically

tested

on

a regular bases,

and are maintained in a good operating

condition; it was concluded that the systems

were adequate

to ensure

safe

shutdown of the Units from outside the control

room in the event of

a station blackout.

9.

~Ei

N

On February 2, 1990, the team met with senior licensee

management

(identified in paragraph

1) and other licensee

representatives

(identified in Attachment

A) to discuss

the scope

and findings of the

team inspection which reviewed the corrective actions

program at the

Diablo Canyon plant.

Issues

identified during the inspection

were

discussed

in detail.

During the exit meeting,

licensee

management

representatives

made the following remarks in response

to certain of

the items discussed:

Regarding

the System Engineer

and Design System Engineer

programs,

stated that more

DSE rotations to the site were planned;

and that

additional definition would be provided regarding

SE/DSE qualifica-

tion, training,

and responsibilities.

It was expected that these

would be addressed

by about mid-1990 in revisions to the applicable

procedures.

Regarding followup of open corrective actions, stated that manage-

ment was evaluating the establishment

of a central root cause

and

corrective action group.

Regarding

the discussion of outstanding

engineering

work, agreed

with the inspectors'haracterization

of the workload of open

engineering

items;

and stated that the hiring of additional

engineers

is being evaluated.

The licensee

representatives

did not identify as proprietary any

information reviewed by or discussed

with the inspectors

during the

inspection.

Attachment

A

Additional Personnel

Contacted

During the Inspection

D.

J.

A.

G.

D.

D.

  • p

p.

C.

J.

  • T

J.

B.

M.

p.

K.

R.

L.

  • E

G.

  • D

A.

J.

T.

E.

W.

p.

J.

D.

T.

S.

S.

R.

W.

  • T

B.

G.

p.

C.

J.

  • G

W.

R.

J.

M.

K.

p.

S.

0.

A.

L.

D.

L.

E.

W.

C.

J.

A.

W ~

L.

G.

C.

Aaron

Albers

Al 1 en

Anderson

Bar kley

Bauer

Beckham

Bedesem

Belmont

Benitou

Bennett

Blakely

Bri 1 ey

Burgess

Burgess

K.

M.

A.

G.

E.

D.

Cosgrove

Coville

Davis

deUriarte

Elder

El 1 i s

Emmel

A.

L.

F.

J.

R.

D.

H.

L.

M.

C.

T.

D.

R.

W.

L.

0.

S.

J.

C.

T.

Ewart

Farrer

,

Fetterman

Foat

Fridley

Glynn

Goelzer

Grebel

Gross

Hamby

Hanes

Harbor

Harris

Heggli

Henretty

Hicks

Ivora

Jacobson

Kane

Kao

Chan

B. Clark

D. Cobbs

C. Connell

L. Corsiglia

4

Director,

NPG Power Production

Engineerimg

Maintenance

Foreman,

Mechanical

Machinist

Shift Foreman

Shift Foreman

Senior

Power Production Engineer

Senior Nuclear Generation

Engineer

Power Production Engineer

Control Operator

.

Senior Nuclear Generation

Engineer

Manager,

Maintenance

Senior Nuclear Generation

Engineer

Shift Foreman,

Operations

Supervisor,

Plant Engineering

gA Technical Assistant

Electrical Engineer

Supervisor,

Mechanical

Engineering

Electrical Maintenance

Foreman

Acting Project Manager

Assistant

Group Leader, Electrical Distribution

Systems

guality Control Specialist

Supervisor, Reliability Engineering

Supervisor,

gA Program Auditing

Supervisor

Engineer

Electrician

Mechanical

Engineer

Electrical Helper

Control Operator

System

Engineer

Electrical

Group Supervisor

Electrical Maintenance

Engineer

Manager,

Operations

System Engineer.

Steam Generator

Blowdown

System Engineer,

Emergency

Diesel Generators

Regulatory

Complian'ce Supervisor

Senior Electrical Engineer

Machinist

Instrument

and Controls (I

& C) Technician

System Engineer,

Compressed Air System

Supervisor,

Auditing

Senior Engineer,

Technical Auditing

. Auxiliary Operator

Auxiliary Operator,

Operations

gA Engineer

Engineer, Quality Control

Group Support

Technical Assistant,

Operations

Group Leader,

Mechanical

Engineering

Attachment

A -- Additional Persons

Contacted

(continued)

.i

W.

J.

W.

K.

R.

T.

  • Pl

B.

J.

T.

A.

J.

D.

R.

C.

B.

D.

T.

G.

H.

  • W.

W.

S.

J.

B.

D.

B.

  • D

B.

  • R.

F.

  • M

E.

K.

C.

J.

D.

S.

J.

J.

M.

J. Kelly

C. Kelly

J.

Keyworth

Klaesius

P.

Kohout'.

Lee

E. Leppke

S.

Lew

A. Lowrie

A. Nelson

L. Nicholson

J.

Nystrom

W. Ogden

Ortega

J. Parry

H. Patton

W. Patty

W. Pelliseor

P.

Perez

J. Phillips

T.

Rapp

R.

Ryan

N. Sabharwal

E. Skaggs

D. Smith

Spaulding

Supremo

A. Taggart

Tashiro

G. Todaro

A. Toste

R. Tresler

R; VanDemarr

B. Wallace

E. Weber

A. Wejrowski

M. Welch

M. Wilde

Williamson

D. Woessner

C.

Young

W. Zimmermann

Regulatory

Compliance Engineer

Engineer

Emergency

Planning Supervisor

I 8

C Technician

Emergency Safety Supervisor

Senior Mechanical

Engineer

Engineering

Manager

Director, Nuclear Regulatory Affairs

Auxiliary Operator

System Engineer, Auxiliary Feedwater

System

Nuclear Generation

Engineer

Supervisor,

Electrical Planning

Licensing Technical Specialist

System Engineer,

Emergency Lighting

System Engineer,

Compressed

Air

Manager, Reliability Engineering

Shift Supervisor,

Operations

Senior

Systems

Engineer

Consultant

Work Planning Manager

Onsite Safety Review Group Chairman

Unit

1 .General

Foreman,

Mechanical

Design System Engineer, Air Systems

Senior Engineer,

Operations

Group Leader, Electrical Distribution Systems

Group Leader,

Mechanical

Engineering

Consultant

Director, Quality Support

Electrical Maintenance

Engineer

Security Manager

Foreman,

Operations

Project Engineer

Mechanical

Foreman

OPEG Engineer,

Steam Generator

Blowdown

Environmental Qualification Coordinator

Mechanical

Maintenance

Planner

Machinist

Nuclear Generation

Engineer

Consultant

Director, Special

Projects

Director,

QA

Operational

Experience

Assessment

Group

  • Attended exit meeting at

DCPP on February 2, 1990.

0*

'i

Attachment-B

Procedures

Reviewed:During .the Inspection

i

2)

3)

4)

5)

6)

7)

8)

9)

10)

Procedure Title

Control of Main Annunciator Problems

Event Investigation

Justification for Continued

Operations

Technical

Review Groups

Root Cause Analysis

Licensee

Event Report Processing

Non-Routine Notification and

Reporting to the Nuclear

Regulatory

Commission

Relationship

Between Plant

Organizations

and General Office

Staff During Normal Operations

Duties

and Responsibilities

of

the Shift Technical Advisor

Duties

and Responsibilities

of

the Shift Technical

Advisor

General Authorities and

Responsibilities

of Nuclear

Plant Operations

'No.

AP C-154

NPAP C-18

NPAP C-22

NPAP C-23

NPAP C-26

NPAP E-11

NPAP C-ll

NPAP A-10

AP A-10

AP A-51

NPAP A-100

Revision

Date

~Rev.

0

1/1/89

Rev.

3

1/13/90

Rev.

1

1/16/89

Rev.

4

11/25/89

Rev.

0

8/19/89

Rev.

7

12/6/89

Rev,

4

ll/13/87

Rev.

5

9/23/89

Rev.

5

9/23/89

Rev.

3

10/07/87

Rev.

11

ll/18/88

12)

Auxiliary Operators

Routine Plant

Equipment Inspections

Dissemination of Operations

Department Policies

AP A-100 S2

Rev.

1

3/5/88

AP A-100 S3

Rev.

0

6/26/87

14)

15)

16)

General Authorities and Responsi-

bilities of the Shift Foreman

Shift Control

Room Manning

Requirements

General Authorities and Responsi-

bilities of the Shift Foreman

NPAP A-102

NPAP A-104

AP A-150

Rev.

6

6/9/88

Rev.

7

10/25/89

Rev.

3

11/15/88

'

Attachment 'B Procedures

Reviewed, (continued)

17)

18)

19)

20)

21)

22)

23)

24)

25)

26)

27)

28)

29)

30)

31)

32)

35)

Procedure Title

Conduct of Plant Equipment Tests

Surveillance

Testing

and Inspection

Bypass of Safety Functions

and

Control of Jumpers

Mechanical

Bypass,

Jumper

and Lifted

Circuit

8 Accountability System

Control of Lifted Circuitry and

Jumpers

During Maintenance

Cl earances

General

Requirements

for Plant

Maintenance

Programs

Plant Equipment Failure Tracking

and -Trending

Maintenance

and Surveillance of

Environmentally gualified Equipment

Determination of Preventive

Maintenance

I 5

C Department

Preventive

Maintenance

Program

Plant Logs

System Engineering

Program

Compressed Air System

Compressed Air System Lineups

Issuance

and Approval of

On-The-Spot

Changes

to Procedures

Procedures

Identification and Evaluation of

Problems

and Non-Conformances

Standard

Plant Priority

Assignment

Scheme

No.

NPAP C-3

AP C-351

NPAP C-4

AP C-4Sl

AP C-4S3

NPAP C-6

NPAP C-40

AP C-40

S2

NPAP C-41

AP C-62

AP C-"450

NPAP E-6

AP A-350

OP K-1

OP K-1.1

AP E-4S4

NPAP E-4

NPAP C-12

SAP C-81

Rev.

13

6/6/89

Rev.

0

3/4/88

Rev.

6

6/18/87

Rev.

3

3/11/86

Rev.

2

7/7/86

Pev.

3

2/2/S9

Rev.

0

9/4/89

Rev.

8

11/28/89

Rev.

3

Rev.

1

7/7/86

6/6/89

Rev.

4

3/17/89

Rev.

5

Rev.

16

8/14/89

12/10/89

Rev.

8

7/26/89

Rev.

19

12/14/89

Rev.

4

10/1 1/88

Revision

Date

Rev.

7

7/7/86

Pev.

11

4/12/S9

Rev.

6

3/6/86

'

Attachment

C

Plant Records

Reviewed

i

To determine if:problems were:being identified and documented,

an extensive

review of active and completed records

was conducted.

This review covered

the following plant records:

Control

room and operations

logs for the period of November

1

thr ough 'Z2,

1989

26 sequentially

issued action requests

(ARs) (on various plant

equipment)

issued during July 1989

24 open

ARs on the compressed

air system

16 closed

ARs on the compressed

air system

10 ARs for auxiliary feedwater

system

12 maintenance

work orders

on recurring tasks

20 surveillance tests

performed

by operations

and maintenance

on

various

components

and systems

5 corrective maintenance

work orders

40 ARs on the

5 emergency diesel

generators

(EDGs)

17 maintenance

history records on'the

EDGs

6 non-conformance

reports

on the

EDGs

8 STPs

on the

EDGs

12 work orders

on the

EDGs

Partial

review, Safety System Functional Audit and Review

(SSFAR)

for auxiliary feedwater

system,

including concerns

and

recommenda-

tions identified therein

system status

reports for the compressed air, safety injection,

auxiliary feedwater,

emergency diesel

generator,

125V DC, and the

480/4160V

AC systems for the last two quarters

numerous

plant drawings

'

j /

~

~

'Attachment

C -- Plant

Records

Reviewed (continued)

7he following records

and reports

were reviewed at the corporate office:

64 quality evaluations audit finding reports

(gE-AFRs) from the

Safety System Functional Audit and Review (SSFAR) of the Vital

,Electrical Distribution System conducted

from Narch

13 through

April 7,, 1989 (including engineering

responses)

18 ARs related to the

125V

DC from January

1989 to January

1990

all

1989 quarterly system status

reports

on the

125V

DC system

2 design

changes

on the compressed

air

system

the President's

Nuclear Advisory Committee

(PNAC) meeting minutes

for 1989

the Western

Region Joint UtilityAudit (WRJUA) team reports for

1988/89

the General

Office Nuclear

Power Review and Audit Committee

(GONPRAC) charter,

procedures,

gA audits,

selected

ARs and meeting

minutes for the past

6 months

Corporate guality Assurance

reports

included;

45 audit reports;

17

gE-AFRs,

17 nonconformances,

and

2 gA quarterly reports

approximately

50 safety review event followers initiated by the

operating experience

assessment

group

82 ARs and

43 gEs

on measuring

and test equipment calibration

41 gE-AFRs,

53 ARs,

1

SSFAR and

3 months of Nuclear Operations

Support

gC engineering internal audits

approximately

50% of 94 gEs

on

PIMS and

20% of 256 1989

ARs related

to 480/4160

VAC systems

The above discussed

reviews of plant and corporate

records did not reveal

any

significant problems

which had not been entered into the

PINS corrective

action system.

~

'