ML16341E709

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Insp Repts 50-275/88-11 & 50-323/88-10 on 880410-0528. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items & LERs
ML16341E709
Person / Time
Site: Diablo Canyon  
Issue date: 06/16/1988
From: Johnston K, Mendonca M, Narbut P, Padovan L, Pulsipher J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E707 List:
References
50-275-88-11, 50-323-88-10, NUDOCS 8807010434
Download: ML16341E709 (80)


See also: IR 05000275/1988011

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos:

50-275/88-11

and 50-323/88-10

\\

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

+84/~I

Inspectors:

L.

M. Padovan,

Resident

Inspector

Date Signed

K.

E. Johnston,

Resident Inspector

~.~~

c

P.

P. Narbut, Senior Resident

Inspec or

J.

C. Pulsipher,

NRR

Approved by:

M.

M. Mendonca,

Chief, Reactor Projects

Section

1

Date Signed

wl>~ lzS.

Date Signed

+ yr, /d"I

Date Signed

Date Signed

Summary:

Ins ection from A ril 10 throu

h Ma

28

1988

Re ort Nos.

50-275/88-11

and

~/

Areas Ins ected:

The inspection included routine inspections of plant

operations,

maintenance

and surveillance activities, follow-up of onsite

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

25026,

30702,

30703,

37700,

57050,

57080,

60710,

61726,

62703,

70307,

70313,

71707,

71709,

71710,

71881,

73756,

90712,,92700,

92701,

92702,

93702,

and 94703 were applied during

this inspection.

SS07010434

SS0617

PDR

ADOCK 05000275

9

DCD

-2-

Results of Ins ection:

Two violations were identified.

The first dealt with ineffective corrective

action in dealing with the loss of system cleanliness

controls

as described

in

paragraph

13. d.

The second violation dealt with mechanics failing to follow

procedures

during maintenance activities

as described

in paragraph

5.a.

An unresolved

item is described

in paragraph

13.c. dealing with the operability

of the Auxiliary Saltwater

(ASW) system during the period of time that the

heat exchanger differential pressure

setpoint

was raised.

An apparent

weakness

is implied by the situation of uncertain

oper ability of

the

ASW system in that it can

be concluded that system design

bases

have not

been successfully

communicated

to plant personnel

and that the result of this

may have led to, or could lead to, plant personnel

making system setpoint

changes

which they do not recognize

as affecting system operability.

An additional inspector

concern raised during this reporting period is the

perceived lack of timely, effective corrective actions in dealing with

situations

in which plant personnel

made errors.

The two examples

discussed

in the report 'are the subject of violations; specifically repeated

cleanliness

problems

and the failure of mechanics

to follow procedures.

In both cases

the

job at hand

was corrected

but plant management

appeared

content to allow the

normal processes

resolve the root cause of the problems.

The normal process

involves

a nonconformance

report and

a technical

review group meeting,

a

process

that can

and does

take months.

The action that appears

to be missing

is an immediate

response

to ensure

other personnel

involved in similar work

are quickly alerted to the errors

made.

During the reporting period there were good examples of individual plant

personnel

who exercised

an inquisitive safety minded approach

to their work.

Specific examples

were the identification of misaligned detectors

in the main

steam line radiation detectors

by an

I8C technician,

the identification of

improper surveillance

schedules

for time response

testing of vital

instrumentation

channels

by an I8C technician,

and identification of the

possibly generic

problem with containment ventilation butterfly valves

identified by engineers

involved in the integrated

leak rate test.

Additionally, the licensee's

actions leading to the discovery of possible

generic

problems with Westinghouse

ARD relays

was noted

as

an example of

thorough root cause

analysis.

DETAILS

1.

Persons

Contacted

"J.

D. Townsend,

Plant Manager

  • D. B. Miklush, Acting Assistant Plant Manager,

Plant Superintendent

J.

M. Gisclon, Acting Assistant Plant Manager for Support Services

  • C. L. Eldridge, guality Control Manager

K.

C. Doss,

Onsite Safety

Review Group

R.

G. Todaro, Security Supervisor

  • T. Bennett, Acting Maintenance

Manager

D. A. Taggert, Director guality Support

~T. J. Martin, Training Manager

W.

G. Crockett, Instrumentation

and Control Maintenance

Manager

J.

V. Boots, Chemistry and Radiation Protection

Manager

L.

F.

Womack, Operations

Manager

~T.

L. Grebel,

Regulatory Compliance Supervisor

  • S.

R. Fridley, Senior Operations

Supervisor

R.

S. Weinberg,

News Service Representative

W. T.

Rapp,

Chairman,

Onsite Safety Review Group

M. Tressler,

Project Engineer,

NECS

The inspectors

interviewed several

other licensee

employees

including

shift foreman

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

Denotes

those attending the exit interview on May 27,

1988.

2.

0 erational

Status of Diablo Can

on Units 1 and

2

During the reporting period Unit 1 continued its second refueling outage.

Notable occurrences

included the discovery of fatigue cracking in reactor

coolant

pump lubrication system

components,

some evidence of pressurizer

surge line movement, possible generic problems with Westinghouse

ARD

relays, biological growth in diesel

fuel oil day tanks,

combustible fire

barrier material,

and indications

from the ILRT that 48" butterfly valves

used for containment

purge

and exhaust

may have directionally dependent

leak characteristics.

3.

Unit 2 remaining at power for the reporting period.

0 erational

Safet

Verification

71707

a.

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed

control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed

in, the facility Technical Specifications

(TS).

F

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers. were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas of the facility to

observe

the following:

(a)

General plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment and conditions.

(i)

Storage of pressur ized gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

A

lication of the

ualit

Assurance

Pro

ram to Diesel

Generator

Fuel Oil

Tem orar

Instruction 2515/93

Closed

In January

1980, the Office of Nuclear Reactor Regulatory requested

all licensees

to check their guality Assurance

(gA) programs with

respect to diesel

generator

(DG) fuel oil, and to include

DG fuel

oil in their gA programs or provide justification for not doing so.

The inspector verified that the licensee

has included the

DG fuel

oil system in its gA program.

The quality classification list

specified the

DG fuel oil storage

tanks, transfer strainers,

transfer filters, and transfer

pumps

as "g".

This implies that the

provisions of Appendix 8 to 10 CFR 50 apply.

Section

4 of this report addresses

fuel oil problems

encountered

during this reporting period.

No violations or deviations

were identified.

4.

Onsite Event Follow-u

93702

a

On April 13, 1988, with Unit 1 in a refueling outage

and Unit 2 at

100X power, results of a routine 18 month calibration of main steam

line post accident monitoring radiation monitors required all eight

(four per unit). steam line monitors to be declared

inoperable.

The

GM tube detectors

were found to be positioned in their main steam

line shield casks

such that the detectors

did not fully extend into

the shield aperture

and were only partially sensitive to potential

radiation from the steam lines.

Incorrect detector positioning

occurred during original installation

due to poor installation

instructions

and calibration procedural

errors.

Accordingly, the

monitors were considered to have

been inoperable

since August 1983

for Unit 1 and April 1985 for Unit 2.

However, alternate

proceduralized

methodologies

wer e available to identify and assess

steam generator

tube ruptures.

Previous identification of this

problem did not occur since radiation monitor surveillance test

procedure

(STP) I-18R2 specified presentation

of the radiation

source at the detector well top, rather than of the detector

cask

aperture

due to the close proximity of the casks to the main steam

lines.

The licensee

indicated the radiation monitor vendor would be

contacted to evaluate

the appropriateness

of reportability under

Part 21.

Further followup of this event will be done during the

review of licensee

event report 50-275/88-11.

b.

On April 16, 1988, Unit 1 experienced

a spurious

containment

ventilation isolation due to a high radiation alarm on radiation

monitors

RM ll, 28,

and 21.

No cause

was determined.

The licensee

made

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency

10 CFR 50.72 report.

Note:

Licensee

actions to reduce spurious actuations

caused

by radiation monitors

are addressed

in report 50-275/88-13.

C.

On April 19, 1988, Unit 1 experienced

a spurious

containment

ventilation isolation signal

due to a high alarm on RM-12

(containment particulate).

No cause

was determined.

d.

On April 20, 1988, Unit 1 fuel reload

was completed.

On April 22, 1988, for Unit 1, the licensee

determined that

technical specification 3.11.1

had been violated for some period of

time not exceeding

one hour and 10 minutes.

The technical

specification required continuous

sampling of particulate

and iodine

samples of the plant. vent.

This function is usually provided by

radiation monitor RE-24.

Due to planned work on RE-24,

a temporary auxiliary sample

pump had

been properly placed in service prior to securing

RE-24.

During the

ILC work on RE-24, technicians

secured

the temporary

sample

pump,

thereby violating the technical specification.

There

does not appear to be any technical

consequences

to this act.

The unit was in a refueling outage

and local portable air monitoring

equipment

was in place

and monitoring work activities.

Additionally, a vent stack release, if one occurred,

would contain

primarily noble gases

and

a smaller

amount of particulate

and

iodine, if any.

Potential

noble gas release

was monitored during

the entire time by RE-14A and

B and

showed

no release.

Licensee corrective actions will be followed up through

LER 88-12.

On April 23, 1988, Unit 1 experienced

a containment ventilation

isolation due to radiation monitor RM-14A spiking.

No cause

was

determined.

On April 26, 1988,

Regional

management

conducted

an onsite meeting

with licensee

management.

The results

are reported in Inspection

Report 50-275/88-14.

On May 5, 1988, during Unit 1 midloop operation for removal of steam

generator

nozzle

dams,

the licensee

discovered that part of the

reactor vessel

vent arrangement

of the temporary

system,

Reactor

Vessel

Refueling Level Indication Systems

(RVRLIS), had been

removed.

Specifically,

RVRLIS valve 613 had been

removed.

The

licensee

formed an Event Investigation

Team (EIT).

This event

had

no technical

consequence

in that the temporary

system

remained

vented to atmosphere

as it was intended through

a different path.

The error was preliminarily determined to be personnel

error in that

general

construction

personnel

(GC) performed the work without a

clearance.

The activities discussed

in this section involved

apparent

or potential violation of NRC requirements

identified by

the licensee for which appropriate

licensee

actions

were taken or

initiated.

Consistent with Section IV.A of the

NRC Enforcement

Policy, enforcement action

was not initiated by Region

V.

On May 5, 1988, during the performance of a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />

load test

on

Unit 1 diesel

generator 1-1, the licensee

determined that fuel oil

filters were being severely clogged by biological growth.

The

condition identified itself as

a load reduction

due to fuel

starvation.

Operators

switched to the other fuel filter and load

was reestablished.

The inspector

reviewed the licensee justification for continued

operation of Unit 2 (Unit 1 was shutdown for refueling) and the

inspector

determined that the licensee's

analysis of this condition

was acceptable..

The inspector also reviewed the licensee's

plan of action to correct

the situation

as well as to prevent recurrence.

Initial licensee

plans included tank cleaning, biocide treatment

and increased

testing.

Follow-up of this item will be accomplished

through the licensee's

event report.

On May 9, 1988, during planned preventative

maintenance

of Unit 1

reactor coolant

pump bear ings and their lubrication system,

the

r

\\

licensee

noted several failed bolts,

an extruded gasket

and cracked

parts in the assembly

which provide motive force and directs

lubricant flow for the reactor coolant

pump thrust and radial

bearings.

The problem was first identified in RCP 1-2.

Investigation of the

remaining

pumps, indicates at least

one of the cracking problems

may

be generic since the

same failure to a lesser

degree

was evident.

The broken bolts

and

a second cracking problem may be isolated

due

to improper assembly or may be

a generic vibration problem.

The licensee is continuing investigative actions

and has,

subsequent

to the inspection period,

documented this problem in voluntary LER

50-275/88-15.

The licensee is planning corrective actions for Unit

1.

The licensee

has provided justification for continued operation

of Unit 2 in the

LER and the inspectors

review of the

JCO will be

the subject of regional

correspondence

in conjunction with NRR

review.

The residents

followed licensee

actions closely.

Regional

and

NRR

project management

personnel

were in communication with the licensee

on this matter.

Follow-up of this item will be conducted

as part of

normal inspection activities.

On May 10,

1988, the licensee identified the fact that time response

testing for reactor trip and essential

safety feature

instrumentation

had not been conducted in accordance

with the

schedule of frequencies

described

in the technical specifications.

The technical specification require

such instrumentation to be

tested

on

a rotational basis; specifically to be tested

every

"N x

18" months

where

"N" is the number of channels of instrumentation.

The licensee

had not been doing this in all cases

and

had in effect

confused

the number of available channels with the number of

components

(e.g.

steam generators)

and therefore in some

cases

was

testing at lesser

frequency than required.

The licensee

determined that Unit 1, which was shutdown,

was late on

time response

testing for situations

were there were two or less

channels

available.

For Unit 2, the operating plant, the licensee

concluded that

surveillances

were not late for any time response

testing but this

position was predicated

on an assumption that the technical

specification tables (e.g. 3.3.1) did not include any requirement to

test what appear

to be single channel (i.e. N-1) functions every

18

months.

Discussions

of this subject with regional

and headquarter

technical

staff indicated that further review would be required

upon licensee

submittal of an

LER dealing with the subject.

The issue will be

followed up through the

LER process.

On May ll, 1988, during Unit 1 Diesel Generator 1-2's

24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> run,

the foamed fire barrier material

around its'xhaust

stack began to

burn.

The fire was quickly extinguished

and no diesel

generator

inoperability occurred.

The fire barrier material apparently

broke

down when exposed to the

heat of the exhaust pipe with time and became

a flammable material

itself.

The possible

generic considerations

of this event were

related to the regional fire specialist

who will perform follow-up

of this item.

The licensee

removed the fire barrier material

from the other diesel

generator

locations

and is pursuing

a design

change for permanent

corrective action.

Fire watches

have

been set in the interim.

On May 12, 1988, the licensee

made

a 4 hour4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> non-emergency

report due

to the Fuel Handling Building ventilation system switching to iodine

removal

mode

due to a radiation monitor (RM-58) spike.

No cause

was

determined for the spike.

On May 13, 1988, the inspector

became

aware of a nonconformance

report written on April 30 which dealt with a cracked stator inboard

clamping ring on the motor of a Containment

Fan Cooler Unit (CFCU)

motor.

The inspector determined that the problem was not similar to

that described

by

NRC Information Notice 87-30 which described

generic cracks in large vertical electric motors in surge ring

brackets.

The responsible

licensee

engineer stated that the

CFCU crack had

been found as part of a visual inspection during a planned

maintenance activity and was not found to be generic

as determined

by the inspection of the other

CFCU motors (inspected to that time).

On May 18, 1988, Unit 1 commenced pressurization for a integrated

leak rate test (ILRT) of the containment.

The conduct of the test

and its results

are discussed

in section

14 of this report.

During the test it was noted the inside containment valves for

containment

purge supply and exhaust

(RCV 11 and

FCV 660) did not

appear to hold pressure.

Subsequent

to the ILRT the licensee

performed

a local leak rate test of the valves

and found them to be

tight.

The anomalous

leak behavior of the valves, i.e.,

directionally dependent

leak characteristics,

caused

the licensee to

declare

the valves inoperable in Units 1 and 2 and to commence

an

investigation.

At the end of this reporting period, although the seal ring of one

valve had been replaced,

the licensee

had not been able to

pressurize

the valve inside containment to the required level.

The

licensee's

Event Investigation

Team was continuing its efforts to

repair the valves.

This matter will be followed closely as part of

the routine inspection

program.

P ~

On May 19, 1988, Unit 2 experienced

a non reportable

event when an

I&C technician attempted to remove the display screen for the plant

computer.

In removing the screen

a short was caused

which resulted

in the loss of one bus of instrument power (PY-24).

This caused

a

number of bistables

to trip, a number of feedwater controls to go to

manual,

rods to step in, and letdown to isolate.

Subsequent

operator action restored

120

VAC power.

Plant parameter

changes

during the event were minimal due to operator actions.

On May 20, 1988, Unit 1 experienced

a pure water spill estimated to

be 500-1000 gallons of water in the 115 foot elevation of the

Auxiliary Building.

The spill was caused

by a failure of the freeze

seal isolating work on a

CVCS valve.

The licensee is investigating

the cause of the freeze

seal failure.

On April 28, 1988, the inspector

became

aware of a revision to a

nonconformance

report

made

on April 13,

1988.

The nonconformance

NCR DCI-87 EM-N121 was originally written on December 2, 1987,

and

dealt with malfunctions of diesel

generator l-l during test.

Specifically the diesel

picked upload but immediately shed

load.

The problem was narrowed to a binding relay (a Westinghouse

ARD

relay).

The relays binding resulted in varying contact resistance

(40-1300

ohms) which affected logic circuits.

Physical

inspection

noted concrete-like

dust in the relays which was attributed

(initially) to original construction dust.

Subsequently

the licensee

removed

some of the faulty relays

and sent

them to the manufacturer,

Westinghouse,

for analysis.

Westinghouse

determined

and stated in a reply dated

March 8, 1988, that the dust

like material

was

due to degraded

solenoid potting material

and that

the relays

had not been supplied

as safety grade material.

A meeting

was held by the inspector with licensee

personnel

on April

28,

1988.

The results of the meeting indicated that 155 such relays

were installed in the plant with 136 of them in the diesel

generators

and the remainder in non-safety related

uses.

Of the 136 relays,

one in each diesel

generator affects

low voltage

logic circuits in which the contact resistance

problem can affect

their operability.

The five relays, that are affected by contact

resistance,

are in circuits used only when the diesel is being

tested for operability, that is, in parallel with offsite power.

In

an emergency situation i. e.

loss of offsite power (when the diesel

generators

are required to load) the

5 relays would not hamper

actual operability.

The remaining

131 relays are in 125 Vdc

circuits in make or break situations that are not affected by the

contact resistance

change.

Of these,

eight are critical relays with

important functions

such

as engine start and water jacket pressure

relays.

As corrective action, the licensee

has replaced all relays in the

diesel

generator with signs of degradation.

The remaining critical

relays will be replaced during the current Unit 1 refueling outage

and the upcoming Unit 2 refueling outage.

On May 3, 1988, the licensee's

corrective actions,

proposed actions

and justification for continued operation

were discussed

with

regional

and

NRR managers,

and were found acceptable.

On May 26, 1988, the licensee

submitted

a voluntary

LER regarding

the degradation

of the relays.

This item will be followed up with

licensee's

LER 50-275/88-09.

s.

Fire in a Unit 2 Auxiliar

Buildin

Rad Maste

Dr er Cabinet

On May 24, 1988 at approximately 2:00 p.m.

a fire was discovered

inside

a rad waste dryer cabinet.

The dryer, located inside

a

ventilated rad waste tent area inside the Unit 2 Auxiliary Building,

'was being used to dry rad waste filters which had apparently

collected

flammable paint chips.

The fire was initially identified by a roving fire watch who

notified the Operations

and Radiation Protection

departments.

A

health physics technician,

wearing

a respirator,

extinguished the

fire by unplugging the heater

element,

dousing the cabinet with

carbon dioxide,

and placing the filters and rags contained in the

cabinet into a bucket of water.

The fire was out within ten minutes

and

an Unusual

Event was not

declared.

The licensee

suspended all rad waste dryer operations.

~

~

~

~

No violations or deviations

were identified.

5.

Maintenance

62703

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

certified.

a 0

Safet

In ection

S ectacle

Flan

e

On April 26, 1988, the inspector

observed

maintenance activities to

reverse

the spectacle

flange

on the safety injection relief valves

return line to the pressurizer relief tank (PRT).

The spectacle

flange, consisting of a blind flange and an orifice, had been

installed with the blind flange earlier in the outage to facilitate

the local leak rate testing of containment penetration

71.

The

orifice side

needed to be reinserted to return the line to service

for operations

and safety injection system testing.

The inspector found a number of problems with the maintenance

activity:

o

The work package

in the field included only the odd numbered

pages of Maintenance

Procedure

(MP) M-54.4, the procedure

governing the replacement of spiral

wound gaskets

used in this

flange.

The mechanics

were not aware of the fact that half the

procedure

was missing prior to identification by the inspector.

o

The mechanics

were not using the lubricant specified in MP

M-54.4 for the lubrication of bolts.

They were using

Chesterton

instead of Felpro N"5000.

o

The mechanics

were not using the data sheets

included in MP

M-54.4 for recording flange alignment and other important data.

o

The work order was poorly written, in that it did not specify

the use of the data sheets

for

MP M-54.4 and in fact the only

instructions

given for final flange reassembly

were:

"At the

completion of STP,

Mech. Maint. to restore all systems to

operating state,

as required

by engineer

and foreman in

charge."

The problems fall into two categories;

an inadequate

work package,

and mechanics

not following the applicable procedure.

The

work

order was written to cover both the insertion of the blind flange

and the reinsertion of the orifice.

Mhen the package

was reissued

to the field for the reinsertion of the orifice it included only the

above step for the mechanics

to perform which had not been signed

off previously.

The

STP referred to was

STP V-671, the local leak

rate testing of the containment penetration.

The step

does not call

out

MP M-54.4 or its data sheets.

Other steps in the work order,

previously signed off, describe bolt torque

and referred to

MP

M-54.4.

However, those

steps

did not specify that the data sheets

need to be filled out.

Although the inadequate

work package contributed to the problems,

the activity could have

been performed correctly had the mechanics

taken the time to read the package

and have it corrected or

requested

guidance

from their supervisor.

This was not done

and as

a result the wrong lubricant was

used

on the bolts.

The lubricant

used

had not been qualified to be used

on safety related bolting

applications.

Failure to follow MP M-54.4 is an apparent violation

(Enforcement

Item 50-275/88-11-01).

Following identification by the inspector,

the licensee identified a

number of immediate corrective actions:

The bolts were cleaned

and relubricated with Felpro N-5000.

The Maintenance

Manager held a meeting with the maintenance

department to discuss

procedural

compliance,

the need to use

data sheets

included in procedures,

and that only the materials

specified by the procedure

may be used.

The guality Control Manager

gave instructions to the

gC

department

not to approve work orders with instructions

as

general

as "Restore all systems

worked to operating state,

as

required

by engineer or foreman in charge."

10

The licensee

convened

a Technical

Review Group

(TRG) to review the

Nonconformance

Report

(NCR) associated

with this incident.

At the

conclusion of this inspection period %he

TRG had not yet specified

any further corrective actions.

b.

Other Maintenance Activities Observed

The inspectors

observed

and found acceptable

portions of the

following maintenance activities:

o

Auxiliary Salt Water

Pump l-l reinstallation following

overhaul.

o

Unit 1 Auxiliary Building Ventilation System

damper

2A gasket

replacement.

o

Control rod drive mechanism repair activities.

o

Upper internals clearing operations for reassembly.

o

Repairs associated

with reactor coolant

pump lubrication system

cracking.

One violation and

no deviations

were identified.

6.

Survei 1 lance

61726

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

Surveillance activities examined during this period included:

o

Integrated

leak rate testing for Unit 1 containment

described

in

section

14.

o

Surveillance testing of the

ASW/CCW problems identified in section

13. c. of this report.

o

Inservice inspection testing,

section

12. of this report.

o

Surveillance testing of the main steam line radiation monitors

described

in section 4. a. of this report.

o

Diesel fuel oil sampling surveillance

discussed

in section

4. i of

this report.

No violations or deviations

were identified.

7.

En ineerin

Safet

Feature Verification

71710

The inspector walked down accessible

portions of the Units 1 and

2

Auxiliary Saltwater

system including local

and control

room indication

and system breakers.

Findings are discussed

in section 13.c. of this

report.

No violations or deviations

were identified.

8.

Radiolo ical Protection

(71709

The inspectors periodically observed radiological protection practices

to

determine whether the licensee's

program was being implemented in

conformance with facility policies and procedures

and in compliance with

regulatory requirements.

The inspectors verified that health physics

supervisors

and professionals

conducted frequent plant tours to observe

activities in progress

and were generally aware of significant plant

activities, particularly those related to radiological conditions and/or

challenges.

ALARA consideration

was found to be an integral part of each

RWP (Radiation Work Permit).

No violations or deviations

were identified.

9.

Ph sical Securit

71881

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative procedures

including vehicle

and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was

checked during backshift inspections.

No violations or deviations

were identified.

10.

Licensee

Event

Re ort Follow-u

92700

a.

Status of LERs

Based

on an in-office review, the following LERs were closed out by

the resident inspector:

Unit 1:

87-10, 87-16, 87-19, 87-23, 88-02, 88-03, 88-06,

88-12

Unit 2:

87-04, 87-14, 87-23

The

LERs were reviewed for event description,

root cause,

corrective

actions taken,

generic applicability and timeliness of reporting.

No violations or deviations were identified.

11.

0 en Item Follow-u

92701

a.

C Ins ector Failin

To Perform Ins ection

Enforcement

Item

50-275/88-03-03

Closed)

The inspector

reviewed the licensee's

response

to a Notice of

Violation issued

on March 28,

1988 concerning

a guality Control

0

12

Inspector

who stamped

and initialed his acceptance

of cleanliness

on

his inspection plan without visually inspecting inside the body of

Valve No.

8484B for cleanliness.

The inspector

reviewed the corrective actions taken

and found them

acceptable.

Therefore, this item is closed.

Unauthorized Entr

to the Radiolo ical Controls Area

Enforcement

Item 50-323 88-04-01

Closed

The inspector

reviewed the licensee's

response

to a Notice of

Violation issued

on March 28,

1988 concerning the unauthorized entry

of an individual to the Radiological Controls Area (RCA).

In their

response,

the licensee

stated that the 'individual was counseled

by

his supervisor.

In addition,

a review determined that the existing

RCA postings,

procedures

and training program were adequate.

However, the postings for the

RCA were clarified to more clearly

denote entry and exit points,

and the bar rier support

was improved

to reduce

the amount of sag in the yellow-magenta

rope delineating

the

RCA.

Based

on these actions,

no further actions

were

deemed

necessary.

The inspector

reviewed the actions

taken including the changes

to

the

RCA barrier and found them acceptable.

Therefore, this item is

closed.

Revisions to Procedures

Controllin

Maintenance

Performed

on

Ener ized

E ui ment

Follow-u

Item 50-275/87-04-03.

Closed

In response

to findings in Inspection

Report 50-275/87-04 with

respect to inadvertent control rod withdrawal

due to a

miscommunication

between

I&C and Operations,

the licensee

committed

to revise procedures for control of equipment required to be

energized

during maintenance.

The inspector

reviewed Tagging

Requirement

Procedure

AP C-7S1 which had been revised to require

that information tags placed

on equipment

be documented for

installation and removal.

The inspector also reviewed work orders

for systems

required to be energized

during maintenance

and found

that they required the technician to sign off that the Shift Foreman

had been notified prior to performing the work and following

completion.

In addition, the work orders specified where

information tags

were to be hung and required their removal

following maintenance.

Based

on the above,

Open Item

50-275/87-04-03 is closed.

Protected

Area Escort

Res onsibilit

Enforcement

Item

50-275/87-44-01

Closed

NRC Inspection

Reports 50-275/87-44

and 50-323/87-45 contained

a

violation regarding plant security.

In a March 10, 1988, letter

(DCL-88-058)

PG&E addressed

the identified security concerns.

The

inspector

reviewed the licensee's

corrective actions

and determined

them to be acceptable.

Accordingly, this item is considered

closed.

Details pertaining to the corrective actions

are not provided in

13

this report due to the security safeguards

nature of the

information.

e.

Ino erable Unit 1 Rod Position Deviation Monitor

0 en Item

50-275/87-38-02

Closed

Open item 87-38-02 was concerned with root cause

determination of

the "P-250

Rx Alm Axial Flux/Rod Pos" alarm window unexpectedly

clearing during a plant evolution.

As explained in LER 87-19-01,

the cause of the problem was identified to be in a subroutine of the

computer program which controlled alarm functions.

The subroutine

was found to function unpredictably if the rod bank demand values

were initialized improperly.

Corrective actions

were described in

the

LER.

This item is considered

closed.

Entr

into Technical

S ecification

TS 3.0 '

0 en Item

50-275/87-38-03

Closed

This open item was concerned with the root cause

determination of

fuse failures in control rod drives.

As described

in LER

50-275/87-16-01,

fuse failure was attributed to poor solder

connections

at the fuse

end caps.

Corrective actions

were described

in the

LER.

This item is considered

closed.

g.

Di ital Electro-h draulic Control

DEHC

S stem Malfunction

0 en

Item 50-275/87-04-01

Closed

This open item involved inadvertent disruption of the

DEHC load

control (software)

program during turbine maintenance activities.

As corrective action, the licensee

revised Operating

Procedure

C-3: II "Main Unit Turbine-Startup" to add

a caution that after

an

outage or any major turbine maintenance,

the P-2000 computer

(DEHC)

should

be reprogrammed.

Accordingly, this item is considered

closed.

h.

Manual Valve Maintenance

0 en Item 50-275/87-01-03

Closed

A 1987

NRC team inspection identified manual

valves which had not

been

greased

or maintained

by a preventative

maintenance

(PM)

program.

In discussions

with the team members

licensee

management

indicated the Operations

Department would identify valves

needed to

be operated

during accident

and recovery periods,

and these

valves

would be entered into a

PM program.

The licensee

concluded the

necessary

safety system valves were included in the existing sealed

valve checklists

(Operating

Procedure

K-10 "Systems

Requiring Sealed

Valve Checklist" ).

The inspector verified OP K-10 had been revised

to include stroking and lubrication of all sealed

valves,

once every

18 months.

This item is considered

closed.

No violations or deviations

were identified.

14

Inser vice Ins ection

73051)

Several different methods of nondestructive

examination

were observed

by

the inspectors.

These included liquid penetrant

examination (previously

written up in NRC Inspection

Report 87-42), A-scan ultrasonic examination

and visual examination.

The inspector witnessed ultrasonic examination

of a Unit 1 reactor pressure

vessel

stud.

The required

equipment

and

materials,

specified in licensee

procedure

N-UT-3 "Ultrasonic Examination

of Bolting with Diameter

1 Inches

or Greater,"

were observed

to be in

use,

and the specific area,

location

and extent of the examination

was

clearly defined.

The inspector

observed

personnel

perform

a

qualification test

on a calibration standard

made from a spare

vessel

stud,

and observed ultrasonic equipment calibration.

Transducer size,

frequency,

and type were in accordance

with the procedure,

and reject,

damping

and filter settings

were set at minimum values.

No indications

in the stud examined

were detected.

The inspector also observed

the licensee

perform visual inspection of

support

15-95

on the suction piping to

RHR pump 1-2.

Examination of the

rigid support

and

PSA-10 snubber

was performed in accordance

with ISI

Procedure

VT 3/4-1 "Visual Examination of Component

and Piping Supports".

The as-found condition of the rigid support

and snubber

was acceptable,

however,

procedural

discrepancies

were found.

The "Figure 1" and "Figure

2" labeling

was missing from the drawings of page

12 of revision 4 of the

procedure.

The "Hydraulic Snubbers"

(Figure 1) diagram

on page

12

contained

the statement

"...subtract

the 'Z'imension...from the

measured

position setting."

This statement conflicts with training

provided to the ISI examiners.

The drawing on page

14,

above Table 1,

was not clear to ISI personnel

interviewed

by the inspector.

This

drawing should

be revised for clarity.

Finally, on Attachment 1, page

3

of 3 the "post installation verification of snubber/strut

washer

placement"

contained check-off boxes

such

as "thickness,

O.D. acceptable"

and "remaining gap acceptable"

without the procedure

containing guidance

on how to measure

the parameters

or what criteria was being used.

The

inspector

was informed the post installation verification was not a code

requirement.

The licensee

was

made

aware of the procedural

discrepancies

and plans to correct the procedures.

Code repair activities observed

by the inspector,

were previously

documented

in

NRC Inspection

Report 88-07.

No violations or deviations

were identified.

Inde endent

Ins ection

a.

S stem

En ineerin

5-37700-4

The licensee is in the formative stages

of establishing

a system

engineering function, and

has

conducted

information gathering

meetings with other Region

V utilities.

Discussions

with licensee

management

have not established

a projected completion date for the

establishment

and implementation of this program.

15

b.

Post-tri

Review

Events Evaluation/Root

Cause

Determination

5"92700-5

During the periods January

21-22 and April 20-22,

1988, the above

areas

were examined

by the Senior Reactor Engineer,

RV.

The scope

of findings are discussed

below:

Post-tri

Review - Plant Administrative Procedure

AP A-100 Sl,

Revision 3, dated July 29, 1985,

was examined

and records of

the implementation of this procedure for three reactor trips

were examined.

Discussions relating to AP A-100 Sl and related

plant records

were held with licensee

representatives

and the

NRC Resident Inspectors,

from which the following findings and

observations

resulted:

Administrative Procedure

AP A-100 Sl was judged to be adequate

in terms of the scope of post-trip review, evaluation

and

documentation.

The procedure

provides for review and

evaluation of plant and operator

response

as well as the

authorization of plant restart

(by the Plant Superintendent).

The procedure

includes the requirement that,

under

circumstances

where the cause of a reactor trip is not

adequately

explained or where the Shift Foreman

determines

additional analysis is necessary,

prior to restart the Plant

Staff Review Committee will review the associated

transient

data

and will approve return to power operation.

Discussions

with the Resident Inspection staff revealed

instances

where thoroughness

of post-trip review was lacking in

the implementation of the

AP A-100 Sl.

These instances

are

documented

in recent

NRC Inspection Reports.

The Resident

Inspection staff has also expressed

concern regarding

a formal

process for defining and documenting specific actions required

prior to plant restart.

In response

to the Resident

Inspector's

concerns,

licensee

management

has

implemented

a

program for action plan development

and implementation.

(See

section 16.b of this report for licensee

management

commitments

in this regard).

2)

Events Evaluation

and Root Cause

Determination " In evaluating

the licensee's

programs in these

areas,

the following plant

Quality Assurance

and Administrative Procedures

(APs) were

examined

and discussions

relating thereto were held with

responsible

licensee

representatives.

Findings and

observations

resulting from the examination of procedures

and

discussions

held with licensee

representatives

are discussed

below.

QAP 15.8,

Nonconformances,

Revision dated

March 10,

1988

NPAP C-12/NPG-7. 1, Identification and Resolution of Problems

and Nonconformances,

Revision 13, dated

March 22,

1988

NPAP C-16/NPG-7.4,

Human Performance

Evalution

S stem,

Revision

0, dated

March 3,

1986

NPAP C-18/NPG-7.5,

Events Investi ations,

Revision 0, dated

July 14,

1987

NPAP C-23/NPG-7.6,

Technical

Review Grou s, Revision 0, dated

March 10,

1988

A review of the above procedures,

related plant records,

and

discussions

with responsible

plant managers

and supervisors

resulted in the following observations

and findings:

The licensee

has

implemented

a very effective

Human Performance

Evaluation

System

(HPES) program,

having been

an active

participant in this

INPO program from the time of its

initiation some two years

ago.

This program is intended to

focus

on human factor elements

of plant events,

and is aimed at

surfacing for evaluation

human factors concerns

at a low

threshold,

e. g., "near misses".

The program

has

an outreach

aspect,

wherein employees at the plant are encouraged

by direct

mailings, posters

(with associated

forms to submit written

concerns),

etc. in several

locations within the plant and

corporate offices.

During the year

1987,

a total of 39

HPES

root cause

evaluations

were performed relating to various

operational/maintenance

events.

Approximately 25 of these

were

in support of the dispositioning of Nonconformance

Reports

(NCRs).

The licensees

procedures

require formal root cause

determination for all

NCRs, of which there were approximately

135 during the year 1987.

When an additional approximately

15

HPES evaluations for root cause

determination

are

added to the

number of NCRs,

a total of approximately

150 events

were

subjected to formal root cause

determination in the year 1987.

In discussions

with the

NRC inspector,

the Plant Manager

expressed

his view that the threshold for formal root cause

determination

should be lowered to include

a larger population

of events

beyond those for which an

NCR would be initiated in

accordance

with current administrative procedures.

(See Exit

and Management

Meetings section of this report for licensee

management

commitments in this regard).

Desi

n Verification and Confi uration Control:

The Auxiliar

Saltwater

S stem

5-37700-1

37700-2

The inspector reviewed the Auxiliary Saltwater

(ASW) system with

respect to its design basis

and

how that design is implemented in

the operating plant.

The inspector identified the following

weaknesses:

o

The design basis

assumptions

for the

ASW system

have not been

fully implemented into plant procedures

and alarm setpoints.

17

As a result, plant operations

have

been conducted

outside

design basis

assumptions

requiring a review of the

ASW system's

past operability.

o

The licensee

did not have

an adequate

program for design

setpoint control.

As a result,

the annunciator setpoint for

the differential pressure

(dP) high alarm across

the tube side

of'he Component Cooling Water

(CCW) heat exchanger

(Hx) was

raised without the appropriate

design basis

review.

These findings are mitigated by the licensee's

current efforts in

Configuration Management.

Although at the time of this report the

licensee's

program was in its development

stages,

the program,

as

described

by the licensee,

would establish

how design requirements

and assumptions

are to be implemented through plant operations,

maintenance,

and surveillance.

In addition, it would establish

procedural

guidance for setpoint control.

S stem Descri tion and Desi

n Basis

The

ASW system is the ultimate heat sink, designed to cool safety

related

loads during normal operations

and following a design basis

accident.

The system consists of two pumps

headered

at their

discharge

located at the intake structure.

They pump ocean water

through two trains of 24" piping,

up 85 feet over a distance of

approximately

1600 feet and through the tubes of the

CCW Hxs.

At

the discharge of the

Hxs the

ASW is discharged at 68 feet above

sea

level

and cascades

to the ocean.

The tube side of the

CCW Hx has

a

differential pressure

transmitter with a high and low annunciation

in the control

room.

The inspector

reviewed

and discussed

the

ASW design with the system

design engineers

at the licensee

s office in San Francisco.

The

licensee

could not provide the original design calculation.

Much of

the original design took place in the late

'60s

and early '70s

when

complete

records

were not kept.

The system

was assembled

around

1973 and tested in 1974 and 1975.

In 1982, during the design

verification program

(DVP), the licensee

performed calculations

based

on as-built conditions to verify the

ASW system could meet its

design basis.

The limiting parameter for the

ASW system

was determined to be

CCW

temperature

following a design basis

Loss of Coolant Accident

(LOCA).

The limiting component

was determined to be the centrifugal

charging

pump lube oil coolers which was rated at up to 132 degrees

F for 20 minutes.

It was determined that containment could be kept

below allowed temperature

and pressure limits during a

LOCA with two

of five containment

fan cooler units

(CFCUs).

Licensee calculations

M-305 Revision

3 assumes

the following:

o

An initial ASW temperature

of 64 degrees

F.

Above 64 degre'es

F

ocean temperature,

the Technical Specifications

require the use

of both Hx.

18

o

A pre-LOCA

CCW temperature

of 80 degrees

F.

This is based

on

the

maximum normal

CCW loads.

o

The use of five CFCUs.

All five CFCUs start

on a Safety

Injection System signal.

Operator action would be required to

shut

down a

CFCU at it's breaker.

o

ASM flow of 10,700

gpm which is ba ed on flow taken from the

manufacturers

pump curve assuming

"mean low-low water" level of

-2.6 .feet mean

sea level

(MSL) and the

Hx tube outlet at

atmospheric

pressure.

o

A fouling factor,

used in the heat transfer coefficient of

0.001.

The

can

the

for

results

concluded that given these conditions,

one train of ASW

remove the post-LOCA hea$

added to the

CCW system without having

CCM outlet exceeding

132

F.

The licensee did not take credit

any operator action.

Desi

n Basis

vs Plant Confi uration and Procedures

The

the

the

inspector

reviewed plant configuration

and procedures

against

above design basis

assumptions.

The following is a summary of

discrepancies

found:

o

The Hx dP HI alarm setpoint

was 167" water whereas

a clean

Hx

dP of 75" water was

assumed

in the design calculations.

The

following section discusses

this finding in more detail.

o

The Inlet bay low level alarm was set at -10'SL whereas

a

level of -2.6'as

assumed

in the design calculations.

The

effect of a lower inlet bay level would be to lower suction

head

and consequently

discharge

head resulting in less flow.

o

ASME Code Section

XI allows

pump performance to drop to lOX of

its reference

whereas

the design calculations

took pump

performance

from the

pump curve without allowing for

degradation.

o

The

CCW Hx shell side outlet temperature

high alarm setpoint

was set at 120 degrees

whereas

the highest

normal operating

temperature

was

assumed

to be 80 degrees.

If during normal

operations

CCW temperature

rose

above

80 degrees,

the unit

would be operating outside design assumptions.

o

Plant Procedures

address

actions to be taken if both

ASW pumps

fail (cross-tie with other unit) and if CCW pumps fail (reduce

system heat loads

such that

CCW temperature

is less than

95

degrees)

but not actions to be taken if one

ASW train does not

provide sufficient cooling.

0

o

Plant procedures

did not specifically state that operators

could remove from service

CFCUs during a

LOCA to remove heat

loads

from the

CCW system.

o

Annunciator Response

Procedure

PK-0101 in step

7a.

allows

operators

to throttle the

CCW Hx tube side outlet valve if ASW

pump

dP is less that the Section XI limit.

The procedure

did

not have operations notify engineering to evaluate

the

operability of the pump.

The first three findings listed raised questions

of the

ASW system's

ability to perform its function under conditions less conservative

than

assumed

in its design basis calculations.

The inspector discussed

these findings with the Project Engineer for

Diablo Canyon

who committed to provide

a written analysis of ASW

system operability to the

NRC by June 7, 1988.

Pending

a review of

the analysis this item is Unresolved

(Open Item 50-275/88-11-02).

These findings also

show that many design

assumptions

were not

incorporated into plant operations.

As corrective action for the

ASW system,

the licensee

plans to establish

what design assumptions

need to be implemented

and revise procedures,

alarm setpoints,

instrumentation

and documentation

as necessary.

To address

these

concerns

on a larger scale,

the licensee

had initiated a

Configuration Management

program in November 1987.

As described

by

the licensee,

this program would address

the issue of design basis

implementation in plant operations.

Although the significance of

these findings as related to general

design basis

understanding

and

implementation is mitigated by the Configuration Management

Program,

continued attention

needs to be focused

on this issue.

Set oint Control

The inspector

investigated

the basis for the annunciator

setpoint

for dP across

the

CCW Hx tubes,

pressure

switches

PS 45 and 46.

It

was determined that the setpoint of 167" of water had been

established

in March 1987 following a design

change to install

pressure

transmitters

and switches with a higher range.

The design

change

had been initiated in 1985 by the operations

department

since

Hx fouling dP across

the

Hxs was routinely above the existing

setpoint of 110" during normal operations.

The engineering

reviewers of the design

change erroneously

determined that the

change did not affect equipment important to safety or equipment

important to environmental quality.

In the general

notes contained

in the design

change

package Project Engineering

author ized

Operations to revise the setpoints for PS 45 and 46 but did not give

them specific guidance

except to state that Operations

should follow

up by revising drawing 101938 (Non-Safety Instrument Setpoints) with

a field change.

Operations

revised the setpoint

from 110" to 167" basing the

revision

on a calculation of only one limiting condition; the

maximum flow velocity through the tubes.

The flow velocity

0

20

according to the vendor should

be kept below 7 feet per second;

167"

correlates

to 6.8 fps.

Upon subsequent

investigation,

the inspector

found that safety

related

Drawing Nos.

060836 (for Unit 1) and 061236 (for Unit 2),

"Instrument Setpoint Requirements"

Table II lists the high alarm

setpoint for PS 45 and 46 to be 4 psid which corresponds

to 110.7".

The cover note to the drawing states

"Table II of this drawing lists

other non-instrument

Class

1A setpoints

which engineering

has

determined to be appropriate to meet various

FSAR commitments."

This design drawing was not reviewed or changed

when the setpoints

of PS 45 and 46 where changed.

This is a failure of Engineering not

to reevaluate

the basis for the original setpoint

and is an apparent

violation of Criterion III, "Design Control," of 10 CFR 50 Appendix

8 but will be treated

as unresolved until the significance of the

ASW/CCW systems

operating with a 167" differential pressure

setpoint

is resolved.

Following the meeting of the Technical

Review Group

for the

ASW system

Non Conformance

Report,

Operations

put an

administrative limit on

CCW Hx tube side

dP of 110" pending the

resolution of the basis for the 110" setpoint.

Subsequently, it was

determined that the

dP setpoints

in Drawing Nos.

060836

and 061236

to control the low alarm setpoint satisfied the

FSAR commitment for

a control

room alarm on

ASW piping failure.

Regardless,

system

performance is directly effected

by Hx fouling and requires setpoint

control.

The licensee

was in the final stages

of a comprehensive

revision to the setpoint control program at the time of this

finding.

These revisions

appear

adequate

to ensure that important

setpoints

are reviewed against the design basis.

Cleanliness

Control Problems

5-92700-4

In previous resident inspector report (Inspection Report

50-275/88-07),

two cleanliness

problems

were identified during the

performance of refueling outage work.

The two areas

examined

previously were the removal of thermocouple

connoseals

on March 21

and spare control rod drive mechanism

work on the removal of the

reactor vessel

head

on April 6, 1988.

During this reporting period the control of cleanliness

problems

continued.

On April 9, 1988, quality control

(gC) personnel

issued

a stop work on

CRDM cleanliness

requirements.

The stop work was

lifted later that day after corrective action was taken.

The action

consisted of erecting barriers

around the refueling cavity that were

shown later to be ineffective.

Additionally a memo was issued

by

engineering to the engineering task coordinators

regarding

cleanliness

controls.

Subsequent

events

showed that this memorandum

was ineffective in precluding further occurrences.

On April 12, 1988,

gC inspectors identified that cutting fluid and

chips were being allowed to enter crevice areas

on the reactor

vessel

head.

Accordingly, a stop work was issued.

Subsequently,

the licensee

implemented corrective actions.

These corrective

actions consisted of cleaning the crevices

and revising the

procedure for cutting to include

a gC holdpoint to verify barriers

21

were installed.

Corrective actions did not include personnel

reinstruction

even though the procedure

used

had

a specific caution

note requiring steps

be taken to preclude fluids from entering the

crevices.

On April 22, 1988, during the attempt to reinstall the upper

internals,

work was stopped

by the refueling crew due to the

sighting of debris

on the upper internals which was initially

reported

as tools (pliers, nuts,

and washers).

The debris

was

retrieved

and determined to be

a broken "tie wrap" (a plastic strap

ordinarily used to secure electrical

cable to cable trays)

and paint

chips.

The inspector attended

the licensee's

corrective action meeting

on

April 22, l988.

The inspector

entered

containment with the engineer

assigned

the responsibility to determine

the probable

source of the

debris

on the upper internals.

The engineers

in charge of the job did not "save the evidence"

upon

debris retrieval, but rather

had it placed in radioactive waste.

It

was retrieved

by the licensee

and the inspector

observed that the

tie wrap looked old (yellowing in color as

opposed to new white) and

the paint chips were yellow paint.

The conclusion

drawn was that

the tie wrap probably

came from the reactor vessel

head

and its

cable trays.

The inspector

then examined the work area

on top of

the reactor vessel

head

and noted several

unsatisfactory

conditions.

The removed

head

was stored

immediately adjacent to the, refueling

cavity; most of the components

on the

head

do not hang over the

cavity, but a portion of the cable tray area

does

hang over the

pool.

The tie wrap found on the internals

was directly under the

head area cable tray.

The inspector

found additional

broken tie

wraps in the cable tray area which had the potential to fall.

Additionally, on the upper area of the head

(where work had been

underway to remove

and replace digital rod position indicator (DRPI)

stacks for CROM weld repair access)

the inspector

found a great deal

of dirt (up to 1/4" thick) including broken microphone

ceramics

abandoned

in place since pre-operational

testing.

The engineer in

charge of that work explained that prior to removing any

DRPI coils,

the local area

around the

DRPI coil was vacuumed,

and that any dirt

dislodged would fall straight

down and not into the refueling

cavity.

However,

he further explained that one of the interlocking

steel plates in .that

same area

had been inadvertently kicked, fell,

bounced off a structure,

and ended

up in the refueling cavity pool,

and was yet to be retrieved.

Therefore,

the logic that dirt and

debris would only fall straight

down appeared

to be faulted.

The inspector discussed

the cleanliness

situation with the engineers

in containment

and with the outage

manager that evening.

All areas

were recleaned

and verified clean, prior to recommencing reactor

assembly.

22

On May 10, 1988, licensee

personnel

identified cleanliness

control

deficiencies in the Unit 1 Spent

Fuel

Pool including an incomplete

tool log.

Corrective actions consisted of completing the tool log.

Cleanliness

control problems

were identified by the

NRC from March

21 to April 22, 1988.

Additionally, gC personnel

issued

two stop

works on the

same subject

and licensee identification of problems

continue.

The licensee's

actions

up to the point of'he inspectors

involvement

were ineffective in that they did not identify additional debris

on

the reactor vessel

head which could be easily dislodged

and find its

way into the refueling cavity and possibly reactor vessel.

This is

a significant condition,

because

debris in the refueling cavity or

reactor vessel

could impact reactor operations

and fuel conditions.

This was true despite

memorandums

of instruction by the engineering

manager

and increased

gC surveillance.

The failure to take timely

effective corrective action to preclude

recurrences

of cleanliness

deficiencies

is an apparent violation of 10 CFR 50 Appendix

B

criterion XVI (Item 50-275/88-11-03).

e.

Pressurizer

Sur

e Line Movement

Trojan Nuclear Power Plant,

located in Region V, has experienced

movement of the pressurizer

surge line possibly

due to thermal

stratification.

The resident inspector contacted

the responsible

engineer at Diablo

Canyon to determine if evidence of movement or lack of it was

available for Diablo Canyon.

The licensee

had taken measurements

of

the pressurizer

surge line in Unit 1 relative to structure in 1983,

1986,

and during the current refueling outage.

Review of the

measurements

showed essentially

no movement of the pressurizer

surge

line relative to structure.

At the close of the inspection report

period the licensee

indicated that

some evidence

such

as pipe

burnishing indicated that in the hot condition the pressurizer

surge

line may be contacting pipe whip restraints.

The licensee

was

analyzing the findings, considering the addition of inservice

instrumentation to detect thermal stratification,

and planned to

pursue resolution with Westinghouse.

The licensee's

resolution will

be followed as

open item 50-275/88-11-04).

One violations and

no deviations

were identified

14.

Containment Inte rated

Leak Rate Test

ILRT

70307

and 70313

a 0

Procedure

Review

The inspector

reviewed the Unit 1 and

2 ILRT procedures

as described

in the licensee's

Surveillance Test Procedure

STP M-7, Revision

7 of

May 5, 1988,

(and the Temporary

Change Notices issued during this

inspection) entitled,

"Containment Integrated

Leakage

Rate Test

ILRT), Type A."

This review was to ascertain

compliance with plant

23

Technical Specifications,

regulatory requirements,

and applicable

industrial standards

as stated in the following documents:

o

Diablo Canyon

Power Plant, Units 1 and 2, Updated Final Safety

Analysis Report

(FSAR), Sections

3.8. 1. 7. 2, 3. 8. 1. 7,4,

and

6. 2. 1.4.

o

Diablo Canyon

Power Plant, Units 1 and 2, Technical

Specifications,

Section 3/4.6. 1.2, "Containment Leakage",

and

3/4.6.1.6,

"Containment Structural Integrity."

o

Appendix J to 10 CFR 50, "Primary Reactor

Containment

Leakage

Testing for Mater Cooled

Power Reactors."

o

American National Standard,

"Leakage-Rate

Testing of

Containment Structures for Nuclear Reactors,"

ANSI N45.4-1972.

o

Topical Report BN-TOP-1, Revision 1, "Testing Criteria for

Integrated

Leakage

Rate Testing of Primary Containment

Structures for Nuclear

Power Plants,"

Bechtel Corporation,

dated

November 1, 1972.

o

American National Standard,

"Containment

System

Leakage Testing

Requirements,"

ANSI/ANS-56. 8-1981.

o

IE Information Notice No. 85-71,

"Containment Integrated

Leak

Rate Tests."

During this procedure

review, the inspector

made the following

observations:

The procedure

requires

the containment. liner weld channels to be

vented. to the containment

atmosphere

during the test,

as is

required.

The inspector

noted that, at other plants,

these

channels

have not been vented during the test

and additional safety review by

the Office of Nuclear Reactor Regulation

(NRR) has

been required to

resolve this issue.

There is a discrepancy

in the procedure

concerning the test

acceptance

criteria.

Section 5.3.3 of the procedure

states that, in

accordance

with the provisions of BN-TOP-1,

Rev.

1, the end of test

95K upper confidence limit (UCL) for the calculated

leakage rate

shall

be less than

La.

However, in Appendix F; on the "Acceptance

Criteria Check Form-Data Sheet,"

the limit is 0.75 La, rather than

La.

The NRC's position is that the regulation,

Appendix J to 10 CFR 50, requires the acceptance

criterion to be 0.75 La,

as

does the

NRC's Topical Report Evaluation,

dated January

15, 1973, which

accepted

BN-TOP-1.

For the present test,

the acceptance

criterion

of 0.75

La was in fact satisfied.

Nevertheless,

the inspector

informed the licensee that section 5.3.3

was inconsistent with

acceptance

criteria requirements.

Section 5.4 and Appendix

F of the procedure

also specify that, for a

24-hour duration full pressure test according to 10 CFR 50, Appendix

24

J and ANSI N45.4-1972,

the calculated

leakage rate shall

be less

than 0. 75 La.

However, section III.A.3.(c) of Appendix J to 10 CFR 50 requires

the calculated

leakage rgte to be corrected for error.

Although no particular method is generally required,

many licensees

use

a 95K UCL, similar to the BN-TOP-1 procedure,

to account for

error.

For the present test,

the BN-TOP-1 procedure

was used.

The

licensee

has

marked

up the procedure with associated

clarifications

to be included in the next normal revision.

Review of Records

The inspector

reviewed calibration records for the instrumentation

used in the ILRT.

That is, the twenty-four resistance

temperature

detectors

(RTDs), six dew point temperature

sensors

(dew cells),

and

two pressure

gauges

used to measure

containment air mass,

and the

flow element

used to measure

the induced leak during the

verification portion of the ILRT.

All instruments

had been

calibrated within the last six months with NBS traceability.

In

situ checking of the instrumentation

had been performed within one

month of the test.

Although the procedure

did not provide instructions for containment

temperature

survey before the test to verify temperature

sensor

locations,

such

a survey was conducted,

as observed

by the inspector

and discussed

in the following section.

The inspector

requested

that the survey results

be included in the licensee's

test report to

the

NRC, which is due within three

months of ILRT completion.

Because

a temperature

survey will probably be performed

on Unit 2 in

preparation for the Unit 2 ILRT planned for Fall 1988, the licensee

should consider developing

a written procedure for this activity.

Observation of Work and Work Activities

Prior to the ILRT, the inspector

observed

a portion of the visual

inspection of the inner surface of the containment,

including the

containment liner.

No evidence of structural deterioration,

apparent

changes

in appearance,

or other abnormal

degradation

were

found.

The inspector

observed

the containment pressurization

equipment,

consisting of eight air compressors,

two after-coolers,

two air

dryers,

and connecting

hoses

and equipment.

During the containment

pressurization

phase,

two of the air compressors

were

out-of-service,

which somewhat

slowed containment pressurization.

Also, during most of the pressurization

phase,

one air dryer failed

to work.

The resulting higher moisture content of the air entering

containment

may have contributed to high relative humidity in the

containment,

which apparently

caused water condensation

on dew cell

No.

2 at the end of the test (during the verification phase).

This

was the apparent

cause of erratic readings

which resulted in removal

of the

dew cell from service.

This is discussed

further below.

The inspector witnessed

a portion of the pre-test

containment

temperature

survey.

Two surveys

were actually performed;

one with

25

the containment

fan cooler units running,

and one without.

This

information gave the licensee

the option to either run or not run

the fan coolers during the ILRT, as the validity of RTD placement

could be confirmed.

During this ILR1, the licensee

chose'to

not run

the fan coolers,

as running then introduces additional

heat sources

or heat sinks (depending

on cooling water flow and temperature)

which are difficult to control.

The licensee

stated that the

temperature

survey did confirm the validity of RTD positioning and

weighting factors.

The inspector requested that the survey data

be

included in the licensee's

report to the

NRC.

The inspector witnessed

selected

portions of the following ILRT

activities listed below and noted the time expended to perform each:

o

Initial pressurization

to 47 psig + 2/-0 psig', approximately

12

hours.

o

ILRT stabilization,

approximately 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />.

o

ILRT data acquisition.

o

Performance

of ILRT, approximately

42 hours4.861111e-4 days <br />0.0117 hours <br />6.944444e-5 weeks <br />1.5981e-5 months <br />, including a failed

initial test,

as discussed

below.

o

Leak rate verification test stabilization,

approximately

1

hour.

o

Leakage rate verification test,

approximately

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, with an

imposed leak rate of 7.5 standard

cubic feet per minute (SCFM),

which equals

La, which is 0.3X per day.

Various electrical

and mechanical

penetrations

were inspected.

Because

the typical containment isolation valve was vented

and

drained both inside

and outside containment,

the licensee

was able

to fit balloons over the ends of the vent lines outside containment,

so that balloon inflation would indicate leakage

pasted

the

containment isolation valve seats.

The licensee

checked

these

balloons approximately every two hours during the test, for

excessive

leaks,

but did not find any through the use of this

device.

During the test stabilization period,

RTD No.

21 failed high,

suddenly reading

121 degrees

F where it and other

nearby

RTDs has

been reading in the 60s.

Dew cell

No.

3 exhibited erratic readings

during the

same period.

Both sensors

had their weighting factors

set to zero

and their original weighting factors were reassigned

to

other nearby sensors for the duration of the test.

A few hours after starting the ILRT itself, it became

apparent that

the containment

was leaking excessively.

After about seven hours,

the measured

leakage rate

(Lam) had stabilized at a value of

approximately

0. 118K per day, whereas

the acceptance

criterion, 0.75

La, equaled

0.075K per day (La=0.3X per day).

Licensee

personnel

searched

exhaustively for leaks using soap bubble solution (Snoop)

and other methods.

Eventually they found that at one of the 48-inch

purge line penetrations,

there

was

a pressure

of 47 psig (or current

containment pressure)

between the two. closed isolation valves.

This

indicated that the valve inside containment

(RCV-ll) was either not

closed completely or was leaking very badly.

However, during the

ILRT, the valves

had been locally (type C) leakage rate tested only

a few days earlier

and

had passed that test easily.

The valve

outside

containment

(RCV-12) was found to have significant packing

leakage

and

some seat

leakage.

Another purge isolation valve outside containment

(FCV-661) in a

different penetration

was also found to have significant packing

leakage,

which would indicate

a leaking inside containment isolation

valve on this penetration.

About 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br /> into the test,

the licensee

opened

a vent valve

(approximately

one inch in diameter)

between

RCV-11 and -12, in an

attempt to depressurize

the space

between

the valves.

After

approximately

15 minutes,

the vent valve was closed

and the attempt

abandoned,

because

the pressure

between the valves

had not decreased

more than

a few psi.

This confirmed that valve RCV-ll was indeed

not limiting leakage

in any substantial

way.

Subsequently,

the licensee

took actions to eliminate or reduce

known

leaks, primarily by tightening

down on valve packing.

When that did

not reduce

leakage sufficiently on valve RCV-12, the licensee

took

the unusual

step of adding

one or more additional packing rings

on

the valve stem and tightened

down on those.

This step nearly

eliminated packing leaks

on valve RCV-12.

When the licensee

took actions to reduce

containment

leakage rate

by

repairing, adjusting,

or altering the containment pressure

boundary,

this caused

the test to be considered

a failure, in accordance

with

section III.A.1.(a) of Appendix J to 10 CFR 50.

In other words, the

containment

was leaking in excess

of the allowable limit, and the

only way to pass

the

test

was to take steps to eliminate leaks.

The licensee's

procedure

STP M-7, Rev.

7, also refers to this

circumstance

as "the initial unacceptable

ILRT," which must then

be

followed by another,

successful

ILRT.

After reducing leaks,

the licensee restarted

the test (or started

a

new test) at 8:44 p.m.

on May 19, 1988, approximately

28 hours3.240741e-4 days <br />0.00778 hours <br />4.62963e-5 weeks <br />1.0654e-5 months <br /> after

the initial start of the test.

Using the methodology of BN-TOP-l,

the test

was successfully

completed

some

12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> later.

There

was

then

some delay in establishing

the superimposed

leakage rate flow

out of the containment for the supplemental

or verification test.

The licensee

has run approximately

200 feet of small-diameter

(0.75

inch) plastic tubing from .a containment penetration to the two

Volumetrics thermal

mass flow meters installed in instrumentation

cabinet in the

DAS (data acquisition system)

shed.

This long,

narrow tubing could only pass

approximately

5 scfm, short of the

needed

7.5 scfm.

Therefore,

the licensee

resorted to a backup

mechanical

rotometer which was placed close to the containment

penetration

to allow the needed

flow.

With this delay and the

27

required (by BN-TOP-1) one hour stabilization period, the

verification test

was started at 11:29 a.m.

on May 20, 1988.

During

the verification test,

dew cell

No.

2, exhibited erratic behavior

which was appearing to cause

the test to fail to meet its acceptance

criteria.

Mhen the licensee

zeroed its weighting factor and

reassigned

the original weighting factor to other

dew cells, the

verification test passed.

The inspector

s preliminary conclusion

was that this action was acceptable,

but,

because it took place

after the inspector completed his inspection

and left the site,

NRC

review of the licensee's

justification for zeroing

dew cell

No. 2,

contained in the licensee

s report to the

NRC, will determine the

final acceptability of the action.

The inspector performed

an independent

computer calculation of

leakage

rates to verify that the licensee's

computer program

was

correctly calculating leakage

rates.

The inspector's

calculations

did indeed verify this.

The licensee's

preliminary results for the final 12 hour1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> Type A

test,

which did not include Type

C additions,

was

a total time

calculated

leakage rate of approximately 0.02K per day with 95K

upper confidence limit (UCL) of approximately 0.073K per day.

The

licensee's

maximum allowable leakage rate (0.75La) for this test

was

0.075K per day.

An approximately

8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> verification test

was

performed with an imposed leak rate of approximately 7.5

SCFM or

0.3X per

day of containment air mass.

The licensee

s verification

test produced

a total time calculated

leakage

rate that fell within

the test acceptance

criteria of approximately 0.095 to 0. 145K per

day.

These preliminary results

appear to be within the allowed

acceptance

criteria.

Conclusions

At the exit meeting held on March 20, 1988, the inspector stated

that the failed initial test would require, in accordance

with

section III.A. 6 of Appendix J to 10 CFR 50 and facility Technical Specification 4.6. 1.2.b., that the schedule for subsequent

Type

A

test

be reviewed

and approved

by the

NRC.

If two consecutive

Type

A

test failures should occur,

then

a Type

A test shall

be performed at

each plant refueling outage or every 18 months, whichever occurs

first, until two consecutive

Type A tests

pass,

whereupon the normal

test schedule

may be resumed.

However, the inspector

emphasized

that, in cases (like this test) where failure can be attributed to a

few specific penetrations,

the

NRC encourages

the licensee to

propose,

as

a formal exemption from the regulation,

a corrective

action plan which would address

the problem penetrations

in lieu of

increased

Type

A test frequency.

Such exemptions

are judged

on a

case-by-case

basis

and are not automatic; it is also unlikely that

the licensee

would be relieved from the first test

on the increased

frequency schedule,

and that

a test would likely have to be passed

successfully

before

an exemption would be granted.

28

e.

Subse

uent Information

After depressurizing

the containment, after completing the ILRT, the

licensee

conducted

a Type

C (local

le'akage rate) test

on RCV-11 and

-12, which passed with no repairs or adjustments

to the valves.

The

licensee

has preliminarily determined that RCV-ll (inside

containment)

may have

been installed,

maintained,

and or tested

improperly so that the valve leaks excessively

during an ILRT (and

so would during a LOCA), but not during the Type

C test,

which is

performed by pressurizing

the volume between

the two isolation

valves in the penetration.

Thus, the Type

C test measures

the

leakage rate through RCV-ll in a direction opposite to that which

would occur during

LOCA. It has

been thought that this

"reverse-direction" testing

was equivalent to testing in the

"forward" direction.

The licensee

also found that the inside

containment isolation in the second

purge line, FCV-660,

had the

same potential problem,

as did the congruent valves in Unit 2.

All

four valves were declared

inoperable,

and Technical Specifications

were satisfied.

Followup will be done under routine inspection.

No violations or deviations

were identified.

15.

Examination of Instrumentation

and Controls

I8C

A special

inspection

was conducted to examine the area of instrumentation

and controls.

The inspection

was performed by an

NRC contractor from

EG8G Idaho experienced

in the I8C area.

The results of the examination

are presented

in detail

as

an enclosure to

this report.

Areas for improvement identified by the inspector

and communicated

to the

licensee at an exit interview conducted

on May 19, 1988, included the

following:

The adequacy of procedures

was found to be mixed.

Repetively

performed surveillance test procedures

(STP's)

were generally found

to be detailed

and adequate.

There

was

one notable exception

and

that was

STP I-33B which is performed every refueling outage for

time response

testing.

STP I-33B was poorly prepared

despite

being

in preparation for several

months.

Loop test procedures

were not

addressed

since they were already

an issue which the licensee

has

laid out a plan to correct.

Corrective

and investigative

maintenance

procedures

in the form of work orders

were mixed in

thei~ quality from good to poor.

The licensee

was cautioned to ensure that procedure

review was

enhanced

to ensure

a critical review prior to issuance

and to ensure

a conformance to a uniform standard of detail.

The licensee

stated

that additional personnel

(5) had been hired to achieve procedure

improvements

and that plans were in place for revising writers

guides for future procedures

to satisfy both

NRC and

INPO

initiatives in this area.

29

The issue of poor procedures

in the

IBC area

and the untimely

correction of those

problems

has

been the subject of previous

inspections.

The recent licensee action to apply resources

to the problem is

encouraging.

The effectiveness

of and timeliness of the licensee's

future actions will continue to be monitored in future inspections.

16.

Exit

a.

Routine Exit

30703

On May 27, 1988,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph l.

The inspectors

summarized

the scope

and findings of the inspection

as described

in

this report.

b.

Exit and

Mana ement Meetin

s

30702

Additionally, in discussions

with senior plant management

on April

22, 1988, the Plant Manager committed to the following:

1)

An action plan will be developed

by May 6, 1988,

and will

address

the following:

The current practice for the development of event response

action plans,

including schedule for implementation, will

be incorporated

in new or revised plant administrative

procedure(s).

Criteria will be incorporated in revised or new

administrative procedure(s)

to lower the threshold for

events

which will be subjected to formal root cause

determination.

Specific consideration will be given to revising current

guality Control/Administrative Procedures

to require root

cause determination in the dispositioning of guality

Evaluation (gE) reports, of which there were

a total of

approximately

660 in the year 1987.

I&C MAINT NANCF.

VALU TION

OF THE

DIABLO CANYON POWER

PLANT

1. 0

INTRODUCTION

An evaluation of the Diablo Canyon

Power Plant

(DCPP) Instrumentation

and Control

(I&C) Maintenance

Department

was performed during the periods

of March 28 through April 8,

and

May 3 through

May 19,

1988.

The

guidelines

used for this evaluation

were the United States

Nuclear

Regulatory

Commission

(NRC) Inspection

Procedures

52051,

52053,

62704,

and

62705.

Some areas of concern with respect to the preparation

and planning

of procedures

and work orders

were identified.

Three primary areas of I&C maintenance activities were the focus of

this inspection:

I)

Are the

I&C technicians technically competent?

2)

Are the procedures

used

by the

I&C technicians

good

procedures?

3)

Do the technicians follow the procedures?

Another question

was raised during the inspection with regards to

Quality Control

(QC) involvement with the

I&C work activities.

Most of the inspection effort was directed at the

I&C maintenance

groups which dealt with the plant protection

systems

and other systems

important to safety.

Therefore,

the caliber of the technicians

and

quality of the work packages

were expected

to be the best representations

of the

I&C maintenance activities.

2.0

CAPABILITIES OF THE TECHNICIANS

The maintenance

and surveillance activities performed

by the

technicians,

for the most part,

were observed to be done in a satisfactory

manner with the technicians

displaying

an adequate

knowledge of the tasks

required within the work packages.

The technicians

spent time acquainting

themselves

with the proper background material

and systems

information to

gain

an understanding

of the tasks to be performed

and to obtain the

necessary

tools

and test equipment prior to beginning their work

activities.

The efforts of removing the device or system

from service,

0

the corrective maintenance

or surveillance activities,

and the task of

returning the device or system

back in service were all performed in an

acceptable

manner.

A few of the technicians

observed

were outstanding

in the skills they

possessed

or their work habits.

A few others

were observed

as either

somewhat lethargic or almost recklessly fast.

Overall however,

the

technicians

seemed

genuinely interested

in doing

a good job and were

conscientious

and professional

with their work.

No unsatisfactory

work

was observed

due to the skills of the technicians.

3.0

ADE(UACY OF THE PROCEDURES

During this inspection,

28 activities associated

with procedures

were

evaluated.

Nine of the activities were

Loop Tests,

11 of the activities

were Surveillance Tests

(STPs),five of the activities were for Corrective

Maintenance,

and three

procedures

were reviewed

as examples of what

some

DCPP

I&C personnel

considered

good procedures.

For all but the three

example procedures,

the work activities of the technicians

as well as the

adequacy of the procedures

were evaluated.

No work activities were

observed with respect to the three

example procedures,

only the procedures

themselves

were reviewed.

3.1

Loo

Test Procedures

Since the

Loop Test Procedures

have received previous attention which

has identified them

as being inadequate,

and

a program to update

and

improve the

Loop Tests

has

been initiated, not much emphasis

was placed

on

these

procedures.

The work activities associated

with these

procedures

was the main interest of the

Loop Tests,

and the technicians

were able to

perform the tests

in spite of the poor procedures,

primarily due to their

familiarity with the system.

3.2

Surveillance Test Procedures

The adequacy of the

STPs

was found to vary.

Some of the

STPs,

such

as

those

performed

on

a frequent basis,

contain

adequate

detail

and

instructions to efficiently complete the task.

However,

even

DCPP

personnel

have recognized

a deficiency in the quality of some of the

STP

procedures

and

have

implemented

a program to update

them.

Examples of the

plant awareness

of the inadequacies

of the procedures

are the rewriting of

STP-I-8B for the Reactor Coolant Flow Transmitters

and STP-I-33B for Time

Response

Testing of the Reactor Trip and Engineered

Safety Features

(ESF)

Logic.

The

SB and

33B procedures

required rewriting because

of a lack of

'detail

and were confusing in giving direction to the technicians.

STP-I-8B is being rewritten to consolidate

several

procedures

and

make

the procedure

more concise.

The writing of this procedure is utilizing.

several

concepts,

such

as

human factors,

and will be used

as

a model for

r

procedures

rewritten in the future.

A review of the rough draft of this

procedure

indicates

a positive step toward standardizing

and improving the

procedures.

A considerable

amount of time was spent reviewing STP-I-33B and

observing the technicians activities while working on this task.

Because

this procedure

was

a new procedure

(approved 4/22/88)

and time response

testing of the safety

systems

is important, it was felt that this

procedure

should

be representative

of the type of procedure

DCPP plans to

produce in the future.

However, this

new procedure

(admittedly better

than the old 33B procedure)

had several

deficiencies

and the

I8C personnel

admit that the procedure is not

a good one despite

having spent

seven

months rewriting the procedure.

The most significant problems with the

new 33B procedure

were

a lack

of specifics

and clarity.

The prerequisites

were vague

and incomplete in

describing the equipment

needed

to set

up the test, (i.e.,"5.

Toggle

switch(s)." vs the actual

number of switches required).

The instructions

for setting

up the test equipment

were

so limited that

a technician

performing the test for the first time, probably couldn't set

up the

equipment without assistance.

Even technicians

that

had previously

performed the test

had difficulties and

had to make several

phone calls to

resolve questions.

The procedure

should contain

enough detail that the

technicians

can perform the tasks without requiring prior experience

with

that particular procedure.

An example of how a lack of adequate

research

and

a lack of detail in

the procedures

creates

problems

was observed

during the performance of

Part

10 of the

33B procedure

which measures

the time response for the

Overtemperature

Delta T Reactor Trip.

Initially, the technicians

could

not obtain repeatable

results for this test.

An on-the-spot tailboard

between

a supervising technician

and engineer

determined that the problem

was due to a module failure.

A Work Order was generated

to check the

module

and it was determined that the module

had not failed.

Further

investigation determined

the problem to be incorrect values given in the

procedure for simulating the hot leg and cold leg temperature

inputs.

For

a test

as important

as the safety

system time response

testing,

adequate

research

and systems

knowledge should ensure that the primary system

temperature

parameters

are correctly entered

in the procedure.

The research

required to write a detailed

procedure

might prevent

some

of this type of confusion

and delay.

Also, dry running

a new procedure

can sometimes

help in debugging the document

so that the final result is

a

procedure that is correct

and efficient to use.

The

ILC Manager indicated

that the

IKC policy is currently to dry run

new and revised

procedures

as

much as practicable.

The

DCPP

I8C Department

agrees

that the

new STP-I-33B procedure

is not

a good model for future procedures

and was not intended to be.

However',

to spend

seven

months rewriting

a procedure that is known to be deficient

appears

Co be self defeating.

This effort indicates either

a lack of

commitment to having good procedures

or an only good enough to get by

approach.

A logical conclusion would be that the procedure

was not given

enough

emphasis

to complete properly and

when it came time to perform the

test,

the procedure

was signed off as good enough

so the task could

proceed.

3.3

Corrective Maintenance

Of the five Corrective Maintenance activities observed,

one of the

Work Orders represented

an excellent effort of planning

and procedural

preparation,

and one of the Work Orders contained

elements

which are

considered

inadequate

and unsatisfactory.

The other three

Work Orders

satisfactorily represent

something

in between

these other two extremes.

The Corrective Maintenance activity associated

with the Unit 2

Pressurizer

Pressure

Transmitter

(PT-474) contained detailed descriptions

not found in most of the other

DCPP maintenance

documents.

Perhaps this

was

due to the high visibility of the consequences

of not performing this

task in

a rigid manner.

However, the tasks

performed, i.e.,

opening

valves, returning to service, etc.,

were explained very explicitly in the

Work Order for this activity.

An example of a Corrective Maintenance

Work Order with virtually no

planning or direction for the technicians

was observed

during the work

performed

on the pressure

switches,

PS-45/PS-46,

for the

CCW Heat

Exchangers.

This Corrective Maintenance

was generated

by Engineering at

the request of Operations

to reduce

the number of nuisance

alarms in the

control

room.

When the request

to perform the work was denied

by

Operations

because it didn't fix their problem,

the engineers

changed

the

Work Order.

The module requiring the correction did not respond

as

expected

and

so another

Work Order was written to "GIVE DIRECTION TO

REPLACE 1PS-46A/46B"

and then the directions

were to

"REPLACE IPS-46A/46B

AS REQUIRED TO

ENSURE

PROPER

LOOP OPERATION."

When the technicians tried

to complete this task,

they discovered that the power supply was

common to

other systems.

The technicians

researched

drawings

and other

documentation

to determine the effects that disturbing the power supply

would have

on other systems

in the plant.

It was determined that the work

could not continue

and was scheduled for a later date.

Operations later

informed the technicians

that the system believed to be affected

was not

in service

anyway,

so the work could have

been

performed at the originally

scheduled

date.

This research

should have

been performed at the planning stage

by an

engineer,

a supervising technician,

or the planner.

The

I&C Technicians,

besides

performing their technical

tasks,

should not be totally

responsible for determining the effects their efforts have

on the overall

plant.

They should

be given direction through the use of detailed,

informative procedures

and work orders.

3.4

Exam le Procedures

The three procedures

reviewed

as examples of what responsible

ISC

personnel felt were good procedures

were maintenance

procedures.

Procedure

I5C MP 4,1-1A for checking the calibration

on an audio

oscillator and power amplifier is an example of an excellent procedure.

This procedure

contains specific prerequisites,

precautions,

and

instructions,

and

was approved

in 1982.

This indicates that the ability

to prepare

good procedures

has

been available at

DCPP in the past.

In

updating the other

ISC procedures,

some of the features of this procedure

should

be considered.

4.0

ADHERENCE TO

PROCEDURES

For most of the

Loop Tests,

STPs,

and Corrective Maintenance

Work

Orders,

the technicians

familiarized themselves

with the tasks to be

performed

and then performed the tasks

per the procedures.

In several

cases

the technicians

appeared

to be

so familiar with the procedure that

it was difficult to determine if the technicians

were actually following

the procedures

or simply filling in the test data.

The only instances

where the technicians

obviously did not follow the

procedures

involved transferring test data from strip chart recorders

to

the data blanks in the procedure.

This occurred during STP-I-338,

where

not only was the data not properly transcribed,

but the strip chart

recordings

were not kept with the work package

where the data could

be

reviewed.

On site follow-up showed this problem to be one of lax follow

through of administrative controls of data, i.e., this problem had

no

technical significance

however.

QUALITY CONTROL INVOLVEMENT WITH IBC WORK ACTIVITIES

While reviewing the

IBC work packages

and observing

I8C technicians

in

the field, an apparent

lack of QC involvement

was noted.

Several of the

IKC technicians

stated that they didn't feel that the

QC personnel

were

qualified to review I8C work anyway.

Therefore,

some time was spent

reviewing the process

by which

QC determines

which jobs are inspected,

and

how many they actually look at.

When the Work Orders

are generated

by the

IEC planners,

a

QC planner

reviews the package

using

a standard checklist.

If the package

contains

the information required

in the checklist then

QC may choose to perform an

inspection or surveillance

on the work activity.

This checklist method

seems to be

a reasonable

attempt at giving all work packages

the

same

level of review and ensuring inspections

are performed

on

a consistent

basis.

E

A computer search

was done to determine

6ow many Work Orders

were

reviewed

and

how many inspections

and surveillances

were performed

on

those

Work Orders.

Data was obtained for the time periods

from

Harch 28,

1988 through April 8,

1988.

and from Hay 2,

1988 through

Hay 13,

1988

During the Harch

28 through April 8 time period,

58 packages

were reviewed with nine inspections

and

10 surveillances

performed.

For

the time period from Hay 2 through

Hay 13,

74 packages

were reviewed with

15 inspections

and five surveillances

performed.

Both of these

samples

indicate that

gC is involved with approximately 30/ of the jobs in the

field.

No attempts

were

made to determine

how intense or effective these

inspections

and surveillances

were,

but it appears

that the

same

amount of

involvement occurred during both time periods.

If inspections

were

required,

then not as

many surveillances

were performed.

When there

were

few inspections,

then more surveillances

were performed.

This amount of involvement

(30%) appears

to be

a reasonable

amount of

review.

6. 0

CONCLUSIONS

The evaluation of the

IKC Haintenance

Department

was performed to

determine if the organization

was operating

in an effective manner

and in

the best

way possible.

The technicians,

both

DCPP and contractors,

performed their tasks with

an average

level of ability and professionalism.

The procedures

used

by the

IEC Haintenance

Department consist of both

good

and

bad procedures.

Some of the

STPs

and maintenance

procedures

represent

adequate,

detailed procedures.

However,

some of the

STP

procedures

and

Loop Tests,

and

some of the Work Orders for Corrective

Haintenance,

lack detail

and direction.

Good procedures

and proper

planning

can not only give instructions

and directions for performing

a

task, they can also prevent the work activities from being performed out

of control.

DCPP agrees

that

some of the procedures

require attention

and

have

implemented

several

programs to update

and improve the procedures.

However, there

are

no strong perceptions

that these

pr'ograms

have

a total

commitment

by the plant staff and that the procedures will be updated

in a

timely manner.

The technicians

adequately

followed the procedures,

especially

when

critical functions or sensitive tasks

were being performed.

v

0

APPENDIX A

The following people were the primary contacts while performing this

evaluation.

lk. G. Crockett

C. A. 'Hetter

J. J.

McCann

A. G. Moore

J.

R. Tinlin

l<. L. Brown

D. 0. Malone

L. Kase

J.

Hickman

D.

R.

Geske

R. S. Fairchild

S.

V. Noe

I8C Haintenance

Manager

IKC Maintenance

General

Foreman

Instrument Haintenance

Foreman

Instrument Haintenance

Foreman

Instrument Maintenance

Foreman

Supervising Technician

Compliance

Engineer

I8C Planner

IKC Planner

Lead

gC Specialist

QC Specialist

gC Specialist

Other persons

interviewed were the

IKC Maintenance

Technicians

and the

management

personnel

attending

the entrance

and exit meetings.

V

I

APPENDIX B.

or

Order

Unit

~Activit

~Sstem

iR0039357

C0013865

R0005365

R0004749

R0004703

R0004798

RQQ10540

R0022494

R0021550

R0022508

R0020429

2

STP- I-16A

1

Corrective Maintenance

1

STP- I-54

1

STP-I-8B3

1

STP- I-8B3

1

STP- I-8B3

1

STP-I-91B

1

LC-21-13B

1

LT-21-18F

1

LT-21-18G

1

STP- I -6B3

R0021791

-

2

LC-10-4

C0030212

R0024828

'0022327

R0022328

R0022329

R0022295

R0005035

R0005034

R0025281

ROQ10982

2

Corrective Maintenance

1

LCV-110 (3-109)

1

LC-7-221A

1

LC-7-221B

1

LC-7-221C

1

LC-7-221D

1

STP-I-72B

1

STP- I-72B

1

STP-I-72B

1

STP- I-33B1

SSPS

Logic Train

B

PS-46A

CCM

PT-506

Hain Turbine

FT-444

RCS

FT-445

RCS

FT-446

RCS

Thermocouple Monitoring System

LS-207

DG 1-2

TS-96

DG 1-2

TS-97

DG 1-2

PT-474

Pressurizer

FIG-641B

RHR 2-2

PT-474

Pressurizer

PC-86

Aux Feed

TH-411D

Delta T Deviation

TH-421D

Delta T Deviation

TM-431D

Delta T Deviation

TM-441D

Delta T Deviation

ENST-1

Seismic Trip

ENST-2

Seismic Trip

ENST-3 Seismic Trip

Reactor Trip & ESF Logic.

F',

}lork Ord er ..gnit.....~Activit

~Sstem

C0032061

C0032191

C0026709

1

Corrective Haintenance

Support for STP-1-3381

1

Corrective Haintenance

TC-411A

Nodule Check

1

Corrective Maintenance

Lead/Lag Hodules

N/A

N/A

N/A

N/A

IKC MP 4.1-1A

N/A

MP I-2.28-1

N/A

MP I-2.14-2

Test Equipment Calibration

RVRLIS Calibration

Reactor Coolant

RTDs

r,

~

PI