ML16341E604

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Insp Repts 50-275/88-04 & 50-323/88-04 on 880131-0305. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities,Followup of Onsite Events, Open Items & LERs
ML16341E604
Person / Time
Site: Diablo Canyon  
Issue date: 03/16/1988
From: Johnston K, Mendonca M, Narbut P, Padovan L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341E603 List:
References
50-275-88-03, 50-275-88-3, 50-323-88-04, 50-323-88-4, NUDOCS 8804130022
Download: ML16341E604 (42)


See also: IR 05000275/1988004

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos:

50-275/88-03

and 50-323/88-04

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

January

31 through March 5,

1988

Approved by:

L.

M. Padovan,

Resident Inspector

K.

E. Johnston,

Resident

Inspecto

~~+~

e c

P.

P. Narbut, Senior Resident

Inspecto

M.

M. Mendonca,

Chief

Reactor Projects

Section

1

Date Signed

~/~ugs

~

Date Signed

Date Signed

Date Signed

~Summaa

Ins ection from Januar

31 throu

h March 5

1988

Re ort Nos.

50-275/88-03

and

50-323/88"04

operations,

maintenance

and surveillance activities, follow-up of on-site

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

30703,

35701,

37700,

61726,

62703,

71707,

71709,

71710,

71881,

90712,

92700,

92701,

92702,

93702,

and 94703 were applied during this inspection.

Results of Ins ection:

Two violations and

no deviations

were identified.

8804130022

880328

PDR

ADOCK 05000275

Q

DCD

DETAILS

Persons

Contacted

  • J. D. Townsend,

Plant Manager

J. A. Sexton, Assistant Plant Manager,

Plant Superintendent

  • J. M. Gisclon, Acting Assistant Plant Manager, .Support Services
  • W. B. McLane, Acting Assistant Plant Manager, Technical

Services

  • C. L. Eldridge, guality Control Manager
  • M. E. Leppke, Onsite Project Engineer
  • K. C. Doss, On-site Safety Review Group
  • T. A. Bennett, Acting Maintenance

Manager

D. A. Taggert, Director guality Support

  • M. J. Angus,

Work Planning

Manager

  • W. G. Crockett, Instrumentation

and Control Maintenance

Manager

J.

V. Boots, Chemistry

and Radiation Protection

Manager

  • L. F.

Womack, Operations

Manager

  • T. L. Grebel, Regulatory Compliance Supervisor

S.

R. Fridley, Senior Operations

Supervisor

  • G. M. Burgess,

Senior

Power Production Engineer

The inspectors

interviewed other licensee

employees

including shift

foreman

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

  • Denotes those attending

the exit interview on March 11, 1988.

0 erational

Status of Diablo Can

on Units I and .2

Unit 1 began

the reporting period at full power and coasted

down during

the period to 64K power due to fuel burnup.

The Unit planned to begin

its second refueling outage

on March 4, 1988, but this was delayed

due to

the Unit 2 reactor trip on March 3, 1988.

Unit 2 operated

at

100% power during the reporting period except for

planned reductions

in power for testing,

an

OP delta

T turbine runback

and

a reactor trip on March 3, 1988, described later in the events

portion of this report.

The Acting Plant Manager for Diablo Canyon,

Mr. J.

D. Townsend,

was

formally selected

as the Plant Manager in February.

He had

been acting

in the capacity since July 1987.

The Region

V Director of Reactor Safety

and Projects,

Mr. D. F. Kirsch,

examined

the site for several

days during the report period

and held

discussions

with plant management.

Key points discussed

were the

need to

ensure plant design

bases

were clearly understood,

transmitted to the

site personnel,

and properly implemented

in the processes

of maintenance

and modifications.

He indicated the

need for management

to clearly

establish

goals,

determine

how to implement

them and

commence

a timely

implementation.

A second

key point discussed

was the need for plant

management

to become

more aware of plant conditions through first hand

observations

and entries into radiologically controlled areas.

The Region

V Reactor

Projects

Branch Chief, Mr. R.

P.

Zimmerman, also

examined the site

on

a different week of the reporting period

and

had

discussions

with plant management.

Key points discussed

were the

apparent

large

number of relatively old (late 1986, early 1987),

uncorrected

action requests

for maintenance

and the lack of approved

annunciator

response

procedures

at the auxiliary operations

control

station.

0 erational

Safet

Verification

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's facility.

'Fhe observations

and examinations of those activities were conducted

on a

daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs)

as prescribed

in the facility Technical Specifications

(TS).

Logs,

instrumentation,

recorder traces,

and other operational

records

were

,

examined to obtain information on plant conditions,

and trends

were

reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on

a sample basis to verify that all pertinent information

of plant status

was relayed.

During each

week, the inspectors

toured the

accessible

areas

of the facility to observe

the following:

(a)

General

plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the licensee's

administrative controls

and approved

procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Essential

safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

Ko violations or deviations

were identified.

~

~

~

4.

Onsite Event Follow-u

a 0

Centrifu al

Char in

.Pum

CCP

1-2

On February 23, 1988, during clearance activities associated

with

corrective maintenance

(shaft seal

replacement)

on

CCP 1-2, the

150

pound class suction piping to the

pump was subjected

to excessive

pressure.

During the

pump clearance

process,

in accordance

with clearance

number 10969,

an auxiliary operator

(AO) attempted to close charging

pump outlet valve CVCS-1-8389B.

The valve was difficult to close,

which the auxiliary operator characterized

as

normal for charging

pump discharge

valves with tight packing, but the

AO believed the

valve was shut.

He then'closed

other specified isolation valves

and

began closing

pump suction valve CVCS-1-8394B

as specified in

the clearance.

As the suction valve neared

the closed position,

water began spraying from I) the packing gland of the suction valve,

2)

a compression fitting on suction line pressure

indicator (PI)

192B,

and 3) the diaphragm of the PI isolation valve I-8484B.

The

pump casing drain valves to the miscellaneous

equipment drain

were

opened to further relieve the pressure

and abate

the spray.

An

auxiliary control operator, after alerting control

room personnel

to

the situation, returned to the

pump discharge

valve and

was able to

close the valve an additional half turn and stop the spray.

Several

hundred gallons of demineralized

CVCS water were routed to the

auxiliary building sump through floor drains before the leaking

piping was isolated.

The licensee's

investigation revealed that high pressure

(about

2400

psi) demineralized

RCS water from the discharge of operating

CCP 1-1

had passed

through the incompletely closed

CCP 1-2 discharge

valve,

and back flowed through

a leaking discharge

check valve (I-8478B)

which pressurized

the

pump suction piping once the suction valve was

closed.

The licensee

developed

an Action Plan to further investigate

the

incident and determine

necessary

corrective actions.

The plan

included procedure

revisions to ensure

the charging

pump suction

pressure

is observed

in future isolations of the charging

pump for

maintenance,

inspection

and repair of the check valve, replacement

of the charging

pump seals,

r epair of the diaphragm valve and other

leaking components,

and performance of engineering

evaluations of

overpressure

effects

on the

pump suction piping and

pump casing.

The engineering

evaluation

determined that the overpressure

condition was acceptable

for continued operation.

The licensee

estimated

the overpressure

achieved

was not greater

than

500 psi

(the design

pressure

is 210 psi).

The acceptance

was

based

on

discussions

with component

vendors, liquid penetrant

examination of

the highest stressed

welds, visual examination for distortion,

calculations

showing stress

levels

remained

below code allowable

limits, and in-service leak test

and

pump operability tests.

Additionally flange bolt torques

were checked for any relaxation

(none found relaxed).

After the completion of corrective actions

and testing the

pump was

declared

operable

and returned to service.

The inspector considered

the following items related to the event

as

open:

o

Manuall

0 crated Casualt

Valves

The licensee's

action plan did not address

the charging

pump

discharge

valve.

The valve was difficult to operate

and was

not initially fully shut.

Subsequent

discussion

indicated that

the licensee

considered

that with check valve leakage,

the high

differential pressure

across

the discharge

valve (a manual

gate

valve)

made closure very difficult and this was satisfactory.

The valve was subsequently

cl'osed with force.

The inspector

asked

the licensee

to consider

the lessons

learned

from other

operating plants.

Specifically, that manual isolation valves

which are counted

on to be functional in casualty or emergency

procedures

ought to be capable of manual operation.

Inspector discussions

with operations

personnel

indicated that

simple design

changes

such

as packing changes

or a racheting

handwheel

might ease

operation of such high head high D/P

valves.

The licensee

committed to examine

manual

valves

used in

casualty situations

to ensure

they are operable

(follow-up item

50-275/88-03-01).

o

Meanin ful Acce tance Criteria for 0 erations

Personnel

The inspectors

spent

some time exploring the operability of

charging

pump 1-2.

This was addressed

carefully because

the

pump had

been

noted to have shaft leakage

on swing shift

February 22, 1988, at

a time when the diesel

generator

servicing the other charging

pump (1-1) was out of service.

The shift foreman

had decided

the

pump 1-2 was operable

but not

desirable

to be operated

because

the leakage,

about

200 ml/min,

would contribute to airborne activity.

Subsequent

discussions

showed that decision to be correct but

not an immediate

and obvious conclusion.

Charging

pump 1-2 was

capable of automatic start

and delivering emergency

flow to the

reactor coolant system if called upon.

Its operability in

a

post

LOCA environment during recirculation from the containment

sump

was questionable

but,

based

on revised estimates

of

acceptable

leakage rates,

was subsequently

determined to be

acceptable.

The guidance available to the shift foreman in making the

proper decision

was lacking,

however.

The guidance available

was found in test procedure

STP P-2B,

"Routine Surveillance Test of Centrifugal

Charging

Pumps,"

which has

as acceptance

criteria:

"Seal

leakage

normal"

(Yes/No), "Ifthis had not been satisfied,

declare

pump

inoperable."

The inspectors

considered this criteria to be insufficient

qualitative or quantitative

acceptance

criteria.

The

FSAR

contained

a limit of 10 cc/hr as

an assumed

seal

leakage for

post

LOCA habitability studies.

At the exit interview licensee

management

stated that

consideration

would be given to defining more reasonable

acceptance

criteria for this and other tests at least to the

point of invoking administrative limits which would trigger

future operability analysis.

The licensee's

actions will be followed up in the course of

future normal inspection functions.

For tracking purposes this

item is opened

and closed in this report (Follow-up item

50-275/88-03-02 - closed).

It should

be noted that this item is similar to the lack of

acceptance

criteria violation associated

with the containment

fan cooler unit drains,

item 50-323/87-38-01.

No violation is

considered

warranted in this case

since qualitative criteria

were provided.

b.

Nuclear

Instrument Inverter IY-13 Failure

On February 9, 1988, operators

discovered

the output of the Unit 1

120 Vac nuclear instrument inverter had degraded

to 60 Vac

Subsequent

investigations

found no breakers

tripped and the smell of

something burning.

The licensee

swapped

loads

and de-energized

the

inverter.

The licensee

subsequently

determined

the inverter transformer

had

failed and this type of failure had been described

in a 1984

Westinghouse

(the transformer manufacturer)

Technical Bulletin.

This event will be described

in Licensee

Event Report

(LER)

50-275/88-06.

The inspector will review this event, its root cause

and proposed corrective actions,

during the course of routine

LER

review.

The Westinghouse Bulletin had provided two options to determine

adequacy.

Either high potential testing or six months of

satisfactory

performance.

Since the licensee's

inverters

had been

in operation greater

than six months,

they were believed to be

acceptable.

Westinghouse

is currently pursuing

10 CFR Part 21

reportability implications of the event.

Unit 2

OP Delta

T Actuation and Turbine Runback

On January

31,

1988, at 4:06 a.m.

PST with Unit 2 at

100 percent

power, the licensee

declared

an unusual

event

as

a result of an

OP'elta

T reactor protection actuation which caused

a turbine runback

to 87 percent

power.

A reactor trip properly did not occur,

as the

OP de'Ita

T reactor trip setpoint

was not reached.

The

OP delta

T control actuation

(C-4) was caused

by inadvertent

steam

loads

induced in the moisture separator

reheaters

(MSRs)

on

the secondary

side of the plant.

A senior reactor operator

(SCO),

performing troubleshooting activities

on

a

MSR shell water level

control valve, shorted

the

120 vdc power supply'o the valve

solenoid which opened

a

120 vdc power supply breaker.

Twelve high

level spill valves from the

MSR high pressure

drain tanks

and

MSR

low pressure

drain tanks

opened

on the loss of power, causing part

of the main steam

and reheat

steam to be bypassed

to the condenser.

The turbine Control system

responded

to the reduced turbine first

stage

pressure

and increased

steam

demand

by opening the turbine

governor valves further.

Tavg decreased

and

as rod control

was in

manual,

the resultant

RCS cooldown resulted

in reactor

power

increasing

to 103.6 percent.

Operators

began to manually reduce

turbine load,

and

120 vdc power was reestablis'hed

to the high level

spill valves closing the valves

(power was reestablished

within

three minutes of the breaker opening).

Steam flow immediately

decreased,

causing

RCS Tavg to increase

to the

OP delta

T rod

stop/turbine

runback setpoint.

Reactor

power was

above

100 percent

for about

two minutes.

The cause of the event

was the

12

MSR high level spill valves

opening

as

a result of the

SCO's troubleshooting activities.

The

SCO had

a voltmeter in the ammeter

mode when

he touched the leads

across

the solenoid valve relay.

This caused

a short of the

120 vdc

to ground.

He had been troubleshooting

the

MSR 2-1B shell level

control

and

had successfully

done

a few voltage

and fuse continuity

checks prior to the event.

The

SCO was not specifically authorized to do the troubleshooting

activities,

and

had

no written instructions.

Additionally, an

Instrumentations

and Controls

(ISC) shift technician

was available

for this purpose.

The problem

had

been previously defined,

and

an Action Request

(AR)

existed

on the

MSR level control valve but had not been acted

on for

several

weeks.

However, the

AR had not been given

a component

code

(Identification

( ID) and Functional

Equipment

Group

(FEG) numbers)

when

it was entered

into the computer

and therefore

was not readily

identifiable and would have required

a search of all Unit 2 main

steam

system

ARs.

Additionally, no caution tags, info tags,

or AR

stickers

were in place to indicate the problem had

been identified.

Following the event,

the licensee

established

an Action Plan.

The

emphasis

of the Action Plan was to properly address

not only the

root cause

but also all other problems identified during the event.

Corrective actions included involvement of the

SCO who personally

took part in addressing

Action Plan items.

The operations

department

established

a written policy on operations

troubleshooting activities, in which the following was stated:

"l.

Operators

shall rely on installed plant instrumentation

and

components

to accomplish troubleshooting activities.

2.

Operators'se

of test equipment for troubleshooting

on

energized/in

service plant equipment shall

be limited to using

hand-held temperature

probes or similar devices.

Use of

volt/ohm meters is limited to checking fuses which have

been

removed from the circuit.

3.

All troubleshooting activities shall

be preplanned,

the

preplanning

session

should include an Action Request

search

on

the component

ID and

FEG for the component in question.

4.

The results of any troubleshooting shall

be documented

on the

AR for the problem in sufficient detail

so that the steps

need

not be repeated."

A number of Action Plan items were established

to evaluate

the

AR

tagging system,

the

AR priority system,

and backshift support for

corrective maintenance activities, specifically in the I8C area.

At

the time of this report these evaluations

had not been

completed but

will be followed by the inspector during routine inspection.

Also,

a number of Action Plan items were initiated to perform long

term evaluations

of the secondary plant systems

involved in the

event,

such

as main turbine

and

MSR control.

Finally, a number of corrective actions

were taken to reevaluate

the

reportability of the event.

The licensee's

Emergency

Plan stated

that an

Op delta

T "actuation" is an Unusual Event.. However,

upon

reevaluation

the licensee

is considering

the turbine runback

initiation as

a control function and not a protective actuation

as

a

reactor trip would be.

The licensee

had not concluded this

evaluation at the time of this report.

'This will be followed up

during routine inspection.

In summary,

the corrective actions

taken appear to be appropriate.

However, this appears

to be another

example of'n event resulting

from plant personnel

going outside or without written procedures.

Other

examples

include the CVI actuation described

in section 4.d.,

the

RHR pipe heating event (inspection report 50-323/87-39),

and

events during the Unit 2 first refueling outage including the

inadvertent diesel

generator start,

the loss of RHR event,

and the

8'avity

drain

down event.

It appears

that the licensee

should focus

greater attention

on this issue.

Unit 1 Containment Ventilation Isolation

Due to the Inadvertent

Groundin

of a Vital Inverter

On February

17, 1988, the licensee

made

a four hour non-emergency

report as

a result of an

ESF actuation,

a Containment Ventilation

Isolation (CVI) on Unit 1.

The CVI occurred

as

a result of the

momentary grounding of'20 Vac Vital Inverter

PY llA.

The ground

occurred

as

a result of a ground wire not being removed during the

the accomplishment of a design

change

on three

chemical

and volume

control

system flow transmitters.

When the associated

120 Vac

breaker

was closed,

to return the transmitters

to service for

testing,

the inverter was momentarily grounded.

This resulted in an

undervoltage

condition which caused

a number of bistables

to trip,

including a CVI.

Prior to the event,

Design

Change Notice (DCN) DCI-SE-39078

was

issued to install fuses for the sensing

head

and the transmitter,

for flow transmitter

(FT) 113 and flow meter

(FM) 113 (emergency

boration flow), FT ill/FM 111 (primary water to the boric acid

blender),

and

FT 110/FM 110 (boric acid blender inlet).

FM 113

provides Technical Specification

emergency boration flow monitoring

which has

a seven

day action statement.,

FM 110 and

FM 111 are part

of the reactor

makeup control system.

During a meeting between

General

Construction

(GCg electrical

and the clearance

coordinator

it was decided that two hours would be sufficient time to perform

the work and that the work should

be performed expeditiously

so that

the reactor

makeup control

system indication would not be out of

service for more time than necessary

to complete the job.

On February 17,

1988, at 8:40 a.m.,

the

GC field engineer

and the

work planning coordinator discussed

the job with the shift foreman.

The

GC field engineer

had not been

aware of the earlier discussions

with the clearance

coordinator which established

that two hours

would be sufficient time to complete the work.

This agreement

was

established

as guidance

on the clearance

request.

During the 8:40

a.m.

meeting,

the shift foreman requested

that the

GC field engineer

have the craft work through lunch, if necessary,

to complete the

job.

During the performance of the

DCN, the lugs

on the power supply

wires from the fuse for FM/FT 113 to FT 113 were judged to require

replacement

and the electrician cut them off and relugged

them.

However, in this condition the replaced wires could not be landed

on

the side of the terminal block specified in the

DCN.

In addition,

after relugging the wires, the circuit could not be restored to its

original configuration.

The step in the work order which required the rewiring also included

a

gC inspection point to verify correct installation.

The

GC field

engineer

discussed

the situation with the

gC inspector

and properly

informed him that to complete the job, the wire would have to be

spliced, requiring splice requests,

jumper requests,

and work order

revisions.

The gC inspector properly informed the

GC field engineer

that

he could not perform his inspection until the

DCN was complete

and left the area.

The

GC field engineer

concluded that by relocating

a terminal

board

by approximately

one inch, the circuit could be terminated

on the

side opposite that identified by the

DCN which he judged would be

different than the

OCN but functionally equivalent.

At ll:30 a.m.,

the field engineer called the shift foreman to inform him that it

would take several

hours to complete the job per the

DCN.

The shift

foreman

responded that he wanted the system

back to provide

indication.

The field engineer

proceeded

to have the terminal block

moved.

At about ll:50 a.m., the field engineer verified as left condition.

He failed to notice

a previously existing ground wire from a

terminal block to

FM 110.

The rewiring had landed

a power lead to

the

same terminal

as this ground.

The

DCN drawing had

shown

no

ground lead to that terminal;

however,

since the ground lead

had not

been noticed, it was not removed,

as it should

have been,

in

-accordance

with the

OCN.

The

GC field engineer

described

the configuration using the

OCN

diagram of connections

to the shift foreman

and shift supervisor.

All parties

agreed that the system would perform as designed in the

described configuration.

The

GC clearance for implementing the

DCN

was reported "off" followed by a report "off for test" to test the

instruments

to verify that they functioned

as left.

These actions

were not made to declare the system indication formally operable

but

to make available primary water and boric acid flow indication.

At 12:23 p.m., operations

energized

the breaker to the flow

transmitters

which, because

of the wiring error, momentarily

grounded the inverter before tripping on overload.

The resultant

undervoltage initiated a containment ventilation isolation.

The root cause of this event can

be attributed to the

GC field

engineer initiating steps to return the system to service prior to

completion of the design

change.

as specified in the

DCN.

Two

contributory causes

were (1) the two hour schedule

which added

unnecessary

pressure

to the field engineer

and (2) that the shift

foreman concurred with the field engineer that the "functional" .

condition was acceptable.

In a Technical

Review Group

(TRG) meeting held on February

26,

1988,

to discuss

the Nonconformance

Report generated

by this event,

similar conclusions

were reached.

The

TRG sighted specific

procedures

governing work order and design

change

implementation.

Specifically, the

GC field engineer

should

have not proceeded

past

the step to rewire the internal wiring, bypassing

a gC inspection

point.

He should

have

had his work order revised to accomplish

those tasks

necessary

to complete the design

change

as prescribed.

10

The licensee

took three corrective actions:

(1)

Verification of satisfactory procedural

guidelines to restrict

activities such

as those of this event.

(2)

Counseling of responsible

individuals (i.e. the

GC field

engineer

and the shift foreman).

(3)

Issuance

of a memorandum stating that systems

are not to be

returned to service in other than the original design

configuration

on the final design configuration unless

a

partial

DCN closure

has

been

documented

and approved

by the

appropriate

supervision.

The memorandum also stated that

a

system is not to be returned to service

unless all modification

quality checks. that are required

have

been completed.

The

memo

was issued to all organizations

affected

by the policy.

\\

The activities discussed

in this section involved apparent

or

potential violations of NRC requirements

identified by the licensee

for which aggressive

and self-critical licensee

actions

were taken.

Consistent with Section IV.A of the

NRC Enforcement Policy,

enforcement action was not initiated by Region

V.

e.

Unit 2 Shift of Fuel Handlin

Buildin Ventilation to Iodine Removal

Mode

On .February 25, 1988, with Unit 2 at 100K power, the Fuel Handling

Building Ventilation System shifted to Iodine Removal

Mode due to a

high alarm

on new fuel area radiation monitor RM-59.

Initial

investigations

indicated that the high alarm was

due to a noise

spike

on RM-59 resulting from resistance

testing

on spent fuel area

radiation monitor RM-58.

Radiation Protection personnel

were in the

area at the time performing

a radiation survey and reported

no

change

in local radiation levels indicating that the alarm was

spurious.

The event

was reportable

under

10 CFR 50.73

and the licensee's

determination of root cause

and corrective actions will be evaluated

in a review of the

LER.

f.

Unit 2 Reactor Tri

Due to Seismic Tri

In ut

On March 3, 1988, at 1:44 p.m.

PDT while at 100K power, the reactor

tripped due to a seismic trip signal.

There

was

no seismic

ev'ent

however.

The seismic trip is initiated by a

2 out of 3 coincidence

in any 2

out of 3 directional detectors,

i.e. x-x or y-y or z-z.

I&C

technicians

were performing seismic trip surveillance testing

on one

channel.

They were

unaware of a failed "x" contact,

not annunciated

by design,

on another

channel.

When they placed the planned "x"

contact in test,

coincidence

was achieved

and the reactor trip

signal

was generated.

0

All safety system

responded

properly.

Two steam

dump valves

had

anomalies

which the licensee

investigated

and corrected.

Operators

response

to the trip was observed

and was satisfactory.

Licensee

management

conducted

an

accurately

captured all relevant

an action plan.

The action plan

the actions required for restart

extensive post trip review,

and

problems identified in the event in

accurately

and clearly, specified

and long term actions.

'k

Licensee

upper plant management

was in attendance

at the post trip

review and corporate

management

delivered

a message

to those in

attendance

which indicated that thorough actions took priority over

a return to service.

The 1'icensee

return-to-service

actions

included repair of a failed

coil in the seismic trip system,

steam

dump system repair and

grooming,

and other repairs

which the unplanned

outage

made

possible.

The licensee

longer range actions

included

a determination of the

need for a design

change to annunciate failed seismic trip channels

and

a review of other control

systems for similar "blind spots."

The licensee's

action plan methodology provided

a clear listing of

problem or investigative areas,

assigned

clear responsibility for

resolution,

required signoff for completion by those responsible

parties

and required documentation of corrective action.

This methodology appeared

to provide

a structured

approach to

actions

and afforded

an opportunity for on-shift management

review,

and upper

management

overview.

The inspector

noted that

new problems

(such

as water intrusion into

steam

dump electrical conduits) which were identified on Friday

night and Saturday

morning were not treated in the

same formal

precise action plan manner.

This situation

was identified to the

plant manager

and was immediately corrected.

Control

Room Ventilation Isolation

CVI

Actuations

on March 4 and

5

1988

Unit 2

On March 4 and 5, 1988, three separate

CVI actuations

occurred which

were

10 CFR 50.72 reportable

events

since they represent

Essential

Safety Feature

(ESF) actuations.

o

The first CVI occurred

on March 4, 1988, at 3:20 p.m.

PDT.

I8C

technicians

were troubleshooting

steam

dump problems which had

occurred during the reactor trip.

When they removed the cover

from an associated

pressure

switch, water drained

from the

switch (which should

have

been

a dry electrical

box).

The

water (or debris

on the water) caused

the switch to burn out

and trip the power supply breaker to it.

The short caused

a

'12

voltage transient

on the affected

120 Vac instrument

bus which

caused

an actuation of'VI and

a Fuel Handling Building

Ventilation System transfer to the Iodine removal

mode.

o

The second

CVI occurred at 9:06 p.m.

on March 4, 1988,

when an

operator performing a clearance

to allow work on the shorted

switch, closed rather than verified open the output breaker

from vital inverter IY-21A.

This action reenergized

the

shor ted switch,

caused

a voltage perturbation which caused

radiation monitor signals to actuate

the

CVI as well as

Fuel

Handling Building Ventilation System transfer to Iodine Removal

Mode and Control

Room Ventilation System transfer.

o

The third CVI occurred at 12:23 p.m.

on March 5, 1988,

due to a

voltage transient

on a 120 Vac instrument

bus (23A).

Train

B

of the

CVI occurred but Train A did not.

Licensee

investigation

showed that the cause of the voltage transient

was troubleshooting/repair

of an excore monitoring channel

(a

wide range

channel installed for

RG 1.97 reading at the Post

Accident Monitoring panel).

When lifting a lead

an arc was

drawn despite

the fact that the technicians

believed they had

depowered

the cabinet.

The arc and resultant voltage perturbation

were of sufficient

duration to cause

a CVI signal but only Train

B actuated.

Two

errors are indicated initially:

Depowering the cabinet using the power breaker in the

upper cabinet should

have

depowered

the wiring being

worked, but did not.

Licensee investigation indicates

that although

power wiring was properly installed per

vendor drawings,

the vendor drawing is in error and

requires

a design

change

DCN to correct it.

The licensee's

field.wiring diagram of connections

also

had

an error which, when wires were lifted to remove

a

faulty power supply,

caused

a defeat of protection set

A

inputs.

This was the reason

the Train A CVI did not

actuate.

The

same

problem was subsequently

found in Unit 1 and was

traced to an improperly performed design

change in 1984 on

both units.

The licensee is preparing

LERs and

NCRs on the above

CVIs.

Licensee

corrective action will be followed through these vehicles.

No violations or deviations

were identified.

5.

Maintenance

The inspectors

observed portions of, and reviewed records

on, selected

maintenance activities to assure

compliance with approved procedures,

technical specifications,

and appropriate

industry codes

and standards.

13

Furthermore,

the inspectors verified maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and replacement

parts

were appropriately

certified.

Dia hra

m Re lacement

on Unit I Valve 8484B

On February 23,

1988,

due to events

described

in Section 4.a of this

report, Unit 1. Charging

Pump 1-2 suction pressure

gauge isolation

valve 8484B developed

leakage

past the diaphragm.

On February 24,

work was initiated to replace

the diaphragm.

The inspector entered

the chargin'g

pump room following the completion of the work and

found

a Quality Control

(QC) inspector signing off QC inspection

points in the work order package.

The resident

inspector

reviewed

the work order and the

QC inspection plan.

One inspection point

required the

QC inspector to verify the torque application

and

another required

him to "visually examine

the valve internals for

cleanliness

prior to close-up of the system."

The valve, which was

located directly above the pump,

was in a surface contamination

area

(SCA) which extended

approximately six feet from the valve.

The resident inspector determined

from the

QC inspector that

he had

not gone into the

SCA to perform the inspection.

To verify the

torque application

he had 'the maintenance

mechanics

show him the

final reading

on the torque wrench which the resident

inspector

found to be acceptable

although not

a good practice.

To satisfy the

other inspection po'ints,. the

QC inspector

had examined the valve

diaphragm

and bonnet prior to installation but did not look at the

valve internals.

The

QC inspector

had verified with the maintenance

mechanic that the valve body was "clean".

The

QC inspector stated

that the job had required

him to wear

a respirator for which he was

not qualified.

He was sent to perform the inspection with the

information that it would not require

a respirator.

The resident

inspector

asked if the

QC inspector

thought the

inspection required

someone

to physically look into the valve body

and that perhaps

he should

have notified his management.

The

QC

inspector

agreed that in hind sight that would have

been prudent.

Subsequent

to the interview, the

QC inspector

informed his

supervisor

and following a reassessment

by radiation protection

was

allowed to perform the inspection without a respirator.

The resident

inspector

discussed

this incident with the

QC

inspector's

supervisor

and the

QC manager

who both stated that the

inspection point required the

QC inspector

to physically look into

the valve body,

as well as

examine

the valve bonnet

and diaphragm

for cleanliness.

The

QC department

has

reviewed this problem with

all

QC inspectors,

and the licensee

has established

an

NCR to assure

thorough resolution of the problem.

Further, disciplinary action

was taken against

the specific

QC inspector.

Finally, the

NRC

inspector determined that the component in question

was not of.a

high safety significance,

because

of the limited size of the opening

and the function of the valve (gauge isolation).

The

QC inspector's failure to perform his inspection

as described

in

his instructions is an apparent violation (Enforcement

Item

50-275/88-03-03).

14

b.

Unit 1 Turbine Driven Auxiliar

Feedwater

Pum l-l Gasket

Re lacement

The inspector. observed

the replacement of a gasket

on the Unit 1

turbine driven Auxiliary Feedwater

(AFW) pump l-l.

An oil leak had

developed

through the gasket

on the bottom of the turbine governor

gear box.

A corrective maintenance activity was generated

to

replace

the gasket.

The inspector

observed that the mechanical

maintenance

jou'rneyman

was qualified and followed his instruction.

During the removal of

the oil, the journeyman

had noted that the oil removed did not match

the oil prescribed

in his instruction.

He brought this to the

attention of a maintenance

engineer.

The engineer

reviewed

Administrative Procedure

(AP) D-753 "Control of Plant Lubricants,"

and determined that it did not specify oil for the turbine driven

AFW pump governor gearbox.

The work planner

had mistakenly

specified the oil listed in AP D-753 for the governor which is

separated

from its gearbox

by a seal.

The engineer

reviewed the

vendor technical

manual

which specified oil for the gearbox

and

made

a change to the work package.

The engineer will follow this

up by

revising

AP 0-753 to specify gearbox oil.

The inspector also observed

the torquing of the drain plate bolts

and observed

the torque wrench calibration check following the

maintenance activities.

C.

Other Maintenance Activities

Maintenance activities associated

with event follow-up were also

examined for this reporting period.

These

included centrifugal

charging

pump seal

replacement,

corrective maintenance

associated

with overpressurizing

the suction piping of the charging

pump, flow

transmitter modifications associated

with the Unit 1 CVI on February

19, 1988,

and corrective maintenance

associated

with the Seismic

Reactor trip of March 3, 1988.

One violation and

no deviations

were identified.

6.

Surveillance

By direct observation

and record review of selected

surveillance

testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

a.

Auxiliar

Feedwater

Pum

Surveillance Test

The inspector

observed

the performance of Surveillance Test

Procedure

(STP)

P-3B, "Routine Surveillance

Test of Motor-Driven

Auxiliary Feedwater,

Pumps" for Unit 2 Auxiliary Feedwater

(AFW) Pump

'-2.

This test fulfills the

ASME Section

XI requirements

to

periodically test the

AFW pumps.

The inspector

reviewed the

0

procedure

against the

ASME Section

XI criteria and found it

acceptable.

The inspector

found that the auxiliary operator performing the test

was familiar with the test

and the system.

The inspector

reviewed

the test results against the associated

action limits and found them

acceptable.

b.

Other Surveillance Activit

Additional surveillance activities were examined in conjunction with

operational

events

described

in paragraph

4.

These

included

centrifugal

charging

pump surveillance testing

and criteria,

and

testing of seismic trips pursuant to the March

3 Unit 2 reactor

trip.

No violations or deviations

were identified.

7.

Radiolo ical Protection

The inspectors periodically observed radiological protection practices

to

determine whether the licensee's

program was being implemented in

conformance with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors verified that health physics

supervisors

and professionals

conducted frequent plant tours to observe

activities in progress

and were generally

aware of significant plant

activities, particularly those related to radiological conditions and/or

challenges.

ALARA consideration

was found to be an integral part of each

RWP (Radiation Work Permit).

a.

Unauthorized Entr

to the Radiolo ical Controls Area

On February

19, 1988, the inspector

observed

an employee of the

licensee

cross

a roped

and posted

boundary into the Radiological

Controls Area

(RCA) without authorization.

The boundary

was

a temporary. barrier at the south

end of the outside

115'tank farm" area.

The temporary barrier was set

up to aid

construction efforts and to ease

access

for vehicles in preparation

of the Unit 1 refueling outage.

The boundary

was delineated.

by

yellow-magenta

rope,

supported

by stanchions,

and marked by postings

reading "Caution, Radiological

Controls Area,

Personnel

Monitoring

Devices

Required

Beyond this Point" and "Radioactive Materials

Area."

This posting was in accordance

with Radiation Control

Procedure

(RCP) D-240, "Posting of Radiologically Controlled Areas."

The inspector

observed

the individual who had current General

Employee Training for access

to the

RCA, read the postings

and then

cross

the barrier.

The inspector notified a Senior

Chemistry and

Radiation Protection

(C8RP) Engineer

who notified

RCA access

control.

The radiation protection control personnel

identified and

escorted

the individual to the normal

access

control at the

85'evel

of the Auxiliary Building.

The individual was wearing

a TLD

the entire time, did not enter any surface

contamination

areas,

and

did not receive

any measurable

exposure.

The inspector

discussed this event with the individual.

The

individual had been touring the perimeter of the plant when

he

came

to the posted barrier.

He interpreted

the posted

requirement for

personnel

monitor ing devices to be fulfilled by his TLD.

He was

also

under

the mistaken

impression that this portion of the

RCA had

recently been returned to general

access.

However, the individual

should have recalled

from General

Employee Training that entry into

the

RCA required the use of a Radiation Work Permit

(RWP),

a Special

Work Permit

(SWP), or other written authorization.

The inspector

observed that for the most part the

RCA boundary

was

posted

as required.

However, the barrier sagged to two feet off the

ground and was not as

imposing as it could have been.

In addition,

a side entry in a fence to the

same area

was posted only with a

"Caution, Radioactive Materials."

Finally, observing

from inside

the

RCA, their were

no postings to state that the barrier was

an

exit of the

RCA.

These findings were discussed

with the

CHIRP

manager

and the senior

CHIRP engineer.

Following these discussions,

the postings at the

RCA barrier were added to read,

"No Entry at

this point."

On the other side the barrier read ."No Exit."

In

addition the barrier was supported

by an extra stanchion.

The individual crossed

the barrier in violation of Radiation Control

Standard

4, "Control of Access" which in section 3.3, "Entry Into

the Controlled Area," states

in paragraph

3.3. 1:

"Except as

exempted

by the Diablo Canyon Technical Specifications written

authorization (usually an

SWP or RWP) is required for all entries

into the controlled area

"and in paragraph 3.3.3." Entry into the

Controlled Area shall

be made only through the normal established

access

control points.

Entry by way of other points

may be

made

only in cases

of emergency

or by authorization of radiation

protection supervision."

This is a potential violation (Enforcement

Item 50-323/88-04-01).

One violation and

no deviations

were identified.

8.

Ph sical Securit

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative procedures

including vehicle

and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was

checked during backshift inspections.

No violations or deviations

were identified.

17

9.

Licensee

Event

Re ort Follow-u

a 0

Status of LERs

Based

on an in-office review, the following LERs were closed out by

the resident inspector:

Unit 1:

86-16

Unit 2:

86-27, 87-03, 87-05,

87-25

The

LERs were reviewed for event description,

root cause,

corrective

actions taken,

generic applicability and timeliness of reporting.

b.

Red Tele

hone vs

LER Trackin

The licensee

has evaluated

the following 10 CFR 50.72 events for

reportability under 50.73

and has determined that 50.73 report is

not required.

The resident

inspectors

have

examined the licensee's

rationale

and determined that regulatory requirements

have

been met.

50.72 Report

Date/Unit

Event

Reference

NCR

etc.

January 31/Unit 2

OP delta

T runback

NCR DC1"88"OP N010

No violations or deviations

were identified.

10 ~

0 en Item Follow-u

a.

Late

Re ortin

of an

En ineered Safet

Feature

ESF

Actuation

0 en

Item 50-323/87-20-03

and 50-323/87-26-03

Closed

In inspection reports

50-323/87-20

and 50-323/87-26,

Notices of

Violation were issued against Unit 2 for the late reporting of ESF

actuations.

The second

Notice of Violation was issued prior to the

complete

implementation of corrective actions

taken in response

to

the first Notice of Violation.

The inspector

reviewed the corrective actions

described

in the

licensee's

responses

of July 22, 1987,

and October 2, 1987, which

appear to be acceptable.

The corrective

actions

were also discussed

in subsequent

management

meetings.

The inspector will continue to

monitor the licensee's

performance

in the area

and reopen this issue

if conditions warrant.

Accordingly, these

open items are closed.

b.

Control of the Installation

and

Removal of Tem orar

Gau

es

0 en

Items 50-323/87-43-02

and 87-43-03

Closed

In a letter dated February

19,

1988, the licensee

responded

to two

notices of violation and

a request for information.

The first

notice of violati'on involved the control of the installation of

18

temporary

gauges

(50-323/87-43-02).

The second notice of violation

concerned

the failure to remove

an installed

gauge in accordance

with procedure.

The information request

concerned

the control of

the installation of a temporary nitrogen manifold to the steam

generator

blowdown line on Unit 2.

The inspector

has reviewed the above letter

and finds the corrective

actions

described

to be acceptable.

Specifically, that test

procedures will .provide additional

assurance

that test equipment

installation and removal

and,

when this is not the case,

that the

test equipment will be controlled using Administrative Procedure

C-4Sl, "Jumpers."

The letter also committed to discuss

these

practices with Operations

and Instrumentation

and Controls

personnel.

In addition, consideration will be given for a design

change to install permanent test equipment

when a high use frequency

warrants it.

The inspector will review the proposed

procedural

revisions

and other commitments during the course of routine

inspection.

These

items are closed.

Main Steam

Line Noise Follow-u

Inspection

Report 50-323/87-45

discussed

main steam line noise

and

the licensee's

efforts to identify its source.

The inspector

questioned

the apparent tardiness

to establish

a comprehensive

program to identify the source of the noise.

A review of the history of the main steam line noise

showed that

following its identification in 1987, attention

was focused

by

different groups,

including plant maintenance

and engineering.

The

reviews included discussions

with the main steam isolation valve

vendor representative

and Unit 2 valve inspection.

The action

request

issued

as

a result of the 1987 investigation identified

three sources

of noise:

(1)

MSIV disc fluttering on the valve stop tubes.

.(2)

Condensation

from an unknown source,

possibly from the main

steam relief valve header,

flashing through the MSIV.

(3)

Noise from in-line calorimeters

abandoned

in place

downstream

of the MSIVs.

The most recent investigation into the noise established

the

same

causes.

In addition, the licensee

concluded that these conditions

did not jeopardize

the integrity of the valves or the system.

The

investigation

however was more detailed

and involved the

coordination of various engineering

and plant groups.

As a result

the information generated

was available to all groups.

A study of

the difficulties in obtaining the whole story from the first

investigation,

including what specifically was looked at and what

was found,

appears

to be

a good argument for the Action Plan/Task

Force method

used in the second investigation

and being implemented

by the licensee

in a number of recent events.

19

d.

Challen

es to the Onsite Fire Bri ade

0 en Item 50-275/87-27-01,

ose

In response

to the NRC's regional fire specialist

inspection report

findings, the licensee

described

the actions

taken to improve the

Onsite Fire Brigade.

These actions

were identified to the regional

specialist

who determined that this item could be closed.

The

actions

included

a procedure revision to limit brigade

response

to

the site boundary,

a replacement fire truck and

a description of

manning options available in the event of a major county fire.

This

item is considered

closed.

e.

Res

onse to

A Audit Findin

s

0 en Item 87-38-05,

Closed

As

a follow-up to previous concerns,

the

RV Enforcement Officer met

seperately

with four individuals employed in the licensee's

quality

control group to discuss their freedom to carryout their assigned

responsibilities.

Without exception, all of the individuals

indicated they had the necessary

freedom to identify problems

and

assure

that adequate

corrective action is initiated.

All of the

individuals said that they had the necessary

management

support to

assure

that their activities are appropriately

performed without

undue interference

from others.

This item is closed.

ll.

Inde endent

Ins ection

During this reporting period it was identified that operators

at the

auxiliary control station were using annunciator

response

procedures

which were not formally controlled procedures

and were in fact authorized

to make

pen

and in changes

to those

procedures

without further approvals.

Discussion with the Operations

manager

indicated that the licensee

had

undertaken

a program to improve annunciator

response

procedures

approximately three years

ago.

At that time control

room annunciator

response

procedures

were approved

by the Operations

Manager, it was then

decided to upgrade

those to

PSRC approval,

and this was done.

At that

time the auxiliary control station did not have annunciator

response

procedures

and

a decision

was

made to have the auxiliary operations staff

develop the procedures

through use,

and to formalize them at

some point

in time.

The operation

manager

committed to formalize the auxiliary

control

board annunciator

response

procedures.

The schedule for this is

to be determined.

This item will be followed-up in future inspection

(Item

50-275/88-03-04).

12.

~Ei

N

On March 11,

1988,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.

Additional topics were discussed

including:

20

o

A rising level of concern

regarding

the tardiness

of implementing

corrective. actions notably in the

I&C area.

These

concerns

were

focused

by a stop work issued against

I&C by

PG&E gA for failure to

update

Measuring

& Test Equipment

(M&TE) procedures

identified 1987.

Likewise, upgrades

of I&C loop tests first identified as

a concern

in 1987

have not been

accomplish

and only a writers guide for loop

tests

has

been

scheduled for completion in July 1988.

Likewise,

a

steam

dump grooming procedure for restart after

a trip identified as

needed

during the Unit 2 return to power in July 1987

was not yet

available after the March 3, 1988, Unit 2 reactor trip.

o

The proposed

commission rule regarding plant employee warning

systems

on backshift regarding

NRC or site management visits.

The

need to ensure that such

systems

do not develop

was discussed.

C

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