ML16154A728

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Insp Repts 50-269/94-31,50-270/94-31 & 50-287/94-31 on 940920-1103.Violations Noted.Major Areas Inspected:Initial Swsopi of 1993
ML16154A728
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 12/16/1994
From: Peebles T, Rogers W
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A726 List:
References
50-269-94-31, 50-270-94-31, 50-287-94-31, NUDOCS 9412280118
Download: ML16154A728 (32)


See also: IR 05000269/1994031

Text

NUCLEA REUNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/94-31, 50-270/94-31, and 50-287/94-31

Licensee: Duke Power Company

422 South Church Street

Charlotte, NC

28242

Docket Nos.:

50-269, 50-270, and 50-287

License Nos.:

DPR-38, DPR-47,

and DPR-55

Facility Name:

Oconee Nuclear Station Units 1, 2, and 3

Inspection Conducted: September 20 through November 3, 1994

Inspector:____

/"- /6

Walter G. Rogers, Team L der

Da e Si ne

Accompanying Personnel: Paul Kellogg

Larry Mellen

Larry King

Curt Rapp

NRC Consultants: D. revatte

Approved by:

Z

Tho as A. P

Da e Si gned

Op

1

--

ee-e

hDate

S4gned

Division of e ctor Safety

SUMMARY

A follow-up to the initial Service Water System Operational Performance

Inspection (SWSOPI) of 1993 was conducted on September 20 through November 3,

1994 according to NRC inspection module 37550 and Temporary Instruction (TI)

2515/118.

RESULTS

The NRC Temporary Instruction for Service Water Inspections (Safety Issues

Management System item TI 2515/118), was not closed since the licensee has yet

to accomplish a number of committed Generic Letter 89-13 actions.

Numerous corrective actions from the previous inspection had not been

adequately accomplished or completed consistent with committed schedules.

Testing of the suction source capability for the low pressure service water

pumps via the siphon mode was not adequate. Deficiencies were identified in

the operational guidance and testing of the Auxiliary Service Water system.

Also, infrastructure weaknesses persist inhibiting efforts to keep design

calculations current.

9412280118 941219

PDR ADOCK 05000269

Enclosure 2

Q

PDR

REPORT DETAILS

1. Inspection Objectives

Numerous problems identified at various operating plants in the country

have called into question the ability of the SWSs to perform their design

function. These problems have included:

inadequate heat removal

capability, biofouling, silting, single failure concerns, erosion,

corrosion, insufficient original design margin, lapses in configuration

control or improper 10 CFR 50.59 safety evaluations, and inadequate

testing. NRC management concluded that an in-depth examination of SWSs

was warranted based on the identified deficiencies.

In the original SWOPI conducted in 1993, the team focused on the

mechanical design, operational control, maintenance, and surveillance of

the SWS and evaluated aspects of the quality assurance and corrective

action programs related to the SWS. Numerous deficiencies were identified

by the team which the licensee responded to in letters on March 14, April

20, May 12 and September 1, 1994. This inspection's primary objectives

were to;

assess the licensee's progress in accomplishing the committed actions

specified in these letters,

verify whether the corrective actions resolved the identified

deficiency and did not compromise SWS performance requirements or

design bases,

assess the licensee's planned and completed (since February 1994)

actions in response to Generic Letter 89-13, "Service Water System

Problems Affecting Safety Related Equipment," and

ascertain why there were discrepancies between information provided to

the team and a recent motor operated valve inspection about LPSW

turbine building isolation valves thrust capabilities and types of

tests performed on these valves in the past.

Another issue not associated with the SWS follow-up was included as part

of this inspection. This issue dealt with a postulated feedwater piping

break within containment. The licensee had provided information and

future corrective actions to mitigate the consequences of such an event.

Therefore, another primary objective of this inspection was to understand

the licensee's present response capability to such an event and ascertain

the status of any design changes to reduce the consequences of such an

event.

The team observations and concerns identified are described in sections 3

through 7 of this report. Personnel contacted and those who attended the

exit on October 27, 1994, are identified in Attachment A. Acronyms and

abbreviations are identified in Attachment B.

Enclosure 2

Report Details

2

2. General Description of SWSs

The SWSs at Oconee encompass numerous systems. These are the CCW

(including the ECCW subsystem), LPSW, HPSW, ASW, SSF DG, HVAC, and steam

generator cooling, the SSF submergible pump subsystem, Keowee

hydroelectric station generator air, thrust bearing, packing box, and main

bearing cooling.

The CCW system is common to all three units and takes suction from the

Lake Keowee intake canal.

Twelve pumps (four per unit) supply a common

cross-connected 42-inch discharge header from which numerous other SWSs

take suction. From this header, cooling water passes through the three

condensers. Upon leaving the condensers, the water discharges through six

lines (two per unit) and returns to Lake Keowee upstream of the intake

canal.

A subsystem of CCW is the ECCW system. If the CCW pumps lose power, ECCW

actuates establishing siphon or gravity flow from the intake canal to the

42-inch header and through the condenser sections. Emergency condenser

discharge lines connect the condensers with the Keowee hydroelectric

station's tailrace. Prior to entering the tailrace, all the discharge

lines connect into one line. ECCW actuation involves the automatic

closure of the condensers' normal outlet valves, opening of the

condensers' emergency outlet valves and opening the emergency discharge

valve to the Keowee tailrace, CCW-8, located in the common discharge

piping. The high points of the ECCW piping are connected to a vacuum

priming system which would remove air entrapped within the system that

could impede siphon operation. The licensee considers CCW supplying the

LPSW pumps as the first siphon and CCW passing through the condensers as

the second siphon.

The CCW system performs two distinct safety functions during the LOCA/LOOP

event.

First, it provides a suction source for other systems including

the safety-related LPSW system, and second it provides cooling water to

the condenser to remove decay heat in the ECCW mode. The CCW pumps

contribute to these safety functions in two ways. First, when power is

lost and they are not operating, they provided a siphon conduit from the

intake canal to the CCW piping from which the LPSW takes suction, and to

the condenser for the ECCW system. Second, at the time when the pumps can

be restarted (up to 1/2 hours per emergency procedures), they continue to

provide water for these same functions. Since dissolved air will tend to

come out of solution when the system is in the siphon mode, at least one

of the CCW pumps must be operated after power is restored in order for the

water to continue to be supplied to the CCW piping.

Within the intake canal, is an underwater dam which can trap approximately

67,000,000 gallons of water if Lake Keowee were to fall below the 770-foot

level.

With the CCW pumps operating, the system is capable of

recirculating water from this impounded area, through the condensers,

through the condenser emergency discharge lines and through normally

closed valve, CCW-9, which discharges into the intake canal.

Enclosure 2

Report Details

3

The LPSW system provides cooling to the RBCUs, LPI coolers, the motor and

turbine driven EFW pump coolers, HPI pump motor coolers, the control room

chilled water system, numerous room coolers, and nonsafety-related turbine

building loads. Units 1 and 2 share three 15,000 gpm pumps with one pump

capable of being powered from two separate safety-related busses. The

Unit 3 LPSW system has two 15,000 gpm pumps. The LPSW pumps take a

suction from the 42" CCW discharge header within the turbine building.

The Unit 1/2 LPSW pumps discharge into a common header that splits into

two supply lines; one supply line for each unit. The unit supply lines

further divide into two separate headers supplying the two trains of

safety-related equipment. The two equipment supply lines then

interconnect into a common line which enters containment. This common

line then splits into three parallel lines; each line supplying one RBCU.

These three RBCU supply lines reconnect into one line on the discharge

side of the RBCUs before exiting containment. Also, branching from the

common discharge header is a supply line to the turbine building loads.

The turbine building supply line then splits to provide cooling to each

unit's turbine building equipment. The Unit 3 RBCU and turbine building

cooling arrangement is similar. A normally closed crosstie line allows

either LPSW system to supply the discharge header of the other LPSW

system.

The HPSW system normally functions as the site's fire protection system.

The system is composed of three pumps, an elevated storage tank, and

  • interconnecting

piping to fire protection deluge valves throughout the

site and to the CCW pumps. The three pumps, two 6000 gpm capacity and one

jockey, take suction from the 42" CCW discharge header. The jockey pump

maintains system pressure. The other two pumps are to make up lost water

inventory in the 100,000 gallon capacity elevated storage tank. The

system constantly supplies cooling and sealing water to the CCW pumps.

The system is capable of supplying cooling water to specific components

normally cooled by the LPSW system such as the HPI pump motor coolers and

the EFW pumps. Though at reduced capacity, the system can provide backup

cooling to the LPSW system through interconnections at the discharge of

the LPSW pumps.

ASW is a system common to all three units. It is designed to provide

cooling to the steam generators. The system was originally designed for

the loss of the intake canal/structure. However, following NUREG 0737

review of the facility for tornado vulnerabilities, the system was

credited in the July 28, 1989, NRC SER to mitigate the consequences of a

tornado. The system can supply cooling water to the high pressure

injection pump motors if the low pressure service water system is

unavailable. The ASW system consists of a suction connection to the unit

2 CCW system at elevation 759.5, a low head, high capacity pump, piping,

and manual valves connected to the emergency feedwater piping in the

penetration rooms of all three units. The ASW pump is operated from the

safety-related Aux Service Switchgear, and the alignment to the SGs is

accomplished manually.

Enclosure 2

Report Details

4

The SSF is a separate onsite building housing the necessary equipment to

maintain all three units in a safe shutdown condition following turbine

building flood, fire, sabotage, and certain classes of tornados or station

blackout. The SWS portion of the SSF is composed of a high head, low

capacity pump and interconnecting piping to all steam generator EFW

discharge lines, solenoid operated flow control valves in the discharge

lines to the steam generators, a pump and piping to cool a tandem diesel

with a common generator, two pumps with a condenser unit to cool the HVAC

within the SSF, and a moveable submersible pump. The SSF ASW, HVAC, and

DG pumps take suction from the Unit 2's CCW pump's discharge header. The

HVAC and DG pumps discharge to the CCW header. There is an option to

divert the DG pump discharge water to the yard drainage system when high

temperature constraints warrants. The submersible pump allows

replenishment of the CCW header from the intake canal.

Lake Keowee is the motive and cooling source for the two hydroelectric

generators which function as Oconee's onsite emergency power. Water flows

from a common penstock, through the turbines and into the tailrace.

Cooling flow comes from a single pipe located in the penstock. Once the

line enters the building housing the hydroelectric units it splits into

two lines, one for each unit. Cooling flow for the turbine bearing oil

cooler, the stuffing box, eight thrust bearing heat exchangers, and six

generator air coolers comes from the unit specific main line.

.

3. Follow-up on Previously Identified Items

The team reviewed all outstanding violations, unresolved items, and

inspector follow-up items identified in the original SWSOPI. For

violations, the corrective actions described by the licensee were

evaluated for adequacy and completeness. The team reviewed whether the

implementation of the corrective actions were accomplished within the time

frames specified by the licensee's NOV response and strengthened the

licensee's QA program procedures or practices to prevent recurrence. If

the corrective action deadline had not occurred, the status of licensee

efforts was ascertained. Unresolved items were updated or dispositioned

depending upon the status of NRC review of these matters. The team

continued to evaluate the matters selected for inspector follow-up. The

status of licensee efforts in these matters also were ascertained. The

team reviewed all matters to ensure the generic implications, if

applicable, were addressed. Inspection findings were:

a. (Open) DEV 50-269, 270, 287/93-25-01 (Deviation A in NRC Inspection

Report 93-25), "Failure to Adequately Perform SWS GL Actions." The

licensee's original response to GL 89-13 was not inclusive of some of

the systems utilizing service water.

In response the licensee indicated a revised response to the GL would

be submitted by September 1, 1994. Included in the September 1, 1994

GL response would be those actions necessary to deal with Keowee

stagnant or intermittent flow. In addition, a schedule for

implementation of modifications and testing of Keowee heat exchangers

Enclosure 2

Report Details

5

would be provided by September 1, 1994. Finally, operating procedures

were created for the Keowee thrust bearing oil heat exchangers and the

generator air coolers by February 4, 1994.

The revised GL response was submitted by September 1, 1994. However,

there were numerous omissions and inadequacies associated with this

response. Therefore, the licensee continues to have not fully

responded to the GL. The omissions and inadequacies outstanding are:

Action I - No date was provided as to when the CCW system

hydraulic model would be benchmarked. No date was provided as to

when the HPSW system hydraulic model would be benchmarked. The

frequency of simultaneous SSF SWS pump testing was not specified.

Action III - No administrative controls existed to ensure the

committed inspection program for the SSF, ASW, and Keowee SWSs

would be accomplished. System engineers interviewed who were to

do the inspection program were unaware of their inspection

responsibilities. There was no criteria by which to judge piping

condition acceptability. Also, no technical bases for the

adequacy of the piping inspection program in terms of scope,

frequency, or corrective action could be ascertained.

Action IV - No date was provided as to when the Keowee single

failure analysis would be completed.

Action V - The GL response referenced a Duke Power Company letter

to the NRC dated April 20, 1994, as providing the discussion on

procedures and training. However, this letter was not applicable

to Action V. Also, the presently docketed correspondence on this

matter indicated that SWS procedures were receiving a two-year

review. This was not correct. The licensee had revised their

procedure review cycle to as long as every six years following a

change to their QA plan.

As indicated above, the licensee's corrective actions to the deviation

included the creation of operating procedures for Keowee thrust

bearing oil heat exchangers and the generator air coolers. However,

the newly created Keowee operating procedures omitted numerous valves

in the Keowee SWSs. These valves included all the generator thrust

bearing cooler inlet valves, and drain valves WL-1, 2, 5, and 6 for

both units.

10 CFR 50, Appendix B, Criterion XVI, "Corrective

Action," requires, in part, that measures be established to assure

that conditions adverse to quality are promptly identified and

corrected. The licensee had developed procedures, but they were not

complete. Failure to adequately correct this condition adverse to

quality is an example of Violation 50-269, 270, 287/94-31-01A,

"Inadequate Corrective Action Controls."

Enclosure 2

Report Details

6

.

b. (Closed) URI 50-269, 270, 287/93-25-02, "Turbine Building Isolation

Single Failure Vulnerabilities."

The licensee's original SER stated that the plant was designed such

that no single failure would prevent safety system functionality in

the event of a LOCA and a LOOP caused by a seismic event. NRC

reviewed the licensee's original SER and because seismic event is a

qualification standard and not an event that requires mitigation,

interpreted that single failure did not apply to seismic event.

Because the reactor coolant system was seismically qualified, a

seismic event did not result in a significant challenge to core

cooling capability. Additionally, NRC credited the SSF as providing

the same safety function as LPSW in the licensee's EFW SER. Based on

NRC's interpretation of seismic event as a qualification standard and

NRC's credit of the SSF in the licensee's EFW SER, no further licensee

action is required. This item is closed.

c. (Open) VIO 50-269, 270, 287/93-25-03 (Violation B in NRC Inspection

Report 93-25), "Failure to Perform Adequate Calculations and

Evaluations to Support Facility Design."

There were seven parts

associated with this violation.

(1) In Item 1, the NPSH of the LPSW pumps was not adequately

considered as a design input in that calculation OSC-5019 was

accepted by the license's engineering personnel with inadequate

NPSH and inadequate technical justification.

The licensee contested this example of the violation.

To better understand the safety significance associated with this

matter the licensee performed a PRA of the conditions necessary

to have inadequate NPSH. The analysis indicated the event was

not a significant accident precursor. However, the information

provided by the licensee in their docketed correspondence

continued to indicate that there was inadequate consideration of

net positive suction head as a design input for the Low Pressure

Service Water pumps. This matter remains open.

(2) In Item 2, no administrative control existed to assure the LPSW's

pump flows used as hydraulic computer model input for the LPSW

system remained valid during quarterly testing of the LPSW pumps.

The licensee responded that the test procedures for LPSW and

other select systems, which do not have clear test acceptance

criteria for pump performance, would be revised by September 1,

1994. In the procedure revision system, engineers would compare

quarterly pump test data, along with full system flow test data,

against computer models and other calculations to ensure the

validity of design basis analyses.

Enclosure 2

Report Details

7

The licensee had included guidance in the quarterly LPSW pump

test procedure ensuring the test results did not invalidate the

hydraulic model.

Discussions with the system engineer indicated

this guidance would be removed and the LPSW pump curve used in

the hydraulic model degraded. The amount of degradation would be

determined by reviewing the decrease in LPSW pump performance

data based on the previous 10-year trend. The quarterly LPSW

pump test acceptance criteria will be modified to reflect the

LPSW pump degradation used in the hydraulic model.

This

violation example is closed. However, transition from the test

procedure to the hydraulic model is considered an Inspector

Follow-up Item 50-269, 270, 287/94-31-02, "Hydraulic Model

Controls Transition."

(3) In Item 3, the commercial grade evaluation for Belzona as a

suitable material for application to the Unit 2 Reactor Building

Cooling Unit tubes was inadequate.

In response the licensee documented that an effort was underway

to obtain dynamic material property data and to analyze Belzona

for usage under cyclic loading and LOCA conditions by

December 16, 1994. Also, a modification to replace the RBCU

cooling coils had been completed on U3 and Ul, and was currently

underway on U2.

The licensee was continuing to analyze Belzona with the targeted

completion date of December 16, 1994. Also, the RBCU cooling

coils had either been replaced or were being replaced during the

inspection period. This example remains open pending completion

of the licensee's Belzona analysis.

(4) In Item 4, the design basis of the ECCW system was not adequately

translated into design documents in that the calculations

supporting ECCW decay heat removal capability did not include

numerous aspects of the design that would reduce decay heat

removal capability.

Two calculations were involved. The first calculation was OSC

2346, "ECCW System Performance Evaluation."

This calculation was

generated to show that the main condenser in the ECCW mode had

the capacity to transfer the required decay heat without

exceeding the condenser pressure limits or causing flashing on

the CCW side which could cause loss of siphon. The initial

inspection report noted that this calculation contained several

non-conservatisms. As partial response to the violation example

the licensee revised the calculation on September 29, 1994

(Rev. 5).

The new calculation was poorly performed and contained new errors

or did not completely address the original concerns. These

deficiencies included:

Enclosure 2

Report Details

8

I

On page 32o, the specific volume of air was used in a

computation to determine the amount of air that would come

out of solution. The value used was IL/kg - the correct

value for water, but not for air. The specific volume of

air at one standard atmosphere is 847L/kg. Therefore, the

result was non-conservative by a factor of 847. When this

was brought to the responsible engineer's attention, he re

reviewed the calculation and found that in the computation

of the dissolved air on page 32n, there was another

offsetting error in the number of gram moles/liter by a

factor of 502. The net result was that the air coming out

of solution, before correction for other non-conservative

factors, increased from 940 ft3 to 1,590 ft3.

Per the

calculation, the non-conservative limit on outgassing was

1,584 ft3 . Therefore, this result was unsatisfactory.

In subsequent discussions with the licensee the reason for

the gram moles/liter error was due to an incorrect

reference. The team inquired what actions had been taken by

the licensee to deal with the ramifications of such an error

and whether the matter had been identified as a condition

adverse to quality. The licensee responded that the

chemistry section (where the reference had been acquired)

had been contacted but, no PIP had been initiated. The

licensee personnel stated that they were waiting to

understand all the problems associated with this calculation

before initiating a PIP.

"

Outgassing of the CCW water had not been accounted for in

the calculation initially reviewed by the team in 1993. The

revised calculation did consider outgassing but not

completely. Specifically, the calculation only considered

the outgassing effects due to the increase in temperature as

the CCW water passed through the condenser; it did not

consider the outgassing due to the reduction in pressure due

to the siphon effect. Also, the calculation did not

consider the expansion of the air after it had outgassed due

to the reduction in pressure from atmospheric, again, due to

the siphon effect.

On page 32m, the revised calculation determined the

allowable volume of air to be outgassed based on the volume

of the condenser waterboxes above the ECCW outlet piping.

This computation was based on the height from the top of the

waterbox to the centerline of the outlet pipe, 7 feet. It

should have been to the top edge of the pipe, 6.5 feet,

which is the point where the pipe would begin to be

uncovered. This reduced the allowable outgassing volume by

7.1 percent from what was calculated.

The revised calculation did not reconcile competing

assumptions associated with the number of available tubes in

Enclosure 2

Report Details

9

the condenser for heat transfer. The revised calculation

assumed one condenser section was out of service. However,

1/2 of a section can be taken out of service under operating

procedures without engineering involvement. Further tube

reduction can be accomplished by tube plugging and Amertap

ball clogging. The licensee responded that only 4.5 percent

(approximately 700 tubes) were plugged, and this would

produce an insignificant effect. This response only

accounted for the tubes that had been taken out of service

and those which the licensee felt might trap the Amertap

balls due to denting or other damage. In generating that

number, the licensee did not consider that in the siphon

flow mode the differential pressure across the condenser

would be extremely low compared to normal operation

sufficiently low that none of the Amertap balls were likely

to pass through the tubes. Therefore, all of the balls

which entered the inlet waterbox would potentially plug

tubes. The licensee had not verified that the assumed out

of service condenser section would compensate for the other

non-conservative mechanisms capable of reducing the number

of tubes for heat transfer.

The original calculation assumed an even flow split to all

three condensers, whereas the piping configurations were

significantly different for each condenser; therefore, this

assumption was not necessarily valid. This assumption

continued in the revised calculation. The licensee

responded that the three units displayed similar condenser

flow values which are considerably higher than the required

flow value. However, the data cited is not for conditions

similar to the conditions described in the calculation;

i.e., flow through all three of the condensers at the

minimum flow rate. Therefore, the conclusion was not

supported by relevant data.

The responsible engineer stated the calculation would be re

performed making the appropriate corrections and also taking into

consideration a number of significant conservatisms that had not

been considered before. Revising the calculation is considered

Inspector Follow-up Item 50-269, 270, 287/94-31-03,

"Reperformance of Calculation OSC-2346."

The second calculation was OSC-2349, "CCW Intake Piping Degassing

in the ECCW Mode."

The calculation was performed to verify the

CCW system's "first siphon" capability for the four-hour SBO

event. It considered the air inleakage into the system and air

outgassing from the water that would tend to break the siphon,

and it established the acceptance criteria for the ECCW system

flow test. The initial inspection report noted that this

calculation contained several discrepancies and nonconservatisms

Enclosure 2

Report Details

10

as well as several conservative assumptions; the net effect of

which could not be determined without a rigorous re-performance

of the analysis.

In the response letter of May 12, 1994, the licensee stated that

this calculation was intended to be applicable for the SBO event

only, and not for the LOCA/LOOP event; a separate calculation

would be generated to analyze that scenario. Therefore, the

30,000 gpm flow assumed for this calculation was appropriate. It

was also stated that the calculation's use of the incorrect

atmospheric pressure would have an insignificant effect on the

analysis. Therefore, no changes were required.

Considering this response, the licensee had no analysis or test

which verified the "first siphon's" design basis safety function

for events involving LOOP such as the LOCA/LOOP event (90,000 gpm

for 1.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />) during the initial inspection. Subsequently, a

new calculation was generated (OSC-5670, Rev. 1, March 17, 1994,

"Required Number of CCW Intake Flow Paths") to provide the

analytical basis for the "first siphon" for the LOCA/LOOP event.

This new calculation revealed a new requirement for the system

configuration to support the design basis conditions; at least

two CCW pump discharge valves on the same eleven foot CCW piping

section were required to meet the siphon flow requirements.

Also, the new calculation contained the following minor

deficiencies which were discussed with the responsible engineer

and were found to have no effect on the results. The responsible

engineer indicated the required revisions would be made to

correct these deficiencies. The deficiencies were:

The test data used as benchmark data in the calculation was

of questionable validity. However, the team reviewed

additional test data which appeared to be valid and would

provide appropriate benchmarks.

The calculation did not address the differences in water

temperature and flow rate between the test data used as

benchmark cases and the design basis case. Although this

left the calculation incomplete, the effects appeared

minimal.

Further team review as to the confirmation of the new calculation

via testing did not exist. There was a test that acquired test

data that would be imputed into the LPSW hydraulic model.

However, this test did not contain acceptance criteria associated

with first siphon performance. Therefore, the test data was not

evaluated as to whether the siphon would operate in the most

demanding design bases conditions (lowest lake level, highest

required flow, etc.).

Also, the first siphon test did not assure

proper protection from air intrusion via a pump flange connection

Enclosure 2

Report Details

11

normally underwater. This connection would be uncovered at lower

acceptable lake elevations. The only other test procedure

associated with the ECCW system verified only the second siphon,

not the first, with all test acceptance criteria associated with

the second siphon.

Independently, the licensee had identified that the ECCW system

testing did not accomplish the technical elements of the team's

findings. However, the licensee viewed these deficiencies as

areas for improvement to the present testing, not as

deficiencies. This position was partially based on the

licensee's belief that the Technical Specifications did not

require a test of the first siphon capability of the ECCW system.

Technical Specification Surveillance Requirement 4.1.2, table

4.1-2, item 7, specifies a condenser cooling water system gravity

flow test be performed each refueling. 10 CFR 50, Appendix B,

Criterion XI, "Test Control," requires, in part, that operational

test procedures demonstrate systems and components will perform

satisfactorily within the acceptance limits contained in

applicable design documents.

10 CFR 50, Criterion V,

"Instructions, Procedures, and Drawings," requires, in part, that

activities affecting quality shall be prescribed by procedures

which include appropriate quantitative or qualitative acceptance

criteria. Failure to perform a test that included the first

siphon as part of the test acceptance criteria and assuring that

such acceptance criteria bounded the acceptable operating range

of the ECCW first siphon is Violation 50-269, 270, 287/94-31-04,

"Inadequate LPSW Suction Source Testing Via the ECCW System."

(5) In Item 5, the design basis of the CCW's system capability to

withstand loss of Lake Keowee was not translated into any design

document.

In response the licensee indicated that a "loss of lake" analysis

would be performed and completed by June 1, 1995. The team

confirmed the licensee had targeted June 1, 1995, for completion

of the analysis.

(6) In Item 6, the design basis of the LPSW's system capability to

function as described in Case B of Abnormal Procedure

AP/1/A/1700/13, "Loss of Condenser Circulating Water Intake

Canal/Dam Failure," Step 5.5.1, was not translated into any

design document.

During this follow-up inspection, the licensee stated that the

analysis had not been started, pending completion of the heatup

analysis of the pond area for the loss-of-dam event (see part E

above).

This was based on the assumption that the latter

analysis was required for input to the former. The team pointed

out that these two heatup conditions occur in completely

different time frames - the former over a period of minutes, or

Enclosure 2

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12

at most hours, the latter over a period of days. Therefore, the

LPSW heatup analysis could be performed starting with the initial

conditions of the pond, and could be performed in parallel with

the pond heatup analysis. The licensee indicated the analysis

would be completed by June 1, 1995.

(7) In Item 7, the design basis of the SSF ASW system capability to

remove decay heat was not adequately translated into design

documents in that a minimum flow less than required by 23 gpm per

steam generator pair was established in calculation OSC-4171.

The calculation had been revised and this concern has been

corrected.

In summary, Items 2 and 7 were closed. All other items remain open

pending licensee actions.

d. (Open) VIO 50-269, 270, 287/93-25-04 (Violation A in Inspection Report

93-25), "Inadequate Evaluation of Conditions adverse to Quality by

Engineering." There were two parts associated with this violation.

(1) In Item 1, the evaluation of PIP 92-454 for a postulated water

hammer within the LPSW piping downstream of the RBCUs did not

include the consequences on the structural integrity of the

piping.

In response to the violation, PIP 93-1031 was written and OSC

6020 performed indicating turbine building flood was the bounding

event. To eliminate the water hammer a flow orifice would be

installed downstream of the potential cavitation and a schedule

for modification implementation would be provided by September 1,

1994.

The provided documentation indicating projected orifice

installation at the next respective refueling outages. However,

the documentation also indicated that corporate engineering had

been requested to conduct detailed computer analysis to determine

if the water hammer would occur on the discharge of the RBCUs.

Based on corporate engineering results, the discharge from the

RBCUs was determined to always be in a condition of two-phase

flow. Any waterhammer would be dampened by the two-phase state.

Therefore, installation of a flow orifice to increase downstream

pressure would have the detrimental effect of eliminating the

dampening effect of the two-phase state. The results of these

tests were to be available at a later date.

(2) In Item 2, the evaluation for corrective action to design study

ONDS 327 and Problem Investigation Report 92-084 of the

postulated response of the HPSW system to the maximum

hypothetical earthquake did not include spurious fire protection

component activations. In response to the violation, the

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13

licensee stated calculation OSC-2280,"LPSW NPSHa and Minimum

Required Lake Level," was revised to account for HPSW system

malfunction. Consequently, SLC 16.9.7 was revised.

The team confirmed the calculation had been performed and the SLC

revised. Also, the licensee indicated that the deluge valve had

been included in the components to be qualified via SQUG.

Item 1 of this violation remains open pending orifice installation or

completion of additional analyses showing the orifices are not

required.

Item 2 is considered closed.

e. (Open) IFI 50-269, 270, 287/93-25-05, "Additional Validation of RBCU

Evaluation Inputs."

There was two inputs in question dealing with

LPSW flow orifice accuracy and assumptions on air flow distribution

The licensee reinstalled the flow orifices after replacing the RBCUs

in all units. The team inspected the piping that was replaced on the

inlet and outlet of the RBCUs for Unit 1 and determined that the

corrosion buildup was minimal. A review of the calculations to show

that the new coolers were operable used data from the cooling water

side to calculate the heat removal capability. It was as.sumed that

the heat removal was the same for the air side and this was used to

calculate the air flow. The team's review of the calculations showed

that there was adequate margin in the coolers' heat removal

capability.

The team observed licensee attempting to take air flow measurements

during the current refueling outage but the attempt was poorly

coordinated and not accomplished. The licensee stated air flow

measurements would be obtained during the next refueling outage. This

inspector follow-up item remains open pending the licensee acquiring

the air flow data.

f. (Open) IFI 50-269, 270, 287/93-25-06, "Actions to Improve Operator

Responses to Abnormal Events." There were three parts associated with

this item.

(1) In part A, the prerequisite for the total loss of LPSW was no

LPSW pump operating; not inadequate LPSW flow. The licensee

revised the prerequisite of the procedure with no problems

identified.

(2) In part B, Abnormal Procedure AP/1/A/1700/13, "Loss of Condenser

Circulating Water Intake Canal/Dam Failure," had several

weaknesses. The licensee generated PIP 0-094-0514 to revise the

procedure and improve operator training to address these

, concerns.

Operator training had been revised and taught to the 1994-95

licensed reactor operator and senior reactor operator class.

Also, other licensed operators would be taught during the 1994-95

Enclosure 2

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14

PTRQ classroom training. The procedure revision was scheduled to

be completed by November 30, 1994.

(3) In part C, potential weaknesses in the operator guidance for

response to a severe tornado were identified. The licensee

indicated that a tornado would be considered as part of an

upcoming exercise to ascertain whether further operator guidance

was warranted.

In summary, part A is closed. Part B will remain open until the

revision to Abnormal Procedure AP/1/A/1700/13, "Loss of Condenser

Circulating Water Intake Canal/Dam Failure," is issued. Part C will

remain open until the exercise is accomplished and any additional

guidance provided.

g. (Open) VIO 50-269, 270, 287/93-25-08 (Violation D in NRC Inspection

Report 93-25), "Inadequate SSF and ECCW Testing."

There were three

parts associated with this violation.

(1) In Item 1, ECCW flow test procedure PT/1/A/0261/07 did not

account for the potential + 2,000 gpm error which could result

from the method used to measure flow - observation of the impact

point of the ECCW discharge flume.

In response the licensee committed to produce an analysis by July

1, 1994, and incorporate its results in the test procedure by

August 1, 1994.

A revision to the analysis, OSC-5629, "ECCW Test Acceptance

Criteria Inputs," was issued on July 13, 1994. There were no

technical discrepancies associated with the new analysis.

However, the results were not incorporated into the test

procedure at the time of the follow-up inspection. The licensee

stated that they had intentionally delayed incorporation until

just before the next required procedure performance at the next

refueling outage so that all other ensuing changes can be

incorporated at the same time in one overall revision. The NRC

had not been informed of the implementation schedule change. The

licensee indicated a letter would be submitted on the schedule

change.

(2) In Item 2, the preoperational test program for the SSF's SWS and

the post-construction flushing procedure for the SSF's discharge

lines to all the SGs were inadequate.

In response the licensee committed to performing reverse flow

testing of each unit's SSF ASW supply piping. Adequate flush

velocities would be achieved during the testing along with water

samples to verify the flush was adequate.

Procedures were revised and the first test (Unit 1) had been

completed. The preliminary results appeared to address the

Enclosure 2

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15

initial concerns. There was provision for assuring the

velocities would be adequate and that condensate would be used to

flush the lines. The procedure also had steps to ensure that the

condensate flow out of sample lines were clear. Also, the

licensee had replaced the SSF feedwater control valves and added

bypass valves to assist in the control of the SSF feedwater flow

to the steam generators. The modifications appeared adequate.

(3) In Item 3, "Periodic Safe Shutdown Facility Auxiliary Service

Water Pump Operability Test," PT/O/A/0400/05, was not performed

under suitable environmental conditions in that the pump was

preconditioned in step 12.2 by venting the pump just prior to it

being started.

In response the licensee committed to eliminate the

preconditioning from the procedures by September 1, 1994. The

team verified the procedure had been adequately revised.

In summary, Item 3 is closed.

Items 1 and 2 remain open pending

completion of corrective action by the licensee.

h. (Closed) IFI 50-269, 270 ,287/93-25-09, "CCWPump NPSH Information."

The initial inspection report noted incomplete documentation of the

NPSH requirements and availability for design basis conditions for the

CCW pumps for the Keowee Dam failure event.

The licensee provided three letters from the pump manufacturer, one

dated June 29, 1967 and two dated July 3, 1967, which had been

discovered after the initial inspection when a vendor letter dated

February 16, 1968, had been provided. These verified the capability

of the pumps to operate at conditions down to lake elevation 770' (the

elevation of the top of the impounded pond weir) and 90'F (the design

temperature for plant components served by LPSW), and down to 767' at

an unspecified temperature, without NPSH problems. This information

encompassed the LOOP/LOCA situation. The licensee indicated there

would be additional attempts to obtain more definitive information

from the vendor on the minimum NPSH requirements.

However, the worst case design basis conditions of available NPSH were

for the loss-of-Lake Keowee event which produced the lowest intake

level and highest intake temperature. This event begins with the

level at the top of the weir and the water at the design maximum

temperature. During the event, the level decreases due to evaporation

and seepage from the impounded area, and the temperature increases as

the CCW water is recirculated to the impounded area carrying the plant

decay heat. The analyses of this event will be completed in response

to Violation 50-269, 270, 287/93-25-03F. Therefore, the acceptability

of the CCW pump NPSH requirements will be reviewed in conjunction with

the completed licensee analysis.

Enclosure 2

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16

i. (Open) DEV 50-269, 270, 287/93-25-10 (Deviation B in NRC Inspection

Report 93-25), "Inadequate HPSW SBO Test."

The test did not properly

establish initial testing conditions and provided weak guidance when

problems were identified. In response the licensee committed to

revise the test procedure.

The test procedure had been revised, and all but one initial issue had

been addressed. For the condition of a severely leaking HPSW pump

discharge check valve, the updated procedure still directed the

operator to isolate the faulty valve and allowed the test to proceed

and the results to be accepted, when the test would not have passed

with the valve un-isolated. The PIP contained a statement that "The

test can continue with the leaking check valve isolated", and a note

still existed in the procedure to make an entry in the turnover sheets

to inform the Operators to shut the affected pump's discharge valve

upon loss of power to prevent excessive losses of the EWST, implying

that a leaking check valve was acceptable with regard to the test

results. As noted in the original inspection report, this is not

acceptable since it is not reasonable to expect that an operator would

isolate the valve before excessive losses from the EWST could have

occurred in an actual SBO event. Numerous, complex operator actions

are necessary to respond to an SB0 event. The guidance for performing

the isolation is not contained in an emergency procedure but on a

rounds checklist.

This deviation remains open pending appropriate resolution to a

leaking HPSW pump discharge check valve when performing the test.

j. (Closed) IFI 50-269, 270, 287/93-25-11, "Jocassee Dam Failure IPE."

Inaccuracies:

contrary to the IPE submittal the SSF could not

withstand the postulated external flood. Also, IPE Submittal report,

Section 3, Subsection 13, indicated there was an 8' waterproof flood

wall around the SSF ground level entrances. The wall was actually 5'

in height.

The licensee stated a supplemental response to the IPE on external

events in 1995 would include re-analysis of risk impact of external

flood. Also, further enhancements would be evaluated as a result of

this re-analysis.

The licensee had not completed the analysis of the Jocassee dam

failure. Calculation OSC-5781, "USQ Evaluation for Change in FSAR

Concerning SSF and Jocassee Flood," provided the justification for

changing the FSAR. The change removed the requirements of SSF

mitigation for a rapid Jocassee Dam failure. This was based, in part,

on PRA data, IPE information, and other information submitted to the

Commission. The revised IPE will be reviewed by the NRC as part of

the external events IPE submittal.

This item is closed.

Enclosure 2

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17

k. (Open) VIO 50-269, 270, 287/93-25-12 (Violation C in NRC Inspection

Report 93-25), "SWS Procedure/Drawing Content or Procedure

Implementation Inadequacies." There were five parts associated with

this violation.

(1) In Item 1, engineering administrative procedures did not

establish a definitive length of time for revising calculations

following design changes.

In the licensee's original response to the violation the licensee

stated that Procedure EDM-101, Engineering Calculations/Analysis,

would be revised to provide the necessary guidance by September

1, 1994. However, in a letter dated September 13, 1994, almost

two weeks beyond the committed dated, the licensee stated that

the plant modification process would be revised by November 1,

1994, to provide the necessary guidance.

The original inspection finding dealt with calculations

associated with the SSF SWSs. With regard to these, many of the

older calculations have been deleted. Some calculation revisions

are on hold while the DBD is being completed. This is scheduled

for mid-1995.

The definition of design documents to be updated with a facility

change had been modified to include affected design calculations.

However, the infrastructure to implement the requirement did not

exist. Other than engineer memory, there was no method to

identify all other calculations affected by the calculation

needing revision. Even if recognized by the engineer, there was

no method to flag that a calculation needed revision. Also, a

calculation could be revised without using the administrative

requirements of the facility change process. Further licensee

actions were necessary to reasonably assure administrative

requirements were properly implemented. This violation remains

open pending such corrective action.

(2) In Item 2, no flow instruments existed to confirm 200 gpm was

being provided to each steam generator or 400 gpm to an un

isolated steam generator by the Auxiliary Service Water pump as

directed by Emergency Procedure EP/1,2,3/A/1800/01, Section 502.

In the response to the violation, the licensee stated the

emergency procedure would be revised and training on the

procedure revision completed by October 1, 1994.

The procedure was revised by the committed date. However, step 7

of the procedure controlled flow via the recirculation valve.

Such an action could not actually control flow to all the units

or SG pairs.

10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures,

and Drawings," requires that activities affecting quality shall

Enclosure 2

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18

be prescribed by documented instructions, procedures, or

drawings, of a type appropriate to the circumstances. Failure to

provide adequate procedural direction to accomplish this task is

violation 50-269, 270, 287/94-31-05, "Inadequate ASW Procedure."

However, the licensee had previously identified the error and was

in the process of revising the procedure. This violation will

not be subject to enforcement action because the licensee's

efforts in identifying and correcting the violation meet the

criteria specified in Section VII.B of the Enforcement Policy.

(3) In Item 3, Keowee Turbine Generator Cooling Water system

drawings, KFD-100A-1.1 and KFD-100A-2.1 did not indicate the

existence of an additional valve downstream of valve 2WL-3 for

Unit 2, the supply line to the air compressor coolers was

interconnected to the 12" main piping for Unit 1, the piping

downstream of valve WL-76 was copper for both Units, or a

consistent piping class break in the supply line to the generator

thrust bearing coolers for both Units.

In the response to the violation, the licensee stated PIP 0-093

0986 was initiated to address these items. Also, the drawings

would be re-verified by walkdown with all identified errors to be

corrected by July 1, 1994.

The KFD-100A-1.1 and KFD-100A-2.1 drawings had been revised in

July 1994. A walkdown of select Keowee mechanical systems with

the revised drawings reflected an additional valve downstream of

valve 2WL-3 for Unit 2 not shown on the drawing. This was one of

the original discrepancies documented in the Notice of Violation.

The team determined through interview with the engineering

personnel involved in the resolution of the PIP that only a

partial walkdown of the service water mechanical systems was

performed through verbal mis-communication. Also, the drawing

editorial change process was used to update the drawings which

contained a limited check for accuracy of the walkdown

activities.

Once the licensee was notified of the drawing discrepancy by the

team, the additional valve downstream of valve 2WL-3 was removed.

However, the licensee failed to adequately correct the design

document error in July 1994 or adequately perform a walkdown of

the mechanical systems.

10 CFR 50, Appendix B, Criterion XVI,

"Corrective Action," requires conditions adverse to quality be

promptly identified and corrected. This is considered an example

of Violation 50-269, 270, 287/94-13-018, "Inadequate Corrective

Action Controls."

(4) In Item 4, a condition adverse to quality report dealing with the

removal of the Keowee Unit 2's turbine guide bearing oil cooler

was neither properly processed nor did it receive a written

operability evaluation.

Enclosure 2

.

Report Details

19

In response to the violation, the licensee stated an operability

evaluation would be completed on the ramifications of removing

the oil cooler from service without declaring the unit inoperable

by November 1, 1994. Also, involved personnel were retrained on

the condition adverse to quality procedure.

The involved personnel were retrained. Also, on November 1, 1994

the licensee satisfactorily completed an operability

determination in calculation KC Unit 1-2-0107, "Keowee Turbine

Guide Bearing Temperature Calculation," with results indicating

the oil cooler was not necessary for unit operability. This

violation example is closed.

(5) In Item 5, the appropriate housekeeping zones were not being

assigned to select maintenance activities at Keowee.

In response to the violation, the licensee stated that all

applicable maintenance procedures would be revised by October 1,

1994. Also, training on housekeeping zone requirements would be

given to Keowee personnel by August 1, 1994.

The applicable procedures were revised, and training was provided

to the Keowee personnel.

However, the training was given 50 days

after the committed date. Keowee personnel were aware the date

assigned was not met and had contacted regulatory assurance

personnel. The regulatory assurance personnel involved did not

understand NRC concurrence would be necessary to extend the

commitment date and stated that the missed commitment date would

be updated in quarterly correspondence with the NRC on electrical

inspection issues.

In summary, Items 2, 3, 4, and 5 are closed.

Item 1 remains open

pending completion of additional licensee corrective actions.

1. (Closed) IFI 50-269, 270, 287/93-25-14, "Review of Revised ASW Pump

NPSH Calculation."

During the original inspection calculation OSC-5125, "ASW NPSH

Analysis," assumed siphon flow from the intake canal to the ASW pump

suction would be in operation following the tornado. However, the

ECCW siphon lacked tornado protection, and would not be operational.

Therefore, the minimum suction height was contingent upon the

inventory losses in the CCW piping as a result of ASW pump operation.

Minimum NPSH for the ASW pump was -2.22 psig which meant that the pump

could draw water from 5.12 feet below the pump's impeller eye and

still have adequate NPSH. However, the licensee failed to consider

the actual configuration of the CCW piping going to the suction of the

ASW pump. Therefore, when the water in the CCW piping dropped to a

height of 770.46 feet, inadequate NPSH would occur. Consequently, the

amount of water available for ASW pump use was noticeably reduced.

Enclosure 2

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20

The licensee failed to correct the calculation and failed to identify

that the error in the calculation constituted a condition adverse to

quality and required the initiation of a PIP. During the follow-up

inspection this failure to initiate a PIP was identified to the

licensee. PIP 94-1500 was subsequently initiated which also

identified OSC-0864, "RC System DH Removal following a Loss of Intake

Structure," as being deficient. The licensee's site directive on the

problem identification process requires the initiation of a condition

adverse to quality report (PIP) when there are errors in design bases

documents and when documents are not updated.

10 CFR 50, Appendix B,

Criterion XVI, "Corrective Action," requires in part that conditions

adverse to quality be promptly identified. Failure to originally

identify this condition adverse to quality by initiating a PIP was an

example of Violation 50-269, 270, 287/94-13-01C, "Inadequate

Corrective Action Controls."

m. (Open) IFI 50-269, 270, 287/93-25-15, Administrative Controls for Lake

Keowee: Calculation OSC-3528, "Keowee Lake Level Minimum

Administrative Limits," had numerous technical weaknesses. The

calculation was an attempt to establish a minimum lake level necessary

to ensue operability of Oconee and Keowee for design basis events.

No further actions had been accomplished since the original

inspection. The licensee indicated that this matter had "dropped

through the cracks" following a reorganization and changes in

personnel within the engineering department. The licensee indicated

an individual would be assigned to address this matter. This issue

remains open pending licensee action.

4. Inspection Report 93-25 Cover Letter Responses

The SWSOPI cover letter dated February 11, 1994, requested a written

response describing analysis, rational or actions planned regarding:

The presence of only one valve isolating the safety-related portion of

the LPSW system from the nonsafety-related turbine building portion.

  • The SSF could not withstand a postulated failure of the Jocassee Dam.

The HPSW system was not designed or maintained commensurate with its

importance to safety.

Also, the cover letter requested the licensee's design control measures,

engineering evaluations, testing program, and the safety classification of

components system be evaluated to determine any necessary programmatic

corrective actions warranted by this inspection report.

In letters dated March 12, 1994, and April 20, 1994, the licensee

discussed these issues defined in the cover letter to the SWSOPI report.

The team reviewed the licensee responses and ascertained the status of the

corrective actions identified within the body of the letters. The results

of the reviews were as follows:

Enclosure 2

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a. LPSW Single Isolation - This matter is closed as discussed in

paragraph 3.b of this inspection report.

b. Ramifications of Jocassee Dam Failure on the SSF - This matter is

closed as discussed in paragraph 3.j of this inspection report.

c. Design and Maintenance of the HPSW System

(1) The initial inspection report discussed that covers for sections

of the trench in which the power and control cables for the CCW

pumps run, as well as the HPSW sealing/cooling water supply line

to the pumps, were not bolted down and could fall into the trench

in a seismic event, potentially damaging these components. It

was also reported that the cover for the structure housing the

ECCW valve CCW-8 was not restrained and could potentially fall on

the valve in a seismic event.

The licensee generated PIP 0-094-504 to perform a minor

modification to provide a seismic design for the trench covers in

question. However, this PIP was closed out on June 29, 1994,

when the design package was completed, but the work still had not

been started at the time of the follow-up inspection. When this

was discovered by the team, the licensee indicated the PIP would

be reopened to ensure completion of the installation work.

The team also found that no actions had been performed on the

structure cover for valve CCW-8, and inspection revealed that one

of the three cover plates was out of position and resting on one

of the other plates, making it particularly vulnerable to a

seismic event. The initial licensee response was that since

functions for which this valve were required did not have to be

considered in conjunction with a seismic event, it did not have

to be seismically qualified. The team pointed out to the

licensee that the requirement for safety-related equipment to be

seismically qualified is solely because it is safety-related; it

is not dependent on there being a seismic event linked to the

event for which it is required.

The licensee indicated the cover would be restored to its proper

location and signs installed on these covers and the trench

covers indicating they must remain in place for the seismic

qualification of the equipment to remain valid.

(2) The initial inspection report discussed that the operator rounds

sheets contained no upper limits on the HPSW flows to the CCW

pumps and motors for sealing and cooling respectively, and that

17 of the 24 flow instruments for these pumps were above the

values used to calculate the 4-hour, SBO capacity of the EWST.

The licensee's response in the March 14, 1994, letter was that if

the EWST SBO test passed, it was irrelevant if the flows were

above the values used in the EWST capacity calculation. This is

Enclosure 2

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22

not correct. Without upper limits on the flow, even with

satisfactory test results, during the one year interval to the

next test, the flow could be significantly increased, without

constraint or indication, potentially rendering the test results

invalid.

During the follow-up inspection, the licensee acknowledged that

upper limits on the flows were appropriate and indicated

necessary actions would be to taken.

(3) The initial inspection report discussed that HPSW performs the

function of providing sealing and cooling water to the CCW pumps

and motors respectively. These flows are set and monitored using

rotameters at the CCW pumps. The initial inspection found that

these instruments were being improperly set and poorly

maintained.

In the licensee's letter response of March 14, 1994, it was

stated that if the flow were actually inadequate, it would

adversely affect pump performance, implying that this reduced

performance would be detected during normal operation. This is

not correct. Normal pump performance is not at all affected by

loss of seal water. This loss only affects its safety-related

function of maintaining the "first siphon" integrity when the

pumps are not running.

(4) The initial inspection report discussed the poor material

condition of the CCW rotameters.

The licensee responded in the March 14, 1994, letter that a PIP

had been written to document the off-scale high reading of a

number of rotameters. As corrective action to this PIP the

licensee initiated a preventative maintenance activity to

periodically clean the rotameters.

The team reinspected these devices during the follow-up

inspection and found essentially the same conditions as the

initial inspection. Ten of the twenty-four instruments contained

significant slime contamination, and one contained three clams,

making the accuracy of their indication questionable. Eleven of

the flow instruments were pegged at the high end of the scale.

Therefore, this parameter was not monitorable with these

instruments.

Since readings from these instruments were taken as a part of the

normal operator rounds, the team reviewed the non-licensed

operator turnover sheets, OP/2/A/1102/20, Enclosure 5.7, and

rounds sheets, Enclosure 5.11, dated October 9, 1994, and

October 10, 1994, to determine if any notation had been made of

their material condition. No notation had been made.

Enclosure 2

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23

Operations supervisors were questioned on the training of

operators regarding recognition of discrepant conditions and how

conditions, such as were found, could exist. Operations

personnel indicated that as long as flow could be determined or

pegged high, since engineering had not established an upper

limit, the condition would not be identified.

The licensee had initiated a PIP and took the corrective action

identified. However, the actions were ineffective. 10 CFR 50,

Appendix B, Criterion XVI, "Corrective Action," requires in part

that conditions adverse to quality be promptly corrected. The

failure of the PIP corrective actions to adequately resolve the

poor material condition of the CCW rotameters or even ensure that

the material condition discrepancies were identified is an

example of Violation 50-269, 270, 287/94-31-OlD, "Inadequate

Corrective Action Controls."

(5) The initial inspection report identified that the HPSW pump check

valves, HPSW-2, 5, and 8 were not being properly tested. Also,

the these valves and the pumps had not been properly classified.

The licensee responded in the March 14, 1994, letter that a PIP

had been written to add these valves to the IST program. Also, a

PIP was written to update the QSM and DBD for the HPSW system.

The team found that the QSM and IST corrective actions were

predicated upon revision of the DBD. The DBD revision was still

in draft form with the corrective action completion schedule

extended to the end of the year.

(6) The initial inspection report discussed the structural capability

of the HPSW system.

The licensee responded in the March 14, 1994, letter that

inspected piping met minimum wall thickness criteria, the hanger

design was acceptable, and appropriate consideration had been

enacted with a revision to the SLC 16.9.7 to account for spurious

HPSW actuation. The response also stated, "Oconee recognizes

that the HPSW System was not required to be designed and

constructed to the seismic design criteria presented in Section

3.7 and 3.9 of the Oconee FSAR."

The team confirmed the SLC had

bee revised. However, the overall design and construction

requirements of the HPSW system continues to be reviewed by the

NRC as part of URI 269, 270, 287/93-13-03, "ECCW System Design

and Testing."

d. Design Control/Engineering Evaluations - The licensee indicated EDM

101, "Engineering Calculations/Analyses," would be revised to clarify

management expectations on the verification and validation of design

inputs and assumptions. Also, all required functions identified in

Enclosure 2

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the mechanical systems DBDs would be reviewed against both the

existing calculational support for that function and the existing

emergency operating procedures and the abnormal procedures.

The team verified the revision to EDM-101 and determined the status of

the mechanical systems DBD review. The review was in its initial

stages.

Also, the team selected another subsystem of the SSF to determine

whether there were additional problems within the design control area.

A review of the SSF RC make-up calculations revealed deficiencies.

Some of the calculational inconsistencies that were similar to those

present in the SSF calculations reviewed during the previous

inspection. The licensee indicated that many of these would be

corrected when the DBD was issued. The DBD was scheduled to be issued

in November 1994.

The most significant deficiency was in OSC-619, "Analysis for the use

of Spent Fuel Pool Inventory for Standby Shutdown Facility."

The

deficiency was the failure to fully account for the high radiation

levels of the Spent Fuel Pool in a timely manner when the water level

dropped to one foot above the top of the spent fuel.

The licensee's

preliminary analysis indicated the radiation levels would be

approximately 2,000,000 Roentgens per hour at the pool surface at 72

hours following loss of fuel pool cooling. There were no time

specific requirements for restoration of fuel pool make up.

Additionally, there were no specific procedural steps for performing

this evolution nor was equipment staged for this repair. This is

Unresolved Item 50-269, 270, 287/94-31-06, "High Spent Fuel Pool

Radiation Levels."

e. Testing - The licensee indicated that significant progress was being

made in developing and implementing integrated system testing. Also,

all required functions identified in the DBDs were being reviewed

against existing test procedures to ensure the function was being

appropriately verified.

The team ascertained the DBD/testing review was in progress.

f. Safety Classification - The licensee indicated that further review as

to whether the QSM was complete was ongoing. For those cases

maintenance and testing procedures would be upgraded consistent with

the Quality Assurance program.

The team recognized the licensee's effort but additional evaluation of

Generic Letter 83-28 and a review of the licensee's response to that

GL would be necessary to fully understand the adequacy of the

licensee's corrective actions in this area.

Completion of these programmatic reviews in the areas of

Testing/QSM/Design Control is an Inspector Follow-up Item 50-269, 270,

287/94-31-07, "Quality Programs Review."

Enclosure 2

Report Details

25

5. Review of Valve LPSW 139 to Close

The licensee had recalculated the closing torque requirements using the

EPRI methodology developed for butterfly valves. These calculations

indicated that the valve operators had sufficient torque to close and seat

the valves. This result differed from the calculation provided with the

licensee's response to IR 93-04 in that there was no assurance that

sufficient torque to seat the valves. The licensee had conducted

laboratory testing for valve closure against high differential pressure

for the new LPSW-139 valve, but no high differential pressure testing has

been conducted on the valve currently installed. As documented in the

licensee's response to IR 93-04, the licensee plans to install the new

LPSW-139 valve in parallel with the current valve during the next Unit 1

outage currently scheduled for October 1995.

6. IST Program Scope versus Appendix B Testing Program Scope

During the initial SWS inspection certain aspects of the licensee's ASW

system testing program as it related to the IST requirements arose.

Specifically, the licensee used a combination of IST and an Appendix B

test program to encompass the testing of the safety-related valves. As a

result of the discussions with the licensee regarding the scope of their

testing program, the team expanded the scope of review to include all

valves included in the Appendix B program which were not included in the

IST program. The results of that review were as follows:

a. The scope of the licensee'sSection XI test program only encompassed

that equipment used to mitigate accidents discussed in chapter 15 of

the FSAR. Due to Oconee's unique design, other equipment not credited

in the chapter 15 accidents is used to mitigate accidents discussed in

other chapters of the FSAR such as a tornado. Therefore, there were

omissions in the ASME Section XI test program.

b. The ASW check valves (LPSW-502) allowing flow to the HPI pump motor

coolers had not been tested. HPI pump motor cooling via the ASW

system was assumed to mitigate the consequences of certain types of

tornadoes and to mitigate the consequences of a complete loss of the

intake canal water. The licensee had previously identified the

testing omission and initiated a PIP. Plans and preparations were

being made to accomplish the testing before the end of the year. This

situation was similar to NCV 50/269, 270, 287/93-25-13, "Omissions of

LPSW Check Valves from IST Program."

c. Other valves necessary to function to mitigate the consequences of a

tornado were not included within the IST program. Most notable were

the atmospheric dump valves (MS 153-156 & 161-164) and the condenser

water box isolation valves (CCW 21-25).

These valves were tested

during shutdown conditions but not at the frequency specified in

Section XI of the ASME code. No relief request had been submitted to

the NRC concerning these valves.

Enclosure 2

Report Details

26

d. Numerous valves associated with the air start and fuel supply systems

to the SSF DGs were not identified as part of the IST program.

However, the valves were being tested at the required frequency.

f. The manual MTOTC bypass valve, LPSW-51, was not identified as

requiring testing, ASME Section XI nor Appendix B. The licensee's

analysis credited its closure (when the MTOTC valve was out of

service) during a LOCA/LOOP. When identified to the licensee PIP 94-438 was initiated.

10 CFR 50.55(a) requires safety related values be included within the

Section XI valve test program. Failure to include the ASW check valves,

atmospheric dump valves, and the MTOTC bypass valve within the scope of

the ASME code Section XI test program is Violation 50-269, 50-270,

50-87/94-31-08, "ASME Section XI Test Program Omissions."

7. Review of High Energy Break Ramifications within Containment and Planned

Corrective Actions

On June 2, 1993, the licensee determined that the original MSLB within

containment analysis was nonconservative and LER 50-269/93-06 was

submitted on the subject. In a letter dated May 27, 1993, the licensee

discussed the rationale as to why there should be continued reliance upon

the control grade integrated control system and operator action prior to

  • implementation

of a long term solution. In a letter dated August 19,

1993, the licensee also discussed the long term solution, an automatic

feedwater line isolation scheme, to be implemented in the 1995/96

timeframe. In a letter dated October 6, 1993, NRC indicated this approach

was viable.

The worst scenario discussed in the licensee's correspondence involved the

MSLB with the accompanied failure of the feedwater control valve to close.

The analysis concluded that containment design pressure would be exceeded

(but structural yield pressure would not be reached) if manual action to

close the feedwater block valve was taken within two minutes.

The team reviewed the containment temperature and pressure curves for this

case of "Without Credit for Automatic Main Feedwater Control and Main

Feedwater Control Valve Sticks Open". This case indicated that the EQ of

equipment (mostly instrumentation) used to mitigate a MSLB was exceeded

from a temperature perspective. The temperature EQ would be exceeded in

the short term and long term.

This observation appeared to contradict other licensee statements in their

correspondence of May 27th and August 19th which stated that the equipment

required to mitigate the consequences of the MLSB was qualified and would

perform its safety function. Discussions with the licensee indicated that

the EQ statement was for the equipment after implementation of the long

term solution for MSLB or in the design bases LOCA, and the equipment had

not been EQ reviewed for the pressures and temperatures in the MSLB with a

control valve failure case. Since this information was not clearly stated

in the licensee's correspondence to the NRC (letters dated May 27, 1993

Enclosure 2

Report Details

27

and August 19, 1993), the team notified the NRR Project Manager

responsible for review of the adequacy of the licensee's response.

Subsequently the Project Manager informed the team that the new

information did not change the original NRC decision on this matter.

The team reviewed the current status of the proposed long term solution.

The licensee stated that the modification would close non safety related

valves and that the equipment would be EQ qualified for MSLB's. The

schedule for implementation of the modification was feasible considering

the fact that advantage will be taken of already installed safety-related

equipment. The licensee indicated that some of the long term solution

discussed in their letter of August 19, 1993, was going to be modified. A

discussion with the NRR Project Manager indicated that the NRC understands

that the licensee intends to submit surveillance and technical

specifications that would ensure the operability of the modification.

8. Exit Interview

The team conducted an exit meeting on October 27, 1994, at the Oconee

Nuclear Power Station to discuss the major areas reviewed during the

inspection, the strengths and weaknesses observed, and the inspection

results. Licensee representatives and NRC personnel attending this exit

meeting are documented in Appendix A of this report. The team also

discussed the likely informational content of the inspection report. The

licensee did not identify any documents or processes as proprietary.

There were three dissenting comments at the exit meeting associated with

the lack of gravity/siphon flow testing, the scope of the ASME code

Section XI valve test program and the failure to initiate a PIP when an

inaccurate reference was used when performing calculation OSC-2346, "ECCW

System Performance Evaluation." The licensee indicated a thorough review

of the inspection findings would be necessary to ascertain the appropriate

responses or corrective actions to the issues identified.

Also, an exit was held with the cognizant SSF engineer associated with the

team's attempt to witness SSF SWS testing. There were no findings since

the test could not be performed due to unanticipated scheduling delays in

establishing the plant conditions for the testing.

Enclosure 2

Report Details

28

ITEM NUMBER

STATUS

PARAGRAPH

DESCRIPTION

93-25-01

Open

3.a

DEV - Failure to Adequately Perform

SWS GL Actions

93-25-02

Closed

3.b

UNR - Turbine Building Isolation

Single Failure Vulnerabilities

93-25-03

Open

3.c

VIO - Failure to Perform

Adequate Calculations and

Evaluations to Support

Facility Design

93-25-04

Closed

3.d

VIO - Inadequate

Evaluation of Conditions Adverse to

Quality by Engineering

93-25-05

Open

3.e

IFI - Additional Validation of RBCU

Evaluation Inputs

93-25-06

Open

3.f

IFI - Actions to Improve

Operator Responses to

Abnormal Events

93-25-08

Open

3.g

VIO - Inadequate SSF and ECCW

Testing

93-25-09

Closed

3.h

IFI - CCW Pump NPSH Information

93-25-10

Open

3.i

DEV - Inadequate HPSW SBO Test

93-25-11

Closed

3.j

IFI - Jocassee Dam Failure IPE

Inaccuracies

93-25-12

Open

3.k

VIO - SWS Procedure/Drawing Content

or Procedure Implementation

Inadequacies

93-25-14

Closed

3.1

IFI - Review of Revised ASW Pump

NPSH Calculation

93-25-15

Open

3.m

IFI - Administrative Controls for

Lake Keowee

94-31-01

Open

3.a,

VIO -

Inadequate

3.k(3)

Corrective Action

3.1

Controls

4.c(4)

94-31-02

Open

3.c(2)

IFI - Hydraulic Model Controls

Transition

94-31-03

Open

3.c(4)

IFI - Reperformance of Calculation

Enclosure 2

Report Details

29

OSC-2346

94-31-04

Open

3.c(4)

VIO - Inadequate LPSW Suction Source

Testing Via the ECCW System

94-31-05

Closed

3.k(2)

NCV - Inadequate ASW Procedure

94-31-06

Open

4.d

UNR - High Spent Fuel Pool Radiation

Levels

94-31-07

Open

4

IFI - Quality Programs Review

94-31-08

Open

8

VIO - ASME Section XI Test Program

Omissions

Enclosure 2

LIST OF PERSONS CONTACTED

Duke Nuclear Power Plant

Persons Contacted

L. Azzarello, Mechanical Engineering

S. Baldwin, Mechanical Systems Engineering

D. Coyle, Mechanical Systems Manager

B. Dolan, Safety Assurance Manager

W. Foster, Maintenance

R. Harris, Mechanical Systems Engineering

W. Horton, Operations Support

D. Hubbard, Maintenance

$ H. Lefkowitz, Mechanical Systems Engineering

  • G. McAninch, Mechanical Systems Engineering
  • B. Millsaps, Mechanical/Civil Engineering
  • $ J. Smith, Regulatory Compliance

R. Swigant, Work Control

U.S. Nuclear Regulatory Commission

  • $ L. Mellen, Reactor Inspector
  • D. Prevatte, Powerdyne Corporation

C. Rapp, Reactor Inspector

W. Rogers, Team Leader

L. King, Reactor Inspector

P. Harmon, Senior Resident Inspector

L. Keller, Resident Inspector

  • Indicates those present at the exit meeting on October 27, 1994

$ Indicates those involved in the exit on November 3, 1994

Enclosure 2, Attachment A

LIST OF ACRONYMS AND ABBREVIATIONS

.

ASME -

American Society of Mechanical Engineers

ASW

-

Auxiliary Service Water

CCW

-

Condenser Cooling Water

CFR

-

Code of Federal Regulations

DBD

-

Design Basis Document

DEV

-

Deviation

DG

-

Diesel Generator

DH

-

Decay Heat

ECCW -

Emergency Condenser Cooling Water

EFW

-

Emergency Feedwater

EPRI -

Electric Power Research Institute

EQ

-

Environmental Qualification

EWST -

Elevated Water Storage Tank

FSAR -

Final Safety Analysis Report

GL

-

Generic Letter

GPM

-

Gallons Per Minute

HPI

-

High Pressure Injection

HPSW -

High Pressure Service Water

HVAC -

Heating Ventilation and Air Conditioning

IFI

-

Inspector Follow-up Item

IPE

-

Individual Plant Examination

IST

-

Inservice Test

LOCA -

Loss of Coolant Accident

LOOP -

Loss of Offsite Power

LPI

-

Low Pressure Injection

LPSW -

Low Pressure Service Water

MSLB

-

Main Steam Line Break

MTOTC -

Main Turbine Oil Temperature Control

NCV

-

Non-Cited Violation

NPSH -

Net Positive Suction Head

NPSHA-

Net Positive Suction Head Available

PIP

-

Problem Investigation Process

PRA

-

Probabilistic Risk Analysis

PSIG -

Pounds per Square Inch Gauge

PTRQ -

Personnel Training Requiremental Qualification

QA

-

Quality Assurance

QSM

-

Quality Standards Manual

RBCU -

Reactor Building Cooling Unit

RC

-

Reactor Coolant

SBO

-

Station Blackout

SER

-

Safety Evaluation Report

SG

-

Steam Generator

SLC

-

Selected Licensee Commitments

SQUG -

Seismic Qualification Utility Group

SSF

-

Safe Shut Down Facility

SWS

-

Service Water System

SWSOPI-

Service Water System Operational Performance Inspection

UNR

-

Unresolved Item

USQ

-

Unreviewed Safety Question

VIO

Violation

Enclosure 2, Attachment B