ML16154A718

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Insp Repts 50-269/94-32,50-270/94-32 & 50-287/94-32 on 940925-1029.Violations Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance Testing,Onsite Engineering & Plant Support
ML16154A718
Person / Time
Site: Oconee  
Issue date: 11/23/1994
From: Harmon P, Sinkule M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML16154A716 List:
References
50-269-94-32, 50-270-94-32, 50-287-94-32, NUDOCS 9412060072
Download: ML16154A718 (15)


See also: IR 05000269/1994032

Text

V REG(

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report Nos.:

50-269/94-32, 50-270/94-32 and 50-287/94-32

Licensee:

Duke Power Company

422 South Church Street

Charlotte, NC 28242-0001

Docket Nos.:

50-269, 50-270 and 50-287

License Nos.:

DPR-38, DPR-47 and DPR-55

Facility Name:

Oconee Units 1, 2 and 3

Inspection Conducted: September 25 - ,October 29, 1994

Inspectors:

P. E. Har

,

enior e dent I pector

DaeSigi~d

W. K. Poertner, Resident Inspector

L. A. Keller, Resident Inspector

P. G H

hr y, Resident Inspector

Approved by:

) L '4/_

C,

M. V. Sinkule, Chief,

Dat Si ned

Reactor Projects Branch 3

SUMMARY

Scope:

This routine, resident inspection was conducted in the areas of

plant operations, maintenance and surveillance testing, onsite

engineering, and plant support. As part of this effort, backshift

inspections were conducted.

Results:

During the inspection period one violation and one non-cited

violation were identified. The violation involved two examples of

failure to follow maintenance procedures (paragraph 3.a).

The

non-cited violation involved an inoperable containment isolation

valve due to post maintenance testng not being performed because

of a maintenance error (paragraph 2.f).

An Inspector Followup Item was identified concerning an

inadvertent venting of the Unit 2 quench tank (paragraph 2.e).

A strength was identified in the area of conduct of testing

(paragraph 3.b).

A weakness was identified in the procedure for operation of the

safe shutdown facility diesel generator (paragraph 3.b).

A weakness was-identified in the health physics program concerning

the control of radiation control zones (paragraph 5).

9412060072 941123

ENCLOSURE 2

PDR ADOCR 05000269

PDR

REPORT DETAILS

1.

Persons Contacted

Licensee Employees

B. Peele, Station Manager

  • E. Burchfield, Regulatory Compliance Manager
  • D. Coyle, Systems Engineering Manager
  • J. Davis, Engineering Manager

T. Coutu, Operations Support Manager

B. Dolan, Safety Assurance Manager

  • W. Foster, Superintendent, Mechanical Maintenance

J. Hampton, Vice President, Oconee Site

  • G. Rothenberger, Operations Superintendent
  • R. Sweigart, Work Control Superintendent

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and staff engineers.

  • Attended exit interview.

2.

Plant Operations (71707)

a.

General

The inspectors reviewed plant operations throughout the reporting

period to verify conformance with regulatory requirements,

Technical Specifications (TS), and administrative controls.

Control room logs, shift turnover records, temporary modification

log, and equipment removal and restoration records were reviewed

routinely. Discussions were conducted with plant operations,

maintenance, chemistry, health physics, instrument & electrical

(I&E), and engineering personnel.

Activities within the control.rooms were monitored on an almost

daily basis.

Inspections were conducted on day and night shifts,

during weekdays and on weekends. Inspectors attended some shift

changes to evaluate shift turnover performance. Actions observed

were conducted as required by the licensee's Administrative

Procedures. The complement of licensed personnel on each shift

inspected met or exceeded the requirements of TS. Operators were

responsive to plant annunciator alarms and were cognizant of plant

conditions.

Plant tours were taken throughout the reporting period on a

routine basis. During the plant tours, ongoing activities,

housekeeping, security, equipment status, and radiation control

practices were observed.

b.

Plant Status

Unit 1 essentially operated at 100% power the entire reporting period.

2

Unit 2 conducted normal power operations until October 6, 1994,

when the generator was taken off line at 12:49 a.m. to begin a

scheduled 40-day refueling outage (U2EOC-14). The refueling

outage continued throughout the remainder of the reporting period.

Unit 3 essentially operated at 100% power the entire reporting

period.

c.

Unit 2 Midloop Operation

On October 9, 1994, the inspectors reviewed the licensee's

procedure for reduced reactor coolant (RCS) inventory during the

Unit 2 outage. The procedure (OP/2/A/1103/11, Draining And

Nitrogen Purging Of RC System, revised July 28, 1994) sets forth

the requirements for reducing RCS inventory. These include: a

minimum of two methods of alarmed level indications utilized to

monitor vessel levels; boron concentrations for safe shutdown

margin; availability of safety equipment; alignment and tagging of

systems and equipment; and two independent RCS temperature

indications.

The inspectors verified that the licensee met the requirements

specified in the procedure prior to entering a reduced RCS

inventory status. The low pressure injection flow rates were

being monitored in the control room via the operator aid computer,

flow indicators, and alarms on annunciator panel 3SA-3 (windows A8

and A9).

RCS temperatures were monitored on the operator aid

computer with alarms set at 125 degrees F, on the inadequate core

cooling monitor display, and on the control room instrument panel

The RCS levels were monitored by permanent instrumentation (LT-5A

and B) and ultrasonic level indicators that were installed

temporarily for mid-loop operating conditions. Levels were

alarmed and monitored on control room instruments and on the

operator aid computer.

In addition, the inspectors verified that configuration control of

containment penetrations was maintained. The equipment hatch was

only opened during the outage as necessary to move equipment in

and out of the reactor building. For the remainder of the time,

the hatch remained-closed. However, it was necessary for some

penetrations to remain open to support the outage work schedule

(i.e., cable penetrations for eddy current testing of the steam

generator tubes). A required closure time was addressed in the

event of a loss of decay heat removal capability.

The licensee maintained a Risk Summary Sheet for the availability

of equipment required to support the plant during reduced

inventory. This sheet included the status of systems, electrical

power sources, RCS makeup supplies, and containment penetrations

with the amount of time anticipated for closure. Based on the RCS

inventory, the "time to boil" was calculated in the event of a

loss of decay heat removal cooling. Overall, the licensee's

3

efforts were determined to be adequate in controlling and

monitoring plant conditions while the RCS inventory was maintained

at mid-loop.

d.

Primary Instrument Air Compressor Fails to Load

On September 28, 1994, the inspector observed the Unit 3 control

room operators respond to a drop in the instrument air header

pressure. The instrument air header pressure dropped to less than

80 psig, which resulted in an automatic swapover to service air

and an.automatic start of the auxiliary instrument air

compressors. The cause of the drop in air pressure was the

failure of the primary air compressor to properly-load after it

was started following maintenance.

Subsequent to maintenance, the primary air compressor was-started

and the backup air compressors were secured using OP/O/A/1106/27,

Enclosure 4.1.

Step 2.20 of Enclosure 4.1 instructed the operator

to remove the backup air compressors from service when the primary

air compressor parameters were stable. These parameters were

listed in step 2.19 of this enclosure. This list of parameters

was not sufficient to determine if the primary air compressor was

properly loading. For example, the list of parameters in step

2.19 included sump pressure and gave the allowable range as 50 to

130 psig, whereas if the compressor was properly loaded the sump

pressure would be greater than instrument air header pressure

(approximately 100 psig).

The cause of the primary air compressor

failing to load was the differential regulators being slightly out

of adjustment. The licensee indicated that OP/0/A/1106/27 would

be modified to require a sump pressure of between 100 and 130 psig

prior to securing the backup compressors. The inspector concluded

that the control room operator response to the low header air

pressure was good, and that the procedure enhancement was

appropriate corrective action.

e.

Inadvertent Venting of the Unit 2 Quench Tank

An inadvertent venting of the Unit 2 quench tank occurred on

October 17, 1994, at approximately 3:00 a.m., as indicated on the

air ejector offgas radiation monitor RIA-40. This was

subsequently determined to have resulted from operator activities

that were in progress to fill the shell side of the 2A Steam

Generator (SG). This evolution required the SG shell side vents

be opened to the quench tank. At the same time, the feedwater and

steam side of the steam generators were at 29" of vacuum. RIA-40

stayed in the alarm condition with the counts decreasing for

approximately 50 minutes. The licensee was unaware that the alarm

condition was due to this evolution.

RIA-40 alarmed again at approximately 2:00 p.m., on October 17,

1994, during the filling of the 2B SG from the 2A SG (shell side

vents open to the quench tank). RIA-40 counts were decreasing at

4

3:00 p.m., when valve 2GWD-1 was opened to vent the pressurizer to

the quench tank as required by the procedure for reducing the RCS

inventory. At this time, RIA-40 alarmed again and it was noticed

that the pressure in the pressurizer had reduced, but the pressure

in the quench tank had not increased as expected. As a result,

the Senior Reactor Operator had the shell side vents on SG 2B

closed and the quench tank pressure began to increase. The RIA-40

alarm subsequently cleared. It was determined that when the shell

side SG vents were open to the quench tank, existing gas was being

drawn into the main condenser and to the atmosphere through the

steam jet air ejectors and the Unit 2 vent stack.

The inspectors will review the events that were in progress which

may have contributed to the failure to detect and correct this

condition in a timely manner. This item will be tracked as

Inspector Followup Item (IFI) 270/94-32-01:

Failure to Detect

Inadvertent Quench Tank Venting.

f.

Inoperable Containment Isolation Valve

On October 5, 1994, the licensee torqued the body to bonnet joint

on valve 1RC-7 to 125 percent of its normal torque value due to a

body to bonnet leak. Valve IRC-7 is the outboard pressurizer

sample containment isolation valve. The maintenance activity was

conducted per Work Order 94068251, Task 01.

The work activity was

commenced at approximately 8:30 a.m. and was completed at

approximately 10:37 a.m. Prior to performing the work activity

the operators in the control room asked the maintenance

technicians performing the work if post maintenance testing of the

valve was required. They were assured that testing would not be

required. At approximately 5:00 p.m., on October 5, 1994, a

performance planner requested that valve IRC-7 be stroke tested to

verify operability of the valve following the maintenance

activity. The control room operators declared the valve

inoperable and isolated the containment penetration and

deactivated the valves upstream of valve 1RC-7 until the required

post maintenance testing could be performed. The valve was stroke

tested satisfactorily; however, a question remained as to whether

a leak test was required to return the containment penetration to

an operable status. Subsequent review by the licensee determined

that a local leak rate test was not required based on the work

activity performed on the valve. The valve was declared operable

on October 7, 1994.

The licensee determined that the failure to declare valve 1RC-7

inoperable prior to performing the maintenance activity was a

result of the maintenance planners entering a not applicable (N/A)

statement on the Post Maintenance Testing (PMT) sheet. The work

order identified that a functional test, stroke test, and leak

rate test was required. The planners marked the signoffs on the

PMT sheet not applicable (N/A) because they stated that the

required tests would be documented on separate task sheets;

5

therefore, the N/A(s) were utilized to indicate that no signatures

were required on the PMT sheet. The maintenance technicians

assumed that the N/Aed steps meant that post maintenance testing

was not required.

A Licensee Event Report (LER) will be submitted to the NRC in

accordance with the requirements of 10 CFR 50.73. Also, as a

result of this problem, the licensee instituted the following

corrective actions:

(1) Work orders planned after October 12, 1994, contain a cross

reference statement on the PMT sheet that links the

controlling task to the supporting tasks that will perform

each retest.

(2) Work orders planned prior to October 12, 1994, but not

scheduled, were reviewed and the N/A(s) struck through and a

cross reference inserted.

(3) Maintenance personnel were informed that N/A(s) on the Post

Maintenance Test Sheet does not indicate that the test is

not required.

The failure to declare valve 1RC7 inoperable and perform the

required post maintenance testing is considered a licensee

identified violation.

However,

this violation will not be subject

to enforcement action because the licensee's efforts in

identifying and correcting the violation meet the criteria

specified in Section VII.B of the Enforcement Policy.

Accordingly, it will be identified as Non-cited Violation (NCV)

50-269/94-32-02:

Inoperable Containment Isolation Valve Due to

Maintenance Error.

Within the areas reviewed, one NCV was identified.

3.

Maintenance and Surveillance Testing (62703 and 61726)

a.

Maintenance activities were observed and/or reviewed during the

reporting period to verify that work was performed by qualified

personnel and that approved procedures adequately described work

that was not within the skill of the craft. Activities,

procedures and work orders (WO) were examined to verify that

proper authorization and clearance to begin work was given,

cleanliness was maintained, exposure was controlled, equipment was

properly returned to service, and limiting conditions for

operation were met.

The following maintenance activities were observed or reviewed in

whole or in part:

(1) Integrated Control System Feedwater Control, B Loop,

IP/0/B/0325/002

6

On October 13, 1994, the inspectors witnessed a calibration

that was in progress on the Unit 2 feedwater main and

startup valve control system. Problems were experienced in

that the control module did not duplicate the bench

calibration after it was reinstalled in the panel.

As a

result, the module was replaced with a new module.

Performance of the activity was in accordance with the

procedure and the effort was determined to be acceptable.

(2) Install and Reconnect 2LPSW-15, Work Order 94082562, Task 05

On October 29, 1994, the inspectors observed portions of the

work activities associated with the reinstallation of Low

Pressure Service Water valve 2LPSW-15. The inspectors

reviewed the work order for adequacy and observed the

completion of the work activity. No deficiencies were

noted.

(3) Engineered Safeguards System Analog Channel B Reactor

Coolant Pressure Channel Calibration, IP/O/A/0310B/004B

The licensee received a Unit 2 Engineered Safeguards (ES)

actuation on October 21, 1994 during the performance of

procedure IP/0/A/0310/004B.

While calibration of channel B

was in progress, channel A was inadvertently placed in the

"range" position as opposed to channel B as required by step

10.7.3.a of the procedure. (Note: The procedure referred to

the switches as A and B and the panel was labeled as

channels 1 and 2).

As a result of the event the licensee

generated Problem Investigation Report 2-094-1493, which

required an evaluation and corrective actions.

Having the two analog channels in a test status

simultaneously resulted in the ES Actuation. The major

events resulting from the actuation were:

-

Emergency start of .Keowee Units 1 and 2

-

The containment purge tripped due to purge valves PR-2

through PR-5 going shut

-

Low pressure service water pumps B and C started

Other ES devices actuated, but the equipment was out of

service as a result of the refueling outage and the

components did not start or realign.

The failure to place the proper switch to the required

position as specified by the procedure is identified as

Example 1 of Violation 270/94-32-03:

Failure To Follow

Procedures.

7

(4) AC Watt Transducer, Two Element, IP/O/A/3955/01

On October 26, 1994, switchgear 2TE experienced an

inadvertent undervoltage trip condition as a result of

testing errors during testing of transducer 2ET42. The

maintenance technicians failed to remove the test leads

attached to the terminal block prior to reclosing the link

and repowering the circuitry that had been taken out of

service for the test. As a result, the test leads made a

path to ground through the test equipment and resulted in

blowing a fuse in the 2TE switchgear when the circuit was

repowered. Step 10.7.17 of IP/O/A/3955/01 removes the test

equipment prior to restoring the plant equipment to service.

Although no signoff was required procedurally for performing

this step, the requirements for performing the activity were

explicit..."Remove test equipment."

Failure to comply with

the requirements of the procedure is identified as Example 2

of Violation 270/94-32-03: Failure To Follow Procedures.

(5) 2DIA Static Inverter Replacement, TN/2/A/288 1/0/AL1

On October 17, 1994, the inspectors observed the

installation of the power cables, ground cable, and alarm

circuitry wiring on the new 2DIA Static Inverter. The

inspectors verified that the work was conducted under an

approved procedure and that the as-left wiring was

consistent with design drawings.

All activities observed

were satisfactory.

(6) Investigate Slow Stroke Time for 3BS-1, Work Order 94079209,

Task 01

On October 16, 1994, motor operated valve 3BS-1 failed to

satisfy performance stroke testing requirements. 3BS-1 is

the 3A reactor building spray pump's discharge isolation

valve, and is given an automatic open signal as part of an

Engineered Safeguard (ES) actuation. The performance test

measured an open stroke time of 14 seconds, as measured on a

stopwatch. The acceptance criteria per PT/3/A/0150/22A was

9 to 13 seconds. The acceptance criteria was based on a

baseline value of 11 seconds. The Final Safety Analysis

Report (FSAR) indicates that this valve is assumed to open

within 15 seconds. The licensee initially declared 3BS-1

inoperable and entered the seven day LCO for an inoperable.

train of building spray. The licensee performed electrical

and mechanical preventive maintenance on the valve operator,

including cleaning contacts and stem lubrication. Multiple

stroke tests were subsequently performed utilizing a Motor

Power Monitor (MPM) to precisely measure the stoke time. A

total of five MPM tests were performed and the stroke time

was consistently 13.5 plus or minus 0.1%. Based on this,

the licensee concluded that the valve was not currently

8

degrading and would meet the 15 second FSAR limit.

Consequently, the LCO was exited. The licensee believed

that maintenance performed during January 1994, which

included limit switch adjustment, may have altered the

baseline for this valve and that this would account for the

slower stroke time. The licensee indicated that they would

perform weekly stroke tests to confirm that the valve was

not degrading. The inspectors observed various portions of

the licensee's troubleshooting efforts including two of the

MPM stroke tests. The inspectors concluded that the

licensee's actions were acceptable.

b.

Surveillance activities were conducted with approved procedures

and in accordance with site directives. The inspectors reviewed

surveillance performance, as well as system alignments and

restorations. The inspector assessed the licensee's disposition

of discrepancies which were identified during the surveillance,

The following surveillance activities were observed or reviewed in

whole or in part:

(1) Control Rod Movement, PT/O/A/600/15

The inspectors witnessed performance of Unit 1 Control Rod

Drive (CRD) movement on October 6, 1994. The purpose of the

procedure was to test CRD operation under actual operating

conditions by moving each rod group a minimum of 2.5 percent

of full travel.

This test met the monthly surveillance

requirements as specified in Technical Specification 4.1.2.

The operators performed the rod movements per the procedure

and were cognizant of plant operating status during the

test. The activity was determined to be performed to

acceptable standards.

(2) Reactor Building Spray Pump Test, PT/1//A/0204/07

Portions of the reactor building spray pump test were

witnessed by the inspectors on September 27, 1994. The

quarterly test was necessary to satisfy TS 3.3.2, 3.3.6,

4.0.4. and 4.5.2, as well as Subsections IWP and IWV of

Section XI to the ASME Code. The performance test

demonstrates operability of the system. During testing of

the 1B Pump, high vibration was detected and determined to

be in the alert range. The pump was determined to be

operable, but the testing frequency was changed and the test

will be performed at 2 times the normal frequency.

As each pump was taken out of service, the appropriate

Limiting Condition for Operation was' entered as required per

step 6.1 of the test procedure. The conduct of testing was

viewed by the inspectors as a strength.

9

(3) Control Room Pressurization Test, PT/1&2/A/0170/03

The inspectors observed portions of this performance test

conducted on October 26, 1994. This test implements the

surveillance requirements .of Technical Specification 4.12.1.

The inspectors verified that the procedural acceptance

criteria was met.

(4) Unit 2 Main Feeder Bus 2 Lockout Test, TT/2/A/610/14

The inspectors observed portions of this temporary test

procedure conducted on October 26, 1994. This test

procedure verified that the Unit 2 Main Feeder Bus 2 lockout

relays operated properly. This test had not been performed

on Unit 2 prior to its performance on October 26, 1994.

During performance of the test, the startup breaker (E2)

failed to trip open when the 86B2 lockout relay was

actuated. Investigation by the licensee determined that

physical interference with the wiring connected to the

contact terminal prevented the actuation contact from

closing. The wiring interference was corrected and the test

was completed without further problems.

The licensee visually inspected the Unit 3 lockouts to

verify that adequate clearance existed between the terminal

lugs and the moving contacts. The Unit

1

main feeder bus

lockout relays had been tested during the previous Unit 1

refueling outage without incident. In spite of the

identified problem, the licensee determined that the Unit 2

Main Feeder Bus had been operable based on the fact that the

startup breaker's redundant trip coil had been operable and

would have operated to open the breaker if an actual fault

had occurred on the Main Feeder Bus.

(5) Unit 2 Control Rod Drive Drop Test, IP/0/A/330/03A

Drop time testing of the Unit 2 control rods was performed

on October 6, 1994.

The unit was shutdown for refueling

outage EOC14 with the reactor coolant system at 532 degrees

F and all 4 reactor coolant pumps running. Results of the

test showed that rod #3 in group #1 dropped at 1.803

seconds, which was slower than the TS limit of 1.66 seconds.

As a result, a second rod drop test was performed and the

same rod (rod #3) dropped at 1.758 seconds. Results of the

second test also showed a second rod, rod #4 in group #1, to

have increased in drop time to greater than the TS limit.

Rod #4 dropped at 1.662 seconds and was the only rod which

increased in drop time from the first to the second test.

A summary of the test results indicated that the drop times

for an additional 8 rods were slow enough (i.e., greater

than 1.40 seconds) to generate doubt that they may not meet

10

TS requirements after operating for another fuel cycle

(approximately 18 months).

One of these rods, rod #1 in

group #1, which dropped at 1.417 seconds during the first

test and at 1.328 seconds during the second test, was

evaluated by the licensee and determined not to be a problem

during the next fuel cycle. Past operating history of the

rod was reviewed and was considered as part of the

operability evaluation.

The slow rod drop times were determined to be a result of

erosion material build-up in the area of the ball checks in

the thermal barrier cooler. The ball checks are required to

raise off their seat to allow RCS coolant flow to enter and

replace the void created in the housing when the rods fall

into the core.

As a result, the thermal barrier coolers were replaced in 8

of the drive shaft housing assemblies with a modified cooler

(modified type A) that increased clearances in the area of

the ball check valves. The 9th assembly was replaced with a

spare rod drive shaft housing assembly that had been cleaned

and restored to the original clearances.

A statistical analysis was done on the Unit 1 control rods.

The analysis indicated that continued operation of Unit 1

would not result in rod drop times greater than Technical

Specification allowable values. However, the licensee

indicated that the operability of the Unit I rods would be

reassessed in April 1995.

The thermal barriers in the Unit 3 CRD shaft housing

assemblies are type C. There have been no reported

problems with CRD drop times associated with ball checks in

the type C thermal barrier coolers.

(6) Turbine Driven Emergency Feedwater Pump Test, PT/1/A/0600/12

On September 26, 1994, the inspectors witnessed performance

testing of the Unit 1 turbine driven emergency feedwater

pump. The test was required to be performed quarterly as

specified per TS to satisfy the American Society of

Mechanical Engineers (ASME),Section XI requirements. The

applicable sections of the TS which relate to pump

operability and stroke testing of valves were 3.4, 4.0.4,

and 4.9.

Personnel performing the test were knowledgeable of the

operation of the equipment and their performance was

determined to be very good.

11

(7) Operation of the SSF Diesel Generator, OP/0/A/1600/10

On October 3, 1994, the inspectors witnessed post

maintenance testing of the Safe Shutdown Facility (SSF)

Diesel Generator. The inspectors noted that step 2.15 of

the test procedure required that the Diesel Engine Log Book

be referenced to determine if the diesel had been operated

less than 700 KW for greater than 2 accumulated hours, in

order to determine if the engine needed to be "desouped" (a

procedure that involves burning out deposits in the exhaust

manifold). The inspectors reviewed the Diesel Engine Log

Book and noted that the information included was inadequate

to determine the exact amount of time the engine had been

operated at less than 700 KW. The licensee agreed that the

Diesel Engine Log Book did not contain sufficient detail to

comply with step 2.15, but stated that they had been

informed by the diesel manufacturer some time ago that the

desouping procedure was not necessary. However, they had

neglected to remove this step from the procedure. The

inspector concluded that this represented a weakness in the

licensee's procedure. The licensee indicated that step 2.15

would be deleted. All other aspects of the procedure were

satisfactory and the diesel and its support equipment met

all acceptance criteria.

(8) -Low Pressure Injection Pump Test, PT/3/A/0203/06A

On October 4, 1994, the inspectors witnessed the performance

of the quarterly operability test of the 3A Low Pressure

Injection (LPI) Pump. The indicated developed head for the

pump was 186 psid, according to instrument 3PG-21. This

exceeded the acceptance criteria of 158.5-181.5 and would

have placed the pump in the alert range. However, the

difference between the indicated pressure on the suction and

discharge gages was 174 psid. Therefore, the licensee

concluded that instrument 3PG-21 was out of calibration and

the developed head of the pump was within the acceptance

criteria. The inspectors agreed with the licensee's

conclusion and determined that all activities observed.were

satisfactory. The licensee plans to recalibrate 3PG-21

prior to the next performance of the procedure.

(9) Turbine Stop Valve Movement Test, PT/O/A/290/04

The inspectors witnessed the monthly test of the Unit 3 main

steam stop valves as required by TS 4.1.

This test closed

each valve approximately 10% in order to verify valve

movement locally and via the control room meter. All

activities observed were satisfactory.

Within the areas reviewed, one violation with two examples was

identified.

12

4.

Onsite Engineering (37551)

During the inspection period, the inspectors assessed the effectiveness

of the onsite design and engineering processes by reviewing engineering

evaluations, operability determinations, modification packages and other

areas involving the Engineering Department.

a.

Turbine Bypass Isolation Test, TT/2/B/0251/46

The inspectors witnessed testing activities to evaluate leakage

through the Unit 2 turbine bypass valves. The test was performed

in accordance with test procedure TT/2/B/0251/46, Turbine Bypass

Isolation Test. The test consisted of evaluating plant MWe output

and condenser vacuum during closure and reopening of the block

valves to each of the bypass valves. The test data was taken via

the operator aid computer and was utilized to determine the need

for bypass valve maintenance or replacement during the Unit 2

refueling outage.

Performance of the testing activities was considered to be

acceptable.

b.

10CFR Part 21 Review

The inspectors reviewed a 10CFR Part 21 .issue, identified by

Dresser-Rand dated August 5, 1994, that related to a deficiency

with the Gimple trip throttle valve on the turbine driven

auxiliary feedwater pump at Davis-Besse Unit 1. The reported

deficiency was that the coupling set screw on the trip throttle

valve had not engaged the valve stem and therefore, the stem

travel was impaired.

The Duke Power General Office reviewed the subject report and

determined that Gimple valves were utilized at their Catawba and

McGuire Nuclear Stations. As a result, problem identification

report (0-G94-0365) was issued to initiate preventative measures

at those sites. However, the licensee determined that Gimple

valves did not exist at the Oconee Nuclear Station and no

corrective actions were necessary.

The inspector verified that General Electric turbines were

installed at the Oconee Nuclear Station and that Gimple valves

were not utilized.

No violations or deviations were identified.

5.

Plant Support (71750)

The inspectors assessed selected activities of licensee programs to

ensure conformance with facility policies and regulatory requirements.

During the inspection period, the following areas were reviewed:

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radiological controls; radiological effluent, waste treatment, and

environmental monitoring; physical security, and fire protection.

a.

Radiation Protection

During a tour of the turbine building on October 11, 1994, the

inspectors noticed maintenance personnel crossing the

yellow/magenta ropes set up to identify a radiation controlled

zone (RCZ) at main steam reheater 2B2. When the maintenance

personnel were questioned, they informed the inspectors that

health physics (HP) personnel had informed them that it was not

necessary to comply with the rules established for an RCZ since no

radiation hazard existed until the manways were removed from the

heater.

The area HP was summoned to the area and it was verified that the

maintenance personnel had been told that the yellow/magenta ropes

were to be ignored until the manways were removed. The HP

informed the inspectors that the RCZ was set up in advance to get

a "head start" on the outage effort.

The licensee's directive, Radiation Protection, Directive No. III

3, Posting of Radiation Control Zones, requires that an RCZ be

identified with a yellow/magenta rope with placards attached

indicating the requirements for entering the zone. Although the

placards had not been installed, the inspectors determined that

allowing personnel to cross back and forth across the

yellow/magenta ropes was a poor practice and a weakness in the

Health Physics Program. The inspectors had identified this poor

practice during a previous refueling outage. At that time, the

licensee agreed to caution workers to treat all RCZ ropes as

boundaries at all times.

After bringing this latest observation to the attention of

licensee management, the inspectors were assured that the practice

would be corrected. The inspectors observed various RCZs

throughout the remainder of the reporting period and did not

identify any instances where the yellow/magenta ropes were being

ignored.

No violations or deviations were identified.

6.

Exit Interview

The inspection scope and findings were summarized on November 2, 1994,

with those persons indicated in paragraph 1 above. The inspectors

described the areas inspected and discussed in detail the inspection

findings addressed in the summary and listed below. The licensee did

not identify as proprietary any of the material provided to or reviewed

by the inspectors during this inspection.

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Item Number

Description/Reference Paragraph

50-270/94-32-01

IFI:

Failure to Detect Inadvertent Quench

Tank Venting (paragraph 2.e).

50-269/94-32-02

NCV:

Inoperable Containment Isolation

Valve Due to Maintenance Error (paragraph

2.f).

50-270/94-32-03

VIO:

Failure to Follow Procedures - Two

Examples (paragraph 3.a).

(III