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MONTHYEARML13304B4452013-10-28028 October 2013 Revised License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Project stage: Request ML13351A3432013-12-19019 December 2013 Acceptance of Requested Licensing Action License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Project stage: Acceptance Review ML14127A4622014-05-12012 May 2014 Request for Additional Information Regarding License Amendment Request to Modify Specification 3.8.4 Setpoint Project stage: RAI MNS-14-045, Responses to Request for Additional Information Related to License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Dated October 28, 20132014-06-0303 June 2014 Responses to Request for Additional Information Related to License Amendment Request for One-Time Change to Technical Specification 3.8.4, DC Sources-Operating for Battery Replacement Dated October 28, 2013 Project stage: Response to RAI ML14178B2322014-07-14014 July 2014 Request for Additional Information Regarding License Amendment Request to Modify Technical Specification 3.3.2 Setpoint Project stage: RAI ML14231A6342014-09-10010 September 2014 Issuance of Amendments Regarding Technical Specification 3.8.4, DC Sources-Operating, Project stage: Approval ML15202A6612015-07-27027 July 2015 Acceptance Review of License Amendment Request Temporary Changes to Technical Specifications for Correction of Nuclear Service Water System Degraded Condition Project stage: Acceptance Review ML15196A3862015-08-0404 August 2015 Notice of Consideration of Issuance of Amendment to Facility Operating License, Proposed No Significant Hazards Consideration Determination, and Opportunity for a Hearing and Order Imposing Procedures for Document Access To.. Project stage: Other MNS-15-062, Response to Request for Additional Information Regarding License Amendment Request (LAR) for Temporary Changes to Technical Specifications for Correction of an 'A' Train Nuclear Service Water System (Nsws) Degraded Condition2015-08-11011 August 2015 Response to Request for Additional Information Regarding License Amendment Request (LAR) for Temporary Changes to Technical Specifications for Correction of an 'A' Train Nuclear Service Water System (Nsws) Degraded Condition Project stage: Response to RAI ML15196A6162015-08-13013 August 2015 Duke Energy Carolinas, LLC, McGuire Nuclear Station, Units 1 and 2 - License Amendment Application; Opportunity to Comment, Request a Hearing, and Petition for Leave to Intervene; Order Project stage: Other ML15243A4082015-08-28028 August 2015 NRR E-mail Capture - Draft RAI for Nsws Temp AOT Extension Project stage: Draft RAI ML15252A2762015-09-14014 September 2015 Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension Project stage: RAI MNS-15-073, Response to NRC Letter Dated August 27, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension2015-09-24024 September 2015 Response to NRC Letter Dated August 27, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension Project stage: Request MNS-15-078, Response to NRC Letter Dated September 14, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension2015-10-0808 October 2015 Response to NRC Letter Dated September 14, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension Project stage: Request ML15289A5552015-10-26026 October 2015 Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension Project stage: RAI ML15343A0122015-12-0707 December 2015 Response to NRC Letter Dated 10/26/2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension. Project stage: Request MNS-16-005, Response to Request for Additional Information (RAI) During January 12, 2016, NRC Teleconference Pertaining to License Amendment Request for Nuclear Service Water System Allowed Outage Time Extension2016-02-10010 February 2016 Response to Request for Additional Information (RAI) During January 12, 2016, NRC Teleconference Pertaining to License Amendment Request for Nuclear Service Water System Allowed Outage Time Extension Project stage: Response to RAI 2015-12-07
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Category:Letter type:MNS
MONTHYEARMNS-18-044, Independent Spent Fuel Storage Installation (Isfsi), Submittal of 10 CFR 72.48 Summary Report from September 15, 2016 to July 26, 2018, No Changes, Tests, or Experiments2018-07-26026 July 2018 Independent Spent Fuel Storage Installation (Isfsi), Submittal of 10 CFR 72.48 Summary Report from September 15, 2016 to July 26, 2018, No Changes, Tests, or Experiments MNS-18-036, Redacted Response to the Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado Generated Missiles2018-07-0303 July 2018 Redacted Response to the Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado Generated Missiles MNS-18-042, Independent Spent Fuel Storage Installation (ISFSI)2018-06-28028 June 2018 Independent Spent Fuel Storage Installation (ISFSI) MNS-18-040, Submittal of Information Related to Pressurizer Surge and Spray Nozzle Thermal Sleeves Attachment Welds for License Renewal2018-06-26026 June 2018 Submittal of Information Related to Pressurizer Surge and Spray Nozzle Thermal Sleeves Attachment Welds for License Renewal MNS-18-039, Independent Spent Fuel Storage Installation (ISFSI)2018-06-19019 June 2018 Independent Spent Fuel Storage Installation (ISFSI) MNS-18-001, Application to Revise Technical Specifications to Adopt TSTF-234-A Revision 1, Add Action for More than One Dpri Inoperable2018-05-31031 May 2018 Application to Revise Technical Specifications to Adopt TSTF-234-A Revision 1, Add Action for More than One Dpri Inoperable MNS-18-030, 2017 Annual Radiological Environmental Operating Report2018-05-15015 May 2018 2017 Annual Radiological Environmental Operating Report MNS-18-029, Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-A2018-05-0909 May 2018 Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-A MNS-18-029, McGuire Nuclear Station, Units 1 and 2 - Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-2018-05-0909 May 2018 McGuire Nuclear Station, Units 1 and 2 - Resolution of Commitments Related to Review Request for the Aging Management Program and Inspection Plan for the McGuire Nuclear Station Units 1 and 2 Reactor Vessel Internals to Implement MRP-227-A MNS-18-028, Annual Radioactive Effluent Release Report2018-04-25025 April 2018 Annual Radioactive Effluent Release Report MNS-18-017, Non-Voluntary License Amendment Request (LAR) to Correct Non-Conservative Technical Specification 3.4.11 - PORVs2018-02-26026 February 2018 Non-Voluntary License Amendment Request (LAR) to Correct Non-Conservative Technical Specification 3.4.11 - PORVs MNS-18-018, McGuire, Units 1 & 2, Submittal of Emergency Plan Implementing Procedure Changes2018-02-22022 February 2018 McGuire, Units 1 & 2, Submittal of Emergency Plan Implementing Procedure Changes MNS-18-009, McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 18-12018-01-31031 January 2018 McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 18-1 MNS-18-003, End of Cycle 25 In-service and Steam Generator In-service Inspection Summary Reports2018-01-11011 January 2018 End of Cycle 25 In-service and Steam Generator In-service Inspection Summary Reports MNS-17-050, Review Request for the Aging Management Program and Inspection Plan for the Reactor Vessel Internals to Implement MRP-227-A2017-12-13013 December 2017 Review Request for the Aging Management Program and Inspection Plan for the Reactor Vessel Internals to Implement MRP-227-A MNS-17-048, Response to Request for Additional Information License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies2017-12-12012 December 2017 Response to Request for Additional Information License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies MNS-17-026, Submittal of License Amendment Request Proposing to Revise the Bases for Protection from Tornado-Generated Missiles2017-12-0808 December 2017 Submittal of License Amendment Request Proposing to Revise the Bases for Protection from Tornado-Generated Missiles MNS-17-042, McGuire Nuclear Station, Unit 1, Submittal of Cycle 26, Revision 0, Core Operating Limits Report2017-10-0909 October 2017 McGuire Nuclear Station, Unit 1, Submittal of Cycle 26, Revision 0, Core Operating Limits Report MNS-17-040, (Mns), Units 1 and 2 - Supplement to the High Frequency Supplement to Seismic Hazard Screening Report, Response NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force ..2017-09-27027 September 2017 (Mns), Units 1 and 2 - Supplement to the High Frequency Supplement to Seismic Hazard Screening Report, Response NRC Request for Information Pursuant to 10 CFR 50.54(f) Regarding Recommendation 2.1 of the Near-Term Task Force .. MNS-17-038, Startup Ascension Summary Report Measurement Uncertainty Recapture Power Uprate2017-09-25025 September 2017 Startup Ascension Summary Report Measurement Uncertainty Recapture Power Uprate MNS-17-039, McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 17-12017-09-19019 September 2017 McGuire Nuclear Station, Units 1 and 2, Submittal of Emergency Plan, Revision 17-1 MNS-17-031, License Amendment Request for Temporary Changes to Technical Specifications to Address an 'A' Train Nuclear Service Water System (Nsws) Non-Conforming Condition2017-09-14014 September 2017 License Amendment Request for Temporary Changes to Technical Specifications to Address an 'A' Train Nuclear Service Water System (Nsws) Non-Conforming Condition MNS-17-037, Submittal of Summary Report of Evaluations Performed Pursuant to 10 CFR 50.59 Changes, Tests, and Experiments During the Period from January 1, 2016 to March 31, 20172017-08-10010 August 2017 Submittal of Summary Report of Evaluations Performed Pursuant to 10 CFR 50.59 Changes, Tests, and Experiments During the Period from January 1, 2016 to March 31, 2017 MNS-17-033, Snubber Program Plan for the Fourth Ten-Year Lnservice Testing (IST) Interval2017-08-0202 August 2017 Snubber Program Plan for the Fourth Ten-Year Lnservice Testing (IST) Interval MNS-17-034, 16C4435-RPT-002, Rev. 1, 50.54(f) NTTF 2.1 Seismic High Frequency Confirmation for McGuire Nuclear Station.2017-07-24024 July 2017 16C4435-RPT-002, Rev. 1, 50.54(f) NTTF 2.1 Seismic High Frequency Confirmation for McGuire Nuclear Station. MNS-17-030, Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal2017-06-28028 June 2017 Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal MNS-17-023, Response to Request for Additional Information to License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies2017-05-25025 May 2017 Response to Request for Additional Information to License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies MNS-17-016, Nuclear Regulatory Commission (NRC) Annual Commitment Change Report2017-05-18018 May 2017 Nuclear Regulatory Commission (NRC) Annual Commitment Change Report MNS-17-020, Transmittal of McGuire, Units 1 and 2, 2016 Annual Radiological Environmental Operating Report2017-05-0505 May 2017 Transmittal of McGuire, Units 1 and 2, 2016 Annual Radiological Environmental Operating Report MNS-17-019, McGuire Nuclear Station, Units 1 and 2 - Submittal of Annual Radioactive Effluent Release Report2017-04-28028 April 2017 McGuire Nuclear Station, Units 1 and 2 - Submittal of Annual Radioactive Effluent Release Report MNS-17-008, Letter of Intent to Submit Plant-Specific Reactor Vessel Internals Inspection Plans2017-02-23023 February 2017 Letter of Intent to Submit Plant-Specific Reactor Vessel Internals Inspection Plans MNS-16-092, License Amendment Request to Revise Technical Specifications Section 5.5.2, Containment Leakage Rate Testing Program for Permanent Extension of Type a and Type C Leak Rate Test Frequencies2016-12-19019 December 2016 License Amendment Request to Revise Technical Specifications Section 5.5.2, Containment Leakage Rate Testing Program for Permanent Extension of Type a and Type C Leak Rate Test Frequencies MNS-16-091, License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity.2016-12-0808 December 2016 License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity. MNS-16-086, Emergency Plan, Revision 16-42016-12-0707 December 2016 Emergency Plan, Revision 16-4 MNS-16-078, Written Notification Joslyn Clark Overload Heater Element Part No. 24552016-10-19019 October 2016 Written Notification Joslyn Clark Overload Heater Element Part No. 2455 MNS-16-077, Responding to Request for Additional Information Related to License Amendment Request to Implement a Risk-informed Performance-Based Fire Protection Program2016-09-29029 September 2016 Responding to Request for Additional Information Related to License Amendment Request to Implement a Risk-informed Performance-Based Fire Protection Program MNS-16-070, Response to Request for Additional Information to Relief Request 16-MN-0032016-08-18018 August 2016 Response to Request for Additional Information to Relief Request 16-MN-003 MNS-16-060, Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2016-08-18018 August 2016 Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident MNS-16-062, Relief Request 16-MN-003 Alternative to Defect Removal Prior to Performing Temporary Repair Activities on Three-Inch-Diameter Nuclear Service Water System Piping2016-08-10010 August 2016 Relief Request 16-MN-003 Alternative to Defect Removal Prior to Performing Temporary Repair Activities on Three-Inch-Diameter Nuclear Service Water System Piping MNS-16-046, License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity2016-06-30030 June 2016 License Amendment Request for Technical Specification 3.6.14, Divider Barrier Integrity MNS-16-056, License Amendment Request, One-Time Extension of Appendix J Type a Integrated Leakage Rate Test Interval, Response to Request for Additional Information2016-06-30030 June 2016 License Amendment Request, One-Time Extension of Appendix J Type a Integrated Leakage Rate Test Interval, Response to Request for Additional Information MNS-16-053, Relief Request 16-MN-002, Alternative to Defect Removal Prior to Performing Repair Activities on Nuclear Service Water System Piping2016-06-23023 June 2016 Relief Request 16-MN-002, Alternative to Defect Removal Prior to Performing Repair Activities on Nuclear Service Water System Piping MNS-16-052, Supplement to License Amendment Request for the Removal of Superseded Technical Specification Requirements, Dated May 5, 2016, TAC Nos. MF7682 and MF76832016-06-16016 June 2016 Supplement to License Amendment Request for the Removal of Superseded Technical Specification Requirements, Dated May 5, 2016, TAC Nos. MF7682 and MF7683 MNS-16-042, Withdrawal of Relief Request Serial No. 15-MN-0022016-05-17017 May 2016 Withdrawal of Relief Request Serial No. 15-MN-002 MNS-16-020, License Amendment Request Removal of Superseded Technical Specification Requirements2016-05-0505 May 2016 License Amendment Request Removal of Superseded Technical Specification Requirements MNS-16-041, Supplement to Final Notification of Full Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design Basis External Events and with Order EA-12-051..2016-05-0505 May 2016 Supplement to Final Notification of Full Compliance with Order EA-12-049, Order Modifying Licenses with Regard to Requirements for Mitigation Strategies for Beyond Design Basis External Events and with Order EA-12-051.. MNS-16-036, Relief Request 16-MN-001, Limited Weld Examinations2016-04-28028 April 2016 Relief Request 16-MN-001, Limited Weld Examinations MNS-16-039, Submittal Revising Attachment s of License Amendment Request to Implement a Risk-Informed Performance-Based Fire Protection Program2016-04-26026 April 2016 Submittal Revising Attachment s of License Amendment Request to Implement a Risk-Informed Performance-Based Fire Protection Program MNS-16-026, Transmittal of Updated Final Safety Analysis Report, Revision 192016-04-0505 April 2016 Transmittal of Updated Final Safety Analysis Report, Revision 19 MNS-15-068, License Amendment Request to Technical Specification (TS) 3.6.13, Ice Condenser Doors.2016-03-24024 March 2016 License Amendment Request to Technical Specification (TS) 3.6.13, Ice Condenser Doors. 2018-07-03
[Table view] Category:Response to Request for Additional Information (RAI)
MONTHYEARRA-23-0154, Duke Energy - Response to Request for Additional Information Regarding Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1)2023-07-20020 July 2023 Duke Energy - Response to Request for Additional Information Regarding Proposed Alternative for Pressurizer Welds in Accordance with 10 CFR 50.55a(z)(1) RA-23-0136, Duke Energy Response to Request for Additional Information Regarding Proposed Alternative for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1)2023-07-20020 July 2023 Duke Energy Response to Request for Additional Information Regarding Proposed Alternative for Steam Generator Welds in Accordance with 10 CFR 50.55a(z)(1) RA-23-0142, Mcguire, Units 1 and 2, Oconee, Units 1, 2, and 3, H. B. Robinson, Unit 2, Response to Request for Additional Information Regarding the License Amendment Request to Revise Restrictive Technical Specification Surveillance Require2023-07-0707 July 2023 Mcguire, Units 1 and 2, Oconee, Units 1, 2, and 3, H. B. Robinson, Unit 2, Response to Request for Additional Information Regarding the License Amendment Request to Revise Restrictive Technical Specification Surveillance Require RA-23-0076, Supplement to Response to Request for Additional Information (RAI) Regarding McGuire Nuclear Station Unit 1 Spring, 2022 Outage Steam Generator Tube Inspection Report2023-03-16016 March 2023 Supplement to Response to Request for Additional Information (RAI) Regarding McGuire Nuclear Station Unit 1 Spring, 2022 Outage Steam Generator Tube Inspection Report RA-23-0024, Response to Request for Additional Information (RAI) for Relief Request for RPV Reactor Coolant System Welds2023-02-28028 February 2023 Response to Request for Additional Information (RAI) for Relief Request for RPV Reactor Coolant System Welds RA-23-0025, End of Cycle 28 (M1R28) Steam Generator Tube Inspection Report Response to Request for Additional Information (RAI)2023-02-15015 February 2023 End of Cycle 28 (M1R28) Steam Generator Tube Inspection Report Response to Request for Additional Information (RAI) RA-22-0147, Duke Energy Carolinas, LLC, and Duke Energy Progress, LLC, Response to Request for Additional Information (RAI) Regarding License Amendment Request for Relocating the Duke Energy Emergency Operations Facility2022-05-13013 May 2022 Duke Energy Carolinas, LLC, and Duke Energy Progress, LLC, Response to Request for Additional Information (RAI) Regarding License Amendment Request for Relocating the Duke Energy Emergency Operations Facility RA-22-0102, Response to Request for Additional Information (RAI) Regarding Revision 1 of DPC-NE-1007-P, Conditional Exemption of the EOC Mtc Measurement Methodology2022-04-0707 April 2022 Response to Request for Additional Information (RAI) Regarding Revision 1 of DPC-NE-1007-P, Conditional Exemption of the EOC Mtc Measurement Methodology RA-22-0003, Response to Requests for Additional Information for Reactor Vessel Closure Stud Exam Extension Alternative2022-01-31031 January 2022 Response to Requests for Additional Information for Reactor Vessel Closure Stud Exam Extension Alternative RA-21-0259, Response to Request for Additional Information for Request to Use Provisions of a Later Edition and Addenda of the ASME Boiler and Pressure Vessel Code, Section XI for Repair/ Replacement Activities in Accordance with 10 CFR 50.55a(g)(42021-10-0404 October 2021 Response to Request for Additional Information for Request to Use Provisions of a Later Edition and Addenda of the ASME Boiler and Pressure Vessel Code, Section XI for Repair/ Replacement Activities in Accordance with 10 CFR 50.55a(g)(4 RA-21-0063, 1, 2; Catawba Nuclear Station 1, 2; H. B. Robinson Steam Electric Plant 2; Mcgguire Nuclear Station 1, 2; Oconee Nuclear Station 1, 2, 3; Shearon Harris Nuclear Power Plant 1 - Response to RAI Re Amend for Emergency Plan2021-03-11011 March 2021 1, 2; Catawba Nuclear Station 1, 2; H. B. Robinson Steam Electric Plant 2; Mcgguire Nuclear Station 1, 2; Oconee Nuclear Station 1, 2, 3; Shearon Harris Nuclear Power Plant 1 - Response to RAI Re Amend for Emergency Plan RA-21-0032, Duke Energy - Response to Requests for Additional Info for Request to Use a Provision of Later Edition & Addenda of the ASME Boiler & Pressure Vessel Code, Section XI for Repair/Replacement Activities in Accordance with 10 CFR 50.55a(g)(42021-02-11011 February 2021 Duke Energy - Response to Requests for Additional Info for Request to Use a Provision of Later Edition & Addenda of the ASME Boiler & Pressure Vessel Code, Section XI for Repair/Replacement Activities in Accordance with 10 CFR 50.55a(g)(4)( RA-21-0017, Response to Request for Additional Information Re License Amendment Request to Revise Tech Spec 3.8.1 to Reduce Emergency Diesel Generator Maximum Steady State Voltage2021-01-29029 January 2021 Response to Request for Additional Information Re License Amendment Request to Revise Tech Spec 3.8.1 to Reduce Emergency Diesel Generator Maximum Steady State Voltage RA-20-0087, Response to Request for Additional Information Regarding Request for Alternative in Accordance with 10CFR 50.55a(z)(1) to Delay the Update of the ASME Code of Record for the First Inspection Period2020-04-0202 April 2020 Response to Request for Additional Information Regarding Request for Alternative in Accordance with 10CFR 50.55a(z)(1) to Delay the Update of the ASME Code of Record for the First Inspection Period RA-19-0189, Supplement to Response for Request for Additional Information Regarding License Amendment Request Proposing Changes to the Technical Specifications 3.8.12019-04-0808 April 2019 Supplement to Response for Request for Additional Information Regarding License Amendment Request Proposing Changes to the Technical Specifications 3.8.1 RA-19-0004, Response to NRC for Additional Information (RAI) Regarding License Amendment Request Proposing Changes to the Technical Specifications 3.8.1 for Catawba Nuclear Station, Units 1 and 22019-03-0707 March 2019 Response to NRC for Additional Information (RAI) Regarding License Amendment Request Proposing Changes to the Technical Specifications 3.8.1 for Catawba Nuclear Station, Units 1 and 2 RA-19-0026, Response to Request for Additional Information (RAI) Regarding Proposed Alternative to the Depth Sizing Qualification Requirement of Appendix Viii, Supplements 2 and 10 (18-GO-001)2019-02-11011 February 2019 Response to Request for Additional Information (RAI) Regarding Proposed Alternative to the Depth Sizing Qualification Requirement of Appendix Viii, Supplements 2 and 10 (18-GO-001) RA-19-0005, Response to NRC Request for Additional Information Regarding Review Request of the Aging Management Program and Inspection Plan for the Reactor Vessel Internals to Implement MRP-227-A2019-01-30030 January 2019 Response to NRC Request for Additional Information Regarding Review Request of the Aging Management Program and Inspection Plan for the Reactor Vessel Internals to Implement MRP-227-A RA-18-0229, Response to NRC Request for Additional Information Regarding License Amendment Request Proposing Changes to the Technical Specification 3.8.12018-12-0303 December 2018 Response to NRC Request for Additional Information Regarding License Amendment Request Proposing Changes to the Technical Specification 3.8.1 RA-18-0213, Response to the Second Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado-Generated Missiles2018-11-0101 November 2018 Response to the Second Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado-Generated Missiles ML18191A5642018-07-10010 July 2018 Attachment 3 - Response to NRC Request for Additional Information MNS-18-036, Redacted Response to the Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado Generated Missiles2018-07-0303 July 2018 Redacted Response to the Request for Additional Information Regarding the License Amendment Request to Revise the Licensing Bases for Protection from Tornado Generated Missiles ML20052D9362018-07-0303 July 2018 Response to Nrg Request for Additional Information (RAI) Regarding NAC Magnastor Cask Loaded to Incorrect Helium Backfill Density MNS-17-048, Response to Request for Additional Information License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies2017-12-12012 December 2017 Response to Request for Additional Information License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies ML17349A1572017-12-12012 December 2017 Response to Request for Additional Information Regarding License Amendment Request for Temporary Changes to Technical Specifications to Address the 'A' Train Nuclear Service Water System Non-Conforming Condition RA-17-0039, Response to Request for Additional Information (RAI) Regarding 10 CFR 50.55a(z)(1)Proposed Alternative to ASME Section XI Threads in Flange Examination (17-GO-001)2017-08-0909 August 2017 Response to Request for Additional Information (RAI) Regarding 10 CFR 50.55a(z)(1)Proposed Alternative to ASME Section XI Threads in Flange Examination (17-GO-001) RA-17-0035, Supplement to License Amendment Request Proposing Changes to Technical Specification 3.5.1, AC Sources - Operating.2017-07-20020 July 2017 Supplement to License Amendment Request Proposing Changes to Technical Specification 3.5.1, AC Sources - Operating. MNS-17-030, Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal2017-06-28028 June 2017 Response to March 12, 2012, Request for Information Enclosure 2, Recommendation 2.1, Flooding, Required Response 3, Flooding Focused Evaluation Summary Submittal RA-17-0030, Response to Request for Additional Information Regarding Application to Reverse Technical Specifications to Adopt Multiple Technical Specification Task Force Travelers2017-06-0808 June 2017 Response to Request for Additional Information Regarding Application to Reverse Technical Specifications to Adopt Multiple Technical Specification Task Force Travelers MNS-17-023, Response to Request for Additional Information to License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies2017-05-25025 May 2017 Response to Request for Additional Information to License Amendment Request Permanent Extension of Type a and Type C Leak Rate Test Frequencies CNS-16-066, Stations - Supplemental Information Regarding Reevaluated Seismic Hazard Screening and Prioritization Results - Response to NRC Request for Information, Per 10CFR50.54(f) Regarding Recommendation 2.1 of the Near-Term Task..2016-10-20020 October 2016 Stations - Supplemental Information Regarding Reevaluated Seismic Hazard Screening and Prioritization Results - Response to NRC Request for Information, Per 10CFR50.54(f) Regarding Recommendation 2.1 of the Near-Term Task.. ML16294A2542016-10-13013 October 2016 Response to Request for Additional Information Regarding Relief Request 16-MN-002, Alternative to Defect Removal Prior to Performing Repair Activities on Nuclear Service Water System Piping RA-16-0035, Response to Request for Additional Information (RAI) Regarding Application for Emergency Operations Facility (EOF) Consolidation2016-10-0303 October 2016 Response to Request for Additional Information (RAI) Regarding Application for Emergency Operations Facility (EOF) Consolidation ML16244A0602016-08-18018 August 2016 Response to Request for Addition Information to RR 16-MN-003 MNS-16-070, Response to Request for Additional Information to Relief Request 16-MN-0032016-08-18018 August 2016 Response to Request for Additional Information to Relief Request 16-MN-003 MNS-16-060, Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident2016-08-18018 August 2016 Spent Fuel Pool Evaluation Supplemental Report, Response to NRC Request for Information Regarding Recommendation 2.1 of the Near-Term Task Force Review of Insights from the Fukushima Dai-ichi Accident ML16230A0062016-08-11011 August 2016 Response to Request for Additional Information Regarding License Amendment Request to Technical Specification 3.6.13, Ice Condenser Doors RA-16-0027, Response to NRC Regulatory Issue Summary 2016-09 Preparation and Scheduling of Operator Licensing Examinations2016-07-14014 July 2016 Response to NRC Regulatory Issue Summary 2016-09 Preparation and Scheduling of Operator Licensing Examinations MNS-16-056, License Amendment Request, One-Time Extension of Appendix J Type a Integrated Leakage Rate Test Interval, Response to Request for Additional Information2016-06-30030 June 2016 License Amendment Request, One-Time Extension of Appendix J Type a Integrated Leakage Rate Test Interval, Response to Request for Additional Information MNS-16-023, Response to Request for Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding License Amendment Request for Control Room Chilled Water System Technical Specifications2016-03-16016 March 2016 Response to Request for Supplemental Information Needed for Acceptance of Requested Licensing Action Regarding License Amendment Request for Control Room Chilled Water System Technical Specifications ML16056A2422016-02-18018 February 2016 Response to Request for Additional Information Regarding the License Amendment Request (LAR) to Change the Emergency Plan to Upgrade Emergency Action Levels Based on NEI 99-01, Revision 6 MNS-16-005, Response to Request for Additional Information (RAI) During January 12, 2016, NRC Teleconference Pertaining to License Amendment Request for Nuclear Service Water System Allowed Outage Time Extension2016-02-10010 February 2016 Response to Request for Additional Information (RAI) During January 12, 2016, NRC Teleconference Pertaining to License Amendment Request for Nuclear Service Water System Allowed Outage Time Extension MNS-16-008, Expedited Seismic Evaluation Process (ESEP) Closeout, Response to NRC Request for Information, Per 10 CFR 50.54(f) Regarding Recommendations 2.1 of the Near-Term Task Force Review of Insights from the Fukushima..2016-02-0404 February 2016 Expedited Seismic Evaluation Process (ESEP) Closeout, Response to NRC Request for Information, Per 10 CFR 50.54(f) Regarding Recommendations 2.1 of the Near-Term Task Force Review of Insights from the Fukushima.. MNS-16-009, Response to NRC Letter Dated December 9, 2015, Request for Additional Information Regarding Request for Exemption from Title 10 of the Code of Federal Regulations (10 CFR) Part 74.19(c)2016-02-0404 February 2016 Response to NRC Letter Dated December 9, 2015, Request for Additional Information Regarding Request for Exemption from Title 10 of the Code of Federal Regulations (10 CFR) Part 74.19(c) RA-16-0006, Response to NRC Request for Additional Information (RAI) Regarding Application to Use Alternate Fission Gas Gap Release Fractions2016-02-0101 February 2016 Response to NRC Request for Additional Information (RAI) Regarding Application to Use Alternate Fission Gas Gap Release Fractions MNS-16-003, Response to Request for Additional Information (RAI) Regarding License Amendment Request to Revise Technical Specification 3.3.1, Reactor Trip System (RTS) Instrumentation2016-01-0707 January 2016 Response to Request for Additional Information (RAI) Regarding License Amendment Request to Revise Technical Specification 3.3.1, Reactor Trip System (RTS) Instrumentation ML15343A0122015-12-0707 December 2015 Response to NRC Letter Dated 10/26/2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension. MNS-15-093, Response to Request for Additional Information Regarding License Amendment Request Regarding Residual Heat Removal System2015-11-13013 November 2015 Response to Request for Additional Information Regarding License Amendment Request Regarding Residual Heat Removal System MNS-15-078, Response to NRC Letter Dated September 14, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension2015-10-0808 October 2015 Response to NRC Letter Dated September 14, 2015, Request for Additional Information Regarding License Amendment Request, Nuclear Service Water System Allowed Outage Time Extension MNS-15-077, Expedited Seismic Evaluation Process (ESEP) Report (CEUS Sites), Response to NRC Request for Information, Per 10CFR50.54(f) Regarding Recommendations 2.1 of the Near-Term Task Force Review of Insights from the Fukushima..2015-10-0808 October 2015 Expedited Seismic Evaluation Process (ESEP) Report (CEUS Sites), Response to NRC Request for Information, Per 10CFR50.54(f) Regarding Recommendations 2.1 of the Near-Term Task Force Review of Insights from the Fukushima.. 2023-07-07
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~DUKEVice President DUKE ENERGYMcGuire Steven NuclearD.capps Station Duke Energy MG01VP I112700 Hagers Ferry Road Huntersville, NC 28078 o: 980.875.4805 f: 980.875.4809 Steven.Capps~duke-energy.com 10 CFR 50.90 October 08, 2015 Serial: MNS-1 5-078 U.S.' Nuclear Regulatory Commission Washington, DC 20555-001 ATTENTION: Document Control Desk Duke Energy Carolinas, LLC (Duke Energy)
McGuire Nuclear Station, Units 1 and 2 Docket Nos. 50-369 and 50-370 Renewed License Nos. NPF-9 and NPF-17
Subject:
Response to NRC letter dated September 14, 2015, "McGuire Nuclear Station, Units 1 AND 2: Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension (TAC NOS. MF2983 AND MF2984)"
References:
- 1. Duke Energy Letter dated June 30, 2015, "License Amendment Request for Temporary Changes to Technical Specifications for Correction of an 'A' Train Nuclear Service Water System (NSWS) Degraded Condition" (Agencywide Documents Access and Management System (ADAMS) Accession No. ML15191A025).
- 2. Nuclear Regulatory Commission (NRC) Letter dated July 27, 2015 "McGuire Nuclear Station, Units 1 and 2 - Acceptance Review of License Amendment Request RE:
Temporary Changes to Technical Specifications for Correction of Nuclear Service Water System Degraded Condition (TAC NOS. MF6409 AND MF641 0)" (ADAMS Accession No. ML15202A661)
- 3. Duke Energy Letter dated August 11, 2015, "Response to Request for Additional Information Regarding License Amendment Request for Temporary Changes to Technical Specifications for Correction of an 'A' Train Nuclear Service Water System (NSWS) Degraded Condition (TAC Nos. MF6409 and ME 6410)" (ADAMS Accession No. ML15247A066)
- 4. NRC Letter dated August 27, 2015, "McGuire Nuclear Station, Units 1 AND 2: Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension (TAC NOS. MF2983 AND MF2984)"(AASAcsinN.L53A1)**0_
US Nuclear Regulatory Commission October 08, 2015 Page 2
- 5. Duke Energy Letter dated September 24, 2015, "Response to Request for Additional Information Regarding License Amendment Request for Temporary Changes to Tech~nical Specifications for Correction of an 'A' Train Nuclear Service Water System (NSWS) Degraded Condition (MF2983 AND MF2984)"
- 6. NRC Letter dated September 14, 2015, "McGuire Nuclear Station, Units 1 AND 2:
Request for Additional Information Regarding License Amendment Request Nuclear Service Water System Allowed Outage Time Extension (TAC NOS. MF2983 AND MF2984)" (ADAMS Accession No.ML15252A276)
By letter dated June 30, 2015 (Reference 1), Duke Energy requested a license amendment for the Renewed Facility Operating Licenses (FOL) and Technical Specifications (TS) for the McGuire Nuclear Station, Units 1 and 2, to allow temporary changes to TS 3.5.2, Emergency Core Cooling System (ECCS) - Operating; TS 3.6.6, Containment Spray System (CSS); TS 3.7.5, Auxiliary Feedwater (AFW) System; TS 3.7.6, Component Cooling Water (CCW) System; TS 3.7.7, Nuclear Service Water System (NSWS); TS 3.7.9, Control Room Area Ventilation System (CRAVS); TS 3.7.11, Auxiliary Building Filtered Ventilation Exhaust System (ABFVES),
and TS 3.8.1, AC Sources- Operating.
By letter dated August 11, 2015 (Reference 3), Duke Energy responded to NRC letter dated July 27, 2015 (Reference 2), request for additional information (RAI) needed for completion of NRC staff review of the proposed LAR.
By letter dated September 24, 2015 (Reference 5), Duke Energy responded to NRC letterdated August 27, 2015 (Reference 4), RAI needed for completion of NRC staff review of the proposed LAR.
By letter dated September 14, 2015 (Reference 6), the NRC provided Duke Energy a third RAI needed for completion of the NRC staff review of the LAR. The enclosure provides Duke Energy's responses to the RAI questions.
There are no new regulatory commitments with this submittal. However, Attachment 1 in the enclosure revises existing commitments 2 and 21 from their original form in Reference 1.
The June 30, 2015, LAR concluded that the proposed change presents No Significant Hazards Considerations, and does not require an environmental assessment. This conclusion has not changed as a result of the RAI responses in the enclosure.
US Nuclear Regulatory Commission October 08, 2015 Page 3 Pursuant to 10 CFR 50.91, a copy of this LAR has been forwarded to the appropriate North Carolina state officials.
Please direct any comments or questions regarding this submittal to George Murphy at (980) 875-5715.
I declare under penalty of perjury that the foregoing is true and correct. Executed on October 08, 2015.
Sincerely, Steven D. Capps
Enclosure:
Response to Request for Additional Information
US Nuclear Regulatory Commission October 08, 2015 Page 4 cc wI/
Enclosure:
C. Haney Administrator, Region II U.S. Nuclear Regulatory Commission Marquis One Tower 245 Peachtree Center Ave., NE, Suite 1200 Atlanta, GA 30303-1257 J. Zeiler NRC Senior Resident Inspector McGuire Nuclear Station G. E. Miller, Project Manager U.S. Nuclear Regulatory Commission 11555 Rockville Pike Mail Stop 0-8 G9A Rockville, MD 20852-2738 W. L. Cox, Ill, Section Chief North Carolina Department of Environment and Natural Resources Division of Environmental Health Radiation Protection Section 1645 Mail Service Center Raleigh, NC 27699-1 645
ENCLOSURE Response to Request for Additional Information
Response to Request for Additional Information REQUEST FOR ADDITIONAL INFORMATION BY THE OFFICE OF NUCLEAR REACTOR REGULATION RELATED TO A LICENSE AMENDMENT REQUEST SUPPORTING CORRECTION OF A NUCLEAR SERVICE WATER SYSTEM DEGRADED CONDITION DUKE ENERGY CAROLINAS. LLC MCGUIRE NUCLEAR STATION, UNITS 1 AND 2 DOCKET NOS. 50-369 AND 50-370 By letter dated June 30, 2015 (Agencywide Documents Access and Management System (ADAMS) Accession No. ML15191A025), Duke Energy Carolinas, LLC (Duke Energy) submitted a license amendment request (LAR) to temporarily change McGuire Nuclear Station (MNS), Units 1 and 2, Technical Specifications (TSs) for correction of a degraded condition affecting the 'A' Train of the nuclear service water system (NSWS). The requested amendment would temporarily change the following TSs to allow the inoperability of the 'A' Train of the NSWS for a total of up to 14 days: TS 3.5.2, Emergency Core Cooling System (ECCS) -
Operating; TS 3.6.6, Containment Spray System (CSS); TS 3.7.5, Auxiliary Feedwater (AFW)
System; TS 3.7.6, Component Cooling Water (CCW) System; TS 3.7.7, Nuclear Service Water System (NSWS); TS 3.7.9, Control Room Area Ventilation System (CRAVS); TS 3.7.11, Auxiliary Building Filtered Ventilation Exhaust System (ABEVES), and TS 3.8.1, AC Sources-Operating. The 'A' Train of the shared NSWS would be inoperable while the safety-related supply from the MNS Nuclear Service Water Pond was drained and isolated to correct a degraded condition affecting that line.
Based on the NRC staff's review of this amendment request, the NRC staff has determined the following additional information is necessary to support completion of its technical review:
SCVB-RAI-001 The license amendment focuses on the temporary alignments and changes requested for the NSWS, however, these changes impact other systems. For the CSS, CRAVS, and the ABFVES:
- a. Explain the available capabilities of the above systems during the time when the requested temporary TS would be enacted.
- b. Discuss the impact of any deviations from standard alignment and operation of the systems.
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Response to Request for Additional Information Duke Energy Response SCVB-RAI-001
- a. "Explain the available capabilities of the above systems during the time when the requested temporary technical specifications changes would be enacted."
The 'A' Train of the CRAVS, ABFVES, and 0SS are supported by 'A' Train NSWS as discussed in Reference 1. These systems are expected to remain in their normal operating alignments during the time that the temporary TS changes would be enacted.
These systems will be operated in accordance with their respective normal operating procedures during the extended completion time of the proposed LAR.
The 'A' Train, safety related systems supported by NSWS will remain functional while the temporary TS changes are in affect but not operable due to the unavailability of the NSW flow path from the 'A' Standby Nuclear Service Water Pond (SNSWP). These systems remain capable of meeting their individual safety functions for all design bases events excluding the loss of the Low Level Intake (LLI) caused by a significant seismic event.
The 'B' Train NSWS and all supported SSCs are expected to remain operable during the time that the temporary TS changes would be enacted.
- b. Discuss the impact of any deviations from standard alignment and operation of the systems.
The ABEVES will be affected by the use of a second access manway in the auxiliary building. The access manway when open will have controls in place to ensure that the auxiliary building ventilation boundary is maintained.
No system deviations for CSS or CRAVS are expected or planned.
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Response to Request for Additional Information SRXB-RAI-001 While the approach taken in the proposed LAR is a qualitative risk approach, please address the need to preclude potentially high-risk plant configurations that could result if additional equipment, not associated with the proposed change, is taken out of service during the proposed Allowed Outage Time (AOT) extension. Provide a justification to limiting the prohibition of discretionary maintenance to the following systems:
- a. 1A EDG;
- b. 2A EDG;
- c. The 'A' Train of NSWS excluding the activities described in the LAR for the 'A' Train NSWS piping to the SNSWP;
- d. The 'B' Train of NSWS, ECCS, CSS, AFW, CCW, CRAVS, ABFVES or the EDGs;
- e. The switchyard and other offsite power sources; and
- f. The SSF.
Specifically, provide a justification for not implementing a broader limitation on discretionary maintenance (e.g., such as that of the cited STPNOC precedent (ML050100291), "S TPNOC will not perform any planned voluntary maintenance in Unit 1 during the extended AO T (EAO T) that would increase the ICCDP.').
Duke Energy Response SRXB-RAI-001 The MNS Electronic Risk Assessment Tool (ERAT) shows that plant risk remains green during performance of activities under the extended completion time of the proposed LAR. The tool considers both internal and external initiating events with the exception of seismic events. MNS will be voluntarily setting the ERAT risk to yellow using the built in code SSA (Safety Significant Activity), which will cause the risk condition color to be "YELLOW." This action will focus site attention on the significance of the proposed LAR activities.
A broader limitation for restricting maintenance activities during the proposed amendment activities is not necessary because no discretionary maintenance will be performed that could adversely affect site focus On the LAR activities during the extended Completion Time (CT). As discussed in the LAR, no discretionary maintenance or discretionary testing will be planned on either NSWS Train except for the 'A' Train NSWS piping to the SNSWP. Additionally, no discretionary maintenance or discretionary testing will be performed on any of the equipment listed in Attachment 1, Regulatory Commitment 6.
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Response to Request for Additional Information SRXB-RAI-002 The LAR lists the following equipment to be protected during the AOT extension of the 'A' train of NSWS:
- a. 'B' Train NSWS
- b. 1B EDG
- c. 2B EDG
- d. 1iBECCS
- e. 2B ECCS
- f. 1lB CSS
- g. 2B CSS
- h. 1B AFW
- i. 2B AFW
- j. 1B CCW
- k. 2B CCW I. BCRAVS
- m. B ABFVES
- n. Auxiliary Building WZ Sump and equipment supporting function of sump Provide a discussion on the criteria used to determine the protected equipment. Include a justification for not including the turbine driven AFW pump, Containment Ventilation Cooling Water (RV) system and the Standby Shutdown Facility (SSF) standby makeup pump, which appears to be important to managing the risk of the proposed AOT extension.
Duke Energy Response SRXB-RAI-002 Fleet Directive AD-OP-ALL-0201, Protected Equipment, provides the guidance for identifying equipment to be protected. The procedure guidance for selection of protected equipment is based on risk and unavailability of SSCs. Both the 1A and 2A NSWS pumps will remain available and functional during the extended CT allowed for under the proposed license amendment. The ERAT risk also would remain green for the proposed amendment request activities. However, MNS agrees to modify the protected equipment list provided in Reference
- 1. The Turbine Driven AFW pump, the Containment Ventilation Cooling Water (RV) system, and the Standby Shutdown Facility including the standby makeup pump were added to the list of protected equipment documented in commitment 21, in Attachment 1.
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Response to Request for Additional Information SRXB-RAI-003 Clarify whether any maintenance will be allowed on the 'A' Train NSWS that would impact the ability of the system to operate taking suction from the Lake Norman Low Level Intake (LLI)
(even if these activities are within the 72 completion time) during the period that the Standby Nuclear Service Water Pond (SNSWP) suction is not available for the 'A' train of NSWS.
Specifically, address what is meant by the following statement in section 3.5 of the LAR:
Any maintenance that is performed on the remaining portions of the 'A' Train NSWS during the period in which the 'A' NSWS piping from the SNSWP is not available will be limited to a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time.
Duke Energy Response SRXB-RAI-003 The statement "Any maintenance that is performed on the remaining portions of 'A' Train NSWS during the period in which the 'A' NSWS from the SNSWP supply piping is not available will be limited to a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time" was included in the proposed amendment to ensure that use of the extended CT was applicable only to the activities described in the LAR. The LAR also included the following statement: "During this period, no discretionary maintenance or discretionary testing will be planned on either NSWS Train except for the 'A' Train NSWS piping to the SNSWP described in this proposed amendment". This condition was added to minimize impact on the stability and ability of the 'A' Train NSWS to operate taking suction from the Lake Norman LLI.
MNS will revise the current statement in commitment 2 of Reference 1 to read as follows: "Any maintenance that is performed on the remaining portions of 'A' Train NSWS during the period in which the 'A' NSWS piping from the SNSWP is not available will be evaluated for impact on the ability of the system to operate while taking suction from the Lake Norman Low Level Intake (LLI) and will be limited to a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time". This is documented in Attachment 1.
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ATTACHMENT 1 Regulatory Commitments
REGULATORY COMMITMENTS The following table identifies those actions committed to by Duke Energy in this document. Any other statements made in this licensing submittal are provided for informational purposes only and are not considered to be regulatory commitments. Please direct any questions you may have in this matter to George Murphy at 980-875-5715.
( Any maintenance reainig portions of 'A' Train NSWS during the period in which the 'A' NSWS piping from the SNSWP is not available will be evaluated for impact on the ability of the system to operate while taking suction from the Lake Norman Low Level Intake (LLI) and will be limited to a 72 hour8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> completion time.
3 The 'B' Train NSWS will be placed in its ESFAS alignment to the SNSWP water source with the 'B' Train pumps in standby prior to starting the LAR activity and remain in this alignment until the 'A' Train NSWS SNSWP water source is restored and ready for post maintenance testing.
4 Procedures will be established to provide an additional defense in depth contingency that could be used in the event of an extremely low probability of a loss of the Lake Norman water source due to a seismic event. The procedures will ensure that system operation is maintained within design limits (less than or equal to 2 NSWS pumps running on a header), control of maximum system flow, and that system configuration prevents interaction of the degraded equipment with the functional equipment.
5 Fukushima Response FLEX modifications will be installed and the FLEX strategies
____will be available for implementation as additional defense-in-depth on both units.
6 During the period in which the 'A' NSWS suction path from the SNSWP is non-functional, no discretionary maintenance or discretionary testing will be planned on the following:
- a. 1AEDG
- b. 2A EDG
- c. The 'A' Train of NSWS excluding the activities described in the LAR for the
'A' Train NSWS piping to the SNSWP.
- d. The 'B' Train of NSWS, ECCS, CSS, AFW, CCW, CRAVS, ABFVES or the EDGs
- e. The switchyard and other offsite power sources
____ f. The SSF 7 A condition in which repairs could impact the ability of an SSC to perform its Safety Function would result in termination of activities. The inspection may identify a condition that cannot be resolved within the 14 day completion time. Should such a condition be identified then the system will be restored to its current OBDN condition.
If the ROV survey presents any opportunities for a less intrusive or less time consuming solution for addressing the OBDN condition, then these opportunities will be pursued, as appropriate.
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8 In an activity planned to be performed this summer separate from the 14 day completion time repair activity, 0RN-7A will be tested for leakage and adjusted if necessary to minimize leakage.
9 In an activity planned to be performed this summer separate from the 14 day completion time repair activity the SNSWP isolation flange will be test fitted to the 'A' SNSWP pipe.
10 Procedure guidance will establish controls to limit evacuation air pressure to less than
___a predetermined value in order to prevent air intrusion into the operating NSWS.
11 Dedicated personnel with procedure guidance will be provided to close the pathway from the auxiliary building on the affected 'A' Train NSWS piping from the SNSWP in the event of any of the following:
- An Engineered Safety Feature (ESF) actuation
- Entry into RPIOIAI57001006 Natural Disasters
- Entry into RPIOIAN57001007 Earthquake 12 This activity will be controlled under the Infrequently Performed Test or Evolution (IPTE) process defined in Fleet Directive AD-OP-ALL-i106, "Conduct of Infrequently Performed Tests or Evolutions", and Duke Energy's Work Management and Execution procedures.
During periods when the new NSWS manway is open, dedicated personnel having communication to the main control room with procedures to continuously monitor and respond to 0RN-7A leakage will be in place. If leakage increases and reaches the pre-determined leak rate limit, the repair activity will be stopped, and the manway will be closed. If conditions prevent the prompt closure of the manway, then operations will place the 'B' NSWS train in operation, secure 'A' NSWS operations and isolate the 'A' NSWS train to stop the leakage.
14 If the second personnel access opening is necessary, then prior to the opening of the system an evaluation of leakage will be performed to validate proper isolation and that leakage is within expected limits.
15 McGuire will communicate with the Transmission Control Center (TCC) to ensure that the McGuire Control Room is notified in the event of potential grid disturbances in order that an appropriate plant response can be formulated.
16 The Work Control Center or 0CC will monitor weather forecasts and radar during the activities that require the NSWS piping personnel access points to be open to assess the potential for severe weather conditions (tornado, thunderstorms).
17 Training will be provided in accordance with the Systematic Approach to Training (SAT) process to Operations personnel on this TS change and the associated evolution to inspect and correct the degraded condition in the 'A' NSWS supply piping from the SNSWP.
18 Operations will review applicable abnormal operating procedures related to the response to an earthquake, the loss of the Lake Norman and the loss of NSWS prior to making 'A' NSWS suction path from the SNSWP inoperable and each shift until 'A' Train NSWS operability is restored.
19 The repair work on the NSWS 'A' Train suction from the SNSWP will be scheduled during a period in which hurricanes and tornadoes have a lower likelihood of
___occurrence.
20 The Outage Command Center (OCC) will be manned while performing the activities Page 3 of 5
authorized by this amendment.
21 The following list of equipment will be protected:
- a. 'B' Train NSWS
- b. 1B EDG
- c. 28 EDG
- d. 1B ECCS
- e. 2B ECCS
- f. 1B CSS
- g. 2B CSS
- h. 1BAFW
- i. 2B AFW
- j. 1B CCW
- k. 2B CCW I. B CRAVS
- m. B ABEVES Sp. Unit 1 TDCAP "L
- q. Unit 2TDCAP ,
- r. Unit 1 Containment Ventilation Cooling Water System (RV) 22 If required-to b-e i"nsta" le 'e ne a p ing o e oocate*d-on the 'A' Train NSWS piping in the auxiliary building will be designed and installed in accordance with the Engineering Change Process.
23 Foreign Material Exclusion (FME) will be controlled during the proposed activities in accordance with AD-MN-ALL-0002, Foreign Material Exclusion (FME). Any debris resulting from the obstruction removal activity will be mechanically cleaned out before the system is closed for return to service per FME plan developed in accordance with the above procedure. The system will be video inspected and reversed flushed from the LLI to the SNSWP with isolation to downstream components to force any sediment back to the SNSWP.
24 Following 'A' Train NSWS restoration, testing will be performed to verify that the as left NSWS performance meets or exceeds pre-activity performance including 'A' Train NSW pump NPSH conditions.
25 Prior to entering the 14 day CT perform an evaluation to ensure that there will be no anticipated impact to 'A' NSWS water supply from the LLI from Alewife fish the during 14 day CT.
26 The new personnel access piping opening (in the auxiliary building) will be controlled by using procedures developed or revised for this purpose to maintain positive control
___of the opening and to prevent an unmonitored release.
27 The ERAT program includes the option to use a SSA (Safety Significant Activity) code which will cause the risk condition color to be "YELLOW". MNS will use this
____code during the activities described in this LAR.
28 Designated operators will be available to execute the manual actions associated with aligning the affected unit's 'A' Train NSWS pump to the 'B' NSWS SNSWP via the Main Supply Crossover piping.
29 If the contingency personnel access opening is installed, then Security personnel will establish the proper controls and compensatory measures prescribed by security procedures and the security plan.
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30 In support of the contingency the following conditions will be established before the start of activities in the LAR:
- The 'A' valve (0RN-14A) will be opened prior to the evolution and power will be removed from the valve operator.
- The 'B' valve (0RN-1 5B) will be maintained closed with the ESFAS signal from each unit blocked prior to the evolution. Maintaining 0RN-1 5B closed with power removed satisfies operability requirements for the 'B' Train NSWS.
The 'B' valve (0RN-1 5B) can be opened from the control room after power is restored if conditions warrant the use of this contingency.
31 Operations will utilize the concurrent dual verification process when operating 0RN-7A.
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