ML15239A059

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SALP Repts 50-269/92-01,50-270/92-01 & 50-287/92-01 for 900801-920201.Overall Performance Acceptable
ML15239A059
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 04/06/1992
From: Ebneter S
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15239A058 List:
References
50-269-92-01, 50-269-92-1, 50-270-92-01, 50-270-92-1, 50-287-92-01, 50-287-92-1, NUDOCS 9205050171
Download: ML15239A059 (29)


See also: IR 05000269/1992001

Text

ENCLOSURE

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

INSPECTION REPORT NUMBERS

50-269/92-01, 50-270/92-01 AND 50-287/92-01

DUKE POWER COMPANY

OCONEE UNITS 1, 2 AND 3

AUGUST 1, 1990 -

FEBRUARY 1, 1992

9205050171 920406

PDR ADOCK 05000269

G

PDR

TABLE OF CONTENTS

Page

I. INTRODUCTION

1...........

1

II. SUMMARY OF RESULTS.....................................

2

III. CRITERIA...............................................3

IV. PERFORMANCE ANALYSIS....................................3

A. Plant Operations...................................3

B. Radiological Controls..................7

C. Maintenance/Surveillance...........................10

D. Emergency Preparedness.............................12

E. Security.........................................

14

F. Engineering/Technical Support......................16

G.

Safety Assessment/Quality Verification ............... 19

V. SUPPORTING DATA AND SUMMARIES ........................... 22

A.

Licensee Activities ................................ 22

B.

Direct Inspection and Review Activities .............. 23

C. Escalated Enforcement Activities .................... 23

D. Management Conferences ............................. 24

E. Confirmation of Action Letters...................... 25

F.

Reactor Trips...................................... 25

G. Review of Licensee Event Reports .................... 26

H. LicensingActivities............................... 27

I. EnforcementActivity............................... 27

.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP)

program is an

integrated NRC staff effort to collect available observations and data on

a periodic basis and to evaluate licensee performance on the basis of

this information.

The program is supplemental to normal regulatory

processes used to ensure compliance with NRC rules and regulations.

It

is intended to be sufficiently diagnostic to provide a rational basis for

allocation of NRC resources and to provide meaningful feedback to

licensee management regarding the NRC's assessment of their performance

in each functional area.

An NRC SALP Board, composed of the staff members listed below, met on

March 13,

1992, to review the observations and data on performance, and

to assess licensee performance in accordance with the guidance in NRC

Manual Chapter NRC-0516, "Systematic Assessment of Licensee Performance".

The Board's findings and recommendations were forwarded to the NRC

Regional Administrator for approval and issuance.

This report is the NRC's assessment of the licensee's safety performance

at the Oconee Units 1, 2 and 3 for the period August 1, 1990, through

February 1, 1992.

The SALP Board for Oconee was composed of:

E. W. Merschoff, Deputy Director, Division of Reactor Safety (DRS),

Region II (RH), (Chairman)

J. R. Johnson, Deputy Director, Division of Reactor Projects (DRP), RH

B. S. Mallett, Deputy Director, Division of Radiation Safety and

Safeguards, RH

A. R. Herdt, Chief, Reactor Projects Branch 3, DRP, RII

D. B. Matthews, Director, Directorate 11-3, Office of Nuclear Reactor

Regulation (NRR)

L. A. Wiens, Project Manager, Project Directorate 11-3, NRR

P. E. Harmon, Senior Resident Inspector, Oconee, DRP, RII

Attendees at SALP Board Meeting:

F. J. Remick, Commissioner

J. Guttmann, Technical Assistant to Commissioner Remick

A. J. Mendiola, Acting Chief, Quality Assurance Section, Division of

Licensee Performance and Quality Evaluation, NRR

G. A. Belisle, Chief, Project Section 3A, DRP, RII

W. H. Miller, Jr., Project Engineer, Project Section 3A, DRP, RII

S. Q. Ninh, Project Engineer, Project Section 3A, DRP, RII

B. B. Desai, Resident Inspector, Oconee, DRP, RH

W. K. Poertner, Resident Inspector, Oconee, DRP, RH

2

II. SUMMARY OF RESULTS

Oconee operated safely during this evaluation period. A loss of decay

heat and an overpressurization event during outage activities were the

result of inadequate control room command and control and ineffective

oversight of shutdown plant operations.

In addition to these outage

events, problems continue to exist in the areas of configuration control

and procedural adherence.

During the last three months of this

assessment period improvement has been noted in the oversight of control

room activities.

Performance in the radiological control area continues to be effective.

A strong ALARA program is evident as well as numerous ongoing projects to

reduce collective dose.

Programs for monitoring/collecting liquid and

gaseous effluents, maintenance of effluent monitoring and environmental

monitoring were effective.

Performance in the maintenance/surveillance area was inconsistent.

Programs such as shifting from reactive to predictive maintenance

activities, thermography and Inservice Inspection remain effective.

Problems continue in areas such as procedural adherence and reactor trips

during surveillance testing.

The licensee continued to maintain a strong emergency response organiza

tion.

Management attention and support was evident.

Several program

strengths were identified which included training and completion of a new

EOF. During two exercises this SALP period as well as during an ALERT in

November 1991 involving a reactor coolant leak, the Emergency Plan was

effectively implemented.

Performance in the security area was superior.

Security management at

both site and corporate was knowledgeable and highly supportive. Due to

a continuing problem with closed circuit televisions being out of

service, many protected area intrusion detection zones had to be

physically assessed.

The Fitness for Duty Program is effectively

implemented.

Design engineering and other support groups have been adequate and

responsive to station needs. Good communications exist between corporate

and site engineering. Engineering successfully implemented several major

modifications. However, poor modification design led to a water hammer

and multiple fittings were inappropriately used to transition between

different pipe sizes.

A new organization change is planned to move

engineering personnel on site in July 1992.

With the exception of shutdown operations, Safety Assessment/Quality

Verification performance demonstrated a thorough approach to assessing

conditions and activities relating to the operation of the plant.

Program initiatives to define the design bases and to investigate

significant operating events are considered strengths.

Several plant

3

modifications have been implemented that have enhanced safety, and some

improvements have been noted in the quality of licensing submittals.

However,

corrective actions have not been effective in preventing

recurrence of problems.

Overview

Performance ratings assigned for the last rating period and the current

period are shown below.

Rating Last Period

Rating This Period

Functional Area

2/1/89 -

7/31/90

8/1/90 -

2/1/92

Plant Operations

1

2

Radiological Controls

1

1

Maintenance/Surveillance

2(Improving)

2

Emergency Preparedness

1

1

Security and Safeguards

2(Improving)

1

Engineering/Technical

1

2

Support

Safety Assessment/

2

2

Quality Verification

III. CRITERIA

The evaluation criteria which were used to assess each functional area

are described in detail in NRC Manual Chapter MC-0516, which can be found

in the Public Document Room files.

Therefore, these criteria are not

repeated here, but will be presented in detail at the public meeting to

be held with licensee management.

IV. PERFORMANCE ANALYSIS

A. Plant Operations

1. Analysis

This functional area addressed the control and performance of

activities directly related to operating the facility,

including fire protection.

While Oconee operated safely during this evaluation period,

recurring procedural violations and events during shutdown and

outage activities have caused significant concern. Performance

in this area has declined during the assessment period because

of these problems due to their number and significance.

Improvement was noted in the last three months of the

assessment period due in part to increased management attention

to conduct of operations and greater attention to detail.

4.

Power Operations

Certain programmatic

areas exhibited problems,

including

configuration control and procedural adherence.

The

configuration control errors involved mispositioned valves,

breaker tagging and equipment being taken out of service on the

wrong unit.

Events involving procedure violations include

mispositioning Low Pressure Service Water valves when a valve

checklist was not performed, sluicing core flood tanks without

a procedure, spilling radioactive resin and water due to

mispositioned valves, and lining up the Lee power station to

the standby bus without degraded grid voltage protection. Some

of these instances of failing to follow procedures also

involved specific decisions to inappropriately deviate from the

procedures,

in that, in two instances operators bypassed

procedural steps without careful consideration of the reason

for that step. Deficiencies in procedural compliance were also

noted in the previous SALP report as an area that should

receive continued management attention.

Based on the above

examples, management has not been fully successful in resolving

this problem.

Operator response to transient and upset conditions from power

was good, particularly with respect to runback management and

trip response. Runbacks were usually stopped by the operators

who were able to diagnose and correct the conditions causing

the runbacks.

During the November 1991

loss of coolant

accident (LOCA),

the operators performed well except for a

problem associated with the operation of the steam station

controls. Overall performance during this event indicated that

the operators were well trained and experienced.

Operators and shift supervisory personnel generally exhibited a

conservative approach to technical issues.

Plant operations

assisted as necessary to resolve technical issues, with special

emphasis placed on teamwork approaches to the resolutions.

The experience level of the shift personnel and the Operations

support group is considered very high. Each of the five shift

crews are staffed with two extra reactor operators. Recently

there has been a resultant decrease in overtime.

Shutdown Operations

Operations personnel sometimes exhibited a lack of attention to

detail.

One instance occurred when operations personnel

secured the cooling water to the operating control rod drive

mechanisms. Another example involved operations personnel not

questioning maintenance personnel performing a hydrostatic test

at the same time that the Reactor Coolant System (RCS)

was

5

being drained down for midloop operations.

Because there was

only a single valve boundary during the hydrostatic test,

leakage by this valve caused an RCS dilution.

Additionally,

both source range nuclear instruments were inappropriately

deenergized on two occasions.

Control room inattentiveness and poor communications at times

resulted in actual events and near misses,

including three

events that resulted in NRC Augmented Inspection Teams (AITs)

being dispatched to review the circumstances involved.

The

event that led to the AIT in March 1991 involved a loss of

decay heat removal

and was caused by incorrect labeling,

inadequate

independent verification,

poor communications

between operations and technical personnel,

procedural

inadequacies and incorrectly using plant drawings.

The events

that led to the second and third AITs in September involved a

loss of decay heat removal

and overpressurizing the Low

Pressure Injection (LPI) system. These events were caused by

failure to implement or follow procedures, inadequate

communications, inappropriate conduct of operator responsi

bilities and inadequate facility management oversight.

Corrective actions implemented in the latter part of the

assessment period produced improvement in attention to routine

evolutions and shift duties.

In particular, communications

between various support groups improved due to work management

changes.

The licensee failed to recognize deficiencies in fundamental

watch standing practices, and command and control of shift

operations which were root causes for the Unit 1 RCS heatup and

the LPI overpressurization events.

However, efforts have been

taken to correct watch standing practices and improvements have

been observed during the latter part of this assessment period.

The Operations Support Group was staffed with experienced

personnel

including a large percentage of licensed,

shift-experienced personnel.

This group provided a valuable

resource to shift crews in several areas including "System

Expert" support, work control screening, scheduling and review,

and procedure review and revision.

Assistance in performing

complex and non-routine evolutions such as mid-loop approach

and High Pressure Injection (HPI)

system full flow testing was

considered a strength.

Attention to detail for planned evolutions was not always

evident. One example was the spill of 800 gallons of water from

the Letdown Storage Tank. This event occurred when operators

assumed a valid tank level indication was in error.

As a

6

result, recurring problems were evident in areas of independent

verification, spills from mispositioned valves, tagging errors,

and other configuration control problems.

Several significant control room modifications were completed

during the period, including ATWS Mitigation System Actuation

Circuitry (AMSAC),

Diverse Scram System, and instrumentation

upgrades addressing Regulatory Guide 1.97 issues. Modification

training for Operations personnel

was generally adequate.

Some instances were noted of a lack of operator familiarity

with recently completed modifications.

These included the

diverse scram system, the radiation monitor system and the

reactor coolant pump vibration monitor system.

Fire Protection Program

The fire protection program as a whole was well implemented.

However, three

problems with

the

use of combustible

scaffolding, inoperable fire barrier between redundant safe

shutdown components and the failure to perform an adequate

operability verification for the Keowee C02 fire suppression

system were identified.

New state of the art fire detection

and control panels have been installed to replace the old

system panels.

Procedures to implement the program are

adequate. The fire brigade was well trained and equipped and

performed satisfactorily during drills.

The TS required fire

protection program audits performed by the licensee were

comprehensive and thorough.

Surveillance and maintenance of

the fire protection features and systems were adequate. System

impairments were generally corrected in a timely manner and

appropriate compensatory measures were established for degraded

conditions.

Nine violations were identified.

Two Severity Level III

violations pertaining to two separate September shutdown events

were issued after the SALP cycle closed.

Two additional

violations were identified but not issued in this SALP period.

2. Performance Rating

Category: 2

3. Recommendations

The NRC is concerned with the execution of control room command

and control functions as well as the effectiveness of

management oversight of plant operations primarily during

shutdown conditions and refueling outages.

Enhanced NRC

inspection during shutdown conditions is recommended.

7

The licensee should evaluate the effectiveness of control room

command and control functions and the effectiveness of work

scheduling and plant operations during shutdown conditions and

the effect on safety system availability.

B. Radiological Controls

1. Analysis

The functional area addresses those activities related to

radiation safety and primary/secondary chemistry control.

Both Radiation Protection and Chemistry were well staffed to

perform scheduled operations.

Supervisors and managers were

well qualified and all positions were filled.

To assist the

health physics (HP)

staff for non-scheduled outages,

the

utility retained 15 HP vendor technicians at each Duke nuclear

site, thereby having another 30 HP technicians available on one

day notice to any site. The newly retained vendor HP group has

added more stability to radiological coverage at the early

onset of unscheduled outages.

Late in the assessment period,

the licensee planned to, but was not providing continuing

training or on-the-job training for the retained vendor

technicians.

The licensee's ALARA program was a strength with contributions

from engineering support and HP guidance, teamwork, and ALARA

techniques inherently designed into modifications and

radiological operations. The licensee's initiatives to reduce

out of core source term and collective dose were numerous. Two

of the more significant initiatives in the assessment period

were the replacement of the 4-inch diameter component Drain

Header and steam generator "J" leg drains, and the replacement

of highly radioactive hot leg shield blocks. As a result, dose

rates in the general areas of the containment basement and

cavities have been reduced by a factor of four and in some

areas by a factor of six.

The newly installed valves in the

component Drain Header and "J" leg drains are designed to

minimize crud build up and the new hot leg shield blocks have

multi-coatings to inhibit the adherence of radioactivity. The

licensee has also used several other methods to reduce the

source term and collective dose,

such as,

crud burst at

shutdown and subsequent filtration, flushing to remove hot

spots, temporary lead shielding, and removal of radioactive

piping no longer in use.

8

The licensee established a collective dose goal of 504

person-rem for 1991 with two scheduled outages.

The goal was

exceeded by 56 person-rem due to three unscheduled outages.

The licensee per-unit collective dose average for the years

1989, 1990 and 1991 was

228,

134,

and 187 person-rem

respectively, for a three year per unit average of 183

person-rem.

This three year average is indicative of the

aggressiveness of the program to reduce the source term and is

low for an older three unit pressurized water reactor.

The licensee's program to control contamination continues to be

effective.

One example was the effective cleanup and

monitoring of a November 1991, spill of reactor coolant due to

a failure of a compression fitting.

The station's program to

reduce contaminated square footage has leveled off over the

past two assessment periods at approximately six percent of the

107,750 square feet of radiologically controlled area (RCA)

as

contaminated.

Two examples where the contamination control

program was not effective were an increased number of personnel

contamination events and low level contaminated items located

outside the RCA.

The licensee experienced 141 personal

contamination events (PCEs)

in 1990 and 294 PCEs in 1991.

The

increase in PCEs can be attributed to two scheduled and three

unscheduled outages and the use of 23 new state-of-the-art

personnel monitors with increased sensitivity.

The licensee's program for monitoring and controlling liquid

and gaseous radioactive effluents was effectively implemented.

The whole body doses were less than one millirem/year each from

the liquid effluents and from the gaseous effluents released

during 1990 and 1991. Those doses were a small percentage of

their respective limits.

The licensee reduced by 62 percent

the fission and activation products released in liquid

effluents between the periods January 1989 through June 1990

and July 1990 through December 1991.

(These periods most

closely

coincide with the previous and current assessment

periods.)

The decrease was due, in part to, the leakage

control program; use of multi-element pre-filters to remove

cobalt and magnesium; use of resins with greater surface area;

and modification of demineralizers to reduce channeling. Also,

administrative procedures were changed to set a limit for the

maximum permissible concentration of cesium in liquid waste.

There was also a 39 percent decrease in noble gas released in

the gaseous effluents during the assessment period as compared

to the previous period. Although there were some increases in

halogens and particulates released in the gaseous effluents

during the assessment period as compared to the previous

9

period,

the licensee attributed these increases to the 3

outages during 1991.

No unplanned gaseous releases were

reported to have occurred during the assessment period but one

unplanned liquid release was reported.

On November 7, 1990, a

container being moved by a truck from one warehouse to another

turned over and approximately 7 gallons of water were spilled

from the container.

One gallon of water containing 9

microcuries was conservately estimated to have entered an open

yard drain.

The licensee's maintenance of effluent monitoring capabilities

was good during this assessment period.

The licensee had

completed installation of new Post Accident Liquid Sampling

(PALS) systems on Units 1 and 2. The new PALS systems have been

brought to operational status for all three units.

The

Radwaste Facility Ventilation Monitoring System was also

returned to operational status during the current assessment

period.

Good progress was made in the modification of the Low Pressure

Service Water (LPSW)

monitoring systems.

These systems have

been inoperable since 1986 due to clogged sample lines.

Correction of the problem required a design change to the

system.

The modification for Unit 3 was completed and the

monitoring system for that unit was returned to service.

It is

anticipated that the Unit 1 and 2 LPSW monitoring systems will

be returned to service by mid 1992.

Significant progress was made during the assessment period in

replacement and upgrade of radiation monitoring instrumenta

tion. Digital readouts, with system failure alarms,

were

installed in the Control Room, the Technical Support Center and

the Radiation Protection office area. This program improvement

project is more than 50 percent complete.

The licensee's environmental monitoring program was effectively

implemented. The program results for 1990 indicated that there

was no significant radiological impact on the health and safety

of the general public resulting from plant operations.

Dose

estimates calculated from environmental monitoring program data

were in reasonable agreement with dose estimates calculated

from effluent release data and were well within 40 CFR 190 dose

limits.

The licensee's performance in the Environmental

Protection Agency's interlaboratory

crosscheck program

indicated that an effective quality assurance program had been

maintained for analysis of environmental samples.

Two violations were identified.

10

2. Performance Rating

Category: 1

3. Recommendations

None

C. Maintenance/Surveillance

1. Analysis

This functional area addresses those activities related to

equipment condition, maintenance, surveillance performance, and

equipment testing.

The maintenance/surveillance functional

area exhibited

inconsistent performance throughout the assessment period.

Predictive

maintenance

and equipment monitoring were

agressively persued and were effective whereas weaknesses were

noted in areas such as procedural adherence, documentation of

problems during troubleshooting and repairs, plant transients

and reactor trips induced by maintenance and surveillance

activities.

The licensee's efforts continued this period to move from a

reactive or corrective maintenance program to a predictive and

preventive approach. Maintenance efforts were at a 60/40 ratio

of predictive to corrective maintenance.

The equipment

vibration monitoring,

pipe erosion/

corrosion,

and valve

maintenance and replacement programs are considered strong

areas. The piping erosion/ corrosion program, which is related

to piping systems with the potential for high energy releases,

has been expanded to include both large and small diameter

piping. Most findings to date involve secondary system piping.

A new thermography program was introduced this period and was

instrumental in resolving several issues such as locating

system leakage and identifying deficient piping insulation.

The station has an obsolete and aging equipment program. This

is a joint maintenance and engineering effort.

During this period,

significant operational

problems

attributable to maintenance activities occurred.

A loss of

coolant event due to improperly installed fittings occurred in

November

1991.

The actual installation of the defective

reactor coolant system fittings occurred several years ago.

The licensee's inspection of all fittings identified this as a

pervasive problem with approximately 25 percent of all fittings

not meeting installation criteria.

The program for

installation was changed after the event.

11

-

The

licensee submitted

one

LER

concerning a missed

surveillance.

One instance of post modification/maintenance

requirements not being performed was identified. This involved

not verifying the alignment of the turbine driven emergency

feedwater pump.

Surveillance activities directly caused or contributed to

several plant trips and events.

These included valving a

reactor coolant system flow transmitter

into service

incorrectly; incorrectly using test equipment during a

surveillance test that caused a reactor trip; and incorrectly

returning a low pressure injection pump flow transmitter to

service.

Equipment performance has adversely affected plant operations.

Specifically, six reactor trips from power were caused by

equipment failures.

These trips included an inadvertent trip

of the condensate booster pump and the failure of the standby

pump to start, a rod programmer problem dropped Group 7 rods

into the core, and a rod transfer switch failed in mid position

during rod transfer.

Several instances of independent verification errors resulted

in instrumentation not being properly returned to service nor

properly verified.

Examples include when instrumentation was

isolated during an LPI flow pump test and when instrumentation

test tees for the RCMUP were not tightened. Two instances were

noted of undocumented work activities involving lifting and

landing leads and replacement parts.

As part of the corporate reorganization plan instituted in

November 1991,

the Construction and Maintenance Department

(CMD) was eliminated. All CMD personnel permanently assigned

to Oconee were integrated into the maintenance department.

Training for CMD workers to site standards was initiated.

Use

of vendors and contractors was minimal, with most support for

modifications, maintenance and outage supplied by Duke Power

personnel.

The maintenance department was well staffed with

knowledgeable and experienced personnel.

A lower tier event investigation, root cause and corrective

action program,

Maintenance Incident Report or MIR,

was

implemented midway through this assessment period.

Program

upgrades were in progress and root cause training had been

completed by several maintenance personnel.

12

The inservice inspection program (ISI)

was being effectively

implemented.

ISI nondestructive examinations were being

conducted

by qualified personnel.

The procedures

and

examination techniques used to conduct examinations were

adequate and documentation of examination results was good.

Deficiencies were noted in the areas of pipe support and tendon

surveillance. Specifically, improper placement of radiography

penetrameters,

improper gap between washers and snubber rod

bearings and incomplete magnetic particle testing (MT)

records

were noted. Additionally, the licensee failed to investigate

and resolve the cause of a 2.5 inch difference in snubber hot

and cold settings from the drawing specifications.

Further

investigation identified that the hot and the cold settings

were reversed on the drawing.

Plant material conditions and routine housekeeping were

generally acceptable.

Instances of Unit 2 outage related

housekeeping problems were noted during a Unit 2 containment

closeout walkdown. This was observed early in the assessment

period; subsequent walkdowns indicated improvement in this

area.

Five violations including one Severity Level III violation were

identified.

2. Performance Rating

Category: 2

3. Recommendations

The Board is concerned with the adverse impact of equipment

performance and surveillance activities on plant operations.

Six reactor trips from power were caused by equipment failures

and surveillance activities caused or contributed to plant

events and trips.

Management attention to this area is

appropriate.

D. Emergency Preparedness

1. Analysis

This area addresses those activities related to the Emergency

Plan,

support for and training of emergency response

organizations both on and offsite, and licensee performance

during emergency exercises and actual events.

During this

assessment period the licensee continued to maintain a strong

emergency response organization capable of providing sufficient

protective measures to ensure public safety in the event of an

emergency.

jIII

13

Management attention and support for emergency preparedness was

evident throughout the period.

Program strengths identified

during inspection activity this assessment period included:

maintenance of emergency response facilities and equipment in a

high state of operational readiness, effective training of

onsite and offsite emergency response personnel and completion

and turnover of a new Emergency Operations Facility with

commitments to initially activate and staff the facility from

the Oconee site rather than from the corporate office.

Oconee demonstrated thorough preparation for dealing with site

emergency situations during an October 1990 partial partici

pation exercise and during a full participation October 1991

exercise.

During both exercises the licensee demonstrated it

could effectively implement the Emergency Plan and its

implementing procedures, effectively assign emergency response

organization responsibilities, and could take suitable actions

to mitigate the on and offsite consequences of the accident

scenarios.

Emergency classification was prompt and correct as

the scenarios progressed and operations of the emergency

response facilities and equipment observed during the annual

exercises were good.

Other exercise strengths identified

included effective fire brigade response and,

during the

October 1990 exercise, an effective response to a real medical

emergency onsite coincidental with the exercise.

Two exercise weaknesses were identified during the October 1990

exercise. The first weakness was a failure to activate the

Technical Support Center in a timely manner. The licensee gave

increased attention to activation timeliness between the

exercises and, during the October 1991 exercise, the licensee

was able to demonstrate prompt activation of the Technical

Support Center.

The second weakness involved numerous

communication problems between the Technical Support Center and

the State Forward Emergency Operations Center which were

subsequently corrected.

Overall,

however, the licensee's

performance during the two exercises was good, with the

licensee meeting their exercise objectives and demonstrating a

capability to protect public health and safety in the event of

a radiological emergency.

Emergency

response facilities were kept in a state of

operational readiness, the TSC was remodeled to include an

enhanced emergency data system, and a significant upgrade was

implemented with the turnover and operation of the new

Emergency Operations Facility.

Emergency Preparedness

(EP)

staffing was well qualified and remained constant throughout

the period.

Late in the assessment period the licensee

committed to significantly increase the staffing level onsite

as a result of a corporate reorganization, which decentralized

14

staff and functions from Charlotte to the Oconee site.

During

the period the licensee made appropriate revisions and upgrades

of the Emergency Plan and EPIPs, conducted challenging drills

and exercises, assured proper upkeep of EP equipment,

and

maintained coordination with offsite support groups.

Management attention to program activities was evident

throughout the period. For example, senior technical staff and

management were assigned to emergency response organization

(ERO) functional areas

and were required to maintain

qualification to support response activities. The ERO training

program was thoroughly defined and supported. Lesson plans and

training modules were organized and appropriate for meeting

stated objectives.

During this assessment period, the licensee's Emergency Plan

was implemented twice in response to events,

one at the

Notification of Unusual Event (NOUE) level and one at the Alert

level.

In each case, the event detection and classification

was prompt and correct, offsite authorities were initially

notified in a timely manner,

good updates and periodic

communications were maintained with state and local emergency

operation centers as well as the NRC, and the onsite emergency

organization responded in an overall effective manner.

Two exercise weaknesses were identified.

2. Performance Rating

Category 1

3. Recommendations

None

E. Security

1. Analysis

This functional area addresses those security activities

related to protection of vital plant systems and equipment, and

the Fitness For Duty Program.

Security management at both the site and corporate levels was

knowledgeable and highly supportive of program activities.

Support was indicated by the implementation of a Protected Area

Upgrade Project, a Physical Performance Test Program and by

changing the contract security force to a proprietary security

force.

These initiatives contributed to a reduction in the

15

security staff turnover rate in this assessment period as

compared to the rate during the last period.

The licensee's primary system to assess alarms is a closed

circuit television system fixed and pantilt-zoom cameras. The

licensee could not fully utilize this system during this SALP

period due to equipment malfunctions and maintenance problems.

This issue was identified during the previous two SALP periods.

As part of a comprehensive Protected Area Upgrade Project, the

licensee put in place plans to address problems with the camera

assessment capabilities.

During this SALP period the licensee

improved the quality of a few of the operating cameras and

began installation of the rest of a new camera assessment

system during the latter part of this SALP period.

During this SALP period, the licensee made improvements in its

detection system.

For example, the licensee reconfigured the

protected area perimeter to improve the zones of detection.

Also, the licensee enhanced the physical structure of the

protected area perimeter barrier.

The licensee was in the

final stage of this upgrade project during the end of the

assessment period.

Other areas of the licensee security program were effectively

operated during this period.

For example,

the licensee's

access control program was enhanced to correct the access

control problems mentioned in the last SALP period.

The

licensee has also improved its program to account for and

identify security keys.

Alarm stations and communication

equipment associated with the stations were operated by capable

and knowledgeable personnel.

The testing and maintenance of

the security equipment were conducted as required.

The licensee had established, maintained and effectively

implemented a security program for the Independent Spent Fuel

Storage Installation (ISFSI).

The licensee's Fitness for Duty Program was effective in

obtaining drug-free workplaces while balancing the rights and

privacy of the workforce. It met the objectives of 10 CFR 26.

The licensee submitted three Security, two Contingency,

one

Training and Qualification, and one Independent Spent Fuel

Storage Installation (ISFSI)

Security Plan revisions during

this period.

These revisions were consistent with

10 CFR 50.54(p) and adequately coordinated.

The security force was well staffed, equipped, and trained to

perform their assigned duties. The security training staff was

dedicated, knowledgeable and motivated.

16

2. Performance Rating

Category:1

3. Recommendations

None

F. Engineering/Technical Support

1. Analysis

This functional area addresses those activities associated with

engineering and technical support, including activities

associated with design of plant modifications, engineering, and

technical support for operations and operator training.

The licensee's engineering (DE)

and other technical support

groups have been responsive to station needs.

Overall

engineering and technical support continues to effectively plan

and implement plant modifications.

The experience level of

engineering and technical personnel and their participation in

generic industry initiatives remains high.

Communications

between DE (General Office) and plant engineering have improved

as a result of reorganization of DE and establishment of an

onsite DE contingent.

Responsiveness to station needs is evidenced by the monitoring

and testing of the reactor building cooling units on line,

identification and investigation of problems associated with

the testing of pressurizer safety valves, and fire detection

system and radiation monitoring equipment upgrades.

Engineering support for successfully implemented modifications

included the emergency feedwater system, Anticipated Transient

Without a Scram

(ATWS)

mitigation safety actuation circuit

(AMSAC),

the diverse scram system and Regulatory Guide 1.97

emergency core cooling system instrumentation.

A main steam

condensate system water hammer event as well as the failure of

a pressure fitting on the Reactor Vessel Level Instrumentation

System (RVLIS)

instrumentation were examples of inadequate

engineering support for modifications.

In the former example,

the modification was not correctly designed and on first use,

resulted in the water hammer.

In the latter example, the

modification depended upon excessive fittings to transition

from a one-inch pipe to a three-eights inch instrument line.

17

DE was actively involved in various industry initiatives such

as resolution of several Generic Letters.

DPC was also

involved in the Operating Experience Program,

Nuclear Plant

Reliability Database System,

Babcock and Wilcox Owner's Group

and various Nuclear Utility Management and Resource Counsel

initiatives.

Continued good communication and cooperation between corporate

and site engineering groups during this assessment period was

evidenced by the motor operated valve test program which

required coordination of engineering calculations, system

reviews,

the development of a program and procedures,

and

implementation of diagnostic testing of valves under design

basis conditions.

Strengths were identifi.ed with the motor

operated (MOV)

program.

These included well documented and

thorough switch setting calculations,

the initiation of

differential pressure testing and knowledgeable personnel.

DE was responsible for the ongoing Design Basis Documentation

(DBD) program. The DBD was started in 1989 to provide accurate

design base documentation of all safety related systems.

This

program continued to involve significant engineering resources.

The program is scheduled to be completed in 1995 and has

resulted in the identification and correction of several

significant electrical system design deficiencies as well as

other system discrepancies.

The Operating Experience Review program was effective and led

to the identification of susceptibility to certain fault types

at the Keowee Hydro units.

Additionally, several breaker

coordination problems were identified during design reviews of

breaker and relay trip settings. The licensee's resolution of

these problems was thorough and timely.

Followup on the

potential for hydrogen intrusion and degradation of high

pressure injection (HPI)

pumps was not effective in that DE

failed to recognize the severity of this issue and actions

necessary to resolve the issue were not timely.

In general,

DE produced procedures were adequate although

instances of inadequate procedures were noted.

Specifically,

procedures involving the installation of compression fittings

and testing of the HPI system were inadequate. The HPI system

was determined to have been inoperable for extended periods due

to improperly installed flow instruments and orifice plates.

The ISI program was effectively implemented by highly skilled

and knowledgeable engineers and technicians, and knowledgeable

and technically competent contractor personnel.

Inspections

were well planned and included use of mock ups for steam

generator work, and use of state-of-the-art equipment.

Test

.

18

results were well documented. The use of previous test results

in evaluation of inspection findings and conservative decisions

relative to inspection findings were noted.

Concerns were identified in the DE and technical support area.

For example the inoperability of a startup transformer was due

to inadequate reading of a manufacturer's relay setting curve

and an inadequate post modification test. Another weakness was

identified during the repair of a pipe crack on a Low Pressure

Injection (LPI)

system dropline.

These included failure to

detect and resolve LPI

pump vibration before the crack

developed, failure to adequately review and pre-plan spool

piece fabrication to prevent distortion, failure to adequately

pre-plan and control purging in the welding process,

and

inability to readily retrieve replacement component quality

records after the repair.

Additional management attention is required in the area of

licensed operator training. Sixteen Generic Fundamental

Examinations were administered during the assessment period

with four failures.

Insufficient effort by the Oconee Training

Department in support of the requalification program was noted.

Some

NRC requested changes provided to examinations were

omitted, and the simulator scenario bank was developed at the

minimum rate.

Operational validation of examination material

was often lacking and some scenarios were short and simplistic.

Poor support was identified during the pre-review of the

January 1992 Initial Examination written portion which resulted

in post examination comments on a large portion of the.

examination.

During simulator examinations, weaknesses were

noted in manual operation of feedwater controls.

The plant

specific simulator exhibited deficiencies in Engineered

Safeguards component modeling and the inability to fail some

major components.

Poor planning of post maintenance testing has resulted in the

submittal of several relief requests requiring expedited review

by the NRC.

During the Unit 1 outage in August 1991, work on a

RCP required removal of the pressurizer safety valve tailpiece.

A request for relief was submitted late in the outage, when the

need for the relief should have been determined when planning

for the outage.

Similar examples occurred during the Unit 2

outage in October 1990,

when three relief requests were

submitted at the end of the outage related to the testing of

repair welds. These relief requests were submitted only a few

days before the approval was needed.

19

Four violations including two Severity Level III violations

were identified.

2. Performance Rating

Category:

2

3. Recommendations

Increased management attention is warranted in the area of

licensed operator training.

Specifically, support of the

requalification examination program is weak and operational

validation of examination material is often lacking.

G. Safety Assessment/Quality Verification

1. Analysis

This functional area addresses those activities related to

implementation of safety policies; amendments,

exemptions and

relief requests; response to Generic Letters, Bulletins, and

Information Notices; resolution of safety issues; reviews of

plant modifications performed under 10 CFR 50.59; safety review

lacommittee

activities;

and the use of feedback

from

self-assessment programs and activities.

During the assessment period several plant modifications and

program changes enhancing plant safety were initiated or

completed. Hardware changes included Emergency Feedwater test

loop installation, a new Radiation Monitoring system,

switchyard access control with fences established, and a new

fire detection system installed in the turbine and auxiliary

buildings.

Design Baseline Documentation (DBD)

reviews of

several safety systems continued during this assessment period.

A "lower tier" event investigation processes for each

organizational unit was initiated.

Management decisions were generally conservative and adequately

considered plant, system, and personnel safety.

Although not

strictly required by TS,

Unit 3 was shut down to repair the

Standby Shutdown Facility (SSF)

Reactor Coolant Makeup System,

and HPI full flow testing was voluntarily initiated.

There

were instances where less conservative approaches were

employed.

These included a decision to continue with RCS

draindown without ultrasonic level instruments in service;

allowing workers to suspend work required to promptly restore

the dewatered Keowee hydro units; and starting up a unit with

an intermediate excore neutron detector inoperable.

20

The corporate and site reorganization has incorporated most

independent,

safety oversight functions under the Safety

Assurance Manager and his staff.

These include Regulatory

Compliance,

Safety Review,

Environmental

Compliance,

and

Emergency Preparedness.

An accurate assessment of the

reorganization's

impact on plant safety and safety

consciousness was not made due to its implementation late in

the assessment period.

The licensee normally demonstrated an aggressive approach to

the resolution of those issues which are clearly safety

significant.

Their actions were generally conservative and

thorough,

and involved interaction with NRR staff when

appropriate.

Examples included the

installation of

modifications to start Emergency Feedwater pumps on low steam

generator level and corrective actions for HPI system operation

in light of SBLOCA concerns.

The licensee continued to support interaction with the NRC

staff to resolve issues,

and ensured that knowledgeable

technical personnel were available. Numerous conference calls

have been held,

and a number of significant meetings were

conducted, such as to provide an overview of the Oconee IPE

submittal, describe the IST program submittal in response to GL 89-04 and discuss the ISI reactor vessel inspection.

Responses to NRC requests were usually provided within the time

frame

requested

and written notice was

provided if

circumstances prevented meeting the requested schedule.

Although the responses were normally timely, the licensee has

been slow to complete some actions.

Examples include

implementing the recommendations of GL 88-14 concerning

instrument air systems,

which is still not completely

implemented and delays in implementing the program recommended

by GL 89-04 on IST programs.

Improvements in the licensee's

program for the procurement and dedication of commercial grade

components was

not implemented in accordance with the

recommended NUMARC schedule, which was endorsed by the NRC.

Licensee proposals and responses were generally well-prepared,

accurate, and thorough. In particular, the quality of proposed

license amendments

has improved during this SALP cycle.

Proposed amendments submitted early in the evaluation period

required supplements to provide clarification, missing

information, or correct errors in the original submittal,

but

more recent submittals have generally required no revision or

additions.

The quality of ISI and IST relief requests were

poor. Some requests were written such that it was difficult to

21

determine what was being requested or the justification for the

relief. Examples included a relief request associated with the

removal of a temporary expandable plug in a LPSW pipe and a

request to modify the inspection schedule of reactor coolant

outlet nozzles.

The licensee's response to Generic Letter

(GL)

88-20,

"Individual Plant Examination," was thorough, well documented,

and included an analysis of external events,

which was not

required to be submitted with the original IPE response.

The

response to NRC Bulletin 88-08, "Thermal Stresses in Piping

Connected to the Reactor Coolant System," only satisfied the

Bulletin recommendations for one Oconee unit. The licensee is

currently preparing a response to a Request For Additional

Information concerning this issue for Units 2 and 3.

The licensee's response to many other issues has been good.

After the NRC raised concerns about the time required to

activate the Oconee Crisis Management Center, the licensee

expeditiously revised the appropriate procedures.

After

deficiencies were identified in the Oconee Technical Specifi

cations relating to shutdown requirements,

the Oconee staff

performed a self-evaluation of their Technical Specifications

and presented the results of their review to the NRC, including

proposed corrective actions.

The response was prepared in a

very short time period and was thorough.

The licensee submitted three Security, two Contingency, one

Training and Qualification, and one Independent Spent Fuel

Storage Installation Security (ISFSI)

Plan revisions during

this period.

These revisions were consistent with 10 CFR

50.54(p) and adequately coordinated.

The ISFSI revision was

forwarded to headquarters for review.

The licensee has developed a program where a Significant Event

Investigation Team (SEIT)

is dispatched to a site after

notification of a significant event.

The SEIT assists the

station safety review group in determining the cause of the

event, safety implications, and necessary corrective actions.

These teams evaluated the shutdown events that occurred at

Oconee Unit 1 in September 1991 and the instrument line leak

that occurred at Unit 3 in November 1991. The teams appeared

to be effective and in the case of the shutdown events, had

findings similar to the NRC AIT findings.

During this assessment period, several events occurred which

reflected management's failure to recognize deficiencies in

fundamental watchstanding practices, and command and control

of shift operations. These events were the loss of decay heat

removal in March and September 1991,

and the overpressuriza

tion of the LPI system in November 1991.

27

3.

Eight Special Reports were submitted but are not

included in the above tabulation.

4. The above information was derived from a review of

LERs

performed by the NRC staff and may

not

completely coincide with the licensee's cause

assignments.

H. Licensing Activities

In addition to QA and security submittals, there were approximately

147 active licensing actions for the three Oconee units during this

SALP period. Of these, 69 were completed. A total of 33 licensing

amendments were submitted and 21 were issued.

I. Enforcement Activity

No. of Deviations and

Violations in Each Functional Area

Dev. V

IV

III

II I

Plant Operations (1)

9

Radiological Controls

2

Maintenance/Surveillance (2)

4

1

Emergency Preparedness

Security

Engineering/Technical

Support (3)

2

2

Safety Assessment/Quality

Verification

TOTAL

17

3

Notes:

(1) Two Severity Level III violations pertaining to two

separate September shutdown incidents were issued

after the SALP Cycle closed.

(2) The Severity Level III violation consisted of three

separate violations, the aggregate of which was

determined to be a Severity Level III.

(3) One Severity Level III violation (269,270,287/

90-17-01) was fully discussed in the previous SALP

period but not counted.

26

June 9, 1991:

Reactor tripped from 100 percent power when when

Group 5 control rods dropped into core during exercise of Rod

12 of Group 12.

July 3, 1991:

Reactor tripped from 100 percent power due to

loss of suction to condensate booster pumps caused by faulty

powdex master controller while bypass valve was not in

automatic.

November 23,

1991:

Reactor tripped from 35 percent power

following a turbine trip on loss of both main feedwater pumps

while shutting down the unit. The unit was being shutdown due

to RCS leakage into containment.

Pressure swings in the

feedwater system caused both feedwater pumps to trip.

January 14, 1992:

Reactor tripped from 94 percent power due to

high steam generator level when both main feedwater pumps

tripped during maintenance troubleshooting operations.

G. Review of Licensee Event Reports (LER)

During the assessment period

32 LERs were analyzed.

The

distribution of these events by cause as determined by the NRC staff

was as follows:

Unit 1

Cause

Totals

or Common Unit 2

Unit 3

Component Failure

6

1

2

3

Design/Procedures

11

10

1

Construction/Fabrication

Installation

4

1

1

2

Personnel

-

Operating Activity

1

1

-

Maintenance Activity

2

1

1

-

Test/Calibration Activity 3

1

1

1

-

Other

1

1

Other

4

2

1

1

Totals

32

17

5

10

Notes:

1. With regard to the area of personnel,

the NRC

considers lack of procedures, inadequate procedures,

and erroneous procedures

to be classified as

personnel error.

2. The Other category is comprised of LERs where there

was a spurious signal a totally unknown cause.

22

Following these events, the licensee took steps to improve the

command and control function for control room operations as

well as to strengthen procedures for assuring safety during

shutdown operations.

Although some improvement was noted

during a Unit 2 refueling outage at the end of this assessment

period, the effectiveness of long term actions has not been

determined.

No violations were identified.

2. Performance Rating

Category: 2

3. Recommendations

None

V. SUPPORTING DATA AND SUMMARIES

A. Licensee Activities

A major reorganization was announced in November

1991,

including relocating Design Engineering to the site.

Implementation of the reorganization has not been fully

completed.

During this assessment period, Unit 1 completed a scheduled

refueling outage in September 1991.

The ten year Inservice

Inspection (ISI), including inspection of the Reactor Coolant

System, was completed during the outage. Several events while

shutdown resulted in two AITs

during this outage.

In

addition, problems with the SSF resulted in a short duration

outage.

Unit 2 completed a scheduled refueling outage in October 1990.

A refueling outage was entered in January 1992.

Unit 3 completed a scheduled refueling outage in March 1991. A

loss of LPI resulted in an AIT on Unit 3 during this outage.

An RCS leak and a subsequent loss of 87,000 gallons of reactor

coolant occurred in November 1991.

This event caused the unit

to be shutdown for over a month.

During the subsequent startup, a through-wall crack in the

decay heat removal dropline, requiring replacement of a portion

of the LPI piping, was discovered.

23

A total of eight automatic and one manual reactor trip occurred

during the assessment period; three trips on Unit 1 and six

trips on Unit 3. In addition several outages of short duration

occurred during the assessment period.

B. Direct Inspection and Review Activities

In addition to the ongoing routine resident inspections, 33 regional

inspections performed at the Oconee facility by the NRC staff, six

special inspections were conducted as follows:

March 12-15, 1991:

Augmented Inspection Team inspection of

loss of decay heat removal event of March 8, 1991.

July 15-19, 1991:

Procurement Assessment.

September 9-13, 1991:

Augmented Inspection Team inspection on

degradation of the low pressure injection system event of

September 7, 1991.

September 20-23, 1991:

Augmented Inspection Team inspection on

over-pressurization of low pressure injection system event of

September 19-20, 1991.

November 23 -

December 21,

1991:

Special inspection of

circumstances associated with primary system leakage due to

failed mechanical fitting on an instrument line for the reactor

coolant system.

December 9-13, 1991: Shutdown Risk Inspection

C. Escalated Enforcement Activities

1. Orders

None.

2. Civil Penalties (CP)

A Severity Level III violation (EA 90-119) was issued for ESF

valves which would have failed in the closed position in lieu

of the open position upon loss of instrument air. ($25,000 CP)

A Severity Level III violation (EA 91-049) was issued for three

violations associated with the Unit 3 loss of decay heat

removal and discharge of approximately 14,000 gallons of water

into the Unit 3 containment (No CP).

24

A Severity Level III violation (EA 91-052)

was issued for

improper installation of flow orifice instrumentation in the

Units 1 and 2 high pressure injection systems. (No CP)

D. Management Conferences

October 18, 1990:

A management meeting was held at the Oconee

Station to discuss the

SALP Board assessment of Oconee's

performance.

December

11,

1990,

and September 4, 1991: A Duke/NRC Interface

Meeting was held at the McGuire facility to discuss issues of

interest to both organizations.

February 12, 1991: A meeting was held at NRC Headquarters for Duke

to give a presentation on the Individual Plant Examination (IPE)

review for the Oconee Station.

February 14,

1991:

A management meeting was held at the Oconee

Crisis Management Center (CMC)

to discuss the activation timeliness

for the CMC in the event of an emergency at the Oconee facility.

March 21, 1991: A management meeting was held in Region II for the

licensee to present details of their investigation of the March 8,

1991, event concerning the loss of decay heat removal capability

while the unit was in cold shutdown.

May 7, 1991:

An enforcement conference was held in Region II to

discuss the circumstances surrounding the March 8, 1991, loss of

decay heat removal capability while the unit was in cold shutdown.

May 22, 1991:

An enforcement conference was held in Region II to

discuss the concerns associated with one high pressure injection

crossover valve in both Units 2 and 3 being incapable of performing

its intended safety function for an extended period of time.

September 25, 1991: A management meeting was held in Region II to

discuss the Unit 1 events associated with the September 7, 1991,

degradation of the decay heat removal and the September 19-20, 1991,

over-pressurization of the low pressure injection system, and the

action taken by Duke on the NRC Confirmation of Action Letter dated

September 20, 1991.

November 5, 1991: A management meeting was held for the licensee to

give a self-assessment of the performance at the Oconee Station from

August 1, 1990.

25

December 18, 1991:

An enforcement conference was held in Region II

to discuss the Unit 1 September 7, 1991, reactor coolant system

heat-up event and the September 19-20, 1991, over-pressurization of

the Unit 1 low pressure injection system event.

E. Confirmation of Action Letters (CAL)

September 20, 1991: A CAL was issued which outlined the actions to

be taken prior to the startup of Unit 1 following the September 7,

1991, degradation of decay heat removal event and the September

19-20,

1991,

over-pressurization of the low pressure injection

system event.

F. Reactor Trips

Unit 1

Three automatic reactor trips occurred:

August 28, 1990:

Reactor tripped from 100 percent power due to

high RCS pressure caused by the trip of Condensate Booster Pump

lB due to spurious signal indicating a closed pump discharge

valve.

May 16, 1991:

Reactor tripped from 100 percent power due to

Flux/Flow imbalance.

All four reactor protection system

channels tripped. The unit event recorder failed immediately

prior to the trip.

October 2, 1991:

Reactor tripped from 73 percent power

following a turbine trip on a false generator lockout signal

caused by a loose electrical connector.

Unit 2

No automatic reactor trips occurred.

Unit 3

Five automatic and one manual reactor trip occurred:

November 13, 1990:

The operators manually tripped the reactor

from 100 percent prior to an automatic trip when all group

seven rods dropped into the core,

due to a faulty rod

programmer.

April 1, 1991:

Reactor tripped from 70 percent power during

power escalation due to spurious activated alarms on diverse

scram system channels 1 and 2.