ML15118A294

From kanterella
Jump to navigation Jump to search
Insp Repts 50-269/98-05,50-270/98-05 & 50-287/98-05 on 980322-0502.Violations Noted.Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support
ML15118A294
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 06/01/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A291 List:
References
50-269-98-05, 50-269-98-5, 50-270-98-05, 50-270-98-5, 50-287-98-05, 50-287-98-5, NUDOCS 9806160291
Download: ML15118A294 (32)


See also: IR 05000269/1998005

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269. 50-270, 50-287, 72-04

License Nos:

DPR-38. DPR-47, DPR-55, SNM-2503

Report No:

50-269/98-05, 50-270/98-05, 50-287/98-05

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station, Units 1, 2, and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

March 22 - May 2, 1998

Inspectors:

M. Scott, Senior Resident Inspector

S. Freeman. Resident Inspector

E. Christnot, Resident Inspector

D. Billings. Resident Inspector

M. Sykes, Resident Inspector, McGuire (Sections 08.3. E8.1)

T. Cooper. Resident Inspector. Crystal River (Sections 07.1.

F8.2)

E. Lea. Project Engineer (Sections 08.1, 08.2. E8.2)

D. Forbes, Regional Inspector (Sections R1.1, R1.2, R2.1.

R5.1, R8.1, R8.2)

H. Whitener, Regional Inspector (Portions of Section M1.1)

J. Blake. Regional Inspector (Sections M1.2. M1.3)

P. Kellogg, Regional Inspector (Section E8.3)

Approved by:

C. Ogle, Chief. Projects Branch 1

Division of Reactor Projects

Enclosure 2

9806160291 980601

PDR ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2, and 3

NRC Inspection Report 50.-269/98-05,

50-270/98-05, and 50-287/98-05

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection, as well as the results of announced inspections

by five region based inspectors. [Applicable template codes and the

assessment for items inspected are provided below.]

Operations

The licensee properly completed the operations and maintenance spent

fuel pool procedural enhancements listed in the Oconee probability and

public risk analysis of December 4, 1996. (Section 03.1, [1C, 2B

Adequate])

Refueling activities on Unit 2 were completed in a professional and

conservative manner. Locating the defueling/refueling administrative

and fuel tracking activities in a separate area adjacent to the control

room was seen as a positive. (Section 04.1, [1A - Good])

The inspectors identified a corrective action violation regarding lack

of quality assurance review of engineering instructions for minor and

temporary modifications. The licensee had identified this low level

problem approximately two years earlier but instances of lack of review

ave continued. (Section 07.1, [SC - Poor])

The corrective actions implemented for the failure to have a procedure

for reactor building closeout were adequate. (Section 08.1. [SC

Adequate])

The corrective actions implemented for the failure to make a timely

notification in accordance with Title 10, Code of Federal Regulations,

Part 50.72 following a reactor trip on March 16. 1996. were adequate.

(Section 08.2, [5C - Adequate])

The addition of operations procedural guidance to verify that fuel

assemblies were properly positioned, the fuel bridge mast was properly

secured, and spent fuel pool water level was maintained at least eight

feet above the fuel storage racks was considered adequate to resolve the

issue of previous occurrences of inadequate procedure control over spent

fuel movement. (Section 08.3. [5C - Adequate])

Retraction of the four-hour notification for the Keowee Unit 1

unanticipated start of April 9, 1998, was appropriate. (Section E2.1,

[lB - Adequate])

The licensee used conservative judgement in declaring Keowee Unit 2

inoperable in response to the April 20, 1998, failure to synchronize due

to the speed adjustment motor. During this normal start for commercial

power generation, an unknown condition was properly addressed with the

operability determination. (Section E2.1, [1A - Adequate])

(II0

2

Maintenance

.Pump,

engine, and valve on-line maintenance was generally completed in a

thorough and professional manner. Personnel were knowledgeable of the

assigned tasks and demonstrated attention to detail.

Procedures were

detailed and actively used on the job. Data was recorded as the steps

were performed and compared to the acceptance criteria. Pre-job

briefings were thorough and communication between test personnel was

good. Work performance during these activities demonstrated that

maintenance processes were positively in place. (Section M1.1, [2B. 3A,

3B - Good])

The licensee properly completed a commitment to adjust the automatic

voltage regulator for the main generators. These corrective actions

were considered adequate resolution of the problem that previously

resulted in a Unit 2 reactor trip. (Section M1.1, [5C - Adequate])

The licensee's augmented inservice inspection programs for the high

pressure injection connections to the reactor coolant system cold legs

ave been improved since the.piping failure in the Spring of 1997.

(Section M1.2, [2B - Adequate])

Inspection and testing of the Unit 2 once through steam generators were

being conducted in a thorough and conservative manner. Unexpected

findings were thoroughly evaluated for significance and potential impact

on the operating units. (Section M1.3. [2B - Good])

The inspectors concluded that the Unit 2 emergency power switching logic

test was successfully performed. This was indicative of adequate y

maintained equipment. (Section M1.4, [2A, 2B - Adequate])

Engineering

A more thorough pre-test review of the quality and completeness of the

procedure for the Unit 2 emergency power switching logic test could have'

precluded some of the minor discrepancies observed during the test and

was considered a weakness. (Section M1.4, [3C - Poor])

The technical resolution of the failure of the Keowee Unit 2 speed

adjustment motor on April 20, 1998, was adequate. (Section E2.1. [5C

Adequate])

The inspectors concluded that the failure of the speed adjustment motor

on April 20, 1998, did not affect the safety function of Keowee Unit 2

but did reflect poorly on the material condition of the speed adjustment

motor. (Section E2.1, [2A, Poor])

Good engineering support was provided and good troubleshooting methods

were used on the speed adjustment motor in response to the April 20.

1998, failure of Keowee Hydro Unit 2 to synchronize. (Section E2.1,

[4B - Good])

The performance of the licensee's failure investigation process team

concerning the Keowee Unit 1 overcurrent and undervoltage disturbance of

April 26, 1998, was excellent. (Section E2.1, [5B. 5C - Excellent])

3

@

0

Changes to low pressure service water system design basis to allow for

use of industry and Nuclear Regulatory Commission guidance concerning

vulnerable target area and probability of impact of a turbine missiles

was considered appropriate. The licensee's effort to understand their

design was adequate. (Section E8.1, [4A - Adequate])

The accountable engineer (individual performing modification) failed to

list a snubber in the Technical Specification surveillance procedure

which caused a required inspection to be missed and resulted in a non

cited violation. (Section E8.2, [3A - Poor])

The licensee's identification of a missed surveillance following a

snubber installation was adequate. (Section E8.2, [5A - Adequate])

Corrective actions identified by the licensee in response to a missed

snubber surveillance test were adequate to provide reasonable assurance

of not missing TS required inspection when new snubbers are installed.

(Section E8.2, [5C - Adequate])

The inspector noted that the siphon seal water, emergency condenser

circulating water, and essential siphon vacuum system test procedures

were well written and required no changes. Only a few enhancements were

identified during the conduct of the procedures. (Section E8.3. [2B

Excellent])

The inspector attended the pre-job briefing for several of the seal

water, emergency condenser circulating water, and essential siphon

vacuum system tests and noted that the briefings were thorough.

(Section E8.3. [3A, 3B - Good])

Good control of the testing evolutions was demonstrated by the test

coordinators. (Section E8.3, [lA - Good])

Plant Support

The inspectors determined the licensee was effectively maintaining

controls for personnel monitoring, control of-radioactive material,

radiological postings, radiation area controls, and high radiation area

controls as required by 10 CFR Part 20. Efforts to reduce personnel

contaminations was positive. (Section R1.1, [IC - Good])

Based on licensee planning efforts to reduce source term and the

licensee's efforts to achieve established exposure goals which were

challenging, the inspectors determined the licensee's programs for

controlling exposures as low as reasonably achievable were effective.

All personnel exposures to date in 1998 were below regulatory limits.

(Section R1.2, [1C - Adequate])

Review of breathing air testing records verified that the licensee was

calibrating breathing air compressor equipment and sampling in-use

breathing air systems for certification in accordance with procedural

requirements. For the tests reviewed, breathing air met Grade D or

better quality requirements. Survey instrumentation had been adequately

maintained. (Section R2.1, [2A - Adequate])

4

The respiratory protection program was being implemented as required by

10 CFR Part 20 Subpart H. (Section R2.1. [1C - Adequate])

The inspectors concluded that the check sources identified by the

inspectors were exempt sources and were controlled appropriately.

(Section R4.1, [IC - Adequate])

Personal frisking practices in the Interim Radwaste Facility were

acceptable. (Section R4.1, [3B - Adequate])

Chemistry personnel were knowledgeable and competent during collection

of a reactor coolant system sample. (Section R4.1, [3A, 3B - Adequate])

Based on the training activities reviewed and interviews, the inspectors

determined the radiation protection technicians had been provided an

adequate level of training to perform routine survey activities

involving radiation and control of radioactive material.

(Section R5.1,

[3B - Adequate])

The proposed change to the Updated Final Safety Analysis Reports for

additional requirements for performing radioactive work in the reactor

coolant pump and ice blast buildings was considered appropriate.

(Section R8.1, [1C - Adequate])

The inspectors identified a configuration control and design violation

for improper bend radius in two locations on the Unit 2 vent radiation

monitors.

(Section R8.2. [2A - Poor])

The failure to include instructions for an electrical damage check of

breakers in the procedure for operational guidelines following a fire

resulted in a non-cited violation. The failure could prevent alignment

of the low pressure injection system following a fire. (Section F8.1.

[1C - Poor])

The licensee's identification and resolution of. deficiencies in

operational guidelines following a fire were adequate. (Section F8.1,

[5A.5C - Adequate])

Due to improper assumptions regarding pressure downstream of the reactor

coolant pump seals, reactor coolant system leakage during a scenario

identified for Title 10, Code of Federal Regulations, Part 50.. Appendix

R, could have exceeded design limits for the reactor coolant makeup

system and resulted in a non-cited violation. (Section F8.2, [1C, 4A

Poor])

The licensee's identification and resolution of a procedure problem

involving excessive reactor coolant pump seal leakage. following a fire

was adequate. (Section F8.2, [5A, SC - Adequate])

Report Details

Summary of Plant Status

Unit 1 began and ended the period at 100 percent power.

Unit 2 began and ended the period in a scheduled refueling outage. Major

outage work completed included the replacement of the 2A1 and 2B1 reactor

coolant pumps and low pressure service water modifications.

Unit 3 began and ended the period at 100 percent power.

Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure (IP)

71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below.

02

Operational Status of Facilities and Equipment

02.1 Operations Clearances (71707)

The inspectors reviewed portions of the following clearances and Block

Tag Outs (BTO) during the inspection period:

2-98-0646

BTO 5

Condenser Circulating Water

(CCW)

2-98-1158

TN/2/A/2932/00

CCW/Siphon Seal Water (SSW)

2-98-0868

BTO 17

Building Spray

The inspectors observed that the clearances were properly prepared and

authorized and that the tagged components were in the required positions

with the appropriate tags in place.

02.2 Engineered Safety Features System Walkdown (71707)

The inspectors performed a walkdown of accessible portions of the

following systems:

Unit 1 Emergency Feedwater System

Unit 2 Emergency Feedwater System

2

.0

Unit 2 Essential Siphon Vacuum System

Unit 2 Siphon Seal Water System

Unit 3 East.Penetration Room Containment Isolation Valves

No discrepancies or concerns were identified.

03

Operations Procedures and Documentation

03.1 Spent Fuel Pool Procedural Controls

a. Inspection Scope (71707)

The inspectors independently reviewed the implementation of spent fuel

pool procedural enhancements as part of the Oconee probability and

public risk analysis of December 4, 1996.

b. Observations and Findings

The licensee committed to the following enhancements:

Change Procedures OP/1.2,3/A/1102/15. Filling and Draining Fuel

Transfer Canal, to provide explicit steps to close the fuel

transfer canal deep end drains and fill the deep end with one foot

of water before removing fuel transfer tube flanges:

Change Procedure MP/0/A/1405/001, Fuel Transfer Tube Cover Plate

Installation and Removal, to require verification that water is

standing in the fuel transfer canal deep end, the deep end drains

are closed, and fuel transfer tube isolation valves SF-1 and SF-2

are closed using a remote camera before removing fuel transfer

tube flanges: and

Add steps to procedures for spent fuel pool draindown sequences

involving standby shutdown facility (SSF) piping during normal

operation to direct operators to attempt to arrest the draindown

by closing SF-1 and SF-2.

The licensee implemented these enhancements as corrective actions under

Problem Investigation Process (PIP) Report 0-096-2656. The inspectors

determined that all changes were made as stated.

c. Conclusions

The licensee properly completed the spent fuel pool procedural

enhancements listed in the Oconee probability and public risk analysis

of December 4, 1996.

0III

3

04

Operator Knowledge and Performance

04.1 Unit 2 Refueling Activities

a. Inspection Scope (71707)

The inspectors observed portions of the defueling and refueling

activities for Unit 2.

b. Observations and Findings

The inspectors observed control room, spent fuel pool (SFP), and reactor

building (RB) activities by operations personnel. The activities were

conducted in a professional manner with emphasis on attention to detail,

conservative judgement, and timeliness. The inspectors observed that

operators in the control room were aware of the movement of each fuel

assembly by number and monitored appropriate nuclear instrumentation.

Management oversight of operations in the control room ensured focus was

maintained on the refueling and defueling activities. Outside

distractions were minimized by locating the refueling/defueling

activities to the shift supervisor's office whereas they had been

previously located in the control room.

The inspectors also reviewed tapes of the debris scan and core

verification scan. No items were identified for followup.

c. Conclusions.

Refueling activities on Unit 2 were completed in a professional and

conservative manner. Locating the defueling/refueling administrative

and fuel tracking activities in a separate area adjacent to the control

room was seen as a positive.

07

Quality Assurance in Operations

07.1 Review of Licensee Corrective Action Reports

a. Inspection Scope (40500)

The inspectors reviewed a number of licensee PIP reports in order to

identify potential issues and the licensee response to these issues.

b. Observations and Findings

PIP Report 4-098-1682, issued on April 1, 1998. identified that

engineering instructions in Minor Modification 11772, did not receive

Quality Assurance (QA) review prior to issuance. The detailed problem

description of the PIP report stated that this was a repetitive problem

that had been identified on several PIP reports over a two year period.

The inspectors reviewed these PIP reports and confirmed that three

temporary modifications and 12 minor modifications were identified where

the modification was installed without prior QA review of the

engineering instructions. The QA review was required for minor

modifications by Site Directive 2.2.1. Minor Modification Program, dated

July 11, 1996, and for temporary modifications by Site Directive 2.1.4,

4

Control of Temporary Modifications, dated March 30. 1995. Site

Directive 2.1.4 was changed February 2, 1998. However the revision

dated March 30, 1995, applied to al

temporary modifications covered by

the PIP reports listed elow.

The inspectors reviewed the problem evaluations sections for the PIP

reports referenced in PIP Report 4-098-1682 as follows:

PIP Report 0-096-0518 regarding temporary modifications, dated

March 14, 1996, stated the QA review requirement was overlooked.

A team meeting was held May 1. 1996, to review the PIP report.

PIP Report 0-096-2298 regarding minor modifications, dated

November 8, 1996, stated that because engineering instructions

were generic it was not the practice to route them for QA review

unless engineering felt it was necessary. No specific corrective

actions were documented for this PIP report.

PIP Report 3-096-2540 regarding minor modifications, dated

December 4, 1996, stated the missed review was an unintentional

oversight. Training was planned to be conducted but no corrective

actions were documented for this PIP report.

PIP Report 1-097-1747 regarding temporary modifications, dated

June 10. .1997, stated the responsible engineer did not follow

procedure. As corrective action the responsible engineer reviewed

the procedure.

PIP Report 2-097-1580 regarding minor modifications, dated May 20,

1997, acknowledged the failure to follow procedure. As corrective

action a team meeting was held on June 1.8. 1997, to remind all

minor modification preparers that QA personnel must be given the

opportunity to review engineering instructions.

PIP Report 3-097-1614 regarding minor modifications, dated May 26.

1997, stated that the accountable engineer understood that QA .

personnel did not need or want to review engineering instructions

if all work was governed by approved station instructions. The

engineer was counseled and discussed the PIP report with QA

personnel.

PIP Report 1-097-4061 regarding minor modifications, dated

November 13, 1997, stated that the apparent cause was human

erformance. but the problem was resolved as addressed in PIP

Reports 0-096-2298 and 3-096-2540.

PIP Report 1-097-4125 regarding minor modifications, dated

November 18, 1997, stated that the QA engineer was contacted at

home but was not aware of the requirement for QA to review

engineering instructions. No specific corrective actions were

documented for this PIP report.

PIP Report 1-97-4132 regarding minor modifications, dated November

19. 1997, stated the engineering instructions were not specific

instructions but a guideline. The PIP report was discussed at a

5

team meeting on January 8, 1998.

PIP Report 1-098-0054 regarding minor modifications, dated January

7, 1998, referred to PIP Report 1-97-4132 for cause, resolution,

and corrective actions.

PIP Report 0-098-0470 regarding minor modifications, dated

February 1, 1998. was not yet evaluated as of the end of the

inspection period.

The inspectors determined minor and temporary modifications continued to

be issued without the opportunity for QA personnel to review engineering

instructions. The low level problem continued even though it was

identified numerous times since 1996, and there have been several team

meetings and counseling sessions to correct the problem.

The

inspectors determined this constituted a failure to correct a condition

adverse to quality and was a violation of 10 CFR 50, Appendix B,

Criterion XVI. Given that the licensee had opportunities to correct

this problem as a result.of several findings over the previous two

years, this issue will not be subject to discretion. This is identified

as violation (VIO) 50-269,270,287/98-05-01: Inadequate Corrective

Actions for Recurring Problems With Engineering Instructions for Minor

and Temporary Modifications.

c. Conclusions

The inspectors identified a corrective action violation regarding lack

of quality assurance review of engineering instructions for minor and

temporary modifications. The licensee had identified this low level

problem approximately two years earlier but instances of lack of review

have continued.

08

Miscellaneous Operations Issues (92901)

08.1

(Closed) VIO 50-269,270,287/96-20-04: Failure to Have RB Material

Condition Closeout Procedure

This violation identified the failure of the licensee to have a

procedure for RB closeout as required by 10 CFR 50, Appendix B,

Criterion V. The inspectors reviewed the licensee's response to the

violation, in letters submitted to the NRC dated April. 9, 1996, and

October 23, 1997. The inspectors also reviewed PIP Report 0-097-1038,

which the licensee initiated to track the finding identified in the

Notice of Violation (NOV) and the corrective actions identified as a

result of the NOV. The inspectors determined that the corrective

actions were adequate. The inspectors reviewed associated documentation

and verified that the corrective actions identified by the licensee had

been implemented. Based on the completed implementation of the

correction actions, this violation is closed.

08.2 (Closed) VIO 50-269,270.287/96-05-01: Failure to Make Proper 10 CFR

50.72 Notification

This violation documented the failure of the licensee to make a 10 CFR

50.72 notification within the required time period, following a reactor

6

trip on March 16, 1996. The inspectors reviewed the licensee response

to the NOV, and PIP Report 3-096-0536, which the licensee initiated to

track the NOV, and associated documentation. The inspectors reviewed

the corrective actions identified in the PIP. The corrective action

included revisions to selected site procedure and additional training to

selected site personnel. The inspectors verified that the corrective

actions identified in the PIP had been completed. The inspectors

concluded that the licensee's implementation of the corrective action

adequately addressed the concerns associated with the violation. This

violation is closed.

08.3 (Closed) VIO 50-269,270.287/E96-19-01013: Inadequate Procedure Control

Over Movement of Spent Fuel

The inspectors performed followup inspection of licensee corrective

actions to address the failure to provide adequate procedures for fuel

handling activities. The inspectors reviewed revised fuel handling

procedures for activities within the RB, spent fuel building and the

interim spent fuel storage installation. During the review, the

inspectors confirmed that the licensee had incorporated specific

instructions to verify that fuel assemblies were properly positioned in

acceptable storage locations and the fuel bridge mast was properly

secured. The licensee also incorporated procedural guidance to inform

control room operators of fuel handling evolutions in progress and to

provide notifications when these activities were completed or suspended.

In accordance with a commitment made during the February 21, 1996, pre

decisional enforcement conference, the licensee performed a Self

Initiated Technical Audit (SITA) to evaluate and review plant design

basis and fuel handling activities. As a result of the SITA, the

licensee indicated their intention to provide additional guidance to

operators to ensure spent fuel pool water level is maintained at least

eight feet above the top of the irradiated fuel storage racks to have

adequate shielding during SSF events. This was verified to be

implemented in procedures.. The inspectors concluded that the licensee's

implementation of these corrective actions adequately addressed the

concerns associated with the violation. This violation is closed.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707. 61726)

The inspectors.observed all or portions of the following maintenance

activities:

TT/2/A/0750/017

Recovery of Jammed Control Rod Handling Tool,

Revision 0

MP/0/A/1500/009

Fuel Handling Operations, Revision 15

7

PT/0/A/0400/004

Standby Shutdown Facility (SSF) Diesel Engine

Service Water Pump Test. Revision 16

CP/1/A/2002/04D

Test Procedure for Operation of Post Accident

Liquid Sample System. Revision 25

PT/0/A/0750/11

Defueling/Refueling Activities Enclosure 13.1

Fuel Movement Verification Form Core Offload

Sequence. Revision 14

OP/2/A/1106/006

Turbine Driven Emergency Feedwater Pump

Overspeed Test, Revision 78

PT/2/A/0610/001J Emergency Power Switching Test, Revision 18

PT/3/A/0204/007

Reactor Building Spray Pump Test. Revision 50

PT/1/A/0251/003

Concentrated Boric Acid Transfer Pump Test,

Revision 35

PT/3/A/0152/016

Purge System Valve Stroke Test, Revision 1

PT/1/A/0400/007

SSF Reactor Coolant (RC) Make Up Pump Test,

Revision 25

PT/0/A/0400/004

SSF Diesel Engine Service Water Pump Test,

Revision 16

WO 96030944-01

2CCW-14 Repair Seat Leak on Valve

WO 98020989-01

Repair V, Inch Hole in TDEFW Pipe

WO 98010010-01

Repack Unit 2 TDEFW Pump

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and thorough. All work observed-was performed with the

work package present and in use. Technicians were experienced and

knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

The inspectors documented in NRC Inspection Report (IR)

50

269,270.287/97-10. a trip of the Unit 2 reactor, from 100 percent power,

due to the automatic voltage regulator control network not being

properly adjusted. The IR also documented the adjustment of the Unit 2

automatic regulator. The licensee committed to adjusting the Unit 1 and

Unit 3 automatic regulators. The Unit 3 regulator was adjusted during a

forced outage and performed adequately. The Unit 1 regulator was

adjusted during the most recent refueling outage. The regulator

performed adequately during the post refueling runback and power

escalation testing. These actions completed the commitment.

8

c.

Conclusion

The inspectors concluded that the maintenance activities listed above

were completed thoroughly and professionally.

On-line maintenance and surveillance activities involving the 3B reactor

building spray pump, the concentrated boric acid storage tank transfer

pump, the standby shutdown facility diesel engine service water pump,

the standby shutdown facility reactor coolant make-up pump, and valves

in the purge system were generally completed in a thorough and

professional manner. Personnel were knowledgeable of the assigned tasks

and demonstrated attention to detail.

Procedures were detailed and

actively used on the job. Data was recorded as the steps were performed

and compared to the acceptance criteria. Pre-job briefings were

thorough and communication between test personnel were good. Licensee

performance during these evolutions was good.

The licensee properly completed a commitment to adjust the automatic

voltage regulator for the main generators. These corrective actions

were considered adequate resolution of the problem that previously

resulted in a Unit 2 reactor trip.

M1.2 Augmented Inservice Inspection (ISI)

a. Inspection Scope (73753)

The inspector reviewed data from augmented ISI of the high pressure

injection (HPI) connections to the main loop cold legs.

b. Observations and Findings

The licensee radiographed the HPI nozzle connections to the main loop

cold legs to verify that required thermal sleeves were still located

properly. Thermal sleeves were provided to protect the pressure

boundary piping from thermal stresses when relatively cold water is

injected into the operating system.

The inspectors reviewed the radiographs taken-during the current outage,

and compared them with the radiographs taken during the Spring 1997

outage. The comparison showed that there had been no measurable

movement of the thermal sleeves.

The inspectors reviewed ultrasonic test (UT) data from inspection of the

HPI piping and safe-end connections to the nozzle connections. The

inspectors also reviewed the licensee's plans for the UT inspection of

the inner radius of the nozzle connection to the main loop cold legs.

To provide meaningful inspection results, the planned inspections

required the use of a calibration block with cracks rather than notches

as the reference standard.

Receipt of the calibration block was

scheduled for the week of April 12, 1998.

c. Conclusions

The licensee's augmented inservice inspection programs for the high

pressure injection connections to the main loop have been improved since

9

the piping failure in the Spring of 1997.

M1.3 Once Through Steam Generator (OTSG) Inspections

a. Inspection Scope (50002)

The inspector reviewed OTSG-inspection procedures and observed Unit 2

OTSG inspection activities.

b. Observations and Findings

The eddy current inspection of the Unit 2 OTSGs included 100 percent

bobbin coil inspection of the inservice tubes. During the bobbin coil

inspection of the 2A OTSG, the licensee discovered five tubes which had

been improperly installed during the manufacture of the OTSG. The five

tubes involved were installed at locations R21-C28, R21-C29, R22-C30.

R22-C31, and R23-C31. The tubes were installed such that they were in

one location in the lower tubesheet (LTS) and then crossed over to an

adjacent location in the upper tubesheet (UTS). The tube from location

R21-C28 in the LTS crossed to location R22-C30 in the UTS: LTS R22-C30

crossed to UTS R23-C31: LTS R23-C31 crossed to UTS R22-C31: LTS R22-C31

crossed to UTS R21-C29: and finally LTS R21-C29 crossed to UTS R21-C28.

The "twisted-tube" problem was discovered because two of the tubes were

supposed to have been plugged during the Unit 2. End of Cycle-15 (EOC

15) outage: in fact they were only plugged at the LTS. Full-length

bobbin coil eddy current examinations have historically been conducted

from the lower tubesheet of the OTSGs. As a result of eddy current

examinations in EOC-15; tubes R21-C28 and R23-C31 (as indexed from the

lower tubesheet) were found to have rejectable indications and were

plugged. (That is,

locations R21-C28 and R23-C31 on both tubesheets

were plugged.)

During EOC-16 attempts to eddy current inspect locations

R21-C29 and R22-C30, obstructions were noted which turned out to be the

plugs which had been installed at UTS locations R21-C28 and R23-C31.

he licensee generated PIP 2-098-1617 to document the problem,

corrective actions, and potential impact on the operating Units 1 and 3.

The OTSG is a vertical, straight tube heat exchanger. With this design,

the tube locations should match in the upper and lower tubesheets. The

presumption that these tube locations are as designed is the basis by

which all tube inspections and repairs are accomplished. Tube plugging

requires positive identification of the tube by its location in each

tubesheet; because of the design, there is not a requirement that the

tube be verified to be the same tube "hole" in each tubesheet.

To determine the scope of the manufacturing problem, the licensee used

eddy current equipment located on both upper and lower tubesheets to

verify that the remainder of the tubes were at the same tube locations

in both tubesheets. When it was determined that the set of five

"twisted" tubes were unique in the 2A OTSG. the licensee elected to

remove all five tubes from service by plugging.

The licensee conducted in-situ pressure testing of ten tubes from the 2A

OTSG during the EOC-16. The tubes were subjected to test pressures of

1450 pounds per square inch (psi). 2900 psi, and 4300 psi, representing

10

normal operating differential pressure, main steam line break

differential pressure, and Regulatory Guide 1.121 Structural Limit

Pressure, respectively. Tubes tested were as follows:

Tube

Defect Type

Location

Comments

R6-C10

Axial

9th-10th

R20-C28

Mixed

UTE-UTS

Leaker found during bubble

test

R22-C30

Axial

14th-UTS

Mispositioned R21-C28 Lower

R22-C31

Axial

14th-UTS

Mispositioned R23-C31 Lower

R26-C3

Volumetric

2nd-3rd

R32-C2

Axial

12th-13th

R46-C21

Axial

10th-11th

R73-C17

Axial

15th-UTS

R145-C35

Axial

12th-14th

R150-C19

Axial

15th-UTS

The inspectors witnessed the in-situ pressure testing of tubes R22-C30

and R22-C31, which had been left in service with only the LTS plugged.

Both of these tubes successfully passed pressure testing at 1450 psi

(operating differential pressure) and 2900 psi (main steam line break

pressure). Tube R22-C30 passed the Reg. Guide 1.121 structural limit

pressure test at 4300 psi, but R22-C31 developed a through-wall leak at

about 4200 psi.

(The leak was determined to be through an axial

indication just below the UTS.)

The fact that the two defective.tubes,

left in service with only one end plugged, passed the main steam line

break differential pressure test provided assurance that these tubes

should have maintained leak integrity during accident conditions during

the past operating cycle.

The inspectors also reviewed the licensee's justification for continued

operation of Units 1 and 3' considering the potential for having rotated

tube groups similar to the one found in the 2A OTSG. After reviewing

the calcul ations, which included stresses expected if the rotation

occurred between the two closest spaced support plates, and having

witnessed the pressure testing of the 2A OTSG degraded tubes, the

inspectors agreed that there should be'no concern that would require

shutdown and inspection of either of the units prior to the next

scheduled refueling.

c. Conclusions

Inspection and testing of the Unit 2 once through steam generators were

being conducted in a thorough and conservative manner. Unexpected

11

findings were thoroughly evaluated for significance and potential impact

on the operating units.

M1.4 Emergency Power Switching Test

a. Inspection Scope (61726)

The inspectors observed, reviewed, and discussed the performance of the

18-month Technical Specifications (TS) required emergency power

switching test. The test was performed to verify that the main feeder

busses are energized by the most reliable source without operator

actions.

b. Observations and Findings

The test, Procedure PT/2/A/0610/01J, Emergency Power Switching Logic

Functional Test, Revision 18. consisted of manually tripping switchyard

breakers, manually initiating engineered safety channels, and disabling

selected relays. The relays were disabled to ensure that only the load

shed relays would actuate the breakers. During the conduct of the test

the inspectors observed several items which required on the spot

procedure changes and the issuance of test discrepancies. The test

-coordinator issued PIP Report 2-098-2393 to document and track

discrepancies. Among the items were the following:

Enclosure 13.1 required the undervoltage relays for the individual

4160 volt (V) switchgear breakers to be disabled prior to

performing the test, however. Section 12.4 required the same

undervoltage relays to be checked for proper operation following a

power transfer;

Section 8.19, referred to a mislabeled undervoltage relay on a

breaker for the SSF;

Section 12.5 directed the operators to manipulate a switch on the

wrong Engineered Safeguards (ES)

panel. and channel and:

Section 8.33 omitted several breakers from the lists for removal

of red breaker closed indicating bulbs and for verifying voltage

on opened links, and improperly -identified an open link.

The inspectors found from the reviews, observations, and discussions

that none of the changes or discrepancies had an impact on the success

of the test. The inspectors did find that these changes and

discrepancies could have been avoided if a more thorough pre-test

technical and administrative review had been performed.

c. Conclusions

The inspectors concluded that the Unit 2 emergency power switching logic

test was successfully performed. This was indicative of adequately

maintained equipment.

A more thorough pre-test review of the procedure for the Unit 2

emergency power switching logic test could have precluded some of the

12

minor discrepancies observed during the test and was considered a

weakness.

III. Engineering

E2

Engineering Support of Facilities and Equipment

E2.1 Keowee Activities

a. Inspection Scope (37551, 92903. 93702)

The inspectors reviewed drawings, observed activities, reviewed

procedures, and discussed with licensee personnel the circumstances

surrounding three different events affecting Keowee Hydro Units 1 and 2.

b. Observations and Findings

On April 9, 1998, Keowee Units 1 and 2 were operating to the grid

producing commercial power. Both units received an emergency start

signal and separated from the grid as designed. On April 20, 1998,

Keowee Unit 2 failed to synchronize to the grid during a normal start.

On April 26, 1998. with Keowee Unit 1 tied to the grid at 78 megawatts

--and Unit 2 in standby, an undervoltage and an overcurrent condition was

received by Unit 1. The over current condition lasted for one second

and the undervoltage condition lasted for 13 seconds.

The emergency start on April 9. 1998, was caused by an inadvertent start

signal from Oconee Unit 2, which was in refueling outage. Maintenance

activity of wire tracing was being performed in the Keowee Emergency

Start Channel A cabinet in the Oconee Unit 2 cable room. A four hour

non-emergency notification was made to the NRC based on the possibility

that the start was triggered by an Engineered Safeguards Features (ESF)

module. The maintenance activities required the door to the cabinet to

be open. The event occurred when the cabinet and/or relay was bumped.

The licensee initiated PIP K-098-1854 to troubleshoot and attempt to

determine the root cause of the actuation. Subsequently, licensee

personnel were able to duplicate the event, but were unable to pinpoint

the exact cause. Suspected modules were changed out and the licensee

will monitor the system. At the end of the inspection period, the

licensee retracted the notification but indicated that they may submit a

voluntary LER.

When Keowee Unit 2 failed to synchronize during a normal start on April

20, 1998, the licensee declared the unit inoperable and issued PIP

K-098-2061. During the inspectors' review of troubleshooting

activities, the licensee revealed that the speed adjustment motor for

the governor had failed. The cause of the failure was excessive carbon

dust, produced by motor brush operation, in the motor. The motor was

cleaned and the unit was returned to operable status. An inspector

review of the operating controls and schematic, a review of vendor

information on governor operation, and discussions with the licensee

indicated that the failure of the motor did not affect the safety

function of the unit. The motor adjusts the base speed of the unit

between 58 and 63 hertz and it is used to auto synchronize the unit to

the grid during normal start operation. The circuit used to synchronize

13

to the grid automatically is not required during a safety related

emergency start operation. The licensee was considering preventive

maintenance on the motors.

The licensee initiated a failure investigative process (FIP) team and

PIP K-098-2215, to review the April 26.'1998. overcurrent and

undervoltage condition on Keowee Unit 1. Based on the reviews,

observations, and discussions, the inspectors understood the following:

The Oconee Unit 2 control room operators closed a switchyard

breaker to backfeed the unit from the grid through it's main and

auxiliary transformers;

the Keowee operators observed an electrical disturbance and the

Keowee plant computer indicated a high current indication with a

low voltage condition;

the Keowee plant computer indicated that the high current

condition cleared within 1 second and the low voltage condition

lasted for approximately 13 seconds;

a review of the event recordings of such items as the switchyard

yellow buss voltage, the Oconee Units 1 and 3 generator outputs.

and the megavolts reactive (MVARs) indicated that a transient of

approximately 13 seconds occurred when the main and auxiliary

.transformers were brought on to the grid: and

the FIP team did not observe the presence of any phase to phase

detrimental harmonics, a check of the electrical condition of the

transformers indicated no deficiencies, and a review of historical

data indicated that low voltage conditions had occurred during

backfeed operations.

The inspectors found that the 13 second transient on the grid and on the

Oconee units corresponded to the 13 second Keowee low voltage condition.

The inspectors also found that the electrical disturbance observed by

the Keowee operators was a normal MVAR transient resulting from placing

the transformers, a large electrical load, on-to the grid. A review of

historical information indicated that in the past the transformers had

not been placed on to the grid with any of the Keowee units on line.

c. Conclusions

Retraction of the four hour notification for the Keowee Unit 1

unanticipated start of April 9', 1998. was appropriate.

The technical resolution of the failure of the Keowee Unit 2 speed

changer motor on April 20, 1998, was adequate. The inspectors concluded

that the failure of the speed adjustment motor on April 20, 1998. did

not affect the safety function of Keowee Unit 2 but did reflect poorly

on the material condition of the the speed adjustment motor. The

licensee used conservative judgement in declaring the unit inoperable

due to failure of the speed adjustment motor. Good engineering support

was provided and good troubleshooting methods were used on the speed

adjustment motor.

14

The performance of the licensee's failure investigative process team

concerning the Keowee Unit 1 overcurrent and undervoltage disturbance of

April 26, 1998, was excellent.

E8

Miscellaneous Engineering Issues (92903)

E8.1

(Closed) LER 50-269/97-05: Low Pressure Service Water System (LPSW)

Outside Design Basis for High Trajectory Turbine Missile

The circumstances surrounding this item have been previously discussed

in IR 50-269.270,287/97-02 and IR 50-269,270,287/97 -05. Enforcement

discretion for this issue was granted in the cover letter for IR 50

269,270,287/97-05 dated July 18, 1997.

The inspectors evaluated this LER describing operation of the Oconee

Units 1, 2, and 3 outside system design basis for high trajectory

turbine missiles. The inspectors verified that the installed system did

not conform to the design basis description. To correct the situation,

the licensee made changes to the UFSAR to revise the design basis

description for the system. The revision allowed use of industry and

NRC guidance concerning vulnerable target area and probability of impact

of a turbine missile without shielding or separation protection. The

.-

change was submitted for review and accepted by the staff. No

unreviewed safety questions were identified. The inspectors determined

that the revision to the design basis, approved by the staff in

correspondence dated May 16, 1997, was an adequate change to the plant

design and was confirmation that no other corrective actions were

necessary. Additionally, the licensee's effort to understand their

design was adequate. The inspectors also noted that operability of the

LPSW system was maintained. This LER is closed.

E8.2 (Closed) LER 50-269/96-05: Failure to Perform TS Required Inspection

This LER identified an issue in which the licensee failed to perform a

TS required inspection of snubber S/R# 1-03-401H. Specifically, the

licensee failed to perform an 18-month inspection of the snubber as

required by TS 4.18.1. Documentation reviewed indicated that following

a modification, implemented in January 1993, the accountable engineer

failed to ensure that the snubber had been entered into the TS

surveillance maintenance procedure. PIP 1-096-1497 provided corrective

actions to change procedures for engineering personnel to review

snubbers for TS applicability and to ensure proper testing. Following

the review of all associated documentation, the inspectors concluded

that the corrective actions identified by the licensee were adequate to

provide reasonable assurance of not missing TS required inspection when

new snubbers are installed. The inspectors also verified that each of

the corrective actions had been implemented.

The inspectors also concluded that the failure to perform the TS

required inspection was a violation. However, this non-repetitive,

licensee-identified and corrected violation is being treated as an Non

Cited Violation (NCV), consistent with Section VII.B.1 of the NRC.

Enforcement Policy. This is identified as NCV 50-269/98-05-02; Failure

to Perform Snubber Inspection as Required by TS.

15

E8.3 (Closed) Inspector Followup Item (IFI) 50-269.270.287/96-13-03: Testing

of the Modifications to the Low Pressure Service Water System.

The inspectors reviewed the following test procedures:

PT/2/A/0261/007 Revision 18. Emergency CCW System Flow Test

TT/0/A/0251/070 Revision 0, Siphon Seal Water Test

TT/2/A/0261/010 Revision 0, ECCW/ESV Integrated Post-Modification

Test

PT/2/A/0251/023 Revision 8, LPSW Flow Test

The above listed procedures were reviewed for precautions, limitations,

test acceptance criteria and contingency planning.

The inspectors

attended pre-job briefings for the procedures, and witnessed the

performance of portions of each test. The acceptance criteria for each

test was successfully met. The LPSW flow test demonstrated that the new

essential siphon vacuum (ESV) system could maintain the condenser

circulating water (CCW) system headers full of water with one operating

unit (Unit 1) and one shutdown unit (Unit 2) taking LPSW suction from

the unit 2 CCW crossover header in siphon flow.

The inspectors noted that the procedures were well written and required

no changes and only a few enhancements were identified during the

conduct of the procedures. The inspectors attended the pre-job briefing

for several of the procedures and observed that the briefings were

thorough. The briefings included the purpose of the testing, the

precautions and limitations, the general outline of the test, the test

acceptance criteria, and the contingency plans for terminating the test.

Personnel safety and self-checking were emphasized. The importance of

slow deliberate actions were emphasized and caution was stressed. The

inspectors also observed operations shift turnovers. These were

conducted in a very professional manner. The status of the testing was

discussed as well as.the expected results and changes in plant

configurations that would occur during the testing were addressed. The

test coordinators were very effective in conducting the testing and were

very familiar with the procedures. Good control of the testing

evolutions was demonstrated by the test coordinators observed.

This testing demonstrated the ability of the ESV system to maintain the

emergency condenser circulating water (ECCW) first and second siphon for

,a

period of at least eight hours. At the end of the LPSW flow test, the

headers were still full of water and thus were capable of providing

cooling water for the ECCW. These modifications and testing complete

the required actions for the closure of this item on Unit 2. The Unit 3

ESV system was scheduled to be completed during the Fall 1998 outage and

Unit 1 in the Spring 1999 outage. While the test acceptance criteria for

the ECCW/ESV integrated test was met, a review by the licensee's

engineering department identified that the air removal rate was less

than the design rate of the ESV system. Discussion with the float valve

manufacturer indicated that the float may be too light for the test

conditions experienced at the time of the test. The licensee was in the

0process

of modifying and testing different float weights to improve the

16

air removal rate. Based on the results of this testing the licensee was

planning to modify the Unit 2 installed float valves and to re-run the

ECCW/ESV integrated test.

The testing to be conducted on Units 3 and 1 is similar to the testing.

that has been completed on Unit 2. These tests will include a

hydrostatic test of the units piping to the CCW pumps and motors and ESV

tanks and pumps, a Siphon Seal Water (SSW) test to verify adequate SSW

flow to the unit pumps and motors, an ECCW system flow test to verify

the amount of air in leakage, an ECCWLESV integrated test to verify that

the ESV system can remove air from the ECCW siphon headers, and a LPSW

flow test to demonstrate the LPSW pumps can take a suction from the ECCW

siphon for an extended period of time. Successful completion of this

testing on each unit will be identified as IFI 50-269,287/98-05-03:

Units 1 and 3 Low Pressure Service Water Testing.

IV.

Plant Support Areas

R1

Radiological Protection and Chemistry Controls

R1.1 Tour of Radiological Protected Areas

a. Inspection Scope (83750)

The inspectors reviewed implementation of selected elements of the

licensee's radiation protection program as required by 10 CFR Parts

20.1201, 1501. 1502, 1601, 1703, 1802

1902, -and 1904. The review

included observation of radiological protection activities including

personnel monitoring controls, control of radioactive material,

radiological surveys and postings,. and radiation area and high radiation

area controls.

b. Observations and Findings

During tours of the turbine building, reactor building, auxiliary

building, and radioactive waste storage and handling facilities, the

inspectors reviewed survey data and performed'selected independent

radiation and contamination surveys to verify area postings and labeling

of radioactive material.

The inspectors also reviewed storage locations

for radioactive material and radioactive sources. Observations and

survey results determined the licensee was effectively controlling and

storing radioactive material.

However, the inspectors observed three

exempt quantity sources used for source checking instruments that were

not marked as radioactive material. The licensee returned these

unlabeled exempt quantity sources to labeled containers. These exempt

quantity sources are not subject to NRC regulations. The licensee

initiated a PIP to investigate the controls for these sources. Also,

the inspectors discussed the storage of some flammable radioactive

sources in storage lockers with other hazardous materials. The licensee

was in the process of obtaining a special locker for these sources. The

licensee initiated a PIP Report 0-098-1475. to review the controls for

storage and handling of radioactive sources.

17

  • During plant tours, the inspectors observed that extra high radiation

areas (locked high radiation areas) were locked as required by licensee

procedures. The inspectors reviewed key controls for extra high

radiation area and very high radiation area keys. The inspectors

inventoried key storage locations and all keys were accounted for at the

time of the inspection. The licensee had logged keys out to personnel

qualified to work in these areas and the key boxes were locked when not

in use as required by procedure to maintain control of the keys. Logs

reviewed determined the keys had been accounted for once a shift.

However, the inspectors found a means to bypass the lock on a desk that

contained a key to open the box that stored the extra high radiation

keys. The inspector discussed the potential for bypassing existing key

controls with licensee management. The licensee removed the key from

the desk drawer and initiated PIP Report 0-098-1471, to review the

controls for the desk drawer containing the key. The inspectors also

observed appropriate dosimetry controls for these areas were established

in radiation work permits (RWPs) as required by licensee procedures.

The licensee's records determined the licensee was maintaining

approximately 126,081 square feet (ft

2) of floor space as a

radiologically controlled area (RCA). Rpcords also determined the

licensee maintained approximately 559 ft' or less than 1 percent of the

-.RCA as contaminated during the week of the inspection.

The inspectors .reviewed personnel contamination event (PCE) reports

prepared by the licensee to track, trend, determine root cause, and any

necessary followup action. The licensee established a goal of 216 PCEs

for 1998. As of March 26, 1998, approximately 45 PCEs had occurred

during 1998 which included both particles and dispersed contamination

events for clothing and skin contaminations. Licensee efforts in 1998

to reduce personnel contaminations had been positive.

RWPs established for performing work were reviewed. These controls

included the use of RW Ps to be reviewed and understood by workers prior

to entering the RCA. The inspectors reviewed selected RWPs for adequacy

of the radiation protection (RP) requirements based on work scope,

location, and conditions. For the RWPs reviewed, the inspectors noted

that appropriate protective clothing, and dosimetry were required.

During tours of the plant, the inspectors observed the adherence of

plant workers to the RWP requirements.

c. Conclusions

Based on observations and procedural reviews, the inspectors determined

the licensee was effectively maintaining controls for personnel

monitoring, control of radioactive material, radiological postings,

radiation area controls, and high radiation area controls as required by

10 CFR Part 20. Efforts to reduce personnel contaminations were

positive

18

R1.2 Occupational Radiation Exposure Control Program

a. Inspection Scope (83750)

The inspectors reviewed the licensee's implementation of 10 CFR

20.1101(b) which requires that the licensee shall use, to the extent

practicable, procedures and engineering controls based upon sound RP

principles to achieve occupational doses and doses to members of the

public that are As Low As Reasonably Achievable (ALARA).

b. Observations and Findings

The inspectors interviewed licensee personnel and reviewed records of

ALARA program results and activities.

An effective Unit 2 chemical shutdown crudburst had resulted in reactor

building average dose rate reductions of approximately 1 millirem/hour.

Dose rates in the steam generator bowls were reduced by approximately

twenty-one percent. The licensee had established an annual exposure

projection for 1998 of approximately 292 person-rem or 97.3 person

rem/unit. The licensee established an exposure goal of 109 person-rem

for the current Unit 2 refueling outage. At the time of the inspection,

the licensee was tracking approximately 44 person-rem year to date which

was below year to date estimates of 64 person-rem. All personnel.

exposures to date in 1998 were below regulatory limits.

During tours of the facility, the inspectors observed RP technicians

controlling access to work areas to minimize personnel exposure and

briefing workers in the work areas as radiological conditions changed.

The inspectors also observed effective use of shielding, teledosimetry,

remote cameras and wireless communications systems for controlling

personnel exposures during maintenance evolutions.

The inspectors attended an ALARA committee meeting where the licensee

discussed responsibilities of the ALARA committee, current radiation

exposure status for the site, Unit 2 outage exposure-status and goals,

temporary and permanent shielding projects, and future ALARA

initiatives. The meeting was well managed and participation and

attendance by primary committee members was observed to be good.

c. Conclusions

Based on licensee planning efforts to reduce source term and the

licensee's efforts to achieve established exposure goals which were

challenging, the inspectors determined the licensee's programs for

controlling exposures ALARA were effective. All.personnel exposures to

date in 1998 were below regulatory limits.

19

R2

Status of RP&C Facilities and Equipment

R2.1 Breathing Air Testing and Ouality

a. Inspection Scope (83750)

Title 30 CFR 11.121 requires that compressed, gaseous breathing air meet

the applicable minimum grade requirements for Grade D or higher quality.

Title 10 CFR Part 20 Subpart H provides requirements for respiratory

protection programs. Title 10 CFR 20.1501 requires licensees ensure

instruments and equipment used for quantitative radiation measurements

are calibrated.

b. Observations and Findings

The inspectors reviewed and discussed with the licensee representatives

the program for testing and qualifying breathing air as Grade D. The

inspectors examined breathing air manifolds for physical integrity and

current calibration of gauges. In addition, the inspectors further

noted that the supplied air hoods and hoses available for use were

compatible per manufacturer's instructions as were air supplied

respirators and hoses. All respiratory protection equipment observed

during facility tours was being maintained in a satisfactory condition.

During facility tours, the inspectors noted that survey instrumentation

and continuous air monitors observed in use within the RCA were operable

and currently calibrated. The inspectors toured the instrument

calibration room and discussed the portable instrument program with

cognizant personnel. The inspectors determined the licensee had an

adequate number of survey instruments available for use during the

outage and the instruments were being calibrated and source checked as

required by licensee procedures.

c. Conclusions

Review of breathing air testing records verified that the licensee was

calibrating breathing air compressor equipment and sampling in-use

breathing air systems for certification in accordance with procedural

requirements. For the tests reviewed, breathing air met Grade D or

better quality requirements. The respiratory protection program was

being implemented as required by 10 CFR Part 20 Subpart H. Survey

instrumentation had been adequately maintained.

R4

Staff Knowledge and Performance in RP&C

R4.1 Observations of Source Control and Frisking Requirements

a. Inspection Scope (71750)

The inspectors toured radiological areas, interviewed personnel, and

reviewed licensee procedures in accordance with Inspection Procedure

71750 for sampling, personnel monitoring, and control of sources.

20

b. Observations and Findings

The inspectors located and reviewed requirements for the following

sources:

Two Cs-137 sources of approximately 8 microcuries located in the

shift RP area, used for background check sources, were found

attached to two clipboards;

The sources located in the body burden room were contained in a

locked cabinet. These sources were two Eu-152 sources of

approximately 3 microcuries, one old internal check source from a

Victorine 497 (a depleted Uranium source), and two CS-137 sources;

An Am-241 and a Cs-137 source were located in the respirator area

in a cardboard box'with yellow and magenta tape: and,

The source at the Independent Spent Fuel Storage Facility (ISFSI)

area was for frisker background check and was located in a

shielded lead lock box, the source was a depleted Uranium source

also from a Victorine 497.

The above listed sources were identified as exempt sources used for

instrument checks. No NRC requirements for exempt sources were

identified.

While touring the Interim Radwaste Storage Building the inspectors

observed that there was no personnel contamination monitor present. The

facility was part of the RCA and was posted as a radiation area. The

inspectors reviewed the frisking requirements for the facility and

determined that a whole body frisk was required upon exit. There was a

hand-held frisker available that could be used to perform a whole body

frisk. The inspectors later accompanied several RP and chemistry

personnel to the facility; all frisked properly upon leaving.

The inspectors observed a chemistry technician obtaining a reactor

coolant system (RCS) sample.

The technician-wore appropriate personnel

protective devices, observed applicable RP practices, stayed on station

during sample flush and collection, and took satisfactory safety

actions. The procedure was a reference use procedure and was taken to

the sample site. Operations was notified prior to starting to sample

the RCS as required by procedure. The sample sink hood sash was

maintained below the maximum height posted and the sample sink was

posted appropriately. The technician changed gloves frequently and

frisked upon completion of obtaining the sample. The inspectors.

verified that the sample rooms are normally unlocked spaces. The door

to the back of the sample sink is kept locked for contamination control

reasons but is not required to be locked.

c. Conclusions

The inspectors concluded that the check sources identified by the

inspectors were exempt sources and were controlled appropriately.

Personal frisking practices in

the Interim Radwaste Faci ity were

21

acceptable. Chemistry personnel were knowledgeable and competent during

collection of the RCS sample.

R5

Staff Training and Qualification

R5.1 RP Technician Training

a. Inspection Scope (83750)

Training of RP technicians was reviewed to determined whether the

technicians had been provided adequate training in procedures to

minimize radiation exposures and control radioactive material as

required by 10 CFR Part 19.12.

b. Observations and Findings

The inspectors discussed training requirements with training personnel.

reviewed lesson plans and reviewed qualification records for personnel

operating portable survey instruments and count room equipment. The

inspectors compared training records for qualified individuals to daily

and weekly survey records and determined personnel performing equipment

checks had been formally qualified to use the survey instruments. The

inspectors interviewed five personnel and discussed instrument

background checks, source checks, use of sample containers, and counting

procedures. The inspectors also discussed instrument calibration and

counting procedures with cognizant technical personnel. The inspectors

determined the licensee was following established procedures for the use

of counting equipment. During facility tours, the inspectors observed

work practices to determine the effectiveness of surv

activities

involving radiation and control of radioactive materia

c. Conclusions

Based on the training activities reviewed and interviews, the inspectors

determined the radiation protection technicians had been provided an

adequate level of training to perform routine survey activities

involving radiation and control of radioactive material.

R8

Miscellaneous RP&C Issues

R8.1 (Closed) Unresolved Item (URI) 50-269,270,287/97-15-03: Determine the

Applicability of Monitoring Requirements of Criterion 64 of 10 CFR 50

Appendix A and Reporting Requirements of 40 CFR 190 and 10 CFR 50.36a

Regarding Potential of Unmonitored Release Pathways

During tours of the auxiliary building and radioactive waste

storage/handling facilities the week of October 27-31, 1997. the

inspectors observed the licensee had performed radiological work in two

onsite buildings, the reactor coolant pump building and the ice blast

building, not specified as monitored pathways for radioactive material

in the licensee s Offsite Dose Calculation Manual.

The licensee's

review of this issue confirmed only work involving low levels of

radioactive material had been performed in the buildings. The licensee

proposed a change to the UFSAR to provide additional requirements for

the buildings when performing radioactive work. The inspectors reviewed

22

what the licensee did regarding this issue and this issue is closed.

R8.2 (Closed) URI 50-270/98-02-13: Unit 2 Monitor Inlet Sample Tubing Bend

Radius Not as Described by Design Drawings

The inspectors identified on February 11, 1998, the Unit 2 vent RIA

monitor inlet sample tubing for RIA's 43 and 44 did not alppear to have

the correct bend radius in two locations as specified on licensee

configuration control and design drawings number(s) 0-440A, Revision 37

and 0-440B Revision 38, Auxiliary Building Piping Layout Plan. This

concern was addressed as URI 50-270/98-02-13. The licensee initiated a

PIP regarding this item, confirmed the tubing did not have the correct

bend radius, and modified the tubing bend radius as specified on

licensee configuration and design drawings.

10 CFR Part 50. Appendix B, Criterion V. requires that activities

affecting quality shall be prescribed by documented instructions,

procedures, or drawings, of a type appropriate to the circumstances, and

shall be accomplished in accordance with these instructions, procedures,

or drawings. Duke Energy Corporation Topical Report Quality Assurance

Program states Duke Energy Corporation conforms to applicable regulatory

requirements such as 10 CFR 50, Appendix B.

This URI is being upgraded into a violation and is identified as VIO 50

270/98-05-04: Inadequate Configuration Control of Unit 2 RIAs-43 and 44

Particulate and.Iodine Sample Tubing.

F8

Miscellaneous Fire Protection Issues

F8.1 (Closed) LER 50-269/98-007-00: Potential Operation Outside Design Basis

for Appendix R Fire Due to an Inadequate Procedure

The circumstances described in this LER were documented in NRC IR 50

269,270,287/98-02. Affected procedures for LP-1. LP-2, CF-1, and CF-2

were placed on hold pending completion of revisions to incorporate

provisions to prevent closing the breakers during post Appendix R fire

damage assessments. The licensee also plans to develop appropriate

circuit validation process for use during post Appendix R assessments.

The failure to have an adequate procedure for operation of the valves

following a fire is contrary to the requirements of Appendix R. The

inspectors concluded that the licensees' identification and resolution

of this issue were adequate. This non-repetitive, licensee-identified,

and corrected violation is being treated as a NCV consistent with

Section VII.B.1 of the NRC-Enforcement Policy. This is identified as

NCV 50-269,270,287/98-05-05: Inadequate Appendix R Procedure.

F8.2 (Closed) LER 50-269/96-03: Reactor Coolant (RC) Makeup System

Technically Inoperable for Appendix R Scenario Due to Design Analysis

On February 5, 1996, the licensee identified that an evaluation

completed in 1987 had assumptions on Reactor Coolant Pump (RCP) seal

lea kage that did not agree with the assumptions that the licensee was

including in plant procedures. The licensee evaluated the situation and

concluded that when the current RCP seal leakage limits were applied to

an Appendix R scenario, the RC system leakage could have exceeded the

23

reactor coolant makeup system design limits. If an Appendix R fire

caused valve 1HP-276 to spuriously open, the back pressure downstream of

the RCP seals could decrease below the vapor pressure of the liquid

assing through the seal, resulting in two phase flow across the seal.

This could cause, degradation of the seal, possibly resulting in failure

and leakage in excess of design makeup flow.

The licensee took the immediate action of closing 1HP-276 and opening

the breaker to the motor .operator for the valve. The inspector verified

that subsequently, the licensee revised procedures OP/1/A/1104/02, HPI

System, OP/1/A/1102/01, Controlling Procedure for Startup,

PT/1/A/1103/06, Reactor Coolant Pump Operation, and OP/1/A/1102/10,

Controlling Procedure for Shutdown, to assure that when RCS temperature

was greater than 250 degrees F, 1HP-276 would be closed with its breaker

open. The breaker for 1HP-276 was labeled with a warning that closing

the breaker with RCS temperature greater than 250 degrees F was in

violation of the Appendix R requirements. The licensee's identification

and resolution of this issue were adequate. This non-repetitive,

licensee-identified, and corrected violation is being treated as a NCV

consistent with Section VII.B.1 of the NRC Enforcement Policy. This is

identified as NCV 50-269/98-05-06: Reactor Coolant Makeup System

Inoperable for Appendix R Scenario.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors resented the inspection results to members of licensee

management at te conclusion of the inspection on May 6, 1998. The

licensee acknowledged the findings presented. No proprietary

information was identified to the inspectors.

X2

Management Oversight Group Meeting

On April 22, 1998, the NRC Oconee Management Oversight Group met with

Oconee Site Management to discuss trends in licensee performance. This

was the first of the scheduled meetings. Meetings will be scheduled on

an approximate bimonthly agenda.

X3

NRC License Renewal Team Meeting

On April 29, 1998, the NRC met with licensee management to discuss

information and responses for the Oconee reactor building license

renewal evaluation. This meeting was open to the public. This meeting

was to gather information and therefore no specific findings were

identified.

X4

NRC Management Meetings

On April 22, 1998, Mr. Samuel J. Collins, Director of the Office of

Nuclear Reactor Regulation and Mr. Luis Reyes, Regional Administrator.

Region II,

were at the site to tour the facility and meet with licensee

personnel.

24

Partial List of Persons Contacted

Licensee

L. Azzerello, Mechanical Systems Engineering Manager

E. Burchfield. Regulatory Compliance Manager

T. Coutu, Nuclear Section Manager, Valves

T. Curtis, Operations Superintendent

W. Foster, Safety Assurance Manager

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Engineering Manager

W. McCollum, Vice President, Oconee Site

M. Nazar, Manager of Engineering

J. Forbes, Station Manager

J. Smith, Regulatory Compliance

J. Twiggs, Manager, Radiation Protection

Other licensee employees contacted during the inspection included technicians,

maintenance personnel, and administrative personnel.

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP37551

Onsite Engineering

IP37828

Installation and Testing of Modifications

IP40500

Effectiveness of Licensee Controls In Identifying and Preventing

Problems

IP50002

Steam Generators

IP61726

Surveillance Observations

IP62707

Maintenance Observations

IP71707

PlantOperations

IP71750

Plant Support Activities

IP73753

Inservice Inspection

IP83750

Occupational Exposure

IP84750

Solid Radioactive Waste Management and Transportation of

Radioactive Materials

IP92700

Onsite Followup of Written Event Reports

IP92901

Followup - Plant Operations

IP92902

Followup - Maintenance

IP92903

Followup - Engineering

IP92904

Follow

- Plant Support

IP93702

Prompt nsite Response to Events

25

Items Opened, Closed, and Discussed

Opened

50-269,270,287/98-05-01

VIO

Inadequate Corrective Actions for

Recurring Problems With Engineering

Instructions for Minor and Temporary

Modifications (Section 07.1)

50-269/98-05-02

NCV

Failure to Perform Snubber

Inspection as Required by TS

(Section E8.2)

50-269,287/98-05-03

IFI

Units 1 and 3 Low Pressure Service

Water Testing (Section E8.3)

50-270/98-05-04

VIO

Inadequate Configuration Control of

Unit 2 Vent Monitor Particulate and

Iodine Sample Tubing (Section R8.2)

50-269,270.287/98-05-05

NCV

Inadequate Appendix R Procedure

(Section F8.1)

50-269/98-05-06

NCV

Reactor Coolant Makeup System

Inoperable for Appendix R Scenario

(Section F8.2)

Closed

50-269,270,287/96-20-04

VIO

Failure to Have RB Material

Condition Closeout Procedure

(Section 08.1)

50-269,270,287/96-05-01

VIO

Failure to Make Proper 10 CFR 50.72

Notification (Section 08.2)

50-269.270,287/E96-19-01013

VIO

Inadequate Procedure Control Over

Movement of Spent Fuel (Section

08.3)

50-269/97-05

LER

LPSW System Outside Design Basis for

High Trajectory Turbine Missile

(Section E8.1)

50-269/96-05

LER

Failure to Perform TS Required

Inspection (Section E8.2)

50-269,270,287/96-13-03

IFI

Testing of the Modifications the

Low Pressure Service Water System

(Section E8.3)

26

50-269,270,287/97-15-03

URI

Determine the Applicability of

Monitoring Requirements of Criterion

64 of 10 CFR 50 Appendix a and

Reporting Requirements of 40 CFR 190

and 10 CFR 50.36a Regarding

Potential of Unmonitored Release

Pathways Section (Section R8.1)

50-270/98-02-13

URI

Unit 2 Monitor Inlet Sample Tubing

Bend Radius Not as Described by

Design Drawings (Section R8.2)

50-269/98-07-00

LER

Potential Operation Outside Design

Basis for Appendix R Fire Due to an

Inadequate Procedure (Section F8.1)

50-269/96-03

LER

RC Makeup System Technically

Inoperable for Appendix R Scenario

Due to Design Analysis (Section

F8.2)

List of Acronyms

ALARA

As Low As Reasonably Achievable

ASME

American Society of Mechanical Engineers

BTO

Block Tag Outs

B&W

Babcox & Wilcox

CCW

Condenser Circulatin

Water

CFR

Code of Federal Re

ations

ECCW

Emergency Condenser Circulating Water

EOC

End-of-Cycle

ES

Engineered Safeguards

ESF

Engineered Safeguards Features

ESV

Essential Siphon Vacuum

F

Fahrenheit

FT

Square Feet

FIP

Failure Investigation Process

HPI

High Pressure Injection

IFI

Inspector Followup Item

IP

Inspection Procedure

IR

Inspection Report

ISFSI

Independent Spent Fuel Storage Installation

ISI

Inservice Inspection

LDST

Letdown Storage Tank

LER

Licensee Event Report

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

LSE

Less Significant Events

LTS

Lower Tubesheet

MVAR

Megavolt Reactive

NCV

Non-Cited Violation

NOV

Notice of Violation

NRC

Nuclear Regulatory Commission

27

NSD

Nuclear System Directive

OSM

Operations Shift Manager

OTSG

Once Through Steam Generator

PCE

Personnel Contamination Event

PDR

Public Document Room

PIP

Problem Investigation Process

PSI

Per Square Inch

QA

Quality Assurance

RB

Reactor Building

RC

Reactor Coolant

RCA

Radiation Control Area

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RP

Radiation Protection

RWP

Radiation Work Permit

SFP

Spent Fuel Pool

SITA

Self-Initiated Technical Audit

SSC

Structure System Component

SSF

Standby Shutdown Facility

SSW

Siphon Seal Water

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

.-

URI

Unresolved Item

UT

Ultrasonic Test

UTS

Uper Tubesheet

V

Vo

VIO

Violation

WO

Work Order

OneTruhSta0eeao