ML15118A175

From kanterella
Jump to navigation Jump to search
Insp Repts 50-269/96-17,50-270/96-17 & 50-287/96-17 on 961117-1228.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML15118A175
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/27/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A173 List:
References
50-269-96-17, 50-270-96-17, 50-287-96-17, NUDOCS 9702100360
Download: ML15118A175 (53)


See also: IR 05000269/1996017

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287. 72-04

License Nos:

DPR-38, DPR-47, DPR-55, SNM-2503

Report No:

50-269/96-17, 50-270/96-17, 50-287/96-17

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station, Units 1, 2 & 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

November 17 - December 28, 1996

Inspectors:

M.

Scott, Senior Resident Inspector

D. Billings, Resident Inspector

G. Humphrey, Resident Inspector

N. Salgado, Resident Inspector

N. Economos, Reactor Inspector

D. Forbes, Reactor Inspector

R. Moore, Reactor Inspector

P. Kellogg, Reactor Inspector

J. Lenahan, Reactor Inspector

R. Baldwin, Reactor Inspector

R. Aiello, Reactor Inspector

Approved by:

L. D. Wert, Acting Chief, Projects Branch 1

Division of Reactor Projects

ENCLOSURE 2

9702100360 970127

PDR

ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2 & 3

NRC Inspection Report 50-269/96-17,

50-270/96-17, 50-287/96-17

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a six week

period of resident inspection; in addition, it includes the results of

announced inspections by eight regional reactor inspectors.

Operations

A configuration control violation with two examples was identified

this period. The first example involved a mispositioned valve

that resulted in the formation of a void in the Reactor Coolant

System (RCS) during loop fiil (Section 01.2). The second example

involved a mispositioned pressure sensing line isolation valve

which rendered valve 3LP-2 inoperable (Section 01.3).

0

During review of the RCS void issue described above, a weakness in

Control Room (CR) log practices was identified (Section 01.2).

The licensee identified incorrect connections (rolled electrical

power leads) to motor operated valves 2LP-1, 2LP-2, 3LP-1 and 3LP

2. This problem resulted in these valves potentially unable to

perform their safety function of achieving and maintaining safe

shutdown during an Appendix R event. A 10 CFR 50.72 report was

made. A URI was identified on the issue (Section 01.4).

On-going licensee efforts in the area of operator training to

address procedural and equipment changes after the reheater line

rupture event were observed to be adequate. Additionally,

malfunction training conducted on the new digital Integrated

Control System model was considered to be satisfactory (Section

05).

An apparent violation was identified because the plant was not

maintained in accordance with approved procedures, in that an

Operations Procedure was not placed on Administrative Hold to

prevent its use prior to revision. Initially addressed in

Augmented Inspection Team Report 50-269,270,287/96-15, this was a

major factor in the September 24, 1996, Unit 2 water hammer event

(Section 07.1).

The licensee performed an extensive root cause investigation of

two similar safety-related relay failures to assess the

possibility of a generic failure mechanism (Section 08.1).

ENCLOSURE 2

2

Maintenance

Three complex surveillances were professionally and competently

performed, providing excellent status of and critical performance

details for these important safety-related systems (Sections M1.2,

M1.3, and M1.4).

Initially addressed in Augmented Inspection Report 50

269,270,287/96-15, an apparent violation (three examples) was

identified involving the failure to provide a written evaluation

for secondary plant piping not in accordance with the code

referenced in the Updated Final Safety Analysis Report (Sections

M1.5 and E2.4).

An Unresolved Item (URI) was identified concerning certain

replacement stainless steel pipe which had not received sufficient

analysis when it was used to replace existing carbon steel

secondary pipe (Section M1.5).

Observation of secondary plant weld activities during on-going

piping replacement indicated that the welds met the requirements

of the Code, that weld appearance was adequate, and that final

inspection by Quality Control inspectors implemented for this

rep acement effort was a positive step in assuring that good weld

practices were being followed (Section M1.6).

Observation of the 1A Reactor Coolant Pump main flange weld repair.

indicated that the work was well planned and executed, that

welding and non-destructive testing were performed by well trained

individuals, that engineering and technical resources were

adequate, and that supervision of the repair was good (Section

M1.7).

Eight welds on Unit 1 Low Pressure Service Water (LPSW) piping

were not properly inspected resulting in a Violation (Section

M1.8).

A violation was identified for the failure to perform evaluations

of out-of-tolerance Measuring and Test Equipment (Section M4.1).

Engineering.

The turbine building un-reinforced 12-inch concrete floor over

pour was determined not to compromise the seismic qualification of

safety-related equipment in the building (Section E2.1).

A review of modifications and Problem Investigation Process (PIP)

backlogs identified one potential concern, which was identified as'

a URI pending additional review to determine if the wrong type

ENCLOSURE 2

3

fuses installed in the Reactor Building Cooling Units (RBCUs)

caused the RBCUs to be inoperable (Section E2.2).

Review of the steam drain modification implementation indicated

that training, procedures, and the engineering package, although

not completed, were being adequately performed (Section E2.3).

Review of Low Pressure Service Water system modifications status

indicated that engineering has completed approximately 30 percent

of the work on the packages. Work will continue into middle to

late 1997. Water hammer and overpressure issues had diverted

engineering effort (Section E8.4).

Plant Support

The licensee was conducting surveys, posting areas, and labeling

radioactive material as required by procedures (Section R1.1).

The licensee's program for Radiation Work Permit (RWP)

implementation adequately addressed radiological protection

concerns (Section R1.1).

Facility radiological conditions and housekeeping were observed to

be adequate. The licensee had initiated additional contamination

control practices to reduce personnel contamination events

(Section R1.1).

The licensee was continuing to implement program improvements to

maintain exposures As Low As Reasonably Achievable (Section R1.1).

A URI was identified concerning in situ calibrations on

containment high range radiation monitors (Section R2.1).

The licensee was adequately identifying issues of concern for

improvement in the Radiation Protection area through the use of

the Problem Investigation Process, self-assessments, and Quality

Assurance audits (Section R7).

ENCLOSURE 2

Report Details

Summary of Plant Status

Units 1 and 2 remained in cold shutdown for the entire reporting period. The

operators identified a void in the Unit 2 hot leg piping on December 10, 1996,

(Section 01.2).

Unit 3 remained defueled throughout the entire reporting

period.

Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and/or parameters. Identified discrepancies

between the UFSAR and secondary plant piping are addressed in Sections M1.5

and E2.4

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general, the conduct of

operations was professional and safety-conscious: specific events and

noteworthy observations are detailed in the sections below.

01.2 Void in Unit 2 Reactor Coolant System (RCS) Hot Leg Piping

a. Inspection Scope (93702)

The inspectors reviewed the licensee's actions after identification of a

void in the Unit 2 "B"

loop hot leg. The inspectors reviewed the drain

down and refill procedure (OP/A/2/1103/02, Filling and Venting the

Reactor Coolant System and control room logs. The data and actions were

also reviewed by a regional inspector (see Section 01.5).

b. Observation and Findings

The drain down of Unit 2 to midloop for resistance temperature detector

(RTD) maintenance was completed on October 17, 1996. The RCS was

partially refilled on October 18 - 19, 1996, using OP/2/A/1103/02. This

procedure contains a valve checklist to verify valves for the fill and

vent. The 2B Once Through Steam Generator (OTSG) hot leg vent valve

2RC-196 was recorded as having been verified open during the drain down

and refill with no apparent problems. Reportedly, adjacent valves were

aligned closed (per Enclosure 4.3, Raising the Loops) on approximately

October 18, 1996, during the loop fill completion.

ENCLOSURE 2

S

2

On December 1, 1996, the Pressurizer (PZR) level instruments were

recalibrated. The level instruments then indicated approximately 73

inches versus the 80 inches previously observed. The Unit 2 Operations

Manager directed the shift on December 3, 1996, to raise level to 80

inches, but not to exceed 45 psig PZR pressure, (pressure had been

maintained at 38-40 psig). After the PZR was refilled to 80 inches,

pressure increased to 43 psig. The operators reduced pressure down to

38 psig and noted an approximate 10 inch increase in PZR level.

The

cause of the level increase was attributed to a void in a RCS hot leg.

Development of new procedural guidance (Enclosure 4.15 of

OP/2/A/1103/02) for venting the RCS under the existing plant conditions

was completed on December 10, 1996. The hot legs were vented and the

void was determined to be in the 2B OTSG. A makeup of approximately

1922 gallons was required to replace the void. The inspectors

independently verified this value and concluded that the air pocket

would not have air bound the decay heat flow path. There were no

indications of voiding in other RCS locations.

2RC-196 was found closed on December 10, 1996. Investigation by the

licensee revealed that 2RC-196 had been mispositioned (closed) on or

about October 18, 1996, when the 2B OTSG was refilled after the RTD

repair. The mispositioning of 2RC-196 is a violation of Technical

Specification (TS) 6.4.1 and is identified as Example 1 of Violation

(VIO)50-270,287/96-17-06, Failure to Maintain Configuration Control.

The minimum TS required equipment was available for decay heat removal

at all times. However, the inadvertent void formation was significant

since it made the B OTSG unavailable for decay heat removal.

Plant

evolutions had been performed assuming both steam generators were

available for decay heat removal from October 18. 1996, through December

3, 1996.

During review of the operator's logs from October 18, 1996, to December

3, 1996, the inspector noted that approximately 6000 gallons of water

had been added to the RCS via the Low Pressure -Injection (LPI) system

and approximately 2000 gallons of water was accounted for in the seal

leakoff to the quench tank. The inspector questioned Control Room (CR)

personnel and Operations management about the apparent discrepancy

(approximately 4000 gallons). The licensee's followup investigation

accounted for the volume in question which represented approximately 130

  • gpd makeup to the RCS. Losses of approximately 50 gpd were due to

chemistry sampling and approximately 75 gpd due to LPI system losses.

This leakage rate, which was verified by the inspectors, had existed

prior to and following the drain and refill of the RCS. The inspector

concluded that the CR logs should have been more detailed in accounting

for the loss of inventory. The inspectors also noted that the operators

did not have a questioning attitude regarding the amount of water which

was added to the RCS on a daily basis.

ENCLOSURE 2

c. Conclusions

The mispositioning of 2RC-196 was identified as an example of failing

to maintain configuration control. Operation's logging practices and

attention to plant status was identified as a weakness.

01.3 Failure of Valve 3LP-2 to Operate

a. Inspection Scope (71707)

The inspectors reviewed the events associated with the failure of Unit 3

Low Pressure Injection (LPI) Valve 3LP-2 to reposition when its control

room switch was placed in the open position.

b. Observations and Findings

During performance of OP/3/A/1104/04. LPI System Alignment, Enclosure

3.1, step 2.3.3, loop suction valve 3LP-2 failed to open from the

control room switch during unit shutdown on October 5, 1996. This

delayed shutdown to cold conditions. A low pressure interlock had to be

defeated to open the valve. This interlock was designed into the

control system to prevent the valve from opening when the RCS pressure

was above 450 psig. Emergency Operating Procedure EP/3/A/1800/01,

Section CP-601, Cooldown Following Large Loss of Coolant Accident

(LOCA), and procedure OP/3/A/1104/04, LPI System, addressed manipulation

of the 3LP-2 valve.

Sections 6.3.2.2.2 and 6.3.3.2.1 of the UFSAR describe the function of

valve 3LP-2 as a path from the reactor hot leg to the sump to prevent

boron precipitation following a large break LOCA event. The UFSAR

states that 3LP-2 will be opened within 9 hours1.041667e-4 days <br />0.0025 hours <br />1.488095e-5 weeks <br />3.4245e-6 months <br /> into the event.

During

this unit shutdown, the licensee was able to get the valve opened within

approximately 3 hours3.472222e-5 days <br />8.333333e-4 hours <br />4.960317e-6 weeks <br />1.1415e-6 months <br /> by having Instrument and Electrical Technicians

defeat the interlock by "jumpering" switch contacts per procedure

IP/0/A/0100/01, Controlling Procedure For Troubleshooting and Corrective

Maintenance, and Work Request (WR) 96041487.

On October 12, an investigation revealed that an instrument isolation

valve, located between the RCS piping and the pressure sensing device,

had been mispositioned closed. Information indicated that the isolation

valve had leaked when the RCS was at full pressure and the isolated

sensing line became pressurized. When the RCS pressure was lowered

during reactor shutdown, the closed isolation valve contained the higher

pressure in the instrument sensing line. This resulted in valve 3LP-2

eing interlocked closed. The interlock would have apparently been

maintained until the isolation valve was opened or valve leakage allowed

the pressure to leak down below 450 psig.

The failure to maintain the instrument root valve to pressure switch

3RCPS0364 in its proper configuration as required by maintenance

ENCLOSURE 2

(III

4

procedure IP/0/B/203/1G, LPI System Inaccessible Flow Instruments

Calibration. Enclosure 11.4.1, Isolation Valve Open, is a violation of

TS 6.4.1. It is identified as Example 2 of Violation 270,287/96-17-06,

Failure to Maintain Configuration Control.

c. Conclusions

The mispositioning of the 3LP-2 pressure interlock isolation valve was

identified as another example of failing to maintain configuration

control. It was determined that the two configuration control

deficiencies addressed in this Section and 01.2 did not involve a

significant operability issue.

The inspector reviewed Non-Cited

Violation (NCV) 50-269/96-13-01, and concluded that the associated

corrective actions would not have reasonably been expected to prevent

the above examples of configuration control deficiencies.

01.4 Incorrect Electrical Connection of 2LP-1. 2LP-2, 3LP-1 and 3LP-2

a. Inspection Scope (93702)

The inspectors reviewed the events and procedures associated with the

incorrect electrical connection (rolled leads) of the Decay Heat Removal

(DHR) suction valves LP-1 and LP-2 on Units 2 and 3. The motor

actuators on these valves were being replaced on Unit 3 as a part of

refueling activities.

b. Observations and Findings

On December 6, 1996, while performing functional verification of 3LP-1

and 3LP-2 actuator motor rotations, the motors were found to operate

backwards (reversed from control room switch position indication). The

technicians changed the three phase electrical power leads at the MCC to

correct the rotation problems. As part of the work package completion,

the craftsmen submitted "component malfunction"- sheet that was reviewed

by engineering. When the engineer reviewed the sheet, it was discovered

that these leads should never have needed to be rolled at the motor

operator unless the MCC leads had been mistakenly changed previously.

The engineer had the leads installed per plan at both locations.

Each time the motor operator leads were lifted during a maintenance

evolution, a function test was performed from the control room switch.

Between the MCC and the valve actuator motor are a second set of

connection points in the electrical power lead circuits. These are used

to install the Appendix R temporary power supply and control circuits,

if required under emergency conditions. The 3LP-1 and 3LP-2 valves

would work correctly from the control room switch with a double change

of leads - between the MCC and the penetration room, and then, between

the penetration room connection points and the motor. But under this

arrangement, attempting to install the Appendix R temporary power per

the plan would produce incorrect valve motion when energized from

ENCLOSURE 2

5

temporary power panel.

As indicated in Section 01.3, the 3LP-1 and 3LP

2 valves did operate correctly from the switch in the Unit 3 control

room during unit shutdown in October.

The licensee initiated work orders to verify the wiring on similar

Appendix R Unit 1, 2 and 3 valves; LP-1, LP-2, CF-1 and CF-2 (CF-1/2 are

Core Flood Tank Discharge valves). This review identified that 2LP-1

and 2LP-2 were also incorrectly wired. Following identification, wiring

was corrected per approved drawings for 2LP-1 and 2LP-2.

On December 19, 1996, the licensee notified the NRC per 10 CFR 50.72

that, these valves could not have performed the safety function of

achieving and maintaining safe shutdown during an Appendix R event.

Initial indications show that these valves would have operated from the

control room but would not have operated from the Safe Shutdown Facility

(SSF) temporary power valve panel if needed during an Appendix R event.

The licensee was performing a root cause investigation at the end of the

inspection period. A Licensee Event Report (LER) will be generated on

the event.

c. Conclusion

Pending further review of the safety significance and determination of

root cause, this item will remain open as URI 270,287/96-17-07, Failure

to Maintain Appendix R Valve Leads.

01.5 Operability Review of the Unit 2 Decay Heat Removal (DHR) System

a. Inspection Scope (71707)

The inspector reviewed the operability of the Unit 2 DHR system

following the discovery of noncondensible gases in the Unit's RCS "B"

loop. Additionally, the inspector performed a calculation to verify the

licensee's postulation regarding the gases' origin, amount, location and

potential safety consequences to equipment and personnel.

b. Observations and Findings

On December 13, 1996, the inspector conducted an independent review of

the licensee's problem investigation process and their effectiveness in

resolving and dispositioning noncondensible gases that were discovered

in the "B"

loop on Unit 2 on December 3, 1996. The inspector performed

a calculation using the licensee's computer data (which contained a

chronology of RCS pressures and Low Pressure Injection (LPI) pump

suction temperatures from October 18 through December 12, 1996), control

room logs. P&IDs, and reference material from the Unit's FSAR. The

inspector identified that the licensee failed to account for changes in

RCS temperature and pressure. Subsequently, the licensee's calculation

was in error by approximately 10% in the nonconservative direction.

ENCLOSURE 2

c.

Conclusions

The inspector verified by reviewing facility documents that (1)

the

noncondensible gasses did not migrate to the reactor vessel head and (2)

DHR/LPI suction was connected to the unaffected RCS loop (loop "A").

The inspector concluded, based on the material and information provided,

that a gas bubble was not generated in the reactor vessel head and LPI

operability was not challenged by this event.

02

Operational Status of Facilities and Equipment

02.1 Engineered Safety Feature System Walkdowns (71707)

The inspectors used Inspection procedure 71707 to walkdown accessible

portions of the following safety-related systems:

  • Keowee Hydro Station
  • Unit 3 High Pressure Injection (HPI) System
  • Units 1.2, and 3 Reactor Buildings

Equipment operability, material condition, and housekeeping were

generally acceptable with some minor discrepancies that were brought to

the licensee's attention and were corrected. Other discrepancies which

were brought to the licensee's attention for resolution were: a large

paint chip and loose/broken tie wraps in the Unit 2 Reactor Building a

damaged cable and a loose Reactor Coolant Pump motor cover in the Unit 1

Reactor Building.

03

Operations Procedures and Documentation

03.1 Procedure Changes and Revisions For Unit 2 Plant Restart

a. Inspection Scope (71707)

The inspector reviewed the licensee's actions regarding Unit 2

procedures to be revised or initiated for operation of the heater drain

system which was modified following a pipe rupture incident in September

1996.

b. Observations and Findings

The inspector reviewed the status of the procedures identified by the

licensee to be revised or generated for the Unit 2 steam drain

modifications. Major modifications NSM-22901 and NSM-22941 involved the

portion of the system from Moisture Separator Reheaters to the 'A'

Feedwater (FDW) Heaters. Procedure changes were required to provide

instructions for proper operation of the modified system and to improve

operating instructions for existing equipment

ENCLOSURE 2

7

As part of the Unit 2 restart effort, the licensee reviewed other

significant water hammer issues that had been identified previously at

the plant. The issues were collected from the licensee's Event

Investigation Team report generated in response to the September 24

event review of an operator's program for compiling recollected water

hammer events, and a historical search of the Problem Identification

Program (PIP). This effort included systems other than the heater

drains, and the findings were documented in PIP reports 96-2338, 96

2339, 96-2340, 96-2341, 96-2342, 96-2347, and 96-2349. The licensee's

review was to ensure that corrective actions would be adequate to

prevent recurrence and that corrective actions were incorporated into

the new or changed operating procedures. The tracking of this

compilation was controlled by the Operations Department. The following

is a listing of those procedures which were to be reviewed for revision:

Procedure Number Procedure Title

OP/2/A/1102/01

Controlling Procedure for Unit Startup

OP/2/A/1102/02

Reactor Trip Recovery

OP/2/A/1102/04

Operation At Power

OP/2/A/1102/06

Removal and Restoration of Station Equipment

OP/2/A/1102/10

Controlling Procedure For Unit Shutdown

OP/2/A/1104/04

Low Pressure Injection System

OP/2/A/1104/12

Condenser Circulating Water System

OP/2/A/1104/37

Plant Heating

OP/2/A/1106/01

Turbine Generator

OP/2/A/1106/02

Condensate and Feedwater System

OP/2/A/1106/04

Auxiliary Boiler

OP/2/A/1106/08

Steam Generator Secondary Hot Soak, Fill, Drain, and

Layup

OP/2/A/1106/14

Moisture Separator Reheater

OP/2/A/1106/16

Condenser Vacuum System

OP/2/A/1106/22

Auxiliary Steam System

OP/2/A/1106/26

Steam Drain Valve Checklist

PT/2/A/0261/07

Emergency CCW System Flow Test

AP/2/A/1600/09

5SF Auxiliary Service Water System

AP/2/A/1700/19

Loss Of Main Feedwater

In addition to the water hammer issuest

the licensee identified areas

within the plant secondary systems with the potenti-al for being

overpressurized. Specific overpressure corrective actions had included

some modification to those systems that resulted in two procedures being

identified that required revision. These are as follows:

OP/2/A/1104/10

Low Pressure Service Water

OP/2/A/1106/02

Condensate and Feedwater System

The following Unit 2 valves have been designated by the licensee to be

administratively controlled to the listed positions to prevent

overpressure of plant systems. The valves and their associated

ENCLOSURE 2

8

procedural controls will be included in the above procedures. These

administrative controls are short-term resolutions for plant restart.

The long-term corrective actions will be implemented at a later date.

This will include additional modifications and procedure changes to

eliminate the overpressure concerns.

VALVE

POSITION

2CF-53 (Core Flood)

Open

2C-130 (Condensate)

Open

2C-131

Open

2C-132

Open

2C-133

Open

2HD-186 (Heater Drain)

Open

2HD-187

Open

2HD-189

Open

2HD-191

Open

2HD-199

Open

2HD-201

Open

2HD-244

Open

2HV-28 (Heater Vent)

Open

2HV-35

Open

2HV-63

Open

2HV-70

Open

2HV-71

Open

2MS-20 (Main Steam)

Open

2MS-23

Open

2MS-29

Open

2MS-32

Open

2HPE-34 (High Pressure Injection)

Closed

At the close of the inspection period, the licensee had not yet

completed the necessary procedure revisions. Licensee intentions are to

complete this effort prior to Unit 2 restart.

c. Conclusions

The licensee's actions (i.e., compilations of issues, scope of changes,

and equipment review) appear adequate in identifying the procedures and

revision requirements necessary for restarting'and operating the plant

in a safe and orderly manner.

05

Operator Training and Qualification

05.1 Water Hammer Issue - Operator Training

a. Inspection Scope (71707)

The inspectors reviewed operator training on revised and new procedures

that resulted from modifications made to the plant. The modifications

ENCLOSURE 2

9

were implemented to reduce or eliminate steam/water hammers and to

prevent overpressurizing plant equipment.

b. Observations and Findings

The inspectors reviewed the operator training package for the Moisture

Separator Reheater (MSRH)/Heater Drain modifications (NSMs 22901 and

22941). The lesson plan was approved on December 12, 1996. which

described in detail the water hammer event that occurred in Unit 2 on

September 24, 1996, and the modifications that resulted. In addition,

operators were required to observe a steam/water hammer demonstration in

order to heighten their understanding of the effect.

Procedure revisions and enhancements had not been completed at the end

of the reporting period for all the systems modified or affected by

water hammers. Consequently, operator training was not completed, but

the licensee's efforts continued in this area.

c. Conclusions

The inspector determined that the licensee's operator training efforts

to date were acceptable and adequately addressed the modifications and

the water hammer incident.

05.2 Operator Requalification Program (71001)

a. Inspection Scope (71001)

During the period of December 17-20, 1996, the inspector used guidance

from Inspection-Procedure 71001 to review and evaluate'the licensee's

operator requalification program in the area of the Unit 3 Digital

Integrated Control System (ICS) modification training, malfunction

training and evaluation, and job performance measures examination

review.

b. Observations and Findings

The inspector observed approximately four days of malfunction training

on the Unit 1 simulator with the Unit 1 digital ICS model installed.

Each crew training session-observed was comprised of four operators with

one session consisting of five operators. The instructors presented

seventeen credible ICS malfunctions to the operators. The inspector

observed operators practice 9 of the 17 malfunctions during these

sessions. Eight of the 17 malfunctions could not be reasonably acted

upon to prevent a reactor trip and were not practiced. These eight

malfunctions were presented to familiarize the operators of all credible

malfunctions that could occur. The inspector questioned the operators

concerning their ability to operate the new digital ICS. The operators

unanimously responded that they did not feel it would be'a significant

ENCLOSURE 2

10

problem with switching between the new and old ICS on the different

units providing some type of "just-in-time" training was provided.

When changing between the analog and digital models on the Unit 1

simulator, certain instruments (two) and simulator software must be

changed in order for the simulator to operate with the digital ICS

model.

The inspector noted that during the first training session,

those instruments were not swapped out.

Following malfunction training, operator performance was evaluated using

a single Job Performance Measure (JPM). The inspector questioned the

Operations Training Manager concerning the validity and confidence level

gained by using a single JPM to determine the retention of knowledge

following the training presented. The inspector further discussed that

administration of an examination comprised of a singular JPM may not

provide enough data points to infer that mastery of one JPM would

provide the confidence that all tasks were mastered. Administration of

one out of a possible nine JPMs would provide only a 11 percent testing

of all material testable.

At the end of the inspection the Training

Manager decided that one JPM was not sufficient to infer mastery of all

tasks and decided to use two JPMs for the evaluation.

The inspector reviewed the results for the first two weeks of

malfunction training. Three of the thirty one operators who received

this training'and a subsequent single JPM examination failed the

evaluation for a 9.6 percent failure rate. The inspector reviewed all

administered JPMs and follow-up questions and found a generic weakness

in the area of cross-limits.

The inspector reviewed eight of the nine JPMs available for use for the

final JPM evaluation.

At the time of the inspection, eight JPMs were

developed and available for review. The ninth JPM was not scheduled to

be completed until January 20, 1997. Each JPM consisted of the task

used for evaluation and two follow-up questions asked after the JPM was

administered.

c. Conclusions

The inspector concluded that malfunction training conducted on the new

digital ICS model was satisfactory. -All instructors presented the

material in a logical manner and allowed all operators to practice on

each task presented. The training was well received by all operators as

evidenced by their willingness to participate in the training. The

inspector also concluded that operators felt confident with going from

the analog to the digital ICS, providing they receive "just-in-time"

training prior to going to a unit with a different ICS model. The

inspector concluded that care must be taken to swap from the analog to

digital ICS models on the Unit 1 simulator in order to maintain

simulator fidelity and accuracy.

ENCLOSURE 2

The inspector concluded that administration of a singular JPM for

evaluation of training was not a sufficient sample to infer all tasks

were mastered. After discussion with the Operations Training Manager,

this practice of using one JPM was changed to add an additional JPM.

The inspector concluded that the administration of two JPMs with four

follow-up questions would provide a sufficient sample size in order to

infer mastery of tasks.

The inspector concluded that the JPMs developed were satisfactory to

determine operator performance for the tasks identified. The follow-up

questions provided additional information concerning operator knowledge

about the system. The inspector noted from evaluating the followup

questions, that cross-limits knowledge was a generic weakness of those

operators who received the evaluation.

07

Quality Assurance in Operation

07.1 Process for Administratively Controlling Procedures

a. Inspection Scope (40500)

The inspectors reviewed the issue documented in Inspection Report (IR)

50-269,270,287/96-15 associated with the licensee's failure to place the

heater drain Operations Procedure on administrative hold after

deficiencies were noted.

b. Observations and Findings

During the NRC Augmented Inspection Team (AIT) inspection documented in

IR 50-269,270,287/96-15, the inspectors identified that Operations

Procedure OP/2/A/1106/14, Moisture Separator Reheater, had not been

placed on Administrative Hold after necessary changes were identified

during a controlled Unit 2 startup of the system on May 7. 1996. That

startup had identified precautions and guidance that should enhance the

above procedure to make the heater drain system more manageable and less

susceptible to water hammer events during startup. Nuclear Station

Directive (NSD 703.12) Administrative Hold of Procedures, provides

implementing directions for placing procedures on administrative hold

when changes are required. This directive requires that the applicable

procedure shall be removed from the active document control files and be

placed into a designated Administrative Hold file, and that working

copies of the affected procedure .under this hold status be destroyed.

The above procedure was not placed on hold. The intended changes were

planned to be implemented at some future time. Consequently, on

September 24, 1996. station personnel attempted to place the Unit 2

MSRHs in service using the non-enhanced OP/2/A/1106/14, which had not

been placed on Administrative Hold to signify that changes were

necessary. This failure to place OP/2/A/1106/14 on hold is identified

as Apparent Violation (EEI) 50-270/96-17-08, Failure to Use Procedure

Administrative Hold.

ENCLOSURE 2

12

Since the AIT inspection, the licensee has revised Operations Management

Procedure OMP1-9, Use Of Procedures, Section 5.4, Administrative Control

of Procedures Removal From and Restoration to Service. The revision

defines conditions when a procedure should be removed from service, how

the removal is to be accomplished, and the requirements for restoring

the procedure for use. In addition, detailed training was provided to

increase the operator's awareness of the procedure changes.

c. Conclusion

The inspector reviewed the revised procedure and determined that

sufficient instructions were included to prevent recurrence of the

violation documented above.

08

Miscellaneous Operations Issues (92901)

08.1 Undervoltage Relay Failure Analysis

Two Unit 3 relays (27SY3/1C1 and 27SY3/1C2) associated with the

Emergency Power Switching Logic (EPSL) Standby Bus 1, Phase C,

Retransfer to Startup Logic experienced separate failures on November 13

and 19. The licensee actively performed a failure analysis which

determined that the subject Cutler-Hammer relays showed no common mode

failures with generic implication to the remaining relay population. As

part of the failure analysis the licensee performed an inspection of all

energized safety-related Cutler-Hammer relays to identify any damage,

and to ensure that the relay had acceptable date codes. In a letter

from the vendor to the licensee, relays manufactured from 6/74 to 7/76

were identified as possibly .containing an undersized magnet carrier that

could increase the probability of the coil clearing contact failing to

operate properly. Relay 1C2 was the only relay manufactured within the

specified time period. The licensee's inspection effort did not

identify any other problems with date code or damage with the relays.

The inspector concluded that the licensee was aggressive in pursuing the

possibility of a generic failure mechanism on the relays.

08.2 Closed IFI 50-287/96-16-06: ICS Malfunction Training Results

As addressed in Section 05.2, malfunction training on the new digital

ICS model was satisfactory. Accordingly, this item is considered

closed.

ENCLOSURE 2

13

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707, 61726, 62700)

The inspectors observed all or portions of the following maintenance

activities:

WO # 96079756

NSM 22941, Modify Heater Drain System, Unit 2

PT/3/0610/01A

EPSL Normal Source Voltage Sensing Circuit

WO # 96009491

Unit 1 Auto Voltage Regulator Switching

WO # 96013880

NSM 32989, Unit 3 ICS Upgrade

PT/0/A/0250/25

HPSW Pump And Fire Protection Flow Test

WO # 96090249

TT/2/A/610/27, Unit 2 EPSL Relay Contact

Verification

0

TT/0/A/0620/030

Keowee Hydro Load Rejection Test, 4th Quarter

1996

PT/3/A/0251/24

HPI Full Flow Test

OP/3/A/1104/04

LPI System

PT/3/A/0610/O1J

EPSL Functional Test

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and.thorough. All work observed was performed with the

work package present and in active use. Technicians were experienced

and knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that the Maintenance activities listed above

were completed thoroughly and professionally.

ENCLOSURE 2

M1.2 LPI Full Flow Test

14

a. Inspection Scope

On December 21, Operations, Maintenance, and Engineering performed a

Unit 3 full LPI flow test. The inspectors observed and evaluated the

major portions of test during its performance.

b. Observation and Findings

Test procedure TT3/A/150/44, LPI Full Flow Test, was conducted on Unit 3

with the reactor vessel head removed, fuel removed, and Low Pressure

Service Water (LPSW) secured.

During the test, the 3C LPI pump flow

was increased through both trains of LPI coolers to the RCS from 3000 to

4200 gpm in 250 gpm increments. The test checked pump differential

pressure, NPSH pressures, pump motor parameters, LPI cooler suction

temperatures, flow control valve position, and pump vibration levels.

The system engineer supported the test by coordinating data collection

and evaluation of the rough data. Additionally, the licensee checked

vibration levels on the newly installed thermal relief valve

modification (between the large RCS cold leg piping and first downstream

isolation valves) to determine, in part, the acceptability of its

installation per requirements specified in ASME Code OM-3.

c. Conclusions

The test results were satisfactory. Pump performance through each train

met the vendors pump curve within 3 percent. The test was performed in

a professional and controlled manner.

M1.3 High Pressure Injection (HPI) Full Flow Test

a. Inspection Scope

On December 24, Operations and Maintenance performed a Unit 3 HPI full

flow test. The inspectors observed and evaluated the major portions of

test.

b. Observation and Findings

Test procedure PT3/A/251/24, HPI Full Flow Test, was conducted on Unit 3

with the reactor vessel head removed, no fuel in the reactor vessel, and

LPI in service. The test increased 3A and 3B HPI pump flow separately

through both trains of HPI, respectively. Additionally, individual

flows were taken in each of the two branches for each train. The test

verified the operability of the pumps, the pumps' discharge check

valves, Borated Water Storage Tank (BWST)-to-pump suction check valves,

and newly installed branch loop check valves. At several points in the

test, Operations personnel had to perform critical timed evolutions and

coordinate test actions.

ENCLOSURE 2

15

c. Conclusions

The test results were satisfactory. All components tested performed

nominally. The test was performed in a timely and controlled manner.

M1.4 Keowee Load Rejection Test

a. Inspection Scope

On November 26. the licensee performed a load rejection test on both

Keowee hydro-electric units at a new low lake level. This was done to

provide data for a new Selected Licensee Commitments curve limit for

Keowee power production to the grid. The inspectors observed the test.

b. Observation and Findings

The load rejection test was satisfactorily completed per

TT/0/A/0620/030, Keowee Load Rejection Test - 4th Quarter 1996. The

test was well controlled and both Keowee hydro-electric units operated

well.

Both units were very similar in operational characteristics and

control system performance.

During test performance, a fuse blew in the control circuits for Air

Circuit Breaker ACB-7. The breaker loss reduced the number of Keowee

auxiliary power sources. Operations tracked the condition and the test

procedure was appropriately exited. The system engineer and an

electrical maintenance supervisor supported trouble-shooting and repair

of the breaker which was administratively controlled by WO 96094606-01.

All work was well planned and implemented. The failed fuse was in

accordance with the circuit drawings. The breaker was satisfactorily

bench tested prior to returning it to service.

Once in service, the

breaker was cycled under loading prior to returning to the test

procedure.

c. Conclusions

The test met acceptance criteria. Appropriate test gear and support

personnel were available for the test. Trouble-shooting .and corrective

actions regarding the circuit breaker problem were performed with a high

level of professionalism and completeness.

M1.5 Maintenance Corrective Actions Following Water Hammer Event

a. Inspection Scope

The inspectors reviewed maintenance activities conducted as corrective

actions following a water hammer event in September 1996. (Reviews of

operational issues related to that event are described in sections 05.1.

07.1 and E2.3. Inspections of related pipe hanger and support issues

are described in sections E2.1, E2.2, and E2.5.)

ENCLOSURE 2

16

The licensees' reviews after the water hammer and subsequent reheater

steam line rupture identified that some balance of plant piping systems

at Oconee did not meet requirements of the piping code referenced in the

UFSAR. The deficiencies included failure to meet code requirements in

the following major areas:

numerous branch pipe connections were not

properly reinforced, some piping was not properly protected from

overpressure, and some piping may have been replaced with different

material without proper engineering analysis to ensure that design

strength requirements were met. The inspectors reviewed the licensee's

actions to verify adequate overall scope of the reviews after the event.

The inspectors also reviewed some specific corrective actions initiated

to address the identified problems.

b. Observations and Findings

Lack of Reinforcement on Certain Branch Pipe Connections

The licensee's walkdown of Class G heater drain piping revealed that

certain field fabricated branch connections were missing reinforcement

collars/saddles which were typically found on headers depending on

certain local pipe conditions, including pipe size, thickness, pressure,

and temperature rating. In order to investigate this apparent problem,

the licensee established a task group whose objectives were as follows:

0

Conduct engineering evaluations on all Class G branch connections

to determine the scope of field inspections.

Perform detail engineering evaluations using as-built field

measurements to determine code compliance.

Modify/repair all branch connections where calculations showed

they did not meet applicable code requirements.

The screening criteria used to determine which branch connections were

acceptable and therefore exempt from this project were as follows:

Design pressure s 100 psig. This pressure limit was based on

engineering analysis.

Pipe diameter less than 2.5 inches. This pipe size was based on

applicable code requirements and computational analysis.

Pipe wall thickness and reinforcement area. Acceptability based

on calculations specified by the code using the above mentioned

thickness measurements.

The following table depicts the status of the Branch Connection Project

at the start of this inspection.

ENCLOSURE 2

.17

U1

U2

U3

TOTAL

Identified by Engineering as

100%

100%

100%

N/A

needing evaluation (% complete)

Sent to field for inspection

215

214

232

661

Field inspection complete

1

193

1

195

Detailed Engineering evaluation

1

169

1

171

complete

Number requiring modification

0

51

0

51

Number of design packages

0

19.

0

19

to field

By review of the licensee's data generated from field inspections and

engineering calculations, the inspectors ascertained that code required

reinforcement collars were missing from branch connections in the

following systems:

System

Unit 1

Unit 2

Unit 3

Moisture Separator Reheater (MSRH)

20

23

1

Heater Vent & Heater Drain

10

17

1

High, Low Press. Extraction

2

4

0

Auxiliary Steam (AS)

0

1

0

Emergency Feedwater (EFW)

0

0

2

Main Steam (MS)

4

2

0

Feedwater (FW)

5

1

0

Condensate

6

10

0

TOTAL

47

58

4

The inspectors noted that paragraph 104.3 of USAS B31.1-67 Power Piping

Code, (Code) states in part that when a pipe is penetrated by a branch

connection, the size of which weakens the pipe, additional reinforcement

must be provided. The type and amount of reinforcement to be provided

must meet the requirements of paragraph 104.3.1(d). Oconee Updated

Final Safety Analysis Report (UFSAR) Section 3.2.2.2 states, in part,

that Class G piping shall be designed, installed, and tested in

accordance with the USA standard B31.1, 1967 Edition Power Piping Code

(code), requirements. Plant piping was not installed in accordance with

requirements in the piping code referenced in the UFSAR and a written

safety evaluation was not recorded as required by 10 CFR 50.59 (b)(1).

ENCLOSURE 2

18

This is identified as Example 1 of Apparent Violation (EEI) 50

269,270,287/96-17-01. Failure To Complete A Written Safety Evaluation Of

Secondary Plant Piping Not In Accordance With The Piping Code Referenced

In The UFSAR. (Paragraph M1.6 below describes inspection of welding

activities to install the missing reinforcements.)

Overpressurization Protection Issues

As a result of the water hammer event in Unit 2 Second Stage Reheater

(SSRH) piping, the licensee performed an in depth investigation to

review the issue of overpressure protection concerns regarding Class G

piping at Oconee Nuclear Station (ONS). Similar instances of specific

overpressure protection concerns had been identified by Design

Engineering as early as 1989 for several steam systems (AS, MS and Plant

Heat). These concerns were identified as a result of a corrective

action resulting from the Emergency Feedwater (EFW) Safety System

Functional Inspection which found that relief valve MS-92 was

undersized. The licensee's investigation included review of past

concerns documented in PIRs, PIPs and Oconee Engineering Design Basis

(OEDB), and review of ONS Flow Diagrams of secondary systems to identify

other potential code discrepancies.

The issues identified by the above reviews were incorporated into nine

PIPs, which were as follows:

PIP 96-2149 Potential Overpressure of Underrated Components

PIP 96-2150 Overpressure Due to Undersized Relief Valves or No

Relief Valves

PIP 96-2151 Steam Trap Discharge Piping Not Meeting Code

Requirements (ANSI B31.1).

PIP 96-2152 Overpressure Due to Inadvertent Valve Closure.

PIP 94-1391 Hydrogen Overpressure Issue.

PIP 96-2472 HPSW to the Filtered Water System.

PIP 96-1762 LPSW Pump Suction Piping Overpressure.

PIP 96-2486 D Flash Tank Overpressure Issue.

PIP 96-2153 OFD Design Parameter Flag Problems.

By review of selected PIPs and associated engineering assessments

generated in response to the as-built system inspections, the inspectors

noted the following:

Several existing as-built conditions where piping lines could

become overpressurized due to valve location, alignment and or

leakage were listed in PIP 96-2149. Examples of systems where

such conditions were found included: Steam Generator Blowdown

Piping, Feedwater Piping, Main Steam Bypass Pumping Trap Piping,

Low and High Pressure Service Water Piping. Examples of systems

with installed underrated valves included: Steam Trap valves in

the auxiliary steam system, Main Steam Pumping Trap check valves,

and Steam Drain valves.

ENCLOSURE 2

19

PIP 96-2150 listed several examples where the present relief

valves were too small to provide adequate overpressure protection.

These conditions were identified in the Auxiliary Steam and the

Plant Heating Systems. In several instances the licensee could

not retrieve sizing calculations to help determine the adequacy of

the present valve arrangement. Also, in a couple of instances the

system was not equipped with overpressure protection (e.g., Plant

Heating System and Auxiliary Steam, downstream of valve AS-414

where class rating changed from 125 psig to 75 psig).

PIP 96-2151 listed numerous as built examples of steam traps on

the Auxiliary Steam Header to the Radwaste Facility and on the

Steam Drain System where the change in the design pressure rating

occurred immediately after the regulating valve instead of the

last isolation valve as required by the code. Accordingly, the

above PIP listed 11 examples in the Auxiliary Steam system. Oconee

Flow Diagrams (OFD 117J-1.1 and OFD 128A-1.3) and four in the

Steam Drain system, (OFD 122A-1.5,-2.5 and-3.5) where valves and

associated piping required upgrading to meet system pressure and

temperature requirements.

PIP 96-2152 listed 16 examples of as built valve and associated

piping in several systems where an inadvertent closure of a

downstream valve could result in the overpressurization of piping.

An example of such isolation valves included: 1AS-49 on the

Auxiliary Steam system; valve CF-53 on the Core Flood system;

valves CCW-89 or CCW-416 on the Component Cooling system. Other

systems identified as vulnerable to inadvertent valve closure

included heater drain piping between "B" & "C" and, "C" & "D" FDW

Heaters; FW Heater Vents "A," "B,"

"C," and "D"; Discharge and

Suction HDP piping.

To track these findings, the licensee generated spread sheets which

identified pipe sections between valves and or -components where over

pressure protection was lacking or overpressurization could occur under

certain conditions. This tracking system was also used to identify

certain valves, which under certain conditions could see pressures

beyond code allowable ratings. Engineering calculations were being used

to compare the as-built conditions with code requirements. OFDs were

used to mark up the areas where the potential overpressure protection

problems were identified. The inspectors reviewed selected engineering

assessments, evaluations, calculations and OFDs for accuracy and

technical adequacy.

This work effort was performed for Plant Heating,

Condensate, Low and High Pressure Service Water, and Auxiliary Steam

systems.

The majority of the modifications required upgrading,

qualification, and/or replacement of piping: upgrading or replacement of

valves; and the changing of pressure boundaries on the OFDs.

From these reviews, the inspectors ascertained that a total of 71 valves

had been designated for possible overpressure protection modifications

ENCLOSURE 2

20

in the Auxiliary Steam system. Of these. 20 had undergone engineering

evaluations and had been forwarded to Work Control for disposition.

Eight of the 20 valves are shared between the three Oconee Units and

were therefore placed on the licensee's Unit 2 Restart List for early

disposition.

Regarding the OTSG Blowdown Preheat System on Unit 2, OFD 123A-1.3

engineering reviews identified that several valves were underrated.

Typically these valves were rated for 900 psi which was acceptable for

blowdown conditions; however, on a unit trip these valves could see

pressures in the range of 1050 psi, which would be above their design

rating. By document reviews and through discussions, the inspectors

ascertained that there-were approximately eight valves listed in this

category. Some of these valves were shared by two of the three Units

and were scheduled for replacement or removal from the system prior to

Unit 2 restart. At the close of this inspection, none of the work

packages had gone to Work Control for disposition.

Failure to implement design requirements with respect to operating

pressures and temperatures for normal conditions, local conditions and

transients as described in Section 102 of the Code is identified as

Example 2 of the above mentioned Apparent Violation 50-269,270,287/96

17-01.

Replacement of Carbon Steel Piping With Stainless Steel Without

Sufficient Engineering Analysis

The licensee also identified an issue involving the possible use of

unsuitable material on certain piping systems. The issue was the use of

stainless steel piping as a replacement for carbon steel material. Of

particular interest was the question whether adequate engineering

analysis had been performed to assure that design strength requirements

were not being compromised by the replacement of carbon steel piping

with stainless steel piping. This engineering -analysis was required by

Specification OS-0242.00-00-0001, Revision 17 Note 24, which stated in

part that when a choice of two different type materials were specified

by the OFD (i.e., stainless and carbon steel materials) an engineering

evaluation and approval was required prior to the change. PIP 96-2359

was revised to address this question and to assure that an engineering

evaluation was performed and approved as required-. This item was

identified as Unresolved Item 50-269.270.287/96-17-04, Engineering

Evaluation for the Replacement of Carbon with Stainless Steel Piping.

c. Conclusion

Several examples of piping code violations were identified. Numerous

secondary plant branch piping connections were not reinforced as

required by the code referenced in the UFSAR. A large number of

deficiencies associated with overpressure protection on balance of plant

systems were also identified. The inspectors concluded that the

ENCLOSURE 2

21

deficiencies were caused by failure to assure that code design

requirements were translated into appropriate instructions and/or

drawings.

The deficiencies resulted in an inadequate field inspection

and verification program to assure that design requirements were being

adequately implemented by construction.

After some problems were identified following the pipe rupture event on

September 24, 1996, the licensee was quick to respond and took

appropriate actions to identify all as built discrepancies and initiated

actions to assure that the problems were corrected. (Paragraph M1.6

describes additional review of the related welding activities.) The

licensee's response and dedication of engineering construction resources

to address these problems and bring secondary plant systems into code

compliance, was regarded as good.

An unresolved item was identified involving the adequacy of engineering

evaluations of stainless steel piping as a replacement for carbon steel

material.

M1.6 Maintenance Welding (55050)

a. Inspection Scope

This inspection was performed to observe certain aspects of Heater Drain

Pipe modifications as described in NSM-22941 and weld repairs resulting

from a water hammer event in the Unit 2 Moisture Separator Reheater

(MSRH) Drain Pipe System. For more details see IRs 96-15 and 96-16.

The inspector observed welding in progress and reviewed weld process

control records for modifications in the MSRH and the Heater Vent and

Drain piping.

b. Observation and Findings, Unit 2

Modification procedure NSM-22941, Part AM1, was used to provide

instructions and documentation for installation of drain lines,

replacement of damaged piping, reinforcement of certain branch

connections, and the installation of certain check valves to the First

and Second Stage Reheater Drain Tanks A and B. The code of reference in

Section 3.2.2.2 of the Oconee UFSAR, applicable to design and

installation activities of class G piping is the United States of

America Standard Piping Code. B31.1 1967 Edition.

At the start of this inspection period, installation commenced on

reinforcement collars for branch connections of the Heater Vent and

Drain System of Unit 2. As such, the inspector observed the welds

listed below for compliance with Field Weld Data Sheet (FWDS)

requirements, good workmanship practices, and control of filler metal

material. Welder identification numbers were noted for review of their

qualifications.

ENCLOSURE 2

22

Branch Conn.

Drawing/Location

Size

123A-2.3-022

1410F/K4

18"x18"

123A-2.3-026

1410E/G6

18"x6"

123A-2.4-027

1410A/C5

8"x8"

123A-2.4-034

1410A/G5

8"x8"

123A-2.4-037

1410E/D6

8"x8"

As required by the Oconee Welding Manual, work control including

inspections and documentation was done in accordance with procedure

MP/0/B/1810/015, Change 17, and work orders 96091370-01/96090645-01.

Based on the work observed and review of supporting documents, the

inspectors determined that welders were adequately trained to fabricate

these weldments, documentation was consistent with procedural

requirements, and control of filler metal was satisfactory at the work

area and at the issue station. Filler metal certification records were

reviewed and found to be satisfactory. Weld records showed that

completed welds were being inspected by trained Quality Control (QC)

Welding Inspectors.

To verify that field welds were being fabricated and inspected in

accordance with requirements of procedure MP/0/B/1810/015 and Code B31.1

Section 127 Welding, the inspectors selected at random a total of 51

welds of various pipe sizes ranging from about

to 18 inches in

diameter. These welds were shown in drawing numbers 2HD-107, -109.

-111, -112,-113, and -116. Within these areas, the inspectors checked

for weld reinforcement uniformity and height, undercut, arc strikes,

weld spatter, cleanliness, material and welder identification. The

inspectors identified two welds (1 and 11) on Drawing 2HD-107 that

exhibited workmanship anomalies. For example, weld #1 showed that a

short length on one side of the joint had not been adequately welded and

weld #11 showed that the weld reinforcement thickness was slightly above

the allowable. Both conditions were discussed with the cognizant

welding supervisor and the QC supervisor who verified the as found

condition and took immediate corrective action. To prevent recurrence

of this problem, the subject procedure was revised to include a table-of

allowable weld.reinforcement thicknesses for the range of materials

welded.

In addition to this review effort, the inspectors reviewed radiographs

of two welds that had been selected at random by the Maintenance Support

Manager in charge of welding Quality Control. The welds were on the

Heater Drain and the Main Steam systems. Both of these systems were

Duke Class G and were radiographed per Duke's Radiography Procedure NDE

10 Rev. 19 and the acceptance criteria of B31.1-67 Code.

ENCLOSURE 2

23

The subject welds were identified as follows:

Weld No.

Drawing No.

Size

3MS 29

122A-3.2

12"x.688

2HD-108-6

108

3"x.300

Weld and film quality for these radiographs were consistent with code

requirements.

c. Conclusion

The licensee's welding activities observed during this inspection period

met the requirements of the applicable code. In general, weld

appearance was adequate. Fina inspection of welds by QC inspectors

which was implemented for this modification was a positive step in

assuring that good welding practices were being followed in pursuit of

good weld quality. Although this inspection focused on welding

activities, engineering evaluation, calculations, and inspections

relative to Unit 2 MSRH modification, the inspector observed that the

same program applies to and was being implemented in Units 1 and 3.

M1.7 Welding Repair of Primary Coolant Components

a. Inspection Scope

The inspectors reviewed the licensee's actions regarding the

identification and repair of a leak on the 1A2 reactor coolant pump

(RCP) main flange.

b. Observation and findings

The 1A2 RCP has experienced leakage in the area of the seal assembly

over several years. Some of the problems included the seal piping

flange, the radial bearing thermowell, and pump main flange to

lower seal housing. During the last refueling outage (RFO), End of

Cycle (EOC) 16, the licensee performed an interim repair on the seal but

some leakage was observed during startup. The leakage worsened during

this past cycle with significant accumulation of boron crystals observed

at the pump during hot shutdown. An inspection of the suspect area

during the current Unit 1 forced outage revealed crack indications at

the pump main flange bore (face and inner diameter). The crack

indications were subsequently dye penetrant examined to determine the

extent of the defect and to assist in mapping out the exact location. A

repair procedure was developed to: (1)

excavate the defect for analysis.

(2)

grind out the minor indications and perform dye penetrant testing,

and (3)

restore the affected areas back to sound qua lity. Following the

repair, a Minor Modification ONOE-9155 was to be implemented for

machining a new 0-ring groove on the repaired main flange surface. This

ENCLOSURE 2

24

modification will represent a minor design change to the configuration

of the RCS pressure boundary, in the area of the RCP main flange to the

lower housing.

Weld Repair

The 1A2 RCP is a Westinghouse Model 93AS, with a main flange made of a

SA351, Grade CF8 18-8 stainless steel casting. The pump was

manufactured to the ASME Code Section III Class A. 1965 Edition, with

addenda through 1967. The repair was being performed to the ASME Code

Sections III and XI, 1989 Edition requirements. The welding was being

performed by qualified welders who had been given adequate training on a

mockup, by simulating field conditions. The repairs were made with a

Duke qualified weld procedure utilizing the shielded metal arc process

and a stringer bead technique to minimize heat built up and residual

welding stresses. Weld build up was accomplished using E 308 stainless

steel filler metal.

This material has greater strength and sufficient

amounts of delta ferrite to suppress the potential for microcracking

during welding. Component configuration, thickness size, and space

restrictions precluded doing radiography on the repair. In lieu of

radiography, the licensee performed liquid penetrant examination on the

root pass, at each 1/2 inch interval of weld deposit and on the final

pass. At the close of this inspection, Duke was preparing a request to

the NRC for relief from the radiography requirements, since it was not a

viable option due to configuration and location.

In an effort to identify the root cause for these defects, the licensee

removed a boat sample and forwarded it to Westinghouse for analysis. In

addition, the licensee contracted a vendor to perform a fracture

analysis to determine the suitability of the repaired component for

continued service. Also, in reference to the root cause for the

cracking, Duke took field measurements for residual delta ferrite around

the crack and at the immediate area. Results of this investigation

revealed no evidence of measurable ferrite in the immediate area of the

crack but appeared to be within the normal range in the surrounding

area.

Preliminary results from the metallurgical investigation and the ferrite

checks suggest that the crack indications may have been due to a lack of

-adequate amounts of ferrite to prevent cracking during casting

solidification. A copy of the final report will be provided for review

on a future inspection.

c. Conclusion

Evaluation of the RCP main flange crack defects and the subsequent

repairs were well planned and executed. Welding and nondestructive

testing examinations were performed by well trained individuals using

approved procedures that met code requirements. Engineering and

ENCLOSURE 2

25

technical resources were adequate and supervision of the'repair was

good.

M1.8 Modification to Low Pressure Service Water (LPSW) "B"

Line Header

a. Inspection Scope

The inspectors reviewed PIP 96-2059 and evaluated the adequacy of NDE

examinations performed as required by ASME Code Section XI. Code Case N

416-1.

b. Observation and Findings

This item involved a modification on the Unit 1 LPSW where a 24 inch

diameter branch conn iection was attached to the LPSW "B"

Line Header.

The modification was performed on a portion of this system designated as

ISI Class "C"

which corresponds to ASME Code Class 3. As such, the

licensee opted to use ASME Section XI Code Case N-416-1 in lieu of the

required hydrostatic test following pipe installation/construction. The

NRC authorized the licensee to use this Code Case by letter dated March

27, 1996, as Relief Request No.95-GO-001. This Code Case requires that

Non-Destructive Examination (NDE) be performed (on new or weld repairs)

in accordance with methods and acceptance criteria of the applicable

subsection of the 1992 Edition of ASME Code Section III.

As required by

the licensee's applicable procedure QAL-5, ASME Code Section XI, Class 3

welds tested under Code Case N-416-1 must undergo magnetic particle or

liquid penetrant examinations on both root and final weld pass. In

addition, following completion of these NDE requirements, the new line

must undergo a VT-2 pressure test at normal operating pressure and

temperature.

By review and through discussions with cognizant personnel, the

inspectors ascertained that NDE examinations on eight welds on isometric

drawing 1LP474 in Unit 1 did not comply with the requirements of this

Code Case. The Weld Process Control Sheets (WPCS) were filled out

correctly in that they included the NDE requirements of Code Case N-416

1. However, because of an apparent miscommunication, Quality Assurance

(QA) deleted the applicable NDE requirements, meaning that the eight

completed welds received a final visual and a surface examination on the

final pass-which is the typical NDE for Code Class 3 welds. Six of the

eight welds were hydrostatically tested, but not to code requirements.

Upon discovering the problem the licensee issued PIP 96-2059 and took

corrective action. The above mentioned PIP characterized the problem as

a missed surveillance per TS 4.2.1 and Section lB of Appendix A of NSD

203. As such, the licensee declared that the LPSW system was capable of

performing its intended design functions but did not meet the applicable

code requirements. An operability limit was established which required

that the affected Units 1 & 2 remain below 2500 F and declared the

system operable, but degraded. The compensatory measure was that both

ENCLOSURE 2

26

units would remain below 2500 F until the subject welds met all Code

Case N-416-1 requirements or a code relief was granted by the NRC.

Following a review of the aforementioned PIP and discussion with

cognizant licensee personnel, the inspectors concluded that the problem

was not an issue of a missed TS surveillance. Moreover, the inspectors

concluded that the missed NDE was intended to satisfy construction code

and code case requirements. The latter was implemented as an alternate

for the code required hydrostatic test which had to be done before the

line could be turned over to operations.

This failure to implement code and procedural requirements is a

violation of 10 CFR 50 Appendix B Criterion V. This violation was

identified as 50-269/96-17-09: LPSW Modification Did Not Meet ASME Code

NDE Requirements.

c. Conclusion

The licensee did not meet the Code Case requirements or alternate Code

requirements for the subject welds. A violation was identified.

M4

Maintenance Staff Knowledge and Performance

M4.1 Control of Measuring and Test Equipment (MT&E) (37550)

a. Inspection Scope

The inspectors reviewed the licensee's control of M&TE related to

evaluation of out of tolerance (OOT) equipment usage. Applicable

regulatory requirements included 10 CFR 50, Appendix B and the

licensee's approved Quality Assurance (QA) program. The OOT reports and

evaluation activity was reviewed for Maintenance Instrumentation and

Electrical (IAE) tool issue, mechanical tool issue, and Commodities

receipt inspection M&TE.

b. Observations and Findings

Licensee procedures required the evaluation of the measuring and test

activity performed prior to the identification of 00T or lost M&TE.

Maintenance Directive 4.4.1, M&TE Control, dated May 30, 1994, required

evaluations to be performed within 14 working days following the

discovery of OOT or lost M&TE. Procurement procedure. TIP-701.

Instructions for Control of M&TE, dated March 28. 1996, required the

evaluations to be performed in seven working days following discovery of

OOT or lost M&TE. The inspectors reviewed approximately 25 open OOT

reports in the IAE tool issue. Approximately 20 of these were overdue

without approved extensions. The following examples illustrate the age

and equipment types:

ENCLOSURE 2

Instr.#

1227

Date Discovered

Due Date

(includes

extensions)

30933

digital thermometer

10/2/96

11/4/96

31620

digital thermometer

10/3/96

10/25/96

31515

megohm meter

10/10/96

11/5/96

31102

C-clamp calibrator

3/19/96

4/23/96

30824

temp. calibrator

12/6/95

5/2/96

31644

crimping tool

4/17/96

5/14/96

30755

micro-ohm meter

8/2/95

11/9/95

27163

pressure test gage

4/18/95

10/26/95

27104

pressure test gage

6/25/95

7/17/95

Although the 00T reports were appropriately initiated, there appeared to

be inadequate followup to verify the evaluations were performed.

The mechanical tool issue timeliness for OCT evaluations was good in

that there were no open OOT reports. The inspectors reviewed two

completed reports to assess the quality of the evaluations. The OOT

report on micrometer OCMNT-27790, dated February 5, 1996, listed 17

previous use work orders for the device. The evaluation stated that the

previous use was acceptable based on performance of post maintenance

testing (PMT) performed on the work orders. There was no indication of

how the PMT enveloped the measuring or test activity accomplished by the

micrometer. The OT report of lost torque wrench OCMNT-26778, dated

April 1, 1996, also referenced the performance of PMT as the basis for

accepting previous use of the lost wrench. No torque verification was

performed. The inspector discussed the weak evaluation basis with the

licensee and was provided PIP 0-095-1226, dated September 27, 1995,

which provided guidance to maintenance staff for OCT evaluations. This

guidance indicated that PMT was acceptable justification for accepting

previous use of OT or lost M&TE. The inspector concluded that the

evaluations, using the PMT for justification of previous use, did not

adequately assess the previous use of the OT M&TE.

A multi-amp breaker tester in the Commodities receipt inspection area

was discovered OT on September 5, 1996. PIP 4-096-1931 was initiated

on October 7, 1996, and corrective actions for the evaluation of impact

on past usage was required on November 6. 1996. As of November 21,

1996, no evaluations had been performed. This example demonstrated that

the PIP process was not an effective mechanism to assure evaluations

were performed within the applicable procedure time constraints of seven

working days.

The examples identified by the inspector were identified as Violation

50-269.270,287/96-17-02, Failure to Perform Evaluations of Out of

Tolerance M&TE.

0

ENCLOSURE 2

28

c. Conclusion

The licensee did not meet their QA program requirements for M&TE.

Several examples were identified in which timely and adequate

evaluations of out-of-tolerance M&TE were not performed.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) Inspector Followup Item 50-269.270.287/95-12-01: Apparent

Ultrasonic Testing (UT) Examiner and UT Procedure Weakness

This item was written to address certain concerns relative to the

adequacy of Ultrasonic Procedure NDE-600 and its use during field

examinations. In addition, the inspector had determined that although

the subject procedure had been endorsed by Electric Power Research

Institute (EPRI), it was not identical to the EPRI procedure with

respect to the methodology used to determine the presence of geometric

flaws. Accordingly, on July 11, 1995, the inspector attended a

procedure demonstration at the EPRI facility in Charlotte, NC. Since

this demonstration, the following corrective actions have been

implemented:

UT data from Oconee's main coolant piping, inspected using

Procedure NDE-600.- has been reviewed and evaluated by Duke's Level

III UT Examiner and have been found to be correct.

Procedure NDE-600 has been revised to clarify the applicable

attributes for circumferential and axial scans and to clarify that

only two applicable attributes need to be met to call an item a

flaw.

'Appropriate training has been performed to improve understanding

of procedural requirements and applicable revisions.

Based on a review of these completed actions, this IFI is closed.

III. Engineering

E2

Engineering Support of Facilities and Equipment

E2.1 Water Hammer Issue -

Turbine Building (TB) Floor Overpour

a. Inspection Scope (37550. 37551)

The inspectors reviewed the equipment anchorage of TB safety-related

equipment to determine if the non-reinforced 12-inch overpour impacted

the anchorage requirements. Nonsafety-related piping anchored in this

floor had experienced pull-out during a previous water hammer event.

Applicable regulatory requirements were provided by 10 CFR 50, Appendix

B, and the UFSAR.

ENCLOSURE 2

29

b. Observations and Findings

The LPSW and EFW systems are the safety-related systems with equipment

anchored to the TB floor. The anchorage drawings for the LPSW and EFW

pumps indicated that the anchor rods extended below the overpour to the

rebar reinforced portion of the floor. Safety-related pipe supports for

these systems were anchored to the floor with expansion bolts which did

not extend to the reinforced portion. The inspector reviewed the

licensee's civil engineering evaluations of the potential uplift force

which determined the worst case seismic load to be a 6000 pound uplift

force on one support anchor plate. This indicated that the safety

related anchors were adequately supported for seismic loads.

This force

was considerably less than the estimated 26,000 pound pull force

experienced in the moisture reheater water hammer which pulled out an

existing anchor plate.

The LPSW and EFW systems had no history of water

hammer occurrences: therefore, the excessive uplift forces resulting

from water hammer were not a concern.

c. Conclusions

The non-reinforced overpour on the TB floor provided no apparent

limitation on the seismic anchorage of safety-related equipment in this

building. There was no history of water hammer on these systems;

therefore, the anchorage for the safety related equipment was adequate

for the anticipated loading.

E2.2 Water Hammer Issue - Potential Issues in Modification and PIP Backlog

a. Inspection Scope

The inspectors reviewed the backlog of PIPs and modifications to

determine if these contained significant equipment or safety issues. A

list of approximately 1000 open PIPs were reviewed to identify trends or

specific equipment problems. Modifications were a subset of PIPs as

these were developed to resolve PIPs. A more detailed review was

accomplished on 30 PIPs selected from the list. The applicable

regulatory requirements were provided by 10 CFR 50, Appendix B.

b. Observations and Findings

With one exception, no significant equipment or safety issues were

apparent in the backlogs which were not being appropriately addressed.

There were several PIPs since 1990 which identified wrong fuse size or

type installed in equipment circuits.

Discussions with the licensee

indicated that frequently the fuses were oversized which was

conservative with respect to equipment operability. Drawings had been

developed to list the correct fuse size and type for plant equipment

which indicated that the issue was being addressed.

ENCLOSURE 2

30

The inspector noted a potential safety-related equipment problem related

to the Reactor Building Cooling Units (RBCUs). PIP 0-095-0267, dated

February 27. 1995, identified four blown fuse occurrences which resulted

in inoperable RBCUs. These occurred during testing in 1991, 1992, and

1994. The PIP identified that the wrong type fuse was installed in all

RBCUs. Fast acting fuses were installed where time delay fuses were

applicable. Approved controls directed that the fast acting fuses were

to be installed. The fuses were blown as the result of the motor in

rush current on starting the equipment. The Unit 1 fuses were replaced

with time delay fuses on July 23, 1996. Unit 3 fuses were replaced on

June 21, 1995. Unit 2 fuses had not been replaced at the end of the

report period.

The PIP did not identify or address the potential common mode failure of

the RBCUs due to the wrong fuse type. No comparison was made of tested

conditions against expected accident conditions. The information

available was insufficient to determine if an RBCU operability concern

resulted from the fast acting fuses. Pending further review, this item

is identified as URI 50-269,270,287/96-17-03, RBCU Operability Concerns

Due to Wrong Type Fuse in Control Circuit. This item remains open

pending the licensee's evaluation of the RBCU tested conditions versus

accident conditions to assess equipment operability impact.

c. Conclusions

With one exception. no apparent significant equipment or safety issues

were identified in the PIP and modifications backlogs. A URI was

identified to determine if the wrong type fuse in the RBCUs was an

equipment operability concern.

E2.3 Unit 2 Steam Drain Modifications

a. Inspection Scope

The inspectors reviewed modifications NSM ON-22901 and NSM ON-22941 to

the Unit 2 Steam Drain System. The modifications were generated to

reduce water hammers in the steam drains from the Moisture Separator

Reheaters. The inspectors observed day to day implementation of the

modifications in all three plants, particularly Unit 2. These

inspections were performed in addition to the inspections addressed in

Sections M1.5 and M1.6.

b. Observations and Findings

In 1991 and 1993, the licensee had placed a "hold" on modifications NSM

ON-22901 and NSM ON-22941, respectively, due to priority of other

modifications, pre-empting secondary changes. Therefore, the design had

not been completed at the time of the September 24, 1996, pipe rupture

event in Unit 2. After the incident, the licensee procured the services

ENCLOSURE 2

31

of several outside consultants to help better understand water hammers

prior to completing the design on the modifications.

One of the consultants provided general water hammer training to

licensee staff at large. On November 13, 1996, the inspectors witnessed

a steam/water hammer demonstration at the ONS training facility. The

demonstration had evolved from steam/water hammer problems experienced

at another facility that had consequences similar to those experienced

at ONS. The exhibition was shown to all Operations personnel and many

other site personnel. The display was a small scale piping model that

consisted of clear glass piping, valves, colored water, and a heat

source. It closely modeled the portion of the Unit 2 steam drain system

associated with the pipe rupture event. It clearly demonstrated the

reaction of steam and water in low areas of piping that form a loop-seal

and the effects that could be expected. It further dispelled the belief

that water hammers would be eliminated by reducing the rate of steam

flow into a system partially filled with cooler water. This exhibition

and input from vendors resulted in revision changes planned for

operations procedure OP/1,2,3/A/1106/14, Moisture Separator Reheater,

and changes to major NSMs (NSM-22901 and NSM-22941) that are being

implemented during this shutdown period.

The major areas addressed by each modification and inspector activities

are as follows:

Nuclear Station Modification 22941

The inspectors reviewed work activities in progress on an almost

daily basis during the implementation of NSM 22941, Secondary

Systems Control .and Valve Upgrade. The welding activities were

closely monitored by-the inspectors. Major areas of the

modification consisted of the following:

-

.Replacement

of 2MS-112.& 173 main steam valves and

associated control systems that supply steam to the second

stage reheaters in the MSRHs.

-

Installation of check valves for the Second Stage Reheater

Drain Tanks. 2A and 2B.

-

Installation of check valves for the First Stage Reheater

Drain Tanks, 2A and 2B.

-

Relocation and/or replacement of heater drain pressure,

temperature, and level control systems.

-

Installation of low point drains to eliminate condensate in

headers when steam is induced.

ENCLOSURE 2

32

-

Replacement and modification of piping/fittings and hangers

to upgrade system to code requirements and eliminate

potential water/steam hammers.

Nuclear Station Modification 22901

This modification interfaced with NSM 22941 and was performed in

parallel. The inspectors were able to review both modifications

during regular inspections of that plant area. The primary

equipment involved in this modification were:

-

Perform a stress analysis on the Second Stage Reheater Drain

Tank and pipe supports to evaluate hangers and tank nozzle

loadings.

-

Replace heater drain valves, 2HD-25, 26, 29, and 30 to

prevent leakage, steam/water hammer problems, and improve

control of system.

Both NSM 22901 and 22941 were implemented in a methodical and careful

manner. Pipe fitter foreman, QC personnel, overseeing engineers, and

management were routinely seen in the work areas. Cleanliness and fitup

requirements were observed to be met. Welders and pipe fitters were

knowledgeable of the jobs they were performing. Management in charge of

the project were aware of all job aspects and were fully supported by

the design engineers.

Planners were providing good packages to the

workmen.

c. Conclusions

The inspector determined that the licensee's on-going implementation of

the modifications was adequate. Although the licensee has not completed

the modifications and final testing of the modified equipment can not be

completed until system restart, there have been-no deficiencies

identified that should prohibit plant restart.

E2.4 Current Pipe Specification Allows Installation of Piping Material

Unsuitable for Design Pressures

a. Inspection Scope

As described in other sections of this report, the licensee performed

detailed reviews of secondary plant piping issues after a reheater line

ruptured in September 1996. The review indicated that current pipe

specifications were not adequate to ensure that proper material was

used. The inspector reviewed this issue,

ENCLOSURE 2

_

_

_

_

_33

b. Observations and Findings

At the time of this inspection the licensee identified that Pipe

Installation Specification OS-0234.00-00-0001,(300.4), allowed the use

of American Petroleum Institute (API), API-5L carbon steel welded pipe

material for pipe sizes greater than 24 inches. The Power Piping

Quality Assurance (PPQA) Manual that was used during plant construction

specified A-155KC-70 Class material for pipe 26 inches and larger in the

Condensate System. The allowable stress for API-5L material was only

about 70 percent of allowable for A-155KC-70 Class 1. The licensee's

analysis on pipe branch connections within this system indicated the

API-5L material was unsuitable for the applicable design pressures. On

November 12, 1996, the licensee issued PIP 96-2359 and began an in-depth

review of engineering documents to determine if API-5L material was used

on Oconee's Balance of Plant high energy lines. Through telephone

discussions with the cognizant licensee engineer on December 11, 1996.

the inspectors ascertained that a review and evaluation of the original

PPQA, the Oconee Piping Summary (OPS) Manual and the Oconee Flow

Diagrams (OFDs), revealed the following. The only system where A-155KC

70 material was originally specified or installed and could have been

replaced with API-5L, under the OPS Manual and OS-243.00-00-001 in

effect since December 1. 1982, was a section of 30 inch diameter pipe on

the Condensate System. The OPS Manual was subsequently superseded on

May 8, 1984, with OFD series 121A which included material specification

requirements for applicable pipe systems.

Within these areas, the inspectors noted that the error in specifying

API-5L material on large diameter piping was.not identified or corrected

when pipe specifications were updated. This error allowed the material

in question to remain in the pipe specification as an acceptable

replacement material in high energy line applications. This failure to

review material selection for suitability of application on piping

design documents/specifications was identified as Example 3 of Apparent

Violation 50-269,270,287/96-17-01.

During the above mentioned telephone discussion, the licensee's

cognizant engineer indicated that, a review of applicable drawings

disclosed the Condensate System had not been changed or modified since

the original construction where A-155KC-70 was used. A portion of the

"C"

Bleed System with 30 inch diameter piping -was the only other system

where API-5L material could have been used. However, Duke indicated

that this material was acceptable for this application. In conclusion,

the licensee's evaluation and review revealed no instances where API-5L

was misapplied.

ENCLOSURE 2

34

E2.5 Balance of Plant Piping Supports

a. Inspection Scope

The inspectors reviewed engineering involvement in repairs to

balance of plant piping system supports following a water hammer

event on September 24, 1996. which resulted in rupture of the Unit

2 heater drain line and injuries to seven personnel working in the

turbine building.

b. Observations and Findings

Following the September 24, 1996, water hammer event, the licensee

developed a recovery plan to inspect high energy Class G piping

systems to identify deficiencies in the installation of the piping

and pipe supports. The piping systems included the following:

condensate, extraction, main steam, main feedwater, heater drain,

auxiliary steam, and plant heating. These systems were originally

constructed using normal accepted commercial practices but do not

fall under the requirements of 10 CFR 50, Appendix B. The design

parameters for these piping systems were deadweight, thermal, and

internal pressure loads. Seismic loads were not considered in

design of Class G piping per UFSAR Table 3-1.

The inspectors reviewed Oconee procedure titled, "Class G Piping

Support Walkdowns," which was developed to walkdown the high

energy balance of plant piping systems and verify the structural

functionality of each support on the systems. These walkdowns

were not intended to provide as-built verification of existing

support configuration. The procedure provided walkdown

instructions, instructions for examining supports for degraded

conditions, walkdown checklists and summaries, and guidance on

maximum pipe span criteria. The inspectors concluded that the

procedure was adequate to perform the inspections. More than 4000

supports on BOP piping systems were inspected on all three units

utilizing this procedure.

The inspectors reviewed the walkdown packages for the Unit 2

extraction and feedwater systems. There were no isometric piping

drawings available to use for the walkdowns. Instead.licensee

engineers utilized flow diagrams (P&IDs) and plant layout drawings

showing plan and section views of the piping. Review of the

walkdown packages disclosed that pipe support drawings were not

available for approximately one-third of the pipe supports on

these systems. Discussions with licensee engineers disclosed that

the BOP non-safety.related pipe supports were constructed in

accordance with "typical" pipe support drawings. This is a normal

construction practice for these supports. There are no NRC

requirements for the licensee to maintain the pipe support

drawings to demonstrate they comply with Section 121 of B31.1

ENCLOSURE 2

35

regarding design of non-safety related BOP pipe supports.

As a

result of the walkdown inspections, defects were identified by

licensee engineers on several supports. The majority of these.

were minor deficiencies such as bent hanger rods, missing or loose

locknuts, interferences with other structures/components, or

incorrect spring can settings. The pipe support deficiencies were

corrected using maintenance work requests or via minor

modifications.

The original BOP piping design was performed using a computer code

current at the time of the original piping design. A rigorous

stress analysis was performed using a current updated proprietary

program, SUPERPIPE. to qualify the piping and supports on the

heater drain system. As a result of the rigorous analysis,

modifications were implemented for approximately 60 pipe supports.

The modifications involved either removal of some existing

supports, reinforcement of some existing supports. or installation

of new supports. In addition, spring settings were readjusted on

approximately 40 supports. The inspectors reviewed Nuclear

Station Modification (NSM) 22941, Parts AM1 and AS1, which

implemented the support modifications. Since the modification

involved non-safety related piping it was properly designated by

the licensee as non-Q. The inspectors walked down a portion of

the heater drain system and performed a cursory inspection of

eight supports which had been modified under NSM 22941. No

deficiencies were identified with the support modifications.

Since the modifications involved non-safety (non-Q) systems, the

work was not performed under the quality assurance program, and

the modifications were not independently inspected by quality

control personnel. The work was instead inspected by craft

personnel or their supervision. This complies with NRC

requirements.

A rigorous stress analysis was not performed on the piping on the

other six Class G systems listed above. After the walkdowns were

completed a walkdown summary was performed to identify any

potential negative system trends. This was designated as a

flexibility review and was intended to determine if the piping

systems were restrained from thermal expansion at normal operating

temperatures.

c. Conclusions

The licensee's program for followup on the water hammer event

complied with NRC requirements. The licensee was proactive in

following up on the event.

ENCLOSURE 2

~@

36

E2.6 Low Pressure Service Water System Vibration

a. Inspection Scope

The inspectors followed up the licensee's review of flow induced

cavitation in the low pressure service water (LPSW) piping

downstream of the LPI coolers.

b. Observations and Findings

On November 20, 1995, the licensee initiated Problem Investigation

Process (PIP) 0-095-1491 which identified an adverse trend

associated with flow induced cavitation in the LPSW piping

downstream of the LPI coolers. This PIP summarized 12 other PIPs

which had been initiated since 1992 concerning numerous flow

induced problems with the LPSW piping in the proximity of LPSW

flow control valves 251 and 252. Corrective action to address the

adverse trend (PIP 0-095-1491) was to perform vibration testing at

varying flow rates on the LPSW piping downstream of the LPI

coolers. The inspectors reviewed completed test Procedures

TT/1/A/0251/57 and TT/2/A/0251/59, LPSW Vibration Tests, for Units

1 and 2 respectively. The inspectors verified the procedures

contained adequate instructions, precautions, and limitations for

performance of the tests, and that an evaluation was performed in

accordance with 10 CFR 50.59. The results of the testing showed

that peak accelerations (vibrations) occur at system flow rates of

approximately 3000 gallons per minute, which is the design

accident flowrate. The licensee has concluded that the long term

solution to this problem will be replacement of the LPSW 251, 252

flow control valves with new valves of a different design. This

work is scheduled for the next outage on each unit when the new

valves become available.

c. Conclusions

The inspectors concluded that the licensee actions to identify the

adverse trend and implement long term corrective actions to

resolve the problem were appropriate.

E8

Miscellaneous Engineering Issues (92903, 92700)

E8.1 (Closed) Deviation 50-269,270,287/94-19-01: Improper Code Classification

This item addressed a deviation (DEV) from UFSAR requirements which

stated that portions of the Engineered Safeguards. (ES)

System which

could contain recirculated reactor.building sump water following a LOCA

were required to be Class II (Duke Class B).

Portions of the Unit 1 and

3 LPI system piping were classified as Class III (Duke Class C) even

though this piping could contain recirculated reactor building water

ENCLOSURE 2

37

following a LOCA. The licensee's resolution specified in the deviation

response, dated August 25. 1994, was to perform inspections to upgrade

the piping to Class II requirements and perform an Engineering review to

identify other improperly classified piping subject to containing

recirculated reactor building sump water.

The resolution to this issue was documented in PIP 0-94-0678. The

inspectors verified the completion of the corrective actions specified

in the PIP and deviation response. The identified piping was inspected

and upgraded on November 30, 1995. The piping classification review

identified several improperly classified piping runs and resolved these

as documented in the PIP. The 1995 UFSAR update revised the applicable

statement to clarify that the subject piping within containment was not

required to be Class II; however, this piping outside of containment was

required to be Class II. This item is closed.

E8.2 (Closed) Deviation 50-269,270,287/94-19-02: Failure to Meet UFSAR

Requirements Related to System Class Boundary Weld Inspection

This item addressed the UFSAR requirement that piping welds joining two

different piping classes were to be inspected in accordance with the

requirements of the higher classification. Examples were identified in

which welds as piping class breaks were inspected to the requirement of

the lower classification. The licensee's response, dated August 25,

1994, stated that the cause was that UFSAR section 3.2.2.1 was not clear

regarding class break application at piping welds. In particular, the

licensee interpreted that the class break occurred at the valve seat

where a valve was installed at the class break: therefore, there were no

welds joining different piping classes. The response stated that all

examples involved valve welded class breaks. A request for additional

information response dated September 20. 1994, clarified this

classification as applied to one inch piping or less and demonstrated

that adequate weld inspection was specified by the UFSAR. Clarification

of the UFSAR interpretation resolved the deviation.

E8.3 (Closed) Deviation 50-269,270,287/94-24-05: Improper Code Classification

This item addressed an example of improperly classified piping in the

High Pressure Injection system (i.e.. Class II piping classified as

Class III). The concern was the different weld inspection requirements.

The licensee's response to the deviation, dated October 19. 1994, and

December 19, 1994, specified corrective actions to include

reclassification of the subject piping to Class II and a relief request

submittal regarding weld inspection of the installed piping. Request

for Relief No. 95-01 was submitted to the NRC on February 9, 1995, and

accepted by NRC Safety Evaluation Report, dated August 14, 1995.

PIP-094-1685 tracked the revision of the applicable drawings to reflect

the piping class upgrade. Minor modifications OE-8024, 8027, and 8028

revised the drawings and were completed on June 13, 1995.

ENCLOSURE 2

38

E8.4 (Oen) Inspector Followup Item 50-269.270.287/96-13-03: Low Pressure

Service Water Modifications and Testing Issues

This item was opened to track the low pressure service water

modifications which were being implemented to correct several

deficiencies identified during the Service Water Operational Performance

Assessment (SWOPA). The purpose of this inspection was to update the

status of the modifications and review completed work. The scope of the

Oconee Service Water (OSW) Project consists of five major modifications

broken down into 79 Implementation Parts and 6 Minor Modifications. The

major modifications and their parts are listed below.

X2932 - Design and install a new QA-1 seal/cooling water supply

(SSW) to the Condenser Circulating Water (CCW) and Essential

Siphon Vacuum (ESV) pumps and motors from the LPSW system.

52932 Part Al - Install buried headers out to the intake

52932 Part A2 - Install non-buried headers out to the intake

52932 Part A3 - Install headers in Ul and U2 TB

32932 Part A - Install U3 tie ins to the CCW pumps

12932 Part A - Install Ul tie ins to the CCW pumps

22932 Part A - Install U2 tie ins to the CCW pumps

52932 Part B - Remove HPSW tie ins

X3000 -Design and install a new QA-1 ESV system to increase the

reliability and duration of the Emergency Condenser Circulating

Water (ECCW) siphon supply to LPSW.

53000 Part A

Construct a trench across the dike

43000 Part B1

Construction of ESV pad

43000 Part B2 -,Construction of the ESV building

43000 Part B3 - Install ESV building appurtenances

53000 Part C1 - Install cable trench

53000 Part C2 - Install conduit bank and buried piping

53000 Part C3 - Install vacuum pumps and piping

53000 Part C4 - Install vacuum pump power/heat

Trace/instruments

33000 Part C - Tie in to U3 CCW/level switch/ESV pump

controls

13000 Part C - Tie in Ul CCW/Level Switch/ESV pump controls

23000 Part'C

- Tiein to U2 CCW/level switch/ESV pump

controls

33000 Part D - Load removal from 3X51,2,3

13000 Part D - Load removal from 1XSl,2,3

23000'Part D - Load removal from 2 sX1,23

X3001

LPSW system changes to ensue adequate NPSHA

Part A Providing minimum flow protection for the LPSW pumps.

ENCLOSURE 2

39

33001 Part A - Install U3 recirc piping and controls

13001 Part A - Install Ul recirc piping and controls

Part B - Providing an alternate supply to the control room

chillers from the CCW crossover

53001 Part A - Chiller piping

Part C - Providing the capability to isolate the non essential

headers from either Units 1 or 2

33001 Part C - Move control switch for 3LPSW 45 and renumber

to 3LPSW139

13001 Part C - Move control switch for 1LPSW 139

23001 Part C - Provide local flow rate indication

Part D - Removal of LPSW 4 and 5 from ES

33001 Part D - Remove ES from 3LPSW 4 and 5

13001 Part D - Remove ES from 1LPSW 4 and 5

23001 Part D - remove ES from 2LPSW 4 and 5

X3002 - LPSW pump impeller changes

13062 Part A - Changeout 1A LPSW pump impeller

13002 Part B - Changeout 1C LPSW pump impeller

13002 Part C - Changeout 1B LPSW pump impeller

33002 Part A - Changeout 3A LPSW pump impeller

33002 Part B - Changeout 3B LPSW pump impeller

X3003 - Reclassify existing systems and components required to

maintain the ECCW siphon to LPSW to QA-1

Part A - Modify the CCW pump discharge valve controls to prevent

closure following a Loss of Offsite Power (LOOP)

33003 Part A - Upgrade U3 CCW discharge valve controls

13003 Part A - Upgrade Ul CCW discharge valve controls

23003 Part A - Upgrade U2 CCW discharge valve controls

Part B - Reclassify and Upgrade the design of the siphon pressure

boundary

53003 Part B Innage related ECCW reclassification

The inspector reviewed the following documents

Initial Scope Documents for Siphon Seal Water System - Rev 1

ENCLOSURE 2

40

-

Initial Scope Documents for the first siphon pressure boundary

reclassification upgrade - Rev 2

-

Final Scope Document for Buried pipe portion of the siphon seal

water system

-

Final Scope Document for the ESV pad /foundation - Rev 2

-

Final Scope Document for the Intake Pipe Trench - Rev 0

-

Final Scope Document for the ESV System. (buried portions only)

Rev I

-

Final Scope Document for U3 LPSW Pump Minimum Flow Lines - Rev 1

-

Final Scope Document for the removal of the ES signal from valves

3LPSW 4 and 5 - Rev 0

-

Oconee Service Water Project Schedule dated 12-02-96

OSW Project General Project Layout and Modification Parts

Revised 11/18/96

-

OSW Project Team Structure

The inspector attended a project meeting on December 5, 1996, to discuss

the current status and schedule of the OSW project. The schedule was

impacted by the heater piping rupture and is currently delayed pending

the completion of that work. The inspector encouraged the licensee to

develop a new schedule and inform Region II management of their new

completion milestones.

The Unit 3 Modification 33001, installation of the minimum flow

recirculation lines on the LPSW pumps has been completed as well and the

removal of the ES signal from valves 3LPSW 4 and 5. Work is progressing

on the intake dike with an expected completion date of March 31, 1991.

Engineering has completed approximately 30 percent of the work on the

modifications. However, the heater drain piping rupture has stopped all

this work and a new schedule for completion has not been developed as of

the time of this inspection.

This item will remain open pending completion of the modifications and

testing.

ENCLOSURE 2

41

IV.

Plant Support Areas:

R1

Radiological Protection and Chemistry (RP&C) Controls (71750)

R1.1 Tour of Unit 1 and Other Radiologically Protected Areas

a. Inspection Scope (83750)

The inspectors toured work areas to evaluate radiological controls and

conditions of facilities and to evaluate personnel radiation exposure

controls during the ongoing Unit 3 RFO and Units 1 and 2 ongoing

maintenance outages.

b. Observations and Findings

During tours of the facility, the inspectors observed contamination and

radiation surveys being performed and reviewed selected records of

routine and special radiation and contamination surveys performed. Also

during tours of the plant, the inspector independently verified

radiation levels in portions of the Auxiliary Building. The inspectors

reviewed radiological survey maps posted outside rooms/spaces in the

plant used to enhance Radiation Work Permit (RWP) information.

The inspectors reviewed selected routine and special RWPs for adequacy

of the radiation protection requirements based on work scope, location,

and conditions. For the RWPs reviewed, the inspector noted that

appropriate protective clothing, respiratory protection, and dosimetry

were required. During tours of the plant, the inspector observed the

adherence of plant workers to the RWP requirements and discussed the RWP

requirements with selected plant workers and Radiation Protection (RP)

personnel. The licensee had color coded RWPs to enhance the reference of

an RWP for a specific Unit and located the RWPs in areas convenient for

worker review.

The inspectors noted that the licensee's posting and control policies

for radiation areas, high radiation areas, locked high radiation areas,

contamination areas, and radioactive material storage areas were

appropriate. An inventory conducted by the inspectors of the licensee's

key box for controlling keys to locked high radiation areas determined

the keys for those areas were accounted for. At the time of the

inspection, the licensee had appropriately labeled radioactive material

observed consistent with the requirements of 10 CFR 20.1904 and

radiological housekeeping was observed to be adequate. Records reviewed

determined contaminated square footage was averaging approximately 3.0

percent of the total Radiological Controlled Area (RCA) of 126,311

square feet. In 1996, the licensee was averaging approximately 1.5

percent of the total RCA as contaminated during non-outage periods.

Records reviewed also determined the licensee was tracking and trending

personnel contamination events (PCEs) and that approximately 405 PCEs

had occurred in 1996, of which, approximately 94 had occurred during the

ENCLOSURE 2

42

ongoing Unit 3 outage. Although no adverse trends in personnel

contamination controls were noted during the inspection, the inspectors

discussed licensee challenges in minimizing personnel contaminations,

particularly those which may have occurred within the RCA in areas not

posted as contaminated. Records reviewed determined approximately 134

PCEs had occurred in areas not posted as contaminated. The licensee had

initiated some additional contamination controls to address these

challenges, which included: detailed tracking and trending of PCE root

causes, increased RCA boundary surveys, installing small item equipment

monitors at exits to the RCA, increased area mopping of designated

areas, reduced number of egress points from the RCA, and practical

factor training for management personnel who oversee workers exiting the

RCA.

The inspectors reviewed the As Low As Reasonably Achievable (ALARA)

program implementation and results. The inspectors interviewed selected

ALARA staff members and.discussed ALARA planning initiatives for the

work performed during 1995 and 1996. Some of the recent ALARA initiates

discussed included:

Plant shutdown crud burst activities to reduce source term

radioactivity.

A hot spot reduction program primarily accomplished through system

flushes and chemistry boron/lithium controls to reduce corrosion

product transportation.

Source term reduction methods by using increased filtration of the

Reactor Coolant System letdown and replacement of approximately 25

primary valves with stellite free valves.

A modification to normal sump piping to reduce hotspots and

improve sock filter installation which was estimated to save 0.35

Rem per outage.

A ladder installation to improve access to the B1 reactor coolant

pump area to save an estimated 0.4 Rem per outage.

A canal drain line replacement over the emergency sump to save an

estimated 0.5 Rem per outage.

A discussion with licensee representatives and a review of pertinent

records determined the licensee had established an annual site exposure

goal for 1996 of-approximately 339 person-rem. The licensee's 1996

annual site exposure goal was based on operational exposure and one Unit

3 Refueling Outage (RFO). Site exposure accrued in 1996 as of November

18, was approximately 232 person-rem. At the time of the inspection,

the inspectors determined the licensee was continuing to implement

program improvements to .maintain exposures ALARA.

ENCLOSURE 2

43

c. Conclusions

Based on observations during facility tours, procedure reviews,

documentation reviewed, and discussions with licensee personnel, the

inspectors determined the following:

The licensee was conducting surveys, posting areas and labeling

radioactive material as required by procedures.

The licensee's program for RWP implementation adequately addressed

radiological protection concerns and provided for proper control

measures.

Facility radiological conditions and housekeeping were observed to

be adequate. The licensee had initiated additional contamination

control practices to reduce personnel contamination events.

The licensee was continuing to implement program improvements to

maintain exposures ALARA.

R2

Status of Radiation Protection and Control (RP&C) Facilities and

Equipment

R2.1 Process and Effluent Radiation Monitors

a. Inspection Scope (84750)

The inspectors reviewed selected licensee Technical Specifications

(TSs), Duke system procedures, site procedures, and records for required

surveillances on the containment high range radiation area monitors and

portable survey instrumentation to evaluate licensee compliance for

maintaining specific instrumentation as required.

b. Observations and Findings

Selected records reviewed indicated that performance of channel checks,

source checks, channel calibrations, and channel operational tests for

the containment high range radiation monitors were current and that the

containment high range radiation monitors had been calibrated to meet

the frequency specified by licensee TSs 4.0 Table 4.1-1. The inspectors

also observed Licensee TS 4.0 Table 4.1-1 referenced NUREG 0737 II.F.1.3

for the calibration of containment high range radiation monitors 57 and

58. NUREG 0737, Table II.F.1.3 stated containment high range radiation

monitors are to be calibrated in situ and that laboratory calibration is

not acceptable due to the possible differences after in situ

installation. The inspectors determined that the licensee was removing

the detectors from the containment and calibrating the monitors while

the detectors were located in the reactor building penetration room.

The inspectors informed the licensee that this method of calibration did

ENCLOSURE 2

44

not appear to meet the intent of in situ calibration. At the time of

the inspection, the licensee was researching this issue to determine if

existing background information was available to support not calibrating

the monitors in situ. The inspector informed the licensee that until

further information was obtained, this issue would be identified and

tracked as Unresolved Item (URI) 50-259.260,287/96-17-05, In Situ

Calibration of Containment High Range Monitors, pending additional

information from the licensee.

During tours, the inspectors also observed that an adequate number of

portable survey instruments were available for use within the RCA during

the ongoing outages and that the instruments were operable and currently

calibrated in accordance with frequencies specified by licensee

procedures. In addition, the inspectors verified the licensee's whole

body standup and chair counters used for internal monitoring of

radioactivity were currently calibrated.

c. Conclusions

Based on the above reviews, it was concluded that containment high range

radiation monitors and portable survey instruments in use were being

source checked and calibrated on frequencies required by licensee

procedures. However, until further information is obtained, one URI was

identified concerning in situ calibrations on containment high range

radiation monitors pending additional licensee evaluation.

R7

Quality Assurance in Radiation Protection and Chemistry Activities

a. Inspection Scope (83750)

The inspectors reviewed and discussed the licensee's process for

tracking identified radiological issues for the purpose of assessing

followup and corrective actions.

b. Observations and Findings

There had not been any licensee formal audits completed since Audit

SA-96-39(ON)(RA) dated August 27, 1996. which was previously addressed

in NRC Inspection Report 96-16. The licensee's method of tracking

radiological issues was in the PIP program. The inspectors reviewed a

number of PIPs and discussed the significance of several of the PIPs

with the RP PIP coordinator. The inspectors toured a decontamination

facility with a supervisor and discussed supervisory observations and

assessments, and corrective actions. The inspectors determined the

licensee was identifying issues of substance in the area of RP through

the PIP process, supervisory assessments, and QA audits, and was

initiating appropriate corrective action in a timely manner.

ENCLOSURE 2

45

c.

Conclusions

Based on the above reviews, it was concluded that the licensee was

identifying issues of substance for improvement in the RP area and

initiating appropriate corrective action in a timely manner.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on December 31, 1996.

Additional information regarding the two apparent violations was

provided in a phone call with licensee management on January 23, 1997.

The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

X3

Management Meeting Summary

Significant Meeting (61701)

On December 12, 1996. the licensee, several Region II inspectors, and

NRR personnel (via telecommunications) conducted a meeting onsite to

discuss the upcoming Emergency Power and Engineered Safeguards

Functional Test. The discussions focused on the unapproved procedure's

purpose, acceptance criteria, and contingencies.

Partial List of Persons Contacted

Licensee

E. Burchfield, Regulatory Compliance Manager

T. Coutu, Operations Support Manager

D. Coyle, Systems Engineering Manager

T. Curtis, Operations Superintendent

J. Davis-, Engineering Manager

W. Foster, Safety Assurance Manager

J. Ham pton, Vice President, Oconee Site

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

B. Peele, Station Manager

J. Smith. Regulatory Compliance

NRC

D. LaBarge, Project Manager

ENCLOSURE 2

46

Inspection Procedures Used

IP 71750:

Plant Support Activities

IP 71707:

Plant Operations

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 37550:

Engineering

IP 37551:

Onsite Engineering

IP 61701:

Complex Surveillance

IP 83750:

Occupational Exposure

IP 84750:

Radioactive Waste Treatment, AND Effluent AND Environmental

Monitoring

IP 92700:

Onsite Followup of Written Event Reports

IP 93702:

Prompt Onsite Response to Events

IP 71001:

Licensed Operator Requalification Program Evaluation

IP 92901:

Followup - Operations

IP 62700:

Maintenance Program Implementation

IP 55050:

Nuclear Welding Inspection

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 40500:

Effectiveness of Controls in Identifying and Resolving Problems

Items Opened, Closed, and Discussed

O

Opened

50-270.287/96-17-06

VIO

Failure to Maintain Configuration

Control - Two Examples (Sections 01.2 and

01.3)

50-270,287/96-17-07

URI

Failure to MaintainxAppendix R Valve Leads

(Section 01.4)

50-269.270,287/96-17-05

URI

In Situ Calibration of Containment High

Range Radiation Monitors (Section R2.1)

50-269,270,287/96-17-02

VIO

Failure to Perform Evaluations of Out-of

Tolerance M&TE (Section M4.1)

50-270/96-17-08

EEI

Failure to Use Procedure Administrative

Hold (Section 07.1)

50-269.270.287/96-17-03

URI

RBCU Operability Concerns Due to Wrong

Type Fuse in Control Circuit (Section

E2.2)

50-269.270.287/96-17-01

EEI

Failure To Complete A Written Safety

Evaluation Of Secondary Plant Piping Not

In Accordance With The Piping Code

Referenced In The UFSAR - Three Examples

(Sections M1.5 and E2.4)

ENCLOSURE 2

47

50-269/96-17-09

VIO

LPSW Modification did not Meet ASME

Code NDE Requirements (Section M1.8)

50-269,270,287/96-17-04

URI

Engineering Evaluation for the

Replacement of Carbon with Stainless Steel

Piping (Section M1.5)

Discussed

50-269,270,287/96-13-03

IFI

LPSW Modifications and Testing (Section

E8.4)

Closed

50-269.270,287/94-19-01

DEV

Improper Code Classification (Section

E8.1)

50-269,270,287/94-19-02

DEV

Failure to Meet UFSAR Requirements Related

to System Class Boundary Weld Inspection

(Section E8.2)

50-269,270,287/94-24-05

DEV

Improper Code Classification (Section

E8.3)

50-269,-270,287/95-12-01

IFI

Apparent UT Examiner and UT Procedure

Weakness (Section M8.1)

50-287/96-16-06

IFI

ICS Malfunction Training Results (Section

08.2)

List of Acronyms

ACB

Air Circuit Breaker

ALARA

As Low As Reasonably Achievable

ANSI

American Nuclear Society Institute

API

American Petroleum Institute

AS

Auxiliary Steam

BWST

Borated Water Storage Tank

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

CF

Core Flood

CR

Control Room

DHR

Decay Heat Removal

ECCS

Emergency Core Cooling System

ECCW

Emergency Condenser Circulating Water

EEI

Apparent Violation

EFW

Emergency Feedwater

EPSL

Emergency Power Switching Logic

EOC

End Of Cycle

EPRI

Electric Power Research Institute

ENCLOSURE 2

48

ES

Engineered Safeguards

ESV

Essential Siphon Vacuum

FDW

Feedwater

FW

Feedwater

FWDS

Field Weld Data Sheets

GL

Generic Letter

gpd

gallons per day

gpm

Gallons Per Minute

HD

Heater Drain

HDP

Heater Drain Pump

HPI

High Pressure Injection

HPSW

High Pressure Service Water

IAE

Instrumentation and Electrical

IAW

In Accordance With

ICS

Integrated Control System

IFI

Inspector Followup Item

IR

Inspection Report

ISI

Inservice Inspection

JPM

Job Performance Measure

LBLOCA

Large Break LOCA

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LOOP

Loss of Offsite Power

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

-MCC

Motor Control Center

MOV

Motor Operated Valve

MP

Maintenance Procedure

MS

Main Steam

MSRH

Moisture Separator Reheater

M&TE

Measuring and Test Equipment

NCV

Non-Cited Violation

NDE

Non-Destructive Examination

NPSH

Net Positive Suction Head

NPSHA

Net Positive Suction Head Absolute

NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

OE-

Office of Engineering

OEDB

Oconee Engineering Design Basis

OFD

Oconee Flow Diagram

ONS

Oconee Nuclear Station

00T

Out-of-Tolerance

OPS

Operations

OTSG

Once Through Steam Generator

OSW

Oconee Service Water

PCEs

Personnel Contamination Events

PH

Plant Heat

PID

Piping & Instrumentation Drawing

ENCLOSURE 2

I.

49

PIP

Problem Investigation Process

PIR

Problem Identification Report

PMT

Post Maintenance Test

PPQA

Power Piping Quality Assurance

PZR

Pressurizer

PSIG

Pounds Per Square Inch Gauge

QA

Quality Assurance

QC

Quality Control

RBCU

Reactor Building Cooling Unit

RCP

Reactor Coolant Pumps

RCA

Radiological Controlled Area

RC

Reactor Coolant

RCS

Reactor Coolant System

RFO

Refueling Outage

RP

Radiation Protection

RTD

Resistance Temperature Detector

RWP

Radiation Work Permit

SAMA

Scientific Apparatus Manufacturers Association

SDQA

Software and Data Quality Assurance

SSF

Safe Shutdown Facility

SSRH

Second Stage Reheater

SWSOPA

Service Water System Operational Performance Assessment

TB

Turbine Building

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report

USAS

United States American Standard

USQ

Unresolved Safety Question

VIO

Violation

V&V

Validation and Verification

WO

Work Order

WR

Work Request

ENCLOSURE 2