ML14191B125

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Insp Rept 50-261/89-09 on 890418-0510.Violation Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation,Maint Observation,Onsite Followup of Events & Onsite Review Committee Activities
ML14191B125
Person / Time
Site: Robinson 
Issue date: 06/08/1989
From: Dance H, Garner L, Jury K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14191B123 List:
References
50-261-89-09, NUDOCS 8907100036
Download: ML14191B125 (16)


See also: IR 05000261/1989009

Text

9REG,

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/89-09

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket Np.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: April 18 -

May 10, 1989

Inspectors:

L. W. Garner, enior Resid

In ector

Date Signed

K. R Jury,Zsident In pectotfDtSg~

Approved by:

/

K. C. Dance, Section Chief

Ddte"Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, onsite

followup of events, and onsite review committee activities.

Results:

Two violations were identified:

(1) failure to incorporate residual heat

removal design basis leakage into specifications, drawings, and procedures

following a change to the source term, paragraph 5.a; and (2) an inadequate

technical review resulted in End Path Procedure EPP-10 not containing a

precaution concerning potential safety injection pump runout with one pump

injecting into two reactor coolant hot leg loops, paragraph 2.b.

A weakness in Fuel Handling Procedure FHP-003 was observed in that an acceptance

criteria was not provided on a detachable data sheet, paragraph 2.a.

An operational weakness was observed in that an instrument channel associated

with the reactor protection system was assumed to be operable without conducting

an investigation into the reason for momentary bistable actuations, paragraph 2.c.

90C7100036. 8906.24.

PDR

ADOC 000026.1

FDC

2

Determination that EDG fuel injectors require rebuilding during the next

refueling outage is considered an example of a good predictive maintenance

program, paragraph 3.

Retrieval activities associated with a fuel assembly dropped in the spent fuel

pool was well planned, paragraph 5.b.

REPORT DETAILS

1. Licensee Employees Contacted

R. Barnett, Mainte nance Supervisor, Electrical

R. Chambers, Engineering Supervisor, Performance

D. Crocker, Supervisor, Radiation Control

  • ~D.

Crook, Senior Specialist, Regulatory Compliance

  • J. Curley, Director, Regulatory Compliance

C. Dietz, Manager, Robinson Nuclear Project

R. Femal, Shift Foreman, Operations

W. Flanagan, Manager, Design Engineering

  • W.

Gainey, Supervisor, Operations Support

  • E. Harris, Director, Onsite Nuclear Safety

D. Knight, Shift Foreman, Operations

D. McCaskill, Shift Foreman, Operations

R. Moore, Shift Foreman, Operations

  • R. Morgan, Plant General Manager

D. Myers, Shift Foreman, Operations

M. Page, Acting Manager, Technical Support

  • D. Quick, Manager, Maintenance

D. Seagle, Shift Foreman, Operations

J. Sheppard,,Manager, Operations

  • R. Smith, Manager, Environmental & Radiation Control

R. Steele, Acting Supervisor, Operations

  • H. Young, Director, Quality A-ssurance/Quality Control

Other licensee employees contacted included technicians,

operators,

mechanics, security force members, and office personnel.

  • Attended exit interview on May 17, 1989.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors observed licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements,

and that the

licensee management control

system was effectively

discharging its responsibilities for continued safe operation.

These

activities were confirmed by direct observations, tours of the facility,

interviews and discussions with licensee management

and personnel,

independent verifications of* safety system status and limiting conditions

for operation, and reviews of facility records.

Periodically, the inspectors reviewed shif t logs, operations records, data

sheets, instrument traces, and records of equipment malfunctions to verify

operability of. safety-related equipment .and compliance with TS.

Specific

2

items reviewed include control room logs, operating orders, jumper logs,

and equipment tagout records. Through periodic observations of work in

progress and discussions with operations' staff members, the inspectors

verified that the staff was knowledgeable of plant conditions; responding

properly to alarm conditions; adhering to procedures and applicable

administrative controls; and was aware of equipment out of service,

surveillance testing,

and maintenance activities in progress.

The

inspectors routinely observed shift changes to verify that continuity of

system status was maintained and that proper control room staffing

existed. The inspectors also observed that access to the control room was

controlled and operations'

personnel were carrying out their assigned

duties in an attentive and professional manner.

The control room was

observed to be free of unnecessary distractions. The inspectors performed

channel checks and reviewed component status and safety-related parameters

to verify conformance with TS.

During this reporting interval, the inspectors verified compliance with

selected LCOs. This verification was accomplished by direct observation

of monitoring instrumentation, valve positions, switch positions, and

review of completed logs and records.

Plant tours were routinely conducted to verify the operability of standby

equipment, assess.the general condition of plant equipment, and to verify

that radiological controls, fire protection controls and equipment tag out

procedures were being properly implemented.

These tours verified the

following:

the absence of unusual fluid leaks; the lack of visual

degradation of pipe, conduit, and seismic supports; the proper positions

and indications of valves and circuit breakers; the lack of conditions

-which could invalidate

EQ;

the operability and calibration of

safety-related instrumentation; and the operability of fire suppression

and fire fighting equipment and emergency lighting equipment.

The

inspectors also verified that housekeeping was adequate and areas were

free of unnecessary fire hazards and combustible materials.

In the course of the monthly activities, the inspectors included a review

of the licensee's physical security and radiological control programs.

The inspectors verified by general observation and perimeter walkdowns

that measures taken to assure the physical protection of the facility met

current requirements. The inspectors verified station personnel adhered

to radiological controls.

a. Procedure Data Sheet Does Not Provide Acceptance Criteria

During movement of spent fuel into the DSC on April 25, 1989, a

procedure weakness was noted by the inspectors.

Step 8.2.3 of

FHP-003,

revision 5, Fuel Assembly Movement in the Spent Fuel Pit,

requires hourly monitoring and recording of relative humidity on

attachment 9.2.

Neither step 8.2.3, nor attachment 9.2, provides

an acceptance criteria and actions to be taken if

the humidity

3

acceptance criteria is exceeded.

This information is provided in

section 6.0, Precautions and Limitations.

Paragraph 6.16 of this.

section states that relative humidity shall not exceed 70% during

movement of new or spent fuel.

The 70% limitation is contained in

the basis of TS, and hourly monitoring is required per TS 4.12.3.

The inspectors observed that: attachment 9.2 had been detached from

FHP-003 and that section 6.0 was not located in the spent fuel pool

area.

Subsequent to fuel movement, the inspectors inquired of an

operator, the reasoning and basis for recording the humidity

measurements. The operator completing the procedure was aware of the

70% limitation. Not providing an acceptance criteria on a data sheet

which may be removed from the document containing the acceptance

criteria constitutes a weakness in the procedure system.

b. Emergency Procedure Did Not Address SI Pump Runout

On April 4, 1989, the inspectors observed that EPP-10, Transfer to

Hot Leg Recirculation, revision 2, step 3 required both hot leg

injection valves, SI-866A and B, be opened.

Opening SI-866A and B

allows flow into the C and B RC hot leg loops, respectively.

Step

4.6 required two SI pumps be started as available. OST-154, revision

11, Safety Injection System High Head Check Valve Test, contains the

following precautions and limitations:

(1) Do not allow one SI pump to runout beyond 600 gpm or below 500

psig discharge pressure.

(2) At any time that only one SI pump is operating, one of the two

injection headers (cold leg or hot leg) must be isolated to

avoid possible pump runout.

(3) When running flow tests on the SI pumps (discharging to the

system during refueling operations) use only one hot leg path

when operating a single pump.

Two hot leg paths may be used if

two or more SI pumps are operating.

It appears that these statements are based upon a Westinghouse report

entitled Safety Injection System Test Evaluation, issued June 1974.

The report indicates that testing of one SI pump with both hot leg

valves open was "omitted since pump runout flow exceeded allowable

limit".

EPP-10 authorizes operation with only one SI pump without

precautions for potential runout. One reason for EPP-10 revision in

September 1988, was to address that use of one SI pump is an allowed

configuration in some cases.

An inadequate technical review of this

revision was the major contributor in failing to incorporate this

precaution into the procedure.

Failure to address potential runout

with only one SI pump operating is a violation: EPP-10 Inadequately

Addresses Potential Pump Runout With Only One SI Pump Injecting Into

Two Hot Legs, 89-09-01.

4

The inspectors reviewed the applicability of the one SI pump

precaution to injection into three cold legs.

This configuration

would be the expected alignment during a design 'basis LOCA. In 1988,

Westinghouse performed a calculation which demonstrated that this

operating mode would be acceptable; however, the 1974 flow test did

not conduct testing which demonstrated this flow configuration was

acceptable. The inspectors' review of the 1974 flow test results for

other pump combinations into the cold legs, indicates one SI pump

injection into three cold legs may result in operation approaching

runout conditions.

In the exit interview, the licensee indicated that they believe that

runout would not occur for neither the three cold leg injection

pathway nor for the dual hot leg pathway.

However, they did agree

that existing available information supports that a limitation should

be placed on one SI pump injection into the dual hot leg, pathway.

Additional review is required to determine what testing, if any,

should be performed to support operation of the system in the current

configuration. This is an URI: Determine If One SI Pump Injection

Into Three Cold Legs Should Be Demonstrated, 89-09-02.

c. Instrument Evaluations To Determine Operability Needs Enhancement

An operational weakness was observed, in that, an instrument channel

associated with the reactor protection system was assumed to be

operable without conducting an investigation into the reason for

momentary bistable actuations.

The cause was assumed to be known

because of a recent similar problem with a redundant instrument-loop.

Investigation later determined that the instrument was operable. The

details of this issue are discussed below:

On May 3, 1989, the inspectors were informed that RC loop C low flow

instrument

FT-436

appeared to be operating ' erratically.

The

instrument was spiking low 12 to 15 times per shift, thereby causing

momentary low flow bistable actuations.

This condition had begun

approximately three days earlier, after the redundant transmitter

FT-435 had experienced a similar problem.

The FT-435 problem had

been corrected by venting. the transmitter.

The inspectors were

informed that part of the air bubble which had been in FT-435 had

apparently moved into the FT-436 portion of the common high pressure

line. When corrective actions were addressed, the licensee indicated

that they believed that the bubble would dissolve. When asked if the

spiking frequency was decreasing, the licensee indicated that they

believed that it was; however, the number of occurrences had not been

recorded nor trended.. Furthermore, the inspectors were informed that

no troubleshooting had been performed because the spiking was in the

conservative direction and was similar to the FT-435 problem.

The

'inspectors pointed out that there were no alarms or other installed

means by which it could be determined if spiking was occurring in the

5

non-conservative direction.

In addition, spiking of this nature

could be the result of an electrical problem with the instrument

loop.

Comparison of the RTGB indicator with the other two redundant

instruments revealed that FT-436 was varying only slightly from the

other two channels. The inspectors questioned if the instrument's

response time would meet that assumed in transient analysis, and what

the basis was for not declaring the instrument out of. service (i.e.,

tripping the channel to maintain the degree of redundancy specified

by TS 3.5.1.3 and TS Table 3.5-2).

Since the observed spiking was in

the conservative direction (the channel trips), OMM-001, Operations

Conduct of Operations, revisons 19, section 5.14.2.1 was considered

to apply. This section in part addresses channels deviating by a

known

constant amount.

If

this constant deviation is in a

conservative direction, an appropriate trip need not be inserted.

The inspectors do not believe that this section applies to erratic or

spiking instrumentation.

Since the ability of the instrument to

respond within the time assumed had not been addressed,

the

inspectors, after consultation with NRC

Region II

management,

informed the licensee that the channel should be considered

inoperable.

The licensee promptly declared the channel inoperable

and took the action required by TS.

On May 4, plant management

discussed the matter with the inspectors, contending that the spiking

could only occur in the conservative direction and that the

instrument tracked the other channels; therefore, they considered the

instrument was operable.

Furthermore,

since troubleshooting was

hampered by having the channel tripped, the licensee stated their

intent to return FT-436 to service.

Troubleshooting would then be

performed to determine, if possible, the exact nature of the problem

and occurrence trending would be performed. In addition, the licensee

indicated that if the spiking occurrence frequency was not decreasing,

the unit would be reduced below P-8,

the one

RCP trip bypass

permissive setpoint, and the instrument loop would be vented during

the subsequent weekend. After consulting with Region II management,

the inspectors informed the licensee that the NRC did not object to

this course of action. Subsequently, FT-436 was returned to service.

The instrument was not vented since it was spiking only three or four

times during most days. Occasionally, FT-436 would spike as many as

ten times per day. The licensee has also determined from instrument

data that there was no information which indicated that the FT-436

response time to changes in flow was adversely affected.

If the

transmitter is still spiking by the end of May, the licensee plans to

vent the instrument lines when power is decreased for turbine valve

testing.

During the exit interview, the inspectors discussed with plant

management the need to conduct a proper investigation when an

instrument loop is not functioning correctly.

In particular, a

determination needs to be made as to whether an. observed abnormal

behavior indicates an instrument loop may or may not perform its

6

function as described in transient analysis.

In the case discussed

above, the licensee, having assumed the problem was due to air in the

instrument loop, failed to evaluate if this would adversely effect

the 0.2 second instrument loop response time.

The licensee stated

that they believed that the guideline of OMM-001 had applied to

FT-436;

however,

the licensee did agree to review their current

practices in this area.

This review includes contacting other

utilities to determine what actions are typically taken to address

this type of situation. This is an IFI:

Review Actions To Be Taken

When An Instrument Loop Exhibits Random Erratic Behavior, 89-09-03.

One violation was identified within the areas inspected.

3. Monthly Surveillance Observation (61726)

The inspectors observed certain surveillance activities of safety- related

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that: precautions and

LCOs were met; the tests were completed at the required frequency; the

tests conformed to TS requirements; the required administrative approvals

and tagouts were obtained prior to initiating the tests; the testing was

accomplished by qualified personnel in accordance with an approved test

procedure; and the required test instrumentation was properly calibrated.

Upon completion of the testing, the inspectors observed that the recorded

test data was accurate,

complete,

met TS requirements,

and test

discrepancies were properly rectified.

The inspectors independently

verified that the systems were properly returned to service. Specifically,

the inspectors witnessed/reviewed portions of the following test

activities:

OST-010 (revision 9)

Power Range Calorimetric During Power Operation

OST-401 (revision 22)

Emergency Diesels

RST-001 (revision 33)

Radiation Monitor Source Checks

EST-058 (revision 4)

SI-890A and 890B Check Valve Test

The inspectors discussed with the cognizant engineer the A EDG OST-401

test data taken on May 1, 1989.

The engineer indicated that trends on

some cylinder exhaust temperatures indicate deterioration in fuel injector

performance. This does not effect operability of the EDG, and plans are in

progress to have these injectors rebuilt during the next outage.

The

inspectors consider this as an example of good predictive maintenance.

No violations or deviations were identified within the areas inspected.

4. Monthly Maintenance Observation (62703)

The inspectors observed several maintenance activities of safety-related

systems and components to ascertain that these activities were conducted

in accordance with approved procedures, TS, and appropriate industry codes

7

and standards.

The inspectors determined that these activities did not

violate LCOs, and that redundant components were operable. The inspectors

also determined that activities were accomplished by qualified personnel

using approved procedures; QC hold points were established where required;

required administrative approvals and tagouts were obtained prior to work

initiation; proper radiological controls were adhered to; and the effected

equipment was properly tested before being returned to service.

In

particular, the inspectors observed/reviewed the following maintenance

activities:

MST-901 (revision 19)

Radiation Monitoring System

OWP-004 (revision 6)

Containment Spray

WR/JO 89-AEPM1

Repair SI-890B Bonnet to Body Leak

On May 2, 1989, while observing maintenance activities on SI-890B, the B

CV spray pump discharge check valve, the inspectors observed that the only

post-maintenance testing specified on WR/JO 89-AEPM1 was an examination

for external leakage from the valve while at operating conditions.

When

the inspectors questioned if this was all the testing to be performed,

.they were informed that no testing of SI-890B other than that required by

Section XI of the ASME code was required. ASME Section XI requires only a

leak check after a gasket replacement and per a code exemption request

response from the NRC,

disassembly and visual examination of the full

stroke of the check valve is sufficient to comply with Section XI

requirements. These requirements were specified to be performed by the

WR, and it was determined no further testing, such as a partial flow test,

was required. Item 9.,a of Regulatory Guide 1.33, revision 2, as required

by TS 6.5.1.1.1.a,

requires that maintenance which can affect the

performance of safety-related equipment be performed in accordance with

written procedures appropriate to the circumstances. 10 CFR 50, Appendix B,

Criterion V, requires instructions to include appropriate quantitative

or qualitative acceptance criteria for determining that important

activities

have been satisfactorily accomplished.

The inspectors

considered a partial flow test was necessary as a qualitative acceptance

criteria after partial disassembly of the valve.

This item was discussed

with the Plant Manager.

Prior to returning the B CV spray loop to

service, the licensee performed additional testing.

The licensee agreed that additional testing requirements should have been

included on the WR since the valve was almost completely disassembled. A

PLP-026 investigation is to be conducted in order to determine the root

cause for the failure, to include appropriate test requirements, and to

determine what actions, if

any, are required to prevent recurrence.

However, during the exit interview, the licensee stated that a partial

flow test would not be required for a limited work scope such as removal

and replacement of a bonnet with an attached flapper assembly (assuming

the flapper assembly is not disassembled or adjusted).

The inspectors

believe that this type of activity would require partial flow testing.

This belief is based in part on Attachment 1, paragraph 2, of GL 89-04,

8

Guidance on Developing Acceptable Inservice Testing Programs,

issued

April 3, 1989.

This paragraph requires a partial flow test be performed,

if possible, after reassembly. Resolution of what constitutes disassembly

and reassembly of a check valve is considered an URI:

Resolve What

Degree Of Maintenance Activity On Check Valves Warrants A Partial Flow

Test After Reassembly Per GL 89-04, 89-09-04.

No violations or deviations were identified within the areas inspected.

5. Onsite Followup of Events at Operating Power Reactors (93702)

a.

RHR Pit Leakage Design Basis Could Not Be Met During Accident

Conditions

On April 6, 1989, the resident office was notified that a potential

common mode failure of both RHR trains may exist. due to flooding.

The

RHR

pump bays are separated by a concrete shield wall

approximately eight feet high at its lowest point.

The RHR pump

motor pedestal is approximately four feet high. As part of the RHR

system design basis document review, the question was raised whether

the wall was intended to serve a flood protection function.

As

constructed, the wall did not provide separation since the two pump

bays were connected at floor level by a six-inch diameter open ended

pipe. During resolution of this issue on April 10, 1989, the PNSC

and NED determined that the system design basis to detect and isolate

a 50 gpm leak into the RHR pit within 30 minutes did not appear to be

obtainable during accident conditions.

Later that evening, it was

confirmed that during the recirculation mode of operation, a passive

failure resulting in a leak could not be isolated, since high

radiation levels would not allow personnel access to certain manual

valves required for isolation. Anticipated radiation fields could be

as large as several thousand Rem/hr.

Potential passive failures

considered included: flange leaks, pipe.cracks, packing leaks, tube

leaks, and pump seal leaks on either the SW, CCW or RHR components in

the RHR pit. Anticipated radiation levels were based upon the source

term associated with TMI Action Item II.B.2, Shielding Modifications

for Vital Area Access.

Manual valves which would be inaccessable

after initiation of the recirculation phase include:

RHR-752A and B,

the RHR pump suction valves; SW-75,

-76,

-77,

and -78,

the RHR room

coolers'

(HVH-8A and B) supply and return valves; and CC-768A and B,

the RHR pump seal coolers' supply valves.

Inherent to the accident

scenario is the assumption that the RHR pit sump pumps would be

unavailable since they are not environmentally qualified and are not

powered from emergency onsite power.

At the time of discovery, the unit was shutdown for removal of a

loose part from C S/G (see Inspection Report 89-08).

Prior to

resuming power operations, procedure changes and temporary modifica

tions were implemented to address the issue until a permanent solution

is identified.

Independence of the pump bays was established by

9

grouting the six inch diameter pipe.

EPP-9, Transfer to Cold Leg

Recirculation, was revised to:

(1) secure SW to the RHR room coolers

by closing SW-75,

-76,

-77 and -78; (2) isolate the RHR pump suction

lines from one another by closing either RHR-752A or B; and (3)

install a temporary RHR pit level measuring system.

Temporary

modification 89-709 supplied two level devices to be installed by

operators.

Each device, one for each bay, consists of a float, a

cable and counterweight.

The float is to be lowered into the

RHR pump bay,

the cable suspended over a pulley system and the

counterweight hung adjacent to a level scale painted on a wall

outside the RHR pit.

The above mentioned items are to be completed

immediately prior to initiating RHR recirculation. A revision to the

EPP-Foldouts was made to require hourly monitoring of the temporary

level system. A new procedure, EPP-24, Isolation of Leakage in the

RHR Pump Pit, was issued on April 13, 1989.

This procedure provides

instructions on the use of the level system to determine which bay

contains the leak and the steps required to isolate the leak while

still maintaining one RHR pump operating.

The licensee described

this event in LER 89-008.

The acceptability of continued operation until the next refueling

outage based on the above described actions is documented in JCO

89-05. The inspectors reviewed the JCO and associated engineering

evaluations.

Two specific items addressed in the JCO were the

leakage from the CCW and SW systems.

The RHR pump vendor indicated

that the

RHR

pump seals could operate indefinitely at the

temperatures anticipated during the recirculation phase of an

accident. However, it

was considered prudent to have the RHR pump

seal coolers in service; therefore, it

was decided to continue to

supply CCW to the seal coolers during the recirculation phase of an

accident. This was based in part on the determination that leakage

from the CCW lines supplying the

RHR pump seal coolers was a

relatively small contributor to core melt frequency for the assumed

event.

The acceptability of removing the

RHR room coolers from

service by securing service water to HVH-8A and B is documented in EE 88-080.

EE 88-080 was developed to support JCO 88-002, approved

July 1, 1988.

JCO 88-002 addressed operation of the RHR pumps under

post LOCA conditions without HVH-8A and B in service.

HVH-8A and B

were assumed to fail since no

EQ package had been developed to

address the effect of radiation on the fan motors (see Inspection

Report 88-16). JCO 88-002 and EE 88-080 had been previously reviewed

by the inspectors.

The acceptability of these evaluations to the

current issue was confirmed.

The inspectors witnessed shift training on the revised EPP-9 and

newly issued EPP-24.

This training included a field walkdown to

identify the location of manual

valves which would require

manipulation. Additionally, the inspectors witnessed simulation of

the revised section'of EPP-9.

Problems encountered during the

simulation were adequately addressed by the licensee.

These actions

were completed prior to unit restart on April 15, 1989.

10

The UFSAR does not address the design basis statement that an

operator can detect and isolate a 50 gpm leak within 30 minutes.

UFSAR Chapter 6, section 6.3.2.5.5, Recirculation Loop Leakage, does

state that valving is provided to permit the operator to individually

isolate each RHR pump. Manually operated valves RHR-752A and B are

the valves required for isolation of RHR pumps A and B, respectively.

As described in the preceding paragraphs,

these valves are not

accessible due to postulated radiation levels after initiation of

recirculation.

Hence,

the existing RHR configuration does not

reflect the design as described in the UFSAR; however, it appears

that the RHR pit was considered accessible when the plant was

licensed.

Statements contained in analysis WCAP-12070 indicate that

this area is accessible for maintenance on a RHR pump when the other

pump is operating in the recirculation mode.

This analysis was

issued in December

1988 as a compilation of original design

information. This compilation is based upon both documentation and

personal recollections.

The licensee believes that the source term

used in the original plant shielding analysis would support the

statements contained in WCAP-12070.

As discussed previously, the

radiation levels now anticipated are based upon analysis performed to

comply with TMI item II.B.2.

The licensee's review of these.later

calculations indicated that there is a large amount of conservatism

in this analysis.

Thus,

they believe if

this analysis were

reperformed, the areas required for leakage isolation may be

accessible.

Statements provided in WCAP-12070 are the only documented basis

identified to date which indicate that a 50 gpm leak into the RHR pit

must be isolable.

The time criterion is based upon the calculated

time available to isolate a 50 gpm leak prior to RHR motor damage.

The volume in each pump bay (below the RHR motor pedestal) is 200

cubic feet; thus a 50 gpm leak must be isolated within 30 minutes.

The assumption in the calculation was that the two RHR pump bays were

separated. This was not the as-found configuration since the pump

bay sumps were connected by a six-inch diameter pipe. The connection

had probably existed since plant construction.

In a response to NUREG 0737 Item II.B.2, dated December 31, 1980,

the licensee stated:

"This response to NUREG 0737 Item II.B.2

together with the CP&L responses to NUREG 0578 dated December 31,

1979, and supplemented March 31,

1980,

constitutes CP&L's complete

response on this item.

CP&L considers this item to be.complete."

Neither this response nor its referenced documents address the RHR

leakage detection and isolation design criteria.

Hence, during.

implementation of II.B.2 adequate design controls were

not

established to assure design basis were properly incorporated into

design documents and plant procedures.

In summary, the licensee's design basis document review determined

that available information indicates inaccessibility to areas

required to isolate a 50 gpm leak into the RHR pit during the

11

recirculation phase of an accident.

No credit is taken for the RHR

pit sump pumps since they are not powered from emergency onsite power

sources. Futhermore, even if power was available, the installed sump

pumps and associated control circuits cannot be assured to remain

functional since the EQ of these items have not been demonstrated.

Under the above described conditions, a 50 gpm leak or less would

eventually result in sufficient flooding to damage both RHR pump

motors. The loss of both RHR trains during the recirculation phase

would result in the loss of all ECCS capability.

The licensee has

initiated compensating action in hardware and administrative controls

until a long term fix has been approved and implemented during the

next refueling outage. The failure to assure that design basis are

correctly .translated into specifications, drawings, and procedures is

a violation of 10 CFR 50 Appendix B Criterion III: Design Control

Measures Were Not Adequately Established To Assure That The 50 Gpm

Leak Isolation Capability Design Basis Was Correctly Translated Into

Specifications,

Drawings,

and Procedures

For The

RHR System,

89-09-05.

b. Spent Fuel Assembly Disengaged From Grapple During DSC Loading

On April 26, 1989, at approximately 12:35 a.m., a spent fuel assembly

became uncoupled from the fuel handling tool and fell against the

spent fuel pool wall.

Personnel working in the spent fuel pool area

immediately evacuated the area.

Air samples and radiation monitors

showed no increase over normal background levels.

At the time of

occurrence,

a spent fuel assembly was being loaded into a DSC in

preparation for onsite storage in the ISFS facility.

Five fuel

assemblies

had been successfully loaded into the DSC when the

operator experienced difficulty in positioning the sixth.

After

several attempts, the assembly caught on the top DSC grid-work while

being lowered. The grapple cable slackened, the assembly separated

from the tool,

and fell against the spent fuel pool wall.

The

inspectors estimated that the assembly formed a 40 degree angle with

the wall and incurred a 25 degree torsional twist.

The licensee

prepared a special procedure and successfully retrieved the assembly

on April 26.

The assembly was positioned in the fuel elevator for

inspection; no damage was observed. The assembly has been returned

to the spent fuel pool storage location.

The inspectors reviewed the special procedure, attended the PNSC

which approved the special procedure,

and attended the pre-job

briefing.

The inspectors determined that the retrieval activity was

well

planned and contained sufficient safety precautions

and

contingency plans.

Visual inspection of the top nozzle blocks of the assemblies which.

were contained in -the DSC at the time of the event revealed no

assembly damage had occurred.

As a result of the fuel assembly

falling onto the DSC, the DSC was unloaded and removed from the spent

12

fuel pool for repair of minor damage to the grid-work. After repair,

the DSC was returned to the spent fuel pool and successfully loaded

with seven spent fuel assemblies on April 28 without any further

difficulties.

The assembly which fell against the wall will remain

in the spent fuel pool until its final disposition is decided.

Investigation into the event revealed that the most probable cause

was that the tool had been engaged on the leaf springs instead of in

the top nozzle block.

Measurements of the tool revealed no

dimensional reason for the failure to properly engage the assembly.

Thus, either an obstruction had caused the improper latching or an

operator error had occurred. The actual root cause is still being

evaluated;

however,

a potential contributor to this event was

determined to be a loss in fuel handling efficiency.

During the

previous two refueling outages,

fuel movements were performed by

contract personnel.

Immediate corrective action consisted of

retraining the operating crews on fuel handling techniques and

manipulations prior to performing additional fuel movements,

including removal of the five assemblies from the damaged DSC. Also,

potentially contributing to this event was bowing of the fuel

assembly. This phenomena can hinder latching an assembly. Bowing is

much more pronounced on older assemblies due to the pattern in which

they were irradiated.

Long term corrective action is being developed as part of the PLP-026

incident review.process. This is an IFI:

Review Corrective Actions

To Be Addressed In PLP-026 Associated With A Dropped Fuel Assembly,

89-09-06.

One violation was identified within the areas inspected.

6. Onsite Review Committee (40700)

The inspectors evaluated certain activities of the PNSC to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements. In particular, the inspectors attended

the April 26,

1989 PNSC concerning the dropped fuel assembly.

It was

ascertained that provisions of the TS dealing with membership and review

process were met.

Previous meeting minutes were reviewed to confirm that

decisions and recommendations were accurately reflected in the minutes.

No violations or deviations were identified within the areas inspected.

7. Exit Interview (30703)

The inspection scope and findings were summarized on May 17, 1989, with

those persons indicated in paragraph 1.

Excluding item 89-09-05, the

inspectors described the areas inspected and discussed in detail the

inspection findings listed below and in the report summary.

The licensee

13

was informed of item 89-09-05 on June 1, 1989.

Licensee's comments.

concerning particular items are discussed in the appropriate paragraph.

Proprietary information is not contained in this report.

Item Number

Description/Reference Paragraph

89-09-01

VIO -

EPP-10 Inadequately Addresses Potential Pump

Runout With Only One SI Pump Injecting Into Two Hot

Legs, paragraph 2.b.

89-09-02

URI

-

Determine If One SI Pump Injection Into Three

Cold Legs Should Be Demonstrated, paragraph 2.b.

89-09-03

IFI -

Review Actions To Be Taken When An Instrument

Loop Exhibits Random Erratic Behavior, paragraph 2.c.

89-09-04

URI -

Resolve What Degree Of Maintenance Activity

On Check Valves Warrants a Partial Flow Test After

Reassembly Per GL 89-04, paragraph 4.

89-09-05

VIO

-

Design Control Measures Were Not Adequately

Established To Assure That The 50 GPM Leak Isolation

Capability Design Basis

Was Correctly Translated

Into Specifications, Drawings, and Procedures For The

RHR System, paragraph 5.a.

89-09-06

IFI -

Review Corrective Actions To Be Addressed In

PLP-026 Associated With The Dropped Fuel Assembly,

paragraph 5.b.

8. Acronyms and Initialisms

ASME

American Society of Mechanical Engineers

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CP&L

Carolina Power & Light Company

CV

Containment'Vessel

DSC

Dry Shielded Canister

ECCS

Emergency Core Cooling System

EE

Engineering Evacuation

EDG

Emergency Diesel Generator

EPP

End Path Procedures

EQ

Environmental Qualifications

EST

Engineering Surveillance Test

FI

Flow Indicator

FT

Flow Transmitter

FHP

Fuel Handling Procedure

GL

Generic Letter

gpm

Gallons Per Minute

14

HVH

Heating Ventilation Handling

IFI

Inspector Followup Item

JCO

Justification For Continued Operation

LCO

Limiting Condition for Operation

MST

Maintenance Surveillance Test

NED

Nuclear Engineering Department

NRC

Nuclear Regulatory Commission

OMM

Operations Management Manual

OST

Operations Surveillance Test

OWP

Operations Work Procedure

PLP

Plant Procedure

PNSC

Plant Nuclear Safety Committee

QC

Quality Control

RC

Reactor Coolant

RCP

Reactor Coolant Pump

Rem/hr

Roentgen Equivalent Man/Hour

RHR

Residual Heat Removal

RST

E&RC Surveillance Test

S/G

Steam Generator

SI

Safety Injection

SW

Service Water

TS

Technical Specification

UFSAR

Updated Final Safety Analysis Report.

  • URI

Unresolved Item

WCAP

Westinghouse Corporation Atomic Power

WR

Work Request

WR/JO

Work Request/Job Order

.Unresolved

items are matters about which more information is required to

determine whether they are acceptable or may involve violations or

deviations.