ML14181A885
| ML14181A885 | |
| Person / Time | |
|---|---|
| Site: | Robinson |
| Issue date: | 03/06/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML14181A884 | List: |
| References | |
| 50-261-97-01, 50-261-97-1, NUDOCS 9703270304 | |
| Download: ML14181A885 (34) | |
See also: IR 05000261/1997001
Text
U.S. NUCLEAR REGULATORY COMMISSION
REGION II
Docket No:
50-261
License No:
Report No:
50-261/97-01
Licensee:
Carolina Power & Light (CP&L)
Facility:
H. B. Robinson Unit 2
Location:
2112 Old Camden Rd.
Hartsville, SC 29550
Dates:
December 29, 1996 - February 8, 1997
Inspectors:.
B. Desai, Senior Resident Inspector
J. Zeiler, Resident Inspector
C. Payne, Region II Inspector (Sections 01.2,
05.1)
W. Rankin, Region II Inspector (Sections R1.1,
R1.2, R1.3, R1.4)
Management:
R. Crlenjak, Acting Deputy Director, Division of
Reactor Projects, Region II
J. Jaudon, Director, Division of Reactor Safety,
Region II
B. Mallett, Director, Division of Nuclear
Material, Region II
K. Barr, Branch Chief, Plant Support Branch
Approved by:
M. Shymlock, Chief, Projects Branch 4
Division of Reactor Projects
Enclosure 1
9703270304 970306
ADOCK 05000261
G
EXECUTIVE SUMMARY
H. B. Robinson Power Plant, Unit 2
NRC Inspection Report No. 50-261/97-01
This integrated inspection included aspects of licensee operations,
maintenance, engineering, and plant support. The report covered a six-week
period of inspection. In addition to inspections conducted by resident
inspectors, it includes the results of an effluents inspection conducted by a
regional inspector, and an operator requalification program inspection
conducted by a regional inspector.
Operations
The plant was operated in a safe manner. A power reduction and
subsequent increase was appropriately conducted. Power was reduced to
approximately 65 percent to accommodate testing of the Turbine.governor
and stop valves (Section 01.1).
The conduct of operations in the control room was professional and.well
managed. The operators were-alert'and attentive to their duties. Shift
turnover process and associated meeting were effective and efficient
tools for transferring control of.plant operations from one crew to the
next. Though in effect for over one year, the operator workaround
associated with the Inventory Critical Safety Function Status Tree did
not impose undue operational difficulty or complexity for the operators
(Section 01.2).
A walkdown and assessment of the readiness of the Residual Heat Removal
(RHR) System to perform its Emergency Core Cooling System function
determined that the system was well maintained, conformed with plant and.
Updated Final Safety Analysis Report piping drawings, and was aligned in
- accordance with applicable operating procedures. A weakness was
identified in the corrective actions for addressing chronic seat leakage
problems with the RHR heat exchanger control and bypass valves.
(Section 02.1).
Several factors including weak procedures and lack of attention to
detail and self-checking resulted in a Containment gaseous release
- without a source check. However, the effluent release was monitored by
operable instrumentation and the conditions did not significantly change
in the Containment. The safety significance was minor and this issue
was classified as a Non-Cited Violation (NCV) (Sections 03.1 and 08.1)
The License Operator Requalification program continued to meet the NRC
requirements of 10 CFR 55.59. Licensed operator and instructor
performance was satisfactory. The training and evaluation simulator
scenarios were comprehensive and challenged the knowledge, skills, and
abilities of the operators. The training staff was effective at finding
weaknesses in the operator's technicalskills; however, additional
emphasis on correlating training and evaluation with actual plant
operations and management expectations is needed. The Nuclear
Assessment Section assessment was an adequate sampling of the Training
department performance and that the weakness identified with exam
2
security was not an initial or requalification training compromise issue
.(Section 05.1).
The onsite review functions of the Plant Nuclear Safety Committee were
conducted in accordance with Technical Specifications, were well
coordinated, and meeting topics were thoroughly discussed and evaluated
(Section 07.1).
Maintenance
The licensee failed to adequately evaluate and take timely corrective
actions for a degraded Reactor Protection System (RPS) relay problem
prior to its'eventual failure. This issue was identified as a NCV.
Concern was noted with the lack of adequate engineering involvement and
work priority scheduling when repeated anomalous RPS relay operation
occurred during previous testing. A detailed failure investigation
effectively determined the cause of the relay failure. While several
minor work practice deficiencies associated with the relay maintenance
was identified, licensee corrective actions were comprehensive and
included actions to address these deficiencies (Section M1.2).
The planning, preparations, and actual replacement activities associated
with a.failed test relay in the Engineered Safety Features Actuation
System (ESFAS) logic circuitry was conducted in a controlled and safety
conscious manner. The Plant Nuclear Safety Committee was thorough in
its review of.the safety impact of performing the replacement on-line
and installing a jumper in the ESFAS logic circuitry to maintain Train B
ESFAS available during the replacement evolution. Good management
oversight of all phases of the evolution was observed (Section M1.3).
Continued managementattention, including permanent resolution,.is
warranted on flow instrument FI-110 which continues to experience
repetitive failures. However, capability of the boron injection path
through the line was not impacted (Section M2.1).
The failure to adequately implement Technical Specification Surveillance
requirements for testing the Nuclear Instrumentation Power Range
Channels was identified as a NCV (Section M8.1).
Engineering
A 10 CFR 50, Appendix J related issue pertaining to the personnel
airlock testing was identified by the licensee and was determined to be
an example of good questioning attitude. However, it surfaced a
weakness in the modification evaluation process. The personnel airlock
was immediately leak rate tested with satisfactory results. The failure
to test the air lock in accordance with 10 CFR 50, Appendix J was
considered a NCV (Section E2.1).
The identification of the testing inadequacies related to the Auxiliary
Feedwater (AFW) pumps was considered as an example of good questioning
3
attitude. The failure to test the AFW pumps in accordance with the
requirements of ASME Section XI was considered a NCV (Section E2.2).
The Robinson Engineering Site Services organization was realigned such
that the engineering manager now reports to the Director of Site
Operations (Section E6.1).
Plant Support
Primary and Secondary water chemistry parameters were being maintained
well below regulatory and administrative limits (Section R1.1).
An effective program continued to be maintained to monitor and control
liquid and gaseous effluent to small percentages of regulatory and
administrative limits, thereby minimizing the potential dose at the site
boundary (Section R1.2).
The program for monitoring external exposure and tracking dose within
the Radiation Controlled Area (RCA) was determined to be effective.
However, for outside the RCA, one Unresolved Item (URI) was identified
based on the failure to adequately demonstrate accurate and reasonable
dose monitoring and dose assignment practices and procedures for
radiation workers onsite (Section R1.3).
)
The radiological controls program was being effectively implemented with
.good occupational exposure controls demonstrated. The As Low As
Reasonably Achievable (ALARA) program was effectively reducing total
site dose which achieved in 1996 a record low level for the site in an
outage year. The licensee experienced a relatively high level of
personnel contamination events in 1996 which represents a continuing
challenge in the licensee's radiological control program (Section R1.4).
An URI relative to RCA quarterly survey data and the consequences
involved was identified (Section R1.5).
2
The inspector observed shift turnover in the control room and attended
associated shift turnover meetings. Operators were noted to arrive
30-45 minutes before their shift to familiarize themselves with current
plant conditions and shift activities that had occurred since they last
operated the plant. The inspector observed that these reviews were
thorough, comprehensive and included a complete control board walkdown.
The shift turnover meetings were chaired by the offgoing Shift
Supervisor and participants included all members of the oncoming shift.
These meetings were well run by the Shift Supervisor and were observed
to be informative, succinct and brief. Typically, the meetings lasted
no longer than 15 minutes.
The inspector reviewed the operator workaround that exists relative to
the Reactor Coolant System (RCS) Inventory CSFST. The condition
periodically manifests when power is below approximately 70 percent and
it involves the RCS Inventory CSFST turning into "YELLOW" path (priority
lower than 'RED" which requires immediate operator attention) and is
indicative of the RCS dynamic head below 100 percent. The condition
becomes an operator workaround because it requires manual inventory
tracking, by the operator, of the inventory CSFST. The inspector
determined that procedures were in place to check the validity of all
off-normal CSFSTs. The inspector did note.that dne recently certified
Shift Technical Advisor (STA) was not aware that this workaround was in
effect and was unfamiliar with the circumstances associated with its
cause. During interviews, the inspector determined that control room
operators (including the STA noted above) would respond properly when
this situation arises. This problem is scheduled for corrective action
by June 1, 1997.
c. Conclusions
The inspector concluded that the conduct of operations in the control
room was professional and well managed. The operators were alert and
attentive to their duties. The inspector also concluded that the shift
turnover process and associated meeting were effective and efficient
tools for transferring control of plant operations from one crew to the
next. Though in effect for over one year, the inspector concluded that
the operator workaround associated with the Inventory CSFST did not
impose undue operational difficulty or complexity for the control room
operators.
02
Operational Status of Facilities and Equipment
02.1 Engineered Safety Feature System Walkdown of Residual Heat Removal
a. Inspection Scope (71707)
The inspector performed a walkdown of accessible portions of both trains
of the Residual Heat Removal (RHR) System. The actual plant
configuration was compared to plant drawings, the Updated Final Safety
Analysis Report (UFSAR) description, and system lineup procedures. RHR
System lineup procedures completed prior to startup from the previous
3.
refueling outage were reviewed to ensure that the system had been
aligned properly. The status of outstanding maintenance was reviewed to
verify RHR System readiness for performing its Emergency Core Cooling
System (ECCS) function.
b. Observations and Findings.
The inspector performed a walkdown of accessible portions of the RHR
System to compare the actual plant configuration with plant piping
drawing No. 5379-1484, Rev. 33 and UFSAR.Figure 6.3.2-2, Flow Diagram
Safety Injection System, Sheet 2. Each accessible valve in the RHR
System flowpath was verified from Control Board indication or by field
visual observation to be in its proper position as specified by
operations lineup procedures. The applicable procedures for placing the
RHR System in its ECCS standby mode included Operating Procedure
(OP)-201, Residual Heat Removal System, and General Procedure (GP)-02,
Cold Shutdown to Hot Subcritical at No Load Tavg. The inspector
reviewed the completed copies of these procedures to verify that they
had been properly performed prior to startup from the previous refueling
outage. No discrepancies were identified from these reviews.
The inspector noted no significant material condition problems during
walkdowns of accessible portions of the RHR System. A minor boric acid
buildup and small liquid buildup just below the "A" RHR Pump vent line
was identified and discussed with operations personnel.
The licensee
initiated a work request to investigate and repair this leak.
The inspector reviewed all open work items (Action and Work Requests)
for the RHR System. There were a total of 12 outstanding items, the
majority of these involved minor insulation and/or boric acid buildup
problems. None of these items were considered to be significant enough
to present any system performance problem.
The inspector witnessed portions of the Ticensee performance of
Inservice pump and valve testing for the "A" RHR Pump. Testing was
performed in accordance with Operations Surveillance-Test (OST)-251-1,
RHR Pump A and Components Test, Rev. 3. The inspector reviewed the pump
operating data collected during the test and verified that it met the
procedure acceptance criteria. All of the pump operating parameters
were well within their acceptance values indicating good pump
performance.
During review of OST-251-1, the inspector learned that the RHR heat
exchanger outlet and bypass valves, HCV-758 and FCV-605, were
experiencing a high amount of seat leakage. HCV-758 controls flow
through the heat exchangers and FCV-605 controls flow that bypasses the
heat exchangers. These valves are used to control the cooldown and
heatup rates during decay heat removal mode of RHR operation. The
leakage would not result in any degradation of the safety-related
accident mitigation function of the RHR system. Based on discussions
with the operators, this chronic -seat leakage problem had existed for
years and the operators had repeatedly identified the condition as
4
causing RHR temperature control complications. While this problem had
been tracked by operator workarounds in the past, it was currently not
on the work around list. The inspector discussed this problem with.the
RHR system engineer and licensee management. It was learned that the
licensee had made several attempts over the years to reduce the leakage
with little success and had decided to cope with the problem as it
existed. The inspector noted, however, that operating procedures and
operator training materials failed to account for this problem. This
leakage problem has contributed to at least one event where
inappropriate operator actions to compensate for the leakage caused the
Low Temperature Overpressure Protection system to actuate. The
inspector concluded that the licensee failure to consider these
procedural and training changes to be a weakness when it was decided to
cope with the leakage condition. The licensee initiated CR 97-00284 to
address the inspector's concern.
c.
Conclusions
The inspector determined that the ECCS function of the RHR System was
well maintained,-conformed with plant and UFSAR piping drawingsiand was
aligned in accordance with applicable.operating procedures. The
inspector identified a weakness in the licensee's corrective actions for
addressing chronic seat leakage problems with the RHR heat exchanger
control and bypass valves.
03
Operations Procedures and Documentation.
03.1 Gaseous Release Without Appropriate Source Check on Radiation Monitor
a. Inspection Scope (71750 and 71750)
The inspector reviewed, discussed, and assessed the circumstances
surrounding a Containment gaseous release that was made on January 10,
1997, without performing a source check on Containment Radionoble Gas
Monitor (R-12), as required by Technical Specification (TS) 4.19.2.1.
CR 97-00059 was generated by the licensee as a result of this incident.
Licensee Event Report (LER) 50-261/97-01-00, TS Violation Due to Missed
Surveillance Requirements, was submitted as a result of this incident.
b. Observations and Findings
Outside air temperature variations and its effect on Containment
pressure/temperature and instrument air bleed, necessitates periodic
venting of Containment atmosphere. TS 3.6.2 requires that Containment
pressure be maintained less than 1.0 psig. Control room operators
monitor containment pressure and when the need arises, vent the
Containment using Operations Procedure (OP)-921, Containment Air
Handling, and Effluents Monitoring Procedure (EMP)-022, Gaseous Waste
Release Permits. The containment air is then vented through the plant
vent and is accomplished by opening the Containment Pressure -Relief
Switch as-directed in OP-921.
15 4.19.2.1, requires that a source check
be performed on R-12 prior to initiating the release to ensure accurate
5
monitoring of the ongoing release. The source check is performed using
EMP-022.
On January 10, 1997, the Containment was vented (release # 97-0010-G)
without the performance of a source check on R-12 as required by
TS 4.19.2.1. The venting lasted several minutes before the operator
performing the evolution realized that the required source check had not
been performed. The source check was subsequently completed
satisfactorily. The failure to perform a source check as required by
TS 4.19.2.1 prior to.a release is considered a violation.
A licensee investigation determined that several factors contributed to
the problem. These included:
procedural weakness in that OP-921 did
not specifically require verification that a source check has been
performed prior to initiating the release; .layout and sequence of steps
in EMP-022 such that the step associated with the source check was not
obvious to the operator performing the evolution; the unfamiliarity with
the evolution on part of the operator who had recently been licensed;
and the lack of an operations crew brief prior to initiation of the
release.
The licensee initiated several corrective actions to preclude recurrence
of this incident. These included, planned revision to EMP-022 and
OP-921 to better reflect the need for the source check. The inspector
confirmed that there was no significant change in Containment
radiological conditions during the release. Further, R-14 (Plant Vent
monitorlocated down stream of R-12), R-11 (Containment particulate
monitor), as well as R-12 were operable, including the capability to
automatically isolate the Containment release if activity above pre-set
limits was detected.
c. Conclusions
The inspector concluded that several factors including weak procedures,
and a lack of attention to detail resulted in a Containment gaseous
release without a source check. However, the effluent release was
monitored by operable instrumentation and the conditions did not
significantly change in the Containment. Consequently, the safety
significance was minor. Licensee corrective actions were prompt and
adequate. This licensee-identified and corrected violation is being
treated as a Non-Cited Violation (NCV) consistent with Section VII.B.1
of the NRC Enforcement Policy. This NCV will be documented as NCV.
50-261/97-01-01: Failure to Perform A Source Check Prior to Gaseous
Release.
6
05
Operator Training and Qualification
05.1 Licensed Operator Regualification Training
a. Inspection Scope (71001)
The inspector reviewed the licensee's requalification program for
licensed reactor operators and senior reactor operators. The inspector
also reviewed and discussed the Nuclear Assessment Section (NAS)
Training and Qualification Assessment report (R-TQ-96-01) dated
January 16, 1997.
b. Observations and Findings
LICENSED OPERATOR REQUALIFICATION (LOR).
The inspector observed the
licensed operator requalification annual operating and biennial written
examinations for shift and staff operators. The inspector noted that
the evaluation scenarios were well developed and exercised the operators
on a wide variety of normal, abnormal, and emergency conditions. The
inspector noted that both Operations, and Training department managers
were actively involved in evaluating operator performance during the
simulator scenarios. The inspector also observed .that the post-scenario
critiques by the training staff were generally accurate and identified
significant performance deficiencies, as appropriate. A good practice
was noted involving the use of specific examples being listed to
describe individual operator errors or weaknesses. This practice helps
the operator to better relate his actual performance to management's
standard or expectation.
Several areas for improvement were identified by the inspector and
communicated to Training management. The inspector noted a difference
in operator communications during simulator scenarios and the cues given
i-n job performance measures (JPMs). For example, an operator was
observed during the simulator examination giving the Inside Auxiliary
Operator (AO) an order to locally start the "B"
EDG by "placing the
control switch to local and punch the start button." In contrast,
JPM-IP-048 (rev. 4) is the same task but directs the operator to
"locally start 'B'
Emergency Diesel Generator (EDG) and energize
emergency electrical bus E-2 in accordance with procedure EPP-1,
Attachment 6."
Attachment 6 contained many more actions and alternative
actions for the operator to perform than just going to local control and
pushing the START button. The expected level of operator performance
was significantly different for each of these orders, yet they were both
intended to accomplish the same action. This inconsistency has the
potential for providing negative operator training. Similarly, the
inspector noted that role play of operator communications was not always
conducted during performance of the inplant JPMs. When role play was
done, management expectations and standards for communications were
reinforced with the operators. When role play was not done,
communications were poor and conduct of the JPM was awkward. The
inspector also identified that the initiating cue for JPM-IP-026
.
(Rev. 5), "Establish Charging Flow to the RCS per DSP-002" was
7
incomplete. The cue stated that Auxiliary Building actions of DSP-002
were complete up to step 19. In fact, the actions of DSP-002,
Attachment 3, were complete up to step 19. This oversight did not cause
any noticeable operator performance problem because the operator was
handed a copy of the attachment as a part of the JPM.
SIMULATOR FIDELITY. The inspector identified one simulator fidelity
problem and an administrative oversight during the inspection. During
Resident Inspector review of the RHR System (see Section 02.1), it was
noted that the RHR heat exchanger bypass and outlet valves were
experiencing a high amount of seat leakage. The licensee had made
several attempts to reduce this leakage with little success, and had
determined to cope with the problem as it existed. The inspector found
that the licensee's training materials and simulator modeling failed to
account for this problem. Operator training did not adequately prepare
the operators for handling the condition. The licensee submitted a CR
in response to this finding and initiated efforts to upgrade the
training materials and simulator modeling. This was one example of poor
interdepartmental communications and poor recognition of the impact of
an equipment problem on operator performance.
Training Administrative Procedure TAP-409, (rev. 1), "Conduct of
Simulator Training and Evaluation", paragraph 8.7.7 required a periodic
control room review to ensure that control room equipment that will be
out of service, or has special operating requirements, for longer than
90 days, was identified and reflected in the setup of the simulator.
The inspector identifi.ed that control room "blue dots" were not
evaluated .for applicability contrary to Training management expectation.
The licensee submitted a Condition Report in response to this finding
and initiated a review of control room blue dots for applicability and
scheduled training of the instructors regarding the scope of this
requirement.
NAS ASSESSMENT. The Nuclear Assessment Section issued a report (R-TQ-.
96-01) on January 16,'1997 documenting the findings of their review of
the Robinson Training and Qualification Program. Three weaknesses were
identified in the report. The inspector noted that the third weakness
concerned the potential of compromising exam security, or the perception
of it, due to Robinson's Training management practices. Of the three
examples discussed, one was an interpretation error of examination
security made by supervision that was corrected by management the same
day. A second example involved the use of a training instructor as a
simulator operator during requalification examinations, thus violating
the exam security agreement. The inspector determined that this issue
was not an exam security problem because the simulator operators have no
control over the content of the examination. Training management has
modified their 'training instructions to correct this confusion in the.
exam security agreement. The last example entailed the availability of
the exam banks to the operators. The inspector found that only the
open-reference question bank (Part B) was actually made available.
Existing NRC guidance from NUREG-1021, "Operator Licensing Examiner
Standards" allows exam banks to become uncontrolled (i.e., do not have
8
to impose extraordinary control or security measures) once the Part B
bank reaches 350 questions. The Robinson Part B bank was 800 questions.
NUREG-1021 does not-preclude release of licensee exam banks to their
operators. The report also noted that both Brunswick and Harris nuclear
plants have discontinued releasing their banks. This inconsistency
between corporate licensees should be resolved. The NRC does not
encourage release of examination banks to the operators because it could
lead them to "study to the bank" rather than learning and understanding
the lesson material.
c. Conclusions
The inspector concluded that the licensee's LOR program continues to
meet the NRC requirements of 10 CFR 55.59. Licensed operator and
instructor performance was satisfactory. The training and evaluation
simulator scenarios were comprehensive and challenged the knowledge,
skills and abilities of the operators. The training staff was effective
at finding weaknesses in the operator's technical skills; however,
additional emphasis on correlating training.and evaluation with actual
plant operations and management expectations is needed.* The inspector
concluded that the NAS assessment was an adequate sampling of the
Training department performance and that the weakness identified with
exam security was not an initial or LOR training compromise issue.
07
Quality Assurance In
Operations
07.1 Plant Nuclear Safety Committee Meeting
.a. Inspection Scope (40500)
The inspector evaluated certain activities of the Plant Nuclear Safety
Committee (PNSC) to determine whether the onsite review functions were
conducted in accordance with TS and other regulatory requirements.
b. Observations and Findings
The inspector periodically attended PNSC meetings during the report
period. The presentations were thorough and the presenters readily
responded to .all questions. The committee members asked probing
questions and were well prepared. The committee members displayed
understanding of the issues and potential risks. The inspector
considered that the chairman appropriately limited discussion to the
issues and their safety ramifications.
c. Conclusions
The inspector concluded that the onsite review functions of the PNSC
were conducted in accordance with TSs. The PNSC.meeting attended by the
inspector was well coordinated and meeting topics were thoroughly
discussed and evaluated.
9
08
Miscellaneous Operational Issues (92901)
08.1 (Closed) LER 50-261/97-01-00, TS Violation Due to Missed Surveillance
Requirements: This LER was issued on February-9, 1997 because a source
check was not performed on RMS-12 prior to a containment pressure relief
on January 10, 1997. The details associated with the event are
discussed in Section 03.1 of this report. The LER is closed.
II.-Maintenance
M1
Conduct of Maintenance
M1.1 General Comments
a. Inspection Scope (61726 and 62707)
The inspector observed all or portions of the following maintenance
.related WRs/JOs and surveillances and reviewed the associated
documentation:
OST-401-2
Emergency Diesel Generator B Slow Speed Start,
Rev. 2
OST-251-1
RHR Pump A and Component Test, Rev. 3
WR/JO 97-AAGX1
Replace RPS Relay TR-2
WR/JO 96-AGJCI
Troubleshoot and RepairESFAS Relay TC-412C1
- X(B)
OST-201-A & B
MDAFW System Component
OST-202
SDAFW System Component Test
EST-10
Containment Personnel Airlock Leakage Test
E
MST 20 & 21
Reactor Protection Logic Train A & B At Power
- (Monthly)
b. Observations and Findings
The inspector observed that these activities were generally performed by
personnel who were experienced and knowledgeable of their assigned
tasks. Work and surveillance procedures were present at the work
location and being adhered to.
Procedures provided sufficient detail
and guidance for the intended activities. Activities were properly
authorized and coordinated with operations prior to start. Test
equipment in use was calibrated, procedure prerequisites were met,
system restoration was completed, and surveillance acceptance criteria
were met.
c. Conclusions
The inspector concluded that maintenance and surveillance activities
were performed satisfactorily. More specific details and observations
made of these activities were documented in other sections of the
report.
10
M1.2 Reactor Protection System Relay Coil Binding Failure
a. Inspection Scope (62707)
The inspector reviewed the events, causal factors and corrective actions
taken in response to the abnormal operation of the Reactor Protection
System (RPS) relay associated with Loop 1 Overtemperature Delta
Temperature (OTDT) beginning December 27, 1996, the relay's subsequent
failure on January 15, 1997, and eventual replacement on January 16.
b. Observations and Findings
On January 15, Instrumentation and Control (I&C) personnel were
performing MST-021, Reactor Protection Logic Train "B"
At Power
(Monthly)*.
This test verifies the proper operation of Train B.RPS logic
in accordance with the surveillance requirements of TS Table 4.1-1.
During testing, the Loop 1 OTDT reactor trip bistable failed to actuate
when the test signal was initiated. While repeating this portion of
testing two additional times-without success, I&C personnel observed
that the associated Train B RPS relay (TC-412C1-X(B)) for Loop 1 OTDT
failed to "drop out" as expected.. This was determined via .visual
observation that the relay's mechanical plunger remained in the
retracted position.
The on-call manager and I&C Supervisor were contacted and a decision was
made to replace the relay. Following this decision, I&C personnel
noticed that a paper label surrounding the relay plunger was peeled up
and was in contact with the plunger. I&C personnel believed that this
paper could have interfered with the operation of the plunger. With
permission of the Shift Supervisor, the paper was removed. When the.
plunger was touched while removing the paper, the relay dropped out.
The relay was tested repeatedly with successful results. Following
discussions with the on-call manager and I&C Supervisor, it was decided
not to replace the relay. Train B RPS was restored to normal after
completing testing in accordance with MST-021 successfully.
.The next morning, licensee management decided that further analysis of
the relay was necessary and directed the relay to be replaced. When the
first relay electrical power lead was lifted during the replacement
activity, the relay failed to drop out as expected. The relay changed
state as the second lead was lifted.
The relay was sent offsite for a detailed materials analysis to
determine the cause of the failure. The results of this analysis
determined that the failure was caused by internal binding of the
relay's contact assembly due to an.attachment pin contacting the inside
surface of the relay casing, and not the paper label.
This pin is used
to attach the contact assembly to the moving core and was most likely
positioned incorrectly during initial manufacture and had gradually
worn.
On January 21, the inspector reviewed the maintenance activities
conducted the night of January 15 and discussed these activities with
the individuals involved. The inspector identified the following
maintenance work practices deficiencies/concerns associated with these
activities as follows:
Engineering was not contacted and involved in the relay failure
discussions and subsequent.maintenance troubleshooting,
A work request was not initiated and planned for use at the work
site for the activities performed by maintenance personnel.
While
I&C personnel later documented the removal of the paper around the
relay plunger under an existing work request (96-AGJC1), this work
request had not been at the job site during the conduct of the
activity,
Work Request 96-AGJC1 was initiated on December 27, 1996, for a
previously identified problem with the relay, but had not been
coordinated with the scheduling of relay testing,
Contact cleaner used to spray safety-related electrical equipment
was not controlled under the licensee's chemical.control program
and apparently had not been evaluated for use in safety-related
applications,
The Control Room operator's logs stated that the test switch
associated with Loop 1 OTDT was sprayed with contact cleaner when
in fact the RPS relay had been sprayed,
After discussing these problems with the Plant Manager, licensee
management directed that the "non-significant" Condition Report
(97-00092), which was initiated by operations when the relay failed, be
upgraded to "Significant." A team was formed to investigate the events
and decisions leading to the relay replacement. The inspector reviewed
CR 97-00092 and determined that the licensee had thoroughly reviewed
this incident and had initiated or planned comprehensive corrective
actions which included the issues identified by the inspector.
Licensee investigation of the relay failure revealed that problems had
been experienced with the relay operation prior to its failure on
January 15. Details of these occurrences are discussed as follows:
On December 27, 1996, while operations was performing testing
associated with procedure OST-005 to verify proper reactor.trip
bistable operation, there was a delay of approximately one minute
between'when Loop 1 OTDT trip bistable switch was taken from trip
to normal and when the bistable light extinguished. The bistable
was placed in the trip condition and the evolution was repeated
with similar delay in bistable light response. Since no delay in
bistable light illumination was noted each time the bistable was
tripped, the operators-considered Loop 1 OTDT still operable.
Work Request 96-AGJC1 was initiated to investigate/repair the
12
problem and the on-call Manager was notified, however, engineering
personnel were not alerted to the incident. Work Request 96-AGJC1
was placed on the Emergent Work List on December 30, 1996, but was
subsequently removed the following day due to the assumption that
the problem was only with the relay picking up on re-energization.
On December 31, similar delay in Loop 1 OTDT bistable light
response was observed when maintenance was conducting routine
testing in accordance with Maintenance Surveillance Test (MST)-003
to verify proper Tavg and Delta-Temperature RPS channel response.
The evolution was repeated with similar but less delayed bistable
light response.
On January 11, 1997, during testing associated with OST-005,
normal bistable light response was reported for Loop 1 OTDT.
On the morning of January 15, the delayed response was observed
while maintenance was performing MST-003.
The inspector concluded from the above occurrences that the licensee had
not been sensitive to indications of relay degradation prior to the
failure on January 15. Operations did not recognize the potential for
relay failure and assumed that the observed delays in the relay picking
up was not a condition that could have resulted in relay failing to
perform its safety function. The inspector considered it a weakness on
the part of operations that this decision regarding relay operability
was made without the benefit of -engineering support.
c. Conclusions
The failure to adequately evaluate and take timely corrective actions
for a degraded RPS relay is considered as a violation. This licensee
identified violation is being treated as a Non-Cited Violation,
consistent with Section VII.B.1 of the Enforcement Policy. This item
was identified as NCV 50-261/97-01-02: Inadequate Corrective Actions
for RPS Relay Degradation. The inspector was concerned with the lack of
adequate engineering involvement and work priority scheduling when
repeated anomalous relay operation was observed during testing. The
licensee performed a detailed failure investigation and effectively
determined the cause of the relay failure. The inspector identified
several minor work practice deficiencies associated with the relay
maintenance on January 15.. Licensee corrective actions were
comprehensive and included actions to address the inspector identified
deficiencies.
M1.3. Replacement of Failed Reactor Safeguards Test Relay TR-2
a. Inspection Scope (61726 and 62707)
The inspector reviewed the licensee's activities associated with the
failure and subsequent replacement of Train B Engineered Safety Features
13
Actuation System (ESFAS) test relay TR-2 associated with the Main .Steam
Isolation logic circuitry.
b. Observations and Findings
On January 16, maintenance personnel were performing routine
surveillance testing of the Train B ESFAS logic circuitry. During this
testing, test relay TR-2, associated with the Main Steam Line Isolation
logic, failed. While failure of this test relay did not result in Train
B ESFAS being inoperable, it prevented the completion of TS required
monthly testing of the Train B Main Steam Isolation logic circuitry.
The licensee determined that the relay needed to be replaced, however,
based on the ESFAS wiring configuration, power could not be removed from
the test 'relay without deenergizing most of the other Train B ESFAS
logic circuitry. In addition, the licensee's TSs did not provide an
allowable outage time for a train of ESFAS to be inoperable. The
licensee recognized that in order to replace the relay, the action
requirement of TS 3.0 would have to be entered since Train B ESFAS would
be considered inoperable.
As a conservative measure, the licensee determined that a jumper could
be placed around the test relay during the replacement evolution to
preclude the actual loss of electrical power to the rest of Train B
ESFAS circuitry. This jumper would allow all but the Main Steam
Isolation function of Train B ESFAS to be capable of operating.
Engineering developed Special Procedure (SP)-1389, Installation of
Jumper for Replacement of Relay TR2, to control the replacement
activity. The inspector reviewed SP-1389 and its associated safety
evaluation. The procedure contained detailed step-by-step instructions
- and precautions for controlling the evolution. The safety evaluation
thoroughly considered the safety impact of installing the jumper,
potential for the jumper to fall off, size of the jumper wiring, etc.
The licensee determined that there would be no impact on the ability of
the opposite train of ESFAS performing its safety function during the
evolution. Based on discussions with engineering personnel
knowledgeable of the ESFAS circuitry and an independent .review of the
ESFAS logic circuitry, the inspector concluded that the licensee had
adequately evaluated the impact of installing the jumper.
A special PNSC meeting was convened at 7 p.m. on January 21 to discuss
the relay replacement activity and draft copy of SP-1389. The inspector
attended the meeting and noted that management.thoroughly discussed the
safety impact of performing the activity on-line. Several good
enhancements were identified to SP-1389. As an added conservative
measure, management directed the relay replacement activity to be
treated as an infrequently performed evolution requiring a Management
Directed Monitor (MDM) to oversee the evolution. The Manager of
Operations was selected as the MDM.
On January 22, the inspector witnessed activities associated with the
relay replacement. The inspector determined that activities were well
14
controlled and had a high level of management attention and oversight.
Personnel responsibilities, precautions, and contingency plans for
unexpected responses, were thoroughly discussed at a pre-job briefing
that was held in the Control Room by personnel involved in the
evolution. The MDM monitored and provided oversight of activities from
the Control Room. The inspector determined that the actual replacement
activity was performed by knowledgeable maintenance personnel who
properly followed SP-1389 and other applicable maintenance requirements.
No problems were encountering during the replacement evolution.
Continuous communication was maintained throughout the activity between
personnel in the Control Room and ESFAS relay room. Good sensitivity
was evidenced by both maintenance and operations personnel involved with
the replacement activities to limit the amount of time in TS 3.0 while
still expediting the completion of work. The total time TS 3.0 was
entered was only one hour and 35 minutes. As required by NRC reporting
requirements, the licensee planned to submit an Licensee Event Report
for the TS 3.0 entry. The day after the relay was replaced, the
licensee identified a minor documentation problem associated with
maintenance personnel failing to update the PMTR database following work
completion.
The inspector examined the failed relay after it was removed. The
relay's control wiring at the junction of the coil housing was badly
burned. The system engineer believed that the relay coil had shorted as
a result of failed control wiring insulation. The failed relay was sent
offsite for further investigation into the cause of the coil failure.
The inspector planned to review the results of the licensee's
investigation as part of followup to the LER.
.c. Conclusions
The inspector concluded that the licensee's planning, preparations, and
actual replacement activities associated with the failed test relay in
the ESFAS logic circuitry were conducted -in
a controlled and safety
conscious manner. The PNSC was thorough in its review of the safety
-impact of performing the replacement on-line and installing a jumper in
the ESFAS logic circuitry to maintain Train "B" ESFAS available during
the replacement evolution. Good management oversight of all phases of
the evolution was observed.
M2
Maintenance and Material Condition of Facilities and Equipment
M2.1 Control Room Emergency Boration Flow Indicator Maintenance Issues
a. Inspection Scope (62707)
During the course of routine plant tours and meeting attendance, the
inspector noted that there appeared to be repetitive problems with the*
control room emergency boratioh path Flow Indicator (FI)-110.
15
b. Observations and Findings
The inspector noted that FI-110 had failed several times in the last
month. A review of maintenance history confirmed that FI-110 had a
history of failures, primarily attributable to boric acid buildup and
its affect on the flow transmitter. Robinson utilizes highly
concentrated boric acid (approximately 20,000 ppm boron) in the Chemical
and Volume Control System (CVCS). FI-110 indicates emergency boration
flow in the control room and is -utilized in the Emergency Operating,
Procedures following a reactor trip, as well as in response to an
Anticipated Transient Without a Scram (ATWS). The inspector expressed
concern to the Plant Manager with regard to the repetitive failures.
Additionally, the inspector discussed the issue with the Maintenance
Rule engineer to assess implications.
The inspector was informed that the problems with the flow indications
did not result in the emergency boration flow path being inoperable and
the alternate paths as well as alternate means of determining flow .
through the emergency boration flowpath were available. Further, the
EOPs, were structured such that not having FI-110 operable in the
control room did not significantly impair recovery actions.
Consequently, licensee process associated with the maintenance rule did
not affect FI-110 related problems. However, the licensee is carrying
this item as a subset of other issues pertaining to the Boric Acid
System in the "TOP TEN" equipment issues list for appropriate
prioritization and attention.
c.
Conclusions
The inspector concluded that continued management attention, including
permanent resolution, is warranted on Fl-110 which continues to
experience repetitive failures.
M8
Miscellaneous Maintenance Issues (92902)
M8.1
(Closed) LER 50-261/96-01-00, Condition Prohibited by Technical
Specifications Due to Inadequate Testing of Nuclear Instrumentation
Power Range channels: This issue involved the licensee's identification
of a discrepancy.in the surveillance tests for the Nuclear
Instrumentation (NIS) Power Range (PR) channels. TS Table 4.1-1,
Item 1, required a bi-weekly continuity check of the NIS PR channel
signals to the RPS Delta-Temperature input circuitry. Due to a
misinterpretation of the surveillance requirement, this testing was not
being completed properly. While licensee procedures tested the
operation of the bistables for Delta-Temperature, the actual signal
being sent from the NIS channels to the Delta-Temperature circuitry was
not being checked. On February 13, 1996, the associated circuitry was
tested and found to be operable.
The licensee revised all surveillance test procedures intended to
perform this overlap circuitry check. The inspector reviewed these
procedures and verified that the changes had been completed. This
16
included a review of Operations Surveillance Test (OST) procedures
OST-001, -002, -003, -004, and -005. No discrepancies were identified.
The licensee determined that this missed surveillance was an isolated
occurrence. The inspector noted that this surveillance discrepancy was
identified by the Team tasked with converting the current TSs to the
improvedStandard Technical Specifications. As part of the Team's
activities, the adequacy of all other TS Table 4.1 instrumentation
surveillances were reviewed. This review was completed in 1996. While
several other minor problems were identified during this review, there
were no other missed TS surveillances or items of non-compliance
identified. This LER was closed.
The inspector determined that licensee's failure to perform bi-weekly
checks of the signal from the NIS PR channels to the Delta-Temperature
circuitry was a TS violation. This licensee-identified and corrected
violation is being treated as a NCV, consistent with Section VII.B.1 of
the NRC Enforcement Policy. This issue was identified as NCV 50-261/97
01-03:
Failure to Adequately Implement TS Surveillance Requirement.
III. Engineering
E2
Engineering Support of Facilities and Equipment
E2.1
Containment Airlock Testing
a.
Inspection Scope (37551)
On January 10, 1997, the licensee identified that the Containment
Airlock (personnel hatch) had not been tested in accordance with the
requirements of 10 CFR 50, Appendix J. Upon discovery, a condition
report (97-00063) was initiated and TS 4.0 was invoked, which required
the testing to be successfully completed within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. The airlock
was satisfactorily tested on January 10, 1997 and compliance with 10 CFR
50 Appendix J was achieved. LER 50-261/97-02-00 was submitted on
February 10, 1997 as a result of this condition.
b. Observations and Findings
Technical Specification 6.12 requires that a containment leakrate
testing program be established to implement the requirements of 10 CFR
50 Appendix J. 10 CFR 50 Appendix J, Containment leakage testing.
requirements include Type B,-local leakrate testing of the Containment
Airlock. These include, the leakrate test prior to initial fuel
loading, at 6-month intervals, and following opening the airlock when
containment integrity is required'. Additionally, per section
III.D.2.(b).(ii) of 10 CFR Appendix J, if the airlock is opened during
periods when containment integrity is not required by plant TS (for
example during certain periods of a refueling outage), then the airlock
is required-to be tested at the end of such periods at pressure not less
than Pa (40 psig) utilizing a full volume test.
17
Prior to the 1996 refueling outage (RFO 17), Robinson utilized the
continuous Penetration Pressurization System (PPS) as an alternative to
full-volume testing required by 10 CFR 50, Appendix J, Section
III.D.2.(b)(ii).
This methodology was accepted by the NRC, as stated in
correspondence from the NRC Office of Nuclear Reactor Regulation to the
licensee in a letter dated August 14, 1989.
A plant modification was implemented during the 1996 refueling outage
that modified the PPS system from a continuous to an intermittent
monitoring system. This modification was performed, primarily due to
maintenance and upkeep related problems with the PPS system. The 10 CFR
50.59 evaluation associated with the modification did not appropriately
interpret and incorporate the basis for the PPS system and its use as an
alternate to the testing requirements of 10 CFR 50, Appendix J, Section
III.D.2.(b)(ii). When the PPS system was modified, the reinstatement of
the requirement to perform a full-volume test as required.by Section
III.D.2.(b).(ii) was not recognized. Consequently, following RFO 17,
the containment airlock was not subjected to a full volume test.
Upon discovery of non-compliance on January 10, 1997, TS 4.0 was entered
which required that the volume test be successfully completed within 24
hours. The licensee successfully tested the airlock utilizing procedure
EST-10, Containment Personnel Airlock Leakage Test (Semiannual).
Following the test, the total Type B and C leakage was 55,276.5 sccm.
The acceptance criteria is less than .6La of 85,629 sccm.
Though the results were within the acceptance criteria, the leakage
through the airlock was noted to be above what the licensee had been
noting during the similar test that is performed at a six-month
frequency. Consequently, the licensee performed troubleshooting to
identify the source of the increased leakage. No direct source.was
identified. Additionally, during the performance of EST-10, the
licensee noted that the administrative acceptance criteria was.set
conservatively based on historically low leakage through the airlock.
This administrative limit was not met; however, as mentioned above, the
total leakage remained below the Appendix J limit of'.6 La.
c.
Conclusions
The inspector concluded that the identification of this issue was an
example of good questioning attitude. However, it surfaced a weakness
in that the modification evaluation was not thorough. The licensee
aggressively performed troubleshooting to identify the potential source
of increased leakage through the airlock. The 10 CFR 50 Appendix J
.
leakage limits were met. The failure to test the airlock in accordance
with Appendix J Section III.D.2.(b)(ii) was identified as a violation.
This licensee-identified and corrected violation is being treated as a
NCV, consistent with Section VII.B.1 of the NRC Enforcement Policy.
This issue was documented as NCV 50-261/97-01-04:
Failure to Conduct
Containment Airlock Testing.
18
E2.2
Auxiliary Feedwater Pump Testing
a. Inspection Scope (61726, 37551, and 40500)
On January 15, 1997, the licensee identified that the two Motor Driven
Auxiliary Feedwater (MDAFW) pumps and the one Steam Driven Auxiliary
Feedwater Pump (SDAFW) had not been appropriately tested in accordance
with American Society of Mechanical Engineers (ASME)Section XI
requirements. An operability evaluation was performed which concluded
that the pumps were operable. Condition Report 97-00081 was initiated
by the licensee to resolve this issue.
b. Observations and Findings
The AFW pumps are tested on a monthly and refueling basis, as required
by TS 4.8, to demonstrate operability. Further, TS 4.0.1 requires that
the test be performed in accordance with ASME Section XI, Article
IWP-3000, Inservice Test Procedures. With regard to the test method,
IWP-3000 requires that the system resistance be varied until either the
measured differential flow or the differential pressure equals the
corresponding reference value. The reference value is established
during pre-operational testing or during the initial inservice run
during power.operation. All subsequent test results are then compared
to the reference value, and any change from the reference value is
requiredto be evaluated for possible indication-of pump degradation.
Additionally, TS 4.8 Bases states that the AFW pumps will be tested by
recirculation.
Testing.procedures OST-201-.A & OST-201-B, MDAFW System Component Test
Train "A" & Train "B", and OST-202, SDAFW System Component Test
accomplish the monthly testing.requirements at Robinson. The A-MDAFW
pump was run with a forward flow of approximately 100 gpm established
through Flow Transmitter (FT)-1424. FT-1424 measures forward flow to
the three Steam Generators (S/Gs). A minimum flow recirculation line
(to the Condensate Storage Tank) upstream of FT-1424 was maintained open
during the performance of OST-201. This minimum flow recirdulation line
did.not have any flow indication. Similarly, the B-MDAFW was tested
utilizing FT-1425 and the flow through the minimum flow recirculation
was not being.measured. After establishing forward flow, the pump
suction and discharge pressures as well as other pump data were
obtained. The SDAFW pump was tested with all flow directed through the
recirculation line, i.e.,.no forward flow to the S/G. The SDAFW pump
utilizes the same recirculation line (i.e. without flow indication) as
the MDAFW pumps. The pump speed, differential pressure, and vibration
data were obtained. AFW pump tests during the refueling outage are
performed through-procedures OST-206, and OST-207 for the MDAFW and
SDAFW pumps. The refueling pump tests comprises of a full flow (to the
S/G), and similar to the monthly tests, the recirculation flow was not
being measured.
The problem with the MDAFW pump testing-methodology was that though a
reference value of 100 gpm was established each time during pump
a *19
testing, the recirculation flow during the pump run was not measured.
Consequently, if that unmeasured recirculation flow changed, potential
pump degradation would not have been detected as required by ASME
Section XI.
With regard to the SDAFW flow, pump speed was utilized'as
the reference value, which was not commensurate with the recommendations
of ASME section XI, IWP 3000. The failure to test the A and B MDAFW
pumps and the SDAFW pump in accordance with ASME Section XI is
considered a violation.
The licensee formally evaluated the testing methodology to determine
operability of the pump. Based on historic test data, the licensee had
confidence that the pumps had not exhibited indications of degradation.
Notwithstanding, an Engineering Service Request (ESR 9700028) was
originated to determine operability.
The monthly test data reviewed
from March 1992 (from 56 tests) for the A MDAFW pump indicated that the
pump differential pressure had been measured between 1391.5 gpm and
1421.7 psi.
No discernable trends were noted, in the oil analysis, or
vibration and temperature data. Similarly, no discernable trends were
noted on the B MDAFW and the SDAFW pumps. Further, the licensee
reviewed the full flow test results performed during refueling with
similar conclusions. Based on this review, the licensee concluded that
the two MDAFW and the SDAFW pumps were operable.' However, the current
flow rates through the recirculation line remained indeterminate.
To obtain current recirculation flow rates, the licensee installed an
externally mounted "Controlotron" flow measuring devise and performed
OST 201-A&B and OST 202. Current licensee plans to comply with the ASME
section XI code are to revise the monthly test procedures, OST 201 and
OST 202, to measure and trend recirculation flow data through the
Controlotron flow device. -For the MDAFW pumps, pump data will be
collected prior to establishing forward flow.
Further, the licensee plans to establish pump flow reference points
during the next refueling outage or an event requiring shutdown.
Following the establishment of.the reference point, the licensee will
utilize the guideline established by NUREG-1482, Guidelines for
Inservice Testing at Nuclear Power Plants, Position 9. This will allow
the licensee to measure the recirculation.flow only during the refueling
tests. The licensee will then continue to perform the monthly tests as
they had prior to the identification of this issue.
The licensee also discussed the circumstances surrounding this issue
with the NRC staff during the IST workshop held in Region II on
February 5, 1997. The NRC staff may incorporate this issue as an
example in the guidance that is planned to be issued relative to IST.
c. Conclusions
The inspector concluded that licensee identification of this issue is
considered as an example of good questioning attitude. The failure to
test the AFW pumps in accordance with the requirements of ASME
Section XI is identified as a violation. This licensee-identified and
20.
corrected violation is being treated as a NCV, consistent with
Section VII.B.1 of the NRC Enforcement Policy. This issue was
documented as NCV 50-261/97-01-05:
Inappropriate Testing of the AFW
pumps.
E6
Engineering Organization and Administration.
E6.1 Engineering Management Realignment
Effective, February 3, 1997, the Robinson Engineering Support Section
(RESS) organization was realigned such that the RESS Manager now
directly reports to the Site Operations Director.
E7
Quality Assurance in Engineering Activities
E7.1 Special UFSAR Review
.A recent discovery of a licensee operating their facility in a manner
contrary to the UFSAR description highlighted the need for a special
focused review that compares plant practices, procedures and/or
parameters to the UFSAR descriptions. While performing the inspection
discussed in this report, the inspector reviewed selected portions of
the UFSAR that related to the areas inspected. The inspector verified
that for the select portions of the UFSAR reviewed, the UFSAR wording
was consistent with the observed plant practices, procedures and/or
parameters.
E8
Miscellaneous Engineering Issues (92903)
E8.1 (Closed) LER 50-261/97-02-00, Technical Specification Violation Due to
Inadequate Surveillance Test: This LER was issued by the licensee on
February 9, 1997 due to a discovery by plant engineering personnel on
January 10, 1997 regarding a 10 CFR Appendix J required surveillance not
being conducted. The details associated with the issued are discussed
in Section E2.1 of this report. This LER is closed.
IV. Plant Support
R1
Radiological Protection and Chemistry Controls
R1.1 Water Chemistry Controls
a. Inspection Scope (84750)
The inspector reviewed implementation of the licensee's water chemistry
control program for monitoring primary and secondary water quality. The
water chemistry program was evaluated against the specific requirements
of TS 3.1.6 which specifies concentrations of dissolved oxygen (DO) and
chloride in the Reactor Coolant System (RCS), TS 3.1.4 which specifies
that total specific activity of the reactor coolant be limited to less
than or equal to one microcurie/gram dose equivalent iodine (DEI), and
21
Table 4.1-2 of TS 4.1 which specifies required sampling frequencies for
these parameters. Licensee implementation of a Secondary Water
Chemistry Program in accordance with Section 3.G (1) of the Plant
Operating License was also evaluated.
b. Observations and Findings
The inspector reviewed Carolina Power and Light Chemistry Procedure
CP-001, "Chemistry Monitoring Program", Revision No. 42, dated
October 5, 1996, and determined that it included provisions for sampling
and analyzing reactor coolant at the prescribed frequency for the
parameters required to be monitored by TSs. Action levels and responses
for out of limit secondary chemistry parameters were also reviewed -as
described in licensee procedure CP-005, "Secondary Chemistry Corrective
Action". These procedures included provisions for monitoring primary
and secondary water quality based on established industry guidelines and
standards. Although the Electric Power Research Institute (EPRI)
guidelines for PWR primary and secondary water chemistry are not
requirements, the inspector used these guides as references for
evaluating the effectiveness of the licensee's program. The inspector
noted that the referenced licensee procedures .listed the sampling
frequency and typical values for each parameter to be monitored. Action
levels applicable to various operational modes were given where
appropriate. Guidance was also provided for actions to be taken if
analytical results exceeded prescribed limits. The inspector determined
that the above guidance and procedures were consistent with applicable
TS requirements and EPRI guidelines.
The inspector also reviewed chemistry statistical analysis reports,
primary and secondary chemistry data, and related data trend plots and
records of analytical results for selected parameters at power
operations during the period July 6, 1995 through December 1996. The
parameters selected included dissolved oxygen, chloride, fluoride,
sulfate, and dose equivalent lodine-131 in reactor coolant, and
dissolved oxygen, iron, sodium, hydrazine, and sulfate in secondary
systems. Those parameters were maintained well within TS limits,
licensee administrative limits, and within EPRI guidelines for the
specific chemistry parameters examined during power operations.
c. Conclusions
Based on the above evaluation, the inspector concluded that the
licensee's water chemistry control program for monitoring primary and
secondary water quality at specified surveillance frequencies had been
implemented in accordance with the licensee's TS requirements for PWR
water chemistry.
- . 2
22
R1.2 Semiannual Radioactive Effluent Release Report
a. Inspection Scope (84750)
TS 6.9 requires the licensee to submit periodic Semiannual Radioactive
Effluent Release Report covering the operation of the facility during
six months of prior operation. Data on solid radwaste shipments was
also provided in the report and evaluated. The inspector evaluated the
data to identify adverse effluent trends and increases in estimated
,doses to the public from effluents, if any, and explain these trends in
the context of operational experience.
b. Observations and Findings
The effluent data presented below were compiled from the licensee's
effluent release reports for the years 1994, 1995, and 1996. The
inspector evaluated the supporting raw data for the effluent release
report covering the years 1994, 1995, and 1996 with emphasis on
identifying any elevated release trends or data anomalies. As shown in
the effluent release summary below, the amount of actiVity released
during 1994, 1995, and 1996 in liquid effluent streams remained
relatively stable, at low levels, and well within release limits. The
amounts of activity released during 1996 as fission gases, iodides, and
particulates in gaseous effluents was also at low levels and within
release limits. Minor variances in gaseous effluent parameters within
operational limits were identified between 1995 and 1996 indicative of
normal steady state power operations. The small increase in gaseous
particulate curies between 1995 and 1996 is attributable to chipping and
painting in various rooms of the plant. No abnormal releases were
identified during the period.
Robinson Radioactive Effluent Release Summary
1994
1995
1996
Abnormal Releases
Liquid
0
0
0
Gaseous
0
0
0
Activity Released (curies)
a.
Liquid
1. Fission and Acti-
5.32E-2
8.76E-2
7.97E-2
vation Products
2. Tritium
2.16E+2
9.93E+2
9.89E+2
3. Gross Alpha
< LLD
< LLD
< LLD
b.
Gaseous
1. Fission and Acti-
5.70E+1
2.67E+0
1.27E+1
vation Gases
2. Iodides
8.18E-7
1.35E-5
3.59E-7
3.-Particulates
2.53E-6
7.74E-6
3.58E-5
4. Tritium
5.58E+0
1.47E+1
. 16E+0
23
The inspector evaluated 1995 and 1996 hypothetical maximum annual dose
estimates to a member of the public located .at the site boundary from
radioactive materials in gaseous and liquid effluents. The doses for
1996 from airborne and liquid effluents were calculated at 1.62E-1 mrem
and 6.82E-3 mrem to the airborne and liquid effluent critical organs,
respectively. The total body dose attributable to liquid effluents for
1996 is 4.90E-3 mrem. These doses were extracted from the licensee's
1995 annual Radiological Environmental Operating Report and from
preliminary dose calculations for 1996 completed in January 1997. The
inspector reviewed the data collection and analysis methodology used by
the licensee in compiling the effluent data with no concerns noted. The
annual average radiation dose to a hypothetical exposed individual from
liquid and gaseous effluents was-less than two tenths of a millirem
which represents a small percentage of the annual limit.
During 1995, the licensee made 87 radwaste disposal shipments, involving
50 cubic meters and 46.85 curies of solid radwaste. During 1996, the
.licensee made 59 waste disposal shipments, involving 26.76 cubic meters
containing 66.74 curies of radwaste. Volume reduction initiatives
included removing "clean" trash drums from the RadiationControl Area
(RCA).
Individuals were required to remove their own trash as they exit
the RCA using the small article monitor for release. Also, chemistry
made improvements in waste water processing that prolonged the life of
waste water resins which further reduced resin radwaste volume.
c. Conclusions
Based on the above evaluation, the inspector concluded that the licensee
had maintained an effective program to monitor and control liquid and
gaseous radioactive effluents-and thereby limited doses to members of
the public to a small. percentage of regulatory limits. Specifically, the
release of radioactive material to the environment from effluents for
1996 was a small fraction of the 10 CFR 20, Appendix B and 10 CFR 50,
Appendix I limits. The projected offsite dose commitments which
resulted from plant effluents were well within the limits specified in,
the TSs and the Offsite Dose Calculation Manual (ODCM). Radwaste volume
reduction from 1995 to 1996 was determined to be on a favorable reducing
trend.
R1.3 External Occupational Exposure Control and Personal Dosimetry
a. Inspection Scope (83750)
The inspector evaluated the adequacy 'of the licensee's program for
monitoring occupational exposures during normal power operations and the
adequacy of the licensee's site dosimetry program. The inspector
evaluated the licensee's monitoring of occupational dose to radiation
workers in buildings close to but outside the RCA, i.e., within the
licensee's protected and controlled areas, to ensure compliance with 10
CFR 20.1502 monitoring requirements.
24
b. Observations and Findings
The inspector reviewed area Thermo Leuminacent Dosimeter (TLD) results
for1996 with focus on exposures in buildings occupied by personnel
within the protected area boundary fence. A review of these TLD results
averaged for a 2080 hour0.0241 days <br />0.578 hours <br />0.00344 weeks <br />7.9144e-4 months <br /> work year indicated several work areas with
elevated doses above natural background but within the regulatory public
dose limit of 100 millirem per year. The inspector's evaluation of the
licensee's dosimetry, monitoring, and general radiation control
procedures indicated the licensee did not treat dose to occupational
workers in buildings outside the RCA as occupational dose and licensee
procedures were generally silent in this regard. However, as defined in
regulation, dose which is received by a worker in the course of
employment during which the.worker's assigned duties involve exposure to
radiation from licensed sources is occupational dose. The licensee was
aware that some workers outside of the RCA were receiving low level
occupational doses incidental to their occupational activities but the
licensee had concluded that these workers were receiving less than the
public dose limit and, therefore, there was no requirement for-the
monitoring of radiation workers in these areas.
The inspector reviewed available dose data for radiation workers outside
the RCA and determined that no workers were exceeding regulatory limits.
However, the inspector reviewed dose monitoring procedures as well as
dose records of other categories of individuals including members of the
public, casual visitors, and the exposure monitoring
practices/procedures for declared pregnant women. No concerns were
identified with respect to public or casual visitors. Under certain
circumstances a situation could be postulated where a declared pregnant
woman may exceed the 50 millirem monitoring limit depending on
background dose subtraction methodology, i.e., subtract from assigned
worker dose less than 100 percent of "background" dose as detected at
the primary access point to the RCA (note discussion of licensee
background dose subtraction practices below). However, no.actual
examples were identified that required monitoring based on a review of
declared pregnant women dose records during the inspection..
.The inspector evaluated the licensee's procedures and practices with
respect to the monitoring and tracking of occupational dose for
radiation workers. The licensee required, by procedure, all radiation
workers entering the RCA to be monitored, is a larger population of
radiation workers than required by regulation. The monitoring of all
workers inside the RCA for dose of record purposes exceeds regulatory
requirements in that.only a fraction of the workers who actually enter.
the RCA will exceed the 500 millirem threshold requiring monitoring.
The licensee was unable to demonstrate adequately during the period of
inspection that occupational dose received by workers outside the RCA
(restricted area) was being considered in the prospective analysis used
to determine if workers required monitoring in accordance with the
requirements of 10 CFR 20.1502. Radiation workers who are required to
be monitored for radiation work in restricted areas, i.e., workers who
are likely to receive greater than 500 millirem in a year based on a
25
prospective analysis of likely dose, are also required to be monitored
for occupational dose received in licensee controlled areas outside the
restricted area. The licensee was unable to produce records or
reference procedures which demonstrated full compliance with the
requirements of 10 CFR 20.1502 for monitoring occupational exposure in
this regard. Additionally, the licensee was asked to demonstrate that
the current dosimetry practice of subtracting 100 percent of
"background" dose from the site wide personnel TLDs stored in badge
racks at the primary access point to the RCA was consistent and within
,regulatory requirements. Since area TLD readings at the badge racks had
millirem readouts higher than area TLD readings at more distant
locations within the controlled area, the inspector concluded some dose
component of what the licensee characterized as "background" was more
accurately described as dose attributable to power operations. Although
the amount of dose in question was at low levels at RNP and of minimal
radiological safety significance, the inspector indicated to the
licensee that this practice was non conservative with respect to the
accurate reporting of dose both in terms of cumulative site dose and
individual dose assignments. The licensee was unable to provide
sufficient data to demonstrate.this was conservative safety practice
during the week of inspection.
The licensee indicated further evaluation and time to .prepare a response
was necessary, due in part to the need to coordinate a response with
corporate dosimetry personnel who were housed offsite in the Harris
Energy and Environmental Center at New Hill, N. C.. These inspection
concerns were unresolved at the end of the inspection and will require
further evaluation of licensee data which the licensee committed to
prepare as a corporate response which would address the specific
concerns identified. Furthermore, licensee nuclear generation group
procedures did not adequately address these specific issues
procedurally. These issues regarding demonstration of accurate and
reasonable dose tracking and dose assignment practices and the lack of
related procedures were identi'fied to the licensee as an Unresolved Item
(URI) 50-261/97-01-06: -Demonstrate Accurate Dose Monitoring and Dose
Assignment Practices and Procedures.
c. Conclusions
The licensee's program for monitoring external exposure and tracking
dose within the RCA was determined to be effective. Outside the RCA,
however, licensee dosimetry procedures were deficient in that the
monitoring and tracking of occupational dose was not adequately
addressed in procedure. Specifically, procedures which require
monitoring of dose in the controlled area for workers who are required
to be monitored in the RCA and practices for adjusting radiation worker
dose assignments to eliminate all "background" dose, which contains an
operational dose component, were identified to the licensee as issues
requiring further evaluation and procedural treatment as appropriate.
These issues are an Unresolved Item with respect to dose tracking,
assignment of dose, and related procedural improvement.
26
R1.4 Radiological Controls During Power Operations
a. Inspection Scope (83750)
The inspector evaluated the adequacy of licensee radiological controls
with emphasis on external occupational exposure controls during normal
plant operations. The inspector evaluated adequacy of radiological
controls for an Independent Spent Fuel Storage Installation within the
licensee's protected area. Other areas inspected included radiation
area postings, radiation work permit controls, and effectiveness of the
ALARA program. The inspector made tours of the radiation controlled
area, observed compliance of licensee personnel with radiation
protection procedures for routine work evolutions, and conducted
interviews with licensee personnel with respect to knowledge of
radiological controls and working conditions.
b. Observations and Findings
The inspector verified observed controls for external occupational
exposures met applicable regulatory requirements and were designed to
maintain exposures ALARA. The inspector reviewed several radiation work
permits (RWPs) utilized to control ongoing work within the
radiologically controlled area and noted that the controls observed were
appropriate for the described tasks and radiological conditions.
Interviews were conducted with radiation workers in order to determine
the level of understanding of radiation work permit requirements from a
representative cross-section of-plant workers. The workers interviewed
were verified to have signed onto an RWP, were wearing dosimetry
appropriate to their work'activities within the RCA in accordance with
plant procedures, and were performing specific work activities on
appropriate RWPs. The questions asked included the RWP number of the
RWP signed in on, electronic dosimetry dose limits, and general.
radiological working conditions for the areas worked in. A good
knowledge of RWP requirements and of radiological working conditions,
generally, was demonstrated.
The inspector noted significantly upgraded and improved posting
practices throughout the plant. During a tour of the Spent Fuel Pool
the inspector observed no items hanging from the side of the pool and
good radiological controls in place in this area overall. The inspector
observed the decontamination prior to rail shipment of an IF 300 Cask
with good contamination and radiological controls. Radiation workers
during peak traffic periods were observed exiting the RCA fully in
accordance with procedures for frisking out of the RCA to include
properly clearing small articles with the small articles monitor. Pre
job RWP work planning and ALARA briefings for observed ongoing work
evolutions were found to be conducted in an effective manner. During
tours of the plant, the inspector observed RC technicians performing
radiation and contamination surveys in accordance with procedure. Also,
during inspection of the tool issuance rooms, good controls for slightly
contaminated tools inside the RCA and for clean tools outside the RCA
were noted. The inspector performed approximately twenty eight
27
independent contamination surveys (swipes) of areas within the RCA with
relatively high potential for loose contamination to verify that clean
areas within the RCA were being maintained clean. The licensee
continues to be challenged with respect to the effectiveness of
contamination controls based on the relatively high.number of Personnel
Contamination Events (PCEs)-incurred during Refueling Outage (RO) 17
(207 PCEs total for 1996) and based on recent independent nuclear
assessment findings which identified multiple examples of smearable
contamination above contamination control limits in clean areas.
However, during this inspection, all of the swipes were counted and
determined to be within the licensee's procedural limits for loose
contamination. The licensee's ALARA program continues to be effective
in achieving reductions in site exposure. The licensee achieved 166.56
person rem for 1996 against.a goal of 211 person rem which was a record
low for the site during a refueling outage year. The licensee.achieved
63 person rem in 1994 during a non outage year and has established a
1997 site goal of 25 for 1997, also a non outage year. Through
January 28, 1997, the licensee had achieved a site dose of 1.239 rem
against a target dose of 1.901 rem.
The inspector evaluated the adequacy of radiological controls for the
Independent Spent Fuel Storage Installation (ISFSI).
Independent
radiation surveys were taken inside the ISFSI RCA and at the fence line
surrounding the facility. Swipes were taken inside the ISFSI RCA to
determine levels of smearable contamination. The inspector determined
that the radiation levels detected and the smearable contamination
levels identified were within the limits specified in the licensee's
E&RC Surveillance Test Procedure RST-025, "Surveillance of the
Independent Spent Fuel Storage Installation" with no regulatory concerns
noted.
c. Conclusions
The radiological controls program was being effectively implemented with
- good occupational exposure controls observed during normal plant
operating conditions. Good radiological control performance.was
- apparent in the occupational exposure activities observed by the
inspector. Independent contamination surveys identified no loose
contamination levels above contamination control limits. The ALARA
program was controlling site exposures to record low levels for the
site. No regulatory concerns were identified with respect to the
adequacy of controls for the ISFSI facility with the radiation and
contamination levels independently inspected determined to be within
procedural limits.
R1.5 Up-to-Date Radiological Survey Data not Posted at RCA Entrance
a. Inspection Scope (71750)
While conducting a walkdown of the RHR pump room with an auxiliary
operator, the inspector noted that the most current radiological survey
data was not used by a radiation control (RC) technician to inform the
28
inspector and operator of the radiological conditions in the room.. In
addition, RWPs located at the entrance to the RCA did not contain the
most current quarterly radiological survey data reports.
b. Observations and Findings
On February 8, the inspector accompanied an auxiliary operator
conducting a weekly check of equipment status in the RHR pump room.
Before entering the room, the shift RC technician explained the
radiological conditions using what he thought was the most current
radiological survey data report for the room. Routine radiological
surveys of the RCA are conducted at various frequencies; the RHR pump
room was one of 38 areas routinely surveyed every quarter. The
inspector noted that the survey report used by the technician was dated
October 18, 1996. The inspector questioned whether this was the most
current survey since it appeared to be outside the quarterly required
frequency.
After exiting the room, the inspector discussed the survey report again
with the RC technician. At this time, the inspector was shown a more
current quarterly survey report dated January 7, 1997. This survey
report was obtained by the technician from the RWP file folders
maintained in the shift RC desk. The technician indicated that he had
obtained the October survey report from the RWP posting board located at
the entrance to the RCA. This board contains a listing of all "Special"
RWPs. The workers are expected to read and follow the requirements of
these RWPs prior to performing work covered by them. Attached to the
RWPs were area survey reports which provided the radiological conditions
of the RCA areas covered by each RWP. Based on a review of some of the
RWPs, it appeared that all of the quarterly survey reports were from the
previous quarter. Many of the Special RWPs had specific instructions
requiring the worker to review the survey reports attached to the RWP
for the current radiological conditions. Based on.this, the inspector
considered it important that correct and up-to-date survey information
be included so that workers are properly informed of work area
radiological conditions and hazards. While local area maps at the
entrance to RCA rooms and areas also show the current radiological
conditions, the inspector believed that it could be confusing to workers
if conflicting radiological information existed.
The inspector reviewed the January 7 survey record of the RHR room and
determined that radiological conditions had actually improved since the
October survey was performed, In addition, the local survey map located
at the entrance to the RHR pump room had been updated with the most
recent radiological data from the January 7 survey results. Based 6n
this, the inspector determined that there had been no actual
radiological safety consequence in having used the out-dated survey
data. However, the inspector was concerned that there were other
quarterly surveyed areas where the radiological conditions had degraded
since the previous quarter.
30
PARTIAL LIST OF PERSONS CONTACTED
Licensee
H. Chernoff, Supervisor, Licensing/Regulatory Programs
J. Clements, Manager, Site Support Services
D. Crook, Senior Specialist, Licensing/Regulatory Compliance
M. Herrell, Training Manager
C. Hinnant, Vice President, Robinson Nuclear Plant
J. Keenan, Director, Site Operations
B. Meyer,'Manager, Operations
G. Miller, Manager, Robinson Engineering Support Services
R. Moore, Manager, Outages/Scheduling
J. Morris, Acting Maintenance Manager & Electrical / I&C Superintendent
J. Moyer, Manager, Maintenance
D. Stoddard, Supervisor, Operating Experience Assessment
R. Warden, Manager, Nuclear Assessment Section
T. Wilkerson, Manager, Regulatory Affairs
D. Young, General Manager, Robinson Plant
.
NRC
B. Desai, Senior Resident Inspector
J. Zeiler, Resident Inspector
31
INSPECTION PROCEDURES USED
IP 37551:
Onsite Engineering
IP 40500:
Evaluation of Licensee Self-Assessment Capability
IP 61726:
Surveillance Observations
IP 62707:
Maintenance Observation
IP 71707:
Plant Operations
IP 71001:
Licensed Operator Requalification Program Evaluation
IP 71750:
Plant Support Activities
IP 84750:
Radwaste Treatment, Effluent & Environmental Mon.
IP 83750:
Occupational Radiation Exposure
IP 92901:
Followup - Operations
IP 92902:
Followup - Maintenance
IP 92903:
Followup - Engineering
ITEMS OPENED, CLOSED, AND DISCUSSED
Oened
Type
Item Number
Status
Description and Reference
50-261/97-01-01
Closed
Failure to Perform A Source Check Prior to
Gaseous Release (Section 03.1)
50-261/97-01-02
Closed
Inadequate Corrective Actions for RPS
Relay Degradation (Section M1.2)
50-261/97-01-03
Closed
Failure to Adequately Implement TS
Surveillance Requirement (Section M8.1)
50-261/97-01-04
Closed
Failure to Conduct Containment Airlock
Testing (Section E2.1)
50-261/97-01-05
Closed
Inappropriate Testing of the AFW pumps
(Section E2.2)
50-261/97-01-06
Open
Demonstrate Accurate Dose Monitoring and
Dose Assignment Practicesand Procedures
(Section R1.3)
50-261/97-0I-07
Open
Complete Review of Licensee Controls of
Radiological Survey Data (Section R1.5)
32
Closed
LER
50-261/96-01-00
Closed
Condition Prohibited by Technical
Specifications Due to Inadequate Testing
of Nuclear Instrumentation Power Range
Channels (Section M8.1)
LER
50-261/97-01-00
Closed
TS Violation Due to Missed Surveillance
Requirements (Section 08.1)
LER
50-261/97-02-00
Closed
Technical Specification Violation Due to
Inadequate Surveillance Test (Section
E8.1)