ML14181A841

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Insp Rept 50-261/96-10 on 960707-0817.Violations Noted. Major Areas Inspected:Operations,Maint,Engineering & Plant Support
ML14181A841
Person / Time
Site: Robinson 
Issue date: 09/16/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A839 List:
References
50-261-96-10, NUDOCS 9609270210
Download: ML14181A841 (37)


See also: IR 05000261/1996010

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-261

License Nos:

DPR-23

Report No:

50-261/96-10

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

2112 Old Camden Rd.

Hartsville, SC 29550

Dates:

July 7 - August 17, 1996

Inspectors:

J. Zeiler, Acting Senior Resident Inspector

P. Byron, Resident Inspector

R. Chou, Region II Inspector (M1.1)

L. King, Region II Inspector

J. Lenahan, Region II Inspector (E1.1, E1.2, E6,

E7.1)

G. Salyers, Region II Inspector (R1.2)

W. Tobin, Region II Inspector (S1.2)

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

Enclosure 2

9609270210 960916

PDR ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report 50-261/96-10

This integrated inspection included aspects of licensee operations, maintenance,

engineering, and plant support. The report covers a six-week period of resident

inspection; in addition, it includes the results of an engineering inspection by two

Region II inspectors and inspection of aspects of the licensee's spent fuel shipment

program by three Region II inspectors.

Operations

The licensee's preparations for Hurricane Bertha were prompt and thorough.

Good monitoring and assessment of potentially changing weather conditions

were performed during the period (Section 01.2).

The inspectors determined that the downpower evolution to replace a leaking

upper bearing oil cooler to the A Heater Drain Pump was well planned and

coordinated (Section 01.3).

The inspectors concluded that with the exception of a minor Foreign Material

Exclusion Area (FMEA) poor practice, the FMEA controls associated with spent

fuel pool shuffling activities observed were adequate (Section 01.4).

Based on review of the draft 1996 Institute of Nuclear Power Operations

annual assessment of site activities, issues identified were consistent with NRC

perceptions of licensee performance (Section 08.1).

Maintenance

The procedures used for the operation, inspection, and maintenance of the

spent fuel shipping casks and cranes were adequate in providing the details for

conducting work activities. In general, the craft, technicians, and operators

were knowledgeable and skillful in performing their assigned activities;

however, a control problem was identified with ensuring that personnel

protection measures were established along the lift path (Section M1.1).

Maintenance activities associated with the B charging pump packing

replacement were properly performed (Section M1.2).

Routine surveillance test activities were well coordinated and adequately

performed (Section M1.3).

Engineering

The licensee's design change control process was judged to be adequate and

the modification packages reviewed were of good quality (Section E1.1 and

E1.2).

Progress on Robinson Engineering Support Section (RESS) backlog reduction

was noted (Section E6.1).

Self assessments performed by RESS were effective in identifying engineering

performance deficiencies and were useful in providing oversight to

management (Section E7.1).

A Violation was identified involving the licensee's failure to take adequate

corrective actions after it was identified in May 1995 that the design pressure

rating was exceeded for fourteen safety related solenoid operated valves. This

resulted in the design application deficiencies remaining unanalyzed until

May 1996 (Section E8.1).

Plant Support

The inspectors concluded effective procedures were implemented to safely

control irradiated fuel shipment activities. Minor spent fuel cask handling

procedure discrepancies identified were appropriately resolved by the licensee.

A Nuclear Assessment Section (NAS) assessment of the spent fuel shipment

program readiness was thorough and probing. NAS assessment and table top

exercise weaknesses were properly resolved and effective program

enhancements were implemented prior to conducting shipment activities. The

inspectors observed that adequate controls were implemented during the

August 12, 1996, spent fuel shipment (Section R1.2).

A Non-Cited Violation was identified for the failure to affix a radiation material

label on a spent fuel shipping cask container that was located in the Radiation

Control Area (RCA) (Section R1.3).

A Violation was identified for the failure to provide minimum illumination for

several areas of the protected area (Section S1.1).

Report Details

Summary of Plant Status

Unit 2 remained at power during the entire inspection period completing 408 days of

continuous operation. On July 9, a downpower to 82 percent was conducted to

replace the upper bearing oil cooler to the A Heater Drain Pump after a leak was

discovered. On August 7 and again on August 8, power was reduced to 60 percent

after the Heater Drain Pumps tripped unexpectedly. The unit was returned to 100

percent power on August 9 and remained at full power for the remainder of the report

period.

I. Operations

01

Conduct of Operations

01.1

General Comments (71707)

The inspectors conducted frequent control room tours to verify proper staffing,

operator attentiveness and communications, and adherence to approved

procedures. The inspectors attended daily operations turnover, management

review, and plan-of-the-day meetings to maintain awareness of overall plant

operations. Operator logs were reviewed to verify operational safety and

compliance with Technical Specifications (TSs). Instrumentation, computer

indications, and safety system lineups were periodically reviewed from the

Control Room to assess operability. Frequent plant tours were conducted to

observe equipment status and housekeeping. Condition Reports (CRs) were

routinely reviewed to assure that potential safety concerns and equipment

problems were reported and resolved.

In general, the conduct of operations was professional and safety-conscious.

Good plant equipment material conditions and housekeeping was noted

throughout the report period. Specific events and noteworthy observations are

detailed in the sections below.

01.2

Preparations for Hurricane Bertha

a.

Inspection Scope (71707, 71750)

Between July 10-12, the inspectors reviewed licensee preparations in response

for Hurricane Bertha. This included a review of Operations Management

Manual (OMM) procedure OMM-021, Operation During Adverse Weather

Conditions, Rev. 13, and verification that the actions prescribed by the

procedure were properly implemented.

b.

Observations and Findings

On July 10, at 11:30 a.m., the licensee began preparations for the possible

impact from Hurricane Bertha. At the time, the hurricane was still several days

away but was heading toward the site. The licensee initiated actions for a

hurricane warning in accordance with OMM-021. The inspectors reviewed the

procedure and verified that applicable actions were being completed. This

verification also included several walkdowns of the site to ensure that loose

items were properly stored or secured. Only minor items were identified and

discussed with licensee management.

Based on weather projections that hurricane force winds would not be

expected near the site, licensee management decided that a plant shutdown

was not necessary. On July 12, the hurricane passed within approximately

150 miles to the east, traveling from south to north. Maximum sustained winds

of approximately 25-30 mph were observed at the site. No significant damage

occurred onsite. Offsite power was maintained throughout the storm as well as

normal communications.

c.

Conclusions

The inspectors concluded that the licensee's readiness for the Hurricane's

arrival was prompt and thorough. The licensee continuously monitored the

progress and status of the hurricane and was sensitive to the potential for

changing weather conditions that could occur at the site.

01.3

Downpower to Repair Heater Drain Pump Oil Cooler Leak

a.

Inspection Scope (71707)

On July 9, the licensee conducted a downpower to 82 percent in order to

replace the oil cooler tq the A Heater Drain Pump (HDP). The inspectors

reviewed the licensee's activities associated with preparations and conduct of

the downpower evolution.

b.

Observations and Findings

On July 9, the licensee discovered that service water was leaking into the

upper bearing oil cooler to the A HDP. While no appreciable increase in

bearing temperature was observed at the time, the licensee decided to replace

the oil cooler. These activities involved reducing power to 82 percent, stopping

the A HDP, replacing the oil cooler, and returning to full power operation. Prior

to the downpower, operations management issued a Night Order which

described the scope of the activities and provided operator guidance on

3

maneuvering reactor power. Reactor engineering personnel determined that

xenon would not be a concern due to the limited power decrease.

Nonetheless, they provided Operations personnel with power maneuvering

rates to lessen the impact of the transient on core reactivity. The inspectors

verified that a pre-job briefing was held with operations, engineering, and

maintenance personnel to discuss details of the evolution, precautions, and

contingencies for potential problems. The downpower commenced at 10:00

p.m. on July 9. Following replacement of the oil cooler, the unit was returned

to full power at 3:40 a.m. on July 11 without incident.

c.

Conclusions

The inspectors determined that the downpower evolution was well planned and

coordinated. No discrepancies were identified.

01.4

Foreign Material Exclusion Discrepancies

a.

Inspection Scope (71707)

On July 18, the inspectors observed foreign material exclusion area (FEMA)

activities in the area of the spent fuel pool. The licensee was in the process of

shuffling spent fuel in the spent fuel racks in preparation for an upcoming

shipment to the Shearon Harris Nuclear plant. The inspectors reviewed the

FMEA procedure, and the material and personnel equipment logs.

b.

Observations and Findings

The inspectors observed some minor inconsistencies involving a Radiation

Control (RC) Technician in the foreign material exclusion area around the

spent fuel pool. The FMEA boundary was setup around three sides of the

spent fuel pool with a single access control point. A swinging gate was located

at the far end of the FMEA and was labeled as an emergency exit. The

inspectors observed an RC technician enter and exit the FMEA three times

using the emergency exit. The RC technician removed items from the FMEA

through the Access Control Point and reentered the FMEA with the items

through the emergency exit. These items were not logged out and into the

FMEA. While this demonstrated weak FMEA controls, the inspectors observed

no foreign material event.

The inspectors discussed their observations with the licensee. The licensee

counselled the RC technician, and indicated that the FMEA program would be

reassessed.

c.

Conclusions

The inspectors concluded that with the exception of a minor FMEA poor

practices, the FMEA controls associated with spent fuel pool shuffling activities

observed were adequate.

08

Miscellaneous Operations Issues

08.1

Institute of Nuclear Power Operations (INPO) Assessment

a.

Inspection Scope (71707)

The inspectors reviewed the second draft of the INPO annual assessment of

site activities conducted in April 1996.

b.

Observations and Findings

The inspectors found that issues identified were consistent with the NRC

perceptions of licensee performance. No safety significant issues that required

immediate attention were identified.

c.

Conclusions

No regional followup of the INPO identified issues is planned.

II. Maintenance

M1

Conduct of Maintenance

M1.1 Observation of Spent Fuel Cask Liftinq Operations

a.

Inspection Scope (60855)

The inspectors observed portions of spent fuel cask lifting and drying process

activities to verify that the activities were performed in accordance with the

applicable procedures and American National Standards Institute (ANSI)

Codes. The procedures and ANSI Codes used are listed below:

Procedure MMM-009, Operation, Testing, and Inspection of Cranes and

Material Handling Equipment, Rev. 20,

Training Procedure, Crane Operator, Rev. 15,

Procedure SFS-001, IF-300 Shipping Cask Operations, Rev. 13,

5

Procedure SFS-004, Spent Fuel Cask Crane Restricted Mode

Procedure, Rev.9, and,

ANSI B30.2, Overhead and Gantry Cranes.

b.

Observation and Findings

The inspectors observed portions of spent fuel cask operations in preparation

for cask shipment of the Shearon Harris Nuclear Plant. The IF-300 cask used

for this shipment can handle seven assemblies with a total weight for the fuel

and cask of approximately 68 tons. One of the two casks used for this

shipment had initially been lifted, installed at one end of the spent fuel pool,

and loaded with seven assemblies prior to the inspectors' arrival onsite. Since

the cask location was at the end of the spent fuel pool next to the yoke storage

and decontamination pits, the lifting and movement of the cask from the spent

fuel pool to the decontamination pit would not go over any adjacent spent fuel

assemblies.

The inspectors observed the following activities:

Daily morning briefing at 6:00 a.m. on August 6 and 7,

The preparation and movement of the cask closure head from the

decontamination pit to the top of the cask stored in the spent fuel pool,

The connection engagement for the primary yoke to trunnions at two

sides of the cask and the secondary yoke (redundant purpose) to the

bottom of cask,

The lifting from the pool, the movement of the cask from the spent fuel

pool over the yoke storage pit to the decontamination pit, and the

unloading in the decontamination pit,

The demineralized water rinse of wire cables, load block, yokes, etc.,

The tool and equipment lifting using the auxiliary load block,

The lifting and movement of load blocks and yokes back to the storage

pit,

The installation of nuts to tighten the closure head,

The drying process and leak inspection for the cask.

6

During the observation of cask, yokes, and equipment box movement, the

inspectors noticed one problem as discussed below.

The cask was moved over people inside the yoke storage pit as it traveled

from the spent fuel pool over the yoke storage pit to the decontamination pit.

During this move, the lower signalman walked immediately down from the

spent fuel floor to the decontamination pit floor after he directed the crane

operator to move the cask from the spent fuel floor, over the yoke storage pit,

to the decontamination pit. Because the crane operator could not see people

entering the yoke storage pit and the signalman was on the way down to the

decontamination pit, the cask inadvertently passed over people inside the yoke

storage pit. In addition, the upper signalman was also unable to see into the

yoke storage pit at this time. The signalmen did not observe the load path at

all time resulting in the cask movement over people. In this instance, the

licensee had not sufficiently preplanned this lift to ensure that either the entire

lift route was observable by a signalman or operator, or, for those areas not

observed, that controls were in place to restrict entry during the lift. The

problem was identified as a personnel safety hazard issue and did not affect

the actual performance of the cask movement.

The inspectors immediately informed the licensee about this issue. The

licensee issued CR 96-01836, "Lifting Heavy Loads", for evaluation.

The inspectors also reviewed data and completed information in the

performance copy of Procedure SFS-001 and records of crane operator

training, certification, recertification, and medical data for three crane operators

who performed the lift. The annual medical data reviewed included the check

on visual acuity, hearing, color vision, and fitness for crane operation.

c.

Conclusions

Overall, the cask lift was satisfactory. A control problem was identified with

ensuring that personnel safety measures were established along the lift path.

M1.2 B Charging Pump Packing Replacement

a.

Inspection Scope (62703)

On July 18, the inspectors reviewed and witnessed aspects of the packing

replacement of the B Charging Pump.

b.

Observations and Findings

In early July, the licensee identified that reactor coolant system unidentified

leakage had increased. The B Charging Pump was in operation at the time.

After swapping charging pumps, the licensee verified that unidentified leakage

was reduced back to its normal value, indicating that the increased unidentified

leakage was attributed to the B charging pump.

On July 18, the inspectors witnessed aspects of Work Request/Job Order 96

ACL1l for replacing the packing on the B charging pump. The instructions for

performing the packing replacement were contained in Corrective Maintenance

(CM) procedure CM-034, Charging Pump Stuffing Box Maintenance, Revision

9. One of the three pump plungers was also replaced as a conservative

measure after some minor scoring on the outside surface of the plunger was

identified. After completing the work, post-maintenance testing on the pump

was performed in accordance with Operations Surveillance Test (OST)

procedure OST-101-2, Chemical and Volume Control System (CVCS)

Component Test Charging Pump B. The pump was returned to service without

any major problems later that day. No discrepancies were identified.

c.

Conclusions

The inspectors concluded the B charging pump maintenance and testing was

performed in accordance with applicable procedures in a conscientious and

professional manner.

M1.3 Maintenance Surveillance Observations

a.

Inspection Scope (61726)

During the inspection period, the inspectors observed all or portions of various

maintenance surveillance activities performed by the licensee. These

surveillances were performed to meet the surveillance requirements of

applicable sections in TSs. The inspectors verified that approved procedures

were available and in use, test equipment in use was calibrated, test

prerequisites were met, shift pre-job briefings were performed, TS Limiting

Conditions for Operations (LCOs) were entered and adhered to, and testing

was accomplished by qualified personnel. Upon test completion, the

inspectors verified that test data was complete and met acceptance criteria,

and equipment restoration was properly completed. The inspectors observed

all or portions of the following surveillances:

OST-401

Emergency Diesels Slow Speed Start

EST-124

Response Time Testing of Reactor Coolant System RTDs

b.

Observations and Findinqs

The inspectors determined that the surveillances were performed in

accordance with the prescribed procedures. The inspectors reviewed the

results of the surveillance tests and verified that test acceptance criteria were

satisfied. Pre-job briefings were conducted by operations prior to testing which

resulted in good test coordination. The procedures provided detailed

precautions and instructions. The inspectors concluded that the tests were

properly performed.

c.

Conclusions

The inspectors determined that the observed surveillances were well

coordinated and controlled in accordance with applicable surveillance test

procedures.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) Licensee Event Report (LER) 93-015-00, Pressurizer Pressure

Transmitters Out of Calibration: This issue involved the repeated inadequate

calibration of the three pressurizer pressure transmitters due to personnel

error. Personnel performing the calibrations were part of the licensee's outage

traveling crew and were not adequately trained and experienced on the use of

the calibration equipment, specifically, a dead weight testing apparatus

resulting in the wrong weights being used for these transmitters. The

licensee's corrective actions for this problem included retraining traveling crew

personnel on the use of a dead weight tester and revising training

qualifications to include periodic retraining. The inspectors reviewed applicable

training records and qualifications and verified that the committed training

activities were completed. Since this incident, the inspectors noted that this

work is now only performed by site Instrumentation and Control (l&C)

personnel. The inspectors verified that training on the use of dead weight

testing instrumentation was being provided for site l&C personnel. This item is

closed.

M8.2 (Closed) LER 94-003-00, TS Required Shutdown Due to Emerqency Diesel

Generator Inoperability: This event involved the inoperability of the B

Emergency Diesel Generator (EDG) on February 18, 1994, when a locking pin

for the modulating air damper came loose and was propelled through the

engine's air system damaging the scavenging air blower and turbocharger.

The root cause of the damper pin failure was unknown at the time that the

LER was written.

The licensee provided a supplement to this LER (261/94-03-02) on

November 30, 1994, indicating that the root cause of the failure to be

inadequate corrective action for a similar failure of the air intake system

associated with the B EDG on February 12, 1994. The corrective actions for

this event included enhancements in the investigation procedures for plant

events. This issue was also the subject of Violation 50-261/94-08-02. The

licensee's corrective actions for this violation were previously reviewed and

found to be acceptable. The violation was closed in NRC Inspection Report

50-261/95-29. Supplement 2 of this LER (261/94-03-02) was reviewed and

closed in NRC Inspection Report 50-261/96-01. Therefore, based on these

previous reviews, this LER is closed.

M8.3 (Closed) LER 94-011-00, Technical Specification 3.0: Emergency Diesel

Generator Inoperability: This LER identified a condition where the plant was

operating at full power with one EDG out of service for maintenance and the

redundant EDG out of service for approximately three hours per day to meet

the operability testing requirements of the TS. During these testing evolutions

offsite power was available to the unit and operators were located in the room

of the EDG being tested with the ability to manually place the EDG in service

should offsite power be lost.

To resolve this issue, the licensee submitted a TS change request to the NRC

that eliminated, in most cases, the requirement to test the redundant EDG

when the other EDG is inoperable. The inspectors reviewed the TS and

verified that this change had been incorporated into the TS by Amendment

158. Based on this review, this LER is closed.

M8.4 (Closed) LER 94-019-01: TS Violation Due to Exceedinq Pressurizer

Cooldown Rate: This issue involved a condition prohibited by the plant TS.

Specifically, that the TS 3.1.2.3. limit for pressurizer heatup and cooldown had

been exceeded. Notice Of Violation (NOV) 50-261/94-23-02 was issued for

this event on November 28, 1994. The inspectors reviewed the licensee's

response to the violation dated December 27, 1994, and corrective actions for

LER 94-019-01.

The corrective action for Violation 94-23-02, specified in the licensee's

response to the NOV, had been reviewed by the NRC and found to be

adequate and properly implemented. The Violation was closed out in NRC

Report 50-261/95-30.

The inspectors verified that the corrective action specified in the response to

the NOV was the same as that specified in LER 94-019-01. Consequently,

LER 94-019-01 is closed out based on the previous review of the

implementation of corrective action.

10

Ill. Engineering

El

Conduct of Engineering

E1.1

Design Change Processes

a.

Inspection Scope (37550)

The inspectors reviewed the licensee's procedures which control the design

change program.

b.

Observations and Findings

The inspectors reviewed the revisions of the procedures listed below to verify

that design control measures were consistent with 10 CFR 50, Appendix B,

Criterion Ill and 10 CFR 50.59. The following procedures were reviewed:

PLP-032, 10 CFR 50.59 Reviews of Changes, Tests, and Experiments, Rev.7,

dated February 20, 1996; PLP-054, Configuration Control, Rev. 6, dated

July 17, 1996; PLP-064, Engineering Service Requests, Rev.5, dated July 19,

1996; MOD-022, Administrative Procedure for Engineering Service Request

Major Modifications, Rev.4, dated March 16, 1996; MOD-018, Temporary

Modifications, Rev. 16, dated January 23, 1996; EGR-NGGC-003, Design

Review Requirements, Rev. 0, dated June 3, 1996; EGR-NGGC-0005,

Engineering Service Requests, Rev. 1, dated July 29, 1996; and EGR-NGGC

0304, Maintenance of Design Documents, Rev.0, dated November 11, 1995.

The inspectors concluded that the procedures adequately addressed: design

input, training, drawing changes, post-modification testing, design verification,

control of field changes, 10 CFR 50.59 safety evaluations, and As Low As

Reasonably Achievable (ALARA) reviews. The inspectors concluded that

adequate controls were in place to ensure effective implementation of design

changes. However, the inspectors noted that when the new EGR-NGGC

procedures were issued to improve design control activities, previously issued

procedures which they were meant to replace were not deleted and/or

canceled. For example, EGR-NGGC-005 was issued to replace procedures

PLP-064 and MOD-022. The inspectors noted that PLP-064 and MOD-022

were still being maintained current. EGR-NGGC-0005, Engineering Service

Requests, streamlined the process for performing engineering work.

EGR-NGGC-0005 is 88 pages while procedure PLP-064 is 162 pages. The

162 page procedure is very cumbersome to use. The inspectors discussed

with licensee personnel involved in the change to the new procedure the

benefits involved in the change. The responsible engineer now has formalized

responsibility to track through modifications until completion. This includes

reviewing the work request that installs the modification and reviewing the

testing of the modification. The new procedure also contains a matrix that

shows which documents are required by the modification and which are

optional. Procedure EGR-NGGC-005 also contains checklists to simply the

design process. The EGR-NGGC series of procedures are corporate level

procedures being issued to standardize engineering work activities on all three

Carolina Power and Light (CP&L) nuclear plants.

c.

Conclusions

The inspectors concluded that the licensee's design change control procedures

complied with the requirements of 10 CFR 50.59, and 10 CFR 50, Appendix B,

Criterion Ill. However, the inspectors noted that duplicate procedures exist

which could possibly result in confusion in the future and could result in

potential design errors. This was discussed with the licensee.

E1.2

Review of Design Changes and Modification Packages

a.

Inspection Scope (37550)

The inspectors reviewed the design change and modification packages to: 1)

determine the adequacy of the safety evaluation screening and the 10 CFR

50.59 safety evaluations; 2) verify that the modifications were reviewed and

approved in accordance with Technical Specifications and administrative

controls; 3) verify that applicable design bases were included; 4) verify that

Updated Final Safety Analysis Report requirements were met; 5) verify that

both installation testing and post modification testing requirements were

specified so that adequate testing would be accomplished. The inspectors

selected major modifications, minor modifications and a temporary modification

to review. The only difference between major and minor modifications is cost

and engineering involvement.

b.

Observations and Findings

The inspectors reviewed the following design change and modification

packages:

ESR-9400731

Penetration Protection System (PPS) Design Change

Containment Vessel Penetration Repair

ESR-9500327

Dampening Adjustments to Steam Flow Transmitters

ESR-9500633

Main Steam Isolation Valve (MSIV) Manual Control Valve

Delete

12

ESR-9500738

Service Water Header Leak Repair

ESR-9500764

Replacement of End of Qualified Life Environmental

Qualification (EQ) Cables

ESR-9500783

Modify HVH-1,2,3,4 to Leave Butterfly Valves Open

ESR-9500782

Resolve Generic Implementing Procedure (GIP)

Issues for RFO 17

ESR-9500870

Power Operated Relief Valve (PORV) Block Valve Stem

Replacement

The above design change and modification packages were scheduled to be

implemented during the next refueling outage, Refueling Outage 17

(RFO 17). The inspectors found that the modification packages had been

reviewed and approved in accordance with the licensee's design control

procedures and that the format and content of the modification packages was

consistent with the design control procedure. The quality of the modification

packages was good overall with only a few minor discrepancies being noted in

the ESR 9500764 package. These discrepancies included errors in the bill of

materials and incomplete instructions pertaining to cable pulling. Cable pulling

was addressed by Note 6k on Drawing number HBR2-0B060, Electrical

Installation Practices. The note stated that care should be taken to ensure that

cables are not over tensioned during cable pulling; however, there were no

specific requirements for control of pulling tension or side-wall pressure.

Licensee engineers stated that additional instructions would be issued to

address these requirements. None of the noted discrepancies would have

prevented successful implementation of the modification or resulted in an

inadequate modification package. The scope of each modification was found

to be consistent with the problem resolution outlined in the Engineering

Support Request. The 10 CFR 50.59 Safety Evaluations were found to be

adequate. The installation and test instructions were considered adequate to

implement the modification and verify that it performed in accordance with

design. The inspectors also verified that the UFSAR and other documents e.g.

drawings and procedures had been identified in the modification packages for

revision.

The modifications reviewed were prepared using procedure PLP-064.

Changes to the modifications can be processed using either procedure

PLP-064 or EGR-NGGC-005 guidance. The inspectors found that the

basic information was contained in the packages but that it varied in

content due to the flexibility allowed in procedure PLP-064. Examples

included the following: Form 4 which tracked action items was an option

13

and in some cases was included with the procedure and in other cases

it was used in close out to identify open items. Some of the procedures

included the ALARA review and others did not but checked the design

verification checklist as ALARA completed. The inspectors determined

that an ALARA review had been done on these modifications but was

not included in the package. The inspectors obtained copies of the

ALARA review from radiation protection and learned that it had been

accomplished using AP-040, ALARA Planning/ Dose Planning, Rev. 4,

dated June 26, 1996. The inspectors did not find the design verification

checklist in ESR-9500870; however, further review of this issue

disclosed that the licensee used an alternative method to document the

design review. The alternative method was conducted in accordance

with the procedure.

c.

Conclusions

In general, the modification packages were judged to be of good quality

and would not degrade plant performance, safety, or reliability. The

modification packages contained sufficient specifications, drawings and

procedures to be properly installed and tested. The licensee's 10 CFR

50.59 evaluations were completed in accordance with NRC

requirements.

E6

Engineering Organization and Administration

E6.1

Engineerinq Backlog

a.

Inspection Scope (37550)

The inspectors reviewed the backlog of open items in the Robinson

Engineering Support Section (RESS).

b.

Observations and Findings

The backlog of items in the RESS include engineering service requests

(ESRs) which include modifications, temporary modifications, drawing

changes, other engineering documents with outstanding changes, and

other engineering items, including open condition reports and

engineering commitments. The licensee's performance report for the

week of July 31, 1996, showed approximately 600 open engineering

work items. The licensee has recently completed a self-assessment,

discussed in paragraph E7, below, regarding management of the

engineering backlog. Actions were being planned to address the

problems identified during the self-assessment and to continue reduction

of te eginerig

wrk ackog.14

of the engineering work backlog. The long term goal was to reduce the

total number of open items in RESS to less than 200.

c.

Conclusions

The inspectors concluded that the licensee has made progress in

identification of the backlog of engineering work in RESS. Progress was

being made in reduction of the backlog.

E7

Quality Assurance in Engineering Activities

E7.1

Quality Assurance Assessment and Oversight

a.

Inspection Scope (37550 and 37551)

The inspectors reviewed self-assessments performed within the RESS.

b.

Observations and Findings

Self-assessments are part of the overall CP&L quality assurance

program at Robinson. The self-assessments were performed in

accordance with procedure PLP-057, Self-Assessment, Revision 4,

dated November 3, 1995. The results of these assessments were

categorized as strengths, or findings. The self-assessments reviewed

by the inspector were the results from recently completed assessment

numbers RESS96-015, RESS Organization & Administration; and RESS96-026, Environmental Qualification (EQ) Program at Robinson Nuclear

Plant (RNP). Several findings were identified in Assessment 96-026.

Six Condition Reports were written to document discrepancies identified

in the EQ program; however, none of the problems resulted in

identification of any inoperable equipment. The conclusion of the

assessment was that the Robinson EQ program meets overall EQ

requirements.

The inspectors discussed the results of Assessment 96-015 with the site

engineering manager. Several issues were identified regarding management

of the engineering backlog. These included overdue action items, work not

assigned to individuals or assigned to individuals no longer onsite,

discrepancies in the ESR data base, older modifications which require

closeout, and failure to include some items in the open engineering work which

affect the weekly/monthly engineering performance indicators. The final report

for assessment 96-015 had not been completed as of the inspection date;

however, CR number 96-01823 was issued and other CRs were being

prepared to document and disposition findings.

15

c.

Conclusions

The inspectors concluded that the self-assessments performed by RESS

were effective in identifying engineering performance deficiencies and

were useful in providing oversight to management. Managers in RESS

have been proactive in following up on issues identified at other sites to

identify and correct deficiencies in engineering work at RNP.

E7.2

Special UFSAR Review

A recent discovery of a licensee operating their facility in a manner contrary to

the Updated Final Safety Analysis Report (UFSAR) description highlighted the

need for a special focused review that compares plant practices, procedures

and/or parameters to the UFSAR descriptions. While performing the inspection

discussed in this report, the inspectors reviewed selected portions of the

UFSAR that related to the areas inspected. The inspectors verified that for the

select portions of the UFSAR reviewed, the UFSAR wording was consistent

with the observed plant practices, procedures and/or parameters.

E8

Miscellaneous Engineering Issues (37551 and 92903)

E8.1

(Closed) Unresolved Item (URI) 50-261/96-08-01, Review Licensee

Investigation and Resolution of Solenoid Valve Discrepancies:

Background

This issue involved the licensee's evaluations and corrective actions to

address design problems identified with solenoid valves (SOVs). The design

problems were identified after the ASCO 3-way SOV, which controls one of the

two containment isolation valves in the Steam Generator A Blowdown sample

line, was found to be leaking past its vent port while the SOV was deenergized

and closed. Subsequent investigations revealed that the regulated supply air

pressure (85 pounds per square inch gauge (psig)) exceeded the SOV's

maximum design rating (60 pounds per square inch differential (psid)). This

design rating is called the maximum operating pressure differential (MOPD)

and corresponds to the rating of the SOV's internal spring force acting to keep

the supply air from pressurizing the SOV inlet port. Supplying higher air

pressure than the SOV valve is designed for can result in air leaking past its

inlet or vent port seats. While leakage past the vent port does not create a

significant problem, leakage past the inlet port could prevent or interfere with

the closure of the associated air operated valve that the SOV controls. The

SOVs for the other five containment isolation valves in the Steam Generator

16

Blowdown sample lines were also found to be under-rated. All six SOVs in this

application were subsequently replaced.

Licensee Investigations

Further investigation by the licensee determined that this MOPD application

problem was much broader in scope. SOVs in both safety related and non

safety related applications were affected. In an effort to thoroughly investigate

and resolve this problem, engineering initiated an evaluation of the MOPD

versus supplied air pressure to all SOVs in the plant with priorities placed on

safety related applications. This included evaluation of approximately 850

SOVs. The inspectors verified that as the evaluation progressed, CRs were

initiated for MOPD application discrepancies identified. Generally, there were

three main areas of MOPD concerns identified by the licensee. These three

areas were as follows:

1)

MOPD Below Air Regulator Setting:

This area included SOVs where their MOPD was below the setting of

the regulator that was installed upstream to limit air pressure to the

SOV. In these cases, the SOV would be pressurized above its design

rating and leakage could potentially occur. A total of 12 safety related

SOVs were identified in this area. This number included the SOVs

associated with the six Steam Generator Blowdown Sample

Containment Isolation Valves discussed above. The other six SOVs

were for the feedwater flow control and bypass isolation valves. The

licensee performed testing of similar model ASCO SOVs. These valves

were determined to be acceptable for interim use until they could be

replaced during the upcoming refueling outage in September 1996.

2)

MOPD Below Instrument Air System Normal Operating Pressure:

These problems included SOVs with MOPDs that were below 100 psig,

the normal operating pressure of the Instrument Air (IA) system. Credit

was not taken for the pressure regulators to limit pressure since they

were procured as non-safety related components. Assuming the

regulator fails would result in the SOV being pressurized to the normal

IA system pressure. This would allow SOV overpressurization if it were

rated below 100 psig resulting in potential leakage. A total of 28 safety

related valves were identified in this area. The licensee planned to

replace these SOVs during the upcoming refueling outage in September

1996.

17

3)

MOPD Below Instrument Air System Maximum Design Pressure:

While the normal operating pressure of the IA system is 100 psig, its

maximum design pressure is 125 psig. Therefore, the licensee

assumed SOVs with an MOPD less than 125 psig were also susceptible

to overpressurization. Again, credit was not taken for the pressure

regulators. A total of 19 SOVs were identified in this area. The

licensee planned to replace these SOVs during the upcoming refueling

outage in September 1996.

At the end of this inspection period, the licensee was in the process of

completing their evaluation of safety-related SOVs. Similar evaluations were to

be completed for non-safety related SOVs that could have an adverse impact

on the plant.

The inspectors concluded that the licensee was conducting an exhaustive

investigation to completely resolve the SOV MOPD concerns.

Root Cause

The inspectors reviewed the licensee's actions in response to NRC Information

Notice 88-24, Failures of Air-Operated Valves Affecting Safety Related

Systems, dated May 13, 1988. This Notice alerted licensees of potential SOV

overpressurization failures caused by exceeding the MOPD rating. The

inspectors learned that the licensee had failed to evaluate the concerns

addressed by the Notice in 1988 due to an engineering organization oversight.

In February 1995, during an NRC commitment to perform a sample review of

their operating experience program, the licensee became aware that

Information Notice 88-24 had not been adequately evaluated. At that time, CR

95-00549 was initiated to reevaluate the concerns addressed by the Notice.

Action Item #1 of the CR, requested a review of MOPD versus supplied air

pressure for all safety related SOVs. As a result of this review, 14 safety

related SOVs were identified where the supplied air pressure exceeded the

MOPD rating. The evaluator failed to recognize the potential significance of

this finding and did not initiate a separate Condition Report or Operability

Determination for the deficiencies identified. As a result, the impact of the

MOPD discrepancies was not evaluated. The inspectors also noted that the

evaluator was unable to determine the MOPD rating for eight other SOVs due

to their model numbers being unknown at the time. No further review or

apparent attempt was made to determine the model numbers and MOPD

ratings. A status of "unknown" was documented for these valves with respect

to whether their MOPD was exceeded. Action Item #1 was closed after review

by the evaluator's supervisor on May 19, 1995, without having initiated a CR,

operbilty

eterinaion or

18

operability determination, or identifying the missing SOV information. Action

Item #2 of CR 95-00549 stated that the SOVs identified with their MOPD

exceeded would be replaced during the September 1996 refueling outage.

However, the inspectors noted that Work Requests had not been prepared to

ensure that this work would be scheduled. While this action item was still

open in the licensee's CR database, with a due date of Refueling Outage 17

(September 1996), it was unclear whether the action item would have been

identified to have completed the work during the outage.

Conclusion

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires in part, that

measures be established to assure that conditions adverse to quality, such as

failures, malfunctions, defective material and equipment, are promptly identified

and corrected.

The inspectors concluded this issue was a violation of 10 CFR 50, Appendix B,

Criterion XVI, in that the licensee failed to take adequate corrective actions

after it was identified that the supplied air pressure exceeded the MOPD for 14

safety related SOVs. As a result, the adverse conditions remained unanalyzed

until May 1996. This item is identified as Violation (VIO) 50-261/96-10-01:

Inadequate Corrective Actions for SOV Design Discrepancies.

E8.2

(Closed) VIO 261/94-24-01, Inadequate Testing of Alternate AC Power

Source: The licensee responded to this violation in a letter dated November

11, 1994. This violation involved inadequate procedures for testing to

demonstrate the one hour capability of the Station Blackout alternate AC power

source. The licensee's corrective actions involved review of the test data and

procedure changes to improve management controls over test activities. The

licensee concluded that the testing performed demonstrated the station

blackout capability. In an acknowledgement letter to the licensee dated

January 30, 1995, NRC concurred with the licensee that the test activity was

adequate. The inspectors verified that all of the corrective actions had been

completed. The inspectors verified that all test document records were

assembled into a consolidated and readily available package. The licensee's

November 11, 1994, letter also contained a commitment to replace submerged

cables associated with NCV 261/94-24-02 which could not be qualified by

testing. The completion of upgrading or replacing submerged cables as

outlined in Modification M-1165 was completed by end of RFO16. The

inspectors reviewed the modification package documentation and verified that

the unqualified cables were replaced. This item is closed.

19

E8.3 (Open) Inspector Followup Item (IFI) 261/94-08-02, Incorporate 24 Hr Load

Testing into TS Surveillance Requirements: This IFI involved the licensee's

commitment to revise the TSs to require testing during each refueling outage

with a proper power factor to demonstrate the ability of the emergency diesel

generators to carry accident loads. This commitment was part of the

licensee's corrective actions for NRC Violation 50-261/93-07-01. The licensee

submitted the TS change in a letter to NRC dated January 30, 1996. A

request for additional information was sent by the NRC to the licensee on April

12, 1996, which the licensee responded to in a letter dated May 20, 1996.

This IFI will remain open pending review of implementation of the new TS

requirements after the revised TS is issued.

E8.4 (Closed) Escalated Enforcement Item (EEI) 50-261/94-16-04, Inadequate

Control Room Ventilation Testing Program: The Control Room Ventilation

System (CRVS) design was incomplete in that it did not consider all modes of

Heating, Ventilation, and Air Conditioning (HVAC) system lineups and the

effect of these lineups on Control Room habitability. The UFSAR, Sections 6.4

and 9.4.2, requires that the CRVS be capable of maintaining the control room

at a positive differential pressure with respect to adjacent areas and the

outdoors when the CRVS is operated in the emergency pressurization mode.

Neither design reviews nor surveillance testing identified that the CRVS was

unable to meet this requirement.

On May 7, 1994, the licensee identified during special ventilation balancing

testing that air pressure in Room E1/E2 which is adjacent to the control room

exceeded control room pressure. The licensee determined that, under certain

accident conditions, the Auxiliary Building Supply Fan (HVS-1) would continue

to supply air to Room E1/E2 while credit could not be taken for the ventilation

exhaust fan (HVE-7).

This event is described in more detail in Inspection

Report 50-261/94-16 and the licensee's September 29, 1994, response to the

violation.

The licensee revised plant operating procedures and emergency operating

procedures to place restrictions on HVS-1.

Engineering Surveillance Test,

EST-023, Control Room Emergency Ventilation System (once per 18 months),

was revised by Revision 10 to test the CRVS in the "worst case" mode and to

compare Control Room pressure to adjacent areas to ensure positive Control

Room pressure.

The inspector reviewed EST-023, Revisions 10 and 12 and noted that Section

8.6.2 requires that both HVE-7 and HVS-1 be secured prior to taking pressure

measurements in the Control Room and adjacent areas. Abnormal Operating

Procedure, AOP-005, Radiation Monitoring System, Revision 15 was also

reviewed and the response to the Control Room Radiation Monitor alarm is to

20

open the circuit breaker for HVS-1. The inspectors verified that the licensee

revised its procedures and tests the CRVS in the "worst case" mode. The

inspectors consider that the licensee has completed its corrective actions and

this item is closed.

E8.5

(Closed) LER 50-261/94-008-01, Condition Outside Design Basis Due to

Control Room HVAC Inoperability: This event was described and reviewed in

the previous Section E8.4. The item is closed.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls (71750)

R1.1

Tours of the Radiological Control Area (RCA)

The inspectors periodically toured the RCA during the inspection period.

Radiological control practices were observed and discussed with radiological

control personnel including RCA entry and exit, survey postings, locked high

radiation areas, and radiological area material conditions. With one exception

discussed in Section R1.3, the inspectors concluded that radiation control

practices were proper.

R1.2

Irradiated Fuel Shipment

a.

Inspection Scope (40500, 71750, and 86750)

The inspectors reviewed the licensee's requirements and procedures related to

irradiated fuel shipment. The review included a NAS assessment of shipment

readiness and table top exercises conducted with outside agencies.

In addition, the inspectors observed activities associated with the receipt of

empty spent fuel shipping casks, cask loading, decontamination, and the

August 12, 1996 shipment.

b.

Observations and Findings

NAS Assessment of Spent Fuel Shipment Readiness

In May 1996, NAS conducted an assessment of the Robinson spent fuel

shipping program in order to determine the readiness of the program to

conduct effective shipping activities. The results of this assessment were

documented in NAS Report R-SF-96-01, dated May 31, 1996. The inspectors

reviewed the report and determined that the assessment was thorough and

21

probing. The assessment identified one strength, four issues, and one

weakness. The major problems identified involved the following:

Some safety features for the spent fuel handling system which were

described in various licensing documents, were not procedurally

controlled or tested,

The training and qualification of spent fuel team members was not

effectively administered,

The Spent Fuel Shipping Manual, Certificate of Compliance, Safety

Analysis Report, and various technical manuals were not effectively

controlled,

The inspectors verified that CRs were initiated to address the problems

identified and that necessary actions were initiated to correct these problems

prior to initiation of actual spent fuel shipment activities. The inspectors noted

good management attention and sensitivity in correcting these problems prior

to the fuel shipment.

Receipt of Empty Spent Fuel Shippinq Casks

On July 9, the inspectors attended a pre-job briefing held prior to bringing two

empty spent fuel shipping casks on railcars inside the protected area. The

meeting was attended by personnel from maintenance, operations, radiation

protection, and corporate fuel shipping area that had actions or responsibilities

in moving the cask inside the protected area. The inspectors noted that good

discussions were held on the details and logistics for moving the casks. A

management representative was assigned to coordinate the activity in

accordance with PLP-37, for infrequent evolutions. As a result of good

coordination and planning, the casks were brought in without any major

incident. The inspectors reviewed the shipping receipt package, including the

radiological surveys of the railcars, to verify that the railcars were properly

received. No discrepancies were identified.

Table Top Exercise with Outside Agencies

On July 23, the licensee held a "table top" exercise with their staff and a

representative from the South Carolina Emergency Preparedness Divison

(EPD) Director's office. The exercise was to validate the procedures

necessary to address an accident involving the spent fuel shipment. This was

the first spent fuel shipment in several years. The exercise revealed that the

coordination between the licensee and the state organizations needed to be

improved.

On uly31,anoher"tale op"

22

On July 31, another "table top" exercise was held and included representatives

from all the involved South Carolina state and local agencies. The State

Police were concerned about the timely transmission of radiological

information. The differences between the state's and CP&L's emergency plan

was the most significant issue that surfaced during the exercise. The State

EPD had written their plan based on the licensee's plan. The licensee revised

their plan in the interim and had not advised the state of their action. The

issue was resolved by both organizations working together to resolve the

differences which consisted of reporting protocol. The licensee documented

the identified issues in CR 96-01797.

The inspectors concluded that the table top exercises with the outside

agencies revealed communication and coordination weaknesses in sufficient

time to have been resolved prior to the shipment.

Compliance with the Cask Certificate of Compliance

The inspectors reviewed whether the licensee met the conditions specified in

the Model No. 300 Spent Fuel Shipping Cask Certificate of Compliance (COC).

Based on a review of the list of authorized users, the inspectors verified that

Carolina Power & Light was a registered user of the IF-300 spent fuel shipping

cask. The inspectors reviewed Revision 31 of the COC and selected eighteen

of the specifications in the COC for verification of compliance.

The inspectors reviewed the licensee's Irradiated Fuel Data Sheets (IFDS)

dated July 22, 1996. The IFDSs provided information on the fuel's physical

characteristic, fissionable isotopic composition, and history, and a direct

comparison between specifications in the COC fuel requirements and the fuel

being shipped. The inspectors made an independent comparison between the

information in the IFDSs to the fuel's specifications in the COC.

Selected pages from the license's completed procedure, Corrective

Maintenance Procedure CM-M0303, Cask and Equipment Skid Annual

Inspection (IF-300 Series), Revision 6, were reviewed to verify that the casks

were being maintained. The completed procedure indicated that the

maintenance was performed on IF-303 and IF-304 during June and July 1996,

and that the following selected maintenance specifications from the COC were

performed:

96-ACG, Hydrostatic pressure test and annual leakage test

Installation of a new head gasket,

Installation of a new rupture disk,

96-ACG, test of cask precon valves and circle seal valves, and,

23

0 Testing of the relief and reseat pressure for the two neutron shield relief

valves plus their leak test results.

The inspectors reviewed completed procedure, Spent Fuel Shipping Procedure

SFS-001, IF-300 Shipping Cask Operations Revision 13, dated July 30, 1996,

and verified the procedure contained steps for draining and purging the cask.

Purging of the cask was a specification in the COC.

The inspectors determined that all of the COC specifications selected by the

inspectors were completed as required and the licensee was meeting the

conditions specified.

Procedures Controlling the Handling of Spent Fuel Shipments

The inspectors reviewed the licensee's "Spent Nuclear Fuel Shipping Program

Manual" (Plan) Revision 10, dated July 22, 1996, which discussed the Concept

of Operations, Organization and Responsibilities, and Training.

The inspectors reviewed the licensee's Spent Fuel Shipping Procedure

SFS-001, IF-300 Shipping Cask Operations Revision 13, dated July 30, 1996,

which discussed the spent fuel shipment process for receiving and inspection

of the spent fuel container railcars, relocating the cask to the decontamination

building, loading the fuel into the cask, transferring the cask to the

decontamination building, filling the cask with inert gas, and loading the cask

back onto the rail car. The inspectors selected Section 8.20 through 8.23 for a

detailed review. In the review, the inspectors noted that:

In SFS-001, a necessary procedural step to open cask drain valve CD-1

after performing Step 8.2.1.14 was missing. A closer review of the

missing step in SFS-001, revealed that the step was in place in Revision

12, of SFS-001.

It was concluded that while revising SFS-001 Revision

12 after performing a table top review of the procedure, a word

processing error resulted in the step being deleted in Revision 13 of

SFS-001. The inspectors verified that the operators had actually

performed the step and that a procedure step deviation was

documented.

As written, SFS-001 did not appear to accomplish three purges with

inert gas as required in the COC. SFS-001 step 8.21.15 stated that

"When helium exhausts from the drain hose, close the cask fill/drain

valve CD-i". The procedure proceeded to clearly require two distinct

purges. The licensee stated that although not proceduralized or

documented, that during this step, they allowed helium to flow through

the drain hose for approximately 10 to 15 minutes. In order to remove

24

any uncertainties concerning the adequacy of the initial purge, the

licensee performed an additional purge on each of the casks. The

licensee agreed that the procedure was not clear and that it would be

revised to clearly indicate three distinct purges.

The inspectors noted that an independent assessment of the licensee spent

fuel operating procedures was performed by VECTRA Technologies

Incorporated. The inspectors reviewed a letter dated May 23, 1996, from

VECTRA that stated VECTRA had reviewed the licensee's operating

procedures referenced as conditions of approval in the COC and determined

that the criticality control provisions were acceptable.

The inspectors concluded from the review that:

The licensee's Plan was organized and satisfactorily defined roles and

responsibilities in the fuel shipment,

Procedures were in place to maintain the cask, and

Procedures were in place to receive the cask, load spent fuel into the

cask, and ready the cask for shipment.

Radiological Surveys for Shipment

The inspectors reviewed licensee's radiological surveys to verify that the

licensee adequately decontaminated the spent fuel shipping cask to meet the

radiological requirement for transportation specified in 49 CFR 173.441.

The inspectors observed the licensee morning Health Physics briefings of

Radiation Work Permit (RWP) 96-0185 which was used to perform work on the

spent fuel cask. The briefings were detailed and informative. The briefings

updated personnel on the status of the cask decontamination efforts,

radiological conditions, clothing requirements for the area, and where they

were in the procedure. The inspectors accompanied the licensee into the work

areas and observed the licensee Health Physics practices around the cask

decontamination area and the railcar.

The inspectors observed the licensee decontaminate cask IF-304 using high

pressure spray, cleaning solvents, and scouring pads, in the cask

decontamination area. When the radiological surveys indicated that the

surface contamination was below the licensee's limits of 1000 disintegrations

per minute (dpm)/100 centimeter (cm) square, the licensee used procedure

SFS-001, IF-300 Shipping Cask Operations Revision 13 to transfer cask IF-304

from the decontamination area to the railcar.

25

The inspectors observed the licensee load the cask onto the railcar, conduct

radiation surveys around the railcar, perform gamma and neutron surveys

around cask IF-304, and perform contamination surveys (swipes) of the cask

and count the swipes in the lab. Once the surveys were completed, the

inspectors reviewed the licensee's survey sheets. This gamma/neutron survey

also satisfied one of the specifications of the COC discussed above.

After IF-304 cask was loaded onto the railcar, the inspectors conducted an

independent survey of the cask to determine if the radiation and contamination

levels were below the limits in 49 CFR 173.441. The inspectors determined

that the contact readings on the surface of the cask ranged from 2

millirem/hour (mRem/hr) to an isolated area that read 36 mRem/hr and, at 2

meters, radiation levels were less than or equal to 3.5 mRem/hr. The

inspectors also performed an independent surface contamination survey by

performing swipes of ten areas of the cask and observing the licensee count

the swipes. Most of the swipes averaged approximately 100 dpm/100 cm

square. All of the swipes taken by the inspector were less than the licensee's

limit of 1000 dpm/100 cm square.

The inspectors concluded that radiation and contamination levels were below

the transportation limits for shipments contained in 49 CFR 173.441 of 10

mRem/hr at 2 meters, 200 mRem/hr on contact, and less than of 2200

dpm/100 cm square loose surface contamination.

c.

Conclusions

The inspectors concluded effective procedures were implemented to safely

control irradiated fuel shipment activities. Minor spent fuel cask handling

procedure discrepancies identified were appropriately resolved by the licensee.

A NAS assessment of the spent fuel shipment program readiness was

thorough and probing. NAS assessment and table top exercise weaknesses

were properly resolved and effective program enhancements were

implemented prior to conducting shipment activities. The inspectors observed

that adequate controls were implemented during the August 12, 1996, spent

fuel shipment.

R1.3

Inadequate Labeling of Spent Fuel Cask Container

a.

Inspection Scope (71750)

While performing routine inspection activities in the RCA, the inspectors

determined that a loaded spent fuel shipping cask container did not have a

radioactive material label attached. The licensee initiated CR 96-01867 to

address this discrepancy. .

b.

Observations and Findings

On August 12, the inspectors observed the radiological controls for storing two

spent fuel shipping cask containers, loaded on separate railcars, inside the

RCA. The casks had recently been loaded with spent fuel and were awaiting

shipment from the site. The inspectors noted that radiological rope and

posting had been setup around both containers that housed each cask,

however, radioactive material labels were not attached to one of the cask

containers. The inspectors recalled during previous observations over the past

week, that the container had been properly labeled. After notifying RC

personnel of the potential problem, the cask container was surveyed and the

appropriate labels were affixed. The licensee initiated CR 96-01867 to address

this discrepancy.

10 CFR 20.1904, Labeling Containers, requires that containers of licensed

material be labeled with the words "CAUTION, RADIOACTIVE MATERIAL" or

"DANGER, RADIOACTIVE MATERIAL," and provide information regarding the

radiation levels and date the measurement was made. This information is

necessary to alert personnel working in the vicinity of the containers to take

precautions to avoid or minimize exposures. 10 CFR 20.1905 provides certain

exemptions from labeling containers. One of these exemptions include the

case where containers are in transport and the railcars carrying them are

placarded in accordance with the Department of Transportation regulations in

49 CFR 172. The inspectors determined that when the missing label was

identified, the licensee had not yet properly placarded the railcars in

accordance with 49 CFR 172, therefore, the labeling requirements of 10 CFR

20 were still applicable.

The inspectors reviewed the licensee's procedures for controlling the

radiological labeling requirements for containers with radioactive material in

excess of the limits established by Appendix C to 10 CFR 20. This included a

review of the following procedures:

Health Physics Procedure HPP-007, Handling and Storage of

Contaminated and Radioactive Material, Revision 18, and,

HPP-255, Shipping and Receiving the IF-300 Cask, Revision 10.

The inspectors determined that the procedures provided adequate guidance

and expectations for conforming to the requirements of 10 CFR 20.1904,

20.1905, and 49 CFR 172, for labeling containers. Based on discussions with

the licensee, they believed that the label had been removed by RC personnel

on August 11, when the cask was removed from its container and

decontaminated. In accordance with 10 CFR 20, a label is not required to be

27

affixed to the container when the cask is not loaded. Apparently, when the

cask was returned that same day, a label was not re-affixed to the container.

As corrective action, the licensee planned to revise the cask receipt checklist

contained in HPP-255 to include requirements and signoffs that a radiation

label be affixed to the spent fuel shipping container upon receipt and removed

only once the cask is accepted for shipment by the shipping carrier. The

inspectors concluded that this procedure enhancement would provide more

positive labeling controls and should prevent recurrence of this problem.

c.

Conclusions

The inspectors concluded this issue to be a violation of 10 CFR 20.1904 for

failure to label a container of licensed radioactive material in excess of

quantities listed in Appendix C to 10 CFR 20. This failure constitutes a

violation of minor significance and is being treated as a Non-Cited Violation,

consistent with Section IV of the NRC Enforcement Policy. This item will be

identified as NCV 50-261/96-10-02: Failure to Label Spent Fuel Cask

Container in Accordance with 10 CFR 20.

R2

Status of Radiation Protection Controls and Equipment

R2.1

Failure of Radiological Information Management System (RIMS)

a.

Inspection Scope (71750)

The inspectors reviewed the results of the licensee's investigation of loss of

RIMS. Two CRs and exposure estimates of affected individuals were

reviewed.

b.

Observations and Findings

The licensee has an electronic dosimetry system (EDS) and the EDS work

stations for all three sites are connected to a centralized computer. The dose

for each individual leaving the radiological control area is down loaded into the

RIMS database.

On June 8, 1996, RIMS entered a scheduled 33 hour3.819444e-4 days <br />0.00917 hours <br />5.456349e-5 weeks <br />1.25565e-5 months <br /> outage to make software

changes. The licensee took steps not to affect the Access Control software.

The system worked properly when an individual logged in. When the individual

logged out, the local work station indicated that a normal transaction took

place. However, the data was not loaded into the database. The licensee

discovered the problem when it was observed that there was excessive

downtime with PC Access Control. Two CRs were written. CR 96-01481 was

)written

by the site and CR 96-1612 was written by Corporate Radiological

Services.

The site E&RC organization obtained security records to determine who had

entered the RCA and the duration of their stay. The licensee determined that

39 individuals entered the RCA. Thermoluminescent dosimeters (TLDs) of

those individuals were pulled and read to obtain a conservative estimate of the

exposure dose received.

Exposure estimates were made for made for those

individuals without TLDs. The licensee was conservative in their estimates.

All individuals were interviewed and all reviewed and signed their estimated

dose. Thirty-eight mRem was the maximum dose assigned. The inspectors

observed and reviewed the licensee's investigation of the CR.

c.

Conclusions

The inspectors determined that the licensee's investigations and corrective

actions for CR 96-1612 were adequate. The investigation revealed that PC

Access Control software system worked as designed except that the Access

Control Recovery Screen appeared to accept data but did not. The inspectors

considered this incident an isolated occurrence requiring no additional

corrective action.

S1

Conduct of Security and Safeguards Activities (71750 and 81310)

S1.1

Inadequate Lighting of Spent Fuel Cask Rail Cars in the Protected Area

a.

Inspection Scope (71750)

The inspectors observed during a tour of the protected area that the lighting

under two rail cars inside the protected area was not adequate. The

inspectors discussed the discrepancy with security personnel and reviewed the

licensee's Industrial Security Plan and security procedures with regard to

protected area minimum lighting requirements.

b.

Observations and Findings

On July 25, the inspectors observed that extra lighting installed to illuminate

the space under two rail cars that were temporarily located inside the protected

area was inadequate. A string of incandescent light bulbs had been placed on

the outside of one of the cars and a single Halogen lamp was placed on the

ground near the other car. The inspectors observed that one of the

incandescent bulbs and the Halogen lamp had failed. The inspectors notified

the licensee of the lighting discrepancies and questioned whether minimum

lighting illumination under the cars was met under the conditions observed.

29

The licensee later measured the lighting levels under the rail cars and found it

to less than the required 0.2 foot-candles. However, the licensee believed that

the area was adequately backlighted.

The licensee performed an inspection within the protected area during the

evening of July 25 and identified four additional areas which had inadequate

lighting. Two paint sheds, a trailer, and an air compressor were identified as

requiring additional lights or bulb replacement. Corrective action was

completed the next day. CR 96-01731 was issued to document the lighting

discrepancies.

The inspectors later became aware that on July 12, a NAS individual had

identified to security personnel a lighting level concern for another trailer

located inside the protected area. The on-shift security staff failed to followup

on the concern indicating a lack of sensitivity to the lighting requirements.

10 CFR 73.46(c)(4) and 73.55(c)(5) requires that all exterior areas within the

protected area be illuminated to at least 0.2 foot candles measured horizontally

at ground level. In addition, Section 3.1.3 of the licensee's Industrial Security

Plan, Revision 32, dated April 26, 1996, states, in part, "the exterior protected

area will be lighted to a level sufficient for monitoring, surveillance, and

observation requirements, but not less than 0.2 foot-candles measured

horizontally at ground level. Compensatory measures for degraded illumination

(less than 0.2 foot-candles) in exterior portions of the protected area will be in

the form of increased visual surveillance." The inspectors reviewed the

Security surveillance sheets for July 1996. No additional surveillances were

logged for the rail cars indicating that the discrepant conditions had not been

identified.

c.

Conclusions

The installation of security lighting under the rail cars was inadequate, and

routine patrols of the area failed to identify this condition and correct the

deficiencies or implement compensatory measures. The failure to meet the

illumination level of at least 0.2 foot-candles or implement compensatory

measures for the degraded illumination conditions was identified as Violation

50-261/96-10-03: Failure To Follow Security Plan for Minimum Lighting

Requirements.

30

S1.2 Security Controls of Spent Fuel Shipments

a.

Inspection Scope (81310)

The inspectors reviewed the licensee's compliance with 10 CFR 73.37(f) with

regard to advance notification of irradiated fuel shipment, protection of

Safeguards shipment information, and security controls established for

irradiated fuel shipments from the site.

b.

Observations and Findings

By letter dated July 30, 1996, to the NRC the licensee complied with the prior

notification requirements of 10 CFR Part 73.37(f), by providing 10 days

advance notice of a shipment of irradiated fuel. This letter was also furnished

to the designated representatives of the Governors of South and North

Carolina, thus meeting the requirement to provide the states with 7 days

advance notice. The requirements of 10 CFR Part 73.21 were met in that the

licensee stamped as "Safeguards Information" those portions of the letter

which revealed dates, times and routes of the actual shipment.

Throughout this inspection, the licensee's efforts to protect Safeguards

Information from unauthorized disclosure was evident at all levels of

involvement.

Also noted was the compensatory measure utilized at the Robinson perimeter

when the site vehicle barrier was removed to allow the opening of the railroad

gate. An officer was continuously posted who was armed with a contingency

high-power rifle.

The inspectors found that the 3 Escorts were assigned to this shipment were

knowledgeable of their duties and responsibilities. They were also very

familiar with Emergency Procedures and the content of the Emergency Kit

located in the caboose of the train. The Senior Escort, a trained health

physicist from the Harris Nuclear Plant, explained to the inspectors the function

of the three radiation detectors found in this Kit as well as other contingency

equipment located therein. The multi-means of communication from the

locomotive and the caboose were also demonstrated to the inspectors, a

review of logs revealed that prior to the arrival of the CSX locomotive engine

the licensee had verified all telephone numbers, radio frequencies and cellular

capabilities for state, county and local law enforcement agencies along the

route of this shipment.

The inspectors learned that these Escorts were aware of the guidance found in

the following licensee procedures:

31

HPP-256, Advance Notification For Shipments

SEC-2120, Protection of Safeguards Information

HPP-255, Shipping of IF 300 Cask

NGG-006, Spent Fuel Manual

RSP-1.1, Duties of Shipment Escorts

SEP-2.1, Shipment Emergency Duties

On August 12, at 8:28 p.m., the train left the Robinson site and was

periodically monitored by the inspectors throughout the night until it arrived at

the Harris site at 3:45 a.m. the next day. Upon arriving at the Harris facility the

inspectors reviewed the licensee's record of communication checks and

determined that the required checks were accomplished as required every 90

minutes.

c.

Conclusions

The inspectors concluded that the licensee's program for shipping irradiated

fuel was found to be in compliance with 10 CFR Part 73.37. No discrepancies

were identified with the security controls for the spent fuel shipment conducted

on August 12.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

at the conclusion of the inspection on August 26, 1996. An interim exit was

conducted on August 7, 9, and 12, 1996. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

32

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Clements, Manager, Site Support Services

D. Crook, Senior Specialist, Licensing/Regulatory Compliance

C. Hinnant, Vice President, Robinson Nuclear Plant

J. Keenan, Director, Site Operations

R. Krich, Manager, Regulatory Affairs

B. Meyer, Manager, Operations

G. Miller, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outage Management

J. Moyer, Manager, Maintenance

D. Stoddard, Manager, Operating Experience Assessment

R. Warden, Acting Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Environmental Control

D. Young, General Manager, Robinson Plant

NRC

P. Byron, Resident Inspector, Brunswick

J. Zeiler, Acting Senior Resident Inspector

33

INSPECTION PROCEDURES USED

IP 37550:

Engineering

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 60855:

Operation of an Independent Spent Fuel Storage Installation (ISFSI)

IP 61726:

Surveillance Observations

IP 62703:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 81310:

Physical Protection of Shipments of Irradiated Fuel

IP 86750:

Solid Radioactive Waste Management and Transportation of Radioactive

Materials

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Type Item Number

Status

Description and Reference

VIO

50-261/96-10-01

Open

Inadequate Corrective Actions for SOV

Discrepancies (Section E8.1)

NCV 50-261/96-10-02

Open

Failure to Label Spent Fuel Cask Container in

Accordance with 10 CFR 20 (Section R1.3)

VIO

50-261/96-10-03

Open

Failure To Follow Security Plan for Minimum

Lighting Requirements (Section S1.1)

Closed

Type Item Number

Status

Description and Reference

LER

50-261/93-015-00

Closed

Pressurizer Pressure Transmitters Out of

Calibration (Section M8.1)

LER

50-261/94-003-00

Closed

TS Required Shutdown Due to Emergency

Diesel Generator Inoperability (Section M8.2)

LER

50-261/94-011-00

Closed

Technical Specification 3.0: Emergency

Diesel Generator Inoperability (Section M8.3)

34

LER

50-261/94-019-01

Closed

TS Violation Due to Exceeding Pressurizer

Cooldown Rate (Section M8.4)

URI

50-261/96-08-01

Closed

Review Licensee Investigation and Resolution

of Solenoid Valve Discrepancies (Section

E8.1)

VIO

50-261/94-24-01

Closed

Inadequate Testing of Alternate AC Power

Source (Section E8.2)

EEI

50-261/94-16-04

Closed

Inadequate Control Room Ventilation Testing

Program (Section E8.4)

LER

50-261/94-008-01

Closed

Condition Outside Design Basis Due to

Control Room HVAC Inoperability (Section

E8.5)

Discussed

Type Item Number

Status

Description and Reference

IFI

50-261/94-08-02

Open

Incorporate 24 Hr Load Testing into TS

Surveillance Requirements (Section E8.3)