ML14178A442

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Insp Rept 50-261/93-33 on 931121-1225.Violation & Deviation Noted.Major Areas Inspected:Operational Safety Verification, Surveillance & Maint Observation,Engineering Safety Feature Sys Walkdown & Plant Safety Review Committee
ML14178A442
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 01/20/1994
From: Christensen H, Ogle C, William Orders
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A438 List:
References
50-261-93-33, NUDOCS 9402080109
Download: ML14178A442 (12)


See also: IR 05000261/1993033

Text

v REcu

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION il

101 MARIETTA STREET, N.W., SUITE 2900

ATLANTA, GEORGIA 30323-0199

Report No.:

50-261/93-33

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Facility Name: H. B. Robinson Unit 2

Inspection Conducted:

November 21 - December 25, 1993

Lead Inspector:

2

Z4

5&'

W. . Orders, enior esi

t Inspector

Date Signed

Other Inspector:

Lz i-2

Og le,

Residenl/ nsplyor

Date Signed

Approved b :_

_

_

_-_-----

S0. C r stensen, Chief

Date Sgn d

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation,

engineered safety feature system walkdown, plant safety review committee

activities, and followup.

Results:

One Violation was identified which involved a failure to take adequate

corrective action for pressurizer pressure transmitters found out of

tolerance, paragraph 4; a non-cited violation was identified which involved a

failure to have a procedure to control a transfer canal pumpdown, paragraph

3.b; a Deviation was identified which involved the failure to install RHR pump

suction pressure instrumentation as committed to in response to Generic Letter 88-17, paragraph 3.c; and an Inspector Followup Item was identified involving

the need for verification of CV spray and turbine auto stop circuitry

continuity following routine testing, paragraph 3.d.

9402080109 940120

PDR

ADOCK 05000261

Q

PDR

REPORT DETAILS

1.

Persons Contacted

  • R. Barnett, Manager, Projects Management

C. Baucom, Senior Specialist, Regulatory Compliance

D. Bauer, Regulatory Compliance Coordinator, Regulatory Compliance

J. Benjamin, Shift Outage Manager, Outages and Modifications

S. Billings, Technical Aide, Regulatory Compliance

B. Clark, Manager, Maintenance

  • T. Cleary, Manager, Technical Support

D. Crook, Senior Specialist, Regulatory Compliance

  • C. Dietz, Vice President, Robinson Nuclear Project

R. Downey, Shift Supervisor, Operations

J. Eaddy, Manager, Environmental and Radiation Support

S. Farmer, Manager, Engineering Programs, Technical Support

B. Harward, Manager, Engineering Site Support, Nuclear Engineering

Department

  • S. Hinnant, Director, Site Operations

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

E. Lee, Shift Outage Manager, Outages and Modifications

A. McCauley, Manager, Electrical Systems, Technical Support

R. Moore, Manager, Operations

D. Morrison, Shift Supervisor, Operations

D. Nelson, Manager, Outage Management

A. Padgett, Manager, Environmental and Radiation Control

  • M. Pearson, Plant General Manager

D. Seagle, Shift Supervisor, Operations

M. Scott, Manager, Reactor Systems, Technical Support

E. Shoemaker, Manager, Mechanical Systems, Technical Support

W. Stover, Shift Supervisor, Operations

D. Winters, Shift Supervisor, Operations

Other licensee employees contacted included'technicians, operators,

engineers, mechanics, security force members, and office personnel.

  • Attended Exit Interview on January 12, 1993.

Acronyms and initialisms used throughout this report are listed in the.

last paragraph.

2.

Plant Status

The Unit began the report period in a forced outage which began on

November 17, when a drain valve on the discharge of one of the main

feedwater pumps was determined to be leaking. On November 20, 1994, a

RH based Augmented Inspection Team reported to the site to investigate

problems which had been identified with the Unit's restart from RFO15.

During that startup, a number of problems were identified involving

operator performance, and fuel manufacturing errors. Details of that

inspection are delineated in Inspection Report 50-261, 93-34. The Unit

remained shutdown through the end of the report period performing

2

required maintenance on the diesel generators and implementing

corrective actions to equipment and personnel deficiencies identified

during the forced outage.

3.

Operational Safety Verification (71707)

a.

General

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with

regulatory requirements. These activities were confirmed by

direct observation, facility tours, interviews and discussions

with licensee personnel and management, verification of safety

system status, and review of facility records.

To verify equipment operability and compliance with TS, the

inspectors reviewed shift logs, Operation's records, data sheets,

instrument traces, and records of equipment malfunctions. Through

work observations and discussions with Operations staff members,

the inspectors verified the staff was knowledgeable of plant

conditions, responded properly to alarms, adhered to procedures

and applicable administrative controls, cognizant of in-progress

surveillance and maintenance activities, and aware of inoperable

equipment status. The inspectors performed channel verifications

and reviewed component status and safety-related parameters to

verify conformance with TS. Shift changes were routinely

observed, verifying that system status continuity was maintained

and that proper control room staffing existed. Access to the

control room was controlled and operations personnel carried out

their assigned duties in an effective manner. Control room

demeanor and communications were appropriate.

Plant tours and perimeter walkdowns were conducted to verify

equipment operability, assess the general condition of plant

equipment, and to verify that radiological controls, fire

protection controls, physical protection controls, and equipment

tagging procedures were properly implemented.

b.

SFP Draindown

At 5:15 a.m. on December 3, 1993, a SFP low level alarm was

received in the control room. An AO dispatched to investigate

reported that the SFP level was between 36 feet and 36 feet 2

inches, just below the nominal SFP low level alarm setpoint of 36

feet 2.5 inches. The AO observed that the SFP level was

decreasing as a result of the transfer canal pump discharge hose

siphoning SFP water back into the canal when the pump was secured.

The hose was approximately 1 to 2 inches below the surface of the

water. The siphon was broken by lifting the hose clear of the

surface of the SFP and the transfer canal was subsequently pumped

down to restore SFP level.

3

In response to the event, the Operations manager directed the

cessation of SFP transfer canal pumping operations. An ACR was

written and a team formed to review the event. As a result of the

licensee investigation, the need for a procedure to govern the

pumpdown of the SFP transfer was identified. The licensee

committed to developing this procedure prior to February 1994.

The inspectors reviewed log entries associated with the event;

interviewed the cognizant shift supervisor, system engineer, and

the plant manager; and inspected the general arrangement of the

pump discharge hose used to reduce the transfer canal water level.

The inspectors also reviewed the evaluation completed in response

to the ACR for the event.

Based on this effort, the inspectors determined that the.siphoning

occurred as a result of not removing the hose from the higher

elevation SFP following the pumpdown of the transfer canal.

This

pumping was necessitated by weir gate leakage to the canal.

No

procedure existed to govern this evolution. Furthermore, licensee

management was aware of this lack of procedural guidance prior to

the SFP draindown.

While no TS violation occurred as a result of this level

excursion, the inspectors did note that the placement of the hose

had bypassed an anti-siphon hole in the SFP cooling water return

line located at approximately 36 feet 5 inches. This feature is

credited in a safety evaluation in the FSAR as providing

protection against inadvertently siphoning the SFP.

The failure to perform the transfer canal pumpdown in accordance

with a procedure is a violation of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings. This

violation will not be subject to enforcement action because the

licensee's efforts in identifying and correcting the violation

meet the criteria specified in Section VII. B of the Enforcement

Policy. This is identified as a non-cited violation, NCV 93-33

01:

Failure to Proceduralize Transfer Canal Pumpdown.

C.

Preparations For RCS Draindown

The inspectors reviewed preparations for reducing RCS water level

to approximately 16 inches below the vessel flange to support

vessel head reinstallation. This review was documented on a mid

loop/reduced inventory checklist and forwarded to Region II under

separate cover on December 13, 1993.

For this draindown, the

vessel water level remained well above the reduced inventory

setpoint of -36 inches. However, the checklist verifies items

from Generic Letter 88-17 which minimize the potential for and

consequences of a loss of decay heat removal with less than full

vessel.

4

Overall, the inspectors noted that the licensees preparations were

good and in general, fulfilled the recommendations of GL 88-17.

The inspectors did note that the draindown procedure used for this

evolution, did not contain a precaution to minimize perturbations

in RCS level when the vessel inventory was reduced. (This

precaution was contained in the appropriate procedure for reduced

inventory.)

Following questions on this point by the inspectors,

GP-009, Filling, Purification, and Draining of the Refueling

Cavity was revised to include a precaution to this effect.

The inspectors also observed that the licensee's sensitivity to

the plant's performance while in this condition was adequate. For

example, a camera monitor was installed in the control room to

provide a remote indication of the RCS water level as measured on

the tygon tube standpipes. Though the camera monitor has been

used in the auxiliary building in the past, its placement in the

control room was a significant enhancement in the control room

monitoring capability. Furthermore, a watchstander was dedicated

to this monitor when the RCS was lower than 5 feet above the

flange. The inspectors also observed that the responsible control

room watchstanders were cognizant of the RCS water level and

sensitive to variation between the indicators. These observations

are considered strengths.

However, on December 16, 1993, the inspectors observed that all

incore thermocouples displayed "bad" instead of the incore

temperature. The inspectors were advised that this was the result

of RCS temperature being reduced below the 80* F low end setpoint

of the incore thermocouple system. This had been deliberately

accomplished to ensure that the mismatch between the head and

vessel temperatures was within procedural limitations.

The inspectors questioned the shift supervisor and the Engineering

Technical Support staff on the prudence of intentionally disabling

all incore temperature monitoring equipment. The inspectors were

advised that RCS temperature was being raised to restore the

temperature indication. On a subsequent tour of the control room

on December 17, 1993, the inspectors observed that RCS temperature

had been raised and that incore thermocouple indication had been

restored. The inspectors were also advised that since RHR flow

existed through the core, alternate indications of core

temperature conditions existed. Furthermore, the inspectors were

informed that in the event core cooling was lost, core

temperatures would rise and upon exceeding 80' F, the thermocouple

indication would be restored. The inspectors determined from

interviews of Engineering Technical Support personnel that

alternatives to reducing RCS temperature below 80' F and

subsequently disabling the incore thermocouples may have existed.

For example, the head could have been permitted to warm up after

placement on the vessel.

Alternatively, the incore thermocouple

temperature could have been determined using measuring and test

equipment. The inspectors concluded that the licensee's

5

temporarily disabling incore thermocouple temperature indication

with a reduced RCS water level was a Weakness.

In reviewing the licensee's written response to Generic Letter 88-17, Serial NLS 89-024 dated February 1, 1989, the inspectors

noted that the licensee committed to the installation of a

"suction pressure indicator and associated low pressure alarm [on]

the RTGB for each RHR pump."

No such features exist. RHR

indication on the RTGB consists of: RHR total flow, pump discharge

pressures, and temperatures of pump and heat exchanger discharges.

Alarms are provided for low RHR pump cooling water flows, high and

low RHR pump discharge pressures, RHR heat exchanger low flows,

and RHR pump motor overload/trip. In response to the inspectors'

questions on why this commitment was not satisfied, the inspectors

were provided extracts Modification 1011, Instrumentation for Mid

loop Operation. This information documented the licensees

evaluation and subsequent installation of RHR pump discharge

pressure instruments and alarms in lieu of the suction pressure

instrumentation. This is identified as a deviation, DEV 93-33-02,

Failure to Install RHR Pump Suction Pressure Instrumentation as

Committed To In Response To Generic Letter 88-17.

d.

ESFAS/RPS Logic Testing

On December 20, 1993, in response to NRC Information Notice 93-38,

Inadequate Testing of Engineered Safety Features Actuation

Systems, the licensee determined that routine testing performed on

the CV spray system was deficient. Specifically, Maintenance

Surveillance Test Procedures, MST-016:

Containment Pressure

Protection Channel (SET I, II, and III) Testing (Bi-Weekly); MST

022: Safeguard Relay Rack Train "A" (Monthly); and MST-023:

Safeguard Relay Rack Train "B" (Monthly) were all found deficient,

in that, following testing the actuation circuit continuity was

not completely verified. The CV spray system is designed such

that the actuation relays are normally de-energized. On a high

high containment pressure condition, the containment spray logic

matrix operates to energize the CV spray actuation relays. The

licensee determined that no continuity checks were performed on

test switches in series with the input relay coil or the bistable

outputs upon their restoration to the normal position at the end

of the surveillances. The failure to establish this continuity

could interrupt a valid actuation signal and hence, render the

circuit inoperable.

Subsequently, the licensee also determined that similar

deficiencies existed in routine testing performed to verify proper

operation of the turbine auto stop circuitry (reactor trip

coincident with turbine trip if greater than P-7 interlock).

In response to these discoveries, the licensee stated that they

satisfactorily conducted testing to verify the continuity of these

circuits. Furthermore, the licensee was evaluating the need to

6

modify existing testing for these circuits. Pending the

resolution of these reviews this item will be tracked as an

inspector follow-up item, IFI

93-33-03: Need For Verification Of

CV Spray And Turbine Auto Stop Circuitry Continuity Following

Routine Testing.

The inspectors reviewed the operation of the CV spray and auto

stop circuits with the system engineer. Additionally, the

inspectors reviewed portions of the WR/JO used to document the

testing performed after the discovery of the MST deficiencies.

Other than the IFI identified above, the inspectors have no

further questions.

One deviation was identified. Except as noted above, the

area/program was adequately implemented.

4.

Maintenance Observation (62703)

a.

General

The inspectors observed safety-related maintenance activities on

systems and components to ascertain that these activities were

conducted in accordance with TS, approved procedures, and

appropriate industry codes and standards. The inspectors

determined that these activities did not violate LCOs and that

required redundant components were operable. The inspectors

verified that required administrative, material, testing,

radiological, and fire prevention controls were adhered to. In

particular, the inspectors observed/reviewed the following

maintenance activities:

SP-1280

Cycle 16 Fuel Assembly Inspection (Video Review)

WR/JO 93-APAH1

Install New Air Start Distributor On B EDG

WR/JO 93-AKXD1

Replace Pressurizer Transmitter PT-457

WR/JO 93-APAH1

Install New Air Start Distributor On B EDG

b.

Fuel Assembly Inspection

On December 10, 1993, the inspectors reviewed a videotape taken

during the performance of Special Procedure, SP-1280, Cycle 16

Fuel Assembly Inspection. This special procedure was accomplished

to verify the position of gadolinium bearing fuel elements in

assemblies X-43 and X-39. As a result of this special procedure,

the licensee concluded that the gadolinium bearing fuel elements

were properly positioned in these assemblies. Based upon the

inspectors comparisons of fuel element serial numbers recorded on

the videotape and on fuel assembly bundle maps, the inspectors

concurred with this conclusion. The inspectors have no further

questions on this special procedure.

7

c.

EDG Air Start Distributor Maintenance

On December 20, 1993, in response to concerns raised by the

licensee during the root cause analysis of B EDG start failures,

the air start distributor for that engine was replaced. During

the installation of the new distributor, while torquing the drive

shaft nut to the 185 ft - lbs of torque specified in the assembly

procedure, the camshaft threads failed. Following procurement of

a new camshaft, the air distributor was successfully installed on

December 22, 1993.

The engine was successfully operated in accordance with OST-401,

Emergency Diesels (Slow Speed Start), on December 21, 1993. ( A

subsequent failure to start, however, was observed for the engine

on December 26, 1993.)

The inspectors witnessed portions of the air start distributor

maintenance performed on December 20 and 21, 1993. Overall, the

inspectors noted that the maintenance was well performed and the

work was accomplished in accordance with appropriate procedures.

Maintenance supervisory participation was also evident.

Though not in attendance for the camshaft thread stripping, the

inspectors concluded from their review of maintenance

documentation and interviews of cognizant personnel that the

threads were overtorqued as a result of erroneous torque valves

provided by the vendor. The torque valves for this nut provided

by the manufacturer have ranged as high as 480 ft-lbs. In fact,

while attempting to achieve 480 ft-lbs of torque on November 24,

1993, a failure of the air start cam was incurred. The licensee

has revised Corrective Maintenance Procedure, CM-627, Emergency

Diesel Generator Air Start System Maintenance, to reflect a

required torque of 55 ft-lbs. This revision was based on a

written recommendation received from the vendor. The inspectors

reviewed the vendor's letter specifying the revised torque and the

licensee's review performed to change CM-627. The inspectors have

no further questions on this maintenance.

C.

Pressurizer Pressure Transmitter Calibration/Replacement

On November 30, 1993, the licensee determined though a special

calibration, that pressurizer pressure transmitters PT-455 and PT

457 were out of tolerance. These instruments provide pressure

inputs for the low pressure reactor trip, high pressure reactor

trip, and safety injection initiation. Both instruments

experienced a maximum drift of 0.017 mV resulting in both

instruments reading at worst approximately 3.4 psig too high. In

response to this out of tolerance condition the licensee replaced

the two transmitters. Additionally, the licensee performed an

analysis of the out of tolerance condition and concluded that no

violation of TS resulted.

8

The inspectors reviewed the instrument calibration data sheets and

work packages associated with this event as well as the licensee's

evaluation of the as found calibration data. Additionally, on

December 14, 1993, the inspectors witnessed the replacement of PT

457 in accordance with WR/JO 93-AKXD1. The inspectors have no

further questions on this documentation. The inspectors concurred

that no violation of TS occurred.

Inspection Report 93-28 discussed a series of calibrations

performed on PT-455, PT-456, and PT-457 during RFO-15. That

report outlines instrument adjustments of PT-455, PT-456, and PT

457 on October 15, 1993, following drift outside allowed tolerance

just 2 days after the instruments had been calibrated on October

13, 1993. Transmitter PT-456 was also found out of tolerance on

October 15, 1993, however, on November 30, 1993, it was within

calibration tolerances.

10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires

that measures be established to assure that the cause of

conditions adverse to quality be determined and corrective action

taken to preclude repetition. Contrary to the above, on November

30, 1993, the licensee determined that pressurizer pressure

transmitters PT-455 and PT-457 had drifted out of calibration

tolerance. The licensee's corrective action to a similar

occurrence of these instruments drifting out of tolerance between

October 13 and October 15, 1993, failed to prevent this event.

This is identified as a violation, VIO 93-33-04:

Failure To Take

Adequate Corrective Action For Pressurizer Pressure Transmitters

Found Out Of Tolerance.

One violation was identified. Except as noted above, the

area/program was adequately implemented.

5.

Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements. For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were adhered to, the required administrative approvals and

tagouts were obtained prior to test initiation, testing was accomplished

by qualified personnel in accordance with an approved test procedure,

the tests were completed at the required frequency, and that the tests

conformed to TS requirements. Upon test completion, the inspectors

verified the recorded test data was complete, accurate, and met TS

requirements, test discrepancies were properly documented and rectified,

and that the systems were properly returned to service. Specifically,

the inspectors witnessed/reviewed portions of the following test

activities:

OST-401

Emergency Diesels (Slow Speed Start) (EDG B

Only)

9

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

6.

Fire Protection/Prevention Program (64704)

The inspectors toured the plant routinely throughout the report period.

During those tours, the fire protection features of the following areas

were inspected:

Diesel Generator "A" Room

Diesel Generator "B" Room

Safety Injection Pump Room

Auxiliary Building First and Second Level Hallways

Emergency Switchgear Room

Component Cooling Pump Room

Turbine Building

The manual fire fighting equipment, automatic fire detection systems,

and fire area/fire zone boundary walls, floors, and ceilings associated

with the above plant areas were inspected and verified to be in service

or functional.

Based on these observations, it was concluded that the

fire protection features associated with these areas were being

adequately maintained.

During this inspection period, the inspectors did not witness any

instances of inadequate implementation of fire prevention administrative

procedures, such as the posting of fire watches, there have been a

number of cases during the last 6 months in which a fire watch left his

watch station before being relieved. This is considered a weakness in

the licensee's implementation of the fire protection/prevention program

and the instances were identified in Inspection Reports 50-261/93-19 and

50-261/93-21 as Non-cited Violations.

The licensee's implementation of housekeeping procedures were reviewed

during the inspectors' tours. Other than minor discrepancies which were

identified to the licensee and immediately resolved, the licensee's

control of combustibles and flammable materials, liquids and gases, as

well as general housekeeping were found to be adequate.

The inspectors visually verified the proper alignment of the sectional

control valves in the main fire protection water supply system.

Except as noted above, the licensee's fire protection/prevention program

appeared to be adequately implemented.

10

7.

Followup (92700, 92701, 90702)

(Closed) Unresolved Item 93-19-06, Adequacy of Control Room Ventilation

System Surveillance Testing

Unresolved item, URI 93-19-06, documented that testing accomplished by

OST-163 and OST-924 failed to fully comply with the requirements of TS 4.15.f.3. This TS requires verification that on a SI test signal or

high radiation test signal the control room ventilation system switches

into the emergency pressurization mode with flow through the ACU.

Instead, both OSTs merely check for proper alignment of dampers and

starting of fans in the system. In response to the URI, the licensee

stated that OST-750, Control Room Emergency Ventilation System,

Biweekly, verified flow through the ACU while in the emergency

pressurization mode on a biweekly basis. The licensee stated that the

flow data obtained from OST-750 on a biweekly basis in combination with

the observations of OST-163 and OST-924 provided sufficient evidence to

satisfy the requirements of TS 4.15.f.3. However, the licensee also

committed to modifying OST-163 and OST-924 to require the verification

of air flow through the ACU so that each OST can satisfy TS

independently. URI 93-19-06 is considered closed.

8.

Exit Interview (71701)

The inspection scope and findings were summarized on January 12, 1993,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. Dissenting comments were not received

from the licensee. The licensee did not identify as proprietary any of

the materials provided to or reviewed by the inspectors during this

inspection. The following items were identified and reviewed during

this inspection period:

Item Number

Description/Reference Paragraph

NCV 93-33-01

Failure to Proceduralize Transfer Canal

Pumpdown.

DEV 93-33-02

Failure to Install RHR Pump Suction Pressure

Instrumentation as Committed To In Response To

Generic Letter 88-17.

IFI

93-33-03

Need For Verification Of CV Spray And Turbine

Auto Stop Circuitry Continuity Following Routine

Testing.

VIO 93-33-04

Failure To Take Adequate Corrective Action For

Pressurizer Pressure Transmitters Found Out Of

Tolerance.

9.

List of Acronyms and Initialisms

ACR

Adverse Condition Report

ACU

Air Cleaning Unit

AO

Auxiliary Operator

10

11

CFR

Code of Federal Regulation

CM

Corrective Maintenance

CV

Containment Vessel

DEV

Deviation

EDG

Emergency Diesel Generator

FSAR

Final Safety Analysis Report

GL

Generic Letter

GP

General Procedure

IFI

Inspection Followup Item

LCO

Limiting Condition for Operation

MST

Maintenance Surveillance Test

Mv

Milli-volt

NCV

Non-cited Violation

NRC

Nuclear Regulatory Commission

OST

Operations Surveillance Test

psig

Pounds Per Square Inch Gauge

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RTGB

Reactor Turbine Gauge Board

SFP

Spent Fuel Pit

SI

Safety Injection

SP

Special Procedure

TS

Technical Specification

URI

Unresolved Item

VIO

Violation

WR/JO

Work Request/Job Order