ML14178A293

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Insp Rept 50-261/92-27 on 920905-1109.Violations Noted.Major Areas Inspected:Operational Safety Verification,Surveillance Observation & Meeting W/Local Officials
ML14178A293
Person / Time
Site: Robinson 
Issue date: 11/04/1992
From: Christensen H, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A291 List:
References
50-261-92-27, NUDOCS 9211180130
Download: ML14178A293 (18)


See also: IR 05000261/1992027

Text

1

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tRUNITED

STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

C

Report No.:

50-261/92-27

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson Unit 2

Inspection Conducted: September 5 - October 9, 1992

Lead Inspector:

1-,(i

"

/// /

L.

. Gartr,

Senior Resident Inspeptor

Date Signed

Other Inspector* C. R. Ogle, Resident Inspector

Approved by:___

5

H. 0. Christensen, Chief

Dat4 Sined

Reactor Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, and

meeting with local officials.

Results:

Two violations were identified concerning inadequately established procedures

and failure to implement procedures for reduce RCS inventory operations. In

addition, a number of weaknesses and deficiencies were identified with reduced

inventory operations. These included inadequate technical knowledge,

inadequate-communications, an -ineffective Operating Experience Feedback

program, and incomplete logkeeping (paragraph 3).

A violation was identified for failure to secure a containment penetration

with a deactivated closed containment isolation valve within four hours as

required by limiting condition for operation of Technical Specification 3.6.3.

(paragraph 3).

9211180130 921104

PDR ADOCK 05000261

G0

PDR

2

A non-cited violation was identified for failure to establish as adequate

maintenance procedure in that the procedure identified the incorrect isolation

amplifier to be installed in a safety-related circuit (paragraph 5).

The licensee's emergency preparedness response to an Alert condition

associated with a CO2 release in a vital area was good (paragraph 3).

Insufficient procedural precautions and poor configuration control resulted in

the inability to remotely reopen the shutdown cooling isolation valve during

inservice inspection testing (paragraph 3).

Operations conducted a less than thorough RCS leak check (paragraph 4).

1.

Persons Contacted

  • R. Barnett, Manager, Outages and Modifications
  • C. Baucom, Senior Specialist, Regulatory Compliance
  • R. Chambers, Plant General Manager, Robinson Nuclear Project

B. Clark, Manager, Maintenance

T. Cleary, Manager, Technical Support

C. Dietz, Vice President, Robinson Nuclear Project

R. Femal, Shift Supervisor, Operations

W. Flanagan, Manager, Operations

  • W. Gainey, Manager, Plant Support
  • G. Grant, Acting Manager, Operations
  • W. Hammond, Engineer, Quality Assurance
  • J. Harrison, Manager, Regulatory Compliance
  • R. Howell, Senior Specialist, Nuclear Assessment Department

P. Jenny, Manager, Emergency Preparedness

D. Knight, Shift Supervisor, Operations

A. Padgett, Manager, Environmental and Radiation Control

D. Seagle, Shift Supervisor, Operations

  • D. Stadler, Onsite Licensing Engineer, Nuclear Licensing

G. Walters, Operating Event Followup Coordinator, Regulatory Compliance

  • A. Wallace, Shift Operations Coordinator

D. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

NRC Managements Visits

S. Ebneter, Regional Administrator - Region II, E. Merschoff, Division

Director - DRP, E. Adensam, Director -

Project Directorate II-1, R.

Trojanowski - Regional State Liaison Officer, and H. Christensen,

Section Chief - DRP Section 1A were onsite September 24 to visit the

facility, present the SALP to the licensee, and meet with local

officials.

  • Attended exit interview on October 14, 1992.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2.

Plant Status

The unit began the report period in cold shutdown for removal of foreign

material from the SI system and associated safety-related components.

On September 6, decay heat removal was interrupted for a longer period

than anticipated during RHR-750 valve stroke time surveillance testing.

Once closed, the RHR-750 valve could not be reopened remotely due to an

open permissive unknowingly being defeated by the system clearance

established for RWST foreign material inspection activities. The RCS

temperature increased from 136 to 140 degrees F in the time,

approximately 35 minutes, required to manually reopen RHR-750.

2

Inspection, flushing, and cleaning activities of the SI system were

completed on September 10. Modification and SI system performance tests

were also satisfactorily completed on September 10.

After management

review, the A and B SI pumps and the SI system was declared operable on

September 12.

Excessive seal leakoff from the B RCP resulted in reduced

inventory operation from September 12 to 17 while the seal package was

repaired. Bonnet-to-body leak repairs to the CVCS letdown isolation

valves CVC-460A and B and replacement of the control room ventilation

compressor for WCCU 1A subsequently delayed restart until September 23.

The turbine generator was placed in service on September 24 and 100%

power operation was obtained on September 26. At 3:33 a.m. on September

30, an Alert was declared due to a slow release of carbon dioxide fire

suppressant (considered a toxic gas) into pipe alley (mechanical CV

penetration area).

Later that morning, at 9:01 a.m., the Alert was

exited after the supply of carbon dioxide to the leak was depleted and

oxygen levels in the immediate vicinity of the leak, as well as adjacent

areas, were verified to be normal.

The unit continued full power

operation for the remainder of the report period without further

significant operational events.

3. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the inspectors

reviewed shift logs, Operation's records, data sheets, instrument

traces, and records of equipment malfunctions. Through work

observations and discussions with Operations staff members, the

inspectors verified the staff was knowledgeable of plant conditions,

responded properly to alarms, adhered to procedures and applicable

administrative controls, cognizant of in-progress surveillance and

maintenance activities, and aware of inoperable equipment status.

The

inspectors performed channel verifications and reviewed component status

and safety-related parameters to verify conformance with TS. Shift

changes were observed, verifying that system status continuity was

maintained and that proper control room staffing existed. Access to the

control room was controlled and operations personnel generally carried

out their assigned duties in an effective manner. Control room demeanor

and communications were typically adequate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were properly

implemented.

3

Foreign Material Removal From The SI System

Foreign material in the SI system and associated components has

previously been discussed in IR 92-21 and 92-24. During this report

period, the licensee completed implementation of their SI System

Recovery Plan and returned the SI system to service on September 12,

1992. Activities completed included: installation of M-1134, Install

Permanent Strainers In SI Pump Recirculation Lines, for the A and B SI

pumps; inspection of selected SI and RHR piping and components; and,

perform system tests to demonstrate operability. In addition, as

required by Confirmation Of Action Letter, dated September 1, 1992, a

meeting was conducted with Region II management to discuss results of

recovery plan activities and root cause of the event. This meeting was

conducted in the Region II Office on September 8, 1992. After review of

the licensee's presentation, regional management determined that the

actions taken to remove foreign material from the safety-related systems

and components and the inspections performed of these systems and

components provided a reasonable level of confidence that these systems

and components would perform their safety functions if required. Also,

it was determined that the licensee had complied with the conditions of

the Confirmation Of Action Letter and thus could proceed, when ready,

above hot shutdown conditions. During the meeting, the licensee

committed to perform, during the next refuel outage, additional flushes

(or inspections) of piping sections which were deemed impractical to

flush with fuel in the core.

The inspectors inspected selected activities associated with the SI

System Recovery Plan. The inspection activities included: observation

of video camera inspections; verification that foreign material controls

were implemented around open systems, review of post maintenance test

requirements to ensure that reassembled components would function

properly; and, observation of maintenance and modification work

activities. In particular, the inspectors observed the disassembly and

inspection of the A SI pump recirculation line orifice. No foreign

material was found in the line or orifice. The licensee's review of

previous recirculation flow data revealed that the data point used to

determine that a 10% flow reduction had occurred in the A SI pump

recirculation flow was abnormally high. The licensee provided no

explanation for the abnormity. The inspectors agreed that the data was

approximately 2 to 3 gpm higher than normal.

However, since both the A

and B SI pump data was offset by about the same amount and the same

measuring equipment was utilized, it is possible that one of the other

SI system test valves, such as SI-895K or SI-895U, was not fully closed

when the higher than normal data was obtained. The inspectors also

reviewed the material presented during the September 8 meeting and have

no further questions at this time.

Unanticipated Extension Of Loss Of Decay Heat Removal During Testing

On September 6, 1992, during valve stroking per of OST-703, ISI Primary

Side Valve Test, the shutdown cooling supply line isolation valve, RHR

750, could not be reopened using the RTGB control switch. The valve was

4

subsequently manually opened by an operator who had been stationed at

the valve to observe stem travel.

During the approximate 35 minutes it

took to reopen the valve, the observed RCS coolant temperature rise

attributed to the inability to remotely open the valve was approximately

4 degrees F, i.e., 136 to 140 degrees F. For comparison, the similar

temperature rise attributed to securing RHR shutdown cooling was

approximately 13 degrees F.

Subsequent investigation revealed that an open permissive interlock

associated with the RHR pumps' RWST suction isolation valves, SI-862 A

and B, was not present due to the control circuits for these valves

being de-energized. These valve control circuits had been de-energized

to establish a clearance boundary for foreign material inspection

activities of the RWST and associated ECCS pumps' supply piping.

ACR 92-339 was issued to address the root causes of this event.

Immediate corrective actions to preclude this particular event included

identification of a procedure change request to provide a precaution

note in OST-703 to address the valve interlocks associated with RHR-750

and RHR-751 (the redundant isolation valve to RHR-750).

During clearance development, personnel did not identify that the SI-862

A and B control circuit de-energizations would open opening permissive

contacts in the RHR-750 control circuitry. The inspectors verified that

a thorough review of CWD B-190628 sheets 248 and 249 (SI-862A and B

control circuits respectively) would have identified that the opening

control circuit on sheet 212 (RHR-750) was disabled by de-energizing the

SI-862 A and B control circuits. Failure to identify adverse equipment

impacts during the clearance development process was an example of poor

configuration control. The inspectors plan to review the final ACR

package, when available, to verify that adequate corrective actions are

taken.

Reduced Inventory Operation

The inspectors' observations and review of reduced inventory evolutions

revealed several deficiencies. Each of these items are discussed in

more detail in subsequent paragraphs. Associated with the inventory

reduction of September 12, the identified deficiencies included: 1)

inadequate procedures to preclude loss of decay heat removal during

inventory reduction; 2) inadequate technical knowledge to analyze the

consequences of draining the RCS with the PRT pressurized; 3) failure of

the pre-evolution shift briefing to define under what conditions the RCS

inventory was to be accomplished; 4) inadequate communications between

management levels which allowed the inventory reduction to be performed

in a manner other than that envisioned by the Acting Operations Manager;

and, 5) an ineffective OEF program which failed to familiarize

Operations personnel with industry events involving level

instrumentation errors associated with inventory reduction with the RCS

pressurized. On September 13, a subsequent inventory reduction from -25

inches to -34 inches demonstrated a lack of sensitivity by the operating

shift to potentially violating procedure requirements, in that, the

5

inventory reduction was accomplished utilizing only one instrument

channel.

In addition, refilling the PRT on September 16 resulted in the

following findings: 1) the procedure failed to provide precautions

concerning the potential impact of pressurizing the PRT if the PRT is

refilled too rapidly; 2) incomplete logkeeping was demonstrated, in

that, the logs did not record that the initial operator response to an

unexpected reactor vessel water level increase due to the PRT

pressurization was to add more water to the vessel; and, 3) the

Operations corrective action program was poorly implemented in that the

initial response by the operator was not entered into the program for

subsequent analysis and management review. Although a number of

deficiencies were identified during specific reduced inventory

evolutions, no safety significant plant transients resulted from these

items.

ACR 92-343 was issued to document the event sequence associated with the

September 12 inventory reduction and to determine root causes and

required corrective actions. The event sequence as extracted from the

ACR, relevant documentation, and from inspectors' observations of

evolutions in progress follows. On September 10, while performing

preliminary checks to support starting the B RCP, it was discovered that

the no. 1 seal leakoff flow exceeded the 5 gpm procedure maximum

limitation of OP-101, Reactor Coolant System And Reactor Coolant Pump

Startup And Operation. Subsequent attempts to correct the condition

were unsuccessful.

On September 11, plant management, after

consultation with the NSSS, determined that the seal should be removed

and repaired.

Seal removal required the RCS system inventory to be

reduced to below the pump flange, i. e.,

-25 inches below the reactor

vessel head flange. On September 12, prior to the 7:15 a.m. shift

briefing, the inspectors discussed with the Acting Operations Manager

the problem experienced at another utility with vessel water level

instrumentation accuracy due to the RCS being pressurized. The

inspectors were shown the procedure steps which would be used to vent

the RCS system to the CV atmosphere during system draining. At the end

of the shift briefing, the Acting Operations Manager conducted a Case I

briefing, as designated in PLP-037, Conduct Of Infrequently Performed

Test and Evolutions, concerning the scheduled RCS partial draining. The

briefing emphasized that draining the RCS system too rapidly would

result in instrumentation errors. However, the PLP-037 briefing did not

inform the operating crew that the draindown was to be performed with

the RCS vented to the CV atmosphere nor did it include the industry

event discussed by the inspectors. Subsequent to this briefing,

discussions among the operating crew and a chemistry technician resulted

in the decision by the SS to draindown with 5.0 psig nitrogen pressure

on the PRT, an option allowed by GP-008, Draining The Reactor Coolant

System. The decision was based on the desire to minimize corrosion

product formation due to increased oxygen concentrations. The Acting

Operations Manager was not informed of this decision. In preparation

for draining the RCS, the PRT level was lowered to a point at which the

PZR relief line discharge nozzles inside the PRT were uncovered and the

PZR PORVs were blocked open. This allowed the PZR to be vented directly

to the PRT gas space.

6

At 9:40 a.m., draining of the RCS was initiated in accordance with GP

008. At approximately 4:30 p.m. with PZR water level at 15%, the

draindown was stopped while the loop 2 and 3 RCS water level

instruments, LT-403 and LT-404, were placed in service. At this time,

the shift SRO expressed concern to the SS that having nitrogen pressure

on the RCS with the standpipe instrumentation (LT-403 and LT-404 which

feed RTGB level indicators LI-403 and LI-404 respectively) vented to the

CV atmosphere would force water up the standpipes and provide erroneous

indications. He was aware of the rule of thumb that 33 feet of water is

equal to 15 psig. Several people on shift, including the SS, did not

remember that there had been large variations between the instrument

readings when nitrogen pressure was used and when the pressure was

subsequently vented off. The fact that the procedure allowed the system

to be drained in this manner was further construed as evidence that this

would not be a problem. The decision was made to resume the draindown

with 5 psig nitrogen pressure on the PRT and verify that LI-403 and LI

404 would come on scale (zero reading) when vessel level decreased to

the vessel flange top as by indicated RVLIS (flange top is 83.3% on

RVLIS).

Shortly after 5:00 p.m., the inspectors, while verifying that

the inventory reduction was being accomplished in accordance with GP

008, noted that the RCS vent valve to the CV atmosphere, RC-572, was

closed and the alternate method with 5.0 psig nitrogen pressure on the

PRT was being utilized. At this time, the cold calibrated PZR water

level instrument, LI-462 was off-scale low and LI-403 and LI-404 were

not yet on scale. The inspectors discussed the observation with the

Acting Operations Manager who was in the control room at the time. He

was unaware that the PRT and, consequently, the RCS was pressurized.

The inspectors re-iterated that pressurization of the RCS would non

conservatively effect LI-403, LI-404 and their associated tygon tube

indicators inside the CV since these were vented to the CV atmosphere.

Initially, the inspectors were informed that hydraulic losses between

the PRT and the instrumentation would reduce the effect of the pressure

in the PRT and that previous experience had indicated that there was

little difference between level readings taken with the system

pressurized and the system vented. The inspectors indicated that

hydraulic losses would be small and that the system should be considered

a static system. The inspectors requested the licensee to provide the

correction and the basis for the correction which would be used to

adjust LI-403 and LI-404 readings. Subsequent discussions among the

Acting Operations Manager, the SS, the SRO, and I & C technicians

resulted in the decision to stop the draindown, secure nitrogen to the

PRT, and vent the RCS to the CV atmosphere. During the venting process,

the tygon tubes associated with LI-403 and LI-404 were observed to

determine the effect the pressurization had on this instrumentation.

The indicated water level in the vessel was observed to decrease from

approximately 15 feet above the vessel flange to approximately 5 feet

above the vessel flange when the RCS was fully depressurized. The

draindown was then resumed. Later that evening, the licensee discovered

that WR/JOs 92-ANNW1 and 92-ANNX1 which had calibrated LI-403 and LI-404

level indicators prior to initiating the draindown had failed to

specify, as required by GP-008 step 5.1.8, that the associated alarm

switches also be calibrated. The complete instrumentation loops were

  • 0

7

subsequently calibrated. Draindown to -25 inches was completed on the

morning of September 13.

As noted above, inspection activities identified several significant

deficiencies associated with the evolution. The inspectors noted that

with RVLIS not required to be inservice per TS or by GP-008, draining of

the RCS with 5.0 psig of nitrogen on the PRT in accordance with GP-008

would result in loss of decay heat removal.

With a 10 foot non

conservative error in the indicated level verses the actual RCS level,

LI-403 and LI-404 would not come onscale until the actual RCS water

level reached -120 inches below the vessel flange top. However, the RHR

pump providing decay heat removal would cavitate and have to be shutdown

before that level would be reached since the middle of the loop is at

72 inches below the vessel flange. The planned evolution was to stay

about -36 inches so that the provisions concerning midloop operations

(as committed in the licensee's responses to GL 88-17, Loss Of Decay

Heat Removal) would not be required to be implemented. Subsequent NAD

review of previous GP-008 revisions revealed that a typographical error

had apparently occurred during revision 13 (issued April 29, 1988).

Earlier revisions to GP-008 had specified 0.5 psig nitrogen pressure be

used. There was no documentation that the change to 5.0 psig had been

intentional.

The fact that GP-008 was inadequately established so that

compliance with the procedure could potentially cause a significant

operational event is a VIO: Failure To Adequately Establish GP-008 To

Preclude The Loss Of Decay Heat Removal During RCS Inventory Reduction,

92-27-01.

Significant deficiencies were also identified in the OEF program. The

inspectors reviewed the outstanding change request to GP-008 and the

current revision being processed. There was no indication that lessons

learned from the industry event described in IN 92-16 supplement 1,

i.e., a February 1992 loss of decay heat removal event due to inventory

reduction with the PRT pressurized, had been identified to be

incorporated in GP-008. A review of the OEF process revealed that IN 92-16 supplement 1 had been received onsite on June 10, 1992, and at the

time of the inspection, had not been reviewed for applicability to the

site and distributed for action. The large backlog of OEF items had

previously been identified as an issue in June 1992 by the Regulatory

Compliance subunit, which is responsible for the OEF program

implementation. NAD had also previously identified this as a program

weakness and ACR 92-314 had been initiated on August 17, 1992. However,

due to resource limitations, a plan to correct the problem was not

submitted to management until October 8, 1992. At the end of the report

period, the licensee had not established a schedule to work off the

backlog.

The inspectors reviewed training records which revealed, via personnel

initials, that the operating shift involved in the draindown had read

about the industry event as part of the real time training process. A

Westinghouse letter, detailing the event which was later the subject of

IN 92-16 supplement 1, had been included with the reading material

associated with IN 92-16. This material had been distributed during

8

April and May to licensed personnel for their onshift review. An

interview with the SS revealed that he had no previous recollection of

the IN 92-16 supplement 1 event. The procedure writer, who holds an NRC

license and was assigned the preparation of the GP-008 revision 25, had

also reviewed the real time training material.

Thus, the OEF program

was demonstrated to be ineffective in familiarizing personnel with a

significant industry event.

As described in the event narrative above, LT-403 and LT-404 and their

associated alarms were not calibrated as required by GP-008 step 5.1.8

prior to placement in service. This constituted a failure to implement

procedures as required by TS 6.5.1.1.1.a and is a VIO: Failure To

Implement GP-008 In That RCS Water Level Instrumentation Loops Were Not

Calibrated As Required, 92-27-02.

The shift's inability to correctly resolve a technical question

concerning the impact of RCS pressurization on instrumentation

demonstrated a lack of technical expertise, especially in the area of

hydraulics. Furthermore, the failure to request assistance from other

organizations such as Technical Support or to consult the next

management level to resolve a technical difference of opinion among

licensed crew members was considered a weakness.

Communications of management's expectations were not successfully

accomplished. Communications between the SS and the Acting Operations

Manager were inadequate in that the Acting Operations Manager assumed

that the SS knew that the draindown was to be performed with the RCS

vented to the CV atmosphere. When the decision was made to use nitrogen

pressure in the PRT, the SOM was informed but Operations management was

not notified of the decision. Also, the shift PLP-037 briefing was

inadequate, in that, when GP-008 provided instructions for different

methods to be used for inventory reduction, the specific method to

accomplish the task was not discussed. Also, the PLP-037 briefing

failed to discuss significant industry events such as that described in

IN 92-16 supplement 1.

On September 13, it was necessary to further reduce RCS level to allow

additional inspection of the B RCP pump shaft for possible scoring.

This additional draindown involved lowering water level approximately to

a level just above -36 inches, the trigger point for entering midloop

operation. Midloop operation required additional procedural controls

and equipment to be in service.

For example, 2 independent RCS level

channels, one SI pump, and midloop CV integrity were required for

midloop operation. Because meeting these requirements would extend the

outage and level reduction below -36 inches was not necessary, the

decision was made to maintain RCS water level above this trigger value.

At the time of the additional reduction in RCS inventory, LI-403 was

inoperable, reading low by approximately 10 inches, and RVLIS with an

error tolerance of 6% was not sufficiently accurate to perform the

draindown. The draindown was accomplished with use of only one

instrument channel, LI-404. During the morning, the inspectors observed

that RCS inventory as indicated on LT-404 was approximately -33 inches.

9

When the inspectors asked what the indicated RCS level was on the tygon

tubes attached to the LT-403 and LT-404, operating personnel were

unaware of their present reading. Since the tygon tube readings were

known to be approximately 2 inches lower than LT-404, the inspectors

were concerned that midloop operation may have inadvertently been

entered. The SS directed that the tygon tube readings be obtained.

Both tygon tubes were reported to be slightly below -35 inches.

The

tygon tubes were not monitored when the draindown was performed. The

inspectors noted that the control operator's log had recorded at 0:05

a.m. that RCS level had been lowered to -34 inches by LI-404. Thus

based on the fact that at -33 inches on LI-404 the tygon tubes were

below -35 inches, it was possible that at -34 inches on LI-404, the

tygon tubes could have been below -36 inches. However, do to accuracy

of the data it was not possible to say that midloop operation had been

entered for a limited time without the procedural requirements for

midloop operation being met. However, Operations' reliance on one

instrument channel, which was non-conservative relative to other

available indications, to perform an inventory reduction near to a

procedural limitation reflected a lack of sensitively to the potential

to violate procedural requirements.

On September 16, during preparations to refill the RCS, the PRT was

filled from 12% to 70%. During the PRT filling, one and/or both PW

pumps were used. Rapid filling caused the gas volume to be reduced and

the PRT to pressurize. After the PRT high pressure alarm was received,

the PRT vent was opened. However, due to the small size of the vent

path, the control operator also adjusted the fill rate to control the

pressure increase. Approximately 12 minutes after securing the PRT

fill, the control operator observed that LI-404 indicated that RCS level

had changed from -24 increased to -12 inches. Believing that RCS water

level needed to be increased, he opened HCV-121. Within approximately 2

minutes, while observing VCT level and discussing his actions with the

SRO, he realized that HCV-121 should be closed to decrease RCS

inventory. He subsequently restored RCS level to -17 inches, the level

designated by the SS. The event review determined that the PRT pressure

had been allowed to increase to the point at which the elevation

difference between the PRT and PZR was overcome and water had been

forced out of the PRT back into the PZR through the blocked opened

PORVs. The inadvertent water addition to the RCS reflected a lack of

technical knowledge and a failure to pursue the implications of an

observed phenomena. Procedure reviews revealed that precautions or

notes were not provided to warn of this potential consequence when the

PRT is refilled. In addition, the inspectors noted that the initial

operator action which could have compounded the causality was not logged

or entered into a corrective action program. Failure to log the initial

operator action represents inadequate logkeeping. Furthermore, the

failure to capture the operator's response in the Operations corrective

action program for subsequent analyses and management review was

considered a weakness.

Containment Spray Relief Line Leak

10

On September 25, 1992, while performing routine inspection activities,

the inspectors observed leakage from the CS piping. This was reported

to Operations personnel who determined that the leak, approximately 1

drop per 5 seconds, originated at a weld on relief valve SI-871

tailpipe. The tailpipe was repaired on September 26. The inspectors

verified that TS 3.3.2.2.b LCO was entered and that TS 3.3.2.2.c

provisions were complied with when the repair was performed.

Furthermore, the inspectors verified that OST-355, Containment Spray

System Integrity Test (Annual) was successfully performed prior to

returning the system to service.

Failure To Implement TS Action Within Required Time

On October 2, 1992, at approximately 1:30 p.m., while performing OST

701, Inservice Inspection Valve Test (Quarterly), RC-553, a 3/8 inch air

diaphragm operated CV isolation valve on the gas analyzer sample line

from the PRT, failed to open. The valve was left in the closed position

and WR/JO 92-AQGB1 was initiated at 3:59 p.m. to repair the valve. At

approximately 9:00 p.m. on the same day, the SS while performing a

review of the completed OST-701 identified that this valve was a CV

isolation valve and TS 3.6.3 LCO action statement should have been

performed. TS 3.6.3 required that with one or more automatic

containment isolation trip valves inoperable, either: a. restore the

inoperable valve(s) to operable status within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />, or b. isolate the

affected penetration(s) within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> by use of a deactivated automatic

valve(s) secured in the isolation position(s), or c. isolate the

affected penetration(s) within 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> by use of a closed manual

valve(s) or blind flanges(s), or d. be in cold shutdown within the next

36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />.

At 9:16 p.m., the penetration was isolated as required by TS 3.6.3, in that, RC-553 and RC-516 (the redundant CV isolation valve)

were verified to be closed and the power was removed from the valves to

deactivate them in the isolated position. ACR 92-363 was issued on

October 2 to investigate the event and determine corrective actions to

preclude recurrence. Failure to isolate the gas analyzer sample CV

penetration (designated as P-1) with deactivated isolation valves within

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br /> as required by TS 3.6.3 is a VIO: Failure To Isolate Gas

Analyzer CV Penetration Within 4 Hours With Deactivated Isolation Valves

As Required By TS 3.6.3, 92-27-03.

Alert Due To CO2 Release In Pipe Alley

On September 30, 1992 at 3:33 a.m. an Alert was declared due a slow leak

of fire suppressant, CO2 gas, into pipe alley. The Alert was terminated

at 9:01 a.m. that same day after the effected CO2 bottles were verified

to be empty and the oxygen concentrations in pipe alley and adjacent

spaces were verified to be normal.

The CO2 gas was discharged to the

plant stack via means of the normal auxiliary building ventilation

system. Oxygen concentrations measured a few feet away from the leak

location never decreased to more than approximately 90% of the normal

oxygen concentration in air.

The event was initiated when personnel reconnected a refilled CO2 bottle

into slot 1 of the north and south cable vault fire suppression system.

The CO2 bank for these areas was located in the south pipe alley. When

a pilot head discharge hose containing a stuck open solenoid valve, CD

13, was sufficiently reconnected to the pilot head to open the spring

loaded outlet check valve, the fire technician heard the CO2 discharge

into the header and immediately attempted to loosen the connection.

However, this attempt was abandoned when the fire technician heard the

discharge valves on other bottles in the CO2 bank open. The other non

pilot head CO2 bottles opened when the discharge header pressure

exceeded their outlet check valve setpoint. Since there was no valid

fire suppression system actuation signal, the discharge valves into the

north and south vault area remained closed. Therefore, the only release

points from the pressurized system was from leakage associated with the

discharge piping components, i.e., the partially engaged hose

connection. The fire technician left the area and reported the event to

the control room. Actions were then taken to secure the area, evaluate

the potential impact on plant equipment and operations, monitor the

oxygen concentrations within the affect and potentially affected areas,

establish required fire watches, and develop recovery actions. At 8:44

a.m., by using a specially assembled pressure gage (none was available

on the discharge header) each effected CO2 bottle was verified to be

depleted.

ACR 92-358 was initiated on September 30 to investigate the

solenoid valve failure and the resultant event. The inspectors will

review the completed ACR, when available, as part of the routine

inspection program.

The Alert was declared in accordance with OMM-031, Emergency Action

Level Procedure User's Guide, step 5.1.17 which defines CO2 as a toxic

gas. This step states that the decision to declare an Alert for a toxic

gas release should be based upon factors such as the release rate and

the effected area's volume with the intent to determine whether the

release would endanger personnel that require access to equipment

required to safely operate the plant. It was prudent to consider this

event as an Alert since the effected area was the mechanical CV

penetration area and under some plant conditions, personnel would

require rapid access to this area for manual equipment operation. Also,

it was uncertain whether the partially disengaged coupling would remain

together or become separated, i.e., release rate would substantially

increase.

The overall response to the event was good. The OSC and TSC were

activated at 4:30 and 4:43 a.m., respectively. Shift turnover among OSC

and TSC organizations were successfully performed when day shift

personnel arrived at approximately 7:00 a.m..

The initial state and

counties' notifications were issued within 15 minutes (at 3:45 a.m.) and

subsequent followup messages were issued at approximately one hour

intervals (at 4:43, 5:33, 6:43, 7:45, and 8:36 a.m.).

The state and

counties were notified at 9:07 a.m. of the event termination. The NRC

was notified of the event within one hour, at 4:17 a.m.. A press

release was issued at 6:35 a.m. which resulted in several calls to the

12

main switchboard from the general public.

Public relations personnel in

the victors center were utilized to help respond to these inquires.

The South Carolina Emergency Preparedness Department activated a portion

of their facility at 5:42 a.m. and a South Carolina Department Of Health

And Environmental Control representative arrived onsite at 7:30 a.m..

He was briefed by the licensee and visited the effected area. The

inspectors asked the state representative if he had any concerns. He

indicated that he had none.

The inspectors were notified at approximately 3:45 a.m., via the

licensee's beeper system, that an Alert had been declared and that the

TSC and OSC was being activated. The inspectors arrived in the control

room at approximately 4:05 a.m. and monitored the licensee's response to

the event from either the control room or TSC until the Alert was

terminated. The inspectors verified that: the event was properly

classified; notifications were timely and adequate; appropriate measures

were taken to ensure equipment and personnel were not adversely affected

by the release; the TSC was adequately staffed; appropriate

communications were maintained among both onsite and offsite emergency

response organizations; recovery actions were developed considering

ALARA and contingency actions as necessary; and, recovery actions were

properly implemented.

Management Changes

During the inspection period a number of organizational reassignments

became effective. The Technical Support Manager was assigned to NED in

the corporate office. His position was filled by the Technical Support

engineering support supervisor. The NED and NAD onsite unit managers

were transfered to the Brunswick facility. The Technical Support

mechanical supervisor assumed the NED site unit manager position. Until

the NAD site unit manager position is filled, the NAD site unit

engineering assessment manager has been designated as acting manager.

Three violations were identified. Except as noted above, the

area/program was adequately implemented.

4. Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems and components to ascertain that these activities were

conducted in accordance with license requirements. For the surveillance

test procedure listed below, the inspectors determined that precautions

were adhered to and the required administrative approvals were obtained

prior to test initiation. Upon test completion, the inspectors verified

the recorded test data was complete, accurate, and test discrepancies

13

were properly documented and rectified as appropriate. Specifically,

the inspectors witnessed/reviewed portions of the following test

activity:

OST-052

RCS Leakage Test And Examination Prior To Startup

Following An Opening Of The Primary System

OST-052

On September 21, 1992, the inspectors conducted a CV housekeeping and

RCS leakage inspection, as well as, observing Operations personnel

perform part of OST-052. Miscellaneous debris (paper, tape, paint

chips, rubber gloves, etc.) observed by the inspectors were removed by

the HP accompanying the inspectors. Approximately one-quarter cubic

foot of debris was collected. Operations personnel identified and

initiated work requests to repair the following items: pipe cap leak on

A accumulator piping drain line, boric acid buildup on primary sample

valve PS-954A packing gland, boric acid buildup on the connector to the

B loop RCS flow instrument root isolation valve RC-513, and boric acid

buildup on a seal table isolation valve. In addition to these, the

inspectors also noted a pipe cap leak on the C accumulator piping drain

line and a packing leak on FW-45, B S/G wide range level instrument LT

487 root isolation valve. The FW-45 packing leak had caused a small

puddle of water under the B hot leg piping. Based upon the puddle size

and the leak rate, this water puddle was there when Operations personnel

performed their leak check. Failure to detect the puddle indicated that

a less than thorough inspection had been performed by Operations. In

addition, the inspectors observed several areas in which there were

water on the floor due to OSTs and maintenance activities which had been

performed earlier. Since small leaks are easier to detect by the

presence of water on the floor, performing a leak check with water on

the floor due to other activities could easily result in small leaks not

being detected. Thus, the failure to wipe up spilled water prior to

performing a leak check constituted a poor work practice. Primary

leakage is typically maintained low at the site, 0.05 to 0.1 gpm.

No violations or deviations were identified. Except as noted above, the

area/program was adequately implemented.

5. Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS, approved procedures, and appropriate industry codes

and standards.

The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, radiological, and fire

prevention controls were adhered to. In particular, the inspectors

observed/reviewed the following maintenance activities:

WR/JO 92-AMWN1

Support To Video Inspection Of SI Piping

14

WR/JO 92-AMRB2

Install SI Pump Recirculation Strainers

Installation Of Incorrect Isolation Amplifier

On September 24, 1992, power increase was stopped at 40.5% due to the

high steam line flow bistable FC-495 actuating.

Initial troubleshooting

by I & C indicated that the channel had spiked and would not reset due

to loop width at this load.

Load was reduced approximately 1% to clear

the bistable.

At 41% power, FC-495 again actuated.

Investigation

revealed that a recently replaced isolation amplifier, PM-447D,

associated with AMSAC was the incorrect model.

This had placed an

additional 200 ohm resistor into the current loop; thereby, causing the

entire loop to be adversely affected. The isolation amplifier will be

replaced when the correct model can be obtained from the vendor. During

instrumentation data sheet preparation associated with the AMSAC

installation modification, the isolation amplifier model number had been

incorrectly entered on the data sheets for AMSAC modules PM-446D, PM

447D, LM-474B, LM-485B and LM-496B. The correct model number was EIP

E013DD-37 whereas EIP-EO13DD-1, the model number for all other isolation

amplifiers used at the site, was provided on the MMM-006 Appendix B data

sheets. The licensee has initiated procedure changes to correct the

data sheets, as well as, update EDBS with the correct model numbers.

Failure to specify the correct model number on the data sheets

constituted a violation for failure to adequately establish procedures.

This violation will not be subject to enforcement action because the

licensee's efforts in identifying and correcting the violation meet the

criteria specified in Section VII.B of the Enforcement Policy. Hence,

this item is identified as an NCV: Failure To Adequately Establish

Maintenance Procedures For Replacement Of AMSAC Isolation Amplifiers,

92-27-04.

One NCV was identified.

Except as noted above, the area/program was

adequately implemented.

6. Meeting With Local Officials (94600)

On September 24, 1992, the Regional Administrator, the DRP Division

Director, the Regional State Liaison Officer, the Section Chief

responsible for the site, and the inspectors met with local officials

representing the cities of Darlington, Florence, and Hartsville, the

town of Bishopville, and the emergency preparedness organizations for

the State of South Carolina, Chesterfield, Darlington, Florence, and Lee

counties. The local officials expressed no concerns about the operation

of the facility.

7. Exit Interview (71701)

The inspection scope and findings were summarized on October 14, 1992,

with those persons indicated in paragraph 1. The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary. In response to the inspectors'

conclusion involving inadequate logkeeping (see paragraph 3), the

15

licensee indicated that recent emphasis on logkeeping had resulted in an

improving trend in this area. Also, the licensee stated that the root

cause determination to be developed for OMM-027 no.92-046, inadvertent

vessel level increase associated with the PRT repressurization, would

capture the operator's response. The inspectors did not agree that

investigation into why an event occurred would necessarily address the

response to an event. Excluding these items, no additional dissenting

comments were received from the licensee. The licensee did not identify

as proprietary any of the materials provided to or reviewed by the

inspectors during this inspection.

Item Number

Description/Reference Paragraph

92-27-01

VIO - Failure To Adequately Establish GP-008 To

Preclude The Loss Of Decay Heat Removal During

RCS Inventory Reduction (paragraph 3)

92-27-02

VIO - Failure To Implement GP-008 In That RCS

Water Level Instrumentation Loops Were Not

Calibrated As Required (paragraph 3)

92-27-03

VIO - Failure To Isolate Gas Analyzer CV

Penetration Within 4 Hours With Deactivated

Isolation Valves As Required By TS 3.6.3,

(paragraph 3)

The following NCV was identified and reviewed during this inspection

period.

Item Number

Description/Reference Paragraph

92-27-04

NCV - Failure To Adequately Establish

Maintenance Procedures For Replacement Of AMSAC

Isolation Amplifiers (paragraph 5)

8.

List of Acronyms and Initialisms

a.m.

Ante Meridiem

ACR

Adverse Condition Report

ALARA

As Low As Reasonably Achievable

AMSAC

ATWS Mitigating System Actuation Circuitry

ATWS

Anticipated Transient Without Scram

CFR

Code of Federal Regulations

CS

Containment Spray

CV

Containment Vessel

CVC

Chemical & Volume Control

CVCS

Chemical and Volume Control System

CWD

Control Wiring Diagram

DRP

Division of Reactor Projects

0

EDBS

Equipment Data Base System

ECCS

Emergency Core Cooling System

FC

Flow Control

16

gpm

Gallons Per Minute

F

Fahrenheit

GL

Generic Letter

GP

General Procedure

HCV

Hand Control Valve

HP

Health Physics

i.e.

That is

IE

Inspection and Enforcement

I&C

Instrumentation & Control

IN

Inspection Notice

ISI

Inservice Inspection

LCO

Limiting Condition for Operation

LI

Level Indicator

LM

Level Module

LT

Level Transmitter

MMM

Maintenance Management Manual

NAD

Nuclear Assessment Department

NCV

Non-Cited Violation

NED

Nuclear Engineering Department

NOV

Notice of Violation

NRC

Nuclear Regulatory Commission

NSSS

Nuclear Steam System Supplier

OEF

Operating Experience Feedback

OMM

Operations Management Manual

OP

Operations Procedure

OST

Operations Surveillance Test

p.m.

Post Meridiem

PLP

Plant Program

PM

Pressure Module

PORV

Power Operated Relief Valve

PRT

Pressurizer Relief Tank

Psig

Pounds per square inch - gage

PW

Primary Water

PZR

Pressurizer

RC

Reactor Coolant

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RTGB

Reactor Turbine Generator Board

RVLIS

Reactor Vessel Level Instrumentation System

RWST

Refueling Water Storage Tank

SALP

Systematic Assessment of Licensee Performance

SI

Safety Injection

SOM

Shift Outage Manager

SRO

Senior Reactor Operator

SS

Shift Supervisor

TS

Technical Specification

TSC

Technical Support Center

VIO

Violation

VCT

Volume Control Tank

WR/JO

Work Request/Job Order

WCCU

Water Cooled Condensing Unit