ML14176A752

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Insp Rept 50-261/89-12 on 890611-0710.Violations Noted.Major Areas Inspected:Operational Safety Verification,Surveillance & Maint Observation & Operator Requalification Exam Failure Control
ML14176A752
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 07/31/1989
From: Dance H, Garner L, Jury K
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14176A749 List:
References
50-261-89-12, NUDOCS 8908230088
Download: ML14176A752 (10)


See also: IR 05000261/1989012

Text

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UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA ST., N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/89-12

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name:

H. B. Robinson

Inspection Conducted:

June 11 - July 10, 1989

Inspector: /4--

7/3 /

L. W. Garner, Senior Reside t Inspector

D te Si nd

K. R. yry, Resient Insplector

D te Sig d

Approved by:

3/

H. C. Dance, Section Chief

Da e Signed

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, onsite

followup of events,

operator requalification exam failure control,

and

follow-up on previous inspection items.

Results:

One violation with two examples was issued involving inadequate design controls

for OT delta T and OP delta T setpoints.

This is indicative of a lack

of attention to details for control of reactor protection system setpoints,

paragraphs 5.a and 7.

The licensee is in the process of verifying that manual isolation of SW to

non-safety related components can be accomplished in a timely manner if

required, paragraph 5.c.

The licensee is in the process of determining why two spent fuel assemblies

have become unlatched from a fuel handling tool during spent fuel pool fuel

movements, paragraph 5.

Procedure controls and licensee's sensitivity regarding removal of licensed

operations from shift duties upon failure to pass requalification exams are

considered adequate to preclude this situation from occurring, paragraph 6.

PDR ADCr:: 05000261

u

FTC

0I

REPORT DETAILS

1.

Persons Contacted

R. Barnett, Maintenance Supervisor, Electrical

  • J. Benjamin, Engineering Supervisor, Plant Systems

C. Bethea, Manager Training

H. Bryon, Instructor

R. Chambers, Engineering Supervisor, Performance

  • D. Crook, Senior Specialist, Regulatory Compliance

J. Curley, Director, Regulatory Compliance

  • C. Dietz, Manager, Robinson Nuclear Project

R. Femal, Shift Foreman, Operations

W. Flanagan, Manager, Design Engineering

W. Gainey, Supervisor, Operations Support

E. Harris, Director, Onsite Nuclear Safety

D. Knight, Shift Foreman, Operations

D. McCaskill, Shift Foreman, Operations

  • A. McCauley, Principle Engineer, Onsite Nuclear Safety

R. Moore, Shift Foreman, Operations

  • R. Morgan, Plant General Manager

D. Myers, Shift Foreman, Operations

D. Nelson, Maintenance Supervisor, Mechanical

M. Page, Acting Manager, Technical Support

  • D. Quick, Manager, Maintenance
  • D. Sayre, Senior Specialist, Regulatory Compliance

D. Seagle, Shift Foreman, Operations

  • J. Sheppard, Manager, Operations

R. Smith, Manager, Environmental and Radiation Control

  • R. Steele, Operations Coordinator
  • H. Young, Director, Quality Assurance/Quality Control

Other licensee employees contacted included technicians,

operators,

mechanics, security force members, and office personnel.

  • Attended exit interview on July 20, 1989

Acronyms and initialisms used throughout this report are listed in the

last paragraph of the inspection report.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory requirements.

These activities were confirmed by direct observation, facility tours,

interviews and discussions with licensee personnel

and management,

verification of safety system status, and review of facility records.

To verify equipment operability and compliance with TS,

the inspectors

reviewed shift logs, operations' records, data sheets, instrument traces,

and records of equipment malfunctions.

Through work observations and

2

discussions with Operations Staff members,

the inspectors verified the

staff was knowledgeable of plant conditions, responded properly to alarms,

adhered to procedures and applicable administrative controls, cognizant of

in-process surveillance and maintenance activities, and aware of inoperable

equipment status.

The inspectors performed channel verifications and

reviewed component

status and safety-related parameters to verify

conformance with TS.

Shift changes were routinely observed, verifying

that system status continuity was maintained and that proper control room

staffing existed. Access to the control room was controlled and operations

personnel

carried out their assigned duties in an attentive and

professional manner.

Plant tours -and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment,

and to

verify that radiological, fire protection, physical protection, and

equipment tagging procedures were properly implemented.

No violations or deviations were identified.

3. Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities on

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that precautions and

LCOs were adhered to, the required administrative approvals and tagouts

were obtained prior to test initiation, testing was accomplished by

qualified personnel in accordance with an approved test procedure, test

instrumentation was properly calibrated, and the tests were completed at

the required frequency and conformed to TS requirements.

Upon test

completion, the inspectors verified the recorded test data was complete,

accurate,

and met TS requirements,

test discrepancies were properly

documented and rectified, and that the systems were properly returned to

service. Specifically, the inspectors witnessed/reviewed portions of the

following test activities:

OST-10 (Revision 9)

Power Range Calorimetric During Power

Operation

OST-401 (Revision 22)

Emergency Diesels

OST-402 (Revision 9)

Fuel Oil System Flow Test

No violations or deviations were identified.

4.

Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS,

approved procedures,

and appropriate industry codes

and standards.

The inspectors determined that these activities did not

3

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, material,

testing,

radiological,

and fire prevention controls were adhered to.

In

particular, the inspectors observed/reviewed the following maintenance

activities:

WR/JO 89-AFRK1

A Rod Drive MG Set Repair

WR/JO 89-AEZK1

Replacement of A EDG Injector Nozzles

WR/JO 89-AFDT1

Replacement of A EDG Injector Pumps 6 & 8

WR/JO 89-AFTP1

Replacement of A EDG 6 & 8 Thermocouples

The WR's concerning work performed on A EDG was performed in response to a

high differential temperature (>300'F) between cylinders. As a result, on

May 5, 1989, the injector nozzles were replaced on cylinders 6, 7, 10 and

12. After performance of this work, there was still a high differential

temperature between cylinders 6 and 8.

After consultation with the

vendor, four calibrated injection pumps were replaced (WR

89-AFDT1);

however, this work did not correct the temperature problem. At that time,

maintenance decided to replace the cylinders' thermocouples (WR 89-AFTP1);

however, again this did not correct the problem.

As a result, the vendor

is going to perform special diagnostic work on the EDG,

as well as

supplying new injector pumps to try and determine the root.cause and a

permanent solution to the temperature problem.

This diagnostic testing

and evaluation is scheduled during July 1989.

During witnessing of WR 89-AFDT1,

the inspector identified a problem.

The licensee considers replacement of a EDG injector pump to be a "skill of

the craft" work activity and as such, does not require the work performed

  • to be proceduralized.

According to instructions contained on the WR, the

work was to be performed per the vendor's technical manual.

The

technicians performing the work had neither the WR nor the technical manual

at the job location. This in and of itself is not a problem; however, the

vendor's technical manual contains specific torquing requirements in their

instructions for replacing an injector.

Per Plant Program procedure

PLP-013,

Rev. 3, Maintenance Program, Section 4.0, torquing of components

which have specific torque requirements is not defined as a "skill of the

craft" work activity. Section 5.0 of this procedures states that approved

procedures, instructions, or check Tists be utilized when the activity is

beyond the skill of the craft.

There were no instructions contained in

the WR for specific torquing to be performed, nor were the required torque

values documented.

However,

upon review of the completed WR,

the

inspector saw evidence that the torque requirements may have been met as

evidenced by a completed Torque Wrench Certificate of Calibration for this

work. Additionally, the nozzle replacements performed under WR 89-AEZK1

also had torque requirements that were not documented.

In this instance

however, there was a procedure specified to be utilized which did contain

the required torque values as specified in the technical manual.

This WR

also had a completed Torque Wrench Certificate of Calibration attached,

4

thus providing some assurance the torquing was performed.

As part of the

licensee's Maintenance Procedure Upgrade Program scheduled for completion

at the end of 1990,

these type of discrepancies are expected to be

addressed. The adequacy of the Procedure Upgrade Program and initiation

of new procedures when required is considered an URI:

Ensure Adequacy of

Upgraded Maintenance Procedures, 89-12-01.

No violations or deviations were identified.

5. Onsite Followup of Events (93702)

a.

Error in OT delta T and OP delta T Setpoints

On April 10,

1989,

the licensee determined that the full power

delta T value used in the reactor protection circuitry was different

than the value assumed in certain transient analysis.

This

inconsistency introduced non-conservations in both the OT delta T and

OP delta T protection circuit setpoints as defined in TS 2.3.1.1.2.

Evaluation of the significance of this error indicated that there was

sufficient conservatism in the K1 constant of the OT delta T circuit

to more than compensate. for this error.

Hence, the OT delta T

protective funcation if required would have occurred at or before the

time assumed in the transient analysis. However, this was determined

not to be the case for the OP delta temerpature circuit.

The error

was found to result in a non-conservative OP delta T setpoint which

could exceed the TS value by nearly five percent.

Thus, if required

the OP delta T protective circuit would not have responsed as rapidly

as required by TS to limit certain postulated transients.

However,

this error in OP delta T is deemed to have only minor safety

significance in that the OP delta T function serves only as a backup

function to other protection circuits and a five percent error in the

OP delta T setpoint is not of a sufficient magnitude to constitute a

significant degradation of the function.

The above described event is documented in LER 89-007, issued May 17,

1989.

As discussed in the LER,

the inconsistency existed from

February 25, 1989, beginning of cycle 13, to the time of discovery in

April 1989.

The major contributor appears to be a breakdown in

communications between various organizations responsible for design

controls.

During refueling 13, plant modification 959,

RCS Bypass

RTDs,

was implemented to place the RCS hot and cold leg RTDs in the

main coolant piping. During this process,, the licensee failed to

maintain adequate design control to assure that a parameter utilized

in an analysis and defined in TS 2.3.1.1.2.e was correctly translated

into procedures and instructions. This is a violation of 10 CFR 50

Appendix B Criterion III:

Inadequate Design Controls Results in

Non-conservative Reactor Protection System Setpoint, 89-12-02.

See

paragraph 7 for a second example of a Criterion III violation.

5

These two examples indicate a lack of attention to detail involving a

lack of thorough and effective review process for control of.reactor

protection system setpoints.

During the exit, this item was

discussed with licensee management.

b. Unlatching of a Spent Fuel Assembly

During loading of spent fuel assemblies into the DSC on June 23,

1989,

one of the assemblies (K-18)

became partially unlatched from

the fuel handling tool in similar fashion to the occurrence described

in IR 89-09. The sequence of events occurred as follows:

(1) The spent fuel handling tool was latched on assembly K-18 (which

was the fifth assembly being loaded into the DSC)

and proper

latching was verified by Operations and Engineering personnel.

(2) Operations attempted to insert the assembly into the DSC at

which time the assembly "bumped"

the canister key-way causing

the tool cable to slacken (approximately 6").

Simultaneously,

one of four tool latching fingers became unlatched from the

assembly nozzle.

(3) After discussions between Operations and Engineering, it

was

decided that the logical procession was to attempt to set the

assembly into its respective canister position.

While

0IIIact)

t

howeve durig

t

the

han dlito

re-attempting to load the assembly into the canister, a similar

impact resulted; however, during this impact the handling tool

became completely disengaged from the top nozzle and three of

the four tool fingers latched onto the hold down springs.

(4) The situation was discussed and the decision was made to place

the assembly in the nearest old fuel rack location to take

advantage of the large funnel-shaped lead in provided in the

older fuel racks.

The assembly was successfully placed in this

location.

(5)

The

remaining canister locations were successfully loaded

utilizing a newly refurbished handling tool without encountering

further difficulties.

The fuel handling tool being utilized when the unlatchings occurred is the

same tool that was being utilized during the spent fuel assembly drop of

April 26, 1989. After that event, the licensee performed what they

believed to be adequate corrective action and root cause determination.

There was no failure mechanism determined for the April 1989 event based

on corrective actions and attempted root cause determination; the handling

tool was returned to service. Subsequent to the June events described

above, the tool was removed from service, tagged out, and will be sent to

Westinghouse for complete failure analysis including handling tool

6

dimensional checks.

Follow-up for the earlier April event was identified

in IR 89-09 as IFI 89-09-06. For administrative purposes, this item is

considered closed. The inspectors will monitor the root cause analysis

performed-for both events.

This item is an URI:

Review Root Cause

Analysis Performed on Fuel Handling Tool, 89-12-03.

C.

No Justification Exists for Reliance on Manual Isolation of SW to the

Turbine Building Under Certain Postulated Accident Conditions.

While conducting a review of the SW system,

ONS determined that

certain postulated single failures would result in the failure of the

turbine building SW automatic function during accident situations.

These single failures would also result in only two of the four SW

pumps delivering SW-to both safety and non-safety related components.

Existing analysis assumes that the two SW pumps are providing flow to

only the safety related components,

e.g., the turbine building SW

supply valves are isolated.

However,

the original design of the

plant was for manual isolation of the turbine building SW valves by

operation of the remote control switches on the RTGB.

The automatic

isolation was included within the last five years as an operator aid.

As such, the automatic control circuitry was not designed to function

under all potential single failures.

No documentation has been located which provides the time frame

within which the manual isolation must occur.

Failure to.manually

isolate the SW to the turbine building components could eventually

result in degradation or loss of some safety functions.

Thus the

failure to have the isolation time requirement defined placed the

plant in a potential

unanalyzed condition.

However, existing

emergency procedures do require manual isolation of the turbine

building SW supply isolation valves if low SW header pressure occurs.

These steps are to be performed early on in the procedure.

Based

upon the small chance that an accident will occur with the exact

component failures required to initiate the postulated scenarios, and

engineering judgement that existing procedural requirements are

sufficient compensatory measures if such scenarios were to occur, the

licensee believes operation can safely continue until this issue is

resolved.

The licensee has taken steps to inform operating crews of

this issue.

At the close of the report period, the licensee was

actively pursuing verification via analysis and/or possible testing

of the acceptability of reliance on manual isolation of the SW to the

turbine building. Concurrently the licensee is developing possible

modifications to upgrade the automatic isolation function to preclude

single failures. This issue is considered an URI:

Review Resolution

of Single Failure Impact on SW System Performance, 89-12-04.

No violations or deviations were identified.

7

6. Operator Requalification.Exam Failure Controls

As part of an

NRC

concern regarding licensed operators who fail

requalification exams performing shift duties, the inspectors reviewed and

evaluated the licensee's controls in this area.

Training Instruction,

TI-200, Rev. 24, Robinson Plant Operator Requalification Program, provides

a positive control mechanism for ensuring that an operator who fails a

requalification exam is prevented from performing shift duties.

This

instruction contains a methodology for notifying both the individual and

his/her supervision of the failure, and delineates the requalification and

accelerated testing necessary before the individual may return to shift

duties. Additionally, based on discussions with the licensed training

supervisor, this situation has not occurred at this facility in at least

the past eight years.

Thus, established procedural controls, historical

data, and the licensee's sensitivity in this area are considered adequate

to preclude this situation from occurring at HBR.

7. Action on Previous Inspection Findings (92701)

(Closed)

URI 261/88-03-01,

Review OT Delta T Safety Analysis Results.

This item, discussed in IR 88-03, involves discovery that an incorrect

loop transport time had been used in determination of the OT Delta T trip

setpoint.

This item was reported to the NRC by LER 88-002, issued

February 19,

1988,

and by supplement number 01 issued June 6, 1988.

At

the time of discovery, the licensee took immediate action to compensate

for the error by adjusting the K1 constant of the OT Delta T trip setpoint

to 1.09, a more conservative value than the 1.1565 value specified in TS 2.3.1.1.2.d. The LER supplement reported that the TS value of 1.1565 in

the OT delta T trip equation could not have maintained the MDNBR above the

licensed limit of 1.17 during a control rod drop transient initiated from

full power.

The calculated MDNBR for the rod drop transient was

determined to be 1.065.

This value is approximately 10 percent below the

desired 1.17 value.

However, during discussions with cognizant NRC staff

in both Region II

and NRR,

it

was determined that the reduction in

confidence level for prevention of fuel damage during the rod drop

transient had not been significantly affected.

During the evaluation of the safety significance of the incorrect transient

analysis, the contractor performing the evaluation for the licensee failed

to adjust all the parameters necessary to perform the analysis for the rod

drop transient.

This resulted in the licensee verbally -informing the NRC

that the analysis had demonstrated tht the MDNBR for the rod drop

transient had been greater than 1.17 for the incorrect loop transport

time. Subsequent reviews revealed the error and the NRC was notifed as

required. This recent breakdown in control of transient analysis as well

as the problem which initiated the event in 1975 constitute a violation of

NRC requirements. Specifically, these items contributed to the nonconser

vative OT delta T setpoints from 1975 until December 1988 and is the second

8

example of violation 89-12-02 associated with failure to establish

adequate design controls per 10 CFR 50 Appendix B, Criterion III as

discussed in paragraph 5.

With the issuance of the Notice of Violation,

URI 261/88-03-01,

LER 88-002 and supplement LER 88-002-01 are considered

closed.

8.

Exit Interview (30703)

The inspection scope and findings were summarized on July 20, 1989, with

those persons indicated in paragraph 1.

The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. Dissenting comments were not received from the

licensee. Proprietary information is not contained in this report.

Item Number

Description/Reference Paragraph

89-12-01

URI -

Ensure Adequacy of Upgraded Maintenance

Procedures, paragraph 4,

89-12-02

VIO -

Inadequate Design Controls Results in

Non-Conservative Reactor Protection System Setpoints,

paragraphs 5.a and 7.

89-12-03

URI - Review Root Cause Analysis Performed on Fuel

Fuel Handling Tool, paragraph 5.b.

89-12-04

URI - Review Resolution of Single Failure Impact on

SW System Performance, paragraph 5.c.

10. Acronyms and Initialisms

CFR

Code of Federal Regulations

DSC

Dedicated Shielded Canister

EDG

Emergency Diesel Generator

GL

Generic Letter

HBR

H. B. Robinson

IFI

Inspector Followup Item

IR

Inspection Report

LCO

Limiting Condition for Operation

LER

Licensee Event Report

MG

Motor Generator

MDNBR

Minimum Departure from Nucleate-Boiling Ratio

MWt

Megawatts Thermal

NRC

Nuclear Regulatory Commission

NRR

Nuclear Reactor Regulation

ONS

Onsite Nuclear Safety

OST

Operations Surveillance Test

OP delta T

Overpower Delta Temperature

OT delta T

Overtemperature Delta Temperature

9

REV

Revision

RCS

Reactor Coolant System

RTD

Resistant Temperature Detector

RTGB

Reactor Turbine Gauge Board

SW

Service Water

T

Temperature

TI

Training Instruction

TS

Technical Specification

URI

Unresolved Item*

W/R

Work Request

WR/JO

Work Request/Job Order

  • Unresolved items are matters about which more information is required to

determine whether they are acceptable or may involve violations or deviations.