ML13329A226

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Insp Repts 50-206/92-34,50-361/92-34 & 50-362/92-34 on 921201-930108.Violations Noted.Major Areas Inspected: Operational Safety Verification,Radiological Protection, Security & Evaluation of Plant Trips & Events
ML13329A226
Person / Time
Site: San Onofre  
Issue date: 01/26/1993
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13329A224 List:
References
50-206-92-34, 50-361-92-34, 50-362-92-34, NUDOCS 9302180068
Download: ML13329A226 (9)


See also: IR 05000206/1992034

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos.

50-206/92-34, 50-361/92-34, 50-362/92-34

Docket Nos.

50-206, 50-361, 50-362

License Nos.

DPR-13, NPF-10, NPF-15

Licensee:

Southern California Edison Company

Irvine Operations Center

23 Parker Street

Irvine, California

92718

Facility Name:

San Onofre Units 1, 2 and 3

Inspection at:

San Onofre, San Clemente, California

Inspection conducted: December 1, 1992 through January 8, 1993

Inspectors:

C. W. Caldwell, Senior Resident Inspector

D. L. Solorio, Resident Inspector

Approved By:

_________A

_____

/ A?

/ 3

sJ -1

'H. J. Wong, Chief

Date Signed

Reattor ProjectsSection II

Inspection Summary

Inspection on December 1. 1992 through January 8. 1993 (Report Nos.

50-206/92-34, 50-361/92-34, 50-362/92-34)

Areas Inspected:

Routine resident inspection of Units 1, 2 and 3 Operations

Program including the following areas:

operational safety verification,

radiological protection, security, evaluation of plant trips and events,

monthly surveillance activities, monthly maintenance activities, and

independent inspection.

Inspection procedures 61726, 62703, 71707, and 93702

were covered.

Safety Issues Management System (SIMS) Items:

None

Results:

General Conclusions and Specific Findings:

Weaknesses

Several weaknesses were noted in the performance of maintenance and

testing activities. In particular, the inspector noted that Station

Technical personnel (performing an inservice test) did not fully

93021830068 930126

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understand the intent of Radiation Exposure Permit requirements. As a

result, they entered a contaminated area without the requisite protective

clothing specified in the Radiation Exposure Permit (Paragraph 5.a).

The

inspector also noted that-Maintenance craft personnel did not properly

restore a battery charger to its original configuration after testing.

In addition, both their supervisor and a QC inspector (tasked with

oversight of the work activity) did not note the discrepancy (Paragraph

6.a).

Significant Safety Matters:

Summary of Violations:

One violation was identified during this inspection period which involved

the failure by station technical personnel to follow Radiation Exposure

Permit requirements (Paragraph 5.a).

In addition, one non-cited

violation involving failure to follow procedure during restoration from a

battery charger test in Unit 1 was identified (Paragraph 6.a).

Open Items Summary:

During this report period, two new followup items were opened and none

were closed.

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DETAILS

1. Persons Contacted

Southern California Edison Company

H. Ray, Senior Vice President, Nuclear

  • H. Morgan, Vice President and Site Manager
  • R. Krieger, Station Manager

3. Reilly, Manager, Nuclear Engineering & Construction

B. Katz, Manager, Nuclear Oversight

  • R. Rosenblum, Manager, Nuclear Regulatory Affairs

K. Slagle, Deputy Station Manager

R. Waldo, Operations Manager

  • L. Cash, Maintenance Manager
  • D. Breig, Manager, Station Technical
  • M. Short, Manager, Site Technical Services

M. Wharton, Manager, Nuclear Design Engineering

P. Knapp, Manager, Health Physics

  • J. Fee, Assistant Manager, Health Physics

W. Zintl, Manager, Emergency Preparedness

0. Herbst, Manager, Quality Assurance

  • C. Brandt, Quality Assurance

C. Chiu, Manager, Quality Engineering

3. Schramm, Plant Superintendent, Unit 1

  • V. Fisher, Plant Superintendent, Units 2/3

G. Hammond, Supervisor, Onsite Nuclear Licensing

  • J. Jamerson, Lead Engineer, Onsite Nuclear Licensing
  • D. Axline, Engineer, Onsite Nuclear Licensing
  • D. Wilcockson, Onsite Nuclear Licensing

3. Reeder, Manager, Nuclear Training

H. Newton, Manager, Site Support Services

  • R. Neal, Supervising Engineer, Station Technical
  • A. Thiel, Manager, Electrical Systems Engineering, Station Technical
  • W. Frick, Assessment Supervisor, Nuclear Oversight
  • B. Carlisle, Manager, Electrical, Nuclear Engineering
  • M. Herschthal, Manager, Nuclear Systems Engineering, Station Technical
  • Denotes those attending the exit meeting on January 11, 1993.

The inspectors also contacted other licensee employees during the course

of the inspection, including operations shift superintendents, control

room supervisors, control room operators, QA and QC engineers, compliance

engineers, maintenance craftsmen, and health physics engineers and

technicians.

2. Plant Status

Unit 1

Unit 1 was permanently shutdown on November 30, 1992.

0

0

Unit 2

The Unit operated at power during the period.

Unit 3

The Unit operated at power during the period.

3. Operational Safety Verification (71707)

The inspectors performed several plant tours and verified the operability

of selected emergency systems, reviewed the tag out log and verified

proper return to service of affected components.

Particular attention

was given to housekeeping, examination for potential fire hazards, fluid

leaks, excessive vibration, and verification that maintenance requests

had been initiated for equipment in need of maintenance. The inspectors

also observed selected activities by licensee radiological protection and

security personnel to confirm proper implementation of and conformance

with facility policies and procedures in these areas. Several minor

discrepancies were identified and discussed with the shift supervisor for

resolution.

No violations or deviations were identified.

4.

Evaluation of Plant Trips and Events (93702)

Prompt Onsite Response To Events At Operating Power Reactors (93702)

In early December 1992, operators requested that management evaluate the

need for monitoring station service transformer (SST) voltages for the

No. 1, 2 and 4 transformers (there are a total of four transformers) in

Unit 1. The system design engineer was consulted and determined that

480V SST No. 3 had operated with the transformer tap settings configured

for Modes 5 and 6 operation since May 1991. Unit 1 restarted from a

steam generator repair outage in May 1991, without reconfiguring the SST

tap settings for Mode 1 through 4 operation and operated that way until

the shutdown on November 30, 1992.

On December 28, 1992, the system design engineer initiated nonconformance

report (NCR) number 92120064 to document the discrepancy associated with

SST No. 3. Operability of the transformer in Modes 1 through 4 will be

addressed by a Nuclear Engineering Design Organization (NEDO)

analysis

which is scheduled for completion in late January or early February 1993.

The inspector considered that since Unit 1 was permanently shutdown on

November 30, 1992, there was no immediate safety concern. However, since

SST No. 3 tap settings were configured for Modes 5 and 6 during plant

operation, the inspector will review the evaluation when available to

determine if there were any operability concerns when Unit 1 was in Modes

1 through 4 as inspector followup item (50-206/92-34-01).

No violations or deviations were identified.

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5. Bi-Monthly Surveillance Activities (61726)

During this report period, the inspectors observed or conducted

inspection of the following surveillance activities:

a. Observation of Routine Surveillance Activities (Unit 2)

S023-V-3.5.4, "Inservice Testing of Check Valves (Quarterly

Frequency) - Attachment 3, High Pressure Safety

Injection Check Valves"

S023-V-3.4.8, "Saltwater Cooling Inservice Pump Test - 2MP113"

S023-V-3.4.4, "High Pressure Safety Injection Inservice Pump Test

Attachment 1, 2P017"

On December 17, 1992, the inspector observed performance of a

quarterly inservice test (IST) on Unit 2 high pressure safety

injection (HPSI) pump P017 as prescribed in procedure S023-V-3.4.4.

The inspector noted that the engineer and his supervisor crossed

radiological boundaries by reaching into and touching objects within

a contaminated area. However, they were not wearing the required

protective clothing (coveralls, cloth hood, rubber gloves, or

cordero covers) specified by applicable Radiation Exposure Permit

(REP).

Station procedure S0123-VII-9.9, TCN 11-3, "Radiation Exposure

Permit Program," states, in part, that all personnel covered by the

REP shall follow the requirements specified in the REP.

REP-00700,

Revision 16, "Visual Inspection; All Areas Except Containments,"

used by the engineer and the supervisor required that the following

protective clothing be worn for entry into contaminated areas:

coveralls, cloth hood, rubber gloves, and cordero covers. However,

the inspector observed the system engineer reach into a contaminated

area to place a vibration monitoring probe on the pump housing to

take IST vibration data, without wearing the requisite protective

clothing specified in the REP. The inspector also observed the

engineer's supervisor reach into the contaminated area and touch

scaffolding without wearing the requisite protective clothing

specified in the REP.

Failure to adhere to REP requirements is an

apparent violation (50-361/92-34-02).

The inspector noted that the engineer and the supervisor did not

recognize that their performance was in violation of their REP

requirements until Health Physics (HP) management contacted them

subsequent to discussions with the inspector. The inspector was

concerned with the supervisor's performance since his actions could

be interpreted by subordinates (i.e., the system engineer) as

condoning noncompliance with an REP.

In addition, discussions with

several past and present system engineers indicated that reaching in

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without protective clothing was a customary practice (while

performing ISTs) if the pump was in a contaminated area.

On December 17, 1992, HP management initiated two Radiological

Observation Reports (RORs) to document the inspector's observations

in accordance with S0123-VII-9.3, TCN 5-3, "Reporting Radiological

Incidents."

The purpose of the RORs was, in part, to identify

potential and actual radiological incidents and establish a method

to implement corrective actions to prevent recurrence. Copies of

these reports were sent to the appropriate supervision for the

system engineer and the supervisor, requesting response to HP with

corrective actions to prevent recurrence. The inspector reviewed

the ROR responses and considered them acceptable.

Subsequent to discussions with the inspector, in an effort to

preclude further violations of REPs, HP implemented the following

interim actions:

-

ISTs of pumps in contaminated areas were coordinated with

system engineers to facilitate entrance into contaminated

areas. In the case of the HPSI pumps, the contaminated areas

are normally too small to allow individuals to stand inside

them and perform the IST. As a result, HP will expand the

boundary to allow the engineer enough room to work within the

contaminated area.

  • -

Selected ISTs will be monitored to verify system engineer

performance and adherence to REP requirements.

In an effort to preclude further violations of REPs, Station

Technical (STEC) has taken the following interim actions:

-

A memorandum was routed to system engineers to assure they

understand the REP requirements for jobs they perform and that

REP 00700 does not allow reaching into contaminated areas.

-

Engineering supervisors were instructed to observe engineers

and provide coaching on good work practices during their weekly

management monitoring of the engineers.

-

A Technical Division Investigation Report was initiated to

identify root causes for the observed deficiencies.

Long term corrective actions proposed (scheduled to be implemented

late January or early February, 1993) included a coordinated effort

between HP and STEC to develop an REP that will allow system

engineers to reach into contaminated areas for the performance of

pump IST monitoring.

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b. Observation of Routine Surveillance Activities (Unit 3)

S023-3-3.5,

"CEA (Control Element Assembly) Monthly Operability

Test."

S023-3-3.17,

"Main Steam Isolation Valve Operability Test."

Within this area inspected, one violation was identified.

6. Monthly Maintenance Activities (62703)

During this report period, the inspectors observed or conducted

inspection of the following maintenance activities:

a.

Observation of Routine Maintenance Activities (Unit 1)

M092121891000,

"Need To Adjust Station Service Transformer #2 Tap

Setting To Tap #2 to Lower 480V Bus Volts Per S01-9-3

If Outage Exceeds 7 Days."

M092041671000, "Charger Capacity Test."

On December 1, 1992, a capacity test was performed on Unit 1 battery

charger 'A' in accordance with maintenance order (MO) 92041671000

and procedure S0123-1-2.5, "Battery Service and Charger

Surveillance." During preparation for the test, electricians lifted

two of the four cables (one positive and one negative) and

documented that activity on a lifted lead form. However, during

restoration from the test, a different crew of electricians did not

properly reterminate the cables to the original configuration.

As a

result, the charger was inoperable until the next day when it was

realized that it had been improperly configured. This was

complicated by the fact that for a period of time, the redundant

charger, 'B', was inoperable since it had been cleared for

maintenance.

The improper termination by the electricians was due to their

misinterpretation of the lifted lead form (LLF), and failure to

follow procedure. Step 6.6.6.1 of procedure S0123-I-2.5 required

the electrician to lift two of four leads from the charger to allow

room to connect the load bank for testing the charger capacity.

This was done and documented on the LLF. The two lifted leads were

pulled out of the cabinet in such a manner that they were not

visible from the front of the cabinet. When the test was completed,

a second electrical crew did not see the two lifted leads that had

been pulled out of the cabinet. They reviewed the LLF and assumed

that the remaining two connected leads were the leads recorded on

the LLF, and moved them to different terminal posts within the

charger cabinet. Step 6.7.16.1 of S0123-I-2.5 required the

electricians to return the battery charger to the pretest

configuration in accordance with step 6.6.6.1; but, the

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electricians, and their supervisor, failed to follow this step in

the procedure. Additionally, a quality control inspector observing

the work failed to assure proper restoration of the circuits.

In response to this problem, the licensee performed several actions.

The first was to perform a calculation to determine the significance

of operating the charger with two of the four cables connected. The

calculation, A-92-E-003, revealed that current carrying capacity of

the two cables during design basis accident conditions was

sufficient to ensure that some margin remained. As a result of this

effort, the licensee concluded that the safety significance of the

problem was minimal.

The second action was performance of an assessment to determine the

root cause and corrective actions for the event. Maintenance

Division Experience Report 92-008 documented the results of the

licensee's assessment. The licensee determined that the personnel

involved erroneously "locked-on" to what they believed was a

plausible set of circumstances in setting up for the test. Thus,

they did not properly consider the information provided in the

lifted lead form. In addition, the QC inspector did not ensure

verbatim compliance with the maintenance procedure.

For corrective action, the licensee properly restored the charger

cables. In addition, proposed actions for Electrical Maintenance

personnel included review of the incident with all electricians, a

review to ensure adequate implementation of the Maintenance

Stop/Self Checking program, and a review of the event for

disciplinary action. Corrective actions proposed for QC personnel

included training on work package familiarization, inspector

responsibilities, and inspector observation on the job.

Step 6.7.16 to procedure 50123-1-2.5 required that the battery

charger be returned to its original pretest configuration. Step

6.7.18 required that a second qualified person verify that all

cables have been properly terminated. In addition, step 5 of

M092041671 required that QC witness the completion of work to return

the charger to its original configuration.

Failure of the Electrical Maintenance personnel to follow the

requirements of procedure S0123-I-2.5 and of the QC inspector to

follow the requirements of M092041671 is a violation. However, the

issue was licensee identified, was determined to be of low

significance, and corrective actions (proposed and implemented)

appear adequate to minimize the potential for further occurrences.

As a result, this issue is not being cited since the criteria

specified in Section VII.B of the Enforcement Policy were satisfied

(50-206/92-34-03).

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C.,

Observation of Routine Maintenance Activities (Unit 3)

CM92121389000, "Corrective Maintenance - A Fine Crack Has Been

Discovered between Cell 5 (-) and 6 (+) As Documented

On -QA (Quality Assurance) Report 2E-023092. Jumper

Out Cell 6 (Cell 5 Is Presently Jumpered Out) And

Jumper In Spare Cell 62."

M091062381000, "Pressurizer Heater Bank 3E128 Feeder Breaker Control

Check and Relaying Preventive Maintenance."

M092080695000, "Connect Spare Battery Charger to Battery 3D2"

CM92090262000, "Corrective Maintenance - PSV8155 (Unit 3 High

Pressure Safety Injection pump P017 inlet relief

valve) Is Leaking By At A Rate of Approximately 10

Drops Per Minute."

The inspector reviewed test procedure, S023-I-8.88, TCN 1-12,

"Valves-Cold Bench Testing & Calibration of SR & NSR (Safety Related

and Non-Safety Related)," associated with testing of relief valve

PSV8155. During the review, the inspector noted that the wrong lift

pressure acceptance criteria had been written in the procedure. The

inspector pointed out this deficiency to the maintenance craftsmen

who subsequently corrected it.

Followup discussion with maintenance craft and supervision

responsible for documentation of the acceptance criteria determined

that the craft supervisor had simply written in the wrong number in

the procedure. Both the maintenance craftsmen and the supervisor

indicated that they understood the purpose of 'specifying a range for

valve lift pressure in accordance with procedures. The inspector

considered their explanation acceptable and considered that no

further followup action was necessary.

Within this area inspected, one non-cited violation was identified.

7. Exit Meeting

On January 11, 1993, an exit meeting was conducted with the licensee

representatives identified in Paragraph 1. The inspectors summarized the

inspection scope and findings as described in the Results section of this

report.

The licensee acknowledged the inspection findings and noted that

appropriate corrective actions would be implemented where warranted. The

licensee did not identify as proprietary any of the information provided

to or reviewed by the inspectors during this inspection.

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