ML13323A893

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IE Insp Rept 50-206/80-31 on 800929-1031.No Noncompliance Noted.Major Areas Inspected:Plant Operations & Maint, Followup on Response to IE Bulletins & Significant Events
ML13323A893
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 11/26/1980
From: Faulkenberry B, Miller L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13323A892 List:
References
50-206-80-31, NUDOCS 8101210608
Download: ML13323A893 (12)


See also: IR 05000206/1980031

Text

U. S. NUCLEAR REGULATORY COMMISSION

OFFICE OF INSPECTION AND ENFORCEMENT

REGION V

Report No.

50-206/80-31

Docket No.

50-206

License No.

DPR-13

Safeguards Group

Licensee:

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, California 91770

Facility Name:

San Onofre Nuclear Generating Station Unit 1

Inspection at:

San Onofre,

California

Inspection conducted:

September 29 - October 31,

1980

Inspectors:

J).ii2

I/'_<__-_/

L. Miller, Resident In.s.pecto!S

Date Signed

Date Signed

Date Signed

Approved By:

E

/C/-4 /V

B. H. Faulkenberry, Chief, Re cstor Projects Section 2,

Date.Signed

Reactor Operations ad Nucle6'rSupport Branch

Summnary:

Inspection on September 29-October 31, 1980 (Report No. 50-206/80-31)

Areas Inspected:

Routine, resident inspection of plant operations during

long term outage, monthly maintenance and surveillance observations,

follow-up on enforcement items, follow-up on licensee responses to

IE Bulletins, TMI Short Term Lessons Learned verification (Temporary

Instructions 2515/42, 43 and 44), and follow-up on a significant event

(loss of foreing material control inside reactor coolant system).

This

inspection involved 70 inspector-hours onsite by the resident inspector.

Results: No items of noncompliance or deviation were identified.

RV Form 219 (2)

810121-0-'-.."

0 ;

DETAILS

1. Persons Contacted

  • J. Haynes, Manager, Nuclear Operations
  • D. Nunn, Manager, Quality Assurance
  • J. Curran, Plant Manager
  • R. Brunet, Superintendent, Unit 1

M. Wharton, Supervising Engineer, Unit 1

  • D. Dunn, Project Quality Assurance Supervisor
  • J. Tate, Supervisor of Plant Operations
  • G. McDonald, Unit 1 Quality Assurance Supervisor

The inspector also interviewed other licensee employees on the maintenance

and operations staffs during this inspection.

  • Denotes those attending the Exit Interview on October 31, 1980.

2. Inspection of Plant Operations During Long-Term Outage

The inspector observed control room operations for proper shift manning,

for adherence to procedures and limiting conditions for operation, and

for appropriate recorder and instrument indications. Thelinspector

reviewed logs and operating records regularly, and verified that the

radiation controlled.area access points were safe and clean.

The inspector noted that records of surveillance tests required during

the shutdown had been completed, and that the physical security plan

appeared to be properly implemented. Frequent discussions with control

room operators were held by the inspector to discuss their understanding

of the reasons for existing indications and plant conditions. The inspector

frequently toured throughout the facility. The licensee's fire protection

plan appeared to be properly implemented, and the cleanliness of the

facility was adequate.

The inspector reviewed the Temporary Modifications Log (lifted leads

and jumpers) and the active "Clearances."

Selected "Clearance" tags

were verified to be in place as indicated by the records.

The inspector walked down portions of the auxiliary feedwater and chemical

and volume control system to verify they were correctly lined up for

the existing plant status.

Five RWP's were reviewed for proper completion

and five radiation monitoring instruments were checked for operability,

and calibration.

No items of noncompliance or deviations were identified.

3. Month j Surveillance Observations

The Inspector observed licensee personnel measure boron concentrations

perform Portable radiai on detector calibrations, perform area radiation

monitoring system checks$ and perform radiationsuvy.

Srelac

activity was'relatively low.

The activties obusrveys. Surveilance

in accordance with the appropriate procedures st

ngd

were performed

Operation were met where applicable. Logs and records were kept, and

wiere reviewed independently 1where required. The licensee's records

indicate that all surveillances require .

to be cd

ths

period were completed.

Compcetee riecohs

No items of noncompliance or deviations were dentifi

4.

Mot hllalntenance O bservations

a. Routine

Activities

The inspector observed portions of the following maintenance

The inspector determined that these activites did n

oi-t

n conitons

ei

u

d

eioat

The in co

i

for oeration that required administrative

approvals and layouts were obtained Priortoitain thwrk

thaTueet

ofprevceee-at

ntiaing

e oe

that apoed pocedures were being used by qualified Personnel,

prevlcent

Panrsanmteas used were certified, and that fire

rapventior o

ws

more appropriate for the activities.nto

b.

Steam

G

enerator

Re

se acoca1T

Durng hisinspection period, the licensee completed the water

and magnetite grit mixture decontamination of the "Bit and "A" steam

generators and commenced decontamination of the 1'1 steam generator.

In addition the licensee began to in v dul y h e t e s rf c

cindivduaol

honer

them

surfacB"

c o r r s i

o l a e

r f o m a

c h "

B

" s t e a

m g e n e r

a t

o r t u

b e w h i

c h w a s p l a n

n e d

to be sleeved

By the end of this period approximately 1500of th

2500 tubes to be sleeved In the

IB stateea

0 a en

he

The 'Inspector reviewed the licensee's actions taken in-response

to the dilution event of September 21, 1980. These actions were

to revise the 10 CFR 50.59 analysistofrhrdsus

hemars

to e t

ken to

emo e g it rom the reactor coo ant sy stem , to

1nstall a newer type of Inflatable seal which'was designed to-reduce

the likelihood of seal rupture, and to revise the decontami nat ion

procedure to require more frequent monitoring of the system for

rapid inventory losses which might indicate seal .failure.

The

inspector confirmed these actions.

(Item 50-206/80..28-01 Closed).

-3

On October 20, 1980, the inspector reviewed the records of the

decanting of the decontamination waste storage tank performed on

October 19.

This decanting was performed using a temporary hose.

from the decontamination waste storage tank through a filter to

the containment sump, and thence immediately to the west holdup

tank. Licensee samples of the water for radioactivity indicated

the presence of alpha radioactivity.

A licensee representative

stated that these samples would be analyzed offsite using alpha

spectometry to quantify the radioactivity in the samples.

(01

50-206/80-31-02).

On October 22, 1980, licensee personnel informed the inspector

that the decontamination spray arm had fallen off while it was

being used to decontaminate the "A"

steam generator hot leg channel

head, for an unknown period of up to 38 minutes.

While the explanation

and analysis of this event was still being developed by the licensee,

the arm again fell off on October 24; this time for up to sixty

minutes. The arm is in three segments, each connected by a sliding

dovetail joint, with each joint locked by a hand-tightened bolt.

The licensee concluded that due to insufficient care by one operator,

two of these segments had been misassembled on October 22. After

the separation at one joint on that date, the arm had been inspected

  • for

proper assembly, but the inspection had failed to detect the

improper assembly at a second joint, according to a contractor

representative. The contractor conducted immediate.retraining

of all operators who were required to assemble this equipment.

A licensee representative stated that an inspection of the "A"

hot lei channel head would be performed prior to steam generator

closure and appropriate corrective action developed.

The inspector

interviewed the licensee and contractor supervisory personnel,

inspected the equipment to evaluate the licensee's explanation,

and stated that the actions taken appeared adequate to prevent

recurrence. The inspector also stated that the licensee should

report the results of the steam generator inspection once it was

performed.

(01 50-206/80-31-03).

No items of noncompliance or deviations were identified.

5. Followup on Sionificant Event (Loss of Foreign Material Control Inside

the Reactor Coolant System)

On October 10, 1980, the licensee informed the inspector that several

pieces of debris were unaccounted for in the "A" hot leg of the reactor

coolant system. In addition, on October 14, 1980, the Plant Manager

provided the inspector with a list of 12 additional items which had

been recovered from that leg after the initial report on October 10.

Also, he informed the inspector that a metal cover plate for the "A"

steam generator cold leg loop seal had been inadvertently dropped into

the "A" cold leg and could not be immediately recovered.

Prompt discussions between licensee representatives and the NRC were

conducted. These discussions resulted in the Immediate Action Letter

dated October 15, 1980. This letter confirmed that the licensee would

halt all steam generator work until it had revised its written procedures

to incorporate stricter tool control, foreign material exclusion and

steam generator channel head debris inspection requirements. The inspector

subsequently verified that these procedural requirements had beer incorporated

by the licensee.

In addition, the letter confirmed that prior to the resumption of power

operations, the licensee would submit to the Regional Office of Inspection

and Enforcement a written report on the deleterious effects, if any, of

any unrecovered foreign material in the reactor coolant system. This

report, of necessity, must evaluate what amount of foreign material might

not be recovered due to size, location and other considerations (01

50-206/80-31-01).

No items of noncompliance or deviations were identified.

6. Followup on Items of Noncompliance

A.

(Closed) Deficiency (79-12-01)

The inspector reviewed the licensee's response and verfied by review

of the revised procedure, S-A-112, "Station Quality Assurance Program",

that the list of safety-related equipment had been corrected. This

item is C1ose.

B. (Closed) Infraction (79-12-02)

The inspector reviewed the licensee's procedure, S01-II-1.9, "Control,

Calibration, and Maintenance of Measuring and Test Equipment" and

verified that the procedure now included a reference to the four

Roylyn pressure gauges which had cited as not being calibrated

on time.

C. (Closed) Infraction (80-09-01)

Time constraints during which required actions must be taken had

been incorporated into all emergency operating instructions. The

inspector reviewed-a portion of these instructions and stated the

licensee's actions appeared adequate. This item is closed.

D. (Closed) Infraction (80-09-02)

The inspector verified that the licensee s emergency operating

instructions had been reviewed and revised. This completes the

required corrective action for this item.

E.

(Closed) Infraction (80-12-01)

The inspector reviewed the licensee's response and discussed it

with licensee personnel. The inspector verified that the required

data had been subsequently recorded. The inspector stated that

licensee's discussion of the mandatory nature of procedures with

the instrument technicians appeared adequate. This item is closed.

F. (Closed) Deficiency (80-12-02)

The inspector reviewed the licensee's corrective action and measures

to prevent recurrence, and stated that the discussion of the importance

of following procedures with the instrument technicians appeared

to be sufficient. This item is closed.

G. (Closed) Deficiency (80-16-01)

The inspector verified that the licensee had revised its procedures

S01-3-1.3, "Determination of Just Critical Rod Position and Reactor

Shutdown Margin" and the associated calculation form.

The inspector

stated that .the revised form and procedure appeared adequate to

ensure accurate calculation of shutdown margin in the future.

This item is closed.

H. (Oen) PAT Notices of Violation (80-19-02)

(1) The inspector reviewed the licensee amended schedule and progress

report for the revision of all procedures to incorporate requirements

of ANSI N18.7-1976.

The inspector stated that the stretchout

of the schedule was acceptable provided that other commitments

made by the licensee in regard to maintenance personnel retraining

and establishment of a preventive maintenance program were not

also delayed by the proposed postponement of the development

of new maintenance procedures until August 1, 1981. A licensee

representative stated that no modifications of those commitments

was intended.

(2) The inspector reviewed the revised S01-I-1.14 - "General Maintenance

Procedure" and verified that it established requirements for

maintenance schedules and periodic replacement of safety-related

parts with a service life.

(3) The inspector stated that the licensee's commitment to establish

a maintenance retraining program (due November 30, 1980) and

to develop a procedure for fire hose inspections remained

open on this item and would be inspected later.

-6

I. (Closed) Infraction (80-21-01)

The inspector reviewed the licensee's response and verified that

the licensee had established manned control points to prevent future

unauthorized entry with improper clothing or monitoring devices.

This item is closed.

J. (Closed) Deficiency (80-21-02)

The inspector reviewed the licensee's response and verified that

protective clothing requirements for steam generator platform work

appeared to be uniformly applied. This item is closed.

K. (Closed) Infraction (80-21-03)

The inspector reviewed the licensee's response and corrective action

and stated that they appeared adequate. This item is closed.

No items of noncompliance or deviations were identified.

7. Followup On Licensee Responses to IE Bulletins (IEB's)

A. IEB 78-12, 12A (Closed)

The inspector reviewed the licensee's statement in their July 13,

1979 letter (Head to Engelken). According to a licensee representative,

this letter stated that weld material records for the reactor pressure

vessel had not been maintained, but that the vessel had been built

to code. This item is closed.

B.

TEB 79-14 (Open)

The inspector reviewed the current status of the licensee's final

report on this Bulletin with a licensee representative. The representative

stated that the report was not yet available.

C. IEB 79-17 (Closed)

The inspector reviewed the licensee's report: "A Review of Stress

Corrosion .Cracking at San Onofre Unit 1" (Bechtel -

14000-027 dated

February, 1980).

This report reviewed the history of austenitic

stainless steel corrosion at San Onofre.Unit 1 and made three

recommendations:

1. Replace all TP 304 pipe and fittings with TP304L.

2. Provide a protective coating for systems directly or indirectly

exposed to the seacoast environment..

3. Replace the stainless steel braided electrical tracing with

Chemelex 20 PVT-Trace, a fluoropolymer-covered electrical tracing.

-7

Licensee personnel stated that the third recommendation had been

accomplished, and that the first two recommendations would be seriously

considered for long-range corrective action. The inspector stated

that this Bulletin would be closed, but that the contractor's report

would be forwarded for further review by NRC, and the licensee's

progress in accomplishing these recommendations would be monitored.

(01 50-206/80-31-04).

D..

IEB 79-18 (Open)

The inspector determined that the licensee had not yet completed

the installation and checkout of the modified announcing system.

E. IEB 79-23 (0oen)

A licensee representative stated that the test report on the diesel

generator was not yet available for inspection. The inspector

stated that the report would be reviewed when it became available.

F..

IEB 79-25 (Oen)

A licensee representative stated that the test results on overtravel

measurements were not available due to the temporary absence of

personnel familiar with their location. The inspector stated that

the results would be reviewed upon the return of the knowledgeable

parson.

G.

IEB 79-27 (Closed)

The inspector confirmed with a licensee representative that an

emergency procedure for loss of electrical power to the 125 vdc

buses would be prepared sufficiently prior to the unit's return

to power for the Resident Inspector to review and comment on.

(01 50-206/80-31-05). This item is closed.

No items of noncompliance or deviations were identified.

8. Inspection of TMI Task Action Plan Category "A" Requirements

The inspector confirmed that the licensee had completed several TMI

"Lessons Learned" actions, or had initiated action to complete them,

as noted below by the reference to the NRC Action Plan (NUREG 660) item

number:

a.

Task Action Plan (TAP) 1.A.1.1

The inspector verified through discussions with licensee personnel

and review of Operating Instruction S-0-6, "Duties and Responsibilities

and Authority of the Shift Technical Advisor" that the licensee had

stationed interim Shift Technical Advisors as required.

-8

b.

TAP 1.A.1.2

The inspector reviewed Operating Instruction S-0-4, "Watch Engineer's

Authority, Responsibilities and Duties," and a memo from Vice President

for Nuclear Engineering and Operations, R. Dietch, dated January 2,

1980 to verify that the Watch Engineer's duties had been described

as required by this item.

c. TAP 1.C.3

The inspector reviewed Operating Instruction S-0-100, "Station

Operations" and verified that the definition of authority required

had been made by the licensee. He further verified that the Watch

Engineer training program emphasized the safety responsibility

of the Watch Engineer.

d. TAP 1.C.4

The inspector reviewed S-0-100, "Station Operations" and S-A-103,

"Control Room Access," and determined that these procedures made

adequate provisions for controlling control room access.

e. TAP II.D.3

The inspector verified that positive indications of valve position

for the pressurizer power operated relief valves had been installed.

The inspector also reviewed the preoperational test results for this

system. The inspector stated that the licensee's actions adequately

addressed this item.

f. TAP II.E.1.2

The inspector interviewed a licensee representative responsible

for this item who stated that the licensee had agreed with NRR

to implement all seven required criteria in its automatic feedwater

system by January 1, 1981. This system is to be "safety grade."

The representative further stated that this commitment was contingent

upon regional power availability and the availability of required

materials. The inspector determined by observation that the licensee's

present auxiliary feedwater system has been modified by the installation

of a remote manual (from the control room) discharge valve for the

electric-driven auxiliary feedwater pump. The inspector further

noted that a letter from NRR dated December 21, 1979 required that

the licensee not automate the auxiliary feedwater system until

NRR had reviewed and approved the licensee's steam line break and

feedwater break analyses. The licensee representative stated that

these analyses would be submitted to NRR by December 1, 1980. On

the basis of these facts the inspector stated that the licensee's.

actions were acceptable.

-9

g.

TAP II.

E. 3.1

The inspector reviewed the licensee's pressurizer heater power

supply installation.

He observed that the heaters are powered

from 480 Vac buses 1 and 2 which can be powered redundantly from

either onsite or offsite power. The inspector also verified that

Procedure S-3-5.5, "Loss of Coolant", specifically required the

operator to reenergize the necessary groups of pressurizer heaters

to establish and maintain natural circulation. The inspector stated

that the time required to connect pressurizer heaters to their

emergency power source appeared consistent with prompt initiation

and maintenance of natural circulation. The inspector observed

that the interfaces of the pressurizer heaters to the Vital Buses

were through Westinghouse Mode DB-25 ACB's which tripped on overcurrent

or low level in the pressurizer.

The inspector stated that this

appeared to be isolation similar to that used for safety-related

components powered from the vital buses, and that the licensee's

actions appeared acceptable.

h. TAP II.E.4.2

The inspector reviewed the licensee's completed preoperational

test 2.1.4-1, "Diverse Containment Isolation System Test"; observed

the installed equipment in the control room; reviewed the licensee's

list of essential and non-essential systems; verified that all

non-essential systems were isolated by the containment isolation

signal when tested; that resetting of the isolation signal did not

result in automatic reopening of containment isolation valves when

tested; that reopening of containment isolation valves required

deliberate operator action when tested; and that.containment isolation

was initiated by either a safety injection initiation signal or

by high pressure in the containment.

The inspector stated that

the licensee's actions were acceptable.

i.

TAP II.F.2

The inspector observed that a "control grade" primary coolant saturation

meter was installed in the control room which automatically selected

the hottest hot leg loop temperature for control room display.

The inspector noted that the licensee had decided that additional

instrumentation to supplement this meter was unwarranted in their

March 25, 1980 letter to NRR. The inspector stated that the meter

installation in addition to the procedures confirmed in Inspection

Report (50-206/80-12) appeared to adequately address this item.

In addition the inspector stated that Open Items 50-206/80-12-04

and 80-12-05 were closed.

- 10

j. TAP II.G.1

The inspector observed that the licensee had installed a backup

nitrogen pneumatic operation system for the pressurizer power operated

relief valves (PORV's) and PORV block valves. The inspector also

observed that the nitrogen system had been identified as essential,

and the containment isolation system had been appropriately modified.

The inspector noted that this item implied that these valves were

electrically operated, while at San Onofre 1 they are pneumatically

operated, and the pneumatic source of power, the instrument air

system, is not safety related or qualified. The inspector stated

that notwithstanding this anomaly, the licensee's actions appeared

acceptable.

k.

TAP III.A.1.2

The inspector observed that neither the Technical Support Center

(TSC) nor the Operational Support Center (OSC) definitions had

been incorporated into the licensee's Emergency Plan, but noted

that according to a licensee representative the plan would be updated

to reflect these centers as well as other changes by January 1,

1981.

Licensee personnel stated that the facility presently does

not have isometric drawings for some piping systems less than 2"

in diameter, nor photographs of these systems, so that the TSC

set of drawings is incomplete. Furthermore, the inspector noted

that some inaccuracy in the existing facility drawings of safety

related systems had been.recently identified by the inspector (See

Inspection Report 80-16 pp 5-6).

Notwithstanding this, the inspector

stated that it was apparent that the licensee had in fact established

an interim TSC and OSC, and therefore the completion of this item

Was substantially confirmed.

1. TAP III.D.1.1

The inspector reviewed the leak reduction program established by

the license in S-I-1.71, "Maintenance of Auxiliary Radioactive

Systems Outside.Containment", S-111-2.40, "Post Accident Operation

of Radioactive Waste Systems", S-3-3.26, "Leakage Test of Radioactive

Systems Outside Containment", and Technical Specification 4.2,

"Safety Injection and Containment Spray System Periodic Testing.

The inspector observed that the licensee's test program was in

two parts: measurements of leakage from the recirculation loop

outside containment, as required by the Technical Specifications;

and measurements of other leakage from other systems that might

contain highly radioactive fluids during a serious transient.

The licensee has submitted the overall leak rate results to NRR

in a letter dated January 17, 1980. A licensee representative

stated that the implied acceptance criteria for all leakage was

625 "effective" cc/hr, where the Technical Specification weighted

leak rate known as "effective leak rate" is used.

The inspector

-1 1

noted that S-3-3.26 did not specify the plant valve lineup in which

the leakage was measured, and to that extent a different valve

lineup might produce different leak rate data. The licensee was

not able to retrieve the raw test data at the time of the inspection.

The inspector stated that it would be reviewed once the licensee

retrieved it. (01 50-206/80-31-07).

The inspector additionally reviewed the licensee's preventive maintenance

program to reduce leakage to as-low-as-practical, S-I-1.71. The

inspector observed that this procedure only required that when

components were repaired that the use of lower leakage rate materials

or components should be "considered". The inspector stated that this

vague direction to workers was acceptable absent any regulatory

guidance. However, the inspector will monitor the licensee's

implementation of this program to ensure that it is effective.

(01 50-206/80-31-06).

No items of noncompliance or deviations were identified.

9.

Exit Interview

An exit interview (Paragraph 1) was held on October 31, 1980 to summarize

the scope and findings of.this inspection. The inspector also reminded

the licensee of the importance of vigilant fire prevention inside the

containment during this outage, due to the large amounts of combustible

(albeit fire-resistant) polyethylene sheeting being used there. The

inspector noted that the sheeting (Visqueen) releases large quantities

of noxious black smoke when it burns.

A licensee representative stated

that the use of large quantities of this material inside containment

would be reviewed.

(01 50-206/80-31-07).