ML13312A713

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Insp Repts 50-206/93-19,50-361/93-19 & 50-362/93-19 on 930624-0728.Violations Noted.Major Areas Inspected: Operational Safety Verification,Radiological Protection, Security,Evaluation of Plant Trips & Events
ML13312A713
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 08/24/1993
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13312A711 List:
References
50-206-93-19, 50-361-93-19, 50-362-93-19, NUDOCS 9309290179
Download: ML13312A713 (25)


See also: IR 05000206/1993019

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos.

50-206/93-19, 50-361/93-19, 50-362/93-19

Docket Nos.

50-206, 50-361, 50-362

License Nos.

DPR-13, NPF-10, NPF-15

Licensee:

Southern California Edison Company

Irvine Operations Center

23 Parker Street

Irvine, California 92718

Facility Name:

San Onofre Units 1, 2 and 3

Inspection At:

San Onofre, San Clemente, California

Inspection Conducted:

June 24 through July 28, 1993

Inspectors:

C. W. Caldwell, Senior Resident Inspector

J. J. Russell, Resident Inspector

-0. L. Solorio, Resident Inspector

C. M. Re an, NRR Intern

Approved By:

Wgne

.J. Won ,C ie

ign

Reactor Projects Se tion II

Inspecti onSumary

I Apc

i

on

on June

24 thrOuh

Jul 281 1993

(Report

Nos.

50-206/93_19.

019319

50-31

293a19

Areas

Insp

m:

Routine, announced, resident inspection of Units 1, 2 and 3

operations program including the following areas:

operational safety

verification, radiological protection, security, evaluation of plant trips and

events, bi-monthly surveillance activities, monthly maintenance activities

refueling activities, independent inspecti on, quality verification, design

changes, facility modifications, licensee self-assessment, fire protection

followup on items of noncompliance, corrective action programs, engineered

safety feature walkdown, maintenance program implementation, followup on items

of non compliance, licensee event report review, and followup of previously

identified items.

Inspection procedures 35702, 37700, 37701, 40500, 60705,

60710, 61726, 62700, 62703, 64704, 71500, 71707, 71710, 90712, 92700, 92701,

92702, 92720, and 93702 were covered.

Safety

Issues

Manag ient

ystem

(SIMSh- Itens:

None

9309290179 930826

PDR ADOCK 05000206

G

PDR

Resul ts:

General Conclusions and Specific Fidinls:

Strenpths:

Quality Assurance (QA)

surveillances on corrective action implementation

identified an inappropriate change to an abnormal operating instruction (AOl)

(Paragraph 9.a).

QA field observations continue to be a strength (Paragraph

9.b).

Weaknesses:

A weakness was identified concerning inadequate corrective actions for removal

of lagging from a main steam safety valve. In particular, the commitments

made in response to main steam safety valve inoperability in 1990, as

documented in a Licensee Event Report , were not implemented. In addition, a

root cause evaluation for the improper lagging removal from a Unit 2 main

steam safety valve in 1993 determined that the proposed corrective actions for

the 1990 event may not have been adequate even if they had been implemented.

Further, the NRC was concerned that the unlagged valve went unnoticed for

approximately four days (Paragraph 11.a).

A weakness was identified concerning inadequate control of changes to AOIs

(Paragraph 9.a).

The continuing issue associated with controleof sweld dfisler bmaterialrebyou

W

conractor personnel (Paragraph 9.b), with the issues described in previoous

inspection reports also related to contractor deficiencies, indicate that

additional management attention may be warranted in the control of

contractors.

Significant Safety Matters:

SummarY of Violations:

One violation of NRC requirements was identified within the scope of this

inspection for inadequate corrective actions related to the removal of lagging

from a main steam safety valve in Unit 2 on February 8, 1993 (Paragraph 11.a).

One non-cited violation of NRC requirements was identified for inadequate

control of Units 2 and 3 A0Is (Paragraph 9.a).

Open Items Summary:

During this report period, five new followup items were opened and 13 were

closed.

2

DETAILS

i

_Persons Contacted

Souhr

Clfri

Edson Co-many

H. Ray, S

enior Vice President, Power Systems

  • R. Krieger, Vice President and Site Manager

R Rosenbium Vice President, Nuclear Engineering and Technical Support

JR Reilly, Manager, Nuclear Engineering & Construction

  • B. Katz, Manager, Nuclear Oversight

K. Slagle, Deputy Station Manager

  • R. Waldo, Operations Manager
  • L. Cash, Maintenance Manager
  • D. Breig, Manager, Station Technical

M. Short, Manager, Site Technical Services

M. Wharton, Manager, Nuclear Design Engineering

  • P. Knapp, Manager, Health Physics

D. Herbst, Manager, Quality Assurance

C. Chiu, Manager, Quality Engineering

G . Moore, Plant Superintendent, Unit 1

V. Fisher, Plant Superintendent, Units 2/3

  • G. Gibson, Supervisor$ Onsite Nuclear Licensing

. Reeder, manager, Nuclear Training

H. Newton, Manager, Site Support Services

  • T. Rainsberry,

Plant Licensing Manager

  • W. Marsh, Manager, Nuclear Regulatory Affairs
  • T

n

Fee, Health Physics Assistant Manager

  • E. Gatto, Health Physics Training Supervisor
  • A. Thiel Manager, Electrical Systems Engineering
  • R. Giroux, Engineer

Onsite Nuclear

icensing

  • J

Darling, Engineer, Onsite Nuclear icening

  • T. Frey, Engineerin g Aide, Onsite Nuclear Licensing
  • Denotes those attending the exit meeting on August 2, 1993.

The inspectors also contacted other licensee employees during the course

of the inspection, including operations shift superintendents, control

room supervisors, control room operators, QA and O engineers,

compliance engineers, maintenance craftsmen, and health physics

engineers and technicians.

2.

Plant

Status

nt I

The Unit was permanently shutdown on November 30,

1992.

Primary and

secondary systems remained in a "SAFSTOR 1 condition throughout the

inspection report period.

Unit 2

The Unit began the inspection report period with all fuel offloaded to

the Unit 2 spent fuel pool for the Cycle VII refueling outage.

The ten

year reactor vessel inservice inspection was completed on July 12, 1993.

Core reload was completed July 18, 1993. The Unit was in Mode 5 at the

end of the inspection report period.

Unit 3

The Unit began the inspection report period at 100% power.

The Unit

experienced an automatic reactor trip and auxiliary feedwater (AFW)

injection on July 5, 1993, due to a main turbine trip. A gland sealing

steam spill valve failed open causing a loss of gland sealing steam and

a resultant loss of main condenser vacuum. This loss of vacuum caused

the main turbine trip. All safety systems functioned normally.

The

Unit was returned to 100% power on July 7, 1993.

On July 17, 1993, power was reduced to 80% for heat treatment of the

circulating water system.

On July 18, 1993, the Unit resumed full power

operation and continued at 100% power for the remainder of the

inspection report period.

3.

Operational SafetY Verification (62700,

71707)

The inspectors performed several plant tours and verified the operabi

lity of selected emergency systems, reviewed the tag out-log and

verified proper return to service of affected components. Particular

attention was given to housekeeping, examination for potential fire

hazards, fluid leaks, excessive vibration, and verification that

maintenance requests had been initiated for equipment in need of

maintenance.

The inspectors also observed selected activities by

licensee radiological protection and security personnel to confirm

proper implementation of and conformance with facility policies and

procedures in these areas..

a.

Units 2 and 3 Seismic Observations (62700, 71707)

During this inspection period the inspector observed ten instances

in which control of equipment in safety-related areas was not in

accordance with the licensee's program as outlined in station

procedure S0123-1-20, "Seismic Controls -

Seismic Controls During

Maintenance, Testing and Inspection."

Although these individual

observations were of low safety significance, the inspector was

concerned that the corrective actions for this problem may need to

be expanded to involve other organizations.

Control of components in safety-related areas was previously

identified in previous NRC Inspection Report 50-206/93-11.

Corrective actions taken in response to this identificati 'on were

to refamiliarize station and contract maintenance personnel with

the requirements of seismic procedures.

However, the inspector

5

2

considered that many of the instances observed during this

inspection period indicated that personnel outside the maintenance

organizations may also need to be made aware of these

requirements.

In conclusion, the inspector considered that this

issue still warrants management attention.

During the exit meeting the Maintenance Manager indicated that in

selected areas of the maintenance organization a re-trainling

program for 50123-1-1.20 would be initiated.

The Vice President,

Nuclear Generation, acknowledged that further management attention

was required and that a plan was being implemented to address the

seismic restraint issue. Additionally, the Maintenance Manager

indicated that efforts undertaken as a result of findings during

the previous inspection period had resulted in improvements within

the maintenance organizations. The inspectors will review the

effectiveness of these actions in future inspections.

b.

Unit 2 Reactor Coolant Sstem Drain Down

to

idlooJ (71707)

On July 23,

1993, the inspector observed the Unit 2 reactor

coolant system (CS) draindown to approximately 17 inches above

the bottom of the RCS hot leg, in accordance with operating

instruction S023-3-1.8, "Draining The Reactor Coolant System."

The drain down was observed from both the control room and the

containment spray pump room (used to drain down the RCS).

The

drain down was conducted in accordance with proceduresand in a

controlled and professional manner.

No deficiencies were

identified.

No violations or deviations were identified.

4.

Evaluation of

Plant

Trips

andi Events (93702)

a.

Partial Loss of Ann unciators

-

Units

2 and

3

On July 4, 1993, annunciator ground alarms activated on both Units

and on the common boards in the control room.

At this time Unit 2

was defueled and Unit 3 was in Mode 1. The operators then noted

abnormal annunciator operation for annunciators that indicated the

status of electrical systems and plant services for both Units and

reactor services for Unit 3. The-following annunciator boards

were affected: 3UA0063A,B,C; 2/3UA0063D,E; 2UA0063A,B,C;

2/3UAO61AB; and 3U0A56B. This abnormal operation included, at

various times, spurious alarms, alarms that would not reset,

improper audible indication, and audible indication that would not

reset.

The operators entered S023-13-22,

"Loss of Control Room

Annunciators," and increased monitoring of safety-related

parameters.

Maintenance personnel performed troubleshooting and

restored the annunciators to operable status on July 5, 1993.

Maintenance personnel replaced various circuit modules that

3

controlled power to groups of annunciators (AN 1128 modules) and

circuit modules that controlled individual annunciator function

(AN 1123 and AN 1127 modules) in order to correct the problem.

The licensee was evaluating the root cause for the failure of

these circuit modules and had not completed this evaluation at the

end of this report period.

The inspector will review the results

of this root cause analysis as inspector followup item (IFI 50

361/93-19-01).

b.

internals i

nd in Reactor Vessel -

mnit

2

On June 30, 1993, the licensee found two safety injection cold leg

nozzle thermal sleeves in the area of the Unit 2 reactor vessel

flow skirt.

This condition was documented in nonconformance

report (NCR) 93060175. The sleeves were subs Iequently removed.

The licensee was performing a ten year inservice inspection (ISI)

of the Unit 2 reactor vessel at the time. The reactor vessel

internals, including the core support barrel, had been removed in

preparation for the ISI. The licensee documented in the NCR that

there was no operability impact to reactor internal components

which may have been contacted as the sleeves moved from the cold

leg nozzles to the flow skirt. Additionally, the licensee

concluded that the two remaining sleeves would not impact

operability of reactor vessel internals should they become

dislodged.

On July 13,

1993, the licensee found a metallic object lodged

between the Unit 2 reactor vessel and the vessel flow skirt.

The

licensee was using an ultrasonic probe to inspect the vessel when

the metallic object was noted.

Based on visual observations, the

licensee concluded that the object was a steam generator tube

plug.

The licensee concluded that this was one of two tube plugs

that had been discovered missing from their installed tube

locations during a Unit 2 outage in 1988.

The plugs were

Combustion Engineering mechanical tube plugs fabricated from

Inconel 690, and were five inches long with a nominal outside

diameter of 0.650 inches.

The licensee attemptea to dislodge the tube plug using remote

mechanical equipment, but was unsuccessful.

It appeared that the

plug was firmly lodged in its position between the reactor vessel

and the core-flow distribution skirt.

The licensee performed

a

safety analysis when the plugs were first discovered missing in

1988.

On July 13, 1993, a conference call was held with NRC

Region V management and licensee management concerning the

advisability of leaving the plug in place.

The inspector reviewed the safety analysis which had been

submitted to the NRC in 1988.

The inspector concluded that the

safety analysis was adequate in that it demonstrated minimal

safety significance in leaving the plug in place.

The inspector

concluded that the analysis adequately addressed any possible

0

4

damage to the RCS, the fuel, or interconnected systems should the

plug become dislodged from its current position during power

operation.

Based on the conference call and the safety analysis

mentioned above the inspector had no more concerns in this area.

On July 14,

1993, the Unit 2 core barrel was reinstalled with the

plug left lodged as described above.

No violations or deviations were identified.

5.

Bi-MonthlY Surveillance Activities (61726)

During this report period, the inspectors observed or conducted

inspection of the following surveillance activities:

a.

Observation

of Routine Surveillance Activities (Unit

2

S023-II-9.207,

"Bently Nevada Speed Sensor Model 300 HA

and Model TD 80 Tach Driver/Pulse

Transmi tter Cal i brati on."

S023-II-9.501,

"Surveillance Requirement Reactor Coolant

Pump Shaft Speed Sensor to Core Protection

Calculator Calibration."

5023-3-3.12 ISS2, "Integrated System Refueling Test."

b.

Observation of Routine Surveillance Activities (Unit 31

S023-II-9.2071

"Bently Nevada Speed Sensor Model 300 HA

and Model TD 80 Tach Driver/Pulse

Transmitter Calibration."

S023-II-9.501,

"Surveillance Requirement Reactor Coolant

Pump Shaft Speed Sensor to Core Protection

Calculator Calibration."

No violations or deviations were identified.

6.

Monthly Maintenance Activities (62703)

During this report period, the inspectors observed or conducted

inspection of the following maintenance activities:

a.

Observation of Routine Maintenance Activities (Unit 2)

MO93030993001,

"Installation of Seismic Braces to Unit 2

Class 1E Transformer 2B04X."

M093071352000,

"Installation of Seismic Braces to Unit 2

Class 1E Transformer 2B06X."

5

M09307102 7000,

"Flush Water From Unit 2 Emergency Diesel

Generator 2G002 Oil System."

M093031141 000,

"Handwheel is Missing and The Declutch

Lever is Loose,

CCW Valve 2HV6552."

MO921101 55000,

"Disassemble Reactor, Perform Fuel

Movement Activities, and Reassemble the

Reactor."

b.

Observation of Routine Maintenance Activities (Unit 3)

M092092743 000,

"Re-align Cold Leg Temperature Indicator

3TI-9178-3."

No violations or deviations were identified.

7. Engineered Safety

eature System Walkdown - Unit 3 (71710)

The inspector reviewed Auxiliary Feedwater P&IDs against station

operating procedures S023-2-4, "Auxiliary Feedwater System

Operation," and S023-0-17, "Locking of Safety Related Critical

Valves and Breakers."

The inspector also walked down portions of

the system. Inspection activities were ongoing at the end of the

inspection period.

No violations or deviations were identified.

8.

Plant Modification

and Refueling Activities (37700,

37701, 60705,

60710)

a.

Unit 2 Core Reload (60710)

The inspector observed portions of the Unit 2, Cycle VII core

reload activities from the control room and from the reactor

cavity. The inspector concluded that, with the exception

discussed below, core reload activities were conducted in a

controlled and deliberate manner, and that personnel were

cognizant of their duties and responsibilities.

On July 14, 1993, the inspector observed a reactor operator (RD)

performing the duties of the 1/M monitor in accordance with S023

X-7, "Nuclear Fuel Movement for Refueling Cycles."

The inspector

noted that although the RO monitored the 1/M chart recorder, the

RO did not notify the control room engineer (ORE) that the 1/M

chart recorder was trending appropriately (not trending in a

nonconservative manner to ensure there were no criticality

excursions) before the fuel assembly was ungrappled in the core.

The inspector subsequently verified that the CRE had verified that

the 1M chart recorder trended in an appropriate manner before he

notified the refueling machine operator to ungrapple the fuel

assembly in its designated core reload position.

The inspector

6

noted that procedure S023-X-7, also specified the CRE to monitor

the 1/M chart recorder. Thus, there was no safety significance

associated with this incident.

The inspector determined that the reason theul/M monitor did not

inform the CRE before the fuel assembly was ungrappled was because

he had not reviewed the section in S023-X-7 outlining the duties

of the 1/M monitor prior to assuming the position. Although there

was no safety consequence of this observation, the inspector noted

that it was an Operations management expectation that operators be

sufficiently familiar with a procedure such that they can perform

in accordance with the procedure.

The inspector discussed this observation with

a

Operations

management who indicated that as a result improvements would be

made in the training ROs and refueling engineers receive on S023

X-7. Additionally, the licensee indicated that a sign-off step

would be added to S023-X-7 to assure that ROs review the

requirements for the position of the 1/M monitor prior to assuming

the position. The inspector considered these actions adequate.

b.

Design Changes and Modifications (37700, 37701)

The inspector reviewed portions of the following design changes.

These Design Change Packages (DCPs)

were not submitted to the NRC

for approval prior to implementation, as allowed in 10 CFR Part

50.59(b):

o

DCP 2-6605.08,

"Control Room Human Factors

Modifications

0

DCP 2-6827.00,

"Primary Plant Protection System

Circuit Test and Engineered Safety

Features Alarm Modifications"

o

DCP 2-6863.00,

"Shutdown Cooling and Containment

Spray Crossconnect"

o

DCP 2-6974.00,

"Replace 1000/1500 KVA Transformers"

0

DCP 2-6863.01,

"Pressurizer Vent"

The inspector verified that the portions of these DCPs reviewed

were in accordance with the licensee's Technical Specifications

(TS), that the DCPs were controlled by adequate procedures, and

that the DCPs were properly tested before being declared operable.

The inspector verified that procedures had been changed as

necessary and that operators had received adequate training on the

DCPs. The inspector verified that appropriate changes had been

made, or were planned, to applicable drawings, documents, and the

licensee's Updated Final Safety Analysis report. The inspector

walked down portions of these design changes as they were being

7

implemented in Unit 2. The inspector verified that the licensee

planned on reporting these design changes to the NRC as required

in 10 CFR 50.59(b).

Overall, the inspector concluded that these

design changes were accomplished adequately, with one exception.

This exception involved aspects of DCP 2-6974.00 which will be

reviewed in a future inspection as described below. The inspector

also had one minor concern with the training provided for DCP 2

6863.00 as described below.

DCP 2-6974.00. "Replace 1000/1500 KVA Transformers'

This modification controlled the replacement of fourteen 1500 KVA

and fourteen 1000KVA transformers in Units 2 and 3. The licensee

began this replacement with the Class-1E transformers 2BO4X and

286X that provided vital 480 VAC power to Unit 2. Those two

transformers were initially installed, declared operable, and

energized without vendor recommended seismic supports. The

replaced 2BO4X transformer was energized on July 16, 1993,

and the

replaced 2B06X transformer was energized on June 23, 1993. On

July 19, 1993, the licensee discovered that these seismic supports

were not in place, during an unrelated inspectionaand declared

both transformers inoperable.

On July 19,

1993, and July 20,

1993, the licensee installed the seismic supports to these

transformers, declared the transformers operable, and reenergized

them.

The licensee was conducting an analysis to determine the

necessity of these supports and was conducting an investigation

into why they were not installed originally.

These activities

were ongoing at the end of this inspection report period.

The

inspector will review the results of the analysis and the

investigation as unresolved item (URI 50-361/93-19-02).

DCP 2-6863.00, "Shutdown Cooling and Containment

Spray

Crossconnect'

This modification involved a change that connected the containment

spray and spent fuel pool cooling systems and allows the licensee

to use the containment spray (CS) pumps to provide SFP cooling and

to provide shutdown cooling (SC) for the RCS.

The inspector

noted that training had been provided to the licensed Operators by

the licensee'

training staff during the months of March and

April, 1993. The inspector also noted that the two principal

functions of this design change, using CS pumps to provide SFP

cooling and SDC, were used during the Unit 2 Cycle VII refueling

outage. The design change was completed during this outage. The

inspector interviewed licensed Senior Reactor Operators .(SROs) and

ROs who were actively involved in using the CS pumps to provide

SFP cooling and SDC.

The inspector received comments that the

training could be improved.

The inspector noted that pre

evolution briefs had been conducted which enabled the operators to

operate Unit 2 safely, and that no mis-operations of the controls

resulted.

The inspector contacted licensee training staff and

learned that further training was scheduled for the month of

  • II

8

August 1993. The inspector conclsuded that this additionaltI

training was appropriate, but was concerned that complete training

had not been provided to the operators prior to declaring the

design change operable.

The inspector will monitor this

additional training during the course of normal inspection

activities.

This was considered of minor safety significance

since some training had been provided Iadequate pre-evolution

briefs were conducted, and the operators did not mis-operate the

controls.

In summary, the inspector concluded that the portions of the DCPs

inspected were adequate with the exception of DCP 2-6974.00 which will

be further reviewed.

No violations or deviations were identified.

9.

Independent Inpe2tion (35702,

40500, 92720)

a.

eactor CoolantPm

Abnormal

Operatina Insrucion_

age (35702,

40500, 92720)

In January 1993, the licensee's Quality Assurance (QA)

organization identified that AON

o023-13-6,

"Reactor Coolant Pump

(RCP) Seal Failure," Temporary Change Notice (TCN)

o -

(issued in

July 1991),

was inappropriately changed toallow operators to

institute an orderly plant shutdown following a loss of controlled

bleedoff (CBO) flow to the RCP seals.

Specifically, QA personnel

found that there was no documented basis for changing the AOl

The information used to provide the justification for changing the

AOI, was a vendor pump test which documented that the RCPs could

run without component cooling water cooling to the CBO flow.

However, Station Technical personnel misinterpreted the vendor

test and concluded that the RCPs could run without 080 flow

(rather than without CCW cooling).

Immediately after this

discovery the AOI was corrected to require a reactor trip upon

loss of CBO flow. The inspector considered that this observation

by the licensee's QA organization was an example of a well-planned

and well-performed QA surveillance.

The root cause for the inappropriate change to the A01 was

identified to be the failure of an engineering supervisor to

independently verify the accuracy of information provided to the

operations department.

Corrective actions taken included the

development of formal requirements for transmitting information

from Station Technical to Operations. The inspector considered

the licensee's corrective actions adequate.

The inspector noted that during the time TCN 0-7 was in effect

there were no instances where operators used S023-13 6 to

institute an orderly plant shutdown as a result of losing 080 flow

to the RCP seals, therefore there was no safety significance of

the inappropriate TCN.

9

The inspector considered that the TCN 0-7 to S023-13-6 was an

example of inadequate control of a procedural change in that there

was no independent verification of information used to issue a TCN

against the procedure. However, this violation is not being cited

since it was licensee identified, appropriate actions were taken

as a result of the inspector's concerns, there was no safety

significance, and the requirements of Section V.B of the

Enforcement Policy were satisfied, non-cited violation (NCV 50

361/93-19-03).

b.

Welding Filler Material Control (92720)

On July 5, 1993, the site QA organization found uncontrolled

welding filler material during a walk down of the Unit 2 Auxiliary

Feedwater pump turbine work. The material was issued to a

contract welder who had not attended SCE welder training, but had

been provided reading material by his employer which discussed

filler material control.

The inspector noted that this was the

third instance in which QA found uncontrolled welding filler

material during the Unit 2 Cycle VII outage (two involved

contractor employees and one involved SCE personnel).

The

inspector will review the licensee's corrective actions in a

future inspection.

The inspector noted that these observations were examples of an

aggressive QA organization. However, the inspector was concerned

with the number of recent issues involving weaknesses in the

control of contractors.

Specifically, a large number of seismic

concerns were attributed to contractors (identified in NRC

Inspection Report 50-206/93-11),

and contractor attention-to

detail issues (involving the identification of degraded

radiological control barriers, improper placement of a self

reading dosimeter, and inadvertent damage to equipment) were

described in NRC Inspection Report 50-206/93-09, Paragraph 3.b.

Therefore, the inspector concluded that control of contractors,

particularly-during outages, appeared to warrant additional

management attention.

C.

Status of Units 2 and 3 When Defueled (92720)

The inspector reviewed licensee actions for core reload of Unit 2

on July 14, 1993. All of the fuel in the core had been offloaded

to the Unit 2 SFP earlier in the outage. When the licensee was

making preparations to commence the core reload, the inspector

observed that the Control Room Emergency Air Cleanup System

(CREACUS)

was not fully operational.

This was a Limiting

Condition for Operation (LCO) of Unit 2 while in Mode 6.

The

licensee and inspector noted that the Mode status of Unit 2, as

relates to Technical Specifications (TS)

was not well defined with

all fuel removed from the reactor vessel.

When the licensee was ready to commence core reload of Unit 2, the

10

Unit was in a TS Action statement for CREACUS (TS 3.7.5) due to

electrical work being done on one train of CREACUS.

With Unit 3

in Mode 1, the licensee was complying with the applicable TS

ACTION, to restore the inoperable train of CREACUS to operable

status within 7 days or place Unit 3 in Hot Standby.

The licensee interpreted the Unit 2 status as not in Mode 6 for TS

purposes, except for TS 3.7.5. The inspector observed that this

interpretation was stated in a special order issued by the Vice

President, Nuclear Generation,

onl July 14,

1993, to the Operations

department. The inspector also observed that the licensee

commenced core reload with one train of CREACUS inoperable. The

inspector noted that if the Unit was not in Mode 6 then this could

have been considered a Mode change to Mode 6 when core reload was

commenced. The inspector noted that this Mode change would have

been into a Mode for which the LCO for TS 3.7.5 was n

ot met, which

would have been contrary to TS 3.0.4.

The inspector noted that if

Unit 2 had not offloaded the fuel assemblies, the applicable

ACTION would have remained unchanged .

Unit 3 would still have had

to shut down in 7 days regardless of Unit 2 status due to the

wording of this particular TS.

The inspector considered the safety significance of this issue to

be low, but noted that this issue highlighted the problem with TS

which do not specifically recognize defueled conditions. The

Region V staff had discussions with NRR personnel and requested

0

that NRR evaluate the Mode status of the unit when the reactor is

defueled.

The inspectors will assess the licensee's actions in

this instance upon receipt of NRR's evaluation as inspector

followup item (IFI 50-361/93-19-04).

d.

Balance of Plant Inspection - Unit 2 (71500)

During the Cycle VII refueling outage, the inspector conducted

walkdowns of the Unit 2 turbine building .

The inspector observed

activities associated with the turbine overhaul, main feedwater

pumps, and the condenser., The inspector identified no

deficiencies during these walkdowns.

No violations or deviations were identified.

10.

Review of Licensee Event Reports (90712, 92700)

Through direct observations, discussion with licensee personnel, or

review of the records, the following Licensee Event Reports (LERs)

were

closed by onsite review:

Unit 2

93-02, Revision 0,

125 VDC Battery Chargers 2B1 and 2B2 Inoperable

Due To Incorrect 10 CFR Part 21 Evaluation."

0

11

This item indicated that on February 25, 1993, the licensee determined

that battery chargers 2B1 and 2B2 were inoperable following replacement

of the reactor balance circuit cards.

This LER was reviewed previously

by the inspector and the results were documented in. NRC Inspection

Report 50-206/93-09. In that report, the inspector indicated that the

item would remain open since several corrective actions had not been

completed. In particular, the maintenance procedure governing battery

testing, 5023-l-9.14, "Battery Charger Inspection, Cleaning and

Testing," had not been revised to include post-installation verification

and adjustment of current limiter settings.

In addition, the original

10 CFR Part 21 report from the vendor was to be reevaluated for

additional corrective actions and procedure enhancements as deemed

appropriate.

The licensee has completed their reevaluation of the 10 CFR Part 21

report from the vendor, C&D Batteries. The licensee's reassessment

resulted in several actions. These actions included a revision to the

controlling procedures to require recording the "as-found" current limit

setting prior to making the setpoint adjustment.

If the "as-found"

setting should be found less than the TS requirement, then an NCR would

be generated and the appropriate personnel would be notified.

The

licensee also indicated that they would incorporate the new calibration

information received from the vendor into the appropriate maintenance

procedure for current limit setpoint adjustment after it is received

from the vendor. The inspector considered that the licensee's actions

both proposed and implemented were appropriate. This item is closed.

No violations or deviations were identified.

Follow-Up of Previously Identified

Items (64704, 92701)

a.

(Closed)

Unresolved

Item

(50-361/93-02-03).

"Cnfigiration

Control

Issues

In Units 2 and 3."

This item discussed several problems involving improper

configuration control that were identified by the licensee and by

the NRC as follows:

1)

On February 8, 1993, Station Technical personnel identified

that the lagging for Unit 2 main steam

safety valve (MSSV)

2PSV8411 had been removed.

With the lagging removed, the

setpoint was indeterminate and the valve was declared

inoperable.

The lagging had apparently been removed by

Maintenance personnel four days prior. For followup action,

the lagging was replaced, the valve was declared operable,

and NCR 93020012 was issued. As a result of this problem,

the inspector was concerned that work activities on the

valve were not adequate to ensure that configuration control

was maintained, and that it took approximately four days to

identify the discrepancy.

Since this item was identified, the licensee issued LER

12

361/93-001 to report the problem to the NRC and performed a

root cause evaluation of the event.

The evaluation report,

ROE 93-005, was issued on April 13 , 1993, which identified

that the root cause was due to insufficient barriers in the

work planning process to identify that removal of insulation

from the MSSVs would render them inoperable.

The RCE also

indicated that there were several contributing causes

including lack of effective corrective actions from a prior

event involving the MSSVs.

In July 1990, the licensee identified that MSSV setpoints

changed depending if the lagging was on or off. This was

due to changes in the temperature profile of the valve which

affected the spring constant and the lift

setpoint of the

valve.

The licensee issued LER 361/90-008 which indicated that

several corrective actions would be implemented.

One action

in particular was to revise the general maintenance order

(MO)

to require an engineering review prior to removal of

any lagging installed on the MSSVs.

The licensee also

indicated that these Planned actions would ensure that

operability of the MSSVs was properly addressed prior to the

removal of lagging.

However, upon review of the corrective actions implemented,

the inspector noted that the licensee did not revise the

general MO to include an engineering rEtview of the MSSVs.

Instead, the general MO was revised such that insulation

removal from the MSSVs required a separate MO.

In fact,

Engineering review of lagging removal on the MSSVs was not

addressed at all.

The inspector noted that the licensee attributed this

discrepancy to the fact that in 1990, a number of personnel

were responsible for closure actions to regulatory

commitments.

In this specific case, the person who closed

the item took a liberal interpretation of how the corrective

actions identified in the LER could be implemented.

In

addition, the inspector questioned whether the proposed

action to have an engineering review of MSSV lagging removal

would have prevented further problems.

Specifically, the

licensee's RCE noted that not all engineers were aware that

removal of lagging could change the valve setpoint.

After the February 1993 event, the licensee implemented or

proposed corrective actions to0 include, reinstalling the

lagging, installing signs at each MSSV warning about the

implications of lagging removal, and changing the program to

ensure that a warning is included in the computerized

maintenance management system to alert personnel that a MSSV

must be declared inoperable if the valve body insulation is

13

removed. The licensee believed that the changes to the

maintenance management system should prevent this from

reoccurring. The inspector considered that the licensee s

actions both proposed and implemented subsequent to the

February 1993 inoperable MSSV were adequate.

10 CFR Part 50, Appendix B, Criterion XVI, requires that for

significant conditions adverse to quality, measures shall

assure that the cause of the condition is determined and

that corrective actions are taken to preclude repetition.

However, the licensee's corrective actions for the July 1990

event involving inoperability of the Unit 3 MSSVs were not

adequate to prevent the inoperability of MSSV 2PSV8411 in

February 1993.

This inadequate corrective action is

identified as violation (VIO 50-361/93-19-05).

2)

This unresolved-item also identified that on February 1,

1993, the licensee found that the pressure instrument root

valves were open for both Unit 3 containment spray pumps.

This was in conflict with their required position.

The

licensee closed the valves and then performed a walkdown of

all similar root valves in both Units 2 and 3. During the

walkdown, a number of other valves were found open,

including instrument valves for a high pressure safety

injection pump in Unit 2 and eight root valves for the boric

acid makeup systems in Units 2 and 3.

The main concern with

the valve misalignment was that the tubing downstream of

these root valves was not seismically qualified.

As a

result, it was possible that there could be a diversion of

some safety injection flow after a seismic event.

As an immediate corrective action, the licensee restored all

the valves to their intended closed position. In addition,

the licensee performed an Operations Division Experience

Report (ODER) 3-93-06, to determine the cause of the event.

Although, the licensee could not determine exactly how the

valves became mispositioned, they considered that the valves

were not fully closed the last time they were operated to

support in-service testing (IST).

The licensee determined

that the root cause was inadequate interface among

organizations during the use of IST procedures.

The ODER

indicated that the common cause appeared to be the process

of operation by implication.

In particular, the ODER

pointed out that liberal interpretations of the procedures

may have been taken by making some assumptions on the part

of personnel that were incorrect.

For followup to the valve mispositioning occurrences, the

licensee initiated several additional corrective actions.

These included issuance of a policy statement reemphasizing

that valves, switches, and breakers cannot be operated

without a controlling document specifically stating to

  • I

14

A

operate the component.

The licensee indicated that if steps

0

are not specifically identified, then a procedure revision

is required that would require an SRO review of the

operation to help ensure that the as-left condition matches

the system alignment requirements. In addition, the

IST

licensee also evaluated the Station Technical Division1S

procedures that pertain to engineered safety feature (ESF)

pumps to determine if they comply with Operations procedure

requirements. Changes were recommended as necessary. The

inspector considered that the licensee's actions for this

problem were adequate.

The inspector considered that the

licensee's actions were approriate.

This portion of the

unresolved item is closed.

3)

This unresolved item also involved a number of errors that

were identified by the NRC on piping and instrument diagrams

(P&IDs)

41097A and 40197B, "Auxiliary Building Emergency

Chilled Water System Loop A." These errors included a

temperature instrument that was missing, root valves and

temperature instruments reversed on the PlD from their

installed configuration, and drain valves located in places

other than shown on the drawing. The inspector considered

that the most significant error-was a temperature instrument

(TI), 2TI987D, that was moved on the drawing during a recent

drawing change, DCN-3, in October 1992. The drawing change

resulted from a system walkdown in April 1992 to support a

0

system hydrotest. A

number of changes were recommended for

the drawing and were verified by a second individual. A

site problem report (SPR) was generated to initiate the

drawing change. However, the verifier incorrectly

identified that the TI was in the wrong place and modified

the SPR to get it relocated on the drawing.

The licensee assessed this problem in a Nuclear Engineering

and Design Organization (NEDO) Division

investigation

Report, DIR-NEDO-93-0 02.

The licensee determined that the

error with 2TI987D was one of only a few errors with drawing

changes. In this case, the verifier made the change and

introduced the error.

The error that was made was not

identified since there was no Quality Control check of the

recommended change that was made by the verifier. The

licensee also indicated that the current error rate of

drawing changes was less than three percent, which was

within NEDO expectations.

As corrective action, the licensee counseled the individual

who made the error, focusing on attention to detail and

self-checking techniques.

As additional corrective action,

the licensee indicated in the DIR that a procedural

requirement for a quality control check of any new

description of the as-built configuration would be made

prior to revising drawings to ensure that the new

15

description was correct.

The inspector considered that the

licensee's corrective actions were appropriate.

This

portion of the unresolved item is closed.

4)

This unresolved item also involved inaccurate drawings for

the Unit 2 salt water cooling (SWC)

system.

On December 30,

1992, prior to an IST on the Unit 2 SEC pump 2P112 seal

water supply piping valves, the Unit 2 Control Room

Supervisor (CRS)

discussed with the NRC inspector drawing

discrepancies on P&ID 40126A, "Component Cooling Water

System (Salt Water Pumps)."

In particular, the P&ID showed

wrong valve numbers for the seal water supply inlet rhpck

valve 048,' and ball valve 032 for SWC pump 2P113B.

The

drawing deficiencies were determined to be associated with

the valves as labeled on the drawing and not on plant

equipment tags. The CRS indicated that the previous

revision of the drawing was correct and that somehow the

errors were introduced in the latest revision of the drawing

at the time. The CRS also indicated that an SPR would be

initiated to correct the drawing discrepancy. However, on

February 10, 1993, the inspector noted that the control room

drawing had not been changed and found that the SPR

coordinator had not received a request to revise the P&ID.

As a result, the inspector was concerned that there could be

other uncorrected drawing errors.

As a followup to the inspectors concern, NEDO performed an

investigation, NEDO-93-001,

and found that the error was

introduced by a designer who was using the computer assisted

drafted (CAD) program called CATIA.

The problem resulted

when the copy function on CATIA was used to create a

configuration change from one train of SWC to the other.

The designer forgot to revise the valve tag numbers as

appropriate. In addition, a checker only reviewed the

revised portion of the drawing and did not check to see if

the original valves on the drawing had their valve tag

numbers updated.

This was also true for the design

supervisor, who did not detect the error.

The licensee performed an assessment of a number of drawing

changes that were made by the same individuals for a one

month period.

The licensee found that of the 2290 changes

that were made, there were only three minor typographical

errors.

An audit consisting of a review of a random sample

of 20 electrical drawings, consisting of approximately 3700

changes, was performed that found only six minor drafting

errors.

As a result of this evaluation, the licensee

concluded that there was a very small error rate for drawing

changes and that the ones identified were very minor in

nature with the exception of this example, which was

considered to be an isolated error.

As a followup to this problem, the licensee implemented a

16

-I

number of corrective actions including coaching of all

designers on the concept of "self-checking," revising the

procedure for design change notice incorporation and

checking to emphasize attention to detail and the concept of

self-checking, and periodic monitoring of the effectiveness

of self-checking process.

The inspector considered that the

licensee's actions were appropriate.

This portion of the

unresolved item is closed.

The inspector considered that the licensee's actions an

d

evaluations for the misaligned root valves, emergency chilled

water P&IDsf and the salt water cool ing system P&I problems were

appropriate.

The generic issue concerning configuration control

was addressed in NRC Inspection Report 50-206/93-11. In that

report, the inspector identified a violation with several examples

and four non-cited violations for failure to follow procedures.

Most of these procedural adherence problems resulted in

configuration control problems in the Units.

The inspector will

evaluate the licensee's actions on this matter by reviewing the

licensee's response to the Notice of Violation in NRC Inspection

Report 50-206/93-11.

b.

(Closed) Followup Item

50-3611913-0201)_ "Nonrotation of

Operators - Followup of Operator Li sLg Banch

Evaati on.

This item involved the rotation of licensed operators during

licensee-administered requalification examinations. The licensee

evaluated crews using two scenarios run on the plant-referenced

simulator.

The inspector noted that the licensee was not rotating

the positions held by the SROs so that an individual SRO would be

the CRS during one scenario and the Shift Superintendent (SS)

during the other scenario. The inspector was concerned that this

was a change in the methods previously used by the licensee, and

that this was less comprehensive than having the operators rotate

positions. The inspector requested NRC's Operator Licensing

Branch (OLB) provide an evaluation of this issue.

The inspector received OLB's evaluation.

The evaluation stated

"the NRC's expectation is that facility licensees train and

examine their operators in the same crew configurations with which

they normally operate the plant. As a result, crew.members should

rotate between positions in the manner identical to the facility's

rotation practices for both control room operation and crew

evaluations (as specified in the facility's requalification

program). However, it should also be noted that ES-t04, D.1.G (of

the "Examiner Standards", NUREG 1021, Rev.7) states that SROs must

be evaluated in at least one scenario in an SRO licensed crew

position to fulfill their license requirement."

The inspector concluded that the licensee was examining their

operators in the same crew configurations that they used to

operate the plant. The inspector concluded that the nonrotation

17

A

d.

of SROs observed was in accordance with NRC expectations.

This

item is closed.

C.

(Clo

)Folowu

I

Item (50-206/92-12-).

'Missed Iitenal

Commitment -

RE:

Evaluation Of Performing An E ualizin_ Charge On

Unit 1 Vital BatterY

umer

149 Volts.

This item identified that the licensee had apparently not

performed an evaluation of the conditions that led to the

performance of an equalizing charge on Unit 1 vital battery number

2 at 149 volts instead of the nominal 139 volts.

This was an

internal commitment made in the nonconformance report (NCR)

documenting the problem.

The inspector was concerned that the

licensee missed completing this evaluation even though it was a

factor in deciding that an NCV was appropriat e for the original

i ssue-(See NRC Inspection Report 50-206/90-28) .

Subsequent investigation determined that the licensee never

completed the root cause case study, nor was it tracked on the

licensee's regulatory commitment tracking system (RCTS). In

addition, the inspector was concerned the licensee's NCR program

did not include any provisions to track internal commitments made

in NCRs.

Thus, since there was nothing that linked completion of

an NCR to a specific commitment date, it was possible that actions

committed to in any NCR would not be completed in a timely manner

such as this one.

The licensee evaluated the inspector's concern and determined that

they had performed a review of the condition within two months of

the initiation of NCR 90080031.

The evaluation was completed and

the results were included in the logic of the disposition.

However,'because there were no provisions for tracking the due

date of this item, it was not obvious that the issue was resolved.

The licensee also performed an assessment of the tracking

capability of internal commitments and decided to make a software

change to provide capability to track forecast dates for closure

of NCR dispositions. The licensee had expected this to be

completed by January 31,

1993.

The inspector considered that the

licensee's actions, both proposed and implemented, should prevent

recurrence of this problem.

Therefore, this item is closed.

d.

(Closed)

Unresolved Item

( 362/93-11-01). "Control Of E

uipment

In A Seismic Exclusion

Zone

In Unit

3"

On June 23,

1993, the inspector observed that a contractor

tractor-trailer was parked very close to the seismic exclusion

zone (SEZ)

near Unit 3. The SEZ is used to store fire tanker

trucks.

The inspector observed that the tractor-trailer was

parked more than 15 feet from the tanker seismic restraints, as

required.

However,

the tractor-trailer appeared to be parked

within the "two times the height" distance requirement specified

on a nearby sign.

18

The inspector discussed this concern with the licensee who

assessed the situation further. In particular a roving fire

watch was tasked with determining if this was an isolated case or

if there was a more generic problem. The licensee determined that

there were two instances shortly after the June 23 observation in

which equipment exceeded the height limitation specified.

However, in neither case was the fifteen foot restriction

challenged.

For followup action to this concern, the licensee either

implemented or planned to imp lement the following actions:

o

A briefing was conducted with site Security personnel to

ensure that they understood the height limitations.

o

The licensee was assessing the need for a letter to all site

personnel describing the need to keep the SEZ free from

potential hazards.

o

A roving fire watch will be assigned to check that the SEZ

is not challenged during the early portions of the Unit 3

refueling outage.

a

New signage will be installed to better delineate management

expectations for storing equipment near the SEZ.

The inspector considered that the licensee's actions both planned

and implemented were adequate. This item is closed.

e.

(Closed)

nreolved

Item

(5 36193-O2-o2)

"ousekeepifln

Concerns

In

Units

2 and 3"

This item discussed several housekeeping problems that appeared to

cause potential fire or seismic hazards to safety-related

equipment.

These problems included inadequate control of carts in

the spent fuel pool buildings, items stored on top of the Unit 3

diesel generator fuel oil storage vault, and potential fire

hazards found in Units 2 and 3.

The inspector continued monitoring housekeeping conditions since

this problem was first identified.

Subsequent to these issues,

additional problems were noted. In NRC Inspection Report 93-11,

the NRC issued the licensee a Notice of Violation with several

examples and four non-cited violations for failure to follow

procedures.

Most of these procedural adherence problems resulted

in configuration control problems in the Units.

The inspector

will evaluate the licensee's actions on this matter by reviewing

the licensee's response to the Notice of Violation in NRC

Inspection Report 50-206/93-11.

This item is closed.

19

(Closed) Unresolved Item (50-361/93-05-06). 'DIR Issued To Address

Accuracy Of Future LERs."

LER 2-91-007, Revision 0, discussed the shutdown of Unit 2 due to

the loss of CBO flow (seal flow) to an RCP.

'The LER discussed the

licensee's corrective. actions which included changing the RCP AOI

to allow an orderly shutdown following loss of CBO flow to a RCP

(discussed in Paragraph 9.a of this inspection report), and that

Unit 2 RCPs had been reassembled using a special bolt preloading

technique.

During a corrective actions audit the above statements in the LER

were determined to be inaccurate by the licensee's QA group. QA

found that there was no basis for changing the RCP AOI to allow an

orderly plant shutdown, and that documentation of using the

special bolt preloading technique was not complete for two RCPs.

The inspector-noted that the RCPs were

areassembled during the Unit

2 Cycle VII outage using the special bolt preloading technique.

As a result, the licensee indicated that the LER would be revised.

Additionally, a DIR would be initiated to determine the. cause for

the inaccuracies identified by QA, addressing the inspector's

concerns with regard to the accuracy-of future submittal s.

The inspector reviewed the licensee's DIR and noted that the root

cause for the change to the RCP AOI was information provided from

a engineering supervisor to the LER writer which was not

independently verified. Corrective actions included the

development of formal guidance for transmitting information from

Station Technical to Operations which was incorporated into the

Station Technical System Engineer's Roles and Responsibilities

document. The inspector considered the licensee's actions

appropriate. This item is closed.

9.

(Closed) Followup Item (50-361/93-05-05).

"DIR Procedures

Lack

Provisions To Handle Interim CARs."

During a review of DIR report procedural requirements for Nuclear

Oversight, Station Technical, Operations, Maintenance, Health

Physics and Chemistry, the inspector noted that the various

divisions' procedures did not Include provisions for handling the

implementation of interim corrective actions. It was also noted

that time requirements for issuing reports, and extensions for

reports which could not be completed within the recommended time

frame, varied among the divisions. The licensee indicated that

they would initiate efforts to provide more formality in their DIR

procedures throughout the nuclear organization.

The inspector reviewed the nuclear organization procedure S0123

XV-50.39.1, PCN 0-2, "Preparation, Review, And Approval Of

Division Investigation Reports," and noted the licensee had

incorporated guidance to provide for handling the implementation

of interim corrective actions, timeliness of DIRs, and the methods

20

to approve extensions. Additionally

the licensee indicated that

individual division DIR procedures would also be changed to model

the guidance as written in S0123-XV-50.39.1. The inspector

considered the licensee s actions adequate. This item is closed.

Within this area inspected, one violation concerning inadequate

corrective action was identified.

12.

Followi

On tems Of Nncomliance (92702)

a.

(Closed)

Violation

(50-361/92-26-_01.

"Failure To Identify M&TE n

Trav el er s"

This violation identified that personnel were not consistently

implementing the requirement to complete a traveler when measuring

and test equipment (M&TE) was used in the plant. This was

contrary to the requirements established in Section 6.2.4 of

procedure So123-Ir.2, TCN 1-4, "Preparation And Responsibility

Of The M&TE Traveler."

The traveler was used to track the use of

the M&TE so that an evaluation of the uses could be performed

should the M&TE fail a subsequent calibration.

In the December 21,

1992, Reply to a Notice of Violation, the

licensee indicated that corrective actions including formal

training of M&TE users on proper usage and an audit of the M&TE

usage database were performed to identify and resolve all M&TE

usage discrepancies.

These actions were completed on December 1,

1992, when all M&TE uses associated with unreviewed calibration

failures due to deficiencies in the database were evaluated.

Subsequent to the evaluation, NCRs were initiated, evaluating the

potential impact of M&TE calibration failures on plant equipment.

In addition, the licensee instituted monthly monitoring of the

database and other recommendations of a Quality Action Team as a

result of program deficiencies that were identified.

Monthly

tracking of M&TE database was considered as a means for management

to monitor the accuracy of the M&TE traveler database. The

inspector reviewed a monthly monitoring report and considered that

the licensee's actions were appropriate. This item is closed.

b.

(Coe)

Voain

(50361922606). "Failure

To Perform

Proper

Evaluations

n Failed

M&TE."

This violation identified that the cognizant department

supervisors were not consistently documenting the specific reasons

that retests or recalibrations were not required if M&TE failed

its calibration as required in Sections 6.2.4 and 6.2.5 of

procedure S0123-I-1.5 , TCN 1-4, "Evaluation Of Calibrated Items

After M&TE Failure."

In their December 21, 1992, Reply to a Notice of Violation, the

licensee reviewed the six calibration failure notifications (CFN)

21

in question and revised them in accordance with the procedures.

This was accomplished by December 18, 1992 and the licensee

further determined that the original conclusions documented in the

original CFN evaluations had not changed.

In addition, in order to prevent reoccurrence, the licensee

provided periodic retraining for CFN evaluators and developed a

checklist to enhance the CFN evaluation process.

The inspector

reviewed the checklist and considered that the licensee's actions

were appropriate. Therefore, this item is closed.

C.

(Closed) Violation (50-361/92-26-07)

"QA Failure To Assure

Effective Corrective Actions

on

Failed M&TE."

This violation concerned a QA audit of the licensee's M&TE program

in June 1990.

The audit identified instances in which M&TE uses

were not being properly documented on M&TE travelers in accordance

with station procedure S0123-II-1.2, "Preparation And

Responsibility Of The M&TE Traveler."

However, the licensee did

not take adequate actions to correct the deficiencies found in the

1990 QA audit, as evidenced by the number of instances in 1991 in

which M&TE usage was not documented in travelers as required by

procedure.

In their December 21, 1992, Reply to a Notice of Violation, the

licensee stated that corrective actions included a comparison

between the two applicable databases to determine if the M&TE uses

associated with unreviewed calibration failures were evaluated and

corrected as required.

In August 1992, anew procedure for Maintenance division root

cause evaluations was issued.

Procedure S0123-I-1.42

"Maintenance Division Experience Reports (MDERs) u was issued to

require formal RCE training for personnel performing RCEs.

Formal

training in the conduct of root cause evaluations for Maintenance

personnel performing MDERs was conducted from June 1992 through

October 1992.

In addition to the corrective actions mentioned above, the

licensee evaluated* their sampling techniques used when performing

audits to determine why the problems noted by the inspector had

not been identified during the audit. Action was taken to provide

more balanced samples*. This was accomplished by providing

additional training to all QA Auditors based on the results of the

evaluation.

This item is closed.

d.

(Cl osed)

Vi ol ati on

(50-36192-3402).

Fail re

o Adhere

o REP

Reg ui

rements."I

On December 17, 1992, the inspector observed performance of a

quarterly 1ST test on Unit 2 high pressure safety injection pump

2P017.

The inspector noted that the engineer and his supervisor

22

crossed radiological boundaries by reaching into, and touching,

objects within a contaminated area. Neither individual was

wearing the required protective clothing. These actions were

contrary to station procedure S0123-VII-9.9,

TCN 11-3, "Radiation

Exposure Permit (REP) Program."

The licensee's corrective actions included a commitment to develop

specific guidance for engineers working with components within

contaminated areas.

REP 502, "Minor Maintenance Inservice Test

Support," was developed to allow system encineers authorization to

reach into contaminated areas while perforring pump ISTs.

The

inspector verified that all affected personnel had been trained on

REP 502. This item is closed.

13.

Exit Meeting

On August 2, 1993, an exit meeting was conducted with the licensee

representatives identified in Paragraph 1. The inspectors summarized

the inspection scope and findings as described in the Results section of

this report.

The licensee acknowledged the inspection findings and noted that

appropriate corrective actions would be implemented where warranted.

The licensee did not identify as proprietary any of the information

provided to or.reviewed by the inspectors during this inspection.

23