ML070640155

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IR 05000285-06-018; on 10/10/2006 - 02/13/2007; for Fort Calhoun Station; Other Activities
ML070640155
Person / Time
Site: Fort Calhoun Omaha Public Power District icon.png
Issue date: 03/02/2007
From: Anton Vegel
NRC/RGN-IV/DRP
To: Ridenoure R
Omaha Public Power District
References
EA-07-047 IR-06-018
Download: ML070640155 (30)


See also: IR 05000285/2006018

Text

March 2, 2007

EA-07-047

R. T. Ridenoure

Vice President

Omaha Public Power District

Fort Calhoun Station FC-2-4 Adm.

P.O. Box 550

Fort Calhoun, NE 68023-0550

SUBJECT:

FORT CALHOUN STATION - NRC BASELINE INSPECTION

REPORT 05000285/2006018

Dear Mr. Ridenoure:

On February 13, 2007, the U.S. Nuclear Regulatory Commission (NRC) completed an

inspection at your Fort Calhoun Station. A preliminary finding was discussed on December 21,

2006, with Mr. Jeff Reinhart, Site Director, and other members of your staff. After additional

in-office review, a final exit meeting was conducted on February 13, 2007, with Mr. Reinhart and

other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

Specifically, the inspectors reviewed the circumstances surrounding a containment spray valve

that was incorrectly installed on May 11, 2005. The inspectors reviewed selected procedures

and records, observed activities, and interviewed personnel.

As described in Section 4OA5.5 of this report, inadequate Maintenance work instructions

contributed to the improper configuration of containment spray header isolation Valve HCV-345.

Specifically, the lack of detailed instructions or independent verifications, in steps for a

maintenance procedure performed during the Spring 2005 refueling outage, resulted in the

valve disk being installed improperly. This failure resulted in a condition where the actual

position of the valve was nearly opposite of the indicated position. Additionally, your staff failed

to identify the condition during postmaintenance testing. Consequently, this latent degraded

condition existed for an entire operating cycle, approximately 454 days, until the condition

revealed itself during the start of the Fall 2006 refueling outage. Based on review of

circumstance related to this abnormal condition the NRC identified an apparent violation of

10 CFR Part 50, Appendix B Criterion V, Instructions, Procedures, and Drawings for failure to

prescribe adequate procedures for maintenance and testing. The finding was characterized as

an apparent violation and was preliminarily determined to have low to moderate (White) safety

significance.

The condition did not represent an immediate safety concern at the time of discovery due to the

plant being in a shutdown condition where the containment spray system was not required.

The valve was reinstalled in a correct manner shortly after its condition was discovered, and

prior to restart of the unit.

Omaha Public Power District

- 2 -

Regarding the preliminary characterization of the finding as an issue of low to moderate (White)

safety significance, the NRC made this risk determination based upon review of the best

available information at the conclusion of inspection activities. The preliminary risk

determination is included as Attachment 2 to this report. We acknowledge that there are

differences between the NRC risk assessment and those performed by your staff. The final

resolution of this finding will convey the importance to safety by assigning the corresponding

color (i.e., Green - a finding of very low safety significance; White - a finding with some

increased importance to safety, which may require additional NRC inspection; Yellow - a finding

with substantial importance to safety that will result in additional NRC inspection and potentially

other NRC action; Red - a finding of high importance to safety that will result in increased NRC

inspection and other NRC action). This finding appears to have increased safety significance

because it represented a potential to create a flow diversion from the reactor coolant system

during accident conditions. This finding is being considered for escalated enforcement action in

accordance with the NRC Enforcement Policy. The current Enforcement Policy is included on

the NRCs Web site at www.nrc.gov/OE.

Before we make a final decision on this matter, we are providing you an opportunity to

(1) present to the NRC your perspectives on the facts and assumptions that were used by the

NRC to arrive at the finding and its significance at a Regulatory Conference or (2) submit your

position on the finding to the NRC in writing. In either case, to support our final significance

determination, please provide your assessment of the risk significance of this issue. The

assessment should include key assumptions and results of your estimates of changes to the

core damage frequency and large early release frequency. Additionally, your assessment

should include the following:

1)

Your evaluation of the frequency of initiating events that can result in flow

diversion from the reactor coolant system through Valve HCV-345 when the

shutdown cooling system is placed in service.

2)

Your evaluation of operator response to indications of a loss of reactor coolant

system inventory, success paths available to prevent core damage, and

perspectives on human reliability analysis for these scenarios.

3)

Your evaluation of any contribution to the risk significance of this issue from

external event initiators.

4)

Any other detailed technical information or analyses you believe are important to

support an overall risk assessment of the subject issue.

If you request a Regulatory Conference, it should be held within 30 days of your request, and

we encourage you to submit supporting documentation at least one week prior to the

conference in an effort to make the conference more efficient and effective. If a Regulatory

Conference is held, it will be open for public observation, and will require Public Notice. If you

decide to submit only a written response, your submittal should be sent to the NRC within

30 days of the receipt of this letter.

Please contact Jeffrey Clark at (817) 860-8147 within 10 business days of the date of the

receipt of this letter to notify the NRC of your intentions. If we have not heard from you within

Omaha Public Power District

- 3 -

10 days, we will continue with our significance determination and enforcement decision and you

will be advised by separate correspondence of the results of our deliberations on this matter.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for this inspection finding at this time. In addition, please be advised that the

characterization of the apparent violation described in the enclosed inspection report may

change as a result of further NRC review.

In accordance with Code of Federal Regulations, Title 10, Part 2.390 of the NRC's "Rules of

Practice," a copy of this letter and its enclosure will be available electronically for public

inspection in the NRC Public Document Room or from the Publicly Available Records (PARS)

component of NRC's document system (ADAMS). ADAMS is accessible from the NRC Web

site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

A. Vegel, Deputy Director

Division of Reactor Projects

Docket: 50-285

License: DPR-40

Enclosure:

NRC Inspection Report 05000285/2006018

w/attachments: Supplemental Information; Significance Determination Evaluation

cc w/enclosure:

Joe l. McManis, Manager - Licensing

Omaha Public Power District

Fort Calhoun Station FC-2-4 Adm.

P.O. Box 550

Fort Calhoun, NE 68023-0550

David J. Bannister

Manager - Fort Calhoun Station

Omaha Public Power District

Fort Calhoun Station FC-1-1 Plant

P.O. Box 550

Fort Calhoun, NE 68023-0550

James R. Curtiss

Winston & Strawn

1700 K Street NW

Omaha Public Power District

- 4 -

Washington, DC 20006-3817

Chairman

Washington County Board of Supervisors

P.O. Box 466

Blair, NE 68008

Julia Schmitt, Manager

Radiation Control Program

Nebraska Health & Human Services

Dept. of Regulation & Licensing

Division of Public Health Assurance

301 Centennial Mall, South

P.O. Box 95007

Lincoln, NE 68509-5007

Daniel K. McGhee

Bureau of Radiological Health

Iowa Department of Public Health

Lucas State Office Building, 5th Floor

321 East 12th Street

Des Moines, IA 50319

Omaha Public Power District

- 5 -

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (RJC1)

Senior Resident Inspector (JDH1)

Resident Inspector (LMW1)

Branch Chief, DRP/E (JAC)

Project Engineer, DRP/E (JCK3)

Team Leader, DRP/TSS (FLB2)

RITS Coordinator (MSH3)

DRS STA (DAP)

D. Cullison, OEDO RIV Coordinator (DGC)

ROPreports

FCS Site Secretary (BMM)

SUNSI Review Completed: _JAC__ADAMS: T YesG No Initials: _JAC___

T Publicly Available G Non-Publicly Available G Sensitive

T Non-Sensitive

R:\\_REACTORS\\FCS\\2006\\FC2006-18RP JDH.wpd

RIV:RI:DRP/E

SRI:DRP/E

C:DRP/E

SRA:DRS

D:DRS

LMWilloughby

JDHanna

JAClark

RLBywater

DDChamberlain

/RA/

/RA/

/RA/

/RA/

/RA/

2/21/07

2/21/07

2/21/07

2/22/07

2/23/07

DD:DRP sign

ACES

AVegel

MHaire

/RA/

/RA/

03/02/07

02/28/07

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

Enclosure

-1-

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-285

License:

DPR-40

Report:

05000285/2006018

Licensee:

Omaha Public Power District

Facility:

Fort Calhoun Station

Location:

Fort Calhoun Station FC-2-4 Adm.

P.O. Box 399, Highway 75 - North of Fort Calhoun

Fort Calhoun, Nebraska

Dates:

October 10 through February 13, 2007

Inspectors:

J. Hanna, Senior Resident Inspector

L. Willoughby, Resident Inspector

Approved By:

A. Vegel, Deputy Director, Division of Reactor Projects

Enclosure

-2-

SUMMARY OF FINDINGS

IR 05000285/2006018; 10/10/2006 - 02/13/2007; Fort Calhoun Station; Other Activities.

This report documents the NRCs inspection of circumstances related to one train of

containment spray being inoperable for 454 days. The baseline inspection activities were

conducted by resident inspectors. The inspection identified one finding whose preliminary

safety significance was determined to be low to moderate (White). The final significance of

most findings is indicated by their color (Green, White, Yellow, or Red) using NRC Inspection

Manual Chapter 0609, Significance Determination Process. The NRC's program for

overseeing the safe operation of commercial nuclear power reactors is described in NUREG-

1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC-Identified Findings and Self-Revealing Findings

Cornerstone: Mitigating Systems

TBD. The team identified an apparent violation of 10 CFR Part 50, Appendix B,

Criterion V, for the licensees failure to prescribe adequate procedures for

maintenance and testing on containment spray header isolation Valve HCV-345

which led to exceeding a Technical Specification allowed outage time. This

issue was self revealed on September 13, 2006, when reactor coolant water

issued from the containment spray header indicating that either Valve HCV-344

or Valve HCV-345 was not properly seated. The failure to perform adequate

maintenance and testing for this component resulted in one train of containment

spray being inoperable from May 11, 2005 to September 9, 2006, a period of

454-days. This exceeded the Technical Specification 2.4(2) allowed outage time

of 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the reactor is critical.

The issue was more than minor because it affected the equipment performance

attribute of the Mitigating System Cornerstone due to the impact on availability

and reliability of the containment spray system. The finding was preliminarily

characterized under the significance determination process as having low to

moderate safety significance (White) because one train of containment spray

was left in a condition contrary to its design and may have represented a bypass

flow path from the reactor coolant system during an accident condition. This

condition was entered into the Omaha Public Power Districts corrective action

program as Condition Report 200604627. Valve HCV-345 was repaired by the

licensee and is no longer safety concern. The finding has a crosscutting aspect

in the area of human performance, specifically resources, in that complete and

accurate procedures and work packages were not provided (Section 4OA5.5).

B.

Licensee-Identified Violations

None.

Enclosure

-3-

REPORT DETAILS

4.

OTHER ACTIVITIES

4OA5 Other Activities

1.

Background of Maintenance History

During the Spring 2005 Refueling Outage, Omaha Public Power District (OPPD)

performed work on the containment spray header isolation Valves HCV-344(A Header)

and HCV-345 (B Header) to address inconsistent operation identified during previous

testing. On three separate occasions Valve HCV-345 was removed from the system,

disassembled, reassembled, and returned to the system.

The function of the containment spray system is to limit the containment pressure rise

and reduce the leakage of airborne radioactivity from the containment following a

loss-of-coolant accident (LOCA) by providing a means for cooling the containment. This

system reduces the leakage of airborne radioactivity by effectively removing radioactive

particulates from the containment atmosphere. Pressure reduction is accomplished by

spraying cool, borated water into the containment atmosphere, which provides a means

for cooling the containment atmosphere. Heat removal is accomplished by recirculating

and cooling the water through the shutdown cooling heat exchangers. The system is

independent and redundant to the containment air cooling and filtering system.

Removal of radioactive particulates is accomplished by spraying water into the

containment atmosphere. The particulates become attached to the water droplets,

which fall to the floor and are washed into the containment sump.

During the Fall 2006 Refueling Outage, the licensee inspected the valve seat rings, in

part, to determine why reactor coolant water had leaked past the valve and had filled the

spray headers inside containment. While performing this maintenance, the system

engineer determined that the valve disk for Valve HCV-345 was installed nearly

90 degrees out of alignment. Actual valve position, while the valve was in this condition,

was nearly opposite of the remotely indicated position. The resultant effect would be

that if the valve indicated shut (the normal position of the valve) it would in fact be

approximately 66 percent open. Conversely, if the valve received a valid demand signal

to open (the safety position of the valve), it would be approximately 80 percent shut.

The time line below describes the major events and the maintenance history that

resulted in Valve HCV-345 being installed incorrectly and not discovered until

October 2006.

February 26, 2005

Refueling Outage 22 started.

March 17, 2005

Valves HCV-344 and HCV-345 removed from service and

repacked per Work Order (WO) 178429-04 (1st occurrence).

March 25, 2005

Valves HCV-344 and HCV-345 reinstalled in the system.

Enclosure

-4-

May 3, 2005

Valves HCV-344 and HCV-345 removed from service and

repacked per WO 205692-01 (2nd occurrence).

May 6, 2005

Valves HCV-344 and HCV-345 are reinstalled in the system.

May 7, 2005

Postmaintenance test of Valve HCV-345 identified that the valve

did not stroke smoothly. Additionally, the drive shaft was

protruding due to an incorrectly installed split ring retainer from

the second installation, which prevented reinstallation of the cover

plate.

May 9, 2005

Valve HCV-345 removed from service per WO 205692-01

(3rd occurrence). Improperly installed split ring retainer corrected

and valve reinstalled in the system. During work the incorrect

orientation between the drive shaft and the ball was introduced.

May 11, 2005

Work Order 205692 is completed and Valve HCV-345 returned to

service.

May 30, 2005

Criticality achieved following Refueling Outage 22 and the unit

recommences power operation.

June 4, 2005

Outage is started to replace degraded seals on Reactor Coolant

Pumps A and B, which may have represented an opportunity to

identify the incorrectly installed valve.

June 13, 2005

Criticality achieved following reactor coolant pump seal

replacement outage and the unit recommences power operation.

April 29, 2006

Outage is started to replace a degraded seal on Reactor Coolant

Pump D, which may have represented an opportunity to identify

the incorrectly installed valve.

May 6, 2006

Criticality achieved following reactor coolant pump seal

replacement outage and the unit recommences power operation.

September 9, 2006

Refueling Outage 23 started.

September 13, 2006 Reactor coolant water issues from the containment spray

headers.

October 5, 2006

Work Order 234358-01 is processed to replace the seat ring on

Valve HCV-345.

October 6, 2006

Valve HCV-345 is removed from the system.

October 10, 2006

System Engineer identified Valve HCV-345 assembled incorrectly

and Condition Report 200604627 is written.

Enclosure

-5-

2.

Cause Determination

The inspectors reviewed the accuracy and thoroughness of the licensee cause

determination as represented in the lincesees Root Cause Analysis Report, Violation of

Technical Specification 2.4.(1)a.iv. The Reactor Was Made Critical without the

Minimum Required Operable Components.

The HCV 345 containment spray header isolation valve has a Fisher Type 657-8

diaphragm actuator and a Fisher Type U-1009 internal component including a Vee-Ball

disk within the valve. The disk is a wedge-shaped cross-section spanning an arc of 101

degrees. Along the disks axis of rotation is a drive shaft that extends through the valve

packing. On one end of the drive shaft are 16 splines that connect the drive shaft to a

lever arm. The arm is pinned to a rod that is driven by the air-operator. In this manner,

the vertical motion of the air diaphragm and valve shaft are converted to rotational

motion of the ball disk, which should either allow or block flow. Proper operation of the

valve depends upon two critical orientations: (1) the position of the Vee-Ball disk

relative to the splined drive shaft, and (2) the position of the drive shaft to the lever arm.

During the Spring 2005 refueling outage, maintenance was performed on Valve

HCV-345 three times in accordance with Procedure PE-RR-VX-0401S, Inspection and

Repair of Fisher 300U/300UR Control Valves, Revision 2. The procedure directed

maintenance personnel to mark the valve shaft to ensure proper alignment when

reassembled. The first activity repacked the valve, and while it initially passed its

pressure test, the packing started leaking the following day. The licensee then decided

to install a different style of packing material. On the second disassembly to install the

new packing, the split ring retainer was installed incorrectly. This prevented the drive

shaft from being fully inserted into the Vee-Ball disk and necessitated a third

disassemble of the valve. During the third and final disassembly/reassembly, the drive

shaft was inserted into the Vee-Ball disk without ensuring that the orientation matched

that found during disassembly. This resulted in the actual position of the valve being

nearly opposite of the indicated position. Following reassembly and completion of the

work package, Valve HCV-345 was returned to service.

The licensee identified that two failures had occurred. The first was that Valve HCV-345

was installed incorrectly. The licensee identified that the maintenance

Procedure PE-RR-VX-0401S, Inspection and Repair of Fisher 300U/300UR Control

Valves, Revision 2 allowed flexibility of performing selected portions of the procedure

and did not specify risk important steps that could impact final valve alignment. This

was the root cause of the incorrect assembly. A contributing cause was that the

maintenance personnel who annotated the step as not applicable, did not recognize

the importance of proper alignment between the drive shaft and disk, or believed

(incorrectly) that installing the drive shaft with the packing box achieved the same result.

The second failure that was identified by the licensee was that postmaintenance testing

failed to identify the incorrect assembly. The licensee determined that maintenance

personnel had relied on an inadequate procedure without detailed acceptance criteria or

verifications to ensure proper valve operation. This was the root cause as to why the

postmaintenance test failed to identify the incorrect assembly. A contributing cause was

Enclosure

-6-

that misleading markings may have been used to assess the valve position, as opposed

to direct observation of the ball disk. Specifically, the many numerous match marks on

the valve may have been confusing to the maintenance personnel.

The inspectors concluded that the causes identified by the licensee appeared correct

and were achieved through a rigorous review of the circumstances surrounding the

event.

3.

Corrective Actions Taken Following Discovery of Condition

Following discovery of the misaligned valve condition, the licensee instituted or had

planned a number of corrective actions including:

Revised Procedure PE-RR-VX-0401S, Inspection and Repair of

Fisher 300U/300UR Control Valves, to reference manufacturers index marks

and remove direction to add additional match marks during disassembly.

Revised Procedure PE-RR-VX-0401S, Inspection and Repair of

Fisher 300U/300UR Control Valves, to provide acceptance criteria on verifying

the valve open or closed as part of final reassembly and explicitly identify these

steps as postmaintenance testing.

Revised Procedure PE-RR-VX-0401S, Inspection and Repair of

Fisher 300U/300UR Control Valves, to change the format of the procedure to

allow partial performance such as during a packing replacement.

Revised Procedure PE-RR-VX-0401S, Inspection and Repair of

Fisher 300U/300UR Control Valves, to annotate risk-important steps (such as

verification of valve position, i.e., postmaintenance test) and include a second

verifier for these steps.

Identification of all safety related air operated ball and butterfly valves,

determination if any risk-important steps in the associated procedures required

annotation and second verification, and/or verified that adequate post-

maintenance testing existed with appropriate acceptance criteria. Inadequate

procedures were to be revised.

These corrective actions were scheduled to be completed on/before February 28, 2007.

The licensee also identified a number of enhancements that would not necessarily

correct the condition or prevent recurrence, but would improve the maintenance

program for these components. The inspectors noted that the following additional

actions related to the misaligned valve condition had been taken or were planned:

Evaluated the need for acquiring a mock-up of the HCV-345 valve for use in

training personnel.

Enclosure

-7-

Revised the Steamfitter Mechanic Training Program Master Plan to require Just-

In-Time Training prior to outages where shutdown cooling heat exchanger outlet

temperature control Valves HCV-341, HCV-344 or HCV-345 were going to be

disassembled. (Please refer to Section 4OA5.4 below for a discussion of extent

of condition and why these specific valves were identified).

Evaluated whether work on valves similar to Valve HCV-345 should be treated

as a separate training qualification.

Included lessons learned from this event in the applicable training lesson plan for

this model valve.

The inspectors found that the aforementioned corrective actions and enhancements

appeared to be technically acceptable and appropriate. Though the inspectors were

unable to predict with certainty the effectiveness of the corrective actions, the inspectors

verified that the specified actions were planned or had been performed by the licensee

at the completion of the inspection.

4.

Extent of Condition Review

The inspectors evaluated the licensees extent of condition review, specifically as it

related to maintenance of other similar valves. This evaluation was performed to ensure

that valves, or other components, that might have been subject to the same failure

mechanism, were identified and corrected. The licensee identified three factors or

precursors that contributed to the incorrect assembly of the valve. These included:

Procedures that allowed performing certain steps for flexibility and to support

differing work scopes.

Risk important steps were not annotated in the procedures to provide a barrier

when selecting steps to support a specific task.

Equipment allowing alternate orientations for assembly (e.g., multiple splines on

a shaft rather than a keyway, which would permit only one configuration).

The licensee reviewed maintenance procedures and components where all of the

aforementioned elements might exist and lead to a similar failure. The licensee

concluded that there was a low probability of these elements existing with respect to

other components. Further, only three valves were identified as having a similarly

designed shaft with multiple splines: Valves HCV-341, HCV-344, or HCV-345.

Maintenance similar to that performed on Valve HCV-345 had been performed on

Valve HCV-344 during the Spring 2005 refueling outage. On October 12, 2006, the

licensee verified by direct visual inspection that Valve HCV-344 was installed correctly.

A review of maintenance history records showed that Valve HCV-341 had never been

removed from the system. Additional proof that Valve HCV-341 was correctly aligned

was that this component was used to align the shutdown cooling system for continuous

cooling of the core during the most recent refueling outage.

Enclosure

-8-

The licensee also reviewed the extent of condition for the failure of the post-

maintenance test to identify the incorrect assembly. Specifically, maintenance practices

were reviewed to determine if a successful postmaintenance test could be challenged by

the failure of a single individual performing a risk important step. The licensee

concluded that a concern existed, which was limited to the three valves mentioned

above, nonsafety related pumps, and air operated ball and butterfly valves that are not

containment isolation valves. The licensee developed corrective actions to address the

extent of condition concern. (Please refer to Section 4OA5.3 of this report for a full

description).

The inspectors reviewed the completed work orders on Valves HCV-344 and HCV-341

to ensure that during the most recent work on the components that the same failure

mechanism was not introduced. The inspectors concluded that the licensees extent of

condition reviews were adequate to ensure that similar conditions did not exist

elsewhere in the plant.

5.

Maintenance Program

a.

Inspection Scope

The inspectors reviewed the licensees program for maintenance and inspection of

pneumatically operated ball or butterfly valves, particularly as it related to the

misalignment of Valve HCV-345 internals. The inspectors also examined the

inspection/assessment techniques, scope, periodicity, and a sample of past inspection

results. These reviews were conducted in order to assess the appropriateness of

assigned postmaintenance testing for the scope of work performed.

b.

Findings

Introduction. An apparent violation of 10 CFR Part 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings, was identified for the licensees failure to

prescribe adequate procedures for maintenance and testing on containment spray

header isolation Valve HCV-345, which led to exceeding a Technical Specification

allowed outage time. This issue was self-revealed on September 13, 2006, when

reactor coolant water issued from the containment spray headers indicating that either

Valve HCV-344 or HCV-345 was not properly seated. The failure to prescribe adequate

procedures for maintenance and testing for this component resulted in one train of

containment spray being inoperable from May 11, 2005 to September 9, 2006, a period

of 454-days. This exceeded the Technical Specification 2.4(2) allowed outage time of

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> when the reactor is critical.

Description. On September 9, 2006, the licensee shutdown the plant in order to

commence Refueling Outage 23. On September 11, 2006, the licensee placed the

shutdown cooling system in service to maintain cooling to the core. With this system in

service, the two header isolation valves should prevent reactor coolant system water

from entering the containment spray headers. On September 13, 2006, reactor coolant

water issued from the containment spray headers indicating that either Valves HCV-344

or HCV-345 were leaking. The licensee initiated work requests to evaluate the seat

Enclosure

-9-

rings of Valve HCV-345. On October 10, 2006, a system engineer identified that the

valve was assembled incorrectly and Condition Report 200604627 was written.

The inspectors identified several weaknesses in the maintenance and testing of

Valves HCV-344 and HCV-345. Specifically, (1) though it was impractical to flow

borated water to the containment spray headers following maintenance, these valves

could have been tested using alternate means, (2) no independent verifications were

performed during either the maintenance or subsequent testing, (3) the maintenance

procedure allowed the flexibility to mark steps as Not Applicable, and (4) the procedure

did not explicitly state which steps were de facto required postmaintenance testing and

the importance of performing them correctly.

The inspectors determined that the postmaintenance testing performed following valve

disassembly, packing adjustment and reassembly was inadequate to identify the

misalignment of the valve internals. The postmaintenance testing requirements in

Procedure PE-RR-VX-0401S, Inspection and Repair of Fisher 300U/300UR Control

Valves, Revision 2, specified actions such as calibration of the valve actuator and

performance of a valve actuator test. However, these steps would not have detected

the condition that was present (i.e., valve internals installed backwards). The licensee

relied on the aforementioned procedure to perform both the maintenance and

postmaintenance testing without detailed acceptance criteria or independent

verifications. The inspectors determined that the failure to have an adequate

postmaintenance test constituted an apparent violation of NRC requirements.

Analysis. The inspectors assessed this issue using the Significance Determination

Process (SDP). The inspectors concluded that the licensees failure to prescribe

adequate proceures for maintenance and postmaintenance testing was reasonably

within the licensees ability to foresee and correct, should have been prevented and thus

constituted a performance deficiency. The failure to prescribe an adequate procedure

for a postmaintenance test on Valve HCV-345 resulted in Containment Spray Train B

being inoperable from May 11, 2005, to September 9, 2006, a period of 454-days. The

issue was more than minor because it affected the equipment performance attribute of

the Mitigating System Cornerstone due to the impact on availability and reliability of the

containment spray system. This finding has a crosscutting aspect in the area of human

performance, specifically resources, in that complete and accurate procedures and work

packages were not provided.

Though this condition was introduced while the plant was shutdown and likewise was

discovered during a shutdown condition, the inspectors concluded that the condition

should be reviewed using Inspection Manual Chapter 0609, Appendix A, Determining

the Significance of Reactor Inspection Findings for At-Power Situations. This decision

was based on the condition existing during and having safety significance (i.e., an

adverse affect on systems responding to an accident) while at power.

Details of the Phase 2 evaluation and a Phase 3 SDP analysis are documented in

Attachment 2. The preliminary results were that the finding was of low to moderate

safety significance. The most significant contribution to the increase in risk involved

accident scenarios where shutdown cooling was placed in service when containment

Enclosure

-10-

sump recirculation was not required. This would result in a flow diversion from the

reactor coolant system through the containment spray header that required operators to

diagnose and act upon.

Enforcement:

10 CFR Part 50, Appendix B, Criterion V, Instructions, Procedures, and Drawings,

states, in part, that activities affecting quality shall be prescribed by documented

instructions, procedures, or drawings of a type appropriate to the circumstances and

shall be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to this, the licensee failed to develop appropriate instructions or procedures for

maintenance activities, and post maintenance testing, on Valve HCV-345. This failure

resulted in one train of containment spray being inoperable from May 11, 2005 to

September 9, 2006, a period of 454 days. This item has been entered into the

licensees corrective action program as Condition Report 20064627. Pending

determination of final safety significance, this finding is identified as an apparent

violation (AV)05000285/2006018-01, Violation of 10 CFR 50, Appendix B Criterions for

Failure to Prescribe Adequate Procedures for Maintenance and Testing.

(Section 40A5.5)

6.

Operability of Valve HCV-345 Following Repair Activities

The inspectors reviewed the documented test data, including photographs of the as-left

condition of the valve, to verify that the testing was complete and that the equipment

was able to perform the intended safety function. No issues or concerns were identified.

7.

Potential Common Failure Modes and Generic Safety Issues

The inspectors performed searches of operating experience (OE) databases and other

sources. The intent was to identify OE reports of similar problems, both within and

outside of the nuclear industry. Through a review of the licensees condition reporting

system, the inspectors identified one instance of relevant information that was not

discovered by the licensee prior to the time that the condition was introduced in the

Spring 2005 outage. This involved a Fisher Information Notice 2002-01, Fisher Type

SS-84 Vee-Ball Seat Leakage Information, which described a possible misalignment

of the internal components. Specifically it stated, If the connections between the lever

and valve shaft or the valve shaft and Vee-Ball are not correctly aligned, there is a

possibility that the Vee-Ball will not be correctly positioned to provide shutoff when the

actuator strokes to the closed position. This OE had been reviewed by the licensee

and deemed not applicable because it was a slightly different valve model. The

inspectors considered that the design of the components were similar to the U model

Fisher valves installed at Fort Calhoun Station. The inspectors found no other examples

of internal OE.

With respect to external OE, the inspectors identified three instances where Fisher

Vee-Ball valves were incorrectly assembled at other nuclear facilities. Two of these

occurrences, which happened during the 2004/2005 time frame, had also been

Enclosure

-11-

identified by the licensee through the reviews performed by the Root Cause Analysis

team responding to this event. For these two items, the licensee had entered the

information into their OE tracking system and assigned review of those items to

engineering personnel. In reviewing both OE items, the engineering staff incorrectly

concluded that the information was not relevant to the Fort Calhoun Station.

The inspectors found additional OE in the form of an Event Report from Vogtle Electric

Generating Plant - Unit 2. As described in Licensee Event Report 05000425/1989-031-

00, Heater Drain Tank Valve Reassembly Error Leads to Turbine/Reactor Trip, an

error involving reassembly of the valve led to the transient. The cause was described as

follows:

Since the valve was not to be removed from the line, the maintenance crew that

removed the actuator had match-marked the valve in the open position. A

second maintenance crew had rebuilt the actuator and reinstalled it using the

maintenance match marks. A third crew had tested the valve operation and

reinstalled the position indication to match the actuator piston position. After the

reactor trip, the maintenance match marks were checked and were found to

disagree with the valve position indication by 90º. It was then realized that a

reassembly error had occurred in that the actuator piston had been in the closed

position when the actuator was reinstalled . . .

The inspectors did not identify any documents that had evaluated this condition at the

Fort Calhoun Station. Though the inspectors noted that it would not have been

reasonable to expect a licensee to review all Licensee Event Reports issued from other

facilities for potential applicability, this event represented another example of improper

assembly of Fisher valves that had safety consequences.

The inspectors concluded that the licensee had missed multiple opportunities, some of

which were both recent and relevant, to identify the vulnerability to the possible

misalignment of Fisher valve internals.

4OA6 Meetings, Including Exit

A preliminary finding was discussed on December 21, 2006, with Mr. Jeff Reinhart, Site

Director, and other members of your staff. After additional in-office review, a final exit

meeting was conducted on February 13, 2007, with Mr. Reinhart and other members of

your staff. The inspectors confirmed that proprietary information was not provided

during the inspection.

Attachment

A1-1

ATTACHMENT 1: SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

D. Bannister, Plant Manager

B. Blome, Planning Manager

G. Cavanaugh, Supervisor, Regulatory Compliance

T. Dukarski, Manager, Alternate Chemistry

T. Giebelhausen, Probablistic Risk Analysis Tech

A. Hackerott, Supervisor, Probablistic Risk Analysis

A. Hansen, Operating Experience Coordinator

R. Haug, Manager, Radiation Protectio

J. Herman, Manager, Engineering Programs

R. Hohansen, Acting Division Manager, Nuclear Support

J. Kellams, Acting Corrective Action Program

J. McManis, Manager, Licensing

K. Melstad, Supervisor, maintenance

T. Nellenbach, Manager Operations

J. Reinhart, Site Director

C. Schaffer, Nuclear Safety Review Group

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

05000285/2006018-01

AV

Violation of 10 CFR part 50, Appendix B, Criterion V

Instructions Procedures, and Drawings for failure to

Prescribe Adequate Procedures Maintenance and Testing.

(Section 4OA5.5)

LIST OF DOCUMENTS REVIEWED

USAR Section 6.0, Engineered Safeguards

USAR Section 9.3, Shutdown Cooling

Preventative Maintenance records for Valves HCV-344 and HCV-345

Procedure PE-RR-VX-0401S, Inspection and Repair of Fisher 300U/300UR Control Valves,

Revision 2

Procedure OP-ST-SI-3002, Safety Injection System Category A, B, and C Valve Exercise

Test, Revision 24

Attachment

A1-2

Procedure OP-ST-VX-3019, Safety Injection System Remote Position Indicator Verification

Surveillance Test, Revision 15

Work Order 00205692-01, Rebuild/Replace Packing - HCV-345"

Work Order 00229974-01, Replace IA-HCV-341-B1 Tie-Wraps with Tube Clamps

Work Order 00200552-01, HCV-341: Clean Boric Acid from Affected Areas

Work Order 00206035-01, Rebuild/Replace Packing - HCV-344"

Root Cause Analysis Report, Violation of Technical Specification 2.4.(1)a.iv The Reactor Was

Made Critical without the Minimum Required Operable Components

Reactor Plant Event Notification Worksheet for Event #42512, dated April 19, 2006

Reactor Plant Event Notification Worksheet for Event #42896, dated October 10, 2006

Licensee Event Report 05000285/2006-005, Faulty Maintenance Renders One Train of

Containment Spray Inoperable

Condition Reports:

CR 200604627

CR 200604695

CR 200605311

CR 200605315

CR 200605348

CR 200605350

CR 200605352

Maintenance Rule Cause Determination 08190610 for Condition Report 200604695

System Training Manual, Volume 15, Emergency Core Cooling System, Revision 35

LIST OF ACRONYMS

CFR

Code of Federal Regulations

CR

Condition Report

LOCA

Loss-of-Coolant Accident

OE

operational experience

NRC

Nuclear Regulatory Commission

SDP

Significance Determination Process

USAR

Updated Safety Analysis Report

WO

work order

Attachment

A2-1

ATTACHMENT 2:

SIGNIFICANCE DETERMINATION EVALUATION

Significance Determination Process Phase 2 Risk Estimation:

In accordance with Manual Chapter 0609, Appendix A, Attachment 1, User Guidance

for Determining the Significance of Reactor Inspection Findings for At-Power

Situations, the inspectors evaluated the subject finding using the Risk-Informed

Inspection Notebook for Fort Calhoun Station, Revision 2 (The Phase 2 Notebook).

The inspectors and a senior reactor analyst discussed the applicability of worksheets in

the Phase 2 Notebook. Modifications were required. In particular, the licensee's risk

analysis staff identified a potentially significant initiating event involving an interfacing

system LOCA (ISLOCA) from failure of a reactor coolant pump (RCP) seal cooler. The

senior reactor analyst determined that this initiator could be modeled by using the

ISLOCA worksheet of the Phase 2 Notebook with a transfer to the SLOCA worksheet.

Therefore, a "Modified" Phase 2 SDP risk estimation was performed as described

below.

Modified Significance Determination Process Phase 2 Risk Estimation:

Risk Estimation with Containment Spray (CS) Train B Not Functional

The following assumptions were made:

Containment Spray (CS) Train B was not functional with the internals of

Valve HCV-345 installed incorrectly. The licensee's Root Cause investigation

determined that with closed indication, the valve was approximately 66 percent

open; and, with open indication, the valve was only about 20 percent open. For

this analysis, no containment temperature or pressure control credit was given

for any reduced flow through the partially-open valve. The licensee

subsequently performed a thermal-hydraulic analysis to demonstrate success of

the Train B CS system with degraded flow from a 20-percent open valve. This

will be addressed later.

The exposure time was determined by identifying the length of time the CS

system was required to be operable from May 11, 2005, when Valve HCV-345

was assembled incorrectly, to October 10, 2006, when the condition was

discovered. The resulting exposure time was 454 days. Therefore, the greater

than 30 days exposure window was used in Table 1 of the SDP Notebook to

determine the Initiating Event Likelihood (IEL).

Table 2, "Initiators and System Dependency," of the Phase 2 Notebook required

that all Initiating Event Scenarios be evaluated except for Steam Generator Tube

Rupture (SGTR), Anticipated Transient Without Scram (ATWS), and Loss of

Raw Water (LRW). The inspectors and analyst determined that exclusion of

SGTR was a typographical error in the Phase 2 Notebook because CS was a

credited safety function for mitigating a SGTR. Therefore, the SGTR worksheet

was solved.

Attachment

A2-2

Train B of CS was associated with 125 VDC Bus 2. Therefore, when the Loss of

125 VDC Bus 1 (LCDBUS1) worksheet was solved, the remaining mitigation

capability for the CS function was zero. When the Loss of 125 VDC Bus 2

(LDCBUS2) worksheet was solved, the sequence involving the CS function was

included at its base-case value to reflect the reduction in system reliability.

The Component Cooling Water (CCW) system provides cooling water to the

Containment Air Cooling and Filtering System. This CCW flow is divided among

four cooling units in two trains. CCW is supplied to the VA-1A and VA-1B

cooling coils of the Containment Cooling and Filtering Units (VA-3A and VA-3B)

and the VA-8A and VA-8B cooling coils of the Containment Cooling Units

(VA-7C and VA-7D). The containment pressure and temperature control safety

function provided by the Containment Air Cooling and Filtering System is

redundant to the CS system.

The Raw Water (RW) system is a backup for most of the components supported

by the CCW system, including the containment cooling coils. However, the

licensee does not credit RW for success of containment cooling. The lower

pressure of the RW system when supplied to the containment coolers may result

in two-phase flow and inadequate heat removal capabilities. Therefore, RW

backup to the containment cooling coils was not credited for success of

containment temperature and pressure control but it was credited for successful

cooling of the ECCS pumps and the SDC heat exchangers.

The CCW system provides cooling to the reactor coolant pump (RCP) thermal

barrier and integral heat exchanger for controlled bleedoff flow seal cooling. The

licensee's system training manuals state that on an RCP seal cooler heat

exchanger tube rupture, an ISLOCA can occur in the auxiliary building due to

transfer of reactor coolant to the CCW system. This high-pressure fluid was

expected to rupture the CCW surge tank and cause loss of CCW function. In

this event, operators are instructed to close the CCW containment supply and

return isolation valves to the RCP seal coolers (HCV-438A/B/C/D). Closure of

these valves would terminate the ISLOCA outside of containment but was

expected to result in a SLOCA inside of containment because of failure of the

150 psig (design pressure) CCW system piping. The licensee's PRA estimated

that the frequency of an RCP seal cooler tube failure was 3E-4/yr. Therefore,

the analyst modeled this event as equivalent to a SLOCA with IEL = 4. The

remaining mitigation capability credit for containment temperature and pressure

control was estimated as a single train system, represented by the remaining

functional CS Train A' (CNT = 2).

No credit was given for operator recovery of the failed CS Train B. Recovery of

the failed train required repair of HCV-345, which did not meet the acceptance

criteria for operator recovery credit.

An interface exists between the CS and low-pressure safety injection (LPSI)

systems because both systems can use the SDC heat exchangers. During a

normal shutdown and transition to SDC, operators enter containment and close

Attachment

A2-3

CS manual isolation Valves SI-177 and SI-178 to preclude SDC flow from

entering the CS headers and spraying the containment if leakage existed

through Valves HCV-344 or HCV-345. However, if an accident occurred that

involved operators initiating SDC prior to a recirculation actuation signal (RAS) in

accordance with Emergency Operating Procedure (EOP) Attachment 4, "SDC

Without RAS," the finding had the potential to create a flow diversion from the

RCS. The manual valves are not closed during implementation of Attachment 4.

Remotely-operated Valves HCV-344 and HCV-345 would be closed and relied

upon for providing isolation of SDC from the CS headers. When operators

initiated SDC, flow would be diverted from the RCS through the CS header and

unavailable for core cooling even though Valves HCV-344 and HCV-345 had

been closed. This flow diversion to the CS header is assumed to fail the SDC

function. However, the Phase 2 Notebook does not credit the SDC safety

function for mitigating any initiating events and is not evaluated further in

this Modified Phase 2 analysis. It will be addressed later.

Modified Phase 2 Analysis Results Internal Events:

Using the above assumptions, the Modified Phase 2 Analysis results for the non-

ISLOCA initiator worksheets are shown below.

SEQUENCE

IEL

REMAINING MITIGATION

CAPABILITY RATING

RECOVERY

CREDIT

RESULTS

TRANS-PCS-AFW-CNT

1

3+5+5

0

14

TPCS-AFW-CNT

1

3+5

0

9

SLOCA-CNT

3

5

0

8

SORV-BLK-CNT

4

2+5

0

11

MLOCA-CNT

4

4

0

8

LLOCA-CNT

5

4

0

9

LOOP-AIAFW-MDAFW-

CNT

2

3+2+5

0

12

SGTR-SHR-CNT

3

7+5

0

15

MSLB-MSIV2-AFW-CNT

3

2+5+5

0

15

SEQUENCE

IEL

REMAINING MITIGATION

CAPABILITY RATING

RECOVERY

CREDIT

RESULTS

LDCBUS1-AFW-CNT

3

2+2

0

7

LDCBUS2-AFW-CNT

3

5+4

0

12

LCCW-AFW-CNT

3

3+5

0

11

LCCW-SEAL-CNT

3

4+5

0

12

LCCW-RCPTRIP-CNT

3

3+5

0

11

Attachment

A2-4

LIA-AFW-CNT

2

3+5

0

10

The Modified Phase 2 analysis results for the RCP seal cooler ISLOCA initiator are

shown below.

SEQUENCE

IEL

REMAINING MITIGATION

CAPABILITY RATING

RECOVERY

CREDIT

RESULTS

SLOCA-CNT

4

2

0

6

Using IMC 0609, Appendix A, Attachment 1, Table 5, Counting Rule Worksheet, the

summation of the non-ISLOCA and the ISLOCA sequences is equivalent to one

sequence with a risk significance equal to 6. Therefore, the Modified Phase 2 SDP

Analysis result of the risk significance of this finding due to internal events is of low-to-

moderate safety significance (White).

Modified Phase 2 Analysis - Large Early Release Frequency (LERF)

In accordance with Manual Chapter 0609, Appendix A, Attachment 1, Step 2.6,

"Screening for the Potential Risk Contribution Due to LERF," the analyst reviewed the

core damage sequences to determine an estimate of the change in LERF caused by the

finding.

The analyst considered the RCP seal cooler failure with ISLOCA outside of containment

initiator to be part of the plant's baseline risk, up to the point of when the ISLOCA was

isolated to the containment. From that point, the event transferred to the SLOCA event

tree, which did not result in a sequence causing a change in LERF. The only other

sequence considered applicable for LERF was one SGTR sequence, but it was a

negligible contributor. Therefore, for the Modified Phase 2 SDP risk estimation this

finding was considered not significant with respect to an increase in LERF.

Modified Phase 2 Analysis - External Events

In accordance with Inspection Manual Chapter 0609, Appendix A, Attachment 1,

Step 2.5, "Screen for the Potential Risk Contribution Due to External Initiating Events,"

experience with using the Site Specific Risk-Informed Inspection Notebooks has

indicated that accounting for external initiators (fire, flooding, severe weather, seismic,

or others) could result in increasing the risk significance attributed to an inspection

finding by as much as one order of magnitude.

The Modified Phase 2 Analysis result met the criterion for consideration of risk

contribution due to external events (risk estimation increase greater than or equal to

1E-7 per year). Although the Phase 2 Notebook for Fort Calhoun Station does not

currently include external events, the analyst and inspectors qualitatively reviewed

external event applicability. The results of this review were that fire events may be

applicable. However, the fire events were limited to affecting the SDC function, which

was not evaluated in the Modified Phase 2 analysis. Therefore, the contribution due to

external events for the Modified Phase 2 analysis was assumed to be negligible and the

Attachment

A2-5

preliminary significance determination could be represented solely by the contribution

from internal events.

Consideration of Reduced CS Flow vs. Zero CS Flow on Success of CNT Function

(Modified Phase 2 Analysis with CS Train B Functional)

The licensee informed the analyst that the MAAP accident analysis code was used to

evaluate plant response to a severe accident using the as-found configuration (20-

percent open) of Valve HCV-345 with reduced CS flow. The results of these analyses

were documented in PRA Modeling Position White Paper CCF 107-001, Impact of the

HCV-345 Mis-Installation on Containment Performance During Severe Accidents. The

licensee concluded the as-found condition of Valve HCV-345 would provide sufficient

CS flow to mitigate a LLOCA, even with no containment coolers or CS flow from the

unaffected CS Train A. This analysis was not reviewed by NRC staff. However,

HCV-345 is a ball valve, and qualitatively would be expected to allow a significant

fraction of its fully-open flow even if it were only 20-percent open.

Assuming the licensees analysis was correct, the CS system would receive multi-train

credit when determining remaining mitigation capability credit for the CNT safety

function. This additional credit added a 1" to each of the sequence results obtained

above. Therefore, the Modified Phase 2 Analysis result for internal events was

equivalent to one sequence with a risk significance equal to 7, which is a Green result.

As described previously, the SDP Phase 2 Notebook did not include a means to assess

findings affecting the SDC safety function. This finding was determined to not only

affect the performance of CS, but also the performance of SDC if it was initiated in an

accident without a RAS. Therefore, a Phase 3 SDP Analysis was required to address

this impact.

Phase 3 SDP Analysis: Consideration of Additional Severe Accident Scenarios Involving

Initiation of SDC When a RAS Has Not Occurred

The licensee identified that a flow diversion path would be created from the RCS to the

CS header if SDC were placed in service without having closed the inside-containment

manual isolation valves. When Valve HCV-345 was closed by the control room

operator, it would have indicated closed but have remained 66 percent open. For

events that required the operators to initiate SDC when a RAS had not occurred, a flow

diversion from the RCS through the CS header would fail the SDC function. The

licensee's analysis is documented in a white paper, Severe Accident (PRA) Perspective

Regarding Improper Positioning of Containment Spray Header Isolation

Valve HCV-345."

The licensee performed a screening review to determine what initiating events were

likely to progress to SDC initiation without having previously resulted in a RAS. For

those events, the operators would be directed to implement EOP/AOP Attachment 4,

SDC Without RAS. The results of the screening review were:

For LLOCAs and MLOCAs, SDC will not be initiated prior to a RAS. Therefore,

Attachment

A2-6

they were excluded.

For SLOCAs with HPSI flow greater than 220 gpm, the licensees analysis

concluded that at the time the SDC suction valves were opened, HPSI flow was

already sufficient to prevent core damage with no additional operator actions.

For SLOCAs with HPSI flow < 220 gpm and for SGTR and MSLB/FWLB events,

the licensees analysis concluded that at the time the SDC suction valves were

opened, core damage would occur in 90 minutes if operators did not diagnose

the loss of inventory and take action to isolate the leak path. The licensee

determined that the frequency of these initiating events was 1.4E-2/year.

The licensee qualitatively screened out other initiating events from consideration.

They concluded it was improbable for other events to proceed to SDC without

RAS.

The analyst noted that EOPs to address other initiators (such as EOP-02, Loss of Off-

Site Power/Loss of Forced Circulation, and EOP-06, Loss of All Feedwater) contained

provisions to initiate SDC using EOP/AOP Attachment 4. Therefore, other initiators not

included in the licensee's assessment could add to the total risk. The analyst was not

able to verify the licensee's qualitative determination that the other initiators were not

probable.

The licensees analysis described the following evaluation for the severe accident

scenarios under consideration:

Once the operators had successfully achieved plant conditions to support

initiating SDC, they would begin to implement EOP/AOP Attachment 4. When

both SDC valves were opened from the RCS, the operators would be presented

with audible and visible cues that a loss of RCS inventory was occurring. Among

them were: pressurizer low level alarms and containment sump level alarms.

The crew would then diagnose that a loss of RCS inventory was taking place and

take action to terminate the inventory loss by closing a SDC suction valve.

Failure of both SDC suction valves to close due to common cause was

qualitatively considered in the licensees assessment but discounted. The

licensee concluded that should this occur, sufficient time was available to identify

and close another isolation valve, including manual valves. After terminating the

RCS inventory loss, heat removal could continue for an indefinite amount of time

using the steam generators. HPSI flow could be established if necessary.

The licensee performed a human reliability assessment to estimate the total human

error probability (HEP) for failing to diagnose the loss of inventory and act to stop it.

The licensees estimation used the NRCs SPAR-H Human Reliability Analysis Method

and is summarized as follows:

The licensee estimated that once the loss of inventory began, a maximum of

1 minute of delay time would exist prior to the visual and audible cues that a loss

of inventory was occurring. Then the licensee estimated that 1 minute would be

Attachment

A2-7

required to diagnose the problem and decide upon an action. Another 1 minute

was estimated for an operator to complete the required action to terminate the

loss of inventory. The total time available before core damage was 90 minutes.

The licensee assessed the SPAR-H performance shaping factors (PSF) for the

diagnosis and action components of this task, selected PSF multipliers, and

determined the task HEP without formal dependence as follows:

PSF

Diagnosis Multiplier

(Base = 0.01)

Action Multiplier

(Base = 0.001)

Available Time

Extra Time (0.1)

>=50x time required (0.01)

Stress

Nominal (1.0)

Nominal (1.0)

Complexity

Obvious Diagnosis (0.1)

Nominal (1.0)

Experience/Training

Nominal (1.0)

Nominal (1.0)

Procedures

Diagnostic/symptom oriented (0.5)

Nominal (1.0)

Ergonomics

Nominal (1.0)

Nominal (1.0)

Fitness for Duty

Nominal (1.0)

Nominal (1.0)

Work Processes

Nominal (1.0)

Nominal (1.0)

SUBTOTAL

5.0E-5

1.0E-5

TOTAL

6.0E-5

Based on additional discussions the analyst had with the licensee regarding the HRA,

the licensee confirmed that HPSI would be available as a mitigation option if the SDC

flow diversion path was not terminated. HPSI would likely have been operating, and

throttled at the time SDC was initiated. The licensee considered the above HRA for

diagnosis/action to terminate the diversion path to be a simplification. Additional

diagnoses/actions would have further complicated the HRA. However, the licensee

stated that during this scenario, Safety Function Status Checks would have been

performed. One of the checks includes monitoring pressurizer level and restoring as

necessary. Monitoring HPSI stop and throttle criteria is a floating step in the EOPs. The

licensee stated that this is why they considered a "Nominal (1.0)" multiplier appropriate

for the Procedures - Action PSF.

The senior reactor analyst reviewed the licensees assessment and concluded that

some changes to the PSF multipliers selected by the licensee were needed. Using

NUREG/CR-6883 as a reference, the following changes were made:

Changed the Available Time PSF multiplier for Diagnosis to Expansive Time

because the average time for diagnosis was 1 minute, the time available was

greater than twice the average time, and was greater than 30 minutes.

Changed the Stress PSF multipliers for Diagnosis and Action to High. The

Attachment

A2-8

analyst assumed that the task would be performed in a condition of higher-than-

nominal stress, with multiple unexpected alarms at the same time, and that the

consequences of the task represent a threat to plant safety.

Changed the Procedures PSF multiplier for Action to Incomplete. EOP/AOP

Attachment 4 did not contain instructions for what response action the operator

should take to complete the task. Therefore, no credit for procedures could be

given for this task.

The analysts revised HEP assessment was as follows:

PSF

Diagnosis Multiplier

(Base = 0.01)

Action Multiplier

(Base = 0.001)

Available Time

Expansive Time (0.01)

>=50x time required (0.01)

Stress

High (2.0)

High (2.0)

Complexity

Obvious Diagnosis (0.1)

Nominal (1.0)

Experience/Training

Nominal (1.0)

Nominal (1.0)

Procedures

Diagnostic/symptom oriented (0.5)

Incomplete (20.0)

Ergonomics/HMI

Nominal (1.0)

Nominal (1.0)

Fitness for Duty

Nominal (1.0)

Nominal (1.0)

Work Processes

Nominal (1.0)

Nominal (1.0)

SUBTOTAL

1.0E-5

4.0E-4

TOTAL

4.1E-4

The analyst requested peer review of the analysis by staff from the Office of

Nuclear Reactor Regulation. Some changes were proffered, particularly

involving the Procedures PSF multiplier for Action. The staff believed some

credit may be warranted for the Procedures PSF by crediting use of other

procedures (e.g., functional restoration procedures and initiation of emergency

core cooling). Although some reduction in the HEP would result from this

change, the operator actions would involve and require a diagnosis and action

approach different than the one explicitly analyzed here. This approach would

involve additional PSF multiplier changes for diagnosis and action that may

decrease available time, increase complexity, etc. Therefore, the staff

concluded the analyst's HEP assessment result was a reasonable estimate given

available information.

Phase 3 Analysis Conclusion for Severe Accident Scenarios Involving SDC to CS Flow

Diversion (Internal Events)

The increase in core damage frequency due to internal events associated with the

finding is estimated as the product of the initiating event frequency for events that result

in an RCS flow diversion when SDC is placed in service, times the HEP for the task of

Attachment

A2-9

diagnosing and terminating the loss of inventory.

The result using the licensees HEP estimate is:

1.4E-2/year * 6.0E-5 = 8.4E-7/year

The result using the analysts HEP estimate is:

1.4E-2/year * 4.1E-4 = 5.7E-6/year

Therefore, the preliminary significance of this finding due to the increase in core

damage frequency associated with internal events was determined to be of low to

moderate safety significance (White).

Phase 3 Analysis - External Events Assessment

The inspectors and senior reactor analyst qualitatively assessed the contribution due to

external initiators. The only contributor considered to potentially be significant was fire

scenarios. Valves HCV-344 and HCV-345 are on the licensee's safe shutdown

components list in the Fire Hazards Analysis. The valves are identified as having a

necessary function to close to prevent diversion of SDC flow through the CS headers.

The safe shutdown time line indicated that SDC would be established 13 hours1.50463e-4 days <br />0.00361 hours <br />2.149471e-5 weeks <br />4.9465e-6 months <br /> after a

fire event and therefore was not considered a time critical activity. The inspectors

determined that in a control room fire scenario, the licensee would be implementing

AOP-6, "Fire Emergency." AOP-6 identified the potential for spurious operation of

Valves HCV-344 and HCV-345 and proceduralized containment entry to close SI-177

and SI-178 prior to initiating SDC. In other fire scenarios, SDC would also be initiated

using normal system operating procedures which would specify containment entry to

close the manual isolation valves. Based on this discussion, the analyst considered that

fire events did not contribute to the risk significance of this finding. Other external

initiators were considered by the analyst to be negligible.

The licensee had not performed an assessment of external initiators at the time of this

analysis.

Phase 3 Analysis - LERF Assessment for Severe Accident Scenarios Involving SDC to

CS Flow Diversion

The increase in risk associated with LERF is considered if the increase in core damage

frequency is greater than 1E-7/year. Core damage sequences involving a SGTR

initiating event are important with respect to LERF and have a LERF multiplier of 1.

However, use of a LERF multiplier of 1 does not address that the SGTR sequences of

interest here would only include those where the SGTR was successfully mitigated to

the point of initiation of SDC. Therefore, the analyst believed the LERF multiplier would

be much less than 1. Following discussion with staff in the Office of Nuclear Reactor

Regulation, the analyst used a 0.1 LERF multiplier to estimate the significance of

Attachment

A2-10

sequences contributing to LERF.

To determine the contribution in risk due to LERF, the analyst used the frequency of

SGTR events from the licensee's PRA, multiplied times the HEP for SDC failure. Then,

this CDF for SGTR events was multiplied times the LERF multiplier to obtain the LERF

estimate.

For the licensees HEP estimate:

SGTR CDF = 5.91E-3/year * 6.0E-5 = 3.6E-7/year

With a LERF multiplier of 0.1, the increase in LERF is 3.6E-7/year * 0.1 =

3.6E-8/year

For the analysts HEP estimate:

SGTR CDF = 5.91E-3/year * 4.1E-4 = 2.4E-6/year

With a LERF multiplier of 0.1, the increase in LERF is 2.4E-6/year * 0.1 =

2.4E-7/year

Therefore, using the analyst's estimate, the risk significance of this finding with

respect to LERF is White because the result is greater than 1E-7/year.

Confirmatory Phase 3 Analysis Using the SPAR Model

Using the Fort Calhoun Station SPAR Model, Revision 3.31, the senior reactor analyst

attempted to independently model and quantify an increase in core damage frequency

due to the finding.

For simplicity, the analyst accepted the licensees assertion that degraded CS flow

through HCV-345 was sufficient for successful CS function. The ISLOCA initiator,

although it failed CCW and its containment cooling function, did not affect the

functionality of CS. The resulting LOCA inside of containment was assumed large

enough to require a RAS. Therefore, the RCP seal cooler failure and ISLOCA scenario

was eliminated from consideration.

Several of the initiating event trees in the SPAR model contained a top event for the

SDC function. The containment spray header isolation Valves HCV-344 and HCV-345

were included in the SPAR model for success of the CS function (required to open).

However, these valves were not included in the SPAR model for the SDC function

(required to close). Therefore, the SDC flow diversion path was not modeled in the

SPAR model. The analyst chose a SPAR model basic event that would fail the SDC

function as a surrogate for the need to model the flow diversion path. By inspection of

the initiating event trees and fault trees, the analyst determined failing the SDC heat

exchanger outlet valve HCV-341 closed would provide an acceptable surrogate for

modeling the SDC flow diversion scenario while allowing credit for high-pressure

injection and sump recirculation.

Attachment

A2-11

Basic Event SDC-AOV-CC-CLI, SDC Discharge AOV HCV-341, was set equal to

TRUE (failed closed). For a 1-year exposure time, the calculated importance was

1.0E-6. The top three core damage sequences all involved SGTR and represented

almost all of the total increase in risk. The next two sequences involved a transient and

a loss of all feedwater, but they were much lower in significance.

In conclusion, this confirmatory Phase 3 analysis using the SPAR model demonstrated

that the risk significance of this finding due to internal events was an increase in core

damage frequency of 1.0E-6/year. This met the threshold for a finding of low-to-

moderate safety significance (White). With respect to LERF, most of the contribution to

risk associated with this finding was the result of SGTR sequences. Therefore, the

analyst concluded that the significance of this finding with respect to LERF was also

White (increase in LERF greater than 1E-7/year).

References

Risk-Informed Inspection Notebook for Fort Calhoun Station, Revision 2, September 30,

2005

Fort Calhoun SPAR model, Revision 3.31, April 10, 2006

NUREG/CR-6883, "The SPAR-H Human Reliability Analysis Method"

Fort Calhoun White Paper, "Severe Accident (PRA) Perspective Regarding Improper

Positioning of Containment Spray Header Isolation Valve HCV-345"

USAR Section 4.3, Reactor Coolant System, Component and System Design and

Operation

USAR Section 6.3, Engineered Safeguards, Containment Spray System

USAR Section 6.4, Engineered Safeguards, Containment Air Cooling and Filtering

System

USAR Section 7.3, Instrumentation and Control, Engineered Safeguards Controls and

Instrumentation

USAR Section 9.3, Auxiliary Systems, Shutdown Cooling System

USAR Section 9.7, Auxiliary Systems, Component Cooling Water System

System Training Manual Volume 8, Component Cooling Water System

System Training Manual Volume 10, Containment Structure and Ventilation System

System Training Manual Volume 15, Emergency Core Cooling System

Attachment

A2-12

AOP-6, "Fire Emergency"

EOP-00, "Standard Post Trip Actions"

EOP-02, "Loss of Off-site Power, Loss of Forced Circulation"

EOP-03, "Loss of Coolant Accident"

EOP-04, "Steam Generator Tube Rupture"

EOP-05, "Uncontrolled Heat Extraction"

EOP-06, "Loss of all Feedwater"

EOP-20, "Functional Recovery Procedure"

EOP/AOP Attachments, Attachment 4, "SDC Without RAS"