ML053050395

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IR 05000338-05-004, IR 05000339-05-004; 07/01/2005 - 09/30/2005; North Anna Power Station Units 1 & 2. Routine Integrated Resident and Regional Report. Maintenance Effectiveness - Biennial Assessment. Emergency Preparedness Baseline. Radiat
ML053050395
Person / Time
Site: North Anna  Dominion icon.png
Issue date: 10/28/2005
From: Landis K
NRC/RGN-II/DRP/RPB5
To: Christian D
Virginia Electric & Power Co (VEPCO)
References
IR-05-004
Download: ML053050395 (51)


See also: IR 05000338/2005004

Text

October 28, 2005

Virginia Electric and Power Company

ATTN.: Mr. David A. Christian

Sr. Vice President and

Chief Nuclear Officer

Innsbrook Technical Center - 2SW

5000 Dominion Boulevard

Glen Allen, VA 23060-6711

SUBJECT:

NORTH ANNA POWER STATION - NRC INTEGRATED INSPECTION

REPORT NOS. 05000338/2005004 AND 05000339/2005004

Dear Mr. Christian:

On September 30, 2005, the United States Nuclear Regulatory Commission (NRC) completed

an inspection at your North Anna Power Station, Units 1 and 2. The enclosed integrated

inspection report documents the inspection findings, which were discussed on September 22,

2005, with Mr. Jack Davis and other members of your staff.

The inspections examined activities conducted under your licenses as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your

licenses. The inspectors reviewed selected procedures and records, observed activities, and

interviewed personnel.

Based upon the results of this inspection, six self-revealing findings of very low safety

significance (Green) were identified. Five of these were determined to involve violations of

NRC requirements. However, because of their very low safety significance and because they

were entered into your corrective action program, the NRC is treating these five findings as

non-cited violations (NCVs) consistent with Section VI.A of the NRC Enforcement Policy. A

self-revealing violation whose significance determination is to be determined was also identified.

In addition, one licensee-identified violation, which was determined to be of very low safety

significance (Green), is listed in Section 4OA7 of this report. If you contest any non-cited

violation in this report, you should provide a response within 30 days of the date of this

inspection report, with the basis for your denial, to the United States Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, D.C. 20555-0001; with copies to the

Regional Administrator, Region II; the Director, Office of Enforcement, United States Nuclear

Regulatory Commission, Washington, D.C. 20555-0001; and the NRC Resident Inspector at

the North Anna Power Station.

In accordance with 10 CFR 2.390 of the NRCs Rules of Practice, a copy of this letter, its

enclosure, and your response, if any, will be available electronically for public inspection in the

NRC Public Document Room or from the Publicly Available Records (PARS) component of

VEPCO

2

NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Kerry D. Landis, Chief

Reactor Projects Branch 5

Division of Reactor Projects

Docket Nos.: 50-338, 50-339

License Nos.: NPF-4, NPF-7

Enclosures:

Inspection Reports 05000338/2005004 and 05000339/2005004

cc w/encls.:

Chris L. Funderburk, Director

Nuclear Licensing and

Operations Support

Virginia Electric and Power Company

Electronic Mail Distribution

Jack M. Davis

Site Vice President

North Anna Power Station

Electronic Mail Distribution

Executive Vice President

Old Dominion Electric Cooperative

Electronic Mail Distribution

County Administrator

Louisa County

P. O. Box 160

Louisa, VA 23093

Lillian M. Cuoco, Esq.

Senior Counsel

Dominion Resources Services, Inc.

Electronic Mail Distribution

Attorney General

Supreme Court Building

900 East Main Street

Richmond, VA 23219

_________________________

OFFICE

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SIGNATURE

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NAME

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DATE

10/28/2005

10/28/2005

10/28/2005

10/28/2005

10/28/2005

10/28/2005

E-MAIL COPY?

YES

NO YES

NO YES

NO YES

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OFFICE

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SIGNATURE

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DATE

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Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos.: 50-338, 50-339

License Nos.: NPF-4, NPF-7

Report Nos.:

05000338/2005004, 05000339/2005004

Licensee:

Virginia Electric and Power Company (VEPCO)

Facilities:

North Anna Power Station, Units 1 & 2

Location:

1022 Haley Drive

Mineral, Virginia 23117

Dates:

July 1, 2005 - September 30, 2005

Inspectors:

J. Reece, Senior Resident Inspector

G. Wilson, Resident Inspector

W. Loo, Senior Health Physicist, Sections 2PS1, 4OA5

R. Hamilton, CHP Senior Health Physicist, Sections 2OS1, 4OA1, 4OA5

A. Nielsen, CHP Health Physicist, Section 2OS3

F. Wright, Senior Health Physicist, Section 2PS3

L. Miller, Senior Emergency Preparedness Inspector, Sections 1EP2-1EP5, and

4AO1

M. Scott, Senior Reactor Inspector, Section 1R12

M. Maymi, Reactor Inspector, Section 1R12

Approved by: K. Landis, Chief, Reactor Projects Branch 5

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000338/2005-004, IR 05000339/2005-004; 07/01/2005 - 09/30/2005; North Anna Power

Station Units 1 & 2. Routine Integrated Resident and Regional Report. Maintenance

Effectiveness - Biennial Assessment. Emergency Preparedness Baseline. Radiation Safety.

The report covered a three-month period of inspection by the resident inspectors, health

physicists, a senior emergency preparedness inspector, and reactor inspectors from the region.

Six self-revealing Findings were identified. Five of these were determined to be Non-cited

Violations (NCVs). A self-revealing violation whose significance determination is to be

determined was also identified. The significance of most findings is indicated by their color

(Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance

Determination Process (SDP). Findings for which the SDP does not apply may be Green or be

assigned a severity level after NRC management review. The NRCs program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649,

Reactor Oversight Process, Revision 3, dated July 2000.

A.

NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

Green. A self-revealing non-cited violation of 10 CFR 50, Appendix B, Criterion XVI,

was identified regarding a failure to promptly identify and correct deficiencies which

caused anomalies in the Unit 2 channel 1 over-temperature delta-temperature (OTDT)

instrumentation. The anormalies occurred during a lightning storm on July 29, 2003 and

the licensee took no corrective actions to correct the condition. As a result, it was not

until a Unit 2 automatic reactor trip from an OTDT signal on August 5, 2005, during a

lightning storm, that the licensee identified an installation deficiency associated with a

1989 modification. A similar Unit 2 automatic reactor trip from an OTDT signal occurred

during a lightning storm on September 17, 1998.

The finding had an impact on safety based on the deficiencies resulting in two reactor

trips and a third documented near miss event. The finding was more than minor

because it affected the Initiating Events cornerstone objective to limit the likelihood of

those events that upset plant stability and the cornerstone attribute of design control.

The finding is of very low safety significance because it did not contribute to the

likelihood of a primary or secondary system loss of coolant accident, a loss of mitigation

equipment functions or the likelihood of a fire or flood event. This finding contains

aspects relating to the cross-cutting area of problem identification and resolution.

(Section 1R14.1)

Green. A self-revealing finding was identified for untimely corrective action resulting in a

rapid reduction of power on Unit 1 due to a severe oil leak on the valve actuator for

1-EH-TV-100, main turbine auto stop oil interface valve. A similar problem on this valve

resulted in a manual reactor trip on April 19, 2003. Subsequent evaluations from a Unit

2 similar issue determined that torque values as specified by procedure for the valve

actuator diaphragm bolts were below the values as recommended by the vendor, but

untimely corrective actions resulted in a rapid Unit 1 down-power on August 5, 2005.

2

Enclosure

This finding had a credible impact on safety due to the challenge of plant control

systems from the rapid reduction of power. The finding is consequently more than

minor based on the impact to the Initiating Events cornerstone objective to limit the

likelihood of those events that upset plant stability and the cornerstone attribute of

equipment reliability. This finding contains aspects relating to the cross-cutting area of

problem identification and resolution. (Section 1R14.2)

Green. On July 22, 2005, a self-revealing non-cited violation of Technical Specification 5.4.1.a was identified for a failure to follow a surveillance procedure which resulted in

placing an incorrect bistable in a trip condition on Unit 2. Only unexpected control room

alarms occurred as a result of the performance deficiency since no other logic channels

bistables were in trip.

The inspectors determined that the finding is more than minor because it could

reasonably be viewed as a precursor to a more significant event. If another channel in

the logic had already been tripped, the plant would have been adversely affected. The

finding is of very low safety significance (Green) because it did not involve any loss of

coolant accident initiators, did not contribute to both a reactor trip or mitigating system

unavailability, nor increase the likelihood of a fire. This finding contains aspects relating

to the cross-cutting area of human performance. (Section 1R22.1)

Cornerstone: Mitigating Systems

Green. A self-revealing non-cited violation of Technical Specification 5.4.1.a was

identified for an inadequate procedure which resulted in the loss of two Unit 1 safety-

related 480V buses on May 1, 2005.

The finding had a credible impact on safety due to the loss of two safety-related 480V

buses resulting in the loss of power to multiple B train components two minutes after a

containment depressurization signal during a design basis accident. The finding is more

than minor due to the impact on two cornerstones, Mitigating Systems and Barrier

Integrity. A Phase II evaluation of the significance determination process concluded the

finding was of very low safety significance (Green) because only the B train was

affected, a two minute time delay allowed safety-related component reposition, and

emergency procedures identified appropriate operation action for manual component

operation following the fault. This finding contains aspects relating to the cross-cutting

area of human performance. (Section 1R12)

Green. A self-revealing non-cited violation of 10 CFR 50, Appendix B, Criterion III, was

identified for inadequate design controls. During the development of a service water

(SW) expansion joint modification, which was implemented in December 2003, the

licensee failed to verify the design adequacy of adjacent pipe support and restraints.

The design failed to incorporate normal system pressure loads in the design. As a

result, on June 14, 2005, during inspections of the SW expansion joints, the licensee

noted severe damage on adjacent pipe support and restraints. Both the Unit 1 and Unit

2 A and B trains of SW were affected. The SW system was determined to operable

but degraded.

3

Enclosure

This finding had a credible impact on safety based on a design control error which

impacted both trains of the SW system which is a link between the transfer of reactor

decay heat to the plants ultimate heat sink. The finding is more than minor due to the

impact on the Mitigating Systems cornerstone objective to ensure the availability,

reliability, and capability of systems that respond to initiating events to prevent

undesirable consequences (i.e. core damage) and the cornerstone attribute of design

control of plant modifications. The finding is of very low safety significance because the

design deficiency was confirmed not to result in loss of function per Generic Letter 91-

18. This finding contains aspects relating to the cross-cutting area of human

performance. (Section 1R04.2)

TBD. A self-revealing violation of 10 CFR 50, Appendix B, Criterion XVI was identified

for inadequate corrective action resulting in a flood potential for the Unit 1 and 2

safeguards instrument rack rooms. Corrective actions in October 2004, associated with

water from a capped floor drain outside the air conditioning chiller room (ACCR) failed to

identify that back-flow preventers where not installed in the floor drains between the

ACCR and the air conditioning fan room (ACFR). As a result, the lack of floor drain

back-flow preventers was not discovered until July 9, 2005, when water was

unexpectedly transferred between with the ACCR and ACFR. The back-flow preventers

are necessary to prevent leakage in the ACCR from bypassing the flood wall protecting

the ACFR and adjoining safeguards instrument rack room from flooding.

The inspectors determined that the finding had a credible impact of safety based on the

potential for flooding to impact the instrument rack room which contains both trains of

Solid State Protection System cabinets used for engineered safeguards . The finding, if

left uncorrected, would result in a more significant safety concern and is consequently

more than minor. The finding involves a Phase III evaluation for the significance

determination process due to the loss or degradation of equipment specifically designed

to mitigate a flooding event and the impact on two trains of a safety system. This finding

is unresolved pending completion of the significant determination assessment and

involves aspects of the cross-cutting area of problem identification and resolution.

(Section 1R06)

Cornerstone: Barrier Integrity

Green. A self-revealing non-cited violation of Technical Specification 5.4.1.a was

identified for a failure to follow a maintenance procedure. On February 19, 2005, the

Unit 2 B quench spray pump motor breaker overload setpoints were not set in

accordance with procedures. As a result, the pump tripped while starting on August 19,

2005.

The finding had a credible impact on safety due to the starting failure of one of the

components required to reduce containment pressure following a design basis accident.

The finding was more than minor because it affected the Barrier Integrity cornerstone

objective to provide reasonable assurance that the containment physical design barriers

protect the public from radio nuclide releases caused by accidents or events, and the

respective cornerstone of human performance. The finding was determined to be of

4

Enclosure

very low safety significance because it did not impact design deficiencies, result in a loss

of system safety functions, exceed related TS outage times, nor involved a seismic,

flooding, or severe weather initiating event. This finding contains aspects relating to the

cross-cutting area of human performance. (Section 1R22.2)

B.

Licensee-Identified Violation

One violation of very low safety significance was identified by the licensee, and has been

reviewed by the inspectors. Corrective actions taken or planned by the licensee have

been entered into the licensees corrective action program. This violation and corrective

action tracking numbers are listed in Section 4OA7 of this report.

Enclosure

CONTENTS

Summary of Plant Status . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

REACTOR SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R04

Equipment Alignment . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 1

1R05

Fire Protection . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3

1R06

Flood Protection Measures . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 4

1R11

Licensed Operator Requalification Program . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R12

Maintenance Effectiveness . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 6

1R13

Maintenance Risk Assessments and Emergent Work Control . . . . . . . . . . . . . . . . . . . 9

1R14

Operator Performance During Non-Routine Evolutions and Events . . . . . . . . . . . . . . . 9

1R15

Operability Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .12

1R17

Permanent Plant Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .13

1R19

Post-Maintenance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 13

1R22

Surveillance Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 14

1R23

Temporary Modifications . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 16

1EP2 Alert and Notification System Testing . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 17

1EP3 Emergency Response Organizational Augmentation . . . . . . . . . . . . . . . . . . . . . . . . . 17

1EP4 Emergency Action Level and Emergency Plan Changes . . . . . . . . . . . . . . . . . . . . . . 18

1EP5 Correction of Emergency Preparedness Weakness and Deficiencies . . . . . . . . . . . . 18

1EP6 Drill Evaluation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

RADIATION SAFETY . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

2OS1 Access Control to Radiologically Significant Areas . . . . . . . . . . . . . . . . . . . . . . . . . . . 19

2OS3 Radiation Monitoring Instrumentation . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 20

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems . . . . . . 22

2PS3 Radiological Environmental Monitoring Program . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 23

OTHER ACTIVITIES . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA1 Performance Indicator Verification . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 24

4OA2 Identification and Resolution of Problems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 26

4OA4 Cross-cutting Aspects of Findings. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .27

4OA5 Other Activities

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA6 Meetings, Including Exit

. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 28

4OA7 Licensee-Identified Violations . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 29

ATTACHMENT: SUPPLEMENTARY INFORMATION

Key Points of Contact . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

A-1

List of Items Opened, Closed, and Discussed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

A-1

List of Documents Reviewed . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

A-2

Enclosure

REPORT DETAILS

Summary of Plant Status

Unit 1 and Unit 2 began the inspection period at 100 percent power, and remained at or near

100 percent power for the entire reporting period except for minor power reductions to perform

required periodic testing and the following events:

Unit 1 experienced a rapid down-power event on August 5, 2005, due to severe

oil leakage on 1-EH-TV-100, and

Unit 2 experienced an over-temperature delta-temperature (OTDT) automatic reactor trip during a lightning storm on August 5, 2005.

3.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R04

Equipment Alignment

.1

Partial System Walkdowns

a.

Inspection Scope

The inspectors conducted three equipment alignment partial walkdowns to evaluate the

operability of selected redundant trains or backup systems, listed below, with the other

train or system inoperable or out of service. The inspectors reviewed the functional

system descriptions, Updated Final Safety Analysis Report (UFSAR), system operating

procedures, and Technical Specifications (TS) to determine correct system lineups for

the current plant conditions. The inspectors performed walkdowns of the systems to

verify that critical components were properly aligned and to identify any discrepancies

which could affect operability of the redundant train or backup system.

Unit 1 1H Emergency Diesel Generator (EDG) during planned maintenance on

the 1J EDG;

Unit 2 Auxiliary Feedwater 2-FW-3A, during planned maintenance on 2-FW-3B;

and,

Unit 2 Quench Spray 2-QS-P-1A during emergent work on 2-QS-P-1B.

b.

Findings

No findings of significance were identified.

.2

Complete System Walkdown

a.

Inspection Scope

The inspectors performed a detailed walkdown and inspection of the Unit 2 Service

Water (SW) system outside of containment to assess properly alignment and to identify

discrepancies that could impact its availability and functional capacity. The inspectors

2

Enclosure

assessed the physical condition of the pumps, valves, pipe supports, and

instrumentation. The inspection also included a review of the alignment and the

condition of support systems including fire protection, room ventilation and emergency

lighting. Equipment deficiency tags were reviewed and the condition of the system was

discussed with engineering personnel. The operating procedures, drawings and other

documents utilized and reviewed as part of the inspection are listed in the Attachment.

b.

Findings

Inadequate Design Control Results in Degradation of SW Support/Restraints

Introduction. The inspectors identified a self-revealing non-cited violation (NCV)

associated with inadequate design control resulting in degradation of SW system

support-restraints (S/R).

Description. On June 14, 2005, the licensee was performing a preventative maintenance

(PM) inspection of SW expansion joints on plant discharge piping located in the SW tie-in

vault and noticed severely bent or degraded SW S/Rs, 1-SW-PH-3.2 on the B train

discharge header and 1-SW-PH-4.2 on the A train discharge header. Both trains are

shared between Units 1 and 2. An extent of condition walkdown was performed and one

additional S/R, 1-SW-PH-E85.2, was identified with structural damage and documented

in Plant Issue N-2005-2225. The inspectors reviewed and verified the resultant

functional evaluation which concluded that a generic letter (GL) 91-18 (operable but

degraded) condition existed for A and B SW trains. The licensee performed a root cause

evaluation which determined that a design analysis failure occurred during a modification

(Design Change 02-006) which was implemented in December, 2003, and converted the

metal expansion joints to a design using rubber as the flexible component. The

additional pressure component of piping loads associated with the new rubber design

was not translated by engineering personnel to the modification process resulting in

S/Rs too weak to handle the loads associated with normal system operation. The

human performance aspects of the design failure analysis is a noncompliance with 10 CFR 50, Appendix B, Criterion III, which states in part that measures shall provide for

verifying or checking the adequacy of design.

Analysis. This finding had a credible impact on safety based on a design control error

which impacted both trains of the SW system which is a link between transfer of reactor

decay heat to the plants ultimate heat sink. The inspectors reviewed Inspection Manual

Chapter (IMC) 0612 and determined the finding is more than minor due to the impact on

the Mitigating Systems cornerstone objective to ensure the availability, reliability, and

capability of systems that respond to initiating events to prevent undesirable

consequences (i.e., core damage) and the cornerstone attribute of design control of plant

modifications. The inspectors referenced IMC 0609 for the Significant Determination

Process (SDP) and determined that the finding is Green or very low safety significance

because the design deficiency was confirmed not to result in loss of function per GL 91-18. This finding contains aspects relating to the cross-cutting area of human

performance.

3

Enclosure

Enforcement. 10 CFR 50, Appendix B, Criterion III, requires in part that measures shall

provide for verifying or checking the adequacy of design. Contrary to the above,

inadequate verification of a modification, Design Change 02-006, implemented in

December, 2003, to replace SW metal expansion joints with a rubber design resulted in

an operable but degraded condition due to damaged SW system S/Rs discovered on

June 14, 2005. This finding is of very low safety significance or Green, is in the

licensees corrective action program (CAP) as Plant Issue N-2005-2229, and is

characterized as a NCV, consistent with Section VI.A of the NRC's Enforcement Policy:

NCV 05000338, 339/2005004-01, Inadequate Design Control Resulting in Degraded

Service Water Support-Restraints.

1R05

Fire Protection

.1

Fire Drill

a.

Inspection Scope

During a fire protection drill on August 31, 2005, at the Service Water Pump House, the

inspectors assessed the timeliness of the fire brigade in arriving at the scene, the fire

fighting equipment brought to the scene, the donning of fire protective clothing, the

effectiveness of communications, and the exercise of command and control by the scene

leader. The inspectors also assessed the acceptance criteria for the drill objectives and

reviewed the licensees CAP for recent fire protection issues. Documents reviewed are

listed in the Attachment.

b.

Findings

No findings of significance were identified.

.2

Fire Area Tours

a.

Inspection Scope

The inspectors conducted tours of the eleven areas listed below and important to reactor

safety to verify the licensees implementation of fire protection requirements as described

in Virginia Power Administrative Procedure (VPAP)-2401, Fire Protection Program. The

inspectors evaluated, as appropriate, conditions related to: (1) licensee control of

transient combustibles and ignition sources; (2) the material condition, operational status,

and operational lineup of fire protection systems, equipment, and features; and (3) the

fire barriers used to prevent fire damage or fire propagation.

Auxiliary Building (includes Z-18 and Z-20) (fire zone 11a / AB);

Quench Spray Pump House and Safeguards Area Unit 2 (includes Z-16-2) (fire

zone 15-2a / QSPH-2);

Fuel Building (fire zone Z-18 / FB);

Main Control Room (fire zone 2a / CR);

4

Enclosure

Cable Vault and Tunnel Unit 2 (includes Control Rod Drive Room and Z-27-1)

(fire zones 3-2a / CV & T-2);

Cable Vault and Tunnel Unit 1 (includes Control Rod Drive Room and Z-27-1)

(fire zone 3-1a / CV & T-1);

Service Water Pump House (fire zone 12a / SWPH);

Safeguards Area Unit 2 (fire zone Z-16-2 / SA-2);

Safeguards Area Unit 1 (fire zone Z-16-1 / SA-1);

Casing Cooling Tank & Pump House Unit 1 (fire zone Z-41-1 / CCT & PH-1); and,

Casing Cooling Tank & Pump House Unit 2 (fire zone Z-41-2 / CCT&PH-2).

b.

Findings

No findings of significance were identified.

1R06

Flood Protection Measures

a.

Inspection Scope

The inspectors reviewed internal flood protection measures for the Unit 1 and 2 air

conditioning chiller rooms (ACCRs) and adjacent air conditioning fan rooms (ACFRs).

Flooding in the ACCRs and ACFRs could impact risk-significant components in the

instrument rack rooms adjacent to the ACFRs if flood mitigation features were degraded.

ACCR and ACFR protection features were observed to verify that they were installed and

maintained consistent with the plant design basis. The inspectors reviewed the

instrumentation and associated alarms for the rooms above to verify that the

instrumentation was periodically calibrated and that the respective alarms were

appropriately integrated into plant procedures. The inspectors also reviewed licensee

instructions in the event of severe flooding and evaluated the availability of systems,

structures and components (SSCs) for safe shutdown under worst case water levels.

Documents reviewed are listed in the Attachment.

b.

Findings

Inadequate Corrective Action Results in Safeguards Instrument Rack Room Flood

Problem

Introduction. The inspectors identified a self-revealing violation associated with

inadequate corrective action. Back-flow preventers were not installed in floor drains that

resulted in a flood potential for the Unit 1 and 2 Safeguards Instrument Rack Rooms.

The safety significance is under evaluation and thus the item is classified as an

unresolved item (URI).

Discussion. On July 9, 2005, back flush of control room chiller service water strainers

2-HV-S-1A and 1B as directed by engineering transmittal, ET N-05-0034, Operability of

2-HV-P-22C, Service Water Pump for 2-HV-E-4C, was performed in the Unit 2 ACCR.

During this work activity, the licensee observed water discharging from the floor drains in

the adjacent ACFR, and initiated Plant Issue N-2005-2565 to evaluate the absence of

5

Enclosure

back-flow preventers in the floor drains. The licensee initiated a flood watch, declared

the flood walls between the ACCR and adjacent ACFR on Units 1 and 2 inoperable, and

entered a Yellow 6 day maintenance rule risk condition based on the unavailability of the

flood walls to perform their function. The respective ACFR on both units are adjacent

and open to the safeguards instrument rack rooms, which contain the solid state

protection system (SSPS) and process instrumentation and are at a 2 feet lower

elevation. Each instrument rack room has a sump with two pumps rated at 40 gpm each.

On Unit 2 the sump pumps discharge line is hard-piped directly to the ACCR sump.

However, on Unit 1 the sump pumps discharge line is routed to a drain funnel

interconnected to the floor drain system of the adjacent ACFR. The licensee determined

that this funnel did not have a back-flow preventer installed and initiated Plant Issue

N-2005-2597. A subsequent calculation, ME-0782, was performed by the licensee to

evaluate the consequences of a service water line break in either the Unit 1 or 2 ACCRs.

The calculation concluded that the peak flow rate from the Units 1 and 2 ACCRs to

adjacent ACFRs via the floor drain piping was 182.9 gpm and 169.4 gpm respectively.

The inspectors reviewed the licensees corrective action database and determined that

on October 15, 2004, Plant Issue N-2004-4554 was initiated due to water discharge from

a capped floor drain outside of the ACCR. An other evaluation was assigned to

engineering to review this condition for impact on the flood protection assumed for the

ACCR and connecting areas as applicable. This evaluation did not identify and correct

the absence of back-flow preventers in the adjacent ACFR floor drains. The inspectors

also identified that Plant Issue N-1999-3405, which documented operational experience

from Three Mile Island regarding check valves missing from floor drains and the impact

on flood protection, did not result in the identification and correction of this problem. The

inspectors concluded that the inadequate corrective actions for Plant Issue N-2004-4554

is contrary to the requirements of 10 CFR 50, Appendix B, Criterion XVI, which requires

that the establishment of measures to assure conditions adverse to quality are promptly

identified and corrected.

Analysis. The inspectors determined that the finding had a credible impact on safety

based on the potential for flooding to impact both trains of SSPS cabinets used for

engineered safeguards. The inspectors referenced IMC 0612 and determined that if left

uncorrected this finding would result in a more significant safety concern and is

consequently more than minor. Based on a review of IMC 0609 for the SDP, the

inspectors determined the finding would require a Phase III evaluation due to the loss or

degradation of equipment specifically designed to mitigate a flooding event and the

impact on two trains of a safety system. This finding is an URI pending completion of the

significance determination assessment and contains aspects relating to the cross-cutting

area of problem identification and resolution.

Enforcement. 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires the

establishment of measures to assure conditions adverse to quality are promptly and

identified and corrected. Contrary to the above, prompt identification and correction of

deficiencies relating to Plant Issue N-2004-4554 failed to identify and correct the absence

of back-flow preventers in the Unit 1 and 2 ACFRs. This violation is characterized as an

URI pending significance determination, and is identified as URI 05000338,

6

Enclosure

339/2005004-02, Inadequate Corrective Action Results in Safeguards Instrument Rack

Room Flood Problem. This finding is in the licensee's CAP as Plant Issue N-2005-2565.

1R11

Licensed Operator Requalification Program

a.

Inspection Scope

The inspectors observed an annual licensed operator requalification simulator

examination on September 13, 2005. The scenerio, Simulator Examination Guide

SXG-56, involved a loss of instrument air, followed by increased primary plant leakage, a

loss of bearing cooling pumps with subsequent reactor trip, and a small break loss of

cooling accident (LOCA).

The scenario required classifications and notifications that were counted for NRC

performance indicator input. The inspectors observed crew performance in terms of

communications; ability to take timely and proper actions; prioritizing, interpreting, and

verifying alarms; correct use and implementation of procedures, including the alarm

response procedures; timely control board operation and manipulation, including

high-risk operator actions; and oversight and direction provided by the shift supervisor,

including the ability to identify and implement appropriate TS actions. The inspectors

observed the post training critique to determine that weaknesses or improvement areas

revealed by the training were captured by the instructors and reviewed with the

operators.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness

.1

Periodic Evaluation (Biennial)

a.

Inspection Scope

The inspectors reviewed the licensees Maintenance Rule periodic assessments, 2003

Maintenance Rule Periodic Assessment Report [NAPS-SA-03-03, dated 6/11/04] and

2005 Maintenance Rule Periodic Assessment Report [NAPS-SA-03-37, dated 8/15/05]

while on-site the week of August 15, 2005. These reports were issued to satisfy

paragraph (a)(3) of 10 CFR 50.65, and covered the 18 month periods ending August 31,

2003, and ending February 28, 2005, respectively, for Units 1 and 2. The inspection was

to determine the effectiveness of the assessment and that it was issued in accordance

with the time requirement of the Maintenance Rule (MR) and included evaluation of:

balancing reliability and unavailability, (a)(1) activities, (a)(2) activities, and use of

industry operating experience. To verify compliance with 10 CFR 50.65, the inspectors

reviewed selected MR activities covered by the assessment period for the following

maintenance rule component and attendant systems: Control Room Bottled Air, Control

Room Chilled Service Water Motors, High Head Safety Injection pump seals; Service

7

Enclosure

Water Spray Arrays, Reactor Water Storage Tank Chillers. Specific procedures and

documents reviewed are listed in the Attachment to this report.

During the inspection, the inspectors reviewed selected plant work order data,

assessments, modifications, the site guidance implementing procedures, discussed and

reviewed relevant corrective action [plant] issues, reviewed generic operations event

data, attendant MR related meeting minutes, probabilistic risk reports, and discussed

issues with system engineers. Operational event information was evaluated by the

inspectors in its use in MR functions. The inspectors selected work orders and other

corrective action documents on systems recently removed from 10 CFR 50.65 a(1)

status and those in a(2) status for some period to assess the justification for their status.

The inspectors toured and inspected repaired components. The documents were

compared to the sites MR program criteria, and the MR a(1) evaluations and rule related

data bases.

b.

Findings

No findings of significance were identified.

.2

Quarterly Sample

a.

Inspection Scope

For the two equipment issues listed below, the inspectors evaluated the licensees

effectiveness of the corresponding preventive and corrective maintenance. The

inspectors performed walkdowns of the accessible portions of the systems, performed

in-office reviews of procedures and evaluations, and held discussions with system

engineers. The inspectors compared the licensees actions with the requirements of the

Maintenance Rule (10 CFR 50.65) using VPAP 0815, Maintenance Rule Program, and

Engineering Transmittal CEP-97-0018, North Anna Maintenance Rule Scoping and

Performance Criteria Matrix. The inspectors also completed review of unresolved item

(URI) URI 05000338/20050003-01 which is documented in NRC Integrated Inspection

Report Nos. 05000338/2005003. Other documents reviewed are listed in Attachment.

The mechanical seals on pump 2-CH-P-1C were recently replaced with new seals

associated with Work Order (WO) 523899 for 20 ml/min outboard end bell leak on

2-CH-P-1C; and,

The Refueling Water Storage Tanks (RWST) mechanical chillers have had

multiple issues associated with the reliability of these chillers.

b.

Findings

(Closed) URI 05000338/20050003-01, Inadequate Maintenance of a Procedure Results

in Loss of Safety Related 480V Buses.

Introduction. A Green, self-revealing NCV was identified for failure to comply with TS 5.4.1 which resulted in the loss of two safety-related 480V buses on Unit 1.

8

Enclosure

Description. URI 05000338/2005003-01 documented a noncompliance with TS 5.4.1

which involved an inadequate maintenance procedure that resulted in the loss of two

safety-related 480 volt buses, 1J1-2N and 1J1-2S on May 1, 2005. The lack of adequate

instructions for breaker wiring resulted in a termination screw for the B phase field cable

connection to a thermal overload relay penetrating the adjacent insulation on the C

phase field cable connection. The resulting fault caused a flashover event within the

breaker cubicle and resulted in the upstream feeder breaker tripping on overcurrent with

the subsequent loss of the 480V buses.

Analysis. The inspectors referenced IMC 0612 and determined that the finding is more

than minor because it affected the reactor safety Mitigating Systems cornerstone

objective to ensure availability, reliability and capability of systems that respond to

initiating events to prevent core damage and the Barrier Integrity cornerstone objective to

provide reasonable assurance that physical design barriers such as containment protect

the public from radio nuclide releases caused by accidents or events. The attribute of

procedure quality was affected for each aforementioned cornerstone. The inspectors

referenced IMC 0609, for the SDP and determined that a Phase II analysis was required

because the finding affected two cornerstones. This analysis reviewed accidents

resulting in high containment pressure which would initiate a Containment

Depressurization Actuation (CDA) signal which, after a two minute time delay, would

close the affected breaker (to start a radiation monitor sample pump) resulting in the

fault. The analysis also reviewed the emergency procedures (EP) involving those

components which reposition prior to the fault due to the time delay as well as the

components which must be locally, manually controlled after the fault. Completion of the

applicable SDP worksheets of the Risk-Informed Inspection Notebook for North Anna

Power Station resulted in a risk of very low significance (Green) because only the B train

was affected, a two minute time delay allowed safety-related component reposition, and

emergency procedures identified appropriate operation action for manual component

operation following the fault. This finding contains aspects relating to the cross-cutting

area of human performance.

Enforcement. TS 5.4.1 requires that written procedures shall be established,

implemented, and maintained covering the activities in the applicable procedures

recommended by Regulatory Guide (RG) 1.33, Revision 2, Appendix A, February 1978,

of which part 9.e. specifies general procedures for the control of maintenance work.

Contrary to the above, on December 28, 2004, maintenance procedure 0-EPM-0304-01

was not adequate, in that, it failed to provide sufficient instructions to preclude faulty

retermination of wiring in breaker 1-EE-BKR-1J1-2N-B5. This led to an electrical fault

and the loss of 1J1-2N and 1J1-2S MCCs on May 1, 2005. This violation is considered a

Non-cited Violation (NCV), consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000338/2005004-03, Inadequate Maintenance of a Procedure Results in Loss of

Safety Related 480V Buses. This issue is in the licensee's CAP as Plant Issue

N-2005-1615.

9

Enclosure

1R13

Maintenance Risk Assessments and Emergent Work Evaluation

a.

Inspection Scope

The inspectors evaluated, as appropriate, for the six activities listed below: (1) the

effectiveness of the risk assessments performed before maintenance activities were

conducted; (2) the management of risk; (3) that, upon identification of an unforseen

situation, necessary steps were taken to plan and control the resulting emergent work

activities; and (4) that maintenance risk assessments and emergent work problems were

adequately identified and resolved. The inspectors verified that the licensee was

complying with the requirements of 10 CFR 50.65 (a)(4) and the data output from the

licensees safety monitor associated with the risk profile of Units 1 and 2.

Yellow maintenance rule 6-day window entered twice due to Control Room Chiller

area, Fan area, and SSPS Rack Room area flood concerns documented by Plant

Issue N-2005-2565;

Maintenance rule risk evaluation for unplanned Unit 1 down power with

concurrent Unit 2 reactor trip on August 8, 2005;

Maintenance rule risk evaluation for unplanned work on 2-QS-P-11B concurrent

with the components 2-CW-P-2A, 2-SW-MOV-221A, 2-HV-E-4A, 1-EE-BKR-

15J11 and 15D1 and 15D3, including rack work, switchyard and RSSTs;

Maintenance rule risk evaluation for planned restoration of A RSST to

underground line concurrent with the maintenance on 2-CW-P-2A, 2-SW-MOV-

221A, 1-EP-BKR-15A1, 1-FP-P-1, 2-CC-P-1B, 2-EP-BKR-25A1, SWYD, rack

work, B RSSTs on overhead lines, 0-EPM-1805-02, 0-PT-100.2, and 2-PT-44.7;

Maintenance rule risk evaluation for unplanned work on 2-EE-E6-2H concurrent

with the components 1-SW-P-4, 2-SW-MOV-221A, 1-CC-P-1A, 1-EE-BKR-15H12

and 2-MS-PCV-201A; and,

Maintenance rule risk evaluation for unplanned work on 2-EE-EG-2J, concurrent

with the components 2-CW-P-2A, 2-SW-MOV-221A, rack work, switchyard work,

and 1-PT-32.1.1.

b.

Findings

No findings of significance were identified.

1R14

Operator Performance During Non-Routine Evolutions and Events

a.

Inspection Scope

The inspectors reviewed operator logs and plant computer data for the two events listed

below to determine if plant and operator responses were in accordance with plant design,

procedures, and training. The inspectors also evaluated performance and equipment

problems to ensure that they were entered the licensees CAP.

10

Enclosure

The inspectors evaluated the response of the Unit 1 and 2 control room operators

on August 5 and 6, 2005, during an unplanned down power of Unit 1 for

diaphragm replacement on 1-EH-TV-100, and,

The inspectors evaluated the response of the Unit 2 control room operators on

August 5 and 6, 2005, following an automatic reactor trip which occurred during

the Unit 1 down power event above.

b.

Findings

.1

Inadequate Corrective Actions Results in a Reactor Trip

Introduction. A Green, self-revealing NCV was identified for a failure to identify and

correct deficiencies associated with reactor coolant instrumentation resulting in a reactor

trip.

Description. On August 5, 2005, a Unit 2 automatic reactor trip occurred due to actuation

of an OTDT reactor protection signal. A subsequent evaluation determined that a

lightning strike during a storm in progress at the time of the trip caused a transient in

Channel 1 and 2 reactor coolant temperature circuitry resulting in the automatic OTDT

trip signal. The inspectors verified that a reactor trip due to the same actuation signal

occurred during a lightning storm on September 17,1998. The subsequent root cause

evaluation concluded that the event was attributed to an external casual factor since it

was an event (lightning storm) outside the control of the company. Additionally, on July

29, 2003, during a lightning storm a transient was observed on Unit 2 channel 1 OTDT

instrumentation. However, a request for engineering assistance to investigate the

transient was not approved based on the conclusion of extremely dry soil conditions

affecting the grounding grid that year. Following the August 5, 2005, event the licensee

performed a more rigorous root cause evaluation and investigation that identified

ungrounded spare T-hot and T-cold narrow range resistance temperature detector (RTD)

shields that share the same thermowell in the reactor coolant system and same

containment electrical penetration as the active narrow range RTDs. Therefore, an

electrical transient induced by lightning in the spare, unshielded RTD elements was

consequently introduced into the active RTD elements, entered the narrow range

temperature reactor protection circuitry and resulted in the OTDT reactor trip. The

inspectors verified that these RTD shields were required to be grounded to the terminal

boards associated with protection channels 1 & 2 per a modification, DCP 89-41,

implemented in 1989, and properly completed on Unit 1. The inspectors concluded that

the failure to identify and correct the deficiencies associated with the July 29, 2003, event

was contrary to the requirements of 10 CFR 50, Appendix B, Criterion XVI, which

requires the establishment of measures to assure conditions adverse to quality are

promptly identified and corrected.

Analysis. The inspectors determined that the finding had a credible impact on safety

based on the deficiencies resulting in a reactor trip and a documented near-miss event.

The inspectors reviewed IMC 0612 and concluded the finding was more than minor

because it affected the Initiating Events cornerstone objective to limit the likelihood of

11

Enclosure

those events that upset plant stability and the cornerstone attribute of design control.

The inspectors referenced IMC 0609 for the SDP and concluded the finding is of very low

safety significance (Green) because it did not contribute to the likelihood of a primary or

secondary system LOCA, a loss of mitigation equipment functions, or the likelihood of a

fire or flood event. This finding contains aspects related to the cross-cutting area of

problem identification and resolution.

Enforcement. 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires the

establishment of measures to assure conditions adverse to quality are promptly and

identified and corrected. Contrary to the above, prompt identification and correction of

deficiencies relating to modification, DCP 89-41 was not performed following the

aforementioned Unit 2 reactor coolant instrumentation transient occurring on July 29,

2003, which resulted in a Unit 2 automatic reactor trip from actuation of an OTDT reactor

protection signal on August 5, 2005. This finding is of very low safety significance or

Green, is in the licensees CAP as Plant Issue N-2005-3016, and thus is characterized as

an NCV, consistent with Section VI.A of the NRC's Enforcement Policy: NCV 05000339/2005004-03, Failure to Identify and Correct Deficiencies in Instrumentation

Results In Reactor Trip.

.2

Unit 1 Rapid Power Reduction Due to Loss of Turbine Auto Stop Oil Pressure

Introduction: A Green, self-revealing finding was identified for not performing Unit 2

corrective actions in a timely manner on Unit 1. This resulted in the Unit 1 rapid

reduction of power from 100% to ~8% (main turbine off-line) on August 5, 2005.

Description: On August 5, 2005, the licensee rapidly reduced power on Unit 1 due to

severe oil leakage on the actuator for valve, 1-EH-TV-100 (Main Turbine Auto Stop Oil

Interface Valve). Subsequent evaluations determined that the torque specifications of

12-13 ft-lbs as specified in maintenance procedure 0-MCM-1412-01,Main Turbine

Interface Valve Diaphragm Replacement, did not provide adequate clamping force

between the diaphragm and actuator cover flange faces which resulted in diaphragm

movement and oil leakage from the actuator. The inspectors determined that an actuator

oil leak from the same valve resulted in a manual reactor trip due to low electro-hydraulic

or auto stop oil pressure on April 19, 2003. The inspectors reviewed the root cause

evaluation from that event and concluded that the licensee did not contact the vendor for

specific torque values. The inspectors also reviewed a December 2004, event involving

similar leakage on the Unit 2 equivalent valve. In this case, the resultant evaluation

concluded that the interface valve diaphragm torque values should have been 20 ft-lbs

per vendor technical manual 59-264-00006, Fisher Instruction Manual, Types 655 and

655R Actuators for Self-Operated Control. However, the inspectors determined that

associated corrective actions for Unit 1 had not been implemented prior to the August 5,

2005, rapid down-power event.

Analysis: This finding had a credible impact on safety due to the challenge of plant

control systems from the rapid reduction of power. The inspectors referenced IMC 0612

and determined that the finding was more than minor based on the impact to the Initiating

Events cornerstone objective to limit the likelihood of those events that upset plant

12

Enclosure

stability and the cornerstone attribute of equipment reliability. The inspectors referenced

IMC 0609 for the SDP and determined that the finding is Green (very low safety

significance) because it did not contribute to the likelihood of a primary or secondary

system LOCA initiator or a loss of mitigation equipment functions, and did not increase

the likelihood of a fire or internal/external flood. This issue is in the licensees CAP as

Plant Issue N-2005-2984. This finding contains aspects relating to the cross-cutting area

of problem identification and resolution.

Enforcement: Since this finding is associated with nonsafety-related secondary plant

equipment, no violation of regulatory requirements occurred. Therefore, this finding is

identified as a Green finding FIN 05000338/2005004-04, Untimely Corrective Actions for

Actuator Oil Leakage on Turbine Interface Valve Results in Rapid Down Power.

1R15

Operability Evaluations

a.

Inspection Scope

The inspectors reviewed six operability evaluations affecting risk-significant mitigating

systems, listed below, to assess, as appropriate: (1) the technical adequacy of the

evaluations; (2) whether continued system operability was warranted; (3) whether other

existing degraded conditions were considered as compensating measures; (4) whether

the compensatory measures, if involved, were in place, would work as intended, and

were appropriately controlled; (5) where continued operability was considered unjustified,

the impact on TS Limiting Conditions for Operation and the risk significance in

accordance with the SDP. The inspectors review included a verification that the

operability determinations were made as specified by Procedure VPAP-1408, System

Operability.

Plant Issue N-2005-2751, licensee identified problem with oil leaking from 1J

EDG exhaust manifold with the diesel in a stand by condition;

Plant Issue N-2005-2866, during the overspeed test of Station Blackout Diesel

per 0-MCM-0710-03 the BIMBA fuel rack air cylinder did not fully extend after the

diesel tripped as required by acceptance criteria;

Plant Issue N-2005-2927, NRC identified problem with loose control rods on SW

expansion joints 2-SW-REJ-24A through 2-SW-REF-24H;

Plant Issue N-2005-3240, Quench Spray pump operable but degraded due to out

of tolerance A&C phase instantaneous overcurrent settings on breakers;

Plant Issue N-2005-2937, Recirculation Spray seal accumulator high level alarms;

and,

Plant Issue N-2005-3527, ESGR HVAC units 2-HV-AC-7, 2-HV-AV-6 and 1-HV-

AC-7 have access cover latches that are very loose and can be pulled off with

little effort.

b.

Findings

No findings of significance were identified.

13

Enclosure

1R17

Permanent Plant Modifications

a.

Inspection Scope

The inspectors reviewed the completed permanent plant modification DCP 04-019,

Replacing RSST Underground Cables - Unit 1. The inspectors conducted a walkdown of

the installation, discussed the desired improvement with system engineers, and reviewed

the 10 CFR 50.59 Safety Review/Regulatory Screening, technical drawings, test plans

and the modification package to assess TS implications.

b.

Findings

No findings of significance were identified.

1R19

Post Maintenance Testing

a.

Inspection Scope

The inspectors reviewed seven post maintenance test procedures and/or test activities,

as appropriate, for selected risk-significant mitigating systems to assess whether: (1) the

effect of testing on the plant had been adequately addressed by control room and/or

engineering personnel; (2) testing was adequate for the maintenance performed; (3)

acceptance criteria were clear and adequately demonstrated operational readiness

consistent with design and licensing basis documents; (4) test instrumentation had

current calibrations, range, and accuracy consistent with the application; (5) tests were

performed as written with applicable prerequisites satisfied; (6) jumpers installed or leads

lifted were properly controlled; (7) test equipment was removed following testing; and (8)

equipment was returned to the status required to perform its safety function. The

inspectors verified that these activities were performed in accordance with licensee

procedure VPAP-2003, Post Maintenance Testing Program.

Procedure 2-PT-14.2, Charging Pump 2-CH-P-1B per WO 487833 and Plant

Issue N-2005-2472;

Procedure 0-MCM-0701-20, Repair of EDG Pre-lube and Standby Lube Oil

Pumps per WO 604135;

Procedure 2-PT-64.4A, Casing Cooling Pump (2-RS-P-3A) Test per WO 602353;

Procedure 0-ICM-XX-AOV-001, AOV Inspection and Diagnostic Testing per WO 606826 for work on 2-FW-FCV-2499;

Procedure 0-MCM-0701-34, Removal and Installation of EDG Exhaust Manifold,

and 2-PT-82H, 2H EDG Slow Start Test per WO 722151;

Procedure 0-EPM-03202-02 and 0-EPM-302-4, BBC / ITE 480 Volt K-Line

Breaker and Associated Switchgear Cubicle Maintenance per WOs 528002-05,

515205-01, and 528002-03; and,

Procedure 1-PT-74.2A, Component Cooling Pump 1-CC-P-1A Test per WO 722256

14

Enclosure

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing

a.

Inspection Scope

For the nine surveillance tests listed below, the inspectors examined the test procedure,

witnessed testing, and reviewed test records and data packages, to determine whether

the scope of testing adequately demonstrated that the affected equipment was functional

and operable, and that the surveillance requirements of the TS were met:

1-PT-63.1A, Quench Spray System A Subsystem (1-QS-P-1A), an inservice

test,

2-PT-71.2Q, Unit 2 Motor Driven Auxiliary Feedwater (2-FW-P-3A) Pump Test;

1-PT-52.2, Reactor Coolant System Leak Rate (Hand Calculation) VPAP-0502 -

Procedure Process Control;

2-PT-82J, 2J Diesel Generator Test Slow Start Test;

2-PT-63.1B, Quench Spray System - B Subsystem;

2-PT-213.8B, Valve Inservice Inspection (B Train of Safety Injection System);

2-PT-31.7, Pressurizer Level Channel (2-RC-L-2459) Channel Operational Test;

1-PT-75.2B, Unit 1 Service Water Pump (1-SW-P-1B); and,

2-PT-57.1B, Emergency Core Cooling Subsystem - Low Head Safety Injection

Pump (2-SI-P-1B).

b.

Findings

.1

Failure to Follow Procedures During SSPS Testing

Introduction. A Green, self-revealing NCV of TS 5.4.1.a was identified for failure to

implement a surveillance procedure which resulted in placing an incorrect bistable in a

trip condition.

Description. On July 22, 2005, during the performance of SSPS testing on Unit 2 in

accordance with procedure 2-PT-31.7, Pressurizer Level Channel I (2-RC-L-2459)

Channel Operational Test, of which step 6.1.5 requires placement of trip switches BS1

and BS2 on card C1-442 in the trip position, instrument technicians incorrectly placed

switches BS1 and BS2 on card C1-422 (same switch designation but a different card) in

the test position, which initiated an unexpected alarm (LO LO Tave Interlock Loop 1

A-B-C) in the control room. This caused Unit 2, Loop 1 T cold inputs to the SSPS

Relays K148 (Lo Lo Tave)(BS1) and K140 (Lo Tave)(BS2) to fail safe and show a trip

condition. A subsequent review by the inspectors of I/C drawings revealed that these

relays were Channel I inputs for P-12 (Lo Lo Tave Steam Dump Interlock) and feedwater

isolation permissives. The inspectors concluded that since loops two and three were not

in a trip condition, the two out of three logic was not satisfied, and the plant was not

affected.

15

Enclosure

Analysis. The inspectors reviewed IMC 0612 and determined that the finding was more

than minor because it could reasonably be viewed as a precursor to a more significant

event. If another channel in the logic had already been tripped, the plant would have

been adversely affected by the performance deficiency. The inspectors consulted IMC 0609 for the SDP and determined that the finding is Green (very low safety significance)

because it did not involve any LOCA initiators, did not contribute to both a reactor trip or

mitigating system unavailability, nor increase the likelihood of a fire. This finding contains

aspects relating to the cross-cutting area of human performance.

Enforcement. TS 5.4.1.a, requires that written procedures shall be established,

implemented, and maintained per RG 1.33, Appendix A, of which Part 8 stipulates

procedures for surveillance tests. Procedure, 2-PT-31.7.1, step 6.1.5. states, Place the

following comparator trip switches in TEST: On card C1-442, BS1 and BS2. Contrary to

the above on July 22, 2005, step 6.1.5 was improperly implemented in that comparator

switches, BS1 and BS2, on card C1-422 were placed in trip as opposed to the switches

on the correct card, C1-442. This finding is of very low safety significance or Green, is in

the licensees CAP as Plant Issue N-2005-2755, and thus is characterized as an NCV,

consistent with Section VI.A of the NRC's Enforcement Policy: NCV 05000339/2005004-04, Failure to Follow Procedure During Solid State Protection System

Testing.

.2

Failure to Follow Procedures Affecting Safety-Related Breakers

Introduction. A Green, self-revealing NCV of TS 5.4.1.a was identified for a failure to

follow procedures resulting in a trip of the Unit 2 Quench Spray Pump, 2-QS-P-1B.

Description. On August 19, 2005, during performance testing of 2-QS-P-1B per

2-PT-63.1B, Quench Spray System - B Subsystem, the respective motor breaker,

2-EE-BKR-24J1-4, closed and then immediately tripped open. The licensee

subsequently determined that two of the three as-found phase values of the breaker

overload device instantaneous pickup were low when compared to the North Anna

Setpoint Document (NASD) procedure which contains the setpoints, trip times and test

currents for all overload trip devices for 480-volt BBC/ITE K-Line Breakers. Therefore,

the motor starting current of approximately 3028 amps compared to the overload

instantaneous setpoints of 2268 amps and 2912 amps for B and C phases respectively

resulted in a premature trip of the breaker. The licensee previously performed

maintenance on this breaker on February 19, 2005, when the overload devices were set

and tested in accordance with electrical maintenance procedure, 0-EPM-302-02,

BBC/ITE 480-volt K-Line Breaker & Associated Switchgear Cubicle Maintenance,

which references the NASD. Procedure 0-EPM-302-02, step 6.19.4.a.2 states, If the trip

setpoint is within tolerance (80-120 percent) that was recorded in step 6.19.1, then go to

substep 6.19.4.b, and if not, then make adjustments using Attachment 5, Instantaneous

And Short-Time Pickup Adjustment, and repeat steps 6.19.4.a.1 and 6.19.4.a.2.

Contrary to the above, the technician performing the maintenance left the B and C

phase instantaneous overload setpoints low outside of the allowable procedural tolerance

at 3030 & 3002 amps respectively instead of within the allowable procedural tolerance of

3080 to 4620 amps. The licensee determined that a contributing cause was setpoint drift

16

Enclosure

on the associated overload device. However, the inspectors determined that given the

worst case drift, B phase at 812 amps, and an initial setpoint of 3850 amps (middle of

the established ban), the resulting drift would have resulted in a value above the motor

starting current.

Analysis. The inspectors referenced IMC 0612 and determined that the finding was more

than minor because it affected the Barrier Integrity cornerstone objective to provide

reasonable assurance that the containment physical design barriers protect the public

from radio nuclide releases caused by accidents or events and the cornerstone attribute

of human performance. The inspectors referenced IMC 0609 for the SDP and

determined that the finding is Green (very low safety significance) because it did not

impact design deficiencies, result in a loss of system safety functions, exceed related TS

outage times, nor involve a seismic, flooding, or severe weather initiating event. This

finding contains aspects relating to the cross-cutting area of human performance.

Enforcement. TS 5.4.1.a, requires that written procedures shall be established,

implemented, and maintained as documented in RG 1.33, Appendix A, of which Part 9

stipulates procedures for maintenance. Procedure 0-EPM-302-02, step 6.19.4.a.2

stated, If the trip setpoint is within tolerance (80-120 percent) that was recorded in step

6.19.1, then go to substep 6.19.4.b, and if not, then make adjustments using Attachment

5, Instantaneous And Short-Time Pickup Adjustment, and repeat steps 6.19.4.a.1 and

6.19.4.a.2. Contrary to the above, on February 19, 2005, this step was not properly

implemented or followed resulting in improper instantaneous overload setpoints on B

and C phases and a subsequent trip of 2-QS-P-1B. This finding is of very low safety

significance or Green, is in the licensees CAP as Plant Issue N-2005-3225, and thus is

characterized as an NCV, consistent with Section VI.A of the NRC's Enforcement Policy:

NCV 05000339/2005004-05, Failure to Follow Procedures Affecting Safety-Related

Breakers.

1R23

Temporary Plant Modifications

a.

Inspection Scope

The inspectors reviewed two temporary plant modifications to verify that the modifications

did not affect system operability or availability as described by the TS and UFSAR. In

addition, the inspectors verified that the installation of the temporary modifications was in

accordance with the work package, that adequate controls were in place, procedures and

drawings were updated, and post-installation tests verified the operability of the affected

systems.

The temporary plant modifications reviewed were:

Temporary Modification 2005-1759, Install 3" Float Stop Backflow Preventer in

Floor Drains Located in Emergency Switchgear Fan Rooms; and,

Temporary Modification 2005-1761, Construction of a Temporary Dam (approx

1/2" tall) on top of Tandem Seal Package for 1-RS-P-2A to help trouble shoot

numerous seal head tank HI-LO level alarms (IT-C4).

17

Enclosure

b.

Findings

No findings of significance were identified.

Cornerstone: Emergency Preparedness

1EP2 Alert and Notification System Testing

a.

Inspection Scope

The inspectors evaluated the adequacy of licensee methods for testing the alert and

notification system in accordance with NRC Inspection Procedure 71114, Attachment 02,

Alert and Notification System (ANS) Testing. The applicable planning standard 10 CFR Part 50.47(b)(5) and its related 10 CFR Part 50, Appendix E, Section IV.D requirements

were used as reference criteria. The criteria contained in NUREG-0654, Criteria for

Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1, was also used as a

reference.

The inspectors reviewed various documents which are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

1EP3 Emergency Response Organization Augmentation

a.

Inspection Scope

The inspectors reviewed the Emergency Response Organization (ERO) augmentation

staffing requirements and the process for notifying the ERO to ensure the readiness of

key staff for responding to an event and timely facility activation. The inspectors

reviewed the results of the February 22, 2005, unannounced off-hours augmentation drill

and reviewed the backup notification systems. The qualification records of key position

ERO personnel was reviewed to ensure all ERO qualifications were current. A sample of

problems identified from augmentation drills or system tests performed since the last

inspection were reviewed to assess the effectiveness of corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 03, Emergency Response Organization (ERO) Augmentation Testing. The

applicable planning standard, 10 CFR 50.47(b)(2) and its related 10 CFR 50, Appendix E

requirements were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment to this

report.

18

Enclosure

b.

Findings

No findings of significance were identified.

1EP4 Emergency Action Level and Emergency Plan Changes

a.

Inspection Scope

The inspectors evaluated the associated 10 CFR 50.54(q) reviews associated with non-

administrative emergency plan, implementing procedures and Emergency Action Level

(EAL) changes. The inspectors reviewed Emergency Plan revisions 29 and 30 and

reviewed 10 CFR 50.47(q) evaluations for the period covering July 2004 to July 2005.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 01, Emergency Action Level and Emergency Plan Changes. The

applicable planning standard, 10 CFR 50.47(b)(4) and its related 10 CFR 50, Appendix E

requirements were used as reference criteria. The criteria contained in NUREG-0654,

Criteria for Preparation and Evaluation of Radiological Emergency Response Plans and

Preparedness in Support of Nuclear Power Plants, Revision 1 and RG 1.101 were also

used as references.

The inspectors reviewed various documents which are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

1EP5 Correction of Emergency Preparedness Weaknesses and Deficiencies

a

Inspection Scope

The inspectors reviewed the corrective actions identified through the Emergency

Preparedness (EP) program to determine the significance of the issues and to determine

if repeat problems were occurring. The facilitys self-assessments and audits were

reviewed to assess the licensees ability to be self-critical, thus avoiding complacency

and degradation of their EP program. In addition, inspectors reviewed licensees self-

assessments and audits to assess the completeness and effectiveness of all EP-related

corrective actions.

The inspection was conducted in accordance with NRC Inspection Procedure 71114,

Attachment 05, Correction of Emergency Preparedness Weaknesses and Deficiencies.

The applicable planning standard, 10 CFR 50.47(b)(14) and its related 10 CFR 50,

Appendix E requirements were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment to this

report.

19

Enclosure

b.

Findings

No findings of significance were identified.

1EP6 Drill Evaluation

a.

Inspection Scope

On September 13, 2005, the inspectors reviewed and observed the performance of an

simulator drill that involved a loss of Bearing Cooling Pumps with a subsequent reactor

trip, followed by increased primary plant leakage, a small block LOCA and a loss of

instrument air. The inspectors assessed emergency procedure usage, emergency plan

classification, notifications, and the licensees identification and entrance of any problems

into their CAP. This inspection evaluated the adequacy of the licensees conduct of the

drill and critique performance. Drill issues were captured by the licensee in their CAP

and were reviewed by the inspectors.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control to Radiologically Significant Areas

a.

Inspection Scope

Access Control. Licensee activities for monitoring workers and controlling access to

radiologically significant areas were inspected. The inspectors evaluated procedural

guidance and directly observed implementation of administrative and physical controls;

appraised radiation worker and technician knowledge of, and proficiency in implementing,

Radiation Protection (RP) program activities; and assessed worker exposures to

radiation and radioactive material.

Radiological postings and material labeling were directly observed during tours of the

auxiliary building, external buildings and the independent spent fuel storage installation

(ISFSI). Inspectors conducted independent surveys in the auxiliary building and the

ISFSI to verify posted radiation levels and to compare with current licensee survey

records. During plant tours, control of High Radiation Area (HRA), HRA with dose rates

greater than 15 rem/hr and very HRA keys and the physical status of HRA doors were

examined. In addition, the inspectors observed radiological controls for non-fuel items

stored in the spent fuel pools. The inspectors also reviewed selected RP procedures and

radiation work permits (RWPs), and discussed current access control program

implementation with RP supervisors.

20

Enclosure

During the inspection, radiological controls for work activities in HRAs were observed and

discussed. The inspectors observed workers adherence to RWP guidance and Health

Physics Technician (HPT) proficiency in providing job coverage. Controls for limiting

exposure to airborne radioactive material were reviewed and operation of ventilation units

and positioning of air samplers were also observed. The inspectors evaluated electronic

dosimeter alarm set points for consistency with radiological conditions in auxiliary

building, decontamination building and the ISFSI. In addition, the inspectors interviewed

workers to assess knowledge of RWP requirements.

The inspectors evaluated worker exposures through review of data associated with

discrete radioactive particle and dispersed skin contamination events. Controls used for

monitoring extremity doses and the placement of dosimetry when work involved

significant dose gradients were reviewed. The inspectors discussed the processes that

would be used if an individual were to have an uptake of radioactive materials.

RP program activities were evaluated against 10 CFR Part 20; RG 8.38, Control of

Access to High and Very High Radiation Areas in Nuclear Power Plants; and approved

licensee procedures. Licensee guidance documents, records, and data reviewed are

listed in the Attachment.

Problem Identification and Resolution. Five plant issues and two audits associated with

radiological controls, personnel monitoring, and exposure assessments were reviewed

and discussed with RP supervisors. The inspectors assessed the licensees ability to

identify, characterize, prioritize, and resolve the identified issues in accordance with

licensee procedures VPAP-1501, Deviations, and VPAP-1601, Corrective Action.

Specific documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified.

2OS3 Radiation Monitoring Instrumentation

a.

Inspection Scope

Radiation Monitoring Instrumentation and Post-Accident Sampling. During tours of the

auxiliary building and Spent Fuel Pool building, the inspectors observed installed

radiation detection equipment including the following instrument types: Area Radiation

Monitors (ARMs), Continuous Air Monitors (CAMs), Personnel Contamination Monitors

(PCMs), and components of the Post-Accident Sampling System (PASS). The

inspectors observed the physical location of the components, noted the material

condition, and compared sensitivity ranges with the UFSAR. The inspectors also

observed HPT selection and use of portable instruments during a survey of the ISFSI

perimeter fence and support of work in a decontamination building.

In addition to equipment walk-downs, the inspectors observed functional checks and

alarm setpoint testing of various fixed and portable detection instruments. These

21

Enclosure

observations included response checks of portable ion chambers and teletectors, PCMs,

Small Article Monitors (SAMs), Portal Monitors, and a Whole Body Counter (WBC). The

10 CFR Part 61 analysis for Dry Active Waste was reviewed to determine if calibration

and response check sources are representative of the plant source term.

The inspectors reviewed calibration records for a selected PCM, portal monitors, SAM,

and WBC, ARM channel RM-153, Fuel Pit Bridge ARM, and for all Unit 1 containment

high-range ARMs (channels RM-165 and 166). The records were evaluated to determine

frequency and adequacy of the calibrations. Calibration stickers on portable survey

instruments were noted during inspection of storage areas for ready-to-use equipment.

In addition, the inspectors discussed in-place radiation detection system reliability with

the responsible engineer.

Operability and reliability of selected radiation detection instruments were reviewed

against details documented in the following: 10 CFR Part 20; NUREG-0737, Clarification

of TMI Action Plan Requirements; TS Section 3; UFSAR Chapter 12; and applicable

licensee procedures. Documents reviewed during the inspection are listed in the

Attachment.

Self-Contained Breathing Apparatus (SCBA) and Protective Equipment. Selected SCBA

units staged for emergency use in the Control Room and other locations were inspected

for material condition, air pressure, and number of units available. The inspectors also

reviewed maintenance records for components of selected SCBA units for the past five

years and certification records associated with supplied air quality.

Qualifications for licensee staff responsible for testing and repairing SCBA equipment

were evaluated through review of manufacturer training certificates. In addition, selected

Control Room operators were interviewed to determine their knowledge of available

SCBA equipment locations, including corrective lens inserts if needed, and their training

on bottle change-out during periods of extended SCBA use. Respirator qualification

records were reviewed for several Control Room operators and Maintenance department

personnel assigned emergency response duties.

Licensee activities associated with maintenance and use of respiratory protection

equipment were reviewed against 10 CFR Part 20; RG 8.15, Acceptable Programs for

Respiratory Protection; ANSI-Z88.2-1992, American National Standard for Respiratory

Protection; and applicable licensee procedures. Documents reviewed during the

inspection are listed in the Attachment.

Problem Identification and Resolution. Five plant issues and one audit associated with

instrumentation and protective equipment were reviewed and assessed. The inspectors

evaluated the licensees ability to identify, characterize, prioritize, and resolve the

identified issues in accordance with procedure VPAP-1601, Corrective Action.

Documents reviewed are listed in the Attachment.

22

Enclosure

b.

Findings

No findings of significance were identified.

Cornerstone: Public Radiation Safety

2PS1 Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

a.

Inspection Scope

Effluent Processing Equipment. The inspectors reviewed the operability and reliability of

selected radioactive effluent process sampling and detection equipment used for routine

and accident monitoring activities. Inspection activities included review of the most

recent calibration records and direct observation of select monitors. The inspectors

observed the material condition of the effluent monitoring equipment and assessed the

installed configurations, where accessible. The inspectors also reviewed applicable parts

of licensee procedures related to effluent monitoring equipment calibration.

Selected parts of the liquid radioactive waste (radwaste) system were examined and

reviewed with cognizant count room staff. The inspectors discussed with cognizant count

room staff liquid waste release permits. In addition, the inspectors directly observed the

collection and analysis of liquid effluent samples taken from the clarifier tank.

Major waste gas system components were inspected and discussed with cognizant count

room staff. Also, cognizant count room staff were interviewed regarding the gaseous

radwaste system configuration and effluent monitor operation. Inspectors also observed

Instrumentation and Calibration staff performing a calibration of the service water

discharge radiation monitor (RM-SW-108).

Installed configuration, material condition, operability, and reliability for selected effluent

sampling and monitoring equipment were reviewed against details documented in

10 CFR Part 20; UFSAR Section 11, Off-Site Dose Calculation Manual (ODCM); and RG 1.21, "Measuring, Evaluating, and Reporting Radioactivity in Solid Wastes and Releases

of Radioactive Materials in Liquid and Gaseous Effluents from Light-Water-Cooled

Nuclear Power Plants." Procedures and records reviewed during the inspection are

listed in the Attachment.

Effluent Release Processing and Quality Control (QC) Activities. The inspectors directly

observed and evaluated licensee proficiency in effluent release processing during

preparation of a containment purge weekly release permit. The inspectors also reviewed

effluent release procedural guidance.

QC activities regarding gamma spectroscopy and liquid scintillation counting

instrumentation were discussed with cognizant count room staff. The inspectors

reviewed records of daily QC checks and trending data for selected gamma

spectroscopy detectors. In addition, results of the radiochemistry cross-check program

23

Enclosure

were discussed for years 2003 and 2004. The inspectors also reviewed the 2003 and

2004 Annual Effluent Reports to identify any anomalous releases.

Observed task evolutions, offsite dose results, and count room activities were evaluated

against RG 1.21 guidance, 10 CFR Part 20 requirements, Appendix I to 10 CFR Part 50

design criteria, UFSAR details, and ODCM requirements. Documents reviewed are listed

in the Attachment.

Problem Identification and Resolution. Select plant issues associated with effluent

release activities were reviewed and assessed. The inspectors evaluated the licensees

ability to identify, characterize, prioritize, and resolve the identified issues in accordance

with procedure VPAP-1601, Corrective Action, and associated guideline documents.

Documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified.

2PS3 Radiological Environmental Monitoring Program (REMP) and Radioactive Material

Control Program

a.

Inspection Scope

REMP Implementation. The inspectors reviewed the licensees most recent Annual

Radiological Environmental Operating Reports for 2003 and 2004 which described

implementation of the REMP and provided an assessment of the program results.

Information regarding surveillance results, analysis of data, land use census, the

interlaboratory comparison program, and permitted program deviations were evaluated.

The inspector also reviewed and discussed implementation of the REMP with respect to

sampling locations, monitoring and measurement frequencies.

The inspectors observed collection of air particulate filters and charcoal cartridges at five

air sampling stations and assessed sample collection methodology and techniques.

Calibration procedures and records for the air sampling stations were reviewed. The

inspectors also observed thermoluminescent dosimeters (TLDs) placement at eight

locations as described in the ODCM.

Through the above reviews and observations, the licensees practices and

implementation of their radiological monitoring program were evaluated by the inspectors

for consistency with the ODCM, UFSAR, TS, and 10 CFR Part 20 requirements.

Meteorological Monitoring Program. The inspectors reviewed the operability of the

meteorological monitoring equipment and operator access to meteorological data.

Current meteorological monitoring equipment performance was reviewed with the system

engineer. Licensee technicians primarily responsible for equipment maintenance and

surveillance were interviewed by the inspectors concerning equipment performance,

reliability, and routine inspections.

24

Enclosure

Calibration procedures and records for the two most recent calibrations of the

meteorological monitoring instruments for air temperature and for wind speed and

direction were also reviewed. The inspectors evaluated the operability of instruments

and determined the availability of current meteorological conditions displayed in the

Control Room for the primary tower.

Meteorological monitoring program implementation and results were reviewed against

TS, ODCM guidance, and procedures listed in the Attachment.

Unrestricted Release of Materials from the Radiologically Controlled Area (RCA). The

inspectors reviewed and evaluated radiation protection program activities associated with

the unconditional release of licensed materials from RCA locations. Licensee guidance

and implementation of RCA exit monitoring activities were evaluated against 10 CFR Part 20 requirements and applicable procedures documented in the Attachment.

Problem Identification and Resolution. The inspectors reviewed audits, and selected

Plant Issues associated with REMP operations and the program for unrestricted release

of materials from the RCA. The inspectors assessed the licensees ability to identify,

characterize, prioritize, and resolve the identified issues in accordance with licensee

procedures VPAP-1601, Corrective Action. Specific Plant Issues reviewed and evaluated

in detail for these program areas are identified in the Attachment.

b.

Findings

No findings of significance were identified.

4.

OTHER ACTIVITIES

4AO1 Performance Indicator (PI) Verification

Emergency Preparedness PI Verification

a.

Inspection Scope

The inspectors reviewed the licensees procedure for developing the data for the

Emergency Preparedness PI which are: (1) Drill and Exercise Performance (DEP); (2)

ERO Drill Participation; and (3) ANS Reliability. The inspectors examined data reported

to the NRC for the period June, 2004, to June, 2005. Procedural guidance for reporting

PI information and records used by the licensee to identify potential PI occurrences were

also reviewed. The inspectors verified the accuracy of the PI for ERO drill and exercise

performance through review of a sample of drill and event records. The inspectors

reviewed selected training records to verify the accuracy of the PI for ERO drill

participation for personnel assigned to key positions in the ERO. The inspectors verified

the accuracy of the PI for alert and notification system reliability through review of a

sample of the licensees records of periodic system tests.

25

Enclosure

The inspection was conducted in accordance with NRC Inspection Procedure 71151,

Performance Indicator Verification. The applicable planning standards, 10 CFR 50.9

and NEI 99-02,Regulatory Assessment Performance Indicator Guidelines, Revision 3,

were used as reference criteria.

The inspectors reviewed various documents which are listed in the Attachment to this

report.

b.

Findings

No findings of significance were identified.

Radiation Safety PI Verification

a.

Inspection Scope

The inspectors sampled licensee records to verify the accuracy of reported PI data for

the periods listed below. To verify the accuracy of the reported PI elements, the

reviewed data were assessed against guidance contained in NEI 99-02, "Regulatory

Assessment Indicator Guideline," Rev. 3, and the Performance Indicator Frequently

Asked Questions (FAQ) list.

Occupational Radiation Safety Cornerstone

Occupational Exposure Control Effectiveness

The inspectors reviewed the Occupational Exposure Control Effectiveness PI results for

the period of January 2004 through June 2005. For the assessment period, the

inspectors reviewed HP shift log entries, electronic dosimeter alarm logs, and licensee

procedural guidance for collecting and documenting Performance Indicator data. Plant

Issues were reviewed for uptakes and abnormal TLD results. Report section 2OS1

contains additional details regarding the inspection of controls for high dose areas and

review of related Plant Issues. Documents reviewed are listed in the Attachment.

Public Radiation Safety Cornerstone

Radiological Control Effluent Release Occurrences

The inspectors reviewed the Radiological Control Effluent Release Occurrences PI

results for the period of January 2004 through June 2005. For the assessment period,

the inspectors reviewed cumulative and projected doses to the public. The inspectors

also reviewed licensee procedural guidance for collecting and documenting PI data.

Documents reviewed are listed in the Attachment.

b.

Findings

No findings of significance were identified.

26

Enclosure

4OA2 Identification and Resolution of Problems

.1

Daily Review

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify repetitive equipment failures or specific human performance

issues for follow-up, the inspectors performed a daily screening of items entered into the

licensees CAP. This review was accomplished by reviewing daily Plant Issues summary

reports and periodically attending daily Plant Issue Review Team meetings.

.2

Annual Sample Review

a.

Inspection Scope

The inspectors reviewed the licensees assessments and corrective actions for Plant

Issue N-2005-2320, during the performance of 1-PT-71.1Q (1-FW-P-2, Turbine Driven

Auxilliary Feedwater (TDAFW) pump), noted the outboard bearing slinger ring leaking oil

at approximately 3-4 drops per second. The Plant Issue was reviewed to ensure that

the full extent of the issue was identified, an appropriate evaluation was performed, and

appropriate corrective actions were specified and prioritized. The inspectors also

evaluated the Plant Issue against the requirements of the licensees CAP as specified in

VPAP-1601, Corrective Action Program, VPAP-1501, Deviations and 10 CFR 50,

Appendix B. Additional documents reviewed are listed in the Attachment.

b.

Findings and Observations

No findings of significance were identified. On June 21, 2005, the licensee initiated Plant

Issue N-2005-2320 in response to an oil leak on the Unit 1 TDAFW pump outboard

bearing identified during the quarterly surveillance test. The licensee completed a

functional evaluation and declared a GL 91-18 condition (operable but degraded) for the

component. During subsequent testing, the licensee better quantified the leak at 1.58

gallons per day as opposed to the original estimate of 8.5 gallons per day. The

inspectors verified the licensee functional evaluation which considered the following facts

that the design basis accident mission time for TDAFW operation is 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> and that the

pump oil reservoir is maintained at 12 - 18 gallons of which 8 gallons are below pump

suction. This would result in a leakage of .53 gallons during the 8 hour9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> mission time

resulting in the maintenance of pump operability. The inspectors reviewed the history of

bearing oil leaks for the Unit 1 and 2 TDAFW pumps which included work order,

00505761-01, for an oil leak on the Unit 1 TDAFW pump outboard bearing which was

completed on September 18, 2004. The licensee subsequently identified this corrective

action as rework. The inspectors also found for the Unit 2 TDAFW pump an Item

Equivalency Evaluation Review (IEER) report, N95-5022-000, which installed new seals

of a different design due to similar problems of oil leakage. The licensee could not

explain why this same design had not been considered for the Unit 1 TDAFW pump. The

inspectors reviewed the IEER process as implemented by VPAP-0708, Item Equivalency

Evaluation, and the corrective action process as implemented by VPAP-1601 and

VPAP-1501. The inspectors determined that VPAP-0708 did not perform an extent of

27

Enclosure

condition review nor reference, consider or require a plant issue. The inspectors also

determined that neither VPAP-1601 or VPAP-1501 discussed the IEER process as part

of the CAP. The inspectors concluded the failure to implement adequate corrective

action for the Unit 1 TDAFW pump constituted a minor violation. This finding is not yet

captured in the licensees corrective action program.

4OA4 Cross-cutting Aspects of Findings

Section 1R04 describes a finding associated with human performance involving

inadequate design control relating to verification of design adequacy. The inspectors

determined that information relating to the SW system pressure loads was known within

the engineering organization. However, this information was neither transferred into the

modification design, nor was the design verified to ensure the S/Rs were adequate for

the replacement expansion joints.

Section 1R06 describes a finding for inadequate corrective action resulting a flood

problem for the safeguards instrument rack room. The inspectors determined that

previous corrective actions and plant area flood reviews failed to identify the

ACCR/ACFR floor drain flood path.

Section 1R14 documents two findings associated with corrective action problems:

The first finding involves two circumstances in which lightning impacts the same

Unit 2 instrumentation in each case with one involving a reactor trip. For both

cases, the licensee took no corrective action and instead attributed the cause to

either outside the control of the company, or an isolated event from the

extremely dry soil conditions affecting the grounding grid that year; and,

The second finding for inadequate corrective action concerns a failure to involve

the valve vendor to obtain important information relative to the problem. Once the

vendor was involved to obtain the correct torque information for the valve

actuator, actions were untimely and allowed a subsequent leak forcing a unit

shutdown.

Section 1R22 describes two findings associated with human performance relating to a

failure to follow procedure:

The first finding concerning SSPS testing involved two maintenance technicians

of which one incorrectly identified a card on which the trip switches would be

manipulated and the second incorrectly performed independent verification of the

card contrary to procedure requirements; and,

The second finding concerning breaker maintenance involved a supplemental

employee who failed to adhere to procedure requirements to ensure as left

overload setpoints were within the specified band.

28

Enclosure

4OA5 Other Activities

.1

(Closed) Temporary Instruction (TI) 2515/161 Transportation of Reactor Control Rod

Drives in Type A Packages

a.

Inspection Scope

The inspectors reviewed shipping logs and discussed shipment of Reactor Control Rod

Drives (CRD) in Type A packages with shipping staff. The inspectors noted that no

shipments of Reactor CRDs in Type A packages have been made since January 1, 2002.

b.

Findings

No findings of significance were identified.

.2

(Discussed) Temporary Instruction (TI) 2515/163, Operational Readiness of Offsite

Power

Completion of this TI was documented in NRC Inspection Report Nos. 05000338,

339/2005003. However, after an NRC headquarters review of the data provided,

additional information related to the TI was requested. The inspectors collected this

information from licensee discussions, site procedures and licensee documentation. The

information was subsequently provided to the headquarters staff for further analysis.

.3

Independent Spent Fuel Storage Installation (ISFSI) Radiological Controls

a.

Inspection Scope

The inspectors conducted independent gamma and neutron surveys of the ISFSI facility

and compared the results to previous surveys. The inspectors also observed and

evaluated implementation of radiological controls, including RWPs and postings, and

discussed the controls with a HPT and RP supervisory staff. Radiological controls for

loading the ISFSI casks were also reviewed and discussed.

Radiological control activities for ISFSI areas were evaluated against 10 CFR Part 20, 10

CFR Part 72, and applicable licensee procedures. Documents reviewed are listed in

section 4OA5 of the Attachment

b.

Findings

No findings of significance were identified.

4OA6 Meetings, including Exit

On September 22, 2005, the senior resident inspector and the reactor projects branch

chief presented the inspection results to Mr. Jack Davis and other members of the staff.

29

Enclosure

The licensee acknowledged the findings. The inspectors confirmed that proprietary

information was not provided or examined during the inspection.

4OA7 Licensee-Identified Violation

The following finding of very low significance was identified by the licensee and is a

violation of NRC requirements which meets the criteria of Section VI of the NRC

Enforcement Policy, NUREG-1600, for being dispositioned as an NCV.

TS 5.4.1 requires that written procedures shall be established, implemented, and

maintained covering the activities in the applicable procedures recommended by RG 1.33, Revision 2, Appendix A, February 1978, of which Part 2 requires general plant

operating procedures. Contrary to the above, on August 6, 2005, the licensee failed to

implement step 5.36 of operating procedure 1-OP-2.2, Unit Power Operation From

Mode 1 to Mode 2, which requires the performance of power range low setpoint channel

operational tests to comply with TS surveillance requirement 3.3.1.8. The licensee

discovered the procedure noncompliance during plant startup requirements, entered TS

SR 3.0.3 and successfully completed the required testing. The inspectors reviewed IMCs

0612 and 0609, and determined that the finding was of very low safety significance given

the successful completion of the surveillance tests. The licensee has this finding

documented in their CAP as Plant Issue N-2005-2980.

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee personnel

W. Anthes, Assistant Manager, Maintenance

G. Bischof, Director, Nuclear Safety and Licensing

J. Breeden, Supervisor, Radioactive Analysis and Material Control

W. Corbin, Director, Nuclear Engineering

J. Crossman, Assistant Manager, Nuclear Operations

J. Costello, Supervisor, Nuclear Emergency Preparedness (Virginia)

J. Davis, Site Vice President

R. Evans, Manager, Radiological Protection

R. Foster, Supply Chain Manager

S. Hughes, Manager, Nuclear Operations

P. Kemp, Supervisor, Nuclear Safety & Licensing

J. Kirkpatrick, Manager, Maintenance

L. Lane, Director, Operations and Maintenance

J. Leberstien, Licensing Technical Advisor

T. Maddy, Manager, Nuclear Protection Services

M. Main, Component Engineer

C. McClain, Manager, Organizational Effectiveness

F. Mladen, Manager, Nuclear Site Services

B. Morrison, Assistant Engineering Manager

J. Rayman, Emergency Planning Supervisor

H. Royal, Manager, Nuclear Training

M. Sartain, Manager, Nuclear Engineering

J. Scott, Supervisor, Nuclear Training (operations)

G. Salomone, Licensing

R. Williams, Component Engineer

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

05000338, 339/2005004-02 URI

Inadequate Corrective Action Results in Safeguards

Instrument Rack Room Flood Problem (Section 1R06)

Opened and Closed

05000338, 339/2005004-01 NCV

Inadequate Design Control Results in Degradation of SW

Supports/Restraints (Section 1R04.2)05000338/2005004-03

NCV

Inadequate Maintenance of a Procedure Results in Loss of

Safety Related 480V Buses (Section 1R12)05000339/2005004-03

NCV

Failure to Identify and Correct Deficiencies in

Instrumentation Results In Reactor Trip (Section 1R14.1)

A-2

Attachment

05000338/2005004-04

FIN

Untimely Corrective Actions for Actuator Oil Leakage on

Turbine Interface Valve Results in Rapid Down power

(Section 1R14.2)05000339/2005004-04

NCV

Failure to Follow Procedures During Solid State Protection

System Testing (Section 1R22.1)05000339/2005004-05

NCV

Failure to Follow Procedures Affecting Safety-Related

Breakers (Section 1R22.2)

Closed

05000338/2005003-01

URI

Inadequate Maintenance of a Procedure Results in Loss of

Safety Related 480V Buses (Section 1R12)

2515/161

TI

Transportation of Reactor Control Rod Drives In Type A

Packages (Section 4OA5)

Discussed

2515/163

TI

Operational Readiness of Offsite Power (Section 4OA5.1)

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

Documents

List of open work orders for Unit 2 SW components

List of plant issues since 2004 for Unit 2 SW components

TS 3.7.8, "Service Water (SW) System"

Plant Issue N-2005-2927, NRC identified issue with loose tie rods on SW

expansion joints associated with RS heat exchanger supply and return piping.

Plant Issue N-2005-3376, NRC identified issue with loose tie rods on SW

expansion joints associated with the SBO diesel generator.

0-OP-49.1, Service Water System Normal Operation

Module, NCRODP-13-NA, Service Water System

Root Cause Evaluation N-2005-2229, Damaged SW Supports

Engineering Transmittal, ET-CEM-05-0009, Documentation of the Results of the

Structural Review for As-Found Condition of Service Water supports in the Tie-in

Vault and Valve House Expansion Joint Vault, NAPS Units 1 & 2"

Calculation Number, CE-1799, Structural Operability Evaluation for Service

Water Lines in the Tie-In Vault and Valve House Expansion Joint Vault, NAPS 1

& 2"

Drawings

11715-FM-078A, B, C, series of flow diagrams for SW system

11715-PSSK-105AN.01, Sheets 1, 2, Pipe Support 1-WS-PH-E85.1 for

321/4"-WS-E85-151-Q3"

A-3

Attachment

11715-PSSK-105AN.02, Sheets 1, 2, 3, Pipe Support 1-WS-PH-E85.2 for

321/4"-WS-E85-151-Q3"

11715-PSSK-105AK.10, Sheets 1, 2, 3, Pipe Support 1-WS-PH-3.2 for

36"-WS-3-151-Q3"

11715-PSSK-105AK.06, Sheets 1, 2, 3, Pipe Support 1-WS-PH-4.2 for

36"-WS-4-151-Q3"

11715-WMKS-0105AMA, Sheet 1, Inservice Inspection Isometric WS Sys:36",

24", 18" Valve HSE Pipe#1"

11715-FP-5AN, Sheet 1, Plan & Sections Service Water Valve House Piping

11715-FP-5AK, Sheet 1, Service Water Buried Piping Tie-In

11715-WMKS-0105AK, Sheet 1, Inservice Inspection Isometric WS Sys:36"

Tie-In Vault

Section 1R05: Fire Protection

Documents

PI N-2005-3733, NRC identified issue regarding the lack of a corrective action

process to resolve deficiencies identified during fire drills.

UFSAR Section 9.5.1, Fire Protection System

0-FPMP-10.0, "Conduct of Fire Drills"

VPAP-2401, "Fire Protection Program"

Appendix A to Branch Technical Position APCSB 9.5-1, "Guidelines for Fire

Protection for Nuclear Power Plants Docketed Prior to July 1, 1976"

NFPA 27, "Private Fire Brigades, 1981"

Section 1R06: Flood Protection Measures

Documents

ET N-04-0043, Rev.0, Evaluation of the Potential for Flooding of the U2

Emergency Switchgear from the Turbine Building Through U2 Cable Vault Floor

Drain Check Valve, 1-DB-424"

Plant Issue N-2005-2605, Floodwalls, 1-BLD-FLW-7 and 2-BLD-FLW-5, between

the ACCR and ACFR on both units have exceeded their maintenance rule

performance criteria of 40 hours4.62963e-4 days <br />0.0111 hours <br />6.613757e-5 weeks <br />1.522e-5 months <br /> per year.

ET NAF 00-0069, Rev. 0, Summary of Components Considered in the IPE

Internal Flooding Analysis for Surry and North Anna Power Stations, Units 1&2

Calculation Number, ME-0782, Maximum Backflow Flowrate Through Floor Drain

Between Chiller Room and Fan Room - Elevation 252'-0" and 254'-0"

Plant Issue N-2005-2597, Licensee identified issue with air gap in Unit 1

instrument rack room sump pump discharge piping (i.e., piping discharges to a

funnel at elevation of adjacent fan room)

Plant Issue N-1990-0020, IN 83-44-S1, Potential damage to redundant safety

equipment as a result of backflow through the equipment and floor drain system

Plant Issue N-2005-2251, licensee identified issue of modification, DCP

59-92-161 that installed a backflow preventer in the charging pump cubicle drain

as part of the internal flood protection program but station drawing, 11715-FB-9A,

sheet 1 was not revised to add mark numbers to the drawing

A-4

Attachment

Engineering transmittal, ET-CEP-00-0006, Rev. 0, Evaluation of The Potential

For Flooding In The Emergency Switchgear Rooms North Anna Power Station,

Units 1 & 2"

Engineering Work Request,90-131, NP-1971, Outside containment Flooding

Protection, recommended the modification of the instrument rack room sump

pumps for Unit 1 & 2. These pumps are to be automatic with level alarm

indication.

UFSAR Section 9.3.3.2, System Description

Drawings

11715-FB-26A, Plumbing Service Building - Sheet 1 of 1, Revision 18

Section 1R12: Maintenance Effectiveness

Documents

WO 00523899

SDBD- NAPS-QS, Revision 06

WO 00487833, HHSI seal replacement (TYPICAL)

WO 52002302, SW hand torque valve (TYPICAL)

WO 51440701, Replace SI valve stem (TYPICAL)

Response to Adverse Trend Plant Issue N-2005-0478, electrical maintenance

August 2005

Procedures

VPAP-0815, Maintenance Rule Program, Revision 14

STD-GN-0044, Supplemental Maintenance Rule Guidelines, Revision 4

Plant Issues

N-2000-2600, bottled air flow problems

N-2001-2479, HHSI motors (TYPICAL)

N-2002-1125, 1-HV-P-22C motor problems

N-2002-1875, Service water spray arrays

N-2002-2951, refrigerant leak control room chiller

N-2002-3065, HHSI pump seals

N-2003-1801, SW stainless steel MIC problems

N-2004-0053, while repairing compressor terminal plate under WO 489188-01,

found internal compressor motor protection device disabled

N-2004-2193, 1H EDG

N-2004-2368, RWST chillers

N-2004-2382, transform deluge system heat detectors

N-2004-5064, service and instrument air compressor timers

N-2005-0605, 1-HV-P-22A, high vibration control room chiller

N-2005-1615, H/J 480 VAC buses

N-2004-2195, 2-QS-MR-1A #2 fan motor bad and locking up

N-2004-2368, found 01-QS-MR-1B breaker tripped, compressor failed due to

starter contacts welded together

N-2004-4434, RWST temp is 47 degrees with no chiller running

A-5

Attachment

N-2004-4844, observed 14 day trend of U2 RWST temperature shows continual

increase from 42 degrees to 46 degrees

N-2005-1177, DCP and parts delays may require re-evaluation f (a)1 corrective

action dates associated with replacement of 1/2 QS-MR-1A/B

N-2005-2494, 2-CH-P-1C had a 20 ml/minute outboard endbell leak

N-2005-2536, 2-CH-P-1C was disassembled for OB mechanical seal leakage and

high vibes on the OB bearing

N-2005-2584, 2-QS-MR-1A Unit 2 A RWST chiller tripped on oil failure relay

N-2005-2610, 2-QS-MR-1B, Unit 2 B RWST chiller tripped with RWST

temperature at 45 degrees

Section 1R17: Permanent Plant Modifications

Documents

Design Change Package 04-019, RSST 34.5 kV Cable Replacement / North

Anna / Units 1 & 2"

Procedure 1-MOP-26.77, A RSS Transformer and D Transfer Bus, Revision

18

Procedure 1-MOP-26.78, B RSS Transformer and E Transfer Bus, Revision

18-P2

Procedure 1-MOP-26.79, C RSS Transformer and F Transfer Bus, Revision 17

Drawings

11715-FE-1BB

11715-FE-1BD

11715-FE-1A

Section 1R19: Post Maintenance Testing

Documents

Plant Issue N-2005-1061, Valves 1-BC-MOV-127 and 2-BC-MOV-227 are being

installed to support new BC tower returning to service

Procedure 0-ECM-1401-03, General Maintenance of Electrical Motors, Revision

31

Procedure 0-ECM-0206-01, Installation of Lugs, Revision 6

Section 1EP2: Alert and Notification System Testing

Procedures

0-EPM-0501-01, Early Warning System Preventive Maintenance, Revision 14

0-PT-172.3, Early Warning System Polling Function Test, Revision 0

0-PT-172.2, Early Warning System Sirens Activation Monitoring, Revision 2

Records and Data

Siren Problem Tracking Report

Various Plant Issues written against NAPS Sirens

Six Quarterly Data packages from 3/1/04to 4/17/2005 for 0-PT-172.2, Early

Warning System Sirens Activation Monitoring

A-6

Attachment

Miscellaneous

Sterling Siren Technical manual

WPS-2800 Series High Power Voice & Siren System - Installation & Instruction

Manual

Section 1EP3: Emergency Response Organization Augmentation

Procedures

EPIP-3.05, Augmentation of Emergency Response Organization, Revision 2

Records and Data

VPAP-2601, Attachment 3, Augmentation Capability Assessment of Emergency

Response Organization, 02/22/2005 at 1800

VPAP-2601, Attachment 3, Augmentation Capability Assessment of Emergency

Response Organization, 03/18/2004 at 2000

VPAP-2601, Attachment 3, Augmentation Capability Assessment of Emergency

Response Organization, 04/07/2004 at 1900

Section 1EP4: Emergency Action Level and Plan Changes

Records and Data

10 CFR50.54(q) Review for North Anna Power Station Emergency Plan Revision

29

10 CFR50.54(q) Review for North Anna Power Station Emergency Plan Revision

30

North Anna Power Station Emergency Plan Revision 29

North Anna Power Station Emergency Plan Revision 30

Procedures

EPIP-1.01, Emergency Manager Controlling Procedure, Revision 40

EPIP-2.01, Notification of State and Local Governments, Revision 27

EPIP-4.07, Protective Measures, Revision 16

EPIP-1.06, Protective Action Recommendations, Revision 6

Section 1EP5: Correction of Emergency Preparedness Weakness and Deficiencies

Records and Data

Report of Declaration: Notification of Unusual Event Declared at North Anna

Power Station on October 8, 2004

North Anna Power Station June 7, 2005 Training Exercise/Medical Drill Critique

Results, Resolution Report and Ongoing Self Assessment

North Anna Power Station June 7, 2005 Training Exercise/Medical Drill Exercise

Manual

North Anna Power Station May 5, 2005 Training Exercise Critique Results,

Resolution Report and Ongoing Self Assessment

North Anna Power Station May 5, 2005 Training Exercise Manual

North Anna Power Station March 1, 2005 Training Exercise Critique Results,

Resolution Report and Ongoing Self Assessment

North Anna Power Station March 1, 2005 Training Exercise Manual

A-7

Attachment

Section 2OS1: Access Control to Radiologically Significant Areas

Procedures, Manuals, and Guides

Health Physics Procedure Number C-HP-1020.011, Radiological Protection

Action Plan During Diving Activities, Revision 3

Health Physics Procedure Number C-HP-1031.021, Dosimetry Requirements for

Site Restricted Areas, Revision 6

Health Physics Procedure Number C-HP-1031.022, RWP Dosimetry: Exposure

Control Support, Revision 9

Health Physics Procedure Number C-HP-1032.020, Radiological Survey Criteria

and Scheduling, Revision 5

Health Physics Procedure Number Dominion, NAPS, C-HP-1032.060,

Radiological Posting and Access Control, Revision 1

Health Physics Procedure Number C-HP-1032.061, High Radiation Area Key

Control, Revision 2

Health Physics Procedure Number C-HP-1081.010, Radiation Work Permits:

Preparing and Approving, Revision 7

Health Physics Procedure Number C-HP-1081.020, Radiation Work Permits:

RWP Briefing and Controlling Work, Revision 4

Health Physics Procedure Number C-HP-1081.040, Radiation Work Permits:

Providing HP Coverage During Work, Revision 1.14

Station Administrative Procedure (SAP), No. VPAP-1501, Deviations, Revision 17

SAP, No. VPAP-1601, Corrective Action, Revision 20

Radiation Work Permits

Radiation Work Permit 05-2-1212, Obtain a sample from Spent Resin Hold-up

Tank (1-LW-TK-1) in decontamination building basement. [LHRA]

Radiation Work Permit 05-2-1502, General entry during sub-atmospheric

conditions for the purpose of walkdowns, inspections, radiological surveys, minor

maintenance and adjustments [LHRA>15 rem/hr]

Radiation Work Permit 05-2-1503, General entry by Operations, Health Physics,

Security and assorted craft personnel for the performance of routine PTs,

surveys, inspections and corrective maintenance as required. [LHRA > 15 rem/hr]

Radiation Work Permit 05-2-1504, Survey, lifting and transferring radioactive

waste liners to include associated support and placing of material into liner [LHRA

>15 rem/hr]

Corrective Action Program (CAP) Documents/Audits

Audit 03-06: Radiological Protection/ Chemistry, 9/22/2003

Audit 04-08: Radiation Protection & Process Control Programs, 9/20/2004

Plant Issue N-2005-0149-R1, A worker entered a posted Radiation Area in the

TSC without the proper dosimetry (Digital Alarming Dosimetry). The area was

posted as a Radiation Area and Radiation Work Permit required for entry.

Plant Issue N-2005-1467-R1, Observed an increase (3X) in dose rates on the

remote monitoring dosimeter by 1-LW-491 located in the Unit 1 side of demin

alley.

Plant Issue N-2005-1898, Two TLDs with abnormal readings for which a TLD re-

evaluation was requested, were confirmed as having normal response by the

A-8

Attachment

vendor on 05/20/2005. The two individuals TLD readings for the first quarter

2005 were 147 and 163 mrem, while the DAD readings totaled 0 mrem.

Plant Issue N-2005-2010, The HP lock for the Fuel Building Basement to Decon

building basement jail bar door is sticking and will not allow the door to be

opened.

Plant Issue N-2005-2184, Employee issued a DAD against the wrong RWP. The

employee should have issued a DAD against Radiation Work Permit 05-2-1505;

instead the DAD was issued against Radiation Work Permit 05-2-1105

Self Assessment: ITC-SA-04-02, Assessment of NBU for Adverse Trends in

Radiological Protection Events, 04/29/04

Section 2OS3: Radiation Monitoring Instrumentation

Procedures

Health Physics Procedure Number C-HP-1042.450, Self-Contained Breathing

Apparatus Maintenance, Revision 10

Health Physics Procedure Number C-HP-1042.520, Respiratory Protection

Program Equipment Criteria and Verification, Revision 4

Procedure No. 0-FPMP-3, SCBA Operability Test, Revision 2

Procedure No. ICP-RM-1-RMS-165, Containment High Range Radiation

Monitoring System (RMS-165), Revision 14

Procedure No. ICP-RM-1-RMS-166, Containment High Range Radiation

Monitoring System (RMS-166), Revision 15

Calibrations, Surveillance Tests, and Licensee Records

10 CFR Part 61 Analysis, Dry Active Waste (U1, U2, and Common), 12/8/04,

8/30/04, and 9/17/03

FASTSCAN WBC Calibration, 3/16/05

MSA Factory Training Certificates for Individuals Qualified to Repair SCBA Vital

Components

PCM-1B Serial No. 176, Calibrations, 6/10/04 and 6/13/05

PM-7 Serial No. 372, Calibrations, 12/1/04 and 4/18/05

RM-153, Fuel Pit Bridge ARM Calibrations, 11/1/01 and 7/9/03

RM-165 and 166, U1 Containment High Range ARM Calibrations, 165: (9/25/04,

1/15/03, 3/10/03) and 166: (9/24/01, 8/9/01, 1/15/03, 3/10/03)

SAM-11 Serial No. 177A, Calibrations, 12/1/04 and 6/7/05

SCBA Air Regulator Number ND263131, Maintenance History, 7/18/00 - 8/25/04

SCBA Qualification Records, Selected Operations and Maintenance Department

Staff

Service Air Breathing Air Quality Analyses, 11/18/03, 3/24/04, 10/21/04, 3/30/05

Source Certificate Number 98CS5001061, Cs-137 SAM-11 Calibration Source

CAP Documents/Audits

Audit 04-08, Radiation Protection & Process Control Programs, 9/20/04

SAP, No. VPAP-1601, Corrective Action, Revision 20

Plant Issue N-2004-0182, Filter not in motion alarms are occurring frequently on

2-RM-RMS-259

A-9

Attachment

Plant Issue N-2004-0991, 1-RM-RMS-163 spiking and causing numerous Hi-Hi

alarms

Plant Issue N-2004-1384, Teletector failed performance check after being used to

survey HRA

Plant Issue N-2005-0575, Electronic dosimeter not turned on prior to attempted

RCA entry

Plant Issue N-2005-2714, Respiratory qualification report showed incorrect

expiration dates

Section 2PS1: Radioactive Gaseous and Liquid Effluent Treatment and Monitoring

Systems

Procedures, Guidance Documents, and Operating Manuals

Health Physics Procedure Number HP-3010.020, Radioactive Liquid Waste

Release Permits, Revision 9

Health Physics Procedure Number HP-3010.021, Radioactive Liquid Waste

Sampling and Analysis, Revision 17

Health Physics Procedure Number HP-3010.022, Radioactive Liquid Waste

Accountability and Dose Calculations, Revision 6

Health Physics Procedure Number HP-3010.023, Abnormal Liquid Release,

Revision 1

Health Physics Procedure Number HP-3010.030, Radioactive Gaseous Waste

Release Permits, Revision 9

Health Physics Procedure Number HP-3010.031, Radioactive Gaseous Waste

Sampling and Analysis, Revision 21

Health Physics Procedure Number HP-3010.032, Radioactive Gaseous Waste

Accountability and Dose Calculations, Revision 11

Health Physics Procedure Number HP-3010.033, Abnormal Gaseous Release,

Revision 15

Health Physics Procedure Number HP-3010.040, Radiation Monitoring System

Setpoint Determination, Revision 17

SAP, Offsite Dose Calculation Manual (North Anna), Procedure Number VPAP-

2103N, Revision 7

Instrument Calibration Procedure, Number 0-1CP-SW-RM-108, Service Water

Discharge Radiation Monitor (RM-SW-108) Calibration, Revision 4

Records, Data, and Drawings

Calibration Certificates - Beckman LS-6000SC Dated 06/23/03 and Gamma

Products G-5020 Dated 06/02/04

Condenser Air Ejector In-Line Radio Gas Radiation Monitor (RM-SV-121 and 221)

Channel Calibrations, Test Results Dated 10/22/04 and 04/09/05

Discharge Tunnel Effluent Radiation Monitors (RM-SW-130 and 230) Channel

Calibrations, Test Results Dated 05/05/05 and 08/22/04

Radiological Environmental Monitoring Program, 2003

ECCS PREACS Train A and B Filter In-Place Tests (1-HV-FL-3A and 3B), Test

Results Dated 11/14/03 and 04/30/04

A-10

Attachment

Effluent Radiation Monitor Setpoint Records for 01-GW-RM-178-1, 1-SS-RM-125,

1-SV-RM-121, 1-SW-RM-108, 1-SW-RM-130, 1-VG-RM-179-1, 1-VG-RM-180-1,

2-SS-RM-225, 2-SV-RM-221, 2-SW-RM-230, RM-LW-111

Gaseous Effluents Cumulative Dose Summary for 2004 Through May 2005

Heating and Ventilation Flow A (F-HV-1212A) and B (F-HV-1212B) Channel

Calibrations, Test Results Dated 04/26/05

High Capacity Steam Generator Blowdown Radiation Monitors (RM-SS-125 and

225) Calibrations, Test Results Dated 12/15/04 and 03/24/05

Liquid Effluents Cumulative Dose Summary for 2004 Through May 2005

Liquid Waste Batch Release Permit and Record, Permit No. 04-LBATCH-01

Dated 05/14/05

Liquid Waste Clarifier Radiation Monitor (RM-LW-111) Channel Calibration, Test

Results Dated 09/03/04

Miscellaneous Gaseous Release Records, Permit Numbers 04-MGR-54 Dated

05/06/04, 04-MGR-125 Dated 09/13/04, 04-MGR-128 Dated 09/15/04, and 04-

MGR-130 Dated 09/16/04

NAPS, First Quarter 2004 Count Room Confirmatory Measurements

Process Vent Blowers Discharge Flow (1-GW-F-108) Calibration, Test Results

Dated 04/14/04

Process Vent Normal and High Range Effluent Radiation Monitor (GW-RM-178)

Channel Calibration, Test Results Dated 02/01/05

Reactor Containment Release Records, Permit Nos. 04-RXC-01 Dated 05/02/04

and 04-RXC-12 Dated 10/02/04

Results of Radiochemistry Cross Check Program, North Anna Power Station,

Third Quarter 2003

Service Water Discharge Radiation Monitor (RM-SW-108) Calibration, Test

Results Dated 07/20/05

Unplanned Gaseous Release Record, ID No. 05-AGR-01 Dated 04/04/05

Vent Stack A and B Normal and High Range Effluent Radiation Monitors (VG-RM-

179 and 180)

Channel Calibrations, Test Results Dated 02/24/05 and 06/04/04

CAP Documents/Audits

Nuclear Oversight Audit Report, No. 03-11, Offsite Dose Calculation Manual

Radiological Environmental Monitoring Program and Environmental Protection

Program, Dated 02/25/04

SAP, Number VPAP-1601, Corrective Action, Revision 20

Plant Issue N-2003-3417, Operations Failed to Notify the Health Physics Count

Room Prior to Performing Make-Up to the Unit #2 RWST

Plant Issue N-2004-3756, 1-HV-MOD-102A, A Fuel Building Exhaust Fan

Discharge Damper, Was Noted to Not Come Open When Restoring Fuel Building

Ventilation

Plant Issue N-2004-4089, A Service Water Sample From the Catch Basin

244'Auxiliary Building Used for Draining Service Water Prior to Pumping to Storm

Drains indicated the Presence of Licensed Material

Plant Issue N-2005-1121, Received Alert and Hi Alarms on 1-RI-VG-180, B Vent

Stack Gaseous RM

A-11

Attachment

Plant Issue N-2005-2031, While Performing 1-PT-38.1.11 (Liquid Waste

Radiation Monitor), Technicians Noted 1-LW-LCV-111 Repositioned to the Closed

Position on Receiving the Hi-Hi Radiation Alarm on 1-LW-RM-111 During PT

Radioactive Effluent Control Program Evaluation, 4th Quarter 2003 to 2nd Quarter

2005

Section 2PS3: Radiological Environmental Monitoring Program (REMP) and Radioactive

Material Control Program

Procedures and Guidance Documents

Health Physics Procedure Number C-HP-1033.440, NE Technology Sam-9/SAM-

11 Calibration and Operation, Revision 1

Health Physics Procedure Number C-HP-1033.620, Portable Air samplers

Calibration and Operation, Revision 4

Health Physics Procedure Number HP-3051-010, Radiological environmental

monitoring Program, Revision 15

Procedure No. 0-HPS-ISFSI-001, Independent Spent fuel Storage Installation

(ISFSI), Health Physics TLD Survey Surveillance, Revision 3

Procedure Number 0-ICP-MM-DP-1, Primary Meteorological Tower Dew Point

Measuring System Calibration, Revision 6

Procedure Number 0-ICP-MM-RG-1, Primary Meteorological Tower Precipitation

Monitor Calibration, Revision 5

Procedure Number 0-ICP-MM-S-101A, Weather Tower 48 Meter Wind Speed

Calibration, Revision 8

Procedure Number 0-ICP-MM-S-101B, Weather Tower 10 Meter Wind Speed

Calibration, Revision 10

Procedure Number 0-ICP-MM-T-100A, Weather Tower 10 Meter Temperature

Calibration, Revision 9

Procedure Number 0-ICP-MM-T-100B, Weather Tower 10/48 Meter Delta

Temperature Calibration Revision 10

Procedure Number 0-ICP-MM-Temp-1, Primary Meteorological Tower Ambient

Temperature and Differential Temperature Calibration, Revision 11

Procedure Number 0-ICP-MM-Z-101A, Weather Tower 48 Meter Wind Direction

Calibration, Revision 8

Procedure Number 0-ICP-MM-Z-101B, Weather Tower 10 Meter Wind Direction

Calibration, Revision 8

Procedure Number 0-ICP-MM-ZR-1A, Primary Meteorological Tower 10 Meter

Wind Speed and Wind Direction Calibration, Revision 7

Procedure Number 0-ICP-MM-ZR-1B, Primary Meteorological Tower 48 Meter

Wind Speed and Wind Direction Calibration, Revision 8

Procedure Number 0-PT-487.10, Radiological Environmental Monitoring

Program, Land Use Census, Revision 8

Procedure Number 0-PT-487.21, Annual Radiological Environmental Operating

Report, Draft, Revision 5

Procedure Number 0-PT-487.22, Annual Radiological Environmental Operating

Report, Final, Revision 5

Memorandum, North Anna Meteorological Data, 01/28/05

VPAP-1601, Corrective Action, Revision 20

A-12

Attachment

Instrument Calibration and Environmental Data Records

2003 Annual Radiological Environmental Operating Report

2004 Annual Radiological Environmental Operating Report

Calibration Certificate Portable Environmental Air Sampler HiQ, Kit 1, 04/20/05

Calibration Certificate Portable Environmental Air Sampler HiQ, Kit 2, 04/20/05

Calibration Certificate Portable Environmental Air Sampler HiQ, Kit 3, 04/20/05

Calibration Certificate Portable Environmental Air Sampler HiQ, Kit 5, 04/28/05

Calibration Certificate Portable Environmental Air Sampler HiQ, Kit 6, 04/20/05

Framatone ANP Environmental laboratory Analytical Service Semi-Annual Quality

Status Report (January - June 2004)

CAP Documents

Procedure VPAP-1601, Corrective Action, Rev. 20

Plant Issue N-2001-3454, the Interior of the Trailers (Primary and Backup) Are In

Need of Upgrading/Refurbishment, 12/04/2001

Plant Issue N-2003-2304, the Current Assumption Regarding The Charcoal

Cartridge Collection Efficiency for Iodine Is Incorrect, 06/09/03

Plant Issue N-2003-2852-R, Change In Most Limiting Exposure Pathway Grass-

Cow-Milch to Vegetable/Broadleaf Vegetation, 07/23/03

Plant Issue N-2003-2986, Extension Cord Alarmed Sam -11 at Service Building,

08/04/03

Plant Issue N-2003-3342, Sam 9 Contamination Monitors Failed Performance

Check, 09/04/03

Plant Issue N-2004-0129-E1, Worker Alarms PM-7s Located at Protection Area

Exit, 01/14/04

Plant Issue N-2004-0435, Eye Bolt Found Near the Unit 1 Boron Recovery Tank

in the Yard, 02/10/04

Plant Issue N-2004-1389, Individual Alarmed PM-7 at PA When Exiting, 05/02/04

Plant Issue N-2004-1441-E1, Worker Alarmed PM-7 Upon Trying to Exit the PA,

05/04/04

Plant Issue N-2005-1571-E1, Individual Alarmed PM 7 While Attempting to Exit

Protected Area, 05/09/04

Plant Issue N-2004-1654, Individual Alarms PM-7 at Security, 05/11/04

Plant Issue N-2004-1788-E1, Spent Secondary Resin Was Released for Disposal

to Clean Trash, 05/16/04

Plant Issue N-2004-2811-E1, In-coming Positive Whole Body Count, 07/28/04

Plant Issue N-2004-4198, Worker Inappropriately Removed Radioactive Material

From An RCA, 09/30/04

Plant Issue N-2004-5094, Individual Alarmed PM-7 At Security, 11/03/04

Plant Issue N-2004-5126, Shackle Alarmed SAM-11 At Service Building Tool

Crib, 12/02/04

Plant Issue N-2005-1116, Two Acetylene Hoses With Yellow Paint In

Maintenance Shop, 03/22/05

Plant Issue N-2005-1152, Small Sledge Hammer With Yellow and Magenta Paint

Found In Personal Tool Box, 03/23/05

Plant Issue N-2005-2738, NRC Walk-down of Primary Met Tower Express

Concerns of Tree Height, 07/20/05

A-13

Attachment

Radiological Incident Investigation, Contaminated Hammer Found In Mechanics

Tool Box

Radiological Incident Investigation, Contaminated Shackle Found Outside RCA

Radiological Incident Investigation, Contaminated Wire Rope Rigging Found

Outside RCA

Radiological Incident Investigation, Plant Issue N-2003-2986, Contaminated

Extension Cord In Protected Area

Radiological Incident Investigation, Radioactive Material Detected By PM-7 Portal

Monitor Located At Security Exit (East) Badge # 4972

Radiological Incident Investigation, Radioactive Material Detected By PM-7 Portal

Monitor Located At Security Exit Badge # 5857 Plant Issue N-2004-1654

Response to Plant Issue N-2004-0435: Contaminated Eye Bolt Found Outside the

RCA

Section 4OA1: Performance Indicator Verification

Emergency Preparedness

Procedures

DNAP-2605, Emergency Preparedness Performance Indicators, Revision 1

Records and Data

Performance Indicator Monthly Data from January, 2004 thru June, 2005

Radiation Safety

Procedures

Procedure Number HPAP-2802, NRC Performance Indicator Program, Revision 3

SAP, Number VPAP-1501, Deviations, Revision 17

SAP, Number VPAP-1601, Corrective Action, Revision 20

Section 4OA5: Other Activities

ISFSI Radiological Controls

Procedures

Procedure Number 0-HSP-ISFSI-001, Independent Spent Fuel Storage

Installation (ISFSI), Health Physics TLD Survey Surveillance, Revision 3

Procedure Number HP-1020.012, Radiological Protection Action Plan During Dry

Storage Cask Activities, Revision 14

Radiation Work Permits

Radiation Work Permit 05-2-1107, Receive, prep, load, decon, leak test, and ship

the loaded NAC-LWT Cask includes all associated work

Temporary Instruction 2515/161, Transport of Control Rod Drive (CRD) in Type A Packages

Records

Radioactive Material Shipment Log, 01/02 - 06/05