ML052010404

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Errata for San Onofre Nuclear Generating Station, Units 2 and 3, NRC Integrated Inspection Report 05000361-05-003; 05000362-05-003
ML052010404
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 07/20/2005
From: O'Keefe C, Troy Pruett
NRC/RGN-IV/DRP/RPB-D
To: Ray H
Southern California Edison Co
References
Download: ML052010404 (10)


See also: IR 05000361/2005003

Text

July 20, 2005

Harold B. Ray, Executive Vice President

San Onofre, Units 2 and 3

Southern California Edison Co.

P.O. Box 128, Mail Stop D-3-F

San Clemente, CA 92674-0128

SUBJECT: ERRATA FOR SAN ONOFRE NUCLEAR GENERATING STATION, UNITS 2

AND 3, NRC INTEGRATED INSPECTION REPORT 05000361/2005003;

05000362/2005003

Dear Mr. Ray:

Please replace the first page of the Summary of Findings and pages 9 through 12 of NRC

Inspection Report 05000361/2005003; 05000362/2005003 dated July 15, 2005, with the

enclosed revised pages. The purpose of this change is to correct typographical errors.

In accordance with 10 CFR 2.390 of the NRC's Rules of Practice, a copy of this letter and its

enclosure will be made available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Should you have any questions concerning this inspection, we will be pleased to discuss them

with you.

Sincerely,

/RA/ by CFO'Keefe acting for

Troy W. Pruett, Chief

Project Branch D

Division of Reactor Projects

Enclosure:

As stated

Dockets: 50-361

50-362

Licenses: NPF-10

NPF-15

Southern California Edison Co. -2-

cc w/enclosure:

Chairman, Board of Supervisors

County of San Diego

1600 Pacific Highway, Room 335

San Diego, CA 92101

Gary L. Nolff

Power Projects/Contracts Manager

Riverside Public Utilities

2911 Adams Street

Riverside, CA 92504

Eileen M. Teichert, Esq.

Supervising Deputy City Attorney

City of Riverside

3900 Main Street

Riverside, CA 92522

Raymond Waldo, Vice President,

Nuclear Generation

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

David Spath, Chief

Division of Drinking Water and

Environmental Management

California Department of Health Services

P.O. Box 942732

Sacramento, CA 94234-7320

Michael R. Olson

San Onofre Liaison

San Diego Gas & Electric Company

P.O. Box 1831

San Diego, CA 92112-4150

Ed Bailey, Chief

Radiologic Health Branch

State Department of Health Services

P.O. Box 997414 (MS 7610)

Sacramento, CA 95899-7414

Southern California Edison Co. -3-

Mayor

City of San Clemente

100 Avenida Presidio

San Clemente, CA 92672

James D. Boyd, Commissioner

California Energy Commission

1516 Ninth Street (MS 34)

Sacramento, CA 95814

Douglas K. Porter, Esq.

Southern California Edison Company

2244 Walnut Grove Avenue

Rosemead, CA 91770

Dwight E. Nunn, Vice President

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Daniel P. Breig, Station Manager

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

A. Edward Scherer

Southern California Edison

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Brian Katz, Vice President, Nuclear

Oversight and Regulatory Affairs

Southern California Edison Company

San Onofre Nuclear Generating Station

P.O. Box 128

San Clemente, CA 92674-0128

Adolfo Bailon

Field Representative

United States Senator Barbara Boxer

312 N. Spring Street, Suite 1748

Los Angeles, CA 90012

Southern California Edison Co. -4-

Chief, Technological Services Branch

FEMA Region IX

Department of Homeland Security

1111 Broadway, Suite 1200

Oakland, CA 94607-4052

Southern California Edison Co. -5-

Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (KMK)

Senior Resident Inspector (CCO1)

Branch Chief, DRP/D (TWP)

Senior Project Engineer, DRP/D (NFO)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

RidsNrrDipmIipb

W. A. Maier, RSLO (WAM)

SISP Review Completed: _cfo__ ADAMS: : Yes G No Initials: __cfo_

Publicly Available G Non-Publicly Available G Sensitive  : Non-Sensitive

R:\_SO23\2005\SO2005-03RP Errata.wpd

RIV:SPE:DRP/D C:DRP/D

NFOKeefe;df TWPruett

/RA/ CFO'Keefe for

7/20/05 7/20/05

OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

SUMMARY OF FINDINGS

IR 05000361/2005003, 05000362/2005003; 04/08/05 - 06/26/05; San Onofre Nuclear

Generating Station, Units 2 & 3; Integrated Resident and Regional Report; Maintenance

Effectiveness and Temporary Plant Modifications

This report covered a 3-month period of inspection by three resident inspectors, two regional

office inspectors, and one headquarters inspector. The inspection identified one noncited

violation and one finding. The significance of most findings is indicated by their color (Green,

White, Yellow, or Red) using Inspection Manual Chapter 0609, "Significance Determination

Process." Findings for which the significance determination process does not apply may be

Green or be assigned a severity level after NRC management's review. The NRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, "Reactor Oversight Process," Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events

  • Green. The inspectors identified a finding for the failure to develop an adequate

plan to identify hydraulic leakage on Main Feedwater Block Valve 3HV4051.

This issue involved human performance crosscutting aspects associated with

operators failing to identify the leak on normal shift rounds. This issue was

entered into the licensees corrective action program as Action Requests

050401214 and 050401222.

The finding was determined to be greater than minor because it was associated

with the human performance attribute of the initiating events cornerstone and

affected the cornerstone objective of limiting the likelihood of those events that

upset plant stability. Furthermore, if left uncorrected, the finding would have

become a more significant safety concern in that continued hydraulic fluid

leakage from Valve 3HV4051 could result in a plant transient. Using Manual

Chapter 0609, Significance Determination Process, Phase 1 Worksheet, the

finding was determined to have very low safety significance because the

hydraulic fluid leakage had not increased to the point where it would contribute to

both the likelihood of a reactor trip and the likelihood that mitigation equipment or

functions would not be available (Section 1R23).

Cornerstone: Mitigating Systems

the failure to include component deficiencies of a system important to safety in

the maintenance rule program. Specifically, the licensee did not incorporate

piping header failures of the Unit 2 and Unit 3 steam bypass control system into

the maintenance rule program to ensure appropriate monitoring and goal setting

activities were established. This issue was entered into the corrective action

program as AR 050200923.

ENCLOSURE

-9-

1R20 Refueling and Outage Activities (71111.20)

a. Inspection Scope

For the listed outage, the inspectors reviewed the following risk significant outage

activities to verify defense in depth commensurate with the outage risk control plan and

compliance with the Technical Specifications: (1) the risk control plan;

(2) tagging/clearance activities; (3) reactor coolant system instrumentation; (4) electrical

power; (5) decay heat removal; (6) reactivity control; (7) containment closure; (8) heatup

and cooldown activities; and (9) licensee identification and implementation of

appropriate corrective actions associated with outage activities.

  • May 4, 2005, Unit 3 planned outage to repair cracks in the steam bypass header

piping and to repair an external hydraulic leak from main feedwater block

Valve 3HV4051

The inspectors completed one sample.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing (71111.22)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, procedure

requirements, and Technical Specifications to ensure that the six below listed

surveillance activities demonstrated that the SSCs tested were capable of performing

their intended safety functions. The inspectors either witnessed or reviewed test data to

verify that the following significant surveillance test attributes were adequate:

(1) preconditioning; (2) evaluation of testing impact on the plant; (3) acceptance criteria;

(4) test equipment; (5) procedures; (6) jumper/lifted lead controls; (7) test data;

(8) testing frequency and method demonstrated Technical Specification operability;

(9) test equipment removal; (10) restoration of plant systems; (11) fulfillment of ASME

Code requirements; (12) updating of performance indicator data; (13) engineering

evaluations, root causes, and bases for returning tested SSCs not meeting the test

acceptance criteria were correct; (14) reference setting data; and (15) annunciators and

alarms setpoints. The inspectors also verified that the licensee identified and

implemented any needed corrective actions associated with the surveillance testing.

  • April 12, 2005, Unit 2 safety injection Tank 2T-009 surveillance per

Procedure SO123-III-1.1.23, Units 2 and 3 Chemical Control of Primary Plant

and Related Systems, Revision 43

ENCLOSURE

-10-

  • May 5-6, 2005, Unit 3 pressurizer spray Valves 3PV100A and 3PV100B

performance tests per Procedure SO23-I-6.300, Air Operated Valve Diagnostic

Testing, Revision 7

  • May 13, 2005, Unit 3 CCW Pump 3P026 inservice test per Procedure SO23-3-

3.60.3, Component Cooling Water and Seismic Makeup Pump Test, Revision 5

  • May 26, 2005, Unit 2 AFW Pump 2P140 inservice test per Procedure SO23-3-

3.60.6, Auxiliary Feedwater Pump and Valve Testing, Revision 10

  • June 1, 2005, Unit 3 AFW Pump 3P504 inservice test per Procedure SO23-3-

3.60.6, Auxiliary Feedwater Pump and Valve Testing, Revision 10

  • June 16, 2005, Units 2 and 3 sound powered phone system check per

Procedure SO23-6-31, Communication System Operation, Revision 4

The inspectors completed six samples.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications (71111.23)

a. Inspection Scope

The inspectors reviewed the Updated Final Safety Analysis Report, plant drawings,

procedure requirements, and Technical Specifications to ensure that the one listed

temporary modification was properly implemented. The inspectors: (1) verified that the

modification did not have an effect on system operability and availability; (2) verified that

the installation was consistent with the modification documents; (3) ensured that the

postinstallation test results were satisfactory and that the impact of the temporary

modification on permanently installed SSCs was supported by the test; (4) verified that

the modification was identified on control room drawings and that appropriate

identification tags were placed on the affected drawings; and (5) verified that appropriate

safety evaluations were completed. The inspectors verified that the licensee identified

and implemented any needed corrective actions associated with the temporary

modification.

C April 20, 2005, Unit 3 main feedwater block Valve 3HV4051 to Steam

Generator E089 Fermanite repair

The inspectors completed one sample.

ENCLOSURE

-11-

b. Findings

Introduction. The inspectors identified a Green finding for the failure to develop an

adequate monitoring plan to identify a hydraulic fluid leak on main feedwater block

Valve 3HV4051.

Description. On January 20, 2005, the licensee identified that Unit 3 main feedwater

block Valve 3HV4051 had an approximate one drop per second hydraulic fluid leak. On

January 27 the licensee successfully stopped the leak by installing a Furmanite rig

around a leaking fitting on the hydraulic supply piping to the valve.

On April 20 the inspectors walked down portions of the Unit 3 main feedwater system in

order to evaluate the condition of the Furmanite rig that had been installed on

Valve 3HV4051. The inspectors observed that the Furmanite rig was leaking hydraulic

fluid at the rate of approximately 10 drops per minute. Furthermore, the inspectors

observed that the leak collection system revealed enough hydraulic fluid to demonstrate

that the leak had been active for more than one operations shift. Specifically, the catch

basin was full of hydraulic fluid and the tygon tubing that was leading into the 55-gallon

drum had an approximate 8-inch section that was full of hydraulic fluid. The inspectors

informed the Unit 3 control room supervisor of the degraded condition of Valve 3HV4051

and the licensee reinjected additional Furmanite the following day to stop the leak.

Valve 3HV4051 serves as a backup to main feedwater isolation Valve 3HV4052, but it is

not credited in the Updated Final Safety Analysis Report as a containment isolation

valve. The hydraulic system of Valve 3HV4051 serves to keep the valve open against

high pressure nitrogen, and its subsequent loss would result in the valve closing. The

closing of the valve would likely result in the loss of main feedwater and a reactor trip.

The inspectors interviewed operations personnel that were on shift the 3 days prior to

the Furmanite rig leaking on April 20, 2005. The interviews consisted of three field

operators that performed rounds on Valve 3HV4051 and their shift manager. The

inspectors determined that all three operators and the shift manager had a different

understanding of the status of the valve and were either provided incomplete or no

instructions on how to monitor the status of the Furmanite rig on the valve. The

inspectors determined that a monitoring plan had not been established despite the

licensees assessment that the Furmanite rig was susceptible to leakage. The licensee

indicated that operators were expected to monitor the condition of the valve as part of

their normal shift rounds, which included checking equipment for fluid leakage as

described in Procedure OSM-5, Operator Rounds. The licensee subsequently

developed a monitoring plan to ensure that Valve 3HV4051 would be inspected twice

per shift. The value of the monitoring plan was demonstrated when a three to four drop

per minute leak through the Fermanite rig was identified by the licensee on May 2. The

licensee elected not to reinject the valve, but instead permanently repaired it during a

planned shutdown on May 4.

ENCLOSURE

-12-

Analysis. The performance deficiency associated with this finding was the failure to

develop an adequate monitoring plan to identify a hydraulic fluid leak from

Valve 3HV4051. This finding was associated with the initiating events cornerstone. The

finding was determined to be greater than minor because it was associated with the

human performance attribute of the initiating events cornerstone and affects the

cornerstone objective of limiting the likelihood of those events that upset plant stability.

Furthermore, if left uncorrected, the finding would have become a more significant

safety concern in that continued hydraulic fluid leakage on Valve 3HV4051 could result

in a plant transient. Using Manual Chapter 0609, Significance Determination Process,

Phase 1 Worksheet, the finding was determined to have very low safety significance

because the hydraulic fluid leak had not increased to the point where it contributed to

both the likelihood of a reactor trip and the likelihood that mitigation equipment or

functions were not available. This issue involved human performance crosscutting

aspects associated with the failure to identify the hydraulic leak during operator rounds.

Enforcement. No violation of regulatory requirements occurred. The inspectors

determined that the finding did not represent a noncompliance because Valve 3HV4051

is not subject to the requirements of 10 CFR Part 50, Appendix B. While

Valve 3HV4051 serves as a backup to a containment isolation valve, it is not credited in

the Updated Final Safety Analysis Report as a containment isolation valve. This finding

had been entered into the licensees corrective action program as ARs 050401214 and

050401222. This finding is identified as FIN 05000362/2005003-02, Failure to Identify

Hydraulic Leak on Main Feedwater Block Valve 3HV4051.

Cornerstone: Emergency Preparedness

1EP1 Exercise Evaluation (71114.01)

a. Inspection Scope

The inspectors reviewed the objectives and scenario for the 2005 Biennial Emergency

Preparedness Exercise to determine if the exercise would acceptably test major

elements of the emergency plan. The scenario included a loss of electrical power to all

of the main control room alarms, a seized reactor coolant pump, a main steam line

break into the primary containment, and a helicopter crash into the main switchyard

which resulted in a loss of offsite power. The scenario continued with a station blackout

due to failures of the emergency diesel generators, and a steam generator tube rupture

and fuel cladding failure, resulting in an ongoing radioactive steam release to the

environment. The licensee activated all of their emergency facilities to demonstrate

their capability to implement the emergency plan.

The inspectors evaluated exercise performance by focusing on the risk-significant

activities of classification, notification, protective action recommendations, and

assessment of offsite dose consequences in the simulator control room and the

following emergency response facilities:

ENCLOSURE