ML040300067

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IR 05000269-04-007, 05000270-04-007, and 05000287-04-007, on 01/21/04, Oconee, Units 1, 2, and 3, Review of Unresolved Item 05000269,270,287/2003003-002
ML040300067
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 01/29/2004
From: Casto C
Division of Reactor Safety II
To: Rosalyn Jones
Duke Energy Corp
References
EA-04-018, IR-03-002 IR-04-007
Download: ML040300067 (15)


See also: IR 05000269/2004007

Text

January 29, 2004

EA-04-018

Duke Energy Corporation

ATTN: Mr. Ronald A. Jones

Vice President

Oconee Site

7800 Rochester Highway

Seneca, SC 29672

SUBJECT:

OCONEE NUCLEAR STATION - NRC INSPECTION REPORT NO.

05000269/2004007, 05000270/2004007, AND 05000287/2004007

Dear Mr. Jones:

On January 21, 2004 the U.S. Nuclear Regulatory Commission (NRC) completed an in-office

and site inspection to resolve a previously identified issue at your Oconee Nuclear Station. The

purpose of the inspection was to review Unresolved Item 05000269,270,287/2003003-002,

High Energy Line Break (HELB) Accident Scenario Review that was identified in an inspection

performed during the week of June 16 - 20, 2003. The enclosed report documents the results

of this inspection which were discussed on January 27, 2004, with your staff.

This inspection was an examination of activities conducted under your license as they relate to

safety and compliance with the Commissions rules and regulations and with the conditions of

your license. Within these areas, the inspection consisted of selected examinations of records,

documents, discussion with NRC staff, and interviews with licensee personnel.

This report documents an apparent violation which is being considered for escalated

enforcement action in accordance with the General Statement of Policy and Procedure for

NRC Enforcement Actions (Enforcement Policy), NUREG-1600. The current Enforcement

Policy is included on the NRCs Web site at www.nrc.gov; select What We Do, Enforcement,

then Enforcement Policy. The apparent violation involved the application of 10 CFR 50.59 for

a May 2001 revision to the Oconee Updated Final Safety Analysis Report for the HELB analysis

in which the licensee failed to identify Unreviewed Safety Questions and changes involving

more than minimal increase in risk which required prior NRC approval. Since the NRC has not

made a final determination in this matter, no Notice of Violation is being issued for this

inspection finding at this time. In addition, please be advised that the number and

characterization of the apparent violation described in the enclosed inspection report may

change as a result of further NRC review.

DEC

2

An open predecisional enforcement conference to discuss this apparent violation will be

scheduled at a future date. The NRC will contact you regarding this date. The decision to hold

a predecisional enforcement conference does not mean that the NRC has determined that a

violation has occurred or that enforcement action will be taken. This conference is being held

to obtain information to assist the NRC in making an enforcement decision. This may include

information to determine whether a violation occurred, information to determine the

significance of a violation, information related to the identification of a violation, and information

related to any corrective actions taken or planned. The conference will provide an opportunity

for you to provide your perspective on these matters and any other information that you believe

the NRC should take into consideration in making an enforcement decision.

You will be advised by separate correspondence of the results of our deliberations on this

matter. No response regarding the apparent violation is required at this time.

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

\\\\RA\\\\

Charles A. Casto, Director

Division of Reactor Safety

Docket Nos. 50-269, 50-270, 50-287

License Nos. DPR-38, DPR-47, DPR-55

Enclosure:

Inspection Report No. 05000269/2004007, 05000270/2004007, and

05000287/2004007

cc w/encl:

Noel Clarkson

Compliance Manager (ONS)

Duke Energy Corporation

Electronic Mail Distribution

(cc w/encl contd - See page 3)

DEC

3

(cc w/encl contd)

L. E. Nickolson

Safety Assurance Manager (ONS)

Duke Energy Corporation

Electronic Mail Distribution

Lisa Vaughn

Duke Energy Corporation

Mail Code - PB05E

422 South Church Street

P.O. Box 1244

Charlotte, NC 28201-1244

Anne Cottingham

Winston and Strawn

Electronic Mail Distribution

Beverly Hall, Acting Director

Division of Radiation Protection

N. C. Department of Environmental

Health & Natural Resources

Electronic Mail Distribution

Henry J. Porter, Director

Div. of Radioactive Waste Mgmt.

S. C. Department of Health and

Environmental Control

Electronic Mail Distribution

R. Mike Gandy

Division of Radioactive Waste Mgmt.

S. C. Department of Health and

Environmental Control

Electronic Mail Distribution

County Supervisor of

Oconee County

415 S. Pine Street

Walhalla, SC 29691-2145

Lyle Graber, LIS

NUS Corporation

Electronic Mail Distribution

(cc w/encl contd - See page 4)

DEC

4

(cc w/encl contd)

M. T. Cash, Manager

Regulatory Issues & Affairs

Duke Energy Corporation

526 S. Church Street

Charlotte, NC 28201-0006

Peggy Force

Assistant Attorney General

N. C. Department of Justice

Electronic Mail Distribution

Enclosure

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-270, 50-287

License Nos:

DPR-38, DPR-47, DPR-55

Report No:

05000269/2004007, 05000270/2004007 and 05000287/2004007

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station, Units 1, 2, and 3

Location:

7800 Rochester Highway

Seneca, SC 29672

Dates:

June 20, 2003 - January 21, 2004

Inspectors:

M. Scott, Senior Reactor Inspector

Approved by:

Mark S. Lesser, Chief

Engineering Branch 2

Division of Reactor Safety

Enclosure

SUMMARY OF FINDINGS

IR 05000269/2004-007, 05000270/2004-007, 05000287/2004-007; 06/20/2003 - 01/21/2004;

Oconee Nuclear Station, Other Activities.

The inspection was conducted by a senior reactor inspector. An apparent violation was

identified for making a change to the facility in 2001 that involved Unreviewed Safety Questions

and more than a minimal increase in risk, without prior NRC approval pursuant to

10 CFR 50.59. With completion of the Updated Final Safety Analysis Report a (UFSAR)

change, the licensee accepted the attendant, non-conforming safety issues contained therein.

Findings for which the SDP does not apply may be Green or be assigned a severity level after

NRC management review. The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

NRC Identified Findings

Cornerstone: Mitigating Systems

Apparent Violation: The inspectors identified an apparent violation of 10 CFR 50.59

(a)(1) (1999 version of 10 CFR) which states, in part, that the licensee may make

changes in the facility as described in the safety analysis report without prior

Commission approval, provided the proposed change does not involve an unreviewed

safety question (USQ). 10 CFR 50.59 (a)(2) states, in part, that a proposed change

involves an USQ if the probability of occurrence or malfunction of equipment important

to safety previously evaluated in the safety analysis report may be increased, or if it may

create an accident different from any previously evaluated.

On May 17, 2001, the licensee made a change to the facility, as described in the

Updated Final Safety Analysis Report, Section 3.6.1.3, associated with the High Energy

Line Break (HELB) analysis, which involved unreviewed safety questions, and failed to

obtain prior NRC approval. The UFSAR Section was changed to increase the maximum

initiation time following HELB of Emergency Feedwater from 15 to 30 minutes and of

High Pressure Injection from 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> (based on referenced reports and

analysis). The analysis discussed an increased cycling of pressurizer Safety Relief

Valves on steam and water, boiler condenser mode of decay heat removal, and an

unapproved computer code for application to HELB, but failed to recognize that such

changes may increase the probability of occurrence or the consequences of a

malfunction of equipment important to safety or may create an accident different from

any previously evaluated. In addition, the change resulted in more than a minimal

increase in risk. (Section 4OA5)

This is an Apparent Violation pending results of an enforcement conference.

Enclosure

REPORT DETAILS

Other Activities

4OA5 Other Activities

(Closed) URI 50-269, 270, 287/2003003-02, HELB Accident Scenario Review

Introduction. An apparent violation was identified for making a change to the facility in

2001 that involved Unreviewed Safety Questions and more than a minimal increase in

risk, without prior NRC approval pursuant to 10 CFR 50.59.

Description. URI 05000269,270,287/2003003-002, HELB Accident Scenario Review,

was identified concerning Oconee Updated Final Safety Analysis Report (UFSAR)

Section 3.6.1.3 that was changed on May 17, 2001. The change was made prior to

licensee implementation of the revised 10CRF50.59 rule, and therefore was evaluated

as to whether or not it involved an unreviewed safety question (USQ). The inspectors

determined that the change involved some USQs.

The UFSAR change was associated with the licensees high energy line break (HELB)

analysis for main feedwater piping. The escaping water/steam is assumed to disable

the 4160 Volt breakers for at least the motor driven emergency feedwater (EFW) pumps

and for the high pressure injection (HPI) pumps, and the automatic initiation of the

turbine driven EFW pump. The change was to evaluate a delay in the time allowed for

manual restoration of EFW from 15 minutes to 30 minutes and HPI from 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to 8

hours. The EFW time to initiation was extended when it was recognized through

operator action validation timelines, that it took longer than 15 minutes to provide EFW

from other manual sources. The time extension for HPI injection appeared to be related

to the licensees desire to reduce site manning established to support HPI cable

switching to an alternate power source. The resulting effect on plant equipment is that

the pressurizer safety relief valves (SRV) are required to cycle an additional 15 minutes

for up to 30 minutes until EFW is started and will change from relieving steam to

relieving water, reactor coolant system (RCS) subcooling is lost, significant RCS voiding

occurs, natural circulation cooling is lost, and decay heat is removed by the boiler

condensing mode (BCM) for up to eight hours. Delaying EFW initiation may effect the

thermally induced compressive and tensile stresses on the Once Through Steam

Generator (OTSG) tubes resulting from refilling a dryed out steam generator. Extended

reliance on BCM has several implications which have not been reviewed by the NRC,

including computer modeling assumptions, cyclical stresses on the RCS resulting from

pressure spikes and vibration, and a possible reactivity excursion upon reinitiating of

RCS flow due to diluted boron concentration in the cold leg. The inspectors determined

that delaying the initiation of safety systems beyond the existing licensing basis time

requirements may increase the probability or consequences of a malfunction of

equipment (SRV, RCS boundary) and may create the possibility of an accident or

malfunction of a different type than previously evaluated and therefore is a USQ that

requires NRC approval.

2

Enclosure

Safety Relief Valve Concern

The licensees calculation, OSC-7299, revision 0, and referenced report (Duke Power

MDS Report No. OS-73.2) was the basis for the previous recovery times for EFW and

HPI (15 minutes and 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, respectively). Revision 1 to the calculation introduced the

increased recovery times. The 10 CFR 50.59 evaluation indicated that one of the key

assumptions was that the SRVs would lift and reseat with water passing through the

valves. Originally, the SRVs would be challenged and would undergo 5 cycles on steam

in 15 minutes. With the longer recovery times associated with the May 2001 change,

the licensees calculation indicted that SRVs would undergo 6 challenges on steam and

8 additional challenges with water in 30 minutes. The licensees safety evaluation

stated, Increasing the time allowed to re-establish these flows has no significant effect

on the operation of the associated pumps and fluid systems. It additionally stated, As

described in the Safety Review, this activity only allows additional time before equipment

is required to be placed in operation following a postulated HELB. The equipment will

be operated in the same manner as it previously was, so there are no new alignments

associated with this change. Since the equipment is utilized in the same way as it

previously was, the consequences of a malfunction of equipment will not increase.

The inspectors were concerned that the licensees assumption that the SRVs

successfully reseat each time is critical to recovery without core damage. With a stuck

open valve and no safety injection, core damage would result. The inspectors

determined that the licensees assumption did not have adequate basis. The SRVs

were not designed to function in this manner and have not been adequately

demonstrated to perform in this manner. The licensees evaluation did not address that

the increased number of cycles of these valves on steam and the change in medium to

water may increase the probability of a malfunction (i.e., sticking open or closed) and

create the possibility of an accident of a different type (loss of coolant or overpressure).

The evaluation added no more technical content to the discussion on malfunctions.

In the OSC-7299 calculation the two actual SRVs are modeled as one valve. The

calculation does not address the impact on the risk importance of this modeling. NRC

review of the risk indicates that each SRV lift, and the change of medium from steam to

water, has a certain probability of failure. With the increased number of challenges, the

overall probability that the SRV(s) will fail open during the event increases. With a failed

open SRV, and no HPI, core damage will result. Given an increased SRV failure

probability, the delta core damage frequency for the applicable core damage accident

sequences stemming from the HELB initiating event was evaluated by the NRC as

greater than 1E-6. NEI Guidance 96-07 (paragraph 4.3.1, Example three) indicates

that a change to the plant that causes an increase in event frequency exceeding 1E-6

per year would require NRC approval prior to making the change.

The licensee provided additional information to support their position. The licensee

considered the SRVs adequate based upon NRC acceptance of the Electric Power

Research Institute (EPRI) test program on SRVs, which was completed as part of a

Three Mile Island Action Plan item, and a letter from Dresser, the SRV vendor. NRC

3

Enclosure

Safety Evaluation (SER) Report for NUREG-0737, Item II.D.1, Performance Testing of

Relief and Safety Valves for Oconee Unit 1, 2, and 3 (TAC 44600, 44601, 44602) dated

July 19, 1989, accepted SRV performance for UFSAR Chapter 15 accident and

transient scenarios. Reference 8, (EPRI document NP-2628-SR, PWR and Relief

Valve Test Program: Safety and Relief Valve Test Report, December 1982) is the

performance test report on power operated relief valves and SRVs. The report states

that: The objective of the ... Program was to perform full scale operability tests on a set

of primary system relief and safety valves representative of the those utilized in or

planned for use in PWRs ..... The test conditions were selected to be representative of

those expected in participating PWRs based on consideration of limiting UFSAR, cold

overpressrization, and extended high pressure liquid injection events.

The EPRI study was conducted in 1981 and included a Dresser model 31739A SRV

found at Oconee. The Oconee equivalent SRV was tested with several (4) water lifts

and did reseat. It is noted that the valves in the EPRI test had not been exposed to a

containment harsh environment for some portion of a fuel cycle prior to being tested,

which could influence real valve lifts. Although the Oconee similar valve was tested with

consecutive lifts, it had been rebuilt prior to the water lifts. NRC staff opinion is that the

testing was very limited and not sufficient to demonstrate the valves would successively

re-close with multiple actuations of the subject postulated event beyond the limited lifts

addressed in the above-mentioned SER. In the EPRI study, the number of valves

tested is not sufficient from a quality assurance standard to demonstrate high reliability.

The small EPRI sample size could not reasonably provide justification for valve

confidence during consecutive challenges as modeled in the loss of 4160 Volt HELB

scenario unique to Oconee.

The inspectors determined that the SRV performance during the HELB scenario is not

bounded by the EPRI test program, nor by the SER. The SER accepts the Dresser

31739A safety valve blowdown results because it does not impede natural circulation

due to hot leg voiding. Limiting transients are identified as Loss of Main Feedwater

(LOFW) and Feedwater Line Break (FWLB) (Reference 22 of the SER). Generic plant

transients are listed but do not include the loss of 4160 Volt power and TDEFW in a

HELB. The limiting transients assumptions indicate a single failure of one emergency

feedwater pump, a Loss of Offsite Power (LOOP), no credit for PORV actuation among

other things, but does not assume loss of 4160 Volt power, therefore the original

scenarios did not address the unique Oconee vulnerability - loss of 4160 Volt power

resulting in the loss of HPI. With a LOOP, the standard emergency power is sequenced

on and pump injection occurs within a very short time. With these limiting transients, the

RCS/pressurizer fills within several minutes and decay heat is being effectively removed

a short time thereafter. Natural circulation loss is not jeopardized by the scenarios.

With these limiting transients, there is a very unlikely chance of core damage, because

even with an SRV failure, HPI and EFW is promptly available. During these scenarios,

the SRVs lift 3 to 4 times as opposed to the Oconee unique UFSAR change of May

2001, which challenges the SRVs 14 times, eight of which are with water. The change

to Section 3.6.1.3 transient contrasts sharply with above generic limiting scenarios. The

SER does not accept SRV performance as the licensee proposed in the HELB

evaluation.

4

Enclosure

The licensee provided a valve vendor memorandum (dated 9-19-03). The licensee did

not have this information available for the creation of the May 2001 UFSAR change.

Although the memo did provide some information regarding testing on similar valves

under various conditions, the various testing information did not represent the revision 1

HELB transient. The new vendor information did not provide a failure rate on the

subject SRVs and did not address probabilistic reliability of the valves under water lifts.

The vendor information did indicate the valve was capable under two phase lifts

(saturated steam, not saturated water). However, the information stated that there has

been no cycle testing for the Oconee type valve, outside of the EPRI testing. The

inspectors determined the changes in performance required by the SRVs represent a

USQ because the probability of occurrence or a malfunction may be increased, or an

accident of a different type (loss of coolant) may be created.

Delayed EFW Initiation Concern on Steam Generator Tubes

The inspectors questioned the delayed EFW initiation effects on the once through steam

generators (OTSG) under the HELB scenario. The long straight tubes in a Babcock &

Wilcox OTSG have existing axial loading analysis, described in the UFSAR (such as

Section 3.9), due to temperature differences between the OTSG components (tubes to

shell), when refilling a dryed out OTSG. The Oconee Emergency Operating

Procedures have limits on temperature changes (stated to be +100 and -60 degree F

differential temperatures, tensile and compression, respectively for Units 2 & 3). These

limits are assumed to be manageable with immediate injection capability, but with

delayed injection timing could be critical to prevent exceeding the limits. In the loss of

4160 Volt HELB scenario, EFW flow would be delayed for up to 30 minutes instead of

15 minutes and HPI injection is further delayed. With delayed injection, cold to hot leg

temperature differences are driving this divergence combined with other cooling effects.

Thus, the differential temperature across the OTSGs would be a potential

concern/consideration in the scenarios evaluation. Excessive stresses could cause

OTSG tubes to crack or rupture. The inspectors were concerned that these issues had

not been addressed in the licensees evaluative documents. From this the inspectors

concluded that this is a USQ because of the possibility that an accident different from

any previously evaluated may be created, such as a steam generator tube rupture or

excessive accident induced tube leakage concurrent with a HELB.

Boiler Condenser Mode Concern

The introduction of BCM was a new mode of long term (8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />) decay heat removal

added to the UFSAR via the May 2001 change. Per Revision 1 to OSC-7299

calculation, enough volume will be lost from the RCS via the SRVs and Reactor Coolant

Pump (RCP) seals leakage such that, significant voiding will occur, natural circulation

and subcooling is lost, and BCM is relied upon after 30 minutes into scenario. BCM

cooling comes from core decay heat and steam rising up the hot leg and condensing in

the OTSG tubes. This condition or mode could persist up to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br /> under the scenario

until RCS is under some form of pressure and temperature control. The licensee used

RELAP5 software to model the RCS response, which was different than the model

previously used. This computer code has not been approved for use in HELB by the

5

Enclosure

NRC, nor has the NRC been afforded the opportunity to review the licensees

assumptions. The inspectors were unable to conclude that the RELAP5 modeling

reasonably reflected actual conditions, timeline/chronology, and magnitude of changes

in the plant during the scenario. The calculation generally indicated that results were

very sensitive to EFW initiation timeline and other model/scenario facets.

Within the scenario, the reactor coolant significantly boils and chugs as steam is

condensed in the reactor coolant components under saturated RCS and increased

voided volume conditions, thus creating potential component vibration and multiple

pressure spikes that constitute mechanical cycles. There is no practical industry

experience with this mode of cooling or impact discussion of the possible induced stress

and fatigue to plant equipment. The UFSAR (chapters 3 and 5) addresses dynamic

loading and fatigue analysis of primary piping and components. The inspectors were

concerned that the licensees evaluation did not address the challenges to the

mechanical components of the plant with many more dynamic cycles present for up to

eight hours. For example, UFSAR Sections 3.9.1.1 and Table 5.2 indicate cycle

transients that the RCS has been designed to withstand and the HELB/BCM is not

indicated. Additionally, Section 3.9.3 discusses design and dynamic loads to meet

Section 3.1.33 RCS pressure boundary capability criterion. The 10 CFR 50.59 review of

the UFSAR and support documentation did not recognize this potential problem. The

inspectors could not determine the effects of operation in the BCM for an extended

period on plant equipment. From this the inspectors concluded that this is a USQ

because of the possibility that an accident different from any previously evaluated

(structural failures and loss of coolant) may be created.

The inspectors questioned the potential for recriticality with BCM. Babcock and Wilcox

Nuclear Technologies (BWNT) submitted a potential 10 CFR Part 21 report to the NRC

on July 31, 1995. Report number 1995-186 contained a potential safety concern on

post small break loss of coolant accident (SBLOCA). The document was not discussed

in the 10 CFR 50.59 evaluation. The report provided preliminary information on the

potential for core recriticality caused by a reactivity insertion due to moderator dilution

while in BCM. The report reads in part, "During the course of a small break LOCA and

any other transients that involve the partial loss of reactor coolant system (RCS)

inventory, the steam generators may provide an energy sink for part or all of the core

decay heat via boiler/condenser operation. In this mode, steam generated in the core

through boiling is passed through the hot legs to the steam generators and condensed.

The condensate is returned to the core through the cold legs. Because boron volatizes

at a concentration substantially below that of the source, the concentration of boron

carried with the steam is greatly reduced with the result that the boron concentration

downstream from the steam generator is gradually reduced. Evaluation of the boron

carryover fraction with the MULTI-Q code shows that the fraction is temperature

dependent and limited to ten percent for the conditions of interest." In the report, BWNT

had indicated that they would provide additional information at a later date. When asked

by the inspectors, the licensee produced a Framatome document, 77-5002260-00

Evaluation of Potential Boron Dilution Following Small Break Loss-of-Coolant Accident.

This September 1998 document indicated that with HPI and EFW injection from the

onset of small break that a cold leg reactivity insertion on the bump of a RCP would

6

Enclosure

cause a recriticality of 15 to 35 percent with some core damage possible. The

document did not discuss the possible mechanical effects of cool, deborated water in

the core during recriticality (e.g., potential prompt criticality with steam expansion/rapid

core voiding). The inspectors were concerned that due to the timeline differences,

injection pump availability variances, and the potential for natural circulation recriticality,

the conditions of the 1998 document appear to be sufficiently different than those of the

May 2001 HELB transient, that documentation of those differences and the exact

potential for recriticality and potential damage must be evaluated. The licensees

evaluation did not address recriticality potential with the HPI return at eight hours. The

licensees stated position was that although the occurrence of BCM can result in an

addition of positive reactivity under natural circulation, the risk of a significant core

power excursion leading to core damage is low. The 10 CFR 50.59 Rule in effect at the

time the May 2001 evaluation was written did not allow any increase in risk in a facilty

change without prior NRC approval. From this the inspectors concluded that this is a

USQ because of the possibility that an accident different from any previously evaluated

may be created.

Analysis. The finding is not suitable for evaluation using the SDP. The SRV concern

alone was evaluated by separate probabilistic risk analysis. Given the increased SRV

failure probability alone (assumed failure probability with water medium of 0.1), the delta

core damage frequency for the applicable core damage accident sequences stemming

from the HELB initiating event was greater than 1E-6. NEI Guidance 96-07 indicates

that a change to the plant that causes an increase in event frequency exceeding 1E-6

per year would require NRC approval prior to make the change. The significance of this

finding, based on the increase in risk associated with the SRV change alone is low to

moderate.

Enforcement. 10 CFR 50.59 (a)(1) (1999 edition) states in part, that the licensee may

make changes in the facility as described in the safety analysis report without prior

Commission approval, provided the proposed change does not involve an USQ.

10 CFR 50.59 (a)(2) states, in part, that a proposed change involves a USQ if the

probability of occurrence or the consequences of a malfunction of equipment important

to safety previously evaluated in the safety analysis report may be increased or if the

possibility for an accident or malfunction of different from any previously evaluated may

be created.

On May 17, 2001, the licensee made a change to the facility, as described in the

Updated Final Safety Analysis Report, Section 3.6.1.3, associated with the High Energy

Line Break (HELB) analysis, which involved unreviewed safety questions, and failed to

obtain prior NRC approval. Specifically, calculation OSC-7299 was changed to increase

the maximum initiation time following HELB of Emergency Feedwater from 15 to 30

minutes and of High Pressure Injection from 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> to 8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />. The analysis discussed

increased cycling of pressurizer Safety Relief Valves on steam and water and, boiler

condenser mode of decay heat removal, and an unapproved computer code for

application to HELB, but failed to recognize that such changes may increase the

probability of occurrence or the consequences of a malfunction of equipment important

to safety or may create an accident different from any previously evaluated.

7

Enclosure

The licensee has not placed this issue into the corrective action program, or

acknowledged this as a performance deficiency.

This is being treated as an apparent violation (AV), 50-269, 270, 287/2004007-01,

Failure to Obtain Prior NRC Approval to a Change to the Facility involving Unreviewed

Safety Questions on High Energy Line Break Analysis.

4OA6 Meetings, including Exit

The NRC presented the inspection finding to Mr. Noel Clarkson on January 27, 2004 via

a telephone conversation. The licensee acknowledged the finding presented.

Proprietary information is not included in this inspection report.

8

Attachment

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee:

N. Clarkson, Regulatory Compliance Manager

D. Garland, Operations Senior Engineer

L. Nicholson, Safety Assurance Manager, Oconee Nuclear Station

G. Swindlehurst, Nuclear Engineering Manager

NRC personnel:

NRR personnel

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-269, 270, 287/2004007-01

AV

Failure to Obtain Prior NRC Approval to a Change

to the Facility Involving Unreviewed Safety

Questions on High Energy Line Break Analysis

Closed

50-269, 270, 287/2003003-02

URI

HELB Accident Scenario Review