ML040270002

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IR 05000260-03-005 and 05000296-03-005, on 09/28/03 to 12/27/03, Browns Ferry Nuclear Plant
ML040270002
Person / Time
Site: Browns Ferry  Tennessee Valley Authority icon.png
Issue date: 01/26/2004
From: Cahill S
Reactor Projects Region 2 Branch 6
To: Scalice J
Tennessee Valley Authority
References
FOIA/PA-2004-0277 IR-03-005
Download: ML040270002 (28)


See also: IR 05000260/2003005

Text

January 26, 2003

Tennessee Valley Authority

ATTN.: Mr. J. A. Scalice

Chief Nuclear Officer and

Executive Vice President

6A Lookout Place

1101 Market Street

Chattanooga, TN 37402-2801

SUBJECT: BROWNS FERRY NUCLEAR PLANT - NRC INTEGRATED INSPECTION

REPORT 05000260/2003005 and 05000296/2003005

Dear Mr. Scalice:

On December 27, 2003, the US Nuclear Regulatory Commission (NRC) completed an

inspection at your operating Browns Ferry Unit 2 and 3 reactor facilities. The enclosed

integrated quarterly inspection report documents the inspection results, which were discussed

on January 16, 2004 with Mr. Ashok Bhatnager and other members of your staff. Results from

our inspection of your Unit 1 Recovery Project are documented in a separate Unit 1 integrated

inspection report.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

This report documents a self-revealing finding of very low safety significance (Green) which was

determined to involve a violation of NRC requirements. However, because of the very low

safety significance and because the finding was entered into your corrective action program,

the NRC is treating the finding as a non-cited violation (NCV) consistent with Section VI.A of the

NRC Enforcement Policy. If you contest any non-cited violation in the enclosed report, you

should provide a response within 30 days of the date of this inspection report, with the basis for

your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington DC 20555-0001; with copies to the Regional Administrator, Region II; the Director,

Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-

0001; and the NRC Resident Inspector at the Browns Ferry Nuclear Plant.

TVA 2

In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Stephen J. Cahill, Chief

Reactor Projects Branch 6

Division of Reactor Projects

Docket Nos. 50-260, 50-296

License Nos. DPR-52, DPR-68

Enclosure: NRC Integrated Inspection Report 05000260/2003005 and 05000296/2003005

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

TVA 3

cc w/encl: Chairman

Karl W. Singer Limestone County Commission

Senior Vice President 310 West Washington Street

Nuclear Operations Athens, AL 35611

Tennessee Valley Authority

Electronic Mail Distribution Distribution w/encl: (See page 4)

James E. Maddox, Vice President

Engineering and Technical Services

Tennessee Valley Authority

Electronic Mail Distribution

Ashok S. Bhatnagar

Site Vice President

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

General Counsel

Tennessee Valley Authority

Electronic Mail Distribution

Michael J. Fecht, Acting General Manager

Nuclear Assurance

Tennessee Valley Authority

Electronic Mail Distribution

Michael D. Skaggs, Plant Manager

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

Mark J. Burzynski, Manager

Nuclear Licensing

Tennessee Valley Authority

Electronic Mail Distribution

Timothy E. Abney, Manager

Licensing and Industry Affairs

Browns Ferry Nuclear Plant

Tennessee Valley Authority

Electronic Mail Distribution

State Health Officer

Alabama Dept. of Public Health

RSA Tower - Administration

Suite 1552

P. O. Box 303017

Montgomery, AL 36130-3017

TVA 4

Distribution w/encl:

K. Jabbour, NRR

L. Slack, RII EICS

RIDSRIDSNRRDIPMLIPB

PUBLIC

OFFICE DRP/RII DRP/RII DRP/RII DRS/RII DRS/RII DRS/RII

SIGNATURE BLH1 EFC RLM2 via email (GTH1) via email (EXL2) via email (DCP)

NAME BHolbrook EChristnot RMonk GHopper ELea DPayne

DATE 01/23/2004 01/23/2004 01/23/2004 01/23/2004 01/26/2004 01/23/2004

E-MAIL COPY? YES NO YES NO YES NO YES NO YES NO YES NO YES NO

PUBLIC DOCUMENT YES NO

C:\ORPCheckout\FileNET\ML040270002.wpd

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-260, 50-296

License Nos: DPR-52, DPR-68

Report No: 50-260/03-05, 50-296/03-05

Licensee: Tennessee Valley Authority (TVA)

Facility: Browns Ferry Nuclear Plant, Units 2 & 3

Location: Corner of Shaw and Nuclear Plant Roads

Athens, AL 35611

Dates: September 28, 2003 - December 27, 2003

Inspectors: B. Holbrook, Senior Resident Inspector

E. Christnot, Resident Inspector

R. Monk, Resident Inspector

G. Hopper, Senior Operations Engineer (Section 1R11.2)

E. Lea, Senior Operations Engineer (Section 1R11.2)

D. Payne, Senior Reactor Inspector, (Section 4OA5)

Approved by: Stephen J. Cahill, Chief

Reactor Project Branch 6

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000260/2003-005, 05000296/2003-005; 9/28/2003 - 12/27/2003; Browns Ferry Nuclear

Plant, Units 2 and 3; Maintenance effectiveness.

The report covered approximately a three-month period of routine inspection by resident

inspectors and senior operations engineers and resolution of a previously unresolved item by a

regional engineering inspector. One Green non-cited violation (NCV) was identified. The

significance of issues is indicated by their color (Green, White, Yellow, Red) using the

Significance Determination Process in Inspection Manual Chapter 0609, Significance

Determination Process (SDP). The NRCs program for overseeing the safe operation of

commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process,

Revision 3, dated July 2000.

A. Inspector Identified and Self-Revealing Findings

Cornerstone: Initiating Events, Mitigating Systems

Green. Maintenance on Control Rod Drive pump 3A was conducted using an

inadequate maintenance procedure. Work practices were inconsistent with the vendor

manual. Pump seal clearances were improperly set and during the post maintenance

test the pump seal rubbed sufficiently to cause sparking and damage of the new seal.

The inspectors identified a non-cited violation (NCV) (Self-Revealing) of 10 CFR Part

50, Appendix B,Section V, Instructions, Procedures, and Drawings. The finding is

greater than minor in that it affects the mitigating systems cornerstone objective and

degrades the attribute of equipment availability and reliability. The finding is of very low

safety significance based on the operation of the standby pump and all other mitigation

systems were available during the activity. (Section 1R12)

B. Licensee Identified Findings

None

Enclosure

Report Details

Summary of Plant Status

On October 28, 2003 Unit 2 was shutdown for a midcycle outage to repair a steam leak in the

condenser, repair an electro hydraulic fluid leak, and correct component leakage in the drywell.

Unit startup began on November 7, 2003. 100% Rated Thermal Power (RTP) was achieved on

November 10, 2003, and remained there through the end of the inspection period.

On October 25, 2003 Unit 3 reduced power to about 65% RTP to perform power suppression

testing to identify the location of leaking fuel, perform surveillance testing, and complete

scheduled maintenance. Power was returned to 100% RTP on October 28. Power was

reduced to about 70% on November 15, 2003 to repair a cracked weld on the feedwater header

long cycle drain line to the condenser. Temporary repairs were completed and power was

increased to 100% on November 16, 2003. The Unit remained at 100% RTP through the end

of the inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and Emergency

Preparedness

1R01 Adverse Weather Protection (Weather Preparation and Actual Cold Weather

Conditions)

a. Inspection Scope

The inspectors reviewed licensee procedure 0-GOI-200-1, Freeze Protection

Inspections, and reviewed licensee actions to implement the procedure in preparations

for cold weather conditions. The inspectors verified that selected valves and

components listed in the attachments of the procedure were in the position specified by

the procedure. The inspectors reviewed the list of open Problem Evaluation Reports

(PERs) to verify that the licensee was identifying and correcting potential problems

relating to cold weather operations. The inspectors reviewed immediate and planned

corrective actions to verify they were appropriate. In addition, the inspectors reviewed

procedure EPI-0-000-FRZ001, Freeze Protection Program for RHRSW Pump Rooms,

Diesel Generator Building, and the Cooling Tower Pumping Station, to assess

maintenance actions and preparations for cold weather conditions that could affect unit

operation.

On November 25, 2003 while outside temperature was approximately 25 degrees F, the

inspectors completed a walkdown inspection of risk significant systems and components

located in outside areas and buildings that were susceptible to cold weather conditions.

The inspectors observed portable heaters, building openings, and heat tracing light

indications to verify proper operation.

Enclosure

2

The inspectors reviewed recent PERs and discussed cold weather conditions with

operations personnel to assess plant conditions and personnel sensitivity to actual cold

weather conditions. The inspectors conducted a walkdown tour of the main control

rooms to assess system performance and alarm conditions of systems susceptible to

cold weather conditions.

b. Findings

No findings of significance were identified.

1R04 Equipment Alignment (Partial and Complete Walkdown)

.1 Partial System Lineup

a. Inspection Scope

The inspectors performed a partial walkdown of three safety systems listed below to

verify redundant or diverse train operability, as required by the plant Technical

Specifications (TS) while the other train of the system was out of service. In some

cases, the system was selected because it would have been considered an

unacceptable combination from a Probabilistic Safety Assessment (PSA) perspective for

the equipment to be removed from service while another train or system was out of

service. The inspectors walkdown was to verify that selected breaker, valve position,

and support equipments were in the correct position for support system operation. The

walkdown was also done to identify any discrepancies that impacted the function of the

system could lead to increased risk.

The inspectors reviewed identified and resolved equipment alignment problems that

could cause initiating events or impact the availability and functional capability of

mitigating systems or barriers. The inspectors observations of equipment and

component alignment for the partial walkdowns were compared to the alignment

specified in system procedures included in the attachment of the report.

Loop B was out of service for piping replacement

configuration and alignment

while 3DN LPCI MG set out for maintenance.

b. Findings

No findings of significance were identified.

Enclosure

3

.2 Complete System Walkdown

a. Inspection Scope

The inspectors reviewed licensee procedures 3-OI-74, Residual Heat Removal,

Attachment 1, Residual Heat Removal System (RHR) System Valve Lineup Checklist,

Attachment 2, RHR System Panel Lineup, and Attachment 3, RHR System Electrical

Lineup, and conducted a complete system walkdown of the Unit 3 RHR Loop I. The

inspectors observed indications in the control room, on local panels and control stations,

and observed accessible equipment in the plant to verify material condition, and proper

alignment for standby operation. The inspectors compared switch and valve positions

observed in the field to the applicable procedure attachment requirements to verify

proper alignment. The inspectors also verified selected component positions against

plant drawing 3-47E811-1, RHR System Flow, and the system procedures to verify

correct alignment. The inspectors reviewed selected PERs and the PER database to

verify the licensee was identifying and correcting system deficiencies. The inspectors

also reviewed the system health report, operator workaround list, and the maintenance

rule reports to assess the overall system condition.

b. Findings

No findings of significance were identified.

1R05 Fire Protection Walkdown

a. Inspection Scope

The inspectors reviewed licensee procedure, SPP-10.10, Control of Transient

Combustibles, and SPP-10.9, Control of Fire Protection Impairments, and conducted a

walkdown of the six fire areas listed below to verify a selected sample of the following:

licensee control of transient combustibles and ignition sources; the material condition of

fire equipment and fire barriers; operational lineup; and operational condition of selected

components. Also, the inspectors verified that those selected fire protection

impairments were identified and controlled in accordance with the procedure SPP-10.9.

In addition, the inspectors reviewed the Site Fire Hazards Analysis and applicable

Pre-fire Plan drawings to verify that the necessary fire fighting equipment, such as fire

extinguishers, hose stations, ladders, and communications equipment, were in place.

The inspectors reviewed a sampling of fire protection-related PERs to verify that the

licensee was identifying and correcting fire protection problems. Pre-fire Plan drawings

and documents reviewed are included in the attachment to the report.

  • Fire Area 25, Cable Tunnel
  • Fire Area 25, Intake Pumping Structure
  • Fire Area 16, Unit 2 Control Building Elevation 617

Enclosure

4

  • Fire Area 18, Unit 2 Control Building Elevation 606
  • Fire Area 16, Unit 3 Control Building Elevation 606
  • Fire Area 16, Unit 1 Control Building Elevation 593

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

.1 Resident Inspector Quarterly Review of Testing and/or Training Activities

a. Inspection Scope

The inspectors observed portions of an operator annual examination on November 5,

2003. The inspectors observed three different job performance measures (JPMs)

performed on the plant control room simulator. The inspectors reviewed licensee

procedures TRN-11.4, Continuing Training for Licensed Personnel, TRN-11.9, Simulator

Exercise Guide Development and Revision, and OPDP-1, Conduct Of Operations, to

verify that the conduct of training, the formality of communication, procedure usage,

alarm response, and control board manipulations were in accordance with the above-

referenced procedures. The inspectors compared actions contained in the JPMs to

operations procedures to verify they matched. The inspectors reviewed the JPMs to

verify they identified operator actions that were critical to safe operation. The inspectors

also assessed instructor interface and control of the examination process. The specific

JPMs observed included the following:

  • JPM 500, Verification of Offsite Power Availability to 4.16 KV Shutdown Boards

Through FCV-84-19

  • JPM 39, Crosstie CAD to Drywell Control Air

b. Findings

No findings of significance were identified.

.2 Licensed Operator Requalification (Biennial Review)

a. Inspection Scope

During the week of November 17-21, 2003, the inspectors reviewed documentation,

interviewed licensee personnel, and observed the administration of simulator operating

tests and Job Performance Measures (JPMs) associated with the licensees operator

requalification program. Each of the activities performed by the inspectors was done to

assess the effectiveness of the licensee in implementing requalification requirements

identified in 10 CFR 55, Operators Licenses. Evaluations were also performed to

Enclosure

5

determine if the licensee effectively implemented operator requalification guidelines

established in NUREG-1021, Operator Licensing Examination Standards for Power

Reactors, and Inspection Procedure 71111.11, Licensed Operator Requalification

Program. The inspectors also reviewed and evaluated the licensees simulation facility

for adequacy for use in operator licensing examinations. The inspectors observed three

crews during the performance of the operating tests. Documentation reviewed included

written examinations, JPMs, simulator scenarios, licensee procedures, on-shift records,

licensed operator qualification records, watchstanding and medical records, simulator

modification request records and performance test records, the feedback process, and

remediation plans. The records were inspected against the criteria listed inspection

Procedure 71111.11. Documents reviewed during the inspection are listed in the

Attachment.

Following the completion of the annual operating examination testing cycle which ended

on December 4, 2003, the inspectors reviewed the overall pass/fail results of the

individual JPM operating tests, and the simulator operating tests administered by the

licensee during the operator licensing requalification cycle. These results were

compared to the thresholds established in NRC Manual Chapter 609 Appendix I,

Operator Requalification Human Performance Significance Determination Process.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

The inspectors reviewed the two samples listed below for items such as: (1) appropriate

work practices; (2) identifying and addressing common cause failures; (3) scoping in

accordance with 10 CFR 50.65(b) of the maintenance rule; (4) characterizing reliability

issues for performance; (5) trending key parameters for condition monitoring; (6)

charging unavailability for performance; (7) classification and reclassification in

accordance with 10 CFR 50.65(a)(1) or (a)(2); and (8) appropriateness of performance

criteria for SSCs/functions classified as (a)(2) and/or appropriateness and adequacy of

goals and corrective actions for SSCs/functions classified as (a)(1).

  • Unit 2 and 3 containment isolation valves experienced several failures. The

failures were documented as part of the licensees corrective action program in

the following PERs, PER 03-006747-000, PER 03-017441-000, PER 03-002719-

000, and PER 03-021813-000.

Enclosure

6

b. Findings

Introduction: A self-revealing non-cited violation (NCV) (Green) of 10 CFR app. B was

identified for inadequate procedure guidance during maintenance activities on Control

Rod Drive (CRD) pump 3A.

Discussion: On October 14, 2003, CRD Pump 3A was removed from service for a 40

hour inboard seal replacement outage. Maintenance on CRD pump 3A was conducted

using procedure MCI-0-085-PMP001, Control Rod Drive Hydraulic Pump - Worthington

2 WT-810 Disassembly, Inspection, Rework and Reassembly. Following maintenance,

the licensee conducted a post maintenance test (PMT) on the pump by performing

section 8.1 of procedure, 3-OI-85, Control Rod Drive System. During the PMT, the

pump seal rubbed sufficiently to cause sparking and the pump was immediately

secured. Subsequent investigation revealed that the drive collar was up against the

gland plate. The pump was out of service an additional 131 hours0.00152 days <br />0.0364 hours <br />2.166005e-4 weeks <br />4.98455e-5 months <br /> for seal maintenance

rework. Later, upon return to service, oil leaked from the inboard bearing causing

Operations to classify the pump as emergency use only for an additional four days.

The oil leak was caused by misadjustment of the Trico oil bubbler. The bubbler was

later adjusted and the pump returned to service. During the maintenance and rework

activity the redundant CRD pump, 3B, was operable and in service. In addition, all other

high pressure sources of water makeup were available.

The inspectors reviewed maintenance work orders, procedure MCI-0-085-PMP001, and

observed field work and the post maintenance test. The inspectors observed work

practices that were inconsistent with the vendor manual, such as specifically checking

seal clearances, ensuring the seal was wet and thoroughly vented prior to pump startup.

The inspectors also found that the procedure did not provide any guidance for setting

the proper seal clearance, for initial run-in of the seal, or for adjusting the Trico oil

bubbler.

Analysis: The inspectors referred to MC 0612 and determined that the finding was more

than minor in that it is associated with the Mitigating Systems and Initiating Events

cornerstones and affected the respective objectives of equipment performance and

availability. For the Mitigating Systems aspect, the CRD system is credited as a high

pressure source of inventory makeup under certain operational conditions. Additional

unavailability impacts this makeup source. For the Initiating Events aspect, the

unavailability of both CRD pumps leads to a condition where the Unit 3 Technical

Specifications for operability of CRD accumulators requires an immediate unit scram.

The inspectors referred to MC 0609, Significance Determination Process, and

determined that the finding was of very low safety significance (Green) because the

conditional core damage frequency for this scenario duration was less than1E-6, and

the standby pump was available and in service during the activity. Other high pressure

sources of water makeup were also available. Additionally, operations was aware of the

misadjusted oil bubbler and CRD pump 3A could have been operated in an emergency

situation.

Enclosure

7

Enforcement: 10 CFR 50, Appendix B, Criterion V, Instructions Procedures and

Drawings, Requires, in part, that, activities affecting quality shall be prescribed by

documented instructions, procedures, and drawings, of a type appropriate to the

circumstances and shall be accomplished in accordance with the instructions. Contrary

to this, on October 16, 2003, quality procedure MCI-0-085-PMP001 was fully

implemented and resulted in damage to the seal of quality related CRD pump 3A that

required additional seal replacement. The procedure did not contain guidance

necessary to correctly install a new seal or directions on how to correctly adjust the oil

bubbler. Because this violation is of very low safety significance and has been entered

in the licensees corrective action program under PER 03-0020163-000, this violation is

being treated as an NCV, consistent with Section VI.A of the NRC Enforcement Policy:

NCV 05000296/2003005-01, Inadequate Maintenance Procedure for Control Rod Drive

Pump 3A.

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

For the seven risk and emergent work assessments listed below, the inspectors

reviewed licensee actions taken to plan and control the work activities to effectively

manage and minimize risk. The inspectors verified that risk assessments were being

performed as required by 10 CFR 50.65(a)(4). The inspectors reviewed: licensee

procedure SPP-6.1, Work Order Process Initiation; SPP-7.1, Work Control Process; and

0-TI-367, BFN Dual Unit Maintenance, to verify that procedure steps and required

actions were met. Also, the inspectors evaluated the adequacy of the licensees risk

assessments and the implementation of compensatory measures. In addition, the

inspectors conducted a review of scheduled work activities for work week 2352 with

emphasis on risk significant activities for Division I Core Spray and Fast Start Operability

tests for 3A and 3B Diesel generators. These work activities were identified at an

increased risk level (yellow) and was acceptable per the risk assessment.

  • 250 V DC main bank battery all intercell readings failed to meet procedure

acceptance criteria, PER 03-022727 (emergent)

  • Units 2 and 3: Thru wall leak on RHRSW B header piping inside pipe tunnel WO

03-19297-00, B level PER 03-19298-00 (emergent)

  • Units 3: During trouble shooting a leak was discovered in the diaphragm of valve

3-FCV-84-49, drywell or suppression chamber exhaust to SBGT, WO 03-09335-

00 (emergent)

  • 3A EHC Pump Pressure Indicator (3-PI-47-62) isolate and replacement, PER 03-

23296 (scheduled)

  • Work week 2352, covering planned maintenance activities for December 22

through December 28, 2003 (scheduled)

Enclosure

8

  • Units 2 & 3: 3B RHRSW pump motor failed electrical testing during performance

of WO 02-013695-00, motor replaced (emergent)

  • Units 2: HPCI pump experienced an unexpected suction source transfer from the

condensate storage tank to the suppression pool during testing WO 03-024812-

00 and PER 03-024777-00 (emergent)

b. Findings

No findings of significance were identified

1R14 Operator Performance During Non-Routine Evolutions and Events

a. Inspection Scope

On October 24 and 25, 2003, the inspectors observed operator performance during

activities to reduce Unit 3 reactor power to approximately 65% RTP to conduct power

suppression testing to identify possible fuel leaks. The inspectors observed the pre-job

brief and compared observed performance to the requirements of procedure ODM 3-3,

Pre-Evolution, Mid-, and End-of-Shift Briefings. The inspectors also reviewed

procedures OSIL-108, Reactivity Management Expectations, to verify that procedure

requirements were met for the power reduction. In addition, the inspectors compared

operator performance to the requirements of procedure 3-GOI-100-12A, Unit Shutdown

From Power Operation to Cold Shutdown and Reductions in Power During Power

Operations.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the following five operability evaluations to verify the technical

adequacy of the evaluation and ensure that the licensee had adequately assessed TS

operability. The inspectors reviewed the Updated Final Safety Analysis Report (UFSAR)

to verify that the system or component remained available to perform its intended

function. In addition, the inspectors reviewed compensatory measures to verify that

the measures worked as stated and the measures were adequately controlled. Where

applicable, the inspectors reviewed licensee procedure SPP-3.1, Corrective Action

Program, Appendix D, Guidelines For Degraded/Non-conforming Condition Evaluation

and Resolution of Degraded/Non-conforming Conditions, to ensure the licensees

evaluation met procedure requirements. The inspectors also reviewed a sampling of

PERs to verify the licensee was identifying and correcting any deficiencies associated

with operability evaluations.

Enclosure

9

  • Unit 2 flow control valves 2-FCV-77-15 and 16 due to AK18 relay operation

(PER 03-018092-00)

  • Units 2 and 3 control bay habitability zone inleakage due to unqualified duct work

(PER 03-017922-00)

  • Units 2 and 3 common station service transformers A and B load tap changer

control power transformers inadequate for their loads (PER 03-018143-00)

  • Unit 2 and 3 operability of various HFA relays observed as part of the licensees

ongoing inspection of approximately 1720 relays ( B level PER 03-18287-00)

code class 3 Section XI, for very low wall thickness due to rust and pitting

(PER 03-19298-00)

b. Findings

No findings of significance were identified.

1R16 Operator Work-Around (OWA) Review

a. Inspection Scope

The inspectors reviewed the status of OWAs for Units 2 and 3 to determine if the

functional capability of the system or operator reliability in responding to an initiating

event was affected. The review was to evaluate the effect of the OWA on the operators

ability to implement abnormal or emergency operating procedures during transient or

event conditions. The inspectors conducted a detailed review of the selected OWA that

required operators to verify flow of the control room environmental control system within

five hours of initiation due to a possible low flow condition. The OWA was identified at

the highest level priority (1) to expedite corrections. The inspectors also verified that the

OWA had been reviewed in accordance with site procedures and that work orders had

been developed and scheduled for repair. The inspectors also reviewed PER 03-

017922 associated with the OWA to verify that corrective actions had been established

to correct the deficiency. The inspectors compared their observations and licensee

actions to the requirements of Operations Directive Manual 4.11, Operator Work Around

Program and TVAN Standard Department Procedure OPDP-1, Conduct of Operations.

  • OWA 0-031-OWA-2003-0111, verify flow of the control room environmental

control system

b. Findings

No findings of significance were identified.

Enclosure

10

1R19 Post-Maintenance Testing (PMT)

a. Inspection Scope

The inspectors evaluated the following five activities by observing testing and/or

reviewing completed documentation to verify that the PMT was adequate to ensure

system operability and functional capability following completion of associated work.

The inspectors reviewed licensee procedure SPP-6.3, Post-Maintenance Testing, to

verify that testing was conducted in accordance with procedure requirements. For

some testing, portions of MMDP-1, Maintenance Management System, were

referenced.

SR-3.3.1.1.8(5)

  • Unit 2: PMT for 4KV Shutdown Board under voltage lockout relay (0-RLY-211-

000A/03C) following electrical maintenance

  • Unit 3: PMT on 3A Control Rod Drive Pump inboard seal replacement per 3-OI-

85, Control Rod Drive System

  • Unit 3: PMT on 3DN LPCI MG-set per MPI-0-074-BRG001, Inspection,

Lubrication, and Replacement of LPCI MG-Set Couplings and Bearings

  • Unit 3: PMT on RHR heat exchanger 3C following maintenance and cleaning

b. Findings

No findings of significance were identified.

1R20 Refueling and Outage Activities

.1 Unit 2 mid-cycle outage

a. Inspection Scope

Risk

Prior to the mid-cycle outage scheduled for October 28, 2003 - November 7, 2003, to

repair a steam leak in an extraction piping bellows in the condenser, correct leaking

components in the drywell, and repair an Electro Hydraulic leak, the inspectors reviewed

the Unit 2 mid-cycle Outage Risk Assessment Report, to verify that the licensee had

appropriately considered risk, industry experience, and previous site-specific problems

in developing and implementing a plan that assured maintenance of defense-in-depth.

The inspectors specifically reviewed the contingency plans for two Level Orange risk

conditions for decay heat removal during maintenance associated with Residual Heat

Removal Service Water system to verify that specific equipment protective actions were

identified. The inspectors review was compared to the requirements in licensee

procedure SPP-7.2, Outage Management. During identified high risk significant

conditions due to equipment availability and/or system configurations, inspectors

Enclosure

11

reviewed if contingency measures were identified and incorporated into the overall

outage and response plan. The inspectors walked down systems in the plant, observed

control room panel lineups and discussed posted risk conditions with operations and

outage personnel to assess licensee personnel knowledge of the risk condition and

mitigation strategies.

The inspectors reviewed the licensees root cause of the steam leak in the main steam

extraction piping, attended meetings with a bellows vendor expert, and reviewed the

licensees actions with respect to a manufacturing defect that led to the bellows failure.

The inspectors review assessed the adequacy of corrective actions and maintenance

activities prior to unit restart.

The inspectors attended two Plant Operations Review Committee (PORC) unit restart

meetings to assess licensee actions to review and discuss activities completed during

the outage and unit readiness for restart.

Unit Shutdown

The inspectors observed selected activities and monitored licensee controls over outage

activities listed below to verify that procedural and regulatory requirements were met.

The inspectors compared their observations to licensee procedure SPP-12.1, Conduct

of Operations, and 2-GOI-100-12A, Unit Shutdown from Power Operations to Cold

Shutdown and Reduction in Power During Power Operations, to verify that procedure

requirements were met. Part of the activities observed included the following:

  • Unit power reduction with control rods and recirculation system flow
  • Core thermal limit verification
  • Reactivity monitoring and control
  • Startup, shutdown, and realignment of components and systems
  • Realignment and transfer of AC power sources
  • TS instrument and system performance verification

Decay Heat Removal

The inspectors reviewed licensee procedures 2-OI-74, Residual Heat Removal System

(RHR), and conducted a main control room panel walkdown to verify correct system

alignment. The inspectors reviewed operational logs to verify that procedure and TS

requirements to monitor and record reactor coolant temperatures were met. In addition,

the inspectors reviewed controls implemented to ensure that outage work was not

impacting the ability of operators to operate RHR shutdown cooling.

Enclosure

12

Reactivity Control

The inspectors observed licensee performance during shutdown, outage, and startup

activities to verify that reactivity control was conducted in accordance with procedure

and TS requirements. Inspector observations were compared to procedure SPP-10.4,

Reactivity Management, to verify that procedure and TS requirements were met.

Reactivity manipulations observed included the following:

Inspectors also observed the following items to assess licensee performance in the

respective area:

Inventory Control

  • Reactor water inventories and controls including flow paths, system

configurations, and alternate means for inventory addition

  • Operator monitoring and control of reactor temperature and level

Electrical Power

  • Controls over electrical power systems and components to ensure that

emergency power was available as specified in the outage risk report

  • Controls and monitoring of electrical power systems and components and work

activities in the power transmission yard

  • Operator monitoring of electrical power systems and outages to ensure that TS

requirements were met

Containment Control and Closure

  • Verify torus and drywell walkdown and closeout prior to unit restart

Preparations and Unit startup

  • Unit startup checklist
  • Alignment of secondary systems to support startup
  • Pre-job briefing for unit startup
  • Reactivity management briefing

b. Findings

No findings of significance were identified.

Enclosure

13

1R22 Surveillance Testing

a. Inspection Scope

The inspectors either witnessed portions of surveillance tests or reviewed test data for

the seven risk-significant SSCs listed below, to verify the tests met TS surveillance

requirements, UFSAR commitments, and in-service testing (IST) and licensee

procedure requirements. The inspectors review was to confirm the testing effectively

demonstrated that the SSCs were operationally capable of performing their intended

safety functions. IST data was compared against the requirements of licensee

procedures 0-TI-362, Inservice Testing of Pumps and Valves, and 0-TI-230, Vibration

Monitoring and Diagnostics. The inspectors also reviewed procedures OSIL-108,

Reactivity Management Expectations, and ODM 3-3, Pre-Evolution, Mid-, and

End-of-Shift Briefings, to verify that procedure requirements were met for the

surveillance activities. The surveillances either witnessed or reviewed included:

  • 2-SR-3.9.2.2, One-Rod -Out Interlock Functional Test
  • 2-SR-3.6.1.3.5 (SD), Valve Cycled During Cold Shutdown, 2-FCV-74-47, and 48
  • 3-SR-3.5.3.3, RCIC System Rated Flow at Normal Operating Pressure (IST)
  • 2-SI-4.5.C.1(3), RHRSW Pump and Header Operability and Flow Test (IST)

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed licensee procedures 0-TI-405, Plant Modifications and Design

Change Control; 0-TI-410, Design Change Control; SPP-9.5, Temporary Alterations;

and the two temporary modifications listed below to ensure that procedure and

regulatory requirements were met. The inspectors reviewed the associated

10 CFR 50.59 screening against the system design bases documentation to verify that

the modifications had not affected system operability/availability. The inspectors

reviewed selected completed work activities and walked down portions of the systems to

verify that installation was consistent with the modification documents and Temporary

Alteration Control Form (TACF).

battery charger B2-2 with a new charger from Stored Energy Systems (SENS)

Enclosure

14

  • TACF 02-03-069, Revision 0, replace Unit 2 Regenerative Heat Exchanger 2A

shell-side relief valve, 2-RFV-69-571 with new type of valve

b. Findings

No findings of significance were identified

4. OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification

Cornerstones: Mitigating Systems, Initiating Events

.1 Safety System Unavailability - High Pressure Injection System

and Scrams With Loss of Normal Heat Sink

a. Inspection Scope

The inspectors reviewed the licensees procedures and methods for compiling and

reporting PIs, including Procedure SPP-3.4, Performance Indicator for NRC Reactor

Oversight Process, for Compiling and Reporting PIs to the NRC. The inspectors

reviewed raw PI data for the PIs listed below for the fourth quarter 2002 through the

third quarter 2003. The inspectors compared graphical representations, from the most

recent PI report to the raw data to verify that the data was correctly reflected in the

report. The inspectors reviewed licensee procedure SPP 6.6, Maintenance Rule

Performance Indicator Monitoring, Trending and Reporting - 10 CFR 50.65; category A

and B PERs; engineering evaluations and associated PERs; and licensee records to

verify that the PI data was appropriately captured for inclusion into the PI report, and the

PI was calculated correctly. The inspectors reviewed Nuclear Energy Institute (NEI)

99-02, Regulatory Assessment Performance Indicator Guideline, to verify that industry

reporting guidelines were applied.

  • Unit 2 Safety System Unavailability - High Pressure Injection
  • Unit 3 Safety System Unavailability - High Pressure Injection
  • Unit 2 Scrams With Loss of Normal Heat Sink
  • Unit 3 Scrams With Loss of Normal Heat Sink

b. Findings

No findings of significance were identified.

Enclosure

15

4OA2 Identification and Resolution of Problems

a. Inspection Scope

As required by Inspection Procedure 71152, Identification and Resolution of Problems,

and in order to help identify equipment failures or specific human performance issues

for follow-up, the inspectors performed a daily screening of items entered into the

licensees corrective action program. This review was accomplished by a combination

of reviewing hard copies of each condition report, attending daily screening meetings

and accessing the licensees computerized database.

Annual Sample Review

The inspectors selected two PERs for detailed review (PER 03-006967-000 and

00-002340-000). The first PER was associated with the licensees discovery of the

RHRSW discharge flow control valve for RHR heat exchanger 2C stem separated

from the cage; and the second PER dealing with the adequacy of human performance

root cause analysis. The PERs were reviewed to verify that the full extent of the issues

was identified, an appropriate evaluation performed, and appropriate corrective actions

were specified and prioritized. The PERs were evaluated against the requirements of

the licensees CAP as delineated in the Standard Programs and Processes Procedure

SPP-3.1, Corrective Action Program, and 10 CFR 50, Appendix B.

b. Findings and Observations

PER 03-006967-000: There were no identified findings associated with the review of

this sample. The PER was written to evaluate low RHRSW pressure in the 2C RHRSW

subsystem. Hand tightening of valve FCV-23-40, RHRSW discharge flow control valve

for RHR Heat exchanger 2C, indicated valve seat leakage and the PER was revised to

03-006967-001 to disassemble and repair at the first available outage. When the valve

was disassembled during the mid-cycle outage in October, it was found to have its cage

separated from the stem. The inspectors noted, that, though four PERs were written for

emergent difficulties with this valve work, none had a problem description relating

specifically to stem separation. One of the emergent PERs dealt with a problem in

welding activities to weld the valve stem nut to the disc and mentioned that the stem

was separated however, the PER did not specifically focus on the fact that the valve was

found in an unexpected condition, i.e., separated. This was an example of an instance

where a specific PER was not written and the problem description of existing PERs was

incomplete.

PER 00-002340-000: There were no identified findings associated with the review of

this sample. This B Level PER, stated that, in many cases, the human performance root

cause analysis do not get to the fundamental cause of the problem. A search of the

corrective action database revealed that a previous root cause issue was identified in a

1998 PER (98-009421-000). The PER indicated that the analyses of some plant events

did not determine the fundamental reason for human performance deficiencies.

Enclosure

16

The 1998 PER indicated that a sample determined that the root cause analyses for

seven of ten human performance related PERs were weak or inadequate. The root

cause in the PER stated that the inadequacies were caused by failures to follow through

on previously identified corrective actions due to insufficient management oversight.

The inspectors noted that the licensee has now assigned the responsibility for the root

cause analysis (RCA) to the manager of human performance/self-assessment (HP/SA);

expectations for RCAs were that they must include at least one individual who had

attended the RCA training course and the HP/SA manager was to evaluate the need for

refresher training based on RCA quality; develop and pilot a RCA refresher training

course to bring previously trained individuals up to speed on recent changes to the

human performance model, present the refresher training course to all management

review committee(MRC) members, and present the course to personnel identified by

site management to include personnel involved in determination of apparent causes.

The licensee performed an effectiveness review of PER 00-002340-000 and

confirmed that the deficiencies in root causes for human performance did not meet

their expectations. The causal analysis of events triggered by human error continued

to be ineffective in identifying fundamental causes, especially those related to process

and organizational contributors. The inspectors noted that the licensee recently placed

a renewed emphasis on this problem. The inspectors also noted that the root causes

for equipment related problems were generally thorough, detailed, and correct and did

not contain similar root cause deficiencies. This was an example where the

effectiveness of PER corrective actions did not meet licensee managements

expectations.

4OA3 Event Follow-up

Closed: Licensee Event Report (LER) 05000260/2003-005-00: Unplanned Start of DG

A and DG B from Momentary Board Undervoltage

On August 10, 2003, 4KV Shutdown Bus 1 alternate supply breaker failed to

automatically close when the normal supply breaker was manually opened during

electrical switching activities. Operators observed that the alternate supply breaker

failed to close and immediately reclosed the normal supply breaker. As a result, the

shutdown bus lost power for about five seconds. Due to the momentary loss of power

to the shutdown bus, DG A and B automatically started, but did not tie to the bus due

to the short duration of the power loss. Other engineered safety features automatically

started and responded as expected for the loss of power. The licensee determined that

the root cause of the equipment failure was that a connector internal to the breaker had

come off its termination point. The licensee had previously identified that an amber light

on the alternate feeder breaker panel was extinguished and had written an work order

to trouble shoot and repair the problem. However, they failed to realize that the open

circuit that caused the amber light to be extinguished prevented current flow through the

breaker closing coil, thus preventing closure of the alternate supply breaker.

Enclosure

17

The licensee restored equipment to the standby condition, corrected the connection

problem, and initiated long term corrective actions. The LER was reviewed by the

inspectors and no findings of significance were identified. The licensee entered this

problem into the corrective action program as Problem Evaluation Report (PER) 03-

00015160-00.

4A05 Other

(Closed) Unresolved Item (URI) 05000296/2003007-01: Inadequate Unit 3 Fire

Procedure Directs Local Manual Operator Action Be Performed In Location of Fire

During the triennial fire protection inspection (NRC Inspection Report 05000260,

296/2003007, dated November 17, 2003), the inspectors identified a finding having

potential safety significance greater than very low significance, involving procedural

guidance in the Safe Shutdown Instruction (SSI) for Fire Area 13 (Unit 3 480 V RMOV

Board Room 3A) that directed an operator to enter the location of the fire to perform a

local manual action associated with tripping the Unit 3 Reactor Recirculation Pumps

(RRPs). Specifically, Attachment 6, Steps 1.1 and 1.2 of 2/3-SSI-13 directed an

operator to go to 250 V Reactor MOV Board 3A and place the control power breaker

(breaker 1B1) for 4 KV Recirculation Pump Trip (RPT) Board 3-II to off. This action may

not be successful for a severe fire in this room because of the high temperatures, heavy

smoke, low visibility and hazardous plant conditions that would likely be encountered by

the operator while the action is performed. This URI was opened pending further NRC

review of the safety significance of the finding.

The inspectors reviewed licensee calculation ND-Q0999-92116, Appendix R Manual

Action Requirements, Revision 17. This calculation required the RRPs to be tripped

during a severe fire in Fire Area 13 from 4 KV RPT Board 3-II. Additionally, to prevent

potential RRP restart, control power to the RPT board was to be tripped. In general,

RPT control power can be removed by individually opening breaker 1B1 on 250 V

Reactor MOV Board 3A or by totally de-energizing this bus. Normal power to 250 V

Reactor MOV Board 3A is provided from 250 V Battery Board 3 via breaker 203. 250 V

Battery Board 3 is located in different fire area separate from Fire Area 13.

Recognizing that 250 V Reactor MOV Board 3A would be in the location of the fire,

Appendix B, Section Fire Zone/Area 13, of the calculation identified that RPT control

power should be removed by opening breaker 203 in Battery Board Room 3 (to totally

de-energize 250 V Reactor MOV Board 3A.) This requirement was captured in

Attachment 1, Step 1.4.1 of procedure 2/3-SSI-13. Consequently, the operator action at

issue in this URI was redundant and not needed to successfully remove RPT control

power. The licensee initiated a procedure change request (PCR 20031551) to correct

this procedure error.

After reviewing plant operating procedures, operator training and conducting operator

interviews, the inspectors found that several other well known (skill-of-the-craft) methods

were available to the operators for ensuring that the RRPs would be tripped during a

Enclosure

18

severe fire in Fire Area 13. The inspectors concluded that the erroneous procedure

guidance specified in Attachment 6 of 2/3-SSI-13 would have minimal impact on the

operators ability to safely shutdown the Unit 3 reactor. Because this issue has minimal

safety significance and has been documented in the licensees corrective action

program (PER 03-013882-000), this issue is considered to be minor.

URI 05000296/2003007-01 is closed.

4OA6 Management Meetings

Exit Meeting Summary

On January 16, 2004, the resident inspectors presented the inspection results to

Mr. Ashok Bhatnager and other members of his staff, who acknowledged the findings.

The inspectors confirmed that proprietary information reviewed by the inspectors

during the inspection period was returned to the licensee.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Enclosure

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel

T. Abney, Nuclear Site Licensing & Industry Affairs Manager

A. Bhatnagar, Site Vice President

L. Clardy, Site Nuclear Assurance Manager

C. Ottenfeld, Chemistry Manager

R. Jones, Unit 1 Restart Manager

K. Kruger, Assistant Nuclear Plant Manager

J. Lewis, Nuclear Plant Operations Manager

B. Marks, Engineering & Site Support Manager

B. Mitchell, Radiation Protection Manager

J. Ogle, Site Security

P. Olsen, Maintenance & Modifications Manager

M. Skaggs, Nuclear Plant Manager

T. Golden, Operations Site Licensing Engineer

P. Meek, Operations Site Licensing Engineer

J. Wallace, Operations Site Licensing Engineer

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Closed

05000296/2003005-01 NCV Inadequate Maintenance Procedure for Control

Rod Drive Pump 3A (Section 1R12)

05000260/2003-05 LER Unplanned Start of DG A and DG B from

Momentary Board Undervoltage (Section 4OA3.1)05000296/2003007-01 URI Inadequate Unit 3 Fire Procedure Directs Local

Manual Operator Action Be Performed In Location

of Fire (Section 4A05)

Attachment

2

LIST OF DOCUMENTS REVIEWED

Section 1R04: Equipment Alignment

0-OI-23, Attachment 1B, RHRSW system valve lineup checklist Unit 2

0-OI-23, Attachment 2B, RHRSW system panel lineup checklist Unit 2

2-OI-85, Attachment 1, CRD Hydraulic System Valve Lineup Checklist

2-OI-85, Attachment 2, CRD Hydraulic System Panel Lineup Checklist

2-OI-85, Attachment 3, CRD Hydraulic System Electrical Lineup Checklist

Drawing 3-15E500-3

Section 1R05: Fire Area Tours

Fire Hazards Analysis, Volume 1 and 2

Fire Pre-Plans: IS-550, IS 565, CB2-617, CB3-606, CB2-606

Smoke Detector Locations: Procedure 0-SI-4.11.A.1(3)b

Section 1R11.2: Operator Requalification

BFN-TRN-03-007 Self Assessment Report

Browns Ferry Simulator Transient Test Raw Data

Design Change Request Report

Simulator Problem Report

TRN 11.4 Continuing Training For Licensed Personnel

TRN-11.9 Simulator Exercise Guide Development and Revision

TRN 11.10 Annual Requalification Examination Development and Implementation

TRN -11.12 Job Performance Measures Development Administration and Evaluation Manual

TRN-11.14 TVA Operator Licensing examination Security Program

TRN-12 Simulator Regulatory requirements

OPDP-1 Conduct of Operations

Operation Logs

CAD Records

Reactivation Records

Medical Records

Section 1R20.1: Refueling and Outage Activities

0-OI-57A, Switchyard and 4160 Electrical System

2-SR-3.6.1.2.1, Drywell Airlock LLRT

2-SR-3.6.1.3.5(SD), Valves Cycled During Cold Shutdown

2-SI-3.2.12, Verification Of Fail-Safe Position For MSIVs

2-AOI-100-1. Reactor Scram

2-GOI-100-1A, Unit Startup from Cold Shutdown to Power Operations and Return to Full Power

from Power Reductions

2-GOI-200-2, Drywell Closeout

2-OI-68, Reactor Recirculation System

3

Section 4OA1:Performance Indicator (PI) Verification

Procedures

SPP-3.4, Performance Indicator for NRC Reactor Oversight Process, Rev. 0

Desktop Guide for Identification and Reporting of NEI 99-02, Rev. 2 Performance Indicators

Section 40A5: Other

Procedures

2/3-SSI-13, Unit 3 480 V RMOV Board Room 3A, Rev. 5

Calculations

ND-Q0999-920116, Appendix R Manual Action Requirements, Rev. 17

Procedure Change Requests (PCR) Initiated

PCR 20031551, Delete duplicate action to open RPT Control Power breaker on 250V RMOV

Board 3A, dated 11/18/03