ML031390384

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IR 05000255-03-005, 03/24-04/04/03, Nuclear Management Company, Palisades Nuclear Generating Plant; Special Inspection - March 18, 2003
ML031390384
Person / Time
Site: Palisades Entergy icon.png
Issue date: 05/19/2003
From: Grant G
Division Reactor Projects III
To: Cooper D
Nuclear Management Co
References
IR-03-005
Download: ML031390384 (35)


See also: IR 05000255/2003005

Text

May 19, 2003

Mr. Douglas E. Cooper

Site Vice President

Palisades Nuclear Plant

Nuclear Management Company, LLC

27780 Blue Star Memorial Highway

Covert, MI 49043-9530

SUBJECT: PALISADES NUCLEAR GENERATING PLANT

NRC SPECIAL INSPECTION REPORT 50-255/03-05

Dear Mr. Cooper:

On April 4, 2003, the U.S. Nuclear Regulatory Commission (NRC) completed a special

inspection at your Palisades Nuclear Generating Plant to review the circumstances surrounding

two Alert emergency declarations on March 18, and March 25, 2003. The enclosed report

documents the inspection findings which were discussed on April 4, 2003, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The team reviewed selected procedures and records, observed activities, and interviewed

personnel.

On March 18, 2003, a fire started in a safety-related breaker cubicle in the cable spreading

room. An emergency plan Alert (the second lowest of four emergency classification levels)

condition was declared due to a fire that could impact safety-related equipment. Your staff

secured from the Alert after about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> when the fire was extinguished and the source of the

fire was identified.

On March 25, 2003, plant maintenance workers were installing signposts in the parking lot to

designate parking spaces. One of the signposts was driven into a conduit and damaged a

cable which contained protective relay circuitry for all sources of offsite power. An Alert was

declared due to the loss of offsite power combined with the loss of shutdown cooling. The Alert

was downgraded to an Unusual Event (the lowest of four emergency classification levels) after

about 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> when shutdown cooling was restored. Your staff secured from the Unusual Event

on March 27, 2003, when offsite power was restored.

Both of these events could have been avoided. Inadequate breaker maintenance procedures

coupled with a number of human performance errors in the operations and maintenance areas

resulted in the March 18, 2003, cable spreading room fire. In addition, a weakness in the

implementation of your corrective action program was a primary contributor to the

March 25, 2003, loss of offsite power event. Both the human performance and problem

identification and resolution areas were previously identified as substantial cross-cutting issues

D. Cooper -2-

and were discussed in our March 4, 2003 annual assessment letter to you. The human

performance substantial cross-cutting issue was closed in our letter since no findings involving

human performance had been identified since the first quarter of the 2002 assessment period.

However, the human performance errors which occurred on March 18, 2003 indicates that this

area may again be a challenge which warrants your immediate attention. The problem

identification and resolution area was a substantial cross-cutting area which remained open in

our letter since improvements in this area had only recently been implemented. The

March 25, 2003 event indicates that these improvements have not been fully effective and that

further improvements are necessary before this area can no longer be considered a substantial

cross-cutting issue.

Based on the risk and deterministic criteria specified in Management Directive 8.3, NRC

Incident Investigation Program, and Inspection Procedure 71153, Event Followup, and due to

the equipment performance problems which occurred, a Special Inspection was initiated in

accordance with Inspection Procedure 93812, Special Inspection, to evaluate the facts and

circumstances surrounding the events as well as the actions taken by your staff in response to

the unexpected system performance issues encountered. The inspection focused on: (1) the

sequence of events for each Alert; (2) the adequacy of your evaluation of the events and

corrective actions; (3) any common causes or relationship between the two events; (4) the

operational performance issues associated with the repeated attempts to restart charging pump

P-55A; (5) any equipment performance issues during the two events; (6) maintenance

performance issues associated with the missing arc chutes for the charging pump P-55A

breaker; (7) design issues associated with the offsite power configuration and any changes to

address the event; and (8) the emergency plan actions to address the events.

Based on the results of this inspection, two self-revealed findings of very low safety significance

which involved violations of NRC requirements were identified. However, because these

violations were non-willful and non-repetitive and because they were entered into

your corrective action program, the NRC is treating these findings as Non-Cited Violations in

accordance with Section VI.A.1 of the NRCs Enforcement Policy.

The NRC identified one finding for which the final risk significance remains to be determined at

a later date. The finding concerned the failure of site management to take adequate corrective

actions after a series of events during digging and excavating on station property between the

protected area and the switchyard. This finding did not present an immediate safety concern

because compensatory measures were put in place while long-term corrective actions were

being determined and implemented.

If you contest the subject or severity of a Non-Cited Violation, you should provide a

response within 30 days of the date of this inspection report, with the basis for your denial, to

the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC

20555-0001; with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission -

Region III, 801 Warrenville Road, Lisle, IL, 60532-4351; the Director, Office of Enforcement,

U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the Palisades facility.

D. Cooper -3-

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter

and its enclosure will be made available electronically for public inspection in the NRC Public

Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Geoffrey E. Grant, Director

Division of Reactor Projects

Docket No. 50-255

License No. DPR-20

Enclosure: Inspection Report 50-255/03-05(DRP)

cc w/encl: J. Cowan, Executive Vice President

and Chief Nuclear Officer

R. Fenech, Senior Vice President, Nuclear

Fossil and Hydro Operations

L. Lahti, Manager, Regulatory Affairs

J. Rogoff, Esquire, Nuclear Management Company, LLC

A. Udrys, Esquire, Consumers Energy Company

R. Remus, Plant Manager

D. Malone, Site Director

S. Wawro, Nuclear Asset Director, Consumers Energy Company

W. Rendell, Supervisor, Covert Township

Office of the Governor

Michigan Department of Environmental Quality -

Waste and Hazardous Materials Division

Department of Attorney General (MI)

DOCUMENT NAME: C:\ORPCheckout\FileNET\ML031390384.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RIII RIII RIII RIII

NAME EDuncan for EDuncan SReynolds for

CPhillips:dtp GGrant

DATE 05/16/03 05/16/03 05/19/03

OFFICIAL RECORD COPY

D. Cooper -4-

ADAMS Distribution:

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C. Ariano (hard copy)

DRPIII

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No: 50-255

License No: DPR-20

Report No: 50-255/03-05

Licensee: Nuclear Management Company, LLC

Facility: Palisades Nuclear Generating Plant

Location: 27780 Blue Star Memorial Highway

Covert, MI 49043-9530

Dates: March 24 through April 4, 2003

Inspectors C. Phillips, Senior Operations Engineer, Team Leader

J. Lara, Senior Resident Inspector, Kewaunee

C. Brown, Resident Inspector, Clinton

J. Lennartz, Senior Resident Inspector, Palisades

R. Krsek, Resident Inspector, Palisades

H. Gonzales, Nuclear Safety Intern

Approved by: Geoffrey E. Grant, Director

Division of Reactor Projects

SUMMARY OF FINDINGS

IR 05000255-03-05; Nuclear Management Company; 03/24 - 04/04/2003; Palisades Nuclear

Generating Plant; Special Inspection - March 18, 2003, Alert due to cable spreading room fire

and March 25, 2003, Alert due to loss of offsite power and temporary loss of shutdown cooling.

This report covered a 2-week period of special inspection by Region III inspectors and resident

inspectors. Two Green findings and one finding with a significance which is yet to be

determined were identified. The significance of most findings is indicated by their color (Green,

White, Yellow, Red) using Inspection Manual Chapter (IMC) 0609, Significance Determination

Process (SDP). Findings for which the SDP does not apply may be Green or be assigned a

severity level after NRC management review. The NRCs program for overseeing the safe

operation of commercial nuclear power reactors is described in NUREG-1649, Reactor

Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealed Findings

Cornerstone: Initiating Events

  • Green. A finding of very low safety significance was self-revealed during an event when

an operator failed to adhere to a procedure for operating the chemical volume control

system and repeatedly attempted to close a charging pump breaker after the breaker

tripped. In addition, the operator failed to trip primary coolant pumps before primary

coolant system pressure dropped below the minimum pressure for primary coolant

pump operation. The primary cause of this finding was related to the cross-cutting area

of Human Performance.

The finding was more than minor because it could be reasonably viewed as a precursor

to a significant event. The repeated operation of an electrical breaker contrary to

procedural requirements was a contributing cause to the March 18, 2003, cable

spreading room fire. The finding was determined to be of low safety significance

because the failure to follow the procedure did not result in a loss of shutdown cooling or

loss of reactor inventory. This issue was determined to be a Non-Cited Violation of

Technical Specification 5.4.1, which required the implementation of written procedures

covering the chemical volume control system and the reactor coolant system.

(Section 04.1)

  • Green. A finding of very low safety significance was self-revealed during an event when

the licensee failed to have adequate maintenance procedures in place to ensure that

when an electrical breaker was removed to be refurbished, that the arc chutes were

reinstalled before the breaker was placed back in service.

The finding was more than minor because it could be reasonably viewed as a precursor

to a significant event since a fire resulted in the P-55A charging pump breaker when the

arc chutes were not reinstalled after the breaker had been refurbished. The finding was

determined to be of low safety significance because the failure to follow the procedure

did not result in a loss of shutdown cooling or loss of reactor inventory. This issue was

determined to be a Non-Cited Violation of 10 CFR 50, Appendix B, Criterion V,

Instructions, Procedures, and Drawings. (Section 07)

  • TBD. The licensee failed to take effective corrective actions to address a series of

events involving digging and excavating between the protected area and the switchyard.

The finding was more than minor because it could be reasonably viewed as a precursor

to a significant event in that a maintenance technician drove a signpost into the ground

and damaged an electrical cable that resulted in a loss of offsite power and a loss of

shutdown cooling. No violation of regulatory requirements was identified since the act of

driving the signpost into the ground was not an activity affecting quality. (Section 02.2)

B. Licensee-Identified Violations

No findings of significance were identified.

2

REPORT DETAILS

Summary of Plant Events

Synopsis of Events

On March 18, 2003, a fire started in a safety-related breaker cubicle in the cable spreading

room. Although the fire did not spread beyond the cubicle, the room filled with smoke. The

licensee declared an Alert based on the existence of a fire that could affect safety-related

equipment. The licensee secured from the Alert about 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> later when it was determined

that a threat no longer existed.

On March 25, 2003, while shutdown for a refueling outage, a maintenance worker installing a

signpost in the parking lot struck an underground cable and cut and shorted together

conductors for protective circuitry that impacted circuit breakers for all sources of offsite power.

The licensee declared an Alert based on the complete loss of offsite power and the loss of

shutdown cooling. About 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> after the Alert declaration, the licensee downgraded the event

to an Unusual Event based on the recovery of shutdown cooling with both emergency diesel

generators supplying power to the safety-related buses. The licensee secured from the

Unusual Event on March 27, when power from a qualified offsite power source was restored to

the safety-related buses.

March 18, 2003 Cable Spreading Room Fire

On March 18, 2003, the plant was in Mode 5 (Cold Shutdown) and in a solid plant condition.

Two charging pumps were running at maximum speed with maximum letdown flow to expedite

the chemical cleanup of the primary coolant to reduce the coolant activity levels in preparation

for the refueling outage. The night shift operating crew was assigned to increase the

concentration of boric acid in the primary coolant by gravity feeding boric acid solution from the

B boric acid storage tank to the suction of the two running charging pumps. After the

operators realigned the boric acid suction path from the volume control tank to the B boric

acid storage tank, the P-55A charging pump breaker tripped. An operator attempted to restart

the P-55A charging pump three times. Arcing within the P-55A charging pump breaker caused

the failure of the wiring connections to the breaker anti-pump relay. Therefore, the breaker

attempted to re-close more times than the number of times the operator manipulated the

breaker control switch.

The rapid opening and closing of the breaker caused an arc to form within the breaker cubicle.

The breaker design included an arc chute installed on each phase to extinguish any arc that

may form upon breaker opening. However, due to the combination of an inadequate

maintenance procedure and human performance errors when the breaker was previously

refurbished, the P-55A charging pump breaker did not have the arc chutes installed. The

absence of the arc chutes resulted in a phase-to-phase arc forming which increased in

magnitude and ultimately damaged the breaker. The arc caused the cable spreading room to

fill with smoke.

3

The arc current caused the breaker supplying power to load control center (LCC)-12 to trip to

isolate the fault. The fire brigade responded promptly and the problem was quickly brought

under control.

Shutdown cooling continued to operate during the event. The primary coolant system

depressurized and due to human performance errors, the primary coolant pumps were not

secured before plant pressure dropped below the minimum pressure for primary coolant pump

operation.

March 25, 2003 Loss of Offsite Power

On March 25, 2003, with the plant in Mode 6 (Refueling), plant maintenance workers were

installing signs in the parking lot designating parking spaces. One of the signposts was driven

into a conduit and damaged a cable which contained a combination of energized indication

circuitry and de-energized protective relay circuitry. The metal signpost cut and shorted

together several of the conductors within the cable generating a fault signal to the breakers

supplying offsite power to the 345 kilovolt (kV) Rear (R) bus.

The R bus was supplying power to nonsafety-related loads through the startup transformer.

About 30 seconds later, the breaker between the safeguards transformer and the safeguards

bus tripped open resulting in a temporary loss of power to the safety-related buses. The

emergency diesel generators started and energized the safety-related 1C and 1D buses.

Shutdown cooling was lost, but was restored after about 20 minutes when the emergency

diesel generators started and shutdown cooling pumps were re-energized.

An Alert was declared based on the loss of offsite power combined with the loss of shutdown

cooling. The Alert was subsequently downgraded to an Unusual Event after shutdown cooling

was restored. A temporary modification was installed which re-routed the conductor for the

protective relaying of the startup transformer. The licensee secured from the Unusual Event on

March 27, 2003, when offsite power was restored.

Inspection Scope

Based on the risk and deterministic criteria specified in Management Directive 8.3, NRC

Incident Investigation Program, and Inspection Procedure 71153, Event Followup, and due to

the equipment performance problems which occurred, a Special Inspection was initiated in

accordance with Inspection Procedure 93812, Special Inspection.

The purpose of the inspection was to evaluate the facts and circumstances surrounding the

events as well as the actions taken by licensee personnel in response to the unexpected

system performance issues encountered. In particular, the inspection focused on the following:

(1) the sequence of events for each Alert; (2) the adequacy of the licensees evaluation of the

events and corrective actions; (3) any common causes or relationship between the two events;

(4) the operational performance issues associated with the repetitive attempts to restart

charging pump P-55A; (5) any equipment performance issues during the two events; (6)

maintenance performance issues associated with the missing arc chutes for the charging pump

P-55A breaker; (7) design issues associated with the offsite power configuration and any

changes as a result of the event; and (8) the emergency plan actions to address the events.

4

1 REACTOR SAFETY

Cornerstones: Initiating Events and Mitigating Systems

01 Sequence of Events (93812)

a. Inspection Scope

The inspector reviewed logs, alarm printouts, and other documentation; interviewed

licensee personnel; and developed the following sequence of events for the March 18,

2003, cable spreading room fire and the March 25, 2003, loss of offsite power:

March 18, 2003 Cable Spreading Room Fire

Day Time Event Description

3/18 19:00 The plant was in Mode 5, water solid condition with primary

coolant system (PCS) temperature at 120 degrees

Fahrenheit (EF). A chemical soak of the PCS was in progress to

reduce activity levels. Charging pumps P-55A and P-55B were

running with increased letdown flow to aid in PCS cleanup.

Primary Coolant Pumps (PCPs) 1A and 1D were running.

The operating crew made plans to increase boron concentration

in the PCS to that required for refueling activities by realigning the

suction of the charging pumps from the volume control tank (VCT)

to Boric Acid Storage Tank (BAST) T-53B.

20:36 A nuclear control operator (NCO-1) realigned the charging pump

suction from the VCT to BAST T-53B. NCO-1 unexpectedly

observed that BAST level did not change and PCS pressure was

decreasing. NCO-1 attempted to reduce letdown flow by closing

the controller for the letdown backpressure regulator, however

PCS pressure continued to decrease. NCO-1 noticed that

charging flow had decreased from about 107 gallons per minute

(gpm) to about 40 gpm and that charging pump P-55A had

tripped. Licensee personnel later determined that when the

suction source to the charging pump was changed, the suction

pressure decreased. The charging pump low suction pressure

switch had a time delay, but the switch had stuck in the tripped

position.

NCO-1 did not announce the charging pump trip or any other

actions, either before or after they were taken. A second

operator, NCO-2, announced the trip of charging pump P-55A.

NCO-1 attempted to restart P-55A unsuccessfully, but failed to

verify the on/off indication lights for the pump on the control panel.

NCO-1 cycled opened and closed the suction valve to the BAST

5

and again attempted to restart charging pump P-55A. During this

attempt, NCO-1 held the control switch closed for a longer period

under the belief that the control switch had not been closed long

enough during the previous attempt, but again did not visually

verify the pump on/off indication lights. NCO-2 observed that the

charging pump on/off indication lights cycled three or four times.

NCO-1 attempted to start charging pump P-55A unsuccessfully a

third time.

The control room supervisor (CRS) and shift supervisor (SS)

noticed the charging pump low suction pressure alarm and

increased activity at the control panel. The SS noticed that PCS

pressure had decreased below the minimum pressure for PCP

operation and directed the CRS to trip the PCPs. The CRS then

made a statement to trip the PCPs, but did not specifically direct

NCO-1 to trip the pumps. NCO-1 did not hear the statement by

the CRS and therefore did not repeat it back. The CRS was

distracted by a fire alarm from the cable spreading room and did

not ensure his direction to trip the PCPs was carried out. The SS

observed that the direction to trip the PCPs was not carried out

and directed NCO-1 to trip the PCPs. The NCO-1 then tripped

the PCPs. This entire sequence of events occurred over about 37

seconds.

Decreasing PCS pressure required the trip of the PCPs at 235

pounds per square inch absolute (psia) per Standard Operating

Procedure (SOP)-1, Primary Coolant System. However, the A

and D PCPs were not secured until reactor pressure was about

135 psia.

Off Normal Operating Procedure (ONP)-25.1, Fire in Safety

Related Area, was entered due to the cable spreading room fire

alarm.

20:39 The fire brigade was dispatched to respond to the cable spreading

room fire alarm.

20:47 An Alert was declared per the station Site Emergency Plan due to

a fire with the potential to affect safety-related equipment.

22:20 Procedure ONP-25.1 was exited when the fire brigade determined

that the fire was no longer present.

22:38 The Alert was terminated after the licensees investigation

determined that the fire was extinguished and was isolated to the

circuit breaker for charging pump P-55A.

6

March 25, 2003 Loss of Offsite Power

Day Time Event Description

3/25 11:15 The plant was in Mode 6. The 345 kilovolt (kV) switchyard

front (F) bus was supplying power to the safeguards transformer

and through Breaker 152-401 to the safeguards bus (see the last

page of this report for a simplified diagram of the electrical

distribution system). All safety-related 2400 volt alternating

current (Vac) buses were energized from the safeguards bus.

The 345 kV switchyard rear (R) bus was supplying power to the

startup transformer, which was available as a backup power

source to the safety-related 2400 Vac buses. All 4160 Vac buses

and nonsafety-related 2400 Vac buses were energized from

startup transformer feeder breakers. The main generator output

breakers were closed. Motor-operated disconnect M26H5 was

open, interrupting backfeed power to the main transformer. The

reactor vessel head was removed and the reactor cavity was

partially flooded to about 6 feet above the reactor vessel flange.

Nozzle dams were installed in the reactor coolant loops. Service

air was supplied to the nozzle dams to prevent leakage from the

reactor vessel to the coolant loops. Primary coolant system

temperature was 94EF.

11:16 Building and grounds workers replaced two signposts for parking

signs alongside the site access road. The signposts were

installed by pounding them directly into the ground using an

impact tool. The second signpost installed was inadvertently

driven into a buried conduit and shorted together protective relay

conductors. This caused the protective relays to actuate and

resulted in a loss of offsite power and a loss of shutdown cooling.

The control room received numerous alarms indicating that all

switchyard circuit breakers feeding the R bus had opened.

Shortly thereafter, Breaker 152-401 also opened, resulting in a

loss of offsite power.

Operators entered ONP-2.1, Loss of AC [Alternating Current]

Power, and ONP-17, Loss of Shutdown Cooling.

Both emergency diesel generators (EDGs) started and closed

onto their respective buses. Service air was initially lost and was

subsequently realigned to backup nitrogen bottles to provide air to

the nozzle dams.

11:21 Control room operators verified that the 1C and 1D buses were

re-energized from their respective EDGs.

7

11:26 The shift supervisor declared an Alert per the Site Emergency

Plan for the loss of offsite power and loss of shutdown cooling

event.

11:36 Control room operators restored shutdown cooling to service.

Primary coolant system temperature increased from 94EF to

104EF while shutdown cooling was unavailable.

11:57 Control room operators stabilized PCS temperature. The highest

PCS temperature reached was 104EF.

12:06 Control room operators authorized re-opening containment

penetration M7-10 service air to restore air to the nozzle dams.

12:22 Operators restored the service air lineup to containment.

12:31 The site emergency director downgraded the emergency

classification from an Alert to an Unusual Event with shutdown

cooling restored and the EDGs providing power to safety-related

buses 1C and 1D.

13:37 Control room operators exited ONP-17 and continued actions to

restore offsite power.

14:25 Operators reset relay 486 S-X1 in order to re-energize the R bus.

Restoration of the R bus was necessary in order to restore offsite

power transmission line reliability.

14:27 Operators opened disconnect 24R2 to isolate the startup

transformer from the R bus. Control room operators then restored

the R bus. Control room operators did not restore power to the

startup transformer because the cause of the loss of offsite power

remained unknown.

17:30 Operators closed Breaker 152-401 and energized non-safeguards

loads. The cause of Breaker 152-401 to trip remained unknown.

However, licensee management concluded that there was no

existing electrical bus or breaker fault and closed

Breaker 152-401 to supply power to nonsafety-related bus 1E.

The EDGs continued to supply power to safety-related buses 1C

and 1D.

3/27 5:39 The Shift Supervisor authorized the installation of temporary

modification TM-2003-012 for R bus relay 486 S-X1. This

temporary modification replaced conductors associated with

R Bus relay 486 S-X1 with wires in another cable. This allowed

for the realignment of offsite power to safety-related buses 1C

and 1D through the startup transformer.

8

14:47 Operators energized nonsafety-related buses 1E, 1B, 1A, 1G and

1F from the startup transformer.

15:30 Operators paralleled the startup transformer to EDG 1-1 to supply

power to the 1C bus.

15:46 Emergency diesel generator 1-1 was secured.

17:23 Operators paralleled the startup transformer to EDG 1-2 to supply

power to the 1D bus.

17:35 Operators exited ONP-2.1.

17:37 Emergency diesel generator 1-2 was secured. The Unusual

Event was terminated following the restoration of offsite power.

4/4 6:13 Work Order (WO) 24321140, implementing engineering action

request (EAR) 2003-0086, was completed. Control circuits for

offsite power protective relays were transferred to alternate

conductors and the offsite power protective relays were fully

restored.

b. Findings

No findings of significance were identified.

02 Adequacy of Licensee Evaluation of Events and Corrective Actions (93812)

02.1 March 18, 2003 Cable Spreading Room Fire

a. Inspection Scope

On March 18, 2003, charging pump breaker 52-1205 failed and caught fire. The

breaker was contained in LCC-12 in the cable spreading room. The site emergency

director declared an Alert due to the potential impact of the fire on other safety-related

equipment. The team assessed the licensees root cause investigation efforts for this

event. The team interviewed control room operators, electrical maintenance workers

and licensee personnel involved with the investigation. As part of the inspection effort,

the team reviewed the licensees root cause investigation results and performed

independent reviews of the licensees troubleshooting activities. The team also

reviewed design drawings, design basis documents, and the Updated Final Safety

Analysis Report. The team reviewed maintenance controls practices including previous

breaker maintenance and calibration activities.

b. Findings

No findings of significance were identified.

9

The team determined that the licensees troubleshooting efforts were structured and

methodical. A failure mode analysis approach was used to establish a timeline and

potential failure modes chart. This approach facilitated the structured review of potential

failure modes for both the charging pump P-55A supply breaker as well as the low

suction pressure trip of charging pump P-55A which initiated the event. Licensee

personnel demonstrated a focus on gathering as-found data for the sequence of events,

maintenance records, pressure transmitters, operator actions, and operator statements.

Additionally, the licensee performed an extensive as-found investigation into the extent

of damage to LCC-12 that housed the failed breaker. Similarly, the licensee performed

a rigorous extent of condition review to determine if any other breakers were missing arc

chutes and whether problems encountered with the charging pump low suction pressure

trip switches were isolated or generic.

At the end of the inspection, the licensees root cause investigation was not complete

and therefore corrective actions were not yet formalized. The licensee identified that the

cause the cable spreading room fire was the failure to reinstall arc chutes in the P-55A

breaker when the breaker was reinstalled into LCC-12 after it was refurbished in

May 2002. Following the event, the licensee sent the breaker to the manufacturer for a

complete failure mode analysis. The manufacturer identified that the breaker failure

was caused by an arc forming between phases on the breaker and then moving over

the backing insulator to form an arc directly between the breaker stabs entering LCC-12.

The missing arc chutes resulted in a normal arc, formed when a breaker opens, not

being extinguished as designed. A combination of the operator attempting multiple

motor starts in a short time, a stuck low suction pressure trip switch, and burnt wires to

the anti-pump coil in the breaker, caused the breaker to rapidly close and trip open

multiple times when the operator held the control switch in the close position. This

allowed a continuous arc to form, and initiated the fire in the breaker cubicle.

The team concluded that although the root cause investigation was not complete at the

end of the inspection, the licensees evaluation of the event was proceeding

satisfactorily and the root cause investigation efforts were adequate.

02.2 March 25, 2003 Loss of Offsite Power

a. Inspection Scope

On March 25, 2003, the plant experienced a loss of offsite power to the nonsafety-

related and safety-related buses providing power to equipment necessary to maintain

shutdown cooling of the PCS. The team reviewed the licensees root cause

investigation results and performed independent reviews of the licensees offsite power

system design and troubleshooting activities. The team also reviewed design drawings,

design basis documents, and the Updated Final Safety Analysis Report. The team also

interviewed licensee personnel involved with the root cause investigation.

10

b. Findings

Introduction

The team identified a performance deficiency in that the licensee failed to address a

repetitive problem of weak controls over excavation and digging activities. The finding is

greater than minor, but is unresolved pending completion of a significance determination

review. No violation of regulatory requirements was identified.

Description

The licensee used a failure mode analysis approach to establish a timeline and potential

failure modes chart. This approach facilitated the structured review of potential failure

modes, which could have resulted in the loss of offsite power. The licensee focused on

gathering as-found data, and identified the circuit breakers and relays that were

impacted. The licensee reviewed all potential failure modes to identify the likely cause

of the event. The licensee identified several conductors within a common cable which

were routed to various relays that could have caused the loss of offsite power to occur.

The licensee identified that a single cable carried protective relay circuitry for all the

affected breakers. Through interviews and information provided by plant personnel, the

licensee identified that the event was caused by cables being damaged during the

installation of a signpost in a parking lot outside the facilitys protected area. The metal

signpost breeched the plastic conduit wall and penetrated the outer jacket and insulation

of one of the cables routed in the conduit. This conduit was routed between the plant

and the switchyard about 30 inches underground. The damaged cable carried the

conductors associated with the protective relaying scheme for the offsite power system.

The damaged cable actuated protective relaying associated with the switchyard. These

actuations resulted in the opening of various circuit breakers including Breaker 152-401,

main generator breakers, and all four circuit breakers supplying the switchyard R bus.

Collectively, the opening of these circuit breakers removed all offsite power to the plant .

However, there were two instances during the licensees recovery efforts that should

have received more careful consideration. First, licensee personnel made the decision

to close Breaker 152-401 prior to completing a physical inspection of the breaker. At

the time of this decision, the root cause for the breaker trip was unknown. Licensee

personnel determined there was no clear indication of an existing electrical fault and

decided to close the breaker and re-energize nonsafety-related buses from the

safeguards bus. The team concluded that although there was no obvious indication of

an electrical fault, more consideration should have been given to the possibility of a

mechanical failure. The team concluded that licensee management had missed an

opportunity to identify a mechanical problem within the breaker, had one existed.

Second, when the licensee determined that the loss of offsite power occurred at the

same time a signpost was driven into the ground, it was also known that two signposts

were involved. The licensee had excavated the first signpost hole and found minor

damage to an underground conduit. The licensee had also developed a temporary

modification (TM-2003-012) to relocate the protective relay conductors. The licensee

planned to move ahead with the implementation of the temporary modification before

excavation of the second signpost hole. Regional NRC management questioned why

11

the second signpost hole was not excavated prior to proceeding with the temporary

modification. The licensee then identified that it was the second signpost that caused

the damage to the protective relay circuitry cable.

Licensee personnel identified that a contributing cause to the loss of offsite power to the

safety-related buses was the use of a common cable to provide controls for the R bus

load shed relays as well as the F bus load shed/fast transfer relays. Part of the

licensees corrective actions included separating the conductors for protective relays to

different cables.

The licensees root cause investigation assessed the adequacy of existing plant policy

regarding excavation and digging activities within the licensees property. Similarly the

team performed independent reviews of the licensee administrative controls in this area.

During those reviews, the team independently identified that there were several previous

corrective action program (CAP) documents pertaining to problems encountered during

excavating or digging activities. Documents reviewed by the team included the

following:

  • CAP 19522, Unidentified Cable Severed During Excavation, dated June 1999;
  • CAP 08000, Unknown Cables Cut While Digging to Install Fire Protection Piping,

dated August 2000;

  • CAP 26496, Equipment Operator Damaged an Underground Telephone Cable

While Excavating, dated October 2000;

  • CAP 14634, During Excavation Work Digging Equipment Damaged Two Plastic

Conduits, dated July 2001;

  • CAP 30724, Severed Power Cable to the Meteorological Tower, dated

May 2002;

  • CAP 31300, Underground Cable Hit by Municipal Project Resulting in Power

Outage, dated September 2002; and

  • CAP 31378, Unmarked Phone Line Cut During Installation of Domestic Water,

dated September 2002.

Based on discussions with plant personnel and a review of corrective actions associated

with the above CAP documents, the team concluded that the licensee had failed to

address a repetitive problem of weak controls of excavation and digging activities. The

lack of established controls in the form of administrative policies and procedures in this

area contributed to the lack of awareness and sensitivity to potential safety

consequences which could arise during such activities. The licensees preliminary root

cause evaluation similarly concluded that the root cause of the event was that the plant

did not have a written policy or process for excavating and trenching activities.

12

The team concluded that although the root cause investigation was not complete at the

end of the inspection, the licensees evaluation of the event was proceeding

satisfactorily and the root cause investigation efforts were adequate.

Analysis

The team determined that the licensees failure to develop and implement corrective

actions for a repetitive problem of excavating and digging activities damaging buried

components was a performance deficiency warranting a significance evaluation. The

team concluded that the finding was of greater than minor risk significance in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Disposition Screening. This conclusion was based on the licensees failure to develop

and implement corrective actions for several previous similar events. When the loss of

offsite power event occurred the plant was shutdown with the reactor vessel head

removed and the reactor cavity flooded to about 6 feet above the reactor vessel flange.

Inspection Manual Chapter 0609, Significance Determination Process, Appendix A,

SDP Phase 1 Screening Worksheet for IE [Initiating Events], MS [Mitigating Systems],

and B [Barrier Integrity] Cornerstones, states that if the finding is assumed to degrade

the safety of a shutdown reactor then use Appendix G, Shutdown Operations

Significance Determination Process. Utilizing IMC 0609, Appendix G worksheet, PWR

[Pressurized Water Reactor] Cold Shutdown and Refueling Operation RCS [Reactor

Coolant System] Open and Refueling Cavity Level <23 Feet, the team determined this

was a finding that increased the likelihood of a loss of offsite power and therefore

required a Phase 2 analysis. In addition, a Phase 3 analysis was required since the

potential for this event to occur also existed when the plant was operating at power.

This is an Unresolved Item (URI 50-255/03-05-01) pending the completion and review of

these analyses. The licensee entered this issue into their corrective action program as

CAP 034500.

Enforcement

The maintenance technician driving the signpost into the ground was not performing an

activity affecting quality. Therefore, no violation of regulatory requirements was

identified.

03 Event Common Cause Review and Assessment (93812)

a. Inspection Scope

The team interviewed individuals involved in both events, and reviewed pertinent logs,

information, and procedures to identify any common causes or relationships between

the two events.

b. Findings

No findings of significance were identified.

The team did not identify any common causes or relationship between the two events.

13

04 Operator Performance Issues (93812)

04.1 March 18, 2003 Cable Spreading Room Fire

a. Inspection Scope

The team reviewed operator performance during the March 18, 2003, cable spreading

room fire through interviews of the on-shift operating crew, a simulator training

instructor, and licensee management. The team also reviewed operating logs,

operating procedures, abnormal operating procedures, alarm response procedures,

annunciator alarm printouts, system drawings, and operator training records.

b. Findings

Introduction

A Green finding associated with a self-revealed event was identified when a control

room operator repeatedly attempted to start charging pump P-55A and failed to trip the

Primary Coolant Pumps when required. One Non-Cited Violation of Technical

Specification 5.4.1 was identified.

Description

On March 18, 2003, the plant was in Mode 5 (Cold Shutdown) and in a solid condition

with charging and letdown flow increased to aid in PCS cleanup. Operators were

directed to increase the boric acid concentration in the PCS by realigning the charging

water suction from the VCT to BAST T-53B.

Prior to the evolution, the CRS and NCO-1 discussed the activity, but did not involve the

operating crew in a crew briefing. The CRS did not use a pre-job checklist during the

discussion, nor did NCO-1 review or discuss the procedure requirements in SOP-2A,

Chemical and Volume Control System. Instead, with the CRSs knowledge, NCO-1

used a placard intended for use during emergency boration as guidance to perform the

evolution. Since the valves to be operated were the same as those identified in the

placard, the CRS and NCO-1 saw no immediate problem.

Operators calculated that 67.4 gallons of high concentration boric acid solution from the

BAST were required to be added to raise PCS boron concentration to the desired level.

However, operators did not calculate how long this evolution should require or recognize

that the computer screen used to monitor BAST level updated only every 10 seconds.

NCO-1 initiated actions to borate the PCS by shifting the charging pump suction from

the VCT to BAST T-53B. The CRS performed a peer check of the valve manipulations

and then proceeded with other duties. NCO-1 turned away to verify a decrease in BAST

level, but did not observe an immediate change. NCO-1 then turned his attention back

to the control panel and noted that PCS pressure was unexpectedly rapidly decreasing.

Operations management expectations were that operators announce problems and

obtain supervisory approval prior to operating equipment unless the action is an

immediate action within a procedure, which was not the case for this situation.

14

However, without informing anyone else in the control room about the rapidly decreasing

PCS pressure, NCO-1 attempted to arrest the pressure drop by adjusting the

backpressure regulator to reduce the letdown rate from the PCS. As PCS pressure

continued to decrease, NCO-1 again attempted to adjust the backpressure regulator

without verifying charging pump flow. Charging pump P-55A tripped on low suction

pressure about 40 seconds after the VCT discharge valve was closed. At that point, a

second operator, NCO-2, noted that the charging pump had tripped and announced the

trip. NCO-1, without supervisor approval, then reopened the VCT discharge valve, shut

the BAST suction valve, and repeatedly attempted to restart charging pump P-55A. In

9 seconds, NCO-1 unsuccessfully attempted to start pump charging pump P-55A three

times.

Step 5.2.3 of Procedure SOP-2A limited the attempted starts of P-55A to one attempt.

Step 7.5.5.f of SOP-2A required verifying charging flow after shifting to gravity feed.

The licensees investigation later revealed that P-55A charging pump Breaker 52-1205

had no arc chutes installed. In addition, the licensees investigation identified that the

breakers anti-pump relay had its wires burned off, likely from an arc either before or

during an earlier attempt to close the breaker and start the pump. The licensees

investigation also identified that the pump low suction pressure trip switch had stuck

closed so that the low suction pressure trip was locked in. With the anti-pump relay

damaged and the breaker trip signal locked in, the actions of NCO-1 to hold the breaker

control switch in the close position resulted in electrical arcing within the breaker.

Without the arc chutes installed, a fire started within the charging pump P-55A breaker

cubicle. The arc was extinguished when the upstream supply breaker to LCC-12,

Breaker 52-1202, opened as designed on overcurrent.

With NCO-1 attempting to restart the charging pump, PCS pressure continued to

decrease. Neither NCO-1 nor the CRS noticed that PCS pressure was trending toward

the minimum pressure for PCP operation. The SS did notice the trend in PCS pressure

and directed the CRS to trip the PCPs. The CRS made a statement to trip the PCPs,

but did not use effective three-way communications to ensure that NCO-1 understood

and complied with the direction. NCO-1 did not hear the direction given. As a result,

the PCPs were not tripped until the SS directed NCO-1 to trip the PCPs. Consequently,

PCS pressure decreased to below the minimum operating pressure for PCP operation,

a condition that led to minor damage to the 1D PCP seal.

The other running charging pump, P-55B, tripped when LCC-12 bus supply

breaker 52-1202 tripped on high current. Operators verified that adequate shutdown

margin existed, that shutdown cooling remained in operation, and that PCS cooldown

rates had not been exceeded. Operators secured PCS letdown and controlled bleedoff

flow to maintain primary coolant system inventory.

Analysis

The team determined that the control room operator failed to follow procedure

requirements by repeatedly attempting to restart charging pump P-55A, and to secure

the PCPs prior to PCS pressure dropping below the minimum pressure for PCP

operation. The team concluded that the finding had more than minor risk significance in

accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

15

Disposition Screening, because it could reasonably be viewed as a precursor to a

significant event. Inspection Manual Chapter 0609, Significance Determination

Process, Appendix A, SDP Phase 1 Screening Worksheet for IE, MS, and B

Cornerstones, states that if the finding is assumed to degrade the safety of a shutdown

reactor then use Appendix G, Shutdown Operations Significance Determination

Process. Utilizing IMC 0609, Significance Determination Process, Appendix G

worksheet, PWR Cold Shutdown Operation and RCS Closed and S/Gs [Steam

Generators] Available for DHR [Decay Heat Removal], the team determined that since

the event did not result in an inadvertent change in PCS temperature or a loss of level,

the finding was of very low safety significance (Green).

Enforcement

Technical Specification 5.4.1 requires that written procedures be established,

implemented, and maintained covering the activities specified in Regulatory Guide 1.33,

Appendix A. Item 3.a of Appendix A included procedures for the operation of the reactor

coolant system, and item 3.n included procedures for the operation of the chemical and

volume control system. Step 5.2.3 of Procedure SOP-2A, Chemical and Volume

Control System, Revision 50, limited the attempted starts of charging pump P-55A to

one attempt. Procedure SOP-1, Primary Coolant System, Attachment 2, Revision 51,

Step 3, stated, The plant shall be maintained to the left and above the Minimum

Pressure for PCP Operation Curve whenever the Primary Coolant Pumps are

operating. Contrary to the above, on March 18, 2003, a nuclear control operator

attempted to start charging pump P-55A three times after it tripped and failed to trip the

PCPs prior to PCS pressure dropping below the minimum pressure for PCP operation.

However, because of the very low safety significance and because this issue was

entered into the corrective action program, it is being treated as a Non-Cited Violation,

consistent with Section VI.A.1 of the Enforcement Policy (NCV 50-255/03-05-02). This

issue was entered into the licensees corrective action program as CAP 034027.

04.2 March 25, 2003, Loss of Offsite Power

a. Inspection Scope

On March 25, 2003, the resident inspectors responded to the control room after the

offsite power supply to the plant was lost unexpectedly. The team observed the control

room operators response to the event. The team verified that ONP-17, Loss of

Shutdown Cooling, General Operating Procedure (GOP)-14, Shutdown Cooling

Operations, and the Emergency Plan were implemented in a timely and accurate

manner to address the event.

The team walked down control room panels to monitor key plant parameters including

primary coolant system heatup rate. The team also verified that the emergency diesel

generators were operating properly to provide power to plant equipment necessary to

re-establish shutdown cooling.

The Alert was downgraded to an Unusual Event after shutdown cooling was restored

and terminated on March 27, 2003 when offsite power was reliably re-established.

16

b. Findings

No findings of significance were identified.

The team concluded that control room operators responded effectively and in

accordance with plant procedures to the loss of offsite power and resultant loss of

shutdown cooling. Consequently, the event was mitigated in a timely manner. The CRS

demonstrated positive command and control while directing operator actions and the

team noted that communications between the control room operators were clear and

concise while addressing the event.

The CRS immediately entered ONP-17 and methodically initiated actions to re-establish

shutdown cooling which limited primary coolant system heatup to only 10EF.

The control room and auxiliary operators verified that the necessary plant equipment to

support shutdown cooling operations was available and then re-established cooling flow

to the reactor within 20 minutes of the initiation of the event.

05 Equipment Performance Issues - March 18, 2003 Cable Spreading Room Fire (93812)

a. Inspection Scope

The team reviewed the licensees efforts to restore the facility following the March 18,

2003, cable spreading room fire. Additionally, the team reviewed the performance of

equipment during the event.

b. Findings

No findings of significance were identified.

One equipment performance deficiency occurred when the P-55A charging pump

breaker low suction pressure trip switch stuck in the tripped position and contributed to

the event.

The team reviewed the circumstances surrounding the failure of the P-55A charging

pump low suction pressure trip switch including a review of the maintenance and

calibration records for this switch and other similar switches. No other instances of the

P-55A charging pump low suction pressure trip switch or other similar pressure switches

failing closed after actuating were identified.

The team reviewed the selective tripping design for the power sources to the P-55A

charging pump. The team determined that the upstream power supply breaker to

LCC-12, breaker 52-1202, functioned as designed and interrupted power to minimize

the loss of power to plant components while isolating the fault.

The licensee examined LCC-12 and determined that other than smoke and soot, the

damage was isolated to the charging pump breaker enclosure. The team also reviewed

the results of the testing performed to identify potential cable damage or degradation.

The licensees investigation attributed all damage to LCC-12 to the arcing on charging

17

pump P-55A breaker 52-1205. The teams independent review did not identify any

contradictory evidence.

Licensee corrective actions for this event included the installation of new wiring from

LCC-12 to the breaker enclosure and the installation of a replacement breaker. Post

maintenance testing on the new breaker was satisfactory. No concerns were identified.

06 Equipment Performance Issues - March 25, 2003 Loss of Offsite Power (93812)

a. Inspection Scope

The team reviewed the licensees efforts to restore offsite power to the facility.

Additionally, the team reviewed the performance of equipment during protective relay

actuations.

b. Findings

No findings of significance were identified.

There were no significant equipment performance deficiencies during the event. The

team reviewed the fast transfer design for the power sources to the safeguards buses.

In accordance with the facility design, were the safeguards power source to be lost, a

fast transfer would occur to the alternate supply from the R bus through the startup

power transformer 1-2. This fast transfer, however, was dependent on the availability of

the standby source, as indicated by available voltage. During this event, there was no

transfer of power source to the startup power transformer since the R bus was the first

power source lost. The team concluded that the electrical system fast transfer design

functioned as expected in that a fast transfer did not occur to a de-energized bus.

The team reviewed the licensees cable testing results to identify those with potential

cable damage or degradation. Through megger testing of numerous conductors, the

licensee identified several conductors which had less than nominal resistance readings.

Cable MISC-1, which was the only cable actually damaged by the signpost, had five

conductors with less than acceptable megger readings.

Licensee corrective actions to restore offsite power to the safety-related buses and re-

establish system integrity included the repair of the damaged conductors and the use of

existing spare conductors on other cables routed between the plant and switchyard. On

March 27, the Shift Supervisor authorized installation of Temporary Modification

TM-2003-012, Restoration of Startup Power Transformers (1-1, 1-2, and 1-3) Protective

Relaying, for R bus relay 486 S-X1. The team observed portions of the installation of

temporary modification TM-2003-012. The modification was installed to provide for the

use of undamaged conductors in existing cables and lifting of wires routed between the

switchyard and the plant. The team reviewed the modification documentation, including

the associated 10 CFR 50.59 screening. This temporary modification allowed the

station to realign offsite power to safeguards buses 1C and 1D through the startup

transformer. The team also reviewed the completed work order which installed cable

splices to repair the damaged conductors in cable MISC-1. Based on a review of the

records and an observation of activities, no concerns were identified.

18

07 Maintenance Performance Issues (93812)

a. Inspection Scope

The team reviewed the maintenance performance issues associated with the discovery

that charging pump breaker 52-1205 was installed on May 24, 2002 without arc chutes.

The licensee identified that the lack of arc chutes was the primary cause of the cable

spreading room fire. The team reviewed work orders, maintenance procedures,

calibration records, vendor technical manuals, electrical maintenance worker training

and qualifications, clearance order practices, and selected corrective action documents.

The team also interviewed the workers that installed the breaker without the arc chutes

and other electrical maintenance personnel.

b. Findings

Introduction

A finding of very low safety significance was self-revealed during an event when the

licensee failed to have adequate maintenance procedures in place to ensure that when

electrical breakers were removed to be refurbished that the arc chutes were reinstalled

before the breaker was placed back in operation. The finding was determined to be of

low safety significance because the failure did not result in a loss of shutdown cooling or

loss of reactor inventory. One Non-Cited Violation of 10 CFR 50, Appendix B,

Criterion V, Instructions, Procedures, and Drawings, was identified.

Description

The team reviewed the work orders that were used to remove and reinstall P-55A

charging pump breaker 52-1205 prior to the event. Work Order (WO) 2491-2422

removed the breaker (Serial Number 42924-A14-2-4D) for refurbishment on

October 18, 2001, in accordance with the requirements of Procedure Station Power

System (SPS) E-17, Temporary Installation and Removal of Spare Circuit Breakers,

Revision 1. Procedure SPS-E-17, Step 4.2.1 required, During performance of

maintenance, removed parts are to be adequately packaged, identified, and stored so

they are not lost, damaged, or lose traceability to the component from which they were

removed. An entry in the WO remarks section indicated that the arc chutes had been

removed, tagged, and stored in the electrical maintenance shop. Work Order

2411-3520, which reinstalled the breaker on May 24, 2002, made no mention of the arc

chutes. However, there was no procedurally required certification of arc chute re-

installation.

The team reviewed 16 WOs that had removed or installed similar breakers without

finding any discernible pattern of recording the removal or re-installation of the arc

chutes. Five WOs recorded arc chute removal for shipping, five WOs recorded arc

chute installation prior to installation into an LCC, six WOs made no mention of arc

chutes, and only three breakers had both the removal and re-installation of arc chutes

recorded. There was no procedural requirement in SPS-E-17 to remove or install arc

chutes. The SPS system engineer could not recall any specific action or incident that

19

required the removal of the arc chutes from K-Line breakers for shipping. The apparent

intent was to prevent damage to the arc chutes during shipping.

Step 5.4 of Maintenance Procedure SPS-E-6, ITE 480 Volt Breaker Inspection and

Repair, Revision 11, contained instructions for removal, inspection, and re-installation

of arc chutes. However, neither procedure SPS-E-6 nor any other procedure was used

for removal or re-installation of the K-Line breaker arc chutes. The licensee completed

a walkdown of all installed K-line breakers on March 18, 2003, and ensured that no

other breakers were missing arc chutes.

The team reviewed the training records, training course contents, and qualifications of

both of the workers that installed breaker 52-1205 without arc chutes. No issues were

identified. When interviewed by the team, neither of the workers could identify a reason

for not installing the arc chutes although both were aware of the function and

importance of the arc chutes for proper breaker function. The workers had used a

pre-job briefing checklist prior to reinstalling the breaker and both workers were very

experienced. From the work instructions and interviews, the team noted that at one

point the spare breaker and the refurbished breaker were side-by-side for comparison of

the auxiliary contacts, but neither worker identified the absence of the arc chutes.

The team reviewed the work control processes for removing and reinstalling the

breakers. The licensee staff informed the team that separate WOs were routinely used

for breaker removal and reinstallation to facilitate declaring the installed spare and re-

installed original breaker operable following WO closeout. The team reviewed

Procedure 5.01, Processing Work Requests/Work Orders, Revision 27, and found no

requirement for separate work orders. The licensee staff agreed that no identified

process or procedure required closing out the original WO. The team noted that

information on the removal WO had not been carried forward to the re-installation WO

(specifically the removal and storage of the arc chutes) and the licensee staff confirmed

that there was no requirement to carry the information forward to the installation WO.

The team also found that there was no process or procedure that addressed control of

partial equipment shipments for repair and positive controls of the remainder of the

equipment. Likewise, no processes existed for receipt of equipment components that

also addressed control of the remainder of the equipment. Procedure 5.01 stated that,

The assigned supervisor or repair worker is responsible for control of parts associated

with Work Orders; however, the team found that there was no assigned supervisor or

repair worker for closed work orders. Consequently, there was no assurance that

information noted in a work order upon removal of an item would be available for

reference during re-installation.

The team reviewed the operational history of breaker 52-1205 and identified that the

breaker cubicle door had been opened numerous times, after the breaker had been

installed without the arc chutes, in support of eight work orders for protective tagging.

At least one of those work orders included a wiring inspection by electrical maintenance

workers. In addition to the above work orders, electrical maintenance technicians

opened the breaker door to perform an inspection of the breaker dust shields. The

licensee staff agreed that multiple opportunities for both operations and electrical

maintenance personnel to identify that the arc chutes were missing had existed.

20

However, inspection of breakers for such missing components was not a normally

performed activity.

Analysis

The team identified that the licensee performed activities affecting quality without a

procedure or work instructions, specifically removing and/or replacing breaker arc

chutes without instructions to do so. In addition, no procedural guidance existed to

control equipment after it had been partially disassembled and the work order was

closed out. The team concluded that the finding had more than minor risk significance

in accordance with IMC 0612, Power Reactor Inspection Reports, Appendix B, Issue

Disposition Screening, because inadequate maintenance procedures and the

installation of non-conforming equipment in safety-related components could be

reasonably viewed as a precursor to a significant event. Inspection Manual Chapter 0609, Significance Determination Process, Appendix A, SDP Phase 1 Screening

Worksheet for IE, MS, and B Cornerstones, states that if the finding is assumed to

degrade the safety of a shutdown reactor then use Appendix G, Shutdown Operations

Significance Determination Process. Utilizing IMC 0609, Appendix G worksheet, PWR

Cold Shutdown Operation and RCS Closed and S/Gs Available for DHR, the team

determined that since the event did not result in an inadvertent change in PCS

temperature or a loss of level, the finding was of very low safety significance (Green).

The team concluded that the failure to install the breaker arc chutes also increased

the probability of the initiation of a fire. Inspection Manual Chapter 0609, Significance

Determination Process, Appendix F, Determining Potential Risk Significance of Fire

Protection and Post-Fire Safe Shutdown Inspection Findings, states that one of the

fire protection defense in depth elements is the prevention of fires from starting. The

team determined that the failure to install arc chutes increased the likelihood of a fire

in the cable spreading room. As such, further analysis was required as specified by

IMC 0609, Appendix A, SDP Phase 1 Screening Worksheet for IE, MS, and B

Cornerstones, The team reviewed licensee engineering analysis EA-PSA-FIRE-IE-

03-05 and concurred with the results which calculated a fire initiating event frequency of

4.7 x 10-4 per year. To calculate this frequency, the licensee determined that the

frequency of a standing trip signal for breaker 52-1205 was 5.5 x 10-2 per year based on

failure rates associated with one control switch, five external relays, and three internal

breaker relays. In the March 18, 2003 event, the upstream breaker for breaker 52-1205

tripped and the fire was limited to the breaker cubicle. For their analysis, the licensee

assumed that such a fire would not be limited to the breaker cubicle if the upstream

breaker failed to trip. The team noted that this assumption was conservative because

even if the upstream breaker failed to trip, a breaker further upstream would likely trip

thereby limiting the duration of and energy contribution to the fire. The licensee

identified the failure probability associated with the upstream breaker to trip open upon

demand was 8.49 x 10-3.

The team used the Phase 2 process outlined in IMC 609, Appendix F, to determine the

significance of the event given the fire initiating event frequency developed by the

licensee. The team noted that the Phase 1 process outlined in IMC 0609, Appendix F

was not applicable because the finding did not involve fire protection features. For this

evaluation, the team assumed that a fire which was not limited to the breaker cubicle

21

could develop into a widespread fire in the cable spreading room requiring plant

shutdown from outside the control room. The team noted that such an assumption was

conservative since the nearest exposed cables were more than 4 feet above the cubicle

and there was a supply ventilation duct nearby with a design flow rate of 2000 cubic feet

per minute which would tend to disperse hot gases from a cubicle fire before the gases

came in contact with the exposed cables. Using the guidance of IMC 0609, Appendix F,

and the licensee developed fire initiating event frequency, the team determined that the

fire mitigation frequency (FMF) was -5.08. This FMF was calculated based on no credit

for fire barriers or separation, moderate degradation for automatic suppression, and full

credit for manual suppression outside of the control room. Based on a review of

IMC 0609, Appendix F, Table 5.4, the team determined that the FMF correlated to an

approximate frequency of 1 per 105 to 106 years. The failure to have arc chutes in place

was greater than 30 days. Therefore, based on a review of IMC 0609, Appendix F,

Table 5.5, the inspectors determined that the estimated likelihood rating was F. Based

on a review of the text associated with IMC 0609, Appendix F, Figure 4-3, and

IMC 0609, Appendix F, Attachment 1, Example 1C, the inspectors determined that a -1

point credit for post-fire safe shutdown operation was applicable. Therefore, based on a

review of IMC 0609, Appendix F, Table 5.6, Risk Significance Estimation Matrix, the

team concluded that the finding associated with the failure to install arc chutes was of

very low safety significance (Green).

Enforcement

10 CFR 50, Appendix B, Criterion V, Instruction, Procedures, and Drawings, states, in

part, that activities affecting quality shall be prescribed by documented instructions,

procedures, or drawings of a type appropriate to the circumstances and that work shall

be accomplished in accordance with these instructions, procedures, or drawings.

Contrary to the above, on October 19, 2001, licensee personnel removed the arc chutes

from charging pump breaker 52-1205 without procedural guidance, controls, or

documentation, and had no adequate measures in place to prevent the non-conforming

breaker from being returned to service on May 24, 2002.

However, because of the very low safety-significance and because this issue was

entered in the corrective action program, it is being treated as a Non-Cited Violation,

consistent with Section VI.A.1 of the Enforcement Policy (NCV 50-255/03-05-03). This

issue was entered into the licensees corrective action program as CAP 034187.

08 Design Issues Associated With Offsite Power Configuration (93812)

a. Inspection Scope

The team reviewed the offsite and onsite electrical distribution system as described in

various licensing and design bases documents such as the Updated Final Safety

Analysis Report. In particular, the team focused on the facilitys design with respect to

electrical and cable separation requirements. This issue was of concern in light of the

event being caused by damage to multiple conductors in a single cable. This cable

contained protective relay circuitry which affected the normal and alternate power

sources to both safety-related buses.

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b. Findings

No findings of significance were identified.

The team concluded that the design of the electrical circuitry was in conformance with

the licensing basis. From a review of the licensees Updated Final Safety Analysis

Report and licensing documents, the team determined that the plant was designed and

constructed prior to IEEE-308, Standard Criterion for Class 1E Power Systems for

Nuclear Power Generating Stations, requirements. Therefore, the facility may not meet

all design criteria and testing requirements contained in IEEE-308. The adequacy of the

licensees electrical power system was reviewed by the NRC as part of the Systematic

Evaluation Program. The results of these reviews were documented in NUREG-0820,

Integrated Plant Safety Assessment-Systematic Evaluation Program. The team

concluded that the licensees offsite power system, and conformance to existing design

requirements relating to electrical separation and physical separation, had been

previously reviewed and approved by the NRC as part of the evaluation program. No

additional concerns were identified by the team.

Since the facility was designed prior to issuance of 10 CFR 50, Appendix A, General

Design Criteria (GDC) 17, Electrical Power Systems, the installation of a safeguards

transformer in 1989 was considered a modification to improve the capability for reliable

offsite power. Additionally, the design was considered to enhance conformance with,

but not commit compliance to GDC 17.

The original design of the offsite power improvement project was to install the new

control circuits through an existing duct bank between the switchyard and the plant.

Due to difficulties in replacing some existing cables, a new conduit run was installed and

routed between the plant and switchyard. By design, the conduit was installed about

30 inches underground. It was this conduit that was damaged by the signpost being

driven into the ground. Based on the fact that the licensee was not required to provide

physical separation between circuits associated with the R and F buses, the licensee

designed the circuits to use separate conductors within the same cable for the various

protective relay circuitry. This design contributed to the loss of offsite power event.

The licensees interim and permanent repairs to the damaged cables and modifications

to the existing design included provisions to provide additional physical separation

between the circuits for the safeguards transformer and the backup source through the

R bus.

09 Review of Emergency Plan Response Actions (93812)

a. Inspection Scope

The team interviewed members of the control room crew, and reviewed the licensees

Site Emergency Plan, operating logs, technical support center narrative logs, and

applicable event notification forms to determine if the licensee correctly classified the

event and made the proper notifications in a timely manner.

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b. Findings

No findings of significance were identified.

10 Exit Meeting Summary

On April 4, 2003, the team presented the preliminary inspection results to

Mr. D. Cooper and other members of the Palisades Plant management and staff. The

licensee acknowledged the information presented. The team asked the licensee

whether any materials examined during the inspection should be considered proprietary.

No proprietary information was identified.

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KEY POINTS OF CONTACT

Nuclear Management Company

T. Blake, Emergency Planning Manager

D. Cooper, Site Vice President

B. Dotson, Licensing Analyst

P. Harden, Engineering Director

N. Haskell, Nuclear Oversight Manager

L. Lahti, Regulatory Affairs Manager

D. Malone, Site Director

M. Moore, Nuclear Oversight Assessor

T. OLeary, Business Support Manager

G. Packard, Operations Manager

R. Remus, Plant General Manager

U.S. Nuclear Regulatory Commission

S. Reynolds, Deputy Director, Division of Reactor Projects

J. Lennartz, Senior Resident Inspector

R. Krsek, Resident Inspector

LIST OF ITEMS OPENED, CLOSED AND DISCUSSED

Opened

50-255/03-05-01 URI Corrective Actions to Address Digging and Excavating Events

50-255/03-05-02 NCV Failure to Follow Operating Procedures

50-255/03-05-03 NCV Failure to Have Adequate Maintenance Procedures

Closed

50-255/03-05-02 NCV Failure to Follow Operating Procedures

50-255/03-05-03 NCV Failure to Have Adequate Maintenance Procedures

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LIST OF ACRONYMS USED

B Barrier

BAST Boric Acid Storage Tank

CAP Corrective Action Program Document

CRS Control Room Supervisor

DHR Decay Heat Removal

EAR Engineering Action Request

EDG Emergency Diesel Generator

EST Eastern Standard Time

FMF Fire Mitigation Frequency

GDC General Design Criteria

GOP General Operating Procedure

gpm gallons per minute

IE Initiating Events

IP Inspection Procedure

kV Kilovolt

LCC Load Control Center

LPSI Low Pressure Safety Injection

NCO Nuclear Control Operator

NCV Non-Cited Violation

MC Manual Chapter

NMC Nuclear Management Company

NRC Nuclear Regulatory Commission

ONP Off Normal Operating Procedure

PCP Primary Coolant Pump

PCS Primary Coolant System

PSIA Pounds Per Square Inch Absolute

PWR Pressurized Water Reactor

RCS Reactor Coolant System

SDC Shut Down Cooling

SDP Significance Determination Process

S/G Steam Generator

SOP Standard Operating Procedure

SS Shift Supervisor

TBD To Be Determined

URI Unresolved Item

Vac Volts Alternating Current

VCT Volume Control Tank

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LIST OF DOCUMENTS REVIEWED

Documents Reviewed

Palisades Administrative Procedure 4.28, Control of Palisades Switchyard Activities, Revision 0

Palisades Drawing SK-EAR-203-0086-2, Safeguards and Startup Offsite Power Source

Between Plan and Switchyard, Revision 0

Plant Review Committee Overview of Offsite Power Recovery

NRC Evaluation of SEP Topic VII-3, Systems Required for Safe Shutdown, December 1981

Final Safety Analysis Report, Chapter 8

Palisades Offsite Reliability Improvement - Functional Description, GWO 8303, File 114.2,

FC-800

Palisades Offsite Reliability Improvement - Design Plan, GWO 8303, File 110.2, FC-800

Palisades Nuclear Plant, Design Basis Document, 2400 VAC System, July 2001

Palisades Nuclear Plant, Design Basis Document, 345 kV Switchyard, January 1999

Work Request 294427, Perform Circuit Verification on Scheme Associated with Cable MISC-1

Integrated Plant Safety Assessment- Systematic Evaluation Program, NUREG-0820,

October 1982

Integrated Plant Safety Assessment- Systematic Evaluation Program, NUREG-0820,

Supplement 1, November 1983

Work Request 300477, Check and Megger Test Conductors for Cable MISC-1

Temporary Modification TM-2003-012, Restoration of Startup Power Transformers (1-1, 1-2,

and 1-3) Protective Relaying

CAP034185, Emergency Assembly Area Over Capacity.

CAP034187, Alert Declared Due to Fire in Cable Spreading Room.

CAP034198, A and D Primary Coolant Pumps Tripped Below Minimum Operating Pressure.

CAP034237, Capture Operations Lessons Learned following LCC-12 Breaker Fire.

CAP034241, PC-0218A (Charging Pump P-55A Low Suction Trip) Out of Specification.

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CAP034245, PC-0218B (Charging Pump P-55B low suction trip) Found Out of Specification.

CAP034399, Conduct Common Cause Evaluation on the Response to Alert Declaration.

CAP034622, Missed Opportunity to Update FSAR Text During SOP Procedure Revision.

CAP019120, Alert Declared Due to Fire in Cable Spreading Room.

CAP034538, P-55C Potentially Run Without Suction or Discharge Path.

CAP034623, Design Bases Calculation for Charging Flow Not Updated for Operational Change.

Procedure SOP-2A, Chemical and Volume Control System, Revision 50.

Procedure ONP-25.1, Fire Which Threaten Safety - Related Equipment, Revision 12.

Procedure 24912222,Temporary Installation and Removal of Spare Circuit Breakers, Revision 1

Procedure SPS-E-17,Temporary Installation and Removal of Spare Circuit Breakers, Revision 2

Procedure 4.14, Conduct of Operations, Revision 0.

Procedure 4.09, Control of Operator Aids, Revision 7.

Procedure 10.53, Use and Adherence of Procedures and Other Forms of Written Instruction,

Revision 12.

Procedure 4.00, Operations Organization, Responsibilities and Conduct, Revision 23.

Procedure QO-27, Inservice Testing of CVCS Control, Motor-Operated and Check Valves,

Revision 9.

Procedure 5.01, Processing Work Requests/Work Orders, Revision 27.

Procedure QO-17, Inservice Test Procedure - Charging Pumps, Revision 18.

Procedure 1.10, Plant System, Structure, and Component Labeling, Revision 2.

WO SPS 24912222 7, Charging Pump P-551 Breaker

WO SPS 24912222 7, Removed, Tagged and Stored Arc Chutes in Shop.

WO SPS 24113520 1, Charging Pump P-55A Breaker.

P&ID M-202 SH, 1B, Chemical & Volume Control System.

VTD-2881-0009, Installation Maintenance Instructions For Low Voltage Power Circuit Breakers.

28

VTD-2881-0010, Installation Maintenance Instructions For Low Voltage Air-Magnetic Power

Circuit Breakers For K-Line 225A Thru 2000A.

GOP-14, Shutdown Cooling Operations, Revision 17

ONP-17, Loss of Shutdown Cooling, Revision 28

Operations Log Entries, March 25, 2003

EA-PSA-FIRE-IE-03-05; Fire Initiating Event Frequency for Missing Arc Chutes on 480VAC

Circuit Breaker 52-1205; Revision 0

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