Letter Sequence Other |
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Results
Other: ML031280623, ML031680617, ML031681113, ML031970005, ML031970011, ML032110226, ML032200366, ML032200534, ML032260157, ML032330476, ML032330494, ML032340734
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MONTHYEARML0312806232003-05-0808 May 2003 Memo, Bottom Mounted Instrumentation Leakage Issue - Nondestructive Examination and Repair Options Project stage: Other ML0316806172003-06-17017 June 2003 Summary of South Texas, Unit 1 Conference Call Regarding Bottom Mounted Instrumentation Leakage Issue; Status of Activities Project stage: Other ML0316811132003-06-17017 June 2003 Summary of Conference Call with STP Nuclear Operating Co Regarding South Texas, Unit 1, Bottom Mounted Instrumentation Leakage Issue; Status of Activities Project stage: Other NOC-AE-03001555, Summary of ASME Code Calculation Performed for Repair of Bottom Mounted Instrumentation Penetrations2003-07-0202 July 2003 Summary of ASME Code Calculation Performed for Repair of Bottom Mounted Instrumentation Penetrations Project stage: Request ML0319700052003-07-15015 July 2003 Summary of May 20, 2003, Telephone Conference Re. Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Other ML0319700112003-07-15015 July 2003 Summary of May 29, 2003, Telephone Conference Re. Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Other ML0323407342003-07-16016 July 2003 Pacific Northwest National Lab., Assessment of NDE of STP, Unit 1, Bottom-Mounted Instrumentation Nozzles Project stage: Other ML0320901442003-07-17017 July 2003 Handouts for Meeting with South Texas Project Nuclear Operating Company, South Texas Project, Unit 1, Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Meeting NOC-AE-03001568, Revised Summary of ASME Code Calculations Performed for Repair of Bottom Mounted Instrumentation Penetrations2003-07-23023 July 2003 Revised Summary of ASME Code Calculations Performed for Repair of Bottom Mounted Instrumentation Penetrations Project stage: Request ML0321102262003-07-30030 July 2003 Withholding Ltr, Unit 1, Title 10 of the Code of the Federal Regulations Concerning Bottom Mounted Instrumentation Forced Outage Project stage: Other ML0321206412003-08-0808 August 2003 Summary of Meeting with South Texas Nuclear Operating Company Re South Texas Project, Unit 1, Bottom-Mounted Instrumentation (Bmi) Penetration Leakage Issue Project stage: Meeting ML0321003212003-08-0808 August 2003 Summary of Meeting with South Texas Project Nuclear Operating Company, South Texas Project, Unit 1, Bottom Mounted Instrumentation (Bmi) Penetration Leakage Issue Project stage: Meeting ML0320901592003-08-0808 August 2003 Summary of Meeting with South Texas Project Nuclear Operating Company, South Texas Project, Unit 1, Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Meeting ML0322005342003-08-0808 August 2003 Summary of Telephone Conference with South Texas Project Nuclear Operating Company Re South Texas Project, Unit 1, Bottom-Mounted Instrumentation (Bmi) Penetration Leakage Issue; Status of Activities Project stage: Other ML0322003662003-08-0808 August 2003 Summary of Staff Observation/Audit/Assessment of Visit to Framatome, Inc. ASME Design Calculations Project stage: Other ML0322601572003-08-14014 August 2003 Withholding from Public Disclosure, Westinghouse Field Service Procedure STD-FP-1998-8202, Rev Figure 6.1, MB8435 Project stage: Other ML0323304762003-08-21021 August 2003 Summary of 06/19/03 Telephone Conference Status of Bottom-Mounted Instrumentation Penetration Leakage Issue Project stage: Other ML0323304942003-08-21021 August 2003 Summary of 06/12/03 Telephone Conference Status of Bottom-Mounted Instrumentation Penetration Leakage Issue Project stage: Other 2003-07-02
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Category:Memoranda
MONTHYEARML22147A0932022-06-0606 June 2022 2021 Annual Assessment Public Meeting Summary ML22034A3932022-02-16016 February 2022 Calendar Year 2021 Security Baseline Completion Memo ML21140A3892021-05-24024 May 2021 Riv Column 1 EOC 2020 Public Meeting Summary ML19102A0162019-04-16016 April 2019 4/10/2019 Summary of Public Teleconference Regarding Potential Submission of a Relief Request to Allow Use of Carbon Fiber Reinforced Polymer for Selected Piping Repairs at South Texas, Units 1 and 2 ML18304A2902018-11-19019 November 2018 STP ISFSI PSP Rev 23 Review ML18289A5652018-10-16016 October 2018 Memorandum to D. White Technical Assistance Request - Review of Physical Security Plan for the South Texas Project Generating Station Independent Spent Fuel Storage Installation (CAC No.001027) ML18173A0082018-06-20020 June 2018 Cancelling Numerous Inspection Report Numbers ML17233A0082017-08-21021 August 2017 Notification of Administrative Correction to Renewed Facility Operating License ML17187A1782017-07-0606 July 2017 License Renewal Application ML17137A3252017-05-17017 May 2017 Safety Evaluation of LAR by South Texas Project Nuclear Operating Company to Adopt a Risk-Informed Resolution of Generic Safety Issue-191 ML15190A0422017-05-12012 May 2017 the NRC Staff Evaluation of the Final Rule for Continued Storage of Spent Nuclear Fuel for the License Renewal Environmental Review for South Texas Project, Units 1 and 2 ML16334A4002017-03-24024 March 2017 Climate Change Review Analysis for South Texas Project, Units 1 and 2 - License Renewal Application ML16302A0162016-10-12012 October 2016 Corrected After Action Report/ Improvement Plan for Plume Phase Exercise Conducted on 07/13/2016 ML16013A0662016-01-14014 January 2016 Summary of 11/9 and 12/30/15 Conference Calls with STP Nuclear Operating Company to Discuss the Fall 2015 Steam Generator Tube Inspection Activities (CAC No. A11018) ML13330B2222013-12-0505 December 2013 Notice of Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas Project, Units 1 and 2 (TAC MF2400-MF24 ML13324A4942013-11-19019 November 2013 Deferral of Baseline Inspection Activities ML13303A9742013-10-31031 October 2013 PubMtgNotice-Nov13-2013-update ML13119A0802013-04-30030 April 2013 Notice Meeting Via Conference Call with STP Nuclear Operating Company to Discuss Risk-Informed Approach to Resolve Generic Safety Issue 191 for South Texas, Units 1 and 2 ML13101A3142013-04-12012 April 2013 Notice of Meeting Via Conference Call with STP Nuclear Operating Company to Discuss Risk-Informed Approach to Resolve Generic Safety Issue 191 for South Texas, Units 1 and 2 ML13023A3342013-02-25025 February 2013 1/15/2013 Summary of Public Meetings Conducted to Discuss Draft Supplemental Environmental Impact Statement Related to Review of South Texas Project, Units 1 & 2, License Renewal Application ML13046A0652013-02-22022 February 2013 3/5/13 Notice of Preapplication Meeting Via Conference Call with STP Nuclear Operating Company to Discuss License Amendment Request for Fire Protection Program to Credit Additional Operator Actions for South Texas, Units 1 and 2 ML12342A3972013-01-0303 January 2013 Forthcoming Meeting to Discuss the Draft Supplemental Environmental Impact Statement for the License Renewal of South Texas Project, Units 1 and 2 ML12340A1352012-11-27027 November 2012 Meeting Notice by Conference Call with STP Nuclear Operating Company; Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution South Texas Project, Units 1 and 2 ML12331A2922012-11-27027 November 2012 Notice of Meeting by Conference Call with STP Nuclear Operating Company; Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Units 1 and ML12321A1222012-11-20020 November 2012 12/3/12 Notice of Meeting by Conference Call with STP Nuclear Operating Company; Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Unit ML12312A2342012-11-13013 November 2012 Memo to File Summary Verbal Authorization Provided on 11/6/12 for Relief Request RR-ENG-3-10, RPV Head Flange O-Ring Leakoff Lines NDE, Third 10-Year Inservice Inspection Interval ML12243A4042012-09-25025 September 2012 Notice of Prelicensing Meeting with STP Nuclear Operating Company to Discuss Proposed Amendment for Approval of Revised Fire Protection Program Related to Alternate Shutdown Capability for South Texas, Units 1 and 2 ML12261A3012012-09-21021 September 2012 Notice of Forthcoming Public Meeting Via Conference Call with STP Nuclear Operating Company to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach ML12227A5602012-09-12012 September 2012 Summary of Telephone Conference Call Held on August 9, 2012, Between NRC and STPNOC, Concerning Clarification of One Part of Response to RAI 4.3-13. Pertaining to the STP, Units 1 and 2, LRA ML12227A5902012-08-23023 August 2012 9/6/2012 Notice of Meeting by Conference Call with STP Nuclear Operating Company; Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Uni ML12226A4552012-08-15015 August 2012 Forthcoming Meeting with STP Nuclear Operating Company Regarding License Renewal for the South Texas Project, Units 1 and 2 ML12206A3032012-08-0707 August 2012 Summary of Telephone Conference Call Held on 7/3/12, Between the U.S. NRC and STP Nuclear Operating Company, Concerning Debris from Coating Failures - Followup, Pertaining to the South Texas Project, Units 1 and 2, LRA, TAC Nos. ME4936 and ML12146A0202012-05-31031 May 2012 Notice of 6/11/12 Meeting by Conference Call with STP Nuclear Operating Company; Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Unit ML12080A0352012-04-19019 April 2012 Summary of Telephone Conference Call Held on February 22, 2012 Between the U.S. Nuclear Regulatory Commission and STP Nuclear Operating Company, Regarding Requests for Additional Information STP - Record of Conference Call-02222012 on RAIs- ML12080A0552012-04-11011 April 2012 STP - Record of Conference Call-03082012 on RAIs-SGTI-RxHeadStudClosures ML12080A0492012-04-11011 April 2012 STP - Record of Conference Call-03012012 on RAIs-RV Beltline ML12080A0442012-04-11011 April 2012 STP - Record of Conference Call-02092012 on RAIs-TLAAs ML12080A0402012-04-11011 April 2012 STP - Record of Conference Call-020162012 on RAIs-RVIs-31180-etc ML1207400312012-03-15015 March 2012 3/29/12 Notice of Meeting Viaconference Call with STP Nuclear Operating Company to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for Units 1 and 2 ML1203400432012-02-0303 February 2012 Notice of Forthcoming Meeting Via Conference Call with STP Nuclear Operating Company ML1203003642012-02-0202 February 2012 3/8/12 Forthcoming Meeting by Conference Call with STP Nuclear Operating Company to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, U ML1200901012012-01-10010 January 2012 Notice of Forthcoming Public Meeting Via Conference Call with South Texas Project Nuclear Operating Company ML11348A0392012-01-0404 January 2012 and 12/1/11, Summary of Telephone Conference Calls Between the U.S. Nuclear Regulatory Commission and STP Nuclear Operating Company, Concerning Requests for Additional Information Pertaining to the South Texas Project LRA - Set 9 ML11320A1162011-12-0505 December 2011 November 9, 2011, Summary of Telephone Conference Call Held Between the U.S. Nuclear Regulatory Commission and STP Nuclear Operating Company, Concerning Requests for Additional Information Pertaining to the South Texas Project Units 1 and 2 ML1129701092011-11-0101 November 2011 Notice of Meeting Via Conference Call with STP Nuclear Operating Company to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor Sump Performance, Resolution Approach for South Texas, Units 1 & 2 ML1124114192011-10-0404 October 2011 8/22/11 Summary of Meeting with STP Nuclear Operating Company to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Units 1 and 2 (TAC M ML1125101482011-09-15015 September 2011 Notice of Meeting by Conference Call with STP Nuclear Operating Co. to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Units 1 and 2 ML11216A2632011-08-23023 August 2011 Summary of Telephone Conference Call Held on July 28, 2011, Between the U.S. NRC and STP Nuclear Operating Company, Concerning RAI Pertaining to the South Texas Project, LRA ML1121301822011-08-0202 August 2011 Meeting Notice with STP Nuclear Operating Company to Discuss Risk-Informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Units 1 and 2 (TAC ME5358-ME5359 ML1118615292011-07-12012 July 2011 Notice of Conference Call with STP Nuclear Operating Company to Discuss Risk-informed GSI-191, Assessment of Debris Accumulation on Pressurized-Water Reactor (PWR) Sump Performance, Resolution Approach for South Texas, Units 1 and 2 2022-06-06
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May 8, 2003 MEMORANDUM TO: File FROM: Mohan Thadani, Senior Project Manager, Section 1 /RA/
Project Directorate IV Division of Licensing Project Management
SUBJECT:
U.S. NUCLEAR REGULATORY COMMISSION (NRC)
HEADQUARTERS AND REGION IV STAFF TELEPHONE CONVERSATION WITH STP NUCLEAR OPERATING COMPANY (STPNOC) REGARDING SOUTH TEXAS PROJECT (STP), UNIT 1, BOTTOM MOUNTED INSTRUMENTATION (BMI) LEAKAGE ISSUE; NONDESTRUCTIVE EXAMINATION (NDE) AND REPAIR OPTIONS (TAC NO. MB8435)
On April 24, 2003, the NRC Region IV and Headquarter's staff held a telephone conference call with STPNOC, the licensee for STP, Unit 1. The conference call was held as a result of the ongoing discussions related to the identification of apparent leakage at the interface of reactor vessel bottom head and BMI Penetrations 1 and 46. Attachment 1 is a list of the participants.
On this telephone conference call the licensee briefed the NRC staff on the current status of its actions regarding NDE and repair options addressing BMI penetration leakage.
NDE Plans The licensee pointed out several problems of the NDE. The difficulty of access to the nozzles and providing adequate shielding are the primary complication. To maintain shielding, the reactor vessel will have to be flooded. The licensee stated that the underwater camera visual inspection technique has been used by Framatome. The licensee is working with the Electric Power Research Institute to build a life size mockup of the typical BMI penetration. The mockup is expected to be ready in a week and will eventually be at the site.
The licensee is exploring options to perform ultrasonic and eddy current examination of the BMI nozzle tube. The underwater visual exam would cover the J-groove weld surface. The licensee believes that it could qualify the visual examination to provide equivalent resolution as compared to a liquid penetrant examination of the weld surface.
CONTACT: Mohan Thadani, NRR 415-1476
File The licensee is exploring using the Seabrook, Unit 2 reactor vessel to perform liquid penetrant examination of the BMI penetrations to ascertain whether any fabrication related indications exist. The Seabrook, Unit 2 and STP, Unit 1 vessels were manufactured in a similar manner.
Root Cause Analysis The licensee will investigate the condition by continuing its inspection activities, including NDE techniques and metallographic analysis, in order to determine the cause of the leak.
This effort will include visual inspection by qualified inspectors and eddy current or ultrasonic testing. Industry experts will be used in conjunction with the licensee's own expert staff to expeditiously identify the root cause of the condition.
Extent of Condition The licensee will evaluate the impact of the condition on the other 56 BMI penetrations of STP, Unit 1, and all BMI penetrations of Unit 2. The licensee will also apply the NDE techniques to determine whether any reactor vessel material wastage exists.
Repair Options The licensee's repair options involve moving the pressure boundary from inside the vessel to outside the vessel. The selected option will ensure that pressure boundary integrity is maintained. The licensee will also address the need to continue to monitor this area.
The licensee is considering three alternative repair methods: (1) half tube repair which cuts off the lower portion of the tube about midway through the vessel thickness. A temper-bead is applied and a new lower portion is welded in place (using the Code Case N-638 and N-2142-1); (2) encapsulation by welding a tube over the existing stub and attaching to the vessel via temper-bead welding, and (3) use of mechanical clamp and seal device attached to the vessel with rods. In all cases, the pressure boundary is relocated from the original J-groove weld to outside the reactor vessel. The repair will be done with reactor reassembled and fuel loaded. This is necessary so that in-cores can be inserted to reduce the radiation field in the area of the repairs. These repairs will require NRC review and approval.
Briefings to NRC The licensee will have face to face meetings with NRC to review the progress of its efforts at suitable intervals, and continue to hold weekly telephone conferences at 2:00 p.m.
Central Daylight Savings Time on Thursdays, to keep NRC fully informed of the root cause, extent of conditions, and repair methods prior to restarting the unit.
File Public Meetings The NRC staff discussed the benefit of holding a public meeting in the vicinity of STP site at a time closer to the Unit 1 restart. The licensee agreed to support the meeting for the purpose of public outreach.
Docket No. 50-498
Attachment:
List of Participants
LIST OF PARTICIPANTS Licensee's Representatives Gary Parkey - Vice President, Generation Tom Jordan - Vice President, Engineering & Technical Services Ed Halpin - Plant General Manager Mark McBurnett - Manager, Quality & Licensing Will Jump - Manager, Training Steve Thomas - Manager, Plant Design Engineering Alex Kent - Manager, Testing Program Scott Head - Manager Licensing Paul Sera - Manager, Plant Protection Michael Lashley - Supervising Engineer, Testing Engineering Harry Murray - Manger, Facilities Mike Meier - General Manager, Station Support Wayne Harrison - Sr. Staff Licensing Engineer NRC Participants Headquarters Region IV Robert Gramm Pat Gwynn William Reckley Dwight Chamberlain Leonard Wert Charles Marschall Carol Moyer Dale Powers Mark Hartzman Victor Dricks Donnie Harrison James Adams Stephen Monarque Geoff Miller Jack Foster Bill McNeil Mohan Thadani Wayne Sifre Allen Hiser (from home) Lee Ellershaw Stephanie Coffin Tim McConnell Bill Maier Region III Chuck Paulk John Jacobson Attachment
File Public Meetings The NRC staff discussed the benefit of holding a public meeting in the vicinity of STP site at a time closer to the Unit 1 restart. The licensee agreed to support the meeting for the purpose of public outreach.
Docket No. 50-498
Attachment:
List of Participants DISTRIBUTION: See next page ACCESSION NO: ML031280623 *SEE PREVIOUS CONCURRENCES OFFICE PDIV-1/PM PDIV-1/LA RIV-DRP/BC PDIV-1/SC NAME MThadani MMcAllister BJohnson* RGramm*
DATE 5/8/03 5/8/03 05/08/03 05/08/03 OFFICIAL RECORD COPY
MEMORANDUM REGARDING TELEPHONE CONVERSATION BETWEEN NRC AND STPNOC ON APRIL 24, 2003 Dated: May 8, 2003 DISTRIBUTION:
PUBLIC PDIV-1 Reading RidsNrrDlpmLpdiv (HBerkow)
RidsNrrDlpmLpdiv1(RGramm)
RidsNrrPMMThadani RidsNrrLAMMcAllister RidsNrrAdpt (BSheron/MKotzalas)
RidsNrrDlpm (JZwolinski/TMarsh)
RidsNrrDe (RBarrett)
JFoster WBateman SCoffin ESullivan MMitchell KManoly DTerao WJohnson, RIV CPaulk, RIV WCullen WReckley SBloom