Letter Sequence Meeting |
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Results
Other: ML031280623, ML031680617, ML031681113, ML031970005, ML031970011, ML032110226, ML032200366, ML032200534, ML032260157, ML032330476, ML032330494, ML032340734
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MONTHYEARML0312806232003-05-0808 May 2003 Memo, Bottom Mounted Instrumentation Leakage Issue - Nondestructive Examination and Repair Options Project stage: Other ML0316806172003-06-17017 June 2003 Summary of South Texas, Unit 1 Conference Call Regarding Bottom Mounted Instrumentation Leakage Issue; Status of Activities Project stage: Other ML0316811132003-06-17017 June 2003 Summary of Conference Call with STP Nuclear Operating Co Regarding South Texas, Unit 1, Bottom Mounted Instrumentation Leakage Issue; Status of Activities Project stage: Other NOC-AE-03001555, Summary of ASME Code Calculation Performed for Repair of Bottom Mounted Instrumentation Penetrations2003-07-0202 July 2003 Summary of ASME Code Calculation Performed for Repair of Bottom Mounted Instrumentation Penetrations Project stage: Request ML0319700052003-07-15015 July 2003 Summary of May 20, 2003, Telephone Conference Re. Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Other ML0319700112003-07-15015 July 2003 Summary of May 29, 2003, Telephone Conference Re. Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Other ML0323407342003-07-16016 July 2003 Pacific Northwest National Lab., Assessment of NDE of STP, Unit 1, Bottom-Mounted Instrumentation Nozzles Project stage: Other ML0320901442003-07-17017 July 2003 Handouts for Meeting with South Texas Project Nuclear Operating Company, South Texas Project, Unit 1, Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Meeting NOC-AE-03001568, Revised Summary of ASME Code Calculations Performed for Repair of Bottom Mounted Instrumentation Penetrations2003-07-23023 July 2003 Revised Summary of ASME Code Calculations Performed for Repair of Bottom Mounted Instrumentation Penetrations Project stage: Request ML0321102262003-07-30030 July 2003 Withholding Ltr, Unit 1, Title 10 of the Code of the Federal Regulations Concerning Bottom Mounted Instrumentation Forced Outage Project stage: Other ML0321206412003-08-0808 August 2003 Summary of Meeting with South Texas Nuclear Operating Company Re South Texas Project, Unit 1, Bottom-Mounted Instrumentation (Bmi) Penetration Leakage Issue Project stage: Meeting ML0321003212003-08-0808 August 2003 Summary of Meeting with South Texas Project Nuclear Operating Company, South Texas Project, Unit 1, Bottom Mounted Instrumentation (Bmi) Penetration Leakage Issue Project stage: Meeting ML0320901592003-08-0808 August 2003 Summary of Meeting with South Texas Project Nuclear Operating Company, South Texas Project, Unit 1, Bottom Mounted Instrumentation Penetration Leakage Issue Project stage: Meeting ML0322005342003-08-0808 August 2003 Summary of Telephone Conference with South Texas Project Nuclear Operating Company Re South Texas Project, Unit 1, Bottom-Mounted Instrumentation (Bmi) Penetration Leakage Issue; Status of Activities Project stage: Other ML0322003662003-08-0808 August 2003 Summary of Staff Observation/Audit/Assessment of Visit to Framatome, Inc. ASME Design Calculations Project stage: Other ML0322601572003-08-14014 August 2003 Withholding from Public Disclosure, Westinghouse Field Service Procedure STD-FP-1998-8202, Rev Figure 6.1, MB8435 Project stage: Other ML0323304762003-08-21021 August 2003 Summary of 06/19/03 Telephone Conference Status of Bottom-Mounted Instrumentation Penetration Leakage Issue Project stage: Other ML0323304942003-08-21021 August 2003 Summary of 06/12/03 Telephone Conference Status of Bottom-Mounted Instrumentation Penetration Leakage Issue Project stage: Other 2003-07-02
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Category:Meeting Summary
MONTHYEARML24120A2362024-05-0606 May 2024 Summary of March 25, 2024, Presubmittal Teleconference with STP Nuclear Operating Company to Discuss Changes to the Quality Assurance Plan for South Texas Project, Units 1 and 2 ML22252A0432022-09-12012 September 2022 Summary of August 31, 2022, Webinar with STP Nuclear Operating Company to Discuss a Proposed LAR to Revise the Dose Consequence Analysis for Main Steam Line Break and Locked Rotor Analysis Events for STP, Units 1 & 2 ML22147A0932022-06-0606 June 2022 2021 Annual Assessment Public Meeting Summary ML21236A3082021-09-10010 September 2021 Regulatory Audit Summary Regarding License Amendment Request to Revise Moderator Temperature Coefficient Surveillance Requirements ML21222A1192021-08-12012 August 2021 Summary of Meeting with STP Nuclear Operating Company Regarding the License Amendment Request to Revise the Moderator Temperature Coefficient Surveillance Requirements for South Texas Project, Units 1 and 2 ML21140A3892021-05-24024 May 2021 Riv Column 1 EOC 2020 Public Meeting Summary ML20279A8152020-10-20020 October 2020 Summary of September 14, 2020, Presubmittal Teleconference with STP Nuclear Operating Company Regarding the Proposed LAR to Revise the Moderator Temperature Coefficient Surveillance Requirement for South Texas Project, Units 1 and 2 (EPID L ML20189A2832020-07-0707 July 2020 Summary of Region IV Annual Assessment Public Meeting ML20163A5522020-06-12012 June 2020 Summary of April 21, 2020, Teleconference with STP Nuclear Operating Company to Discuss the License Amendment Request to Revise the Emergency Plan for South Texas Project, Units 1 and 2 ML20140A2612020-05-27027 May 2020 May 5, 2020, Summary of Teleconference with STP Nuclear Operating Company to Discuss a Proposed Exigent License Amendment Request to Revise the Pressure of the Safety Injection Accumulators for South Texas Project, Unit 1 ML20107J5482020-04-15015 April 2020 Teleconference Regarding NRC Observations on the March 30, 2020, License Amendment Request to Revise the Emergency Plan STP Nuclear Operation Company South Texas Project, Units 1 and 2, Dockets 50-498 and 50-499 ML20049A0572020-02-26026 February 2020 Summary of February 6, 2020, Meeting with STP Nuclear Operating Company to Discuss a Proposed License Amendment Request to Revise the Emergency Plan for South Texas Project, Units 1 and 2 (EPID L- 2020-LRM-0004) ML19350C5902019-12-17017 December 2019 12/3/19, Summary of Teleconference with STP Nuclear Operating Company to Discuss a Proposed License Amendment Request to Revise the Emergency Plan for South Texas Project, Units 1 and 2, ML19102A0162019-04-16016 April 2019 4/10/2019 Summary of Public Teleconference Regarding Potential Submission of a Relief Request to Allow Use of Carbon Fiber Reinforced Polymer for Selected Piping Repairs at South Texas, Units 1 and 2 ML17005A1002017-01-18018 January 2017 January 4, 2017, Summary of Meeting to Discussion Stp'S Response to Request for Additional Information the Revised Aluminum Bronze Selective Leaching Aging Management Program for All Potentially Susceptible Welds Throughout the Facility ML16279A3312016-10-27027 October 2016 Summary of Public Meeting with STP Nuclear Operating Company Regarding Open Items, Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 (CAC Nos. MF2400-MF2409) ML16272A4362016-10-14014 October 2016 Summary of Public Preapplication Meeting with STP Nuclear Operating Company to Discuss Possible License Amendment Request to Modify Emergency Response Organization for South Texas Project, Units 1 and 2 ML16246A0222016-10-0505 October 2016 Summary of Public Meeting with STP Nuclear Operating Company Regarding Open Items Related to Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 (CAC Nos. MF2400 - MF2409) ML16238A5272016-09-0101 September 2016 Summary of 7/28/16, Public Meeting with STP Nuclear Operating Company to Discuss the License Amendment and Exemption Requests to Use a Risk-Informed Approach to the Resolution of GSI-191 (CAC Nos. MF2400 - MF2409) ML16218A3672016-08-30030 August 2016 07/21/2016 Summary of Public Teleconference Meeting with STP Nuclear Operating Company Discussing Revisions to License Renewal Application Aluminum Bronze Selective Leaching Aging Management Program and Background Document ML16236A0322016-08-23023 August 2016 08/18/2016 Summary of Conference Call With STP Nuclear Operating Company Concerning the Aluminum Bronze Selective Leaching Aging Management Program in the South Texas Project, License Renewal Application ML16236A3042016-08-23023 August 2016 08/11/2016 Summary of Conference Call Between NRC and STP Nuclear Operating Company Concerning the 2016 Annual Update to the South Texas Project License Renewal Application ML16180A0142016-07-25025 July 2016 Summary of Meeting Discussion Between South Texas Project, Units 1 and 2, and NRC Staff Regarding the Revised Aluminum Bronze Selective Leaching Aging Management Program for All Potentially Susceptible Welds Throughout the Facility ML16190A0082016-07-13013 July 2016 Summary of 6/22/2016 Public Meeting with STP Nuclear Operating Company Regarding Open Items, Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 (CAC Nos. MF2400-MF2409) ML16188A0072016-07-0707 July 2016 Summary of Telecon Held on July 5, 2016 With STP Nuclear Operating Company, Concerning Additional Information Pertaining to the STP, License Renewal Application (TAC. Nos. ME4936, ME4937) ML16188A0112016-07-0707 July 2016 Summary of Telecon Held on July 5, 2016 With STP Nuclear Operating Company, Concerning Additional Information Pertaining to the STP, License Renewal Application (TAC Nos. ME4936, ME4937) ML16188A0092016-07-0707 July 2016 Summary of Telecon Held on July 5, 2016 with STP Nuclear Operating Company, Concerning Additional Information Pertaining to the STP, License Renewal Application (Tac. Nos. ME4936, ME4937) - Enclosure 1 ML16175A1082016-06-24024 June 2016 Summary of 4/21/2016 Public Meeting with STP Nuclear Operating Company Regarding Open Items, Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 ML16166A0272016-06-14014 June 2016 Summary of Telephone Conference Call Held on 06/08/2016, Between the USNRC and STP Nuclear Operating Company Response to Request for Additional Information B2.1.18-6 Pertaining to the South Texas Project License Renewal Application ML16092A0852016-04-13013 April 2016 3/17/2016 Summary of Public Meeting with STP Nuclear Operating Company Regarding Open Items, Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 (CAC Nos. MF2401-MF2409) ML16092A0442016-04-11011 April 2016 Summary of 3/3/2016 Public Meeting with STP Nuclear Operating Company Regarding Open Items, Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 (CAC Nos. MF2400-MF2409) ML16088A2432016-04-0101 April 2016 2/18/2016, Summary of Public Meeting with STP Nuclear Operating Company Regarding Open Items, Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 (CAC Nos. MF2400-MF2409) ML16081A2052016-03-24024 March 2016 Summary of Meeting with STP Nuclear Operating Company to Discuss Potential License Amendment Request for South Texas Project, Unit 1 Regarding Permanent Operation with 56 Control Rods ML16074A0412016-03-14014 March 2016 Summary of a Call Held on March 10, 2016, between USNRC and STPNOC, Concerning the Staff's Upcoming Audit Regarding the Amp for the Loss Of Material Due to Selective of Al-Br Welds in the ECW System for the STP LRA (TAC Nos. ME4936 And ME4937) ML16060A1272016-03-0707 March 2016 February 23, 2016, Summary of Conference Calls Held between NRC and STP Concerning Staff's Review of Submerged Closure Bolting Portion of 2014 Annual Update for STP License Renewal Application (TAC ME4936 And ME4937) ML16028A1522016-02-18018 February 2016 1/14/2016 Summary of Public Meeting with STP Nuclear Operating Company Regarding Modifications to the Licensee'S Risk-Informed Generic Safety Issue (GSI) 191 Application and Supplements for South Texas Project, Units 1 and 2 ML16035A4802016-02-12012 February 2016 Jsc Meeting Summary Attachment ML16011A0612016-02-0202 February 2016 Summary of 10/1/15 Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas Project, Units 1 and 2 (CAC MF ML16011A0702016-01-28028 January 2016 Summary of Preapplication Meeting with STP Nuclear Operating Company to Discuss Exigent License Amendment Request to Operate Following Removal of a D6 Control Rod at South Texas Project, Unit 1 ML16033A0072016-01-19019 January 2016 January 19, 2016, Summary of Public Meeting with STP to Discuss the Plant-Specific Aging Management Program, Selective Leaching of Aluminum Bronze, Associated with STP's License Renewal Application ML16013A0662016-01-14014 January 2016 Summary of 11/9 and 12/30/15 Conference Calls with STP Nuclear Operating Company to Discuss the Fall 2015 Steam Generator Tube Inspection Activities (CAC No. A11018) ML15308A0112015-11-30030 November 2015 Record of Conference Call on STP Request for Additional Information Set 34 ML15201A0032015-07-30030 July 2015 7/2/15 Summary of Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas, Units 1 and 2 ML15177A1042015-07-21021 July 2015 4/22/2015 Summary of Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas, Units 1 and 2 (TAC MF2400 t ML15177A2742015-07-21021 July 2015 5/6/2015 Summary of Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas, Units 1 and 2 (TAC Nos. MF24 ML15180A2732015-07-15015 July 2015 6/3/2015 Summary of Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas, Units 1 and 2 (TAC MF2400 to ML15139A3442015-06-11011 June 2015 Summary of Telephone Conference Call Held on May 12, 2015 Between the U.S. Nuclear Regulatory Commission and STP Nuclear Operating Company, Concerning Request for Additional Information, Set 31, Pertaining to the South Texas Project, Licens ML15103A0022015-05-13013 May 2015 Summary of 4/8/15 Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas, Units 1 and 2 ML15084A0032015-04-0606 April 2015 2/4/15 Summary of Meeting with STP Nuclear Operating Company to Discuss Revised Pilot Submittal and Request for Exemptions for a Risk-Informed Approach to Resolve Generic Safety Issue (GSI)-191 at South Texas, Units 1 and 2 (TAC MF2400-MF24 ML15084A0042015-04-0101 April 2015 2/5/2015 Summary of Presubmittal Meeting with STP Nuclear Operating Company to Discuss Integrated Leak Rate Testing Program License Amendment Request for South Texas, Units 1 and 2 2024-05-06
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Text
August 8, 2003 LICENSEE: South Texas Project Nuclear Operating Company FACILITY: South Texas Project, Unit 1
SUBJECT:
SUMMARY
OF THIRD MEETING WITH SOUTH TEXAS PROJECT NUCLEAR OPERATING COMPANY REGARDING SOUTH TEXAS PROJECT, UNIT 1, REACTOR VESSEL AND BOTTOM-MOUNTED INSTRUMENTATION PENETRATION INTERFACE LEAKAGE (TAC NO. MB8435)
On July 17, 2003, STP Nuclear Operating Company (STPNOC), the licensee for South Texas Project (STP), Units 1 & 2, met with the U. S. Nuclear Regulatory Commission (NRC) staff at the NRC Headquarters. The purpose of the meeting was for STPNOC to brief the NRC staff and management regarding STPNOCs concluding efforts to address the issues arising from the April 12, 2003, discoveries of indications of leakage from the STP, Unit 1, bottom mounted instrument (BMI) penetrations 1 and 46. There are 58 BMI penetrations at STP, Unit 1.
At the outset, the NRC staff informed the audience that the NRC staff would not be making any decisions at this meeting. The purpose of the meeting was to gather information to facilitate the NRC staffs comprehensive evaluation of the issues raised.
The STPNOC stated that it has documented its commitments to take follow up actions as outlined in its letter dated July 11, 2003. The NRC staff commented that the letter does not specifically state that the described actions are in fact licensee commitments. The licensee stated that it will provide a follow up in response to the comment.
A list of meeting attendees is included as Enclosure 1 to this summary. Enclosure 2 contains the licensee's presentation view-graphs .
The STPNOC outlined its desired meeting outcomes: (1) to keep NRC fully informed and ensure that NRC has sufficient information to complete its comprehensive assessment; (2) to explain the results of comprehensive nondestructive examination (NDE); and (3) to describe remaining future activities, i.e., to collect boat samples, perform nozzle remnants analyses, and submit a licensee event report supplement. The licensee then summarized its root cause analysis process and planned monitoring and inspection activities. The STPNOC provided answers to NRC questions and understood the remaining NRC needs for information. The STPNOC summarized that the residue found at BMI penetration no. 1 and penetration no. 46 was very small. It indicated a very small leak from the reactor bottom.
NDE Campaign An extensive NDE campaign included ultrasonic testing (UT), enhanced visual examination of J-groove weld surface, volumetric interrogation of vessel base metal for wastage, eddy current testing (ET) of penetration tube inside diameter, ET of J-groove weld surface, profilometry, boroscope examination, Helium leak tests, metallurgical analysis of removed nozzle remnants, and future boat sample analysis.
The licensee stated that the results of the evaluation indicated that the observed leakage was caused by one axial crack in each of the two penetrations. Penetration no. 1 had three crack indications, with one leak path. Penetration no. 46 had two axial indications with one leak path.
Nozzle Repairs The condition was limited to two identified nozzles and the cracks identified were axial in orientation. Evaluation of stresses indicated that circumferential cracking was not likely to occur. The licensee selected the half-nozzle repair method. Repair of both of the leaking nozzles is complete.
Root Cause Process The licensee outlined that there were no circumferential indications, no cracks above or below the J-groove weld, and no material wastage was found. The STPNOC considered two possible causes of crack initiation: (1) The cracks were caused by primary water stress corrosion cracking (PWSCC), or (2) the cracks were caused by a fabrication flaw over-stress in the nozzle and/or weld. The cracks were either propagated by PWSCC or low-cycle fatigue. The licensee then deduced that the facts are not consistent with PWSCC. No cracks were identified in 56 out of 58 BMI nozzles. The cracks were about 4 years old, were about the same age, and did not initiate from the inside diameter of the tubes. The licensee concluded that for PWSCC to be the cause, the expectation would be to observe defects in approximately 20 percent of the penetrations. Hence, defects would be expected in 12 penetrations out of 58 examined, but only 2 penetrations with defects were found.
The residual stresses do not appear to show any correlation with the observed cracks.
Penetration no. 1 and penetration no. 46 differ in residual stresses, and still they are the only penetrations showing crack indications and leakage. Furthermore, some cracks did not appear to be in contact with primary water. Based on the above rationale, the licensee concluded that the root cause of the BMI cracks was fabrication flaws.
The NRC staff commented that the licensees hypothesis did not explain why the fabrication flaws occurred only in penetrations 1 and 46. The licensee responded that it would consider the NRC comment in further evaluation of the root cause.
Monitoring and Inspection Plan The licensee proposed that it will continue the bare metal inspections under its boric acid control program. It will perform UT and enhanced visual testing of the BMI instrumentation at the next Unit 1 vessel inservice inspection program inspection. It will also perform periodic UT of vessel base material around the repaired penetrations, and will perform volumetric examination of Unit 2 penetrations at the next refueling outage with the core barrel removed.
Conclusions The licensee concluded that: (1) the extent of the condition is known, (2) that STPNOC has identified the probable cause as understood at the time, (3) engineering work has been completed, (4) the condition has been corrected by the half-nozzle design repair, (5) the
licensee has confidence in the effectiveness of the repair, and (6) the plant staff is trained and is prepared for start up of the plant.
The NRC staff informed the STPNOC that its boric acid inspection program has been proactive, and that its response to the conditions of leakage in BMI penetrations 1 and 46 has been thorough. The staff asked how is it that STPNOC can perform the operations at STP, Units 1&2, in such a proactive and thoroughly responsive manner. The licensee responded that it is the policy of the STPNOC management to ensure that, when challenges are identified, the company mobilizes the best internal resources and the worlds best contractors to support the resolution of the issues, and to eliminate the challenges.
The NRC staff then asked for public comments for the meeting attendees and the teleconference participants. No comments were offered. The meeting was then adjourned.
/RA/
Mohan C. Thadani, Senior Project Manager, Section 1 Project Directorate IV Division of Licensing Project Management Office of Nuclear Reactor Regulation Docket No. 50-498
Enclosures:
- 1. List of Attendees
- 2. View-graphs (ADAMS Accession No.: ML032090144) cc: see next page
ML032090144) cc w/enclosure: See next page DISTRIBUTION: See Next Page Package No.: ML032090151 Handouts: ML032090144 ADAMS Accession No.: ML032090159 *via e-mail NRC-001 OFFICE PDIV-1/PM PDIV-1/LA RIV PDIV-1/SC NAME MThadani:sab MMcAllister WJohnson* RGramm DATE 8/08/2003 8/08/2003 8/08/2003 8/08/2003 DISTRIBUTION FOR MEETING BETWEEN NRC AND STP NUCLEAR OPERATING COMPANY ON JULY 17, 2003.
Dated: August 8, 2003 DISTRIBUTION:
PUBLIC PDIV-1 RF RidsNrrAdpt (BSheron/MKotzalas) RidsNrrDssa (SBlack/MJohnson)
RidsNrrDlpm (LMarsh/ELeeds) RidsRgn4MailCenter (AHowell)
RidsNrrDlpmLpdiv (HBerkow) RidsNrrDlpmLpdiv1 (RGramm)
RidsNrrPMMThadani RidsNrrLAMMcAllister RidsOgcRp RidsAcrsAcnwMailCenter BBateman MHartzman TMensah EDO Contact, RIV EReichelt TPruett, RIV ESullivan BCullen AHiser SCoffin SBurnell GCheruvenki WJohnson, RIV SBloom RBywater, RIV JFoster
MEETING PARTICIPANTS FOR THIRD MEETING BETWEEN STPNOC AND NRC ON JULY 17, 2003 Licensee Participants Tom Jordan Mark McBurnett Tim Bowman Wayne Harrison Bill Humble Michael Lashley Ulhas Patil Steve Thomas NRC Participants Headquarters Region IV Brian Sheron William Johnson Richard Barrett Russell Bywater Robert Gramm Troy Pruett Stephanie Coffin Ganesh Cheruvenki Scott Burnell Mark Hartzman Other Edmund Sullivan Herb Berkow David Lochbaum, Union of Concerned Scientists Allen Hiser Al Gutterman, Morgan Lewis William Bateman Jim Riley, NEI Mel Fields Paul Gunter, NIRS Eric Reichelt Kazuhiko Kishioka, JAPC Mohan Thadani Altheia Wyche, SERCH Licensing/Bechtel William Cullen Randal Schmidt, PSEG Nuclear Joe Roarty, Def. Nuc. Fac. Safety Jim Osborn, Public Getachen Tesfaye, CEG Jon Kirkwood, CEG Robert Hermann, SIA Enclosure 1
South Texas Project, Unit 1 cc:
Mr. Cornelius F. OKeefe A. H. Gutterman, Esq.
Senior Resident Inspector Morgan, Lewis & Bockius U.S. Nuclear Regulatory Commission 1111 Pennsylvania Avenue, NW P. O. Box 910 Washington, DC 20004 Bay City, TX 77414 Mr. T. J. Jordan, Vice President A. Ramirez/C. M. Canady Engineering & Technical Services City of Austin STP Nuclear Operating Company Electric Utility Department P. O. Box 289 721 Barton Springs Road Wadsworth, TX 77483 Austin, TX 78704 S. M. Head, Manager, Licensing Mr. L. K. Blaylock Nuclear Quality & Licensing Department Mr. W. C. Gunst STP Nuclear Operating Company City Public Service Board P. O. Box 289, Mail Code: N5014 P. O. Box 1771 Wadsworth, TX 77483 San Antonio, TX 78296 Environmental and Natural Resources Mr. C. A. Johnson/A. C. Bakken Policy Director AEP Texas Central Company P. O. Box 12428 P. O. Box 289 Austin, TX 78711-3189 Mail Code: N5022 Wadsworth, TX 77483 Jon C. Wood Matthews & Branscomb INPO 112 East Pecan, Suite 1100 Records Center San Antonio, TX 78205 700 Galleria Parkway Atlanta, GA 30339-3064 Arthur C. Tate, Director Division of Compliance & Inspection Regional Administrator, Region IV Bureau of Radiation Control U.S. Nuclear Regulatory Commission Texas Department of Health 611 Ryan Plaza Drive, Suite 400 1100 West 49th Street Arlington, TX 76011 Austin, TX 78756 D. G. Tees/R. L. Balcom Brian Almon Texas Genco, LP Public Utility Commission P. O. Box 1700 William B. Travis Building Houston, TX 77251 P. O. Box 13326 1701 North Congress Avenue Judge, Matagorda County Austin, TX 78701-3326 Matagorda County Courthouse 1700 Seventh Street Bay City, TX 77414
South Texas Project, Unit 1 cc:
Susan M. Jablonski Office of Permitting, Remediation and Registration Texas Commission on Environmental Quality MC-122 P.O. Box 13087 Austin, TX 78711-3087 Mr. Terry Parks, Chief Inspector Texas Department of Licensing and Regulation Boiler Division P. O. Box 12157 Austin, TX 78711 Mr. Ted Enos 4200 South Hulen Suite 630 Ft. Worth, Texas 76109 Mr. James J. Sheppard President and Chief Executive Officer STP Nuclear Operating Company South Texas Project Electric Generating Station P. O. Box 289 Wadsworth, TX 77483