ML030090566

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IR 05000445-02-009, on 10/07 - 11/01/02, Txu Energy; on 10/07-11/01/2002; Comanche Peak Steam Electric Station; Unit 1, Special Inspection. Non-Cited Violations Noted
ML030090566
Person / Time
Site: Comanche Peak Luminant icon.png
Issue date: 01/09/2003
From: Chamberlain D
Division of Reactor Safety IV
To: Terry C
TXU Energy
References
IR-02-009
Download: ML030090566 (23)


See also: IR 05000445/2002009

Text

January 9, 2003

C. L. Terry, Senior Vice President

and Principal Nuclear Officer

TXU Energy

ATTN: Regulatory Affairs

Comanche Peak Steam Electric Station

P.O. Box 1002

Glen Rose, Texas 76043

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION - SPECIAL TEAM

INSPECTION REPORT 50-445/02-09

Dear Mr. Terry:

On November 1, 2002, the NRC completed a special team inspection at your Comanche Peak

Steam Electric Station, Unit 1. The enclosed report documents the inspection findings, which

were discussed during a public exit meeting on December 10, 2002, with you and other

members of your staff.

This inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

Within these areas, the inspection consisted of selected examination of procedures and

representative records, observations of activities, and interviews with personnel.

The report discusses an apparent violation that involves the failure to identify and correct an

indicated flaw in a steam generator tube during Refueling Outage 1RF08 that resulted in a

steam generator tube leak. Based on the results of this inspection, the significance of this

issue is pending the determination of its safety significance using the Significance

Determination Process described in NRC Inspection Manual Chapter 0609. Since your staff

removed the leaking tube from service, it does not present an immediate safety concern.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for the finding at this time. In addition, please be advised that the number and

characterization of the apparent violation described in the enclosed report may change as a

result of further NRC review.

The report also discusses a noncited violation of very low significance for two examples of

failure to identify significant steam generator tube flaw indications during Refueling

Outage 1RF09.

TXU Energy

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These were evaluated under the risk significance determination process as having very low

safety significance (Green). The NRC has also determined that a violation was associated with

these issues. Because the issue had very low risk significance, and because you entered the

issue in your corrective action program and removed the tubes from service, the violation is

being treated as a noncited violation, consistent with Section VI.A of the Enforcement Policy.

The noncited violation is described in the subject inspection report. If you contest the violation

or significance of the noncited violation, you should provide a response within 30 days of the

date of this inspection report, with the basis for your denial, to the U.S. Nuclear Regulatory

Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the

Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza

Drive, Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear

Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the

Comanche Peak facility.

In accordance with 10 CFR 2.790 of the NRCs "Rules of Practice," a copy of this letter and its

enclosure will be made available electronically for public inspection in the NRC

Public Document Room or from the Publicly Available Records (PARS) component of NRCs

document system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/ by DAP

Dwight D. Chamberlain, Director

Division of Reactor Safety

Docket: 50-445

License: NPF-87

Enclosure:

NRC Inspection Report

50-445/02-09

cc w/enclosure:

Roger D. Walker

Regulatory Affairs Manager

TXU Generation Company LP

P.O. Box 1002

Glen Rose, Texas 76043

George L. Edgar, Esq.

Morgan, Lewis & Bockius

1800 M. Street, NW

Washington, D.C. 20036-5869

TXU Energy

-3-

G. R. Bynog, Program Manager/

Chief Inspector

Texas Department of Licensing & Regulation

Boiler Division

P.O. Box 12157, Capitol Station

Austin, Texas 78711

County Judge

P.O. Box 851

Glen Rose, Texas 76043

Chief, Bureau of Radiation Control

Texas Department of Health

1100 West 49th Street

Austin, Texas 78756-3189

Environmental and Natural

Resources Policy Director

Office of the Governor

P.O. Box 12428

Austin, Texas 78711-3189

Brian Almon

Public Utility Commission

William B. Travis Building

P.O. Box 13326

1701 North Congress Avenue

Austin, Texas 78701-3326

Susan M. Jablonski

Office of Permitting, Remediation and Registration

Texas Commission on Environmental Quality

MC-122

P.O. Box 13087

Austin, TX 78711-3087

TXU Energy

-4-

Electronic distribution by RIV:

Regional Administrator (EWM)

DRP Director (ATH)

DRS Director (DDC)

Senior Resident Inspector (DBA)

Branch Chief, DRP/A (WDJ)

Senior Project Engineer, DRP/A (CJP)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (NBH)

Scott Morris (SAM1)

CP Site Secretary (LCA)

DAPowers (DAP)

SRI:EMB

NRR

C:EMB

C:PBA

D:DRS

WCSifre/lmb

EMurphy

CSMarschall

WDJohnson

DDChamberlain

/RA/

/RA/

/RA/

/RA/

/RA/ by DAP

12/19/02

12/19/02

12/30/02

12/30/02

01/09/03

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-445

License:

NPF-87

Report No.:

50-445/02-09

Licensee:

TXU Energy

Facility:

Comanche Peak Steam Electric Station, Unit 1

Location:

FM-56

Glen Rose, Texas

Dates:

October 7 through November 1, 2002, onsite

Team Leader

W. C. Sifre, Senior Reactor Inspector

Engineering and Maintenance Branch

Inspector:

E. Murphy, Senior Materials Engineer

Materials and Engineering Branch

Office of Nuclear Reactor Regulation

Accompanying

Personnel:

C. Dodd, Consultant

Approved By:

Charles S. Marschall, Chief

Engineering and Maintenance Branch

Division of Reactor Safety

-2-

SUMMARY OF FINDINGS

IR 05000445-02-09; TXU Energy; on 10/07-11/01/2002; Comanche Peak Steam Electric

Station; Unit 1, Special Inspection.

The inspection was conducted by a team of three inspectors, one regional inspector, one

headquarters inspector, and one contractor. The inspection identified three findings. Two of

the findings are characterized as a noncited green violation and one is characterized as an

apparent violation of NRC regulatory requirements. The significance of this apparent violation

has yet to be determined; therefore, the finding remains unresolved. The risk significance of

the apparent violation remains unresolved. The significance of issues is indicated by their color

(green, white, yellow, red) and will be determined using the Significance Determination Process

described in NRC Inspection Manual Chapter 0609. The NRCs program for overseeing the

safe operation of commercial nuclear power reactors is described in NUREG 1649, "Reactor

Oversight Process," Revision 3, dated July 2000.

A.

Inspector-Identified Findings

Cornerstone: Barrier Integrity

TBD. A failure to identify and correct a clearly detectable steam generator tube flaw indication

during eddy current examinations in the 2001 refueling outage (1RF08) resulted in the tube

remaining in service until it leaked in September of 2002. This is an apparent violation of

10 CFR Part 50, Appendix B, Criterion XVI.

The risk significance of the finding is unresolved pending completion of a significance

determination. This finding is greater than minor because it degraded the ability to meet the

cornerstone objective with reactor coolant system leakage. The finding had potential for

greater than very low safety significance because the tube failed the in situ testing, indicating

that it would not have met the design basis requirements for withstanding analyzed

transients. (Section 02.01)

GREEN. Inspectors identified a non-cited violation of 10 CFR Part 50, Appendix B,

Criterion XVI for two examples of failure to perform adequate steam generator eddy-current

examination in the 2002 refueling outage (1RF09). The inadequate examinations resulted in

analyst failure to properly characterize two steam generator tube flaws until the licensee took

corrective actions in response to questions from the NRC inspectors.

This finding is greater than minor because it degraded the ability to meet the cornerstone

objective of reactor coolant system pressure boundary. The failure to identify the flaws could

have resulted in flawed tubes that might have developed leaks if left in service. The

significance of this finding is very low because the in situ tests demonstrated that the tubes

would have met the design basis requirements for withstanding analyzed transients, and prior

to returning the plant to operation the licensee removed the flawed tubes from service

(Section 02.02).

Report Details

SPECIAL INSPECTION ACTIVITIES

01

Inspection Scope

The team conducted a special inspection in response to a primary-to-secondary leak

that began on September 26, 2002, and the resultant shutdown on September 28, 2002.

The team also reviewed the associated steam generator inspections. The team used

Inspection Procedure 93812, Special Inspection Procedure, to evaluate the

effectiveness of the examination methods used to examine the degraded tube during

the previous outage, and determine whether licensee evaluators missed an opportunity

to identify the degraded tube during the previous outage. The team also evaluated the

effectiveness of the examination methods used during the current outage as it related to

detecting flaws similar to that in the leaking tube. The team assessed the effectiveness

of this approach in precluding the recurrence of this type of event. During the

inspection, the team developed a complete sequence of events related to the primary-

to-secondary leak first identified on September 26, 2002. The team also reviewed the

licensee personnels root cause evaluation for completeness and accuracy, and

Independently verified key assumptions and facts of that evaluation.

In addition, the team evaluated the corrective actions and ensured that the extent of

condition was evaluated.

The team reviewed procedures, logs, and corrective action documents. The team also

reviewed the steam generator eddy current data, and interviewed key personnel,

including eddy current analysts.

02

Special Inspection Areas

02.01 Overview of Shutdown and Sequence of Events

a.

Inspection Scope

The inspectors reviewed the licensees response to the steam generator tube leak and

verified that appropriate actions were taken.

b.

Findings

On September 26, 2002, Comanche Peak, Unit 1, was at 99 percent reactor power,

coasting down with the refueling outage scheduled to begin on October 5. At 5:41 a.m.

the Unit 1 control room received a condenser off-gas alarm, Condenser Off-Gas-182,

with a reading of 4.92E-6 uCi/mL. The alarm setpoint was 4.86E-6 uCi/mL and the

licensee determined by review of the data that the parameter had been running close to

the setpoint for the previous 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. Operators notified the chemistry technicians. At

12:43 p.m. the Condenser Off-Gas 182 alarm actuated with a reading of 6.07E-6 uCi/mL

and the No. 2 steam generator main steam line N-16 monitor went into alarm. A

correlation curve reflecting the theoretical equation for the condenser off-gas monitor

was created by chemistry and distributed to the control room. The condenser off-gas

alarm setpoints were adjusted to reflect 30 gallons per day (gpd) and 40 gpd,

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respectively. At 30 gpd, the plant would enter Action Level 1 in accordance with

Procedure ABN-106 and administrative limits. At 40 gpd, maintained for greater than

1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br />, management decided the plant should shut down in a controlled manner. At

10:24 p.m., the N-16 alarm cleared and the reading continued to trend downward.

On September 27, 2002, at 12:19 a.m., the Condenser Off-Gas 182 alarm cleared. At

10:25 a.m., the N-16 alarm returned at an estimated 5.00 gpd. At 10:40 a.m., the

Condenser Off-Gas 182 alarm came in with 9.81E-6 uCi/mL followed by the Condenser

Off-Gas 182 Hi alarm at 10:51 a.m. with a reading of 1.17E-5 uCi/mL. At 1:06 p.m.,

these alarms cleared and peak readings were determined to be 12.8 gpd. These alarms

came in twice more on this day. At 7:54 p.m., the Condenser Off-Gas 182 alarm

reached a peak value of 1.7E-5 uCi/mL and at 10:32 p.m., the Condenser Off-Gas 182

HiHi alarm was greater than the 40 gpd limit at 1.8E-5 uCi/mL. The alarms cleared in

less than an hour so that the shutdown criteria established by licensee management

was not exceeded.

On September 28, 2002, at 1:40 a.m., the Unit 1 control room operators commenced

power reduction in response to the 1-02 steam generator tube leak. The operators

target was to be off-line in 2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br />. The Unit 1 control room operators entered

Section 3.0 of Procedure ABN-106. At 3:12 a.m., the Unit 1 control room operators

performed a planned trip of the Unit 1 reactor and entered Mode 3.

Subsequent inspection and testing by the licensee determined the source of the leakage

to be a stress corrosion crack initiating from the outer diameter surface in the u-bend

region of Tube R41C71 of Steam Generator 2. The licensee also determined through

pressure testing that the tube failed to exhibit structural and accident leakage integrity

margins consistent with the plant design and licensing basis.

02.02 Effectiveness of Previous Examinations

c.

Inspection Scope

The team independently reviewed eddy current test data from the previous (1RF08)

inspection in 2001 for the specific tube location where the leakage developed in

September 2002. The team also reviewed the Comanche Peak, Unit 1, Steam

Generator Eddy Current Analysis Guidelines for Refueling Outage 1RF08, Revision 0.

d.

Findings

Introduction. An apparent violation with risk to be determined was identified in that the

licensee failed to identify and correct a degraded steam generator tube during Refueling

Outage 1RF08 and this failure directly resulted in a steam generator tube leak.

Description. The eddy current test techniques employed for Refueling Outages 1RF08

and 1RF09 included bobbin coil inspections of the tube from end-to-tube end and plus-

point coil inspections at special interest locations described in additional detail below.

Data analysis was performed in accordance with the Comanche Peak, Unit 1, steam

generator eddy current analysis guidelines. The guidelines provided for independent

analysis of all data by a primary analyst team and a secondary analyst team. A

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resolution analyst was responsible for resolving differences noted between the primary

and secondary analysis reports. Two independent resolution analysts from the two

analysis teams had to concur before changing an indication of degradation to a

non-reportable status, which would not require further examination. Differences

between the resolution analysts were resolved by the overall lead analyst with the

concurrence of the licensees Level III analyst. In addition, a Level III qualified data

analyst sampled data to ensure that primary, secondary, and resolution analyst

equipment setups were correct and that discrepancy resolutions were performed

properly and the calls were correctly dispositioned.

The primary data analysis was performed by a computerized automatic data screener.

The automatic data screener was a program that had been qualified to the same

standards as the human analysts; i.e., Appendix G of the EPRI Steam Generator

Examination Guidelines and the site-specific performance demonstration. The program

used a rule base established by the licensee that incorporated the indication reporting

criteria in the eddy current analysis guidelines. For each tube, the automatic data

screener listed indications that satisfied the rule base. Each of these indications was

manually dispositioned as part of the primary analysis process.

Freespan indications found by the primary or secondary analysts, and upheld during

data resolution, were designated as freespan differential signals. A history check was

then performed by the resolution analysts to identify a change in the signal response

over time. Those freespan differential signals that satisfied the guideline change criteria

were considered to be potential flaw indications and were assigned an I-code. In the

analysis guidelines for Refueling Outage 1RF08, the change criteria were a change in

the phase angle response greater than 15 degrees, a 0.5 volt change in amplitude, or

no prior indication over the last two cycles. If associated with a ding or dent, the change

criteria was 10 degrees or no prior indication. A ding refers to localized tube wall

deformation at locations between supports. A dent refers to localized wall deformation

at tube support locations. All locations with an I-code were required to be inspected with

a plus-point probe. All tubes with I-codes confirmed by plus-point were required to be

plugged or repaired.

The teams review found that a clearly detectable indication was present at the leak

location during the previous outage (1RF08) inspection in 2001. The flaw indication was

in Tube R41C71 in Steam Generator 2. This indication measured 0.96 volts at 130 kHz

with a phase angle of 93 degrees and 1.79 volts at 300 kHz with a phase angle of 122

degrees. The indication was outside (did not meet) the reporting criteria in the Refueling

Outage 1RF08 analysis guidelines and was not reported by either the primary or

secondary analyst in 2001.

The applicable reporting criteria during Refueling Outage 1RF08 for freespan bobbin

indications in the absence of a dent or ding signal was a phase angle response

corresponding to 0 percent through wall; i.e., a phase angle response of 84 degrees on

the 130 kHz channel and 118 degrees on the 300 kHz channel. The presence of a dent

or ding signal would cause a flaw signal to rotate out of the normal phase angle window.

-4-

In the presence of a detectable ding signal, the applicable reporting criterion was a

phase angle response of at least 155 degrees on the 130 kHz channel. In the presence

of a detectable dent signal, a distortion of the signal on the 550/130 kHz mix channel

was reportable.

Dings and dents are reportable if they equal or exceed 2 volts on 550 kHz channel for

dings or the 300/130 kHz mix channel for dents. Although dings and dents are not

themselves reportable at less than 2 volts, the flaw indication reporting criteria are

subject to the wider phase angle reporting window for dent/ding locations if dings or

dents are detectable, irrespective of whether the ding or dent exceeds 2 volts.

No ding signal was reported at the flaw location during Refueling Outage 1RF08 by the

primary or secondary analysts. The 0 percent through-wall phase angle criteria was

applied to the 130 and 300 kHz signal. This indicated that the analysts did not see

evidence of a ding signal, irrespective of voltage. The team agreed that there is no

clear evidence of a ding in the Refueling Outage 1RF08 signal response. However, the

team observed a large amount of horizontal noise (about 1.75 volts at 550 kHz)

attributable to probe wobble, which could easily mask a 2 volt ding signal.

The team found that the analysis guidelines provided discretion that may be exercised

by the human analysts when interpreting the signals. Paragraph 1.3 of the TXU eddy

current guidelines stated:

The guidance on signal interpretation is not intended to restrict the

analysts. Conditions encountered which are not clearly addressed in the

guidelines shall be brought to the attention of the lead analyst and the

TXU Eddy Current Level III for concurrence and inclusion into the

guidelines. No deviation from the current guidelines is permitted.

Paragraph 6.4.3 of the guidelines stated, in part,

However, signals may be observed that act like flaws yet cannot be

quantified due to signal distortion . . . In such a case, one of the

appropriate I-codes may be used to characterize the indication.

The team concluded that an experienced analyst should recognize that the large wobble

signal could mask a dent that could distort or rotate an indication outside the reportable

phase angle response criteria. In such a case, the guidelines enabled the analyst to

bring the indication to the attention of the lead analyst and the TXU Level III analyst and

for assigning an I-code. The team determined that the analyst should have recognized

the large wobble signal and should have assigned an I-code.

The team concluded that the following factors contributed to the failure to detect the flaw

indication during Refueling Outage 1RF08:

1.

The probe wobble signal masked a ding signal at the flaw location.

-5-

2.

Non-conservative reporting criteria were applied to the flaw signal. As a result,

the ding signal was not identified.

3.

The primary analysis was strictly rule based (being computerized) and, thus, had

no opportunity to exercise discretion in calling the indication.

4.

The secondary analyst failed to report the indication, which was readily apparent.

It appeared that the analyst dismissed the indication based on strict application

of the guideline reporting criteria for non-dinged locations and failed to recognize

that the large wobble signal could potentially mask dings, which could rotate the

indication outside the reportable phase angle response criteria.

The direct consequence of failure to detect the flaw in Tube R41C71 during Refueling

Outage 1RF08 was that the tube was not removed from service and, therefore,

subsequently degraded to the point that it leaked and no longer satisfied the applicable

tube integrity performance criteria. This occurred because the examination methods

used during Refueling Outage 1RF08, including the analysis guidelines, were not

effective for ensuring that tubes would maintain their integrity until the next scheduled

inspection. The team also concluded that the guideline phase angle reporting criteria

were inappropriate in the u-bend region where the high potential existed for large probe

wobble signals, which may mask the presence of dents or dings.

Analysis. The finding is greater than minor because it adversely affected the reactor

safety barrier integrity cornerstone and degraded the ability to meet the cornerstone

objective of controlling reactor coolant system leakage. The finding also was

determined to have potential safety significance greater than very low significance

because it resulted in a steam generator tube leak and the tube failed in situ testing,

indicating that it would not have met the design basis requirements for withstanding

analyzed transients. The final risk determination is pending evaluation using the

Significance Determination Process described in NRC Inspection Manual Chapter 0609.

Enforcement. The team concluded that for the reasons stated above, the licensee

clearly missed an opportunity to have identified the indication during the previous

inspection. The failure to identify and correct the degraded tube during Refueling

Outage 1RFO8 is an apparent violation of 10 CFR Part 50, Appendix B, Criterion XVI

(APV 50-445/0209-01). The licensee has documented this issue in Smart

Form SMF-2002-003142-00. The risk significance of this apparent violation remains

under review by the NRC.

02.03 Effectiveness of Current Examinations

a.

Inspection Scope

The team reviewed the scope of the licensees Refueling Outage 1RF09 inspection

program and the results obtained. Primary attention was directed to the effectiveness of

the licensees inspection program for detecting freespan cracks such as the one in

Tube R41C71 that was missed during the previous inspection during Refueling

-6-

Outage 1RF08. The team also reviewed the Comanche Peak, Unit 1, Steam Generator

Eddy Current Analysis Guidelines for Refueling Outage 1RF09, Revision 4.

b.

Findings

Introduction. A Green noncited violation of 10 CFR Part 50 Appendix B, Criterion XVI,

was identified for two examples of failure to identify steam generator tube flaw

indications.

Description. The Refueling Outage 1RF09 steam generator inspection program

included a full length bobbin coil examination of all tubes in all steam generators. All

locations where I-codes were found by the bobbin coil examinations were subsequently

examined by plus-point probes. For freespan I-codes, the extent of plus-point

inspection was from the nearest support structure (e.g., tube support plate or anti-

vibration support) on one side of the flaw to the nearest support structure on the other

side of the flaw. Additional plus-point inspections were performed for freespan cracks at

the following special interest locations:

All tube spans between adjacent supports containing greater than 5 volt dents or

dings.

A 20 percent sample of u-bend spans between adjacent supports containing

greater than 2 volt dents/dings.

A 20 percent sample of spans between adjacent supports containing bobbin

freespan differential signals, irrespective of whether they were dispositioned as

I-codes based on history review.

A 100 percent sample of spans between adjacent supports containing freespan

differential signals in u-bends.

Revision 4 of the Comanche Peak, Unit 1, steam generator eddy current analysis

guidelines was utilized for the Refueling Outage 1RF09 initial inspection program. As

corrective action to preclude missing flaws, such as Tube R41C71 in Refueling

Outage 1RF08, Revision 4 included the following key changes to the Refueling

Outage 1RF08 inspection.

The phase angle reporting criteria for freespan indications in the absence of

dings/dents was changed to require only that the 130 kHz signal phase angle

response be less than 160 degrees.

A new reporting criterion added that freespan indications in the absence of

dings/dents exhibit a 20 to 200 degree phase angle response at 550 kHz.

The phase angle change criterion for historical review for freespan differential

indications not associated with dings/dents was changed from 15 to 10 degrees.

In addition, wording was clarified that a two cycle look back is required.

-7-

The rule base for the primary analysis auto data screener was updated to reflect the first

two changes above. The third change only affected the resolution process. The team

witnessed application of the auto data screener with the Revision 4 guideline rule base

to Refueling Outages 1RF07 (1999) and 1RF08 (2001) raw bobbin data at the leak

location. In both cases, the auto data screener identified a freespan differential

indication at the location, which eventually leaked prior to Refueling Outage 1RF09.

The licensees inspection program identified 20 single axial indications, including the

leaker, affecting 11 tubes. The single axial indications fell into two different categories.

The first category included 11 single axial indications (including the leaker), affecting

9 tubes, located between the uppermost hot-leg support (H10) and the uppermost

cold-leg support (C10) including the u-bend region. All except 1 of these indications

were associated with a detectable ding or dent. With the exception of the leak

indication, these indications were short and exhibited low voltage responses, indicating

that they had little structural significance.

The second category included 9 single axial indications affecting 2 tubes, R11C42 in

Steam Generator 2 and R7C17 in Steam Generator 3. These indications were not

associated with detectable dings or dents. They appeared to be oriented end-to-end

along a straight line with some axial distance between them.

The team identified the following concerns with the effectiveness of the inspection:

The secondary analyst failed to identify half of the single axial indications

confirmed with the plus-point coil and not involving greater than 5 volt dents or

dings.

Similarly, half of the single axial indications not associated with greater than

5 volt dents had not been detected during the primary analysis of the bobbin

data. In general, these indications exhibited bobbin coil amplitude responses

less than 0.2 volts. The auto data screener is set up to identify only indications

with amplitude responses above 0.2 volts. The secondary human analysis was

not subject to an amplitude reporting criteria. In one case, the auto data

screener did report a freespan differential indication, but it was inexplicably

deleted by the analyst who prepared the primary analysis report.

Eight of the single axial indications were not identified as freespan differential

indications by either the primary or secondary analysts. These were found

fortuitously rather than by programmatic implementation. The single axial

indications were found only because the licensee performed a plus-point

examination to address a freespan differential indication or large voltage dent

found elsewhere in the same span.

Of particular concern to the team was a long single axial indication at 10.7 inches above

the H5 hot-leg support in Tube R11C42 of Steam Generator 2. This indication was

missed by both the primary and secondary analysts. The indication was 1.6 inches in

-8-

length with a maximum voltage response of 0.26 volts. Depth estimates involve

significant uncertainties for low voltage indications such as this. The measured depth at

the location of the maximum voltage response was 64 percent through wall based on

phase angle. The licensee is required to plug tubes with flaw indications greater than

40 percent through wall.

The failure of the licensee analysts to identify this indication is the first example of a

violation of 10 CFR Part 50, Appendix B, Criterion XVI. Based on the licensees

corrective actions (documented in SMF-2002-003142-00), including pressure testing

and removal of the affected tube from service, this violation is being treated as a

noncited violation consistent with Section VI.A of the NRC Enforcement Policy

(NCV 50 445/0209 02).

To address the missed indication and to ensure that no additional indications were

missed, the licensee elected to perform a complete manual re-analysis of the bobbin coil

data.

Training of participating analysts was focused on the bobbin coil signals associated with

the freespan single axial indications found by plus point probes during the initial data

analysis. Particular attention was directed to the long freespan indications found in

Tubes R11C42 and R7C17, including those missed by the secondary analysts.

The licensee prepared Revision 5 of the steam generator eddy current analysis

guidelines to support the review. Revision 5 added the 300 kHz channel to the channels

to be screened for a differential response. It also required complete history reviews

during resolution. These reviews were now required to extend back to the first inservice

inspection for the subject tube.

To increase confidence in the effectiveness of the analysts, the licensee also inserted

Judas Tube signals into the data stream. A Judas Tube was a tube with known long

single axial indications. The signals from this tube were inserted randomly into the

actual data stream being analyzed. Presumably, the success of the analysts in

detecting the Judas Tube signals from among the actual data under evaluation provided

insight into the ability of the analysts to find similar indications from among the actual

data. Signals for two Judas Tubes were inserted into the data stream. These signals

were the 2002 (1RF09) and 2001 (1RF08) signals for the tube that was missed

(R11C42). The analysts detected the three largest amplitude signals on the tube, which

included the indication that was missed by both the primary and secondary analysts

during the initial data analysis program and that was of particular concern to the team as

previously discussed. The team concluded that the use of the Judas Tube signals had

the additional benefit of heightening the alertness of the data analysts to potential

freespan indications.

-9-

Tube R11C42 was one of two tubes pulled during Refueling Outage 1RF09 for

laboratory testing and examination. Burst testing was completed for this tube at about

the time the review was nearing completion. Preliminary information from the test was

that the burst pressure was 8200 psi. The team concluded that this result provided

further confidence that the analysts were capable of identifying free span cracks well

before they become structurally significant.

Subsequent analysis led to the finding of additional freespan differential indications and

I-codes. Plus-point examination of the I-codes identified six additional tubes with single

axial indications. Three of these tubes were found to contain relatively short single axial

indications at ding locations. The other three tubes contained long single axial

indications or arrays of single axial indications not associated with detectable dents or

dings. One of these tubes, R7C90, was found to contain a 15-inch long array of single

axial indications above the H1 support, and four single axial indications above the

H3 support. Only the largest single axial indication in each of the spans was identified

as a freespan differential indication and designated as an I-code during the third

resolution process. The single axial indications in these spans not identified by the third

analysis were very small amplitude indications (0.1 volts or less), less significant than

some of the single axial indications found in Tube R11C42, which exhibited a high,

8200 psi, burst pressure.

However, the results for the other two tubes with long single axial indications, R7C117

and R4C51 in Steam Generator 3, raised a new issue regarding the effectiveness of the

data resolution process at Comanche Peak. For Tube R7C117, the third analysis

identified a freespan differential indication at 8.6 inches above the H8 support. The

history review confirmed a change in signal and an I-code was assigned. The team

observed, however, that both the primary and secondary analysts had previously

identified a freespan differential indication at this location during the original Refueling

Outage 1RF09 analysis. The resolution process at that time failed to identify a change

in signal relative to 1999 in excess of the specified change criteria and thus, no I-code

was assigned and no plus point probe examination was performed.

Based on a review of the data, the team found that the change in indication since 1999

was clearly observable. The plus-point examination following the third analysis revealed

a relatively large single axial indication with a maximum voltage response of 0.82 volts.

The single axial indication measured over 2.5 inches in length with a depth of 62 percent

through wall at the peak voltage location based on measured phase angle. Amplitude-

based depth measurements ranged as high as 85 percent through wall. This tube was

in-situ pressure tested and successfully sustained three times normal operating

differential pressure (4070 psi) without burst or leakage. The team observed that there

is little basis for confidence that the pressure capacity of this tube was much above

4070 psi or that the tube would have continued to meet the 3 delta P criterion until the

next refueling outage, given the uncertainty of the depth measurements. The licensees

representatives stated their intent to conduct additional testing of the tube and provide

the results to the inspectors when they become available.

-10-

For Tube R4C51, freespan differential indications were identified during the third

analysis at three locations above the H9 support. Each of these was designated during

resolution as an I-code, and plus-point examination revealed single axial indications at

each location. The team observed, however, that freespan differential indications had

been identified at two of these locations by the primary analyst during the original

Refueling Outage 1RF09 analysis. The resolution analyst had overruled one of these

calls as no detectable degradation and had determined that the other had not indicated

a change since 1999 in excess of the change criteria.

The failure of the licensee analysts to identify these indications is a second

example of a violation of 10 CFR Part 50, Appendix B, Criterion XVI. Based

on the licensees corrective actions (documented in SMF-2002-003142-00),

including removal of the affected tube from service, this violation is being treated as

a noncited violation consistent with Section VI.A of the NRC Enforcement Policy

(NCV 50-445/0209-02).

It was the team's opinion that the third analysis was effective in providing confidence

that potentially significant indications were brought to the attention of the resolution

analysts. However, the third analysis raised a new issue with respect to the

effectiveness of the resolution process to ensure that potential freespan indications

stemming from the front line analysis were addressed. In particular, there was concern

regarding the effectiveness of the historical review for changes relative to the change

criteria.

The team discussed the concern with the licensee's representatives. To address the

concern, the licensee elected to perform a new, supplemental history review of all

freespan differential indications from the third analysis.

The licensee prepared guidelines for the supplemental history review, which were

reviewed by the team. These guidelines incorporated a number of improvements, which

the team considered to significantly improve the effectiveness of the analysis in

identifying signals that were potentially changing since the first inservice inspection.

These guidelines called for the historical reviews to be performed by two qualified data

analysts working together as a team. The analysts were to consider all available data,

including the low frequency absolute channel. This reflected a lesson learned from

Tube R7C112 in Steam Generator 3, which showed a clear change in the absolute

signal. Analysts were instructed not only to identify indications with changes exceeding

the specified change criteria, but to identify any indication with a change which, in their

experience and judgement, was beyond that associated with normal eddy current

repeatability. The inspectors considered this change a significant improvement.

The team concluded that this review adequately evaluated each of the freespan

differential signals identified during the third analysis.

Analysis. This finding is greater than minor because it is associated with reactor

coolant system barrier integrity and degraded the ability to meet the cornerstone

objective. The failure to identify the flaws could have resulted in flawed tubes that may

have developed leaks if left in service. The risk significance of this finding is very low

-11-

because the in situ tests demonstrated that the tubes would have met the design basis

requirements for withstanding analyzed transients, and prior to returning the plant to

operation the licensee removed the flawed tubes from service.

Enforcement. The failures of the licensee analysts to identify the significant

indications are a violation of 10 CFR Part 50, Appendix B, Criterion XVI. Based on

the licensees corrective actions (documented in SMF-2002-003142-00) including

removal of the affected tubes from service, this violation is being treated as a

noncited violation consistent with Section VI.A of the NRC Enforcement Policy

(NCV 50-445/0209-02).

02.04 Evaluation of Licensees Root Cause Evaluation

a.

Inspection Scope

The licensee performed root cause evaluations from two standpoints. First was the

assessment of root cause from a crack mechanistic standpoint - why the crack

occurred. Second was a root cause evaluation from a programmatic standpoint - why

wasnt the crack detected and the tube removed from service before the leak occurred

and before the tube integrity performance criteria were no longer satisfied. These

evaluations were in progress while the team was onsite. The team reviewed DRAFT

versions of both evaluations.

b.

Findings

1.

Mechanistic Root Cause

The general root causes of stress corrosion cracking are well documented in

industry literature and include having a material that is susceptible to stress

corrosion cracking, the presence of stress in the material, and an aggressive

environment. Each of these causal factors are known to be present for all PWR

steam generators, particularly those employing Inconel Alloy 600 mill-annealed

tubing as is the case for Comanche Peak Unit 1. The aggressiveness of the

cracking, in terms of time to crack initiation and crack growth rate, can be

aggravated by the presence of residual stress or off-normal stress associated

with dings, dents and scratches, material micro-structure, and secondary water

chemistry.

One potential source of information concerning factors that may have hastened

the onset of freespan cracking at Comanche Peak would be a removed tube

sample containing the section of tubing with the leaking flaw. Because of the

u-bend location of the leaking flaw, the licensee could not remove it for additional

testing. However, sections for two other flawed tubes, i.e., R11C42 and

R25C30, were pulled for laboratory analysis and may provide insights on causes

for the cracking. The pulled tube samples were found by inspection to contain

freespan cracks.

-12-

The license observed that the leaking flaw was located at a ding, which was

apparent on the plus-point scan. Dings and dents are local deformations of the

tube wall which lead to increased local stress levels. Dings are thought to be

incurred during the tube fabrication and installation process. By contrast, dents

occur due to the buildup of magnetite in crevices between the tubing and carbon

steel support plates. Crack initiation at ding and dent locations has been noted

by power reactor licensees.

The licensee had not reached a conclusion about the cause of the leak based on

available information. The licensees representatives stated that they would

provide the inspectors with the final root cause determination based on further

evaluation when it becomes available.

2.

Programmatic Root Cause

The team reviewed a number of licensee draft documents that address the

leaking flaw and why it had been missed in Refueling Outage 1RF08 steam

generator inspections in 2002. These documents included:

A draft document entitled, Anatomy of an Event, reviewed error

precursors, flawed defenses, and latent organizational weaknesses that

could have prevented the missed indication.

A draft document entitled September 2002 Unit 1 Primary to Secondary

Leakage Summary Report.

A note prepared by Steve Swilley (TXU) entitled Comments about

1RF08 Inspection Practices and Application of Ding Technique.

These documents identified the following contributing factors:

The probe wobble signal masked a ding signal at the flaw location.

The unseen ding signal caused the flaw signal to be distorted (rotated)

beyond the phase angle reporting criteria which was applicable to non-

dinged locations. The inspectors considered this criteria non-

conservative for dinged locations.

The primary analysis was rule-based (being computerized). Because the

primary analysis failed to identify the dent, the reporting criteria for non-

dinged locations was applied. Since the dent rotated the flaw beyond this

criteria the analyst did not identify it.

The secondary analyst failed to report the indication.

Although the team agreed with the above contributing factors, the team identified

the following important contributing factors:

-13-

Human error: The secondary analyst failed to report the indication which

was readily apparent. The team determined that the analyst should have

reported the indication. It appears likely the analyst dismissed the

indication based on strict application of the guideline reporting criteria for

non-dinged locations and failed to recognize that the large wobble signal

could potentially mask dings which could rotate the indication outside the

reportable phase angle response criteria.

Procedural inadequacy: The phase angle reporting criteria for freespan

cracks in the absence of dings or dents was inappropriate for two

reasons. One, the reporting criteria for dings and dents was 2 volts.

Dent and ding signals of less than 2 volts can distort or rotate a flaw

indication beyond the phase angle reporting criteria. Two, a large probe

wobble response capable of masking dent and ding signals up to 2.5

volts is an expected condition in the u-bend region. This procedural

inadequacy directly caused the flaw indication to be missed by the

primary automatic data screening analysis because it was entirely rule

based. The human (secondary) analyst applied this guideline criterion

directly and literally. The Figure 3 analysis flow chart in the Refueling

Outage 1RF09 steam generator eddy current analysis guidelines

provided no specific word of caution about the potential for probe wobble

to distort the flaw indication, rendering the reporting criterion

inappropriate. The team determined that procedure established

unnecessarily conservative criteria for reporting flaws.

02.05 Evaluation of Licensees Corrective Actions

a.

Inspection Scope

The inspectors reviewed the licensees corrective actions in response to the steam

generator tube leak.

b.

Fingings

The corrective actions implemented by the licensee have been previously discussed in

this inspection report and involved three sets of actions as follows:

The first set of actions was taken in direct response to the tube leak, and

included opening up the phase angle window reporting criteria to ensure that all

potential distorted indications would be subject to the resolution process for

determination of whether an I-code should be applied to the indication.

The second set of actions was taken in response to team concerns that (1) many

freespan indications were too low in amplitude to be detected by the primary

analysis automatic data screener and (2) that several freespan indications, found

fortuitously by plus-point examination, had been missed by the secondary

(human) analyst. This second set of actions included an independent third party

review of the raw bobbin coil examination data by human analysts who had

-14-

undergone training to sensitize them to the kinds of signals which had been

missed during the original inspection program.

The third set of actions was taken in response to team concerns regarding the

effectiveness of the data resolution analyses implemented during the original

inspection program and third analysis. In particular, the team was concerned

that the history review analyses were not adequately identifying indications,

which had undergone significant change and warranted an I-code designation.

This third set of actions included analysis history reviews for all freespan

differential signals that had not received an I-code designation during the third

analysis.

The second and third sets of corrective actions were taken by the licensee to resolve

NRC concerns. Although these actions did not reveal any additional tubes failing to

meet the tube integrity performance criteria, one indication was found (in Tube R7C112)

during the third analysis that could have challenged the tube integrity criteria during the

next operating cycle as discussed in detail earlier in this report. Thus, the team found

that the licensees corrective action program in response to the leaking tube and

implemented during the original Refueling Outage 1RF09 inspection program (i.e., the

first set of corrective actions) was initially not adequate to establish the extent of

condition and to support operation during the next operating cycle. In response to staff

concerns, additional corrective actions were taken (i.e., the second and third sets of

corrective actions) which led to the finding of several additional freespan indications

including the significant indication in Tube R7C112.

The team found that the corrective actions listed above established a high confidence

that significant indications, which could potentially challenge the tube integrity

performance criteria early in the next cycle were identified and the subject tubes

plugged or repaired. The inspectors considered these corrective actions acceptable.

The licensee will perform an operational assessment to establish that there is a

sufficient bases to operate to its next scheduled refueling outage. This operational

assessment may need to be revised or updated when the results of the tube pull

examinations become available sometime in early 2003.

The team will review the results from the pulled tube examination and the licensees

operational assessment as follow up actions when the results become available.

04

Exit Meeting Summary

The team leader and NRC management representatives presented the special

inspection results to Mr. C. L. Terry, and other members of licensee management on

December 10, 2003, during a public exit meeting. No proprietary information was

identified.

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

S. Lakdawala, Engineering Programs Manager

B. Mays, Smart Team 1 Systems Manager

D. Snow, Senior Nuclear Specialist

M. Sunseri, System Engineering Manager

S. Swilley, Steam Generator Program Manager

C. Terry, Senior Vice President and Principal Nuclear Officer

NRC

D. Allen, Senior Resident Inspector

A. Sanchez, Resident Inspector

ITEMS OPENED AND CLOSED

Opened

50-445/02-09-01

APV

Failure to Identify and Correct a Degraded Steam Generator Tube

during Refueling Outage 1RFO8 (Section 02.01).

Opened and Closed

50-445/02-09-02

NCV

Two Examples of Failure to Identify and Correct Steam Generator

Tube Flaws (Section 02.02).

PARTIAL LIST OF DOCUMENTS REVIEWED

Comanche Peak Unit 1 Steam Generator Eddy Current Analysis Guidelines for 1RF08,

Revision 0

Comanche Peak Unit 1 Steam Generator Eddy Current Analysis Guidelines for 1RF09,

Revision 4

Comanche Peak Unit 1 Steam Generator Eddy Current Analysis Guidelines for 1RF09,

Revision 5

Comanche Peak Unit 1 Steam Generator Eddy Current Analysis Guidelines for 1RF09,

Revision 6

Westinghouse Vendor Procedure STD-FP-1996-7928, Field Procedure for In Situ Testing of

3/4" Steam Generator Tubes

-2-

Contractor NDE Procedures:

TX-ISI-008, VT-1 and VT-3 Visual Examination, Revision 5.

TX-ISI-011, Liquid Penetrant Examination for Comanche Peak Steam Electric Station,

Revision 7.

TX-ISI-070, Magnetic Particle Examination, Revision 6.

TX-ISI-214, Ultrasonic Examination Procedure for Welds in Piping Systems and Vessels,

Revision 2.

TX-ISI-301, Ultrasonic Examination of Ferritic Piping Welds, Revision 1.

TX-ISI-302, Ultrasonic Examination of Austenitic Piping Welds, Revision 1.