ML021960501

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IR 05000298-02-008, on 5/18-24/2002, Nebraska Public Power District, Cooper Nuclear Station, Special Team Inspection Report. Corrective Actions, Event Response
ML021960501
Person / Time
Site: Cooper Entergy icon.png
Issue date: 07/15/2002
From: Clark J
NRC/RGN-IV/DRP
To: Denise Wilson
Nebraska Public Power District (NPPD)
References
IR-02-008
Download: ML021960501 (22)


See also: IR 05000298/2002008

Text

July 15, 2002

David L. Wilson, Vice President of

Nuclear Energy

Nebraska Public Power District

P.O. Box 98

Brownville, Nebraska 68321

SUBJECT:

COOPER NUCLEAR STATION - NRC INSPECTION REPORT 50-298/02-08

AND APPARENT VIOLATION

Dear Mr. Wilson:

This refers to the special inspection conducted from May 18-24, 2002, at the Cooper Nuclear

Station. The purpose of the inspection was to evaluate multiple degraded conditions which

were experienced during startup from a forced outage on May 14, 2002. The enclosed report

presents the results of the inspection which were discussed on June 20, 2002, with Mr. Coyle

and other members of your staff.

This inspection was an examination of activities conducted under your license as they relate to

safety and compliance with the Commissions rules and regulations and with the conditions of

your license. Within these areas, the inspection covered examination of selected procedures

and representative records, observations of activities, and interviews with personnel.

This report discusses one issue that appears to have greater than very low safety significance.

As described in Section 2.03 of this report, this issue involved the failure to take adequate

corrective actions regarding instrument line snubber clogging, which resulted in a failure of the

reactor core isolation cooling system on May 14. The issue was assessed, using the applicable

significance determination process, as potentially being safety significant and, therefore, has

been preliminarily determined to be greater than Green. Risk significant issues represent an

increased importance to safety, which may require additional NRC inspection and potentially

other NRC action.

The issue also appears to be an apparent violation of NRC requirements of 10 CFR Part 50,

Appendix B, Criterion XVI. Title 10 of CFR Part 50, Appendix B, Criterion XVI, requires that a

licensee establish measures to assure that conditions adverse to quality are promptly identified

and corrected. The issue is being considered for escalated enforcement action in accordance

with the General Statement of Policy and Procedure for NRC Enforcement Actions

(Enforcement Policy), NUREG-1600.

Before the NRC makes a final decision on this matter, we are providing you an opportunity to

request a Regulatory Conference where you would be able to provide your perspectives on the

significance of the finding, the bases for your position, and whether you agree with the apparent

violation. If you choose to request a Regulatory Conference, we encourage you to submit your

Nebraska Public Power District

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evaluation and any differences with the NRC evaluation at least one week prior to the

conference in an effort to make the conference more efficient and effective. If a Regulatory

Conference is held, it will be open for public observation. The NRC will also issue a press

release to announce the Regulatory Conference.

Please contact Jeff Clark at (817) 860-8166 within 7 days of the date of this letter to notify the

NRC of your intentions. If we have not heard from you within 10 days, we will continue with our

significance determination and enforcement decision and you will be advised by separate

correspondence of the results of our deliberations on this matter.

Since the NRC has not made a final determination in this matter, no Notice of Violation is being

issued for this inspection finding at this time. In addition, please be advised that the number

and characterization of apparent violations described in the enclosed inspection report may

change as a result of further NRC review.

Based on the results of this inspection, the NRC also identified a finding of very low safety

significance (Green). This finding was determined to involve a violation of NRC requirements.

Because the violation was of very low safety significance, and because it was entered into your

corrective action program, the NRC is treating the finding as a noncited violation, in accordance

with Section VI.A of the NRC's Enforcement Policy. If you contest this violation, you should

provide a response with the basis for your denial within 30 days of the date of this inspection

report, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk,

Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear

Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011;

the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC

20555-0001; and the NRC Resident Inspector at the Cooper Nuclear Station facility.

In accordance with 10 CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its

enclosures will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document

system (ADAMS). ADAMS is accessible from the NRC Web site at

http://www.nrc.gov/NRC/ADAMS/index.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Jeffrey A. Clark, Chief

Project Branch F

Division of Reactor Projects

Docket: 50-298

License: DPR-46

Enclosure:

NRC Inspection Report

50-298/02-08

Nebraska Public Power District

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cc w/enclosure:

Michael T. Coyle

Site Vice President

Nebraska Public Power District

P.O. Box 98

Brownville, Nebraska 68321

John R. McPhail, General Counsel

Nebraska Public Power District

P.O. Box 499

Columbus, Nebraska 68602-0499

D. F. Kunsemiller, Risk and

Regulatory Affairs Manager

Nebraska Public Power District

P.O. Box 98

Brownville, Nebraska 68321

Dr. William D. Leech

Manager - Nuclear

MidAmerican Energy

907 Walnut Street

P.O. Box 657

Des Moines, Iowa 50303-0657

Ron Stoddard

Lincoln Electric System

1040 O Street

P.O. Box 80869

Lincoln, Nebraska 68501-0869

Michael J. Linder, Director

Nebraska Department of Environmental

Quality

P.O. Box 98922

Lincoln, Nebraska 68509-8922

Chairman

Nemaha County Board of Commissioners

Nemaha County Courthouse

1824 N Street

Auburn, Nebraska 68305

Nebraska Public Power District

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Sue Semerena, Section Administrator

Nebraska Health and Human Services System

Division of Public Health Assurance

Consumer Services Section

301 Centennial Mall, South

P.O. Box 95007

Lincoln, Nebraska 68509-5007

Ronald A. Kucera, Deputy Director

for Public Policy

Department of Natural Resources

205 Jefferson Street

Jefferson City, Missouri 65101

Jerry Uhlmann, Director

State Emergency Management Agency

P.O. Box 116

Jefferson City, Missouri 65101

Vick L. Cooper, Chief

Radiation Control Program, RCP

Kansas Department of Health

and Environment

Bureau of Air and Radiation

1000 SW Jackson, Suite 310

Topeka, Kansas 66612-1366

Daniel K. McGhee

Bureau of Radiological Health

Iowa Department of Public Health

401 SW 7th Street, Suite D

Des Moines, Iowa 50309

William R. Mayben, President

and Chief Executive Officer

Nebraska Public Power District

1414 15th Street

Columbus, Nebraska 68601

Nebraska Public Power District

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Electronic distribution by RIV:

Regional Administrator (EWM)

DRP Director (KEB)

DRS Director (EEC)

Senior Resident Inspector (SCS)

Branch Chief, DRP/F (KMK)

Senior Project Engineer, DRP/F (JAC)

Staff Chief, DRP/TSS (PHH)

RITS Coordinator (NBH)

Jim Isom, Pilot Plant Program (JAI)

RidsNrrDipmLipb

Scott Morris (SAM1)

CNS Site Secretary (SLN)

Dale Thatcher (DFT)

R:\\_CNS\\2002\\CN2002-08RP-SCS.wpd

RIV:RI:DRS/EMB

TL:SRI:DRP/F

C:DRP/F

JFMelfi

SCSchwind

JAClark

E - JAClark

E - JAClark

/RA/

7/12/02

7/12/02

7/15/02

OFFICIAL RECORD COPY

T=Telephone E=E-mail F=Fax

ENCLOSURE

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket:

50-298

License:

DPR 46

Report:

50-298/02-08

Licensee:

Nebraska Public Power District

Facility:

Cooper Nuclear Station

Location:

P.O. Box 98

Brownville, Nebraska

Dates:

May 18-24, 2002

Team Leader:

Inspector:

Scott Schwind, Senior Resident Inspector

J. Melfi, Reactor Inspector, Engineering Maintenance Branch

Approved By:

Jeffrey A. Clark, Chief, Project Branch F

SUMMARY OF FINDINGS

Cooper Nuclear Station

NRC Inspection Report 50-298/02-08

IR 05000298/02-08; on 5/18-24/2002; Nebraska Public Power District; Cooper Nuclear Station;

Special Team Inspection Report. Corrective actions, event response.

The inspection was conducted by two team members consisting of one resident inspector and a

region-based engineering and maintenance inspector. The inspection identified one Green

issue. The significance of the issue is indicated by its color (Green, White, Yellow, Red) using

IMC 0609, "Significance Determination Process."

Cornerstone: Mitigating Systems

TBD. The licensee failed to take corrective actions to prevent clogging of instrument

line snubbers which resulted in the inadvertent isolation of the reactor core isolation

cooling system on May 14, 2002. This was an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI.

This finding was evaluated using the significance determination process. The clogging

of instrument snubbers affected the ability of the reactor core isolation cooling system to

perform its safety function. Instrument line snubbers were also installed in

instrumentation for the main steam system, the high pressure coolant injection system,

and the reactor recirculation system which could have affected the ability of those

systems to perform their safety functions. Manual Chapter 0609 requires a Phase 3

determination whenever multiple equipment may be affected by a common cause.

Therefore, further analysis of the safety significance is being performed (Section 2.03).

Green. Technical Specification 5.4.1(a) requires that the licensee establish, implement,

and maintain written procedures recommended in Regulatory Guide 1.33, Revision 2,

Appendix A, February 1978. Appendix A recommends procedures for abnormal, off

normal, or alarm conditions. The inspectors concluded that the guidance contained in

the alarm response procedure for a diesel generator fuel oil day tank low level alarm

was inadequate. Specifically, the procedure directed operators to perform incorrect

actions under a postulated condition that could have resulted in both diesel generators

being inoperable. This was determined to be a violation of Technical Specification 5.4.1(a). This violation is being treated as a noncited violation consistent

with Section VI.A of the NRC Enforcement Policy. This issue was entered into the

licensees corrective action program as Notification 10163642.

This finding was considered to have a potential impact on safety since the inadequate

procedure could result in the failure of both diesel generators following a loss of one

diesel fuel oil transfer pump. This finding was characterized by the significance

determination process as having very low safety significance since credit for recovery

was given, based on fuel consumption rates and adequate procedures to monitor fuel

consumption if both diesels were running (Section 2.04).

Report Details

SPECIAL INSPECTION ACTIVITIES

01

Inspection Scope

On May 14, 2002, Nebraska Public Power District shut down Cooper Nuclear Station

due to problems associated with the digital electrohydraulic (DEH) control system.

Several other degraded conditions were experienced during the plant shutdown and the

following 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />. These included an inadvertent isolation of the reactor core isolation

cooling (RCIC) system and the failure of a diesel generator (DG) fuel oil transfer pump.

A preliminary risk evaluation, performed in accordance with NRC Management

Directive 8.3, concluded that these concurrent conditions presented more than very low

risk. Therefore, a special inspection was performed at Cooper Nuclear Station to

evaluate the degraded conditions and immediate corrective actions and to determine

whether any potential generic safety implications existed. Specifically, this inspection

was conducted to:

1. Develop a sequence of events for the degradation/failure of each of the affected

systems.

2. Determine the adequacy of the licensee's maintenance on the affected systems

between the last outage and the current time.

3. Evaluate the effectiveness of the licensees efforts in identifying and preventing the

failures in these systems, including a review of recent corrective action program

notifications.

4. Identify the extent of effects of the degraded systems, including similar equipment in

redundant trains.

5. Identify system operability concerns that may be related to restart of the facility.

6. Assess whether the licensee's event reporting activities were in compliance with

10 CFR requirements.

7. Determine whether the conditions which existed on or about May 14, 2002, were

linked to a common performance deficiency.

02

Special Inspection Areas

02.01 Overview and Sequence of Events

On May 14, 2002, Cooper Nuclear Station was operating at approximately 20 percent

reactor power and was preparing to synchronize the main generator to the offsite

transmission grid. DEH fluid Pumps A and B were running to support startup of the

main turbine. The following sequence of events then occurred:

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5/14/2002

08:24 p.m.

Control room operators latched the main turbine.

5/14/2002

09:05 p.m.

The control room received an annunciator alarm: TURB

EH FLUID HIGH TEMP.

An operator was dispatched to investigate and found the

local temperature indication to be reading normal (155oF).

5/14/2002

09:10 p.m.

The control room received an annunciator alarm: TURB

EH FLUID SUPPLY FILTER A HIGH D/P.

An operator and engineering personnel responded to the

turbine building and reported that the differential pressure

on the DEH Pump A discharge filter was pegged high and

the differential pressure on the DEH Pump B discharge

filter was starting to increase.

5/14/2002

09:41 p.m.

The control room received an annunciator alarm: TURB

EH FLUID SUPPLY FILTER B HIGH D/P.

Electrohydraulic (EH) pressure was observed lowering

below 1800 psig and stabilized at 1550 psig.

Engineering recommended tripping the main turbine.

5/14/2002

09:44 p.m.

The control room tripped the main turbine.

5/14/2002

09:48 p.m.

The control room entered Abnormal Procedure 2.4DEH,

DEH Abnormal

5/14/2002

09:52 p.m.

Both DEH pump discharge filter differential pressure

gages were observed to be pegged high.

5/14/2002

10:24 p.m.

An EH fluid leak was reported from Intercept Valve 1.

An operator entered the area and isolated the leak by

closing Valve TGF-V-54.

5/14/2002

10:41 pm.

DEH Pumps A and B discharge filter differential pressures

were observed to have lowered to 100 psid.

5/14/2002

10:43 p.m.

The shift manager made the decision to perform a plant

scram based on DEH system parameters.

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5/14/2002

10:51 p.m.

A manual reactor scram was inserted by control room

operators. The plant entered Mode 3.

Main turbine bypass valves responded as required to

control reactor pressure.

5/14/2002

11:10 p.m.

The control room received an annunciator alarm: RCIC

STEAM LINE HIGH FLOW CHANNEL A.

RCIC-MO-16 isolated on a 1/2 Group V isolation signal.

RCIC was declared inoperable.

5/14/2002

11:20 p.m.

An operator was dispatched to the Reactor Building to

check for evidence of an RCIC steam line break. No

evidence of a break was found.

5/15/2002

03:47 a.m.

Control room operators reset the 1/2 Group V isolation

signal.

5/15/2002

04:47 a.m.

The control room declared the main steam bypass valves

inoperable due to degraded conditions on the DEH

system.

5/15/2002

08:05 a.m.

The control room established shutdown cooling using

residual heat removal Loop B.

5/15/2002

11:00 a.m.

Reactor temperature was reduced below 212o F and Mode

4 was declared.

5/15/2002

04:10 p.m.

The control room issued Surveillance Procedure

6.2DG.101, Diesel Generator 31 Day Operability Test

(IST)(DIV 2).

5/15/2002

10:44 p.m.

While performing Procedure 6.2DG.101, the DG 2 fuel oil

transfer pump failed to start as required by step 4.86. The

thermal overloads for the pump motor were found to be

tripped.

5/16/2002

01:17 a.m.

Condition Report 10163513, DGDO XFER P B Overloads

Tripped, was initiated.

5/16/2002

02:27 a.m.

The thermal overloads were reset and the fuel oil transfer

pump restored level to the day tank. The overloads

tripped a second time during this evolution.

5/16/2002

02:59 a.m.

SP 6.2DG.101 was logged as complete.

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5/16/2002

10:10 a.m.

The control room issued a Caution Order for DGDO-2-

XFER PUMP A, to place the switch in the AUTO position

to ensure that the Division 1 had an adequate fuel oil

supply if needed.

5/16/2002

05:07 p.m.

The control room issued Caution Order for DGDO-12-

DGDO-V-19 to close the valve to ensure that the

Division 1 DG has adequate fuel oil supplied, if needed.

5/16/2002

09:34 a.m.

Condition Report 10163642 was written on the DG fuel oil

transfer pump capacity, questioning if one pump could

supply both diesels.

5/17/2002

07:00 a.m.

A modification package was initiated to replace the

1.5 horsepower motor on Transfer Pump 2 with a

3.0 horsepower motor, due to difficulties in procuring

1.5 horsepower motor.

5/18/2002

12:00 p.m.

The new pump motor was tested satisfactorily and the

Division 2 DG was declared operable.

2.02

Digital Electrohydraulic Control System failure

a.

Inspection Scope

The inspectors reviewed operator logs and interviewed station personnel to develop a

sequence of events for the DEH Pump A failure and subsequent system degradation.

Maintenance work orders generated since the last refueling outage and corrective action

program notifications for the past 12 months were reviewed to assess the effectiveness

of the licensees maintenance and corrective action program in identifying and

preventing failures in this system. In addition, the inspectors reviewed the licensees

apparent cause determination and immediate corrective actions for the pump failure.

b.

Findings

No findings of significance were identified.

2.03

RCIC System Isolation

a.

Inspection Scope

The inspectors reviewed operator logs and interviewed station personnel to develop a

sequence of events for the isolation of the RCIC system. Maintenance work orders

generated since the last refueling outage, corrective action program notifications for the

past 12 months, and industry operating experience related to this failure were reviewed

to assess the effectiveness of the licensees maintenance and corrective action program

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in identifying and preventing failures in this system. In addition, the inspectors reviewed

the licensees apparent cause determination and immediate corrective actions for this

failure.

b.

Findings

Description of the Event

On May 14, 2002, the licensee performed a reactor scram and plant cooldown following

a failure in the DEH system. During cooldown and depressurization of the reactor

coolant system, a containment isolation signal was received which caused the RCIC

steam supply line to isolate. There was no demand for RCIC at that time. The isolation

signal was generated by an RCIC high steam flow signal from Differential Pressure

Switch RCIC-DPIS-83. The high steam flow signal cleared in approximately 6 seconds.

The control room dispatched an operator to the reactor building to check for indications

of a steam line break and none were found. Control room operators reset the RCIC

isolation signal approximately 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after the high steam flow signal cleared.

Apparent Cause and Corrective Actions

The licensee concluded that the apparent cause for the spurious isolation signal was a

clogged snubber in the instrument line for Differential Pressure Switch RCIC-DPIS-83.

The licensee determined that these snubbers (small, flow restricting orifices) were

installed in both instrument lines for Switch RCIC-DPIS-83 in order to dampen pressure

perturbations during RCIC turbine starts. One of these snubbers had apparently

become clogged with debris which trapped high pressure fluid in one side of the

pressure switch. Thus, during the plant cooldown and depressurization, the switch

erroneously indicated a differential pressure, indicative of a steam line break.

As an immediate corrective action, the instrument lines for RCIC-DPIS-83 were flushed

and the water was collected for analysis. It contained approximately 19.3 mg of debris

which was determined to be typical carbon steel corrosion products ranging in size up to

0.05 inches. The orifice diameter of the snubbers is only .002 inches. Therefore,

clogging of the snubber by corrosion products was likely the cause of the invalid

isolation signal. In addition, all other safety-related instrument lines containing snubbers

were flushed.

The potential for instrument line snubbers to become clogged and affect instrument

response was communicated to licensees in NRC Information Notice 92-33, Increased

Instrument Response Time When Pressure Dampening Devices Are Installed. This

Information Notice was reviewed by the licensee in 1993 and determined to be

applicable at Cooper Nuclear Station since multiple safety-related pressure instruments,

including instruments in the main steam system, reactor recirculation system, high

pressure coolant injection (HPCI) system, and RCIC system have snubbers installed in

them. This condition was never entered into the corrective action program. Rather, an

action item was generated in the Nuclear Action Item Tracking System (NAITS 92-

0430). As a result, a maintenance work request (MWR 93-1993) was generated to flush

all the affected instrument lines and record as-found conditions. The as-found

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conditions were evaluated qualitatively rather than quantitatively, so the exact amount

and size of the debris particles was unknown. However, of the 26 instruments that were

flushed in 1993, 12 were reported to have had debris in them similar to that which was

flushed from RCIC-DPIS-83 in 2002. The licensee concluded that there were no

immediate operability concerns based on these as-found conditions but determined that

a preventive maintenance procedure should be developed to periodically flush these

instruments. Over the course of the next 4 years, this action item was granted multiple

extensions to its due date and responsibility was transferred between multiple

departments until it was finally closed in 1997 with no further actions taken.

Title 10 of CFR Part 50, Appendix B, Criterion XVI, states that measures shall be

established to assure that conditions adverse to quality are promptly identified and

corrected. The failure to complete corrective actions identified through the review of

Information Notice 92-33 led to the isolation of the RCIC system which was considered a

condition adverse to quality. This is an apparent violation of 10 CFR Part 50,

Appendix B, Criterion XVI (50-298/0208-01). This issue was entered into the licensees

corrective action program as Resolved Condition Report 2002-0895.

Potential for Common Mode Failure

The same instrument line snubbers found in the RCIC differential pressure switches

were also installed in other safety-related instrument lines. Other safety functions

potentially affected by snubber clogging included: main steam line isolation on high

differential pressure or low steam line pressure, HPCI pump trip on low suction

pressure, HPCI turbine lube oil cooler flow, and the flow biased scram setpoints.

Therefore, this issue presented a potential common mode failure for several other

systems. The instruments providing input into the above list of safety functions have

varying instrument line configurations and operating conditions and may not be as

susceptible to clogging by corrosion products as the RCIC instruments. However, the

as-found conditions from the instrument flushes conducted in 1993 noted that corrosion

products were flushed from several of these instruments.

Significance Determination Process

This finding had an actual impact on safety because it rendered the RCIC system

inoperable. RCIC is considered a mitigation system; therefore, the finding was more

than minor and the safety significance was evaluated using Manual Chapter (MC) 0609,

Significance Determination Process. MC 0609, Appendix A, requires a Phase 3

determination whenever multiple equipment may be affected by a common cause.

Therefore, further analysis of the safety significance is being performed. Nevertheless,

an analysis using the Phase 1 and 2 worksheets was performed to preliminarily

characterize the safety significance. This analysis assumed that there were no common

cause affects on other systems and that the condition of the clogged snubber developed

sometime between the last successful surveillance test and May 14, 2002. The last

surveillance was performed 34 days prior to the event; therefore, t/2 (or 17 days) was

used as the exposure time. No credit was given for recovery of RCIC since recovery

from and erroneous isolation signal would involve lifting leads in a panel located outside

of the control room. There was no specific procedure to identify the leads to be lifted

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nor would there be sufficient personnel onsite at all times to complete this task in a

timely manner. This resulted in greater than very low safety significance with the

dominant sequence being high pressure injection during a loss of service water event.

2.04

Emergency DG Fuel Oil Transfer Pump Failure

a.

Inspection Scope

The inspectors reviewed operator logs and interviewed station personnel to develop a

sequence of events for the failure of the Division II emergency DG fuel oil transfer

pump. Maintenance work orders generated since the last refueling outage, corrective

action program notifications for the past 12 months, and industry operating experience

potentially related to this failure were reviewed to assess the effectiveness of the

licensees maintenance and corrective action program in identifying and preventing

failures in this system. In addition, the inspectors reviewed the licensees apparent

cause determination and immediate corrective actions for this failure.

b.

Findings

Diesel Fuel Oil Transfer System General System Description

The diesel fuel oil system is a required subsystem for the DG that provides for the

storage and transfer of clean fuel oil to be used by the DG. For each DG, the system

has a storage tank, transfer pump, day tank, engine-driven fuel oil pump, electric-driven

fuel oil booster pump, injection pumps, and fuel injection nozzles. The fuel oil transfer

pumps move oil from the storage tanks to the day tanks. The diesel fuel oil transfer

system has a normally open crosstie valve (DGDO 19), enabling either fuel oil transfer

pump to supply either day tank. Level switches in the day tanks control the start and

stop of each pump. A float admission valve on the day tank inlet prevents the overfilling

of the day tanks. The licensing and design basis for the DG fuel oil system is to provide

one diesel fuel for 7 days operation under postulated accident loads.

Description of the Event

On May 15, 2002, the licensee was performing a routine monthly surveillance test on the

Division II emergency DG. Following completion of the test, operators attempted to start

the Division II fuel oil transfer pump in order to completely fill the Division II day tank, but

the pump failed to start. The thermal overloads in the supply breaker for the pump

motor were found to be tripped. The thermal overloads were reset and the pump was

started; however, the motor tripped again due to a thermal overload condition. The

Division II emergency DG was declared inoperable but was considered available for use.

Therefore, during a loss of offsite power, it would have started and loaded as designed.

Apparent Cause and Corrective Actions

The licensee concluded that motor winding degradation was the most likely cause for

the Division II fuel oil transfer pump motor failure. This conclusion was supported by

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troubleshooting which identified a measured current imbalance, loss of motor efficiency,

and the lack of a motor bearing degradation. This was a reasonable explanation and

was supported by a sufficient level of detail.

The inspectors reviewed industry operating experience, preventive maintenance

records, and vendor recommended maintenance for this pump and found no previous

opportunities to identify degraded conditions on the pump motor. The only routine

predictive maintenance item performed on the motor was vibration monitoring per the

licensees in-service testing (IST) program. A review of the IST results for the transfer

pump did not reveal any adverse trends in performance. There were no previous

corrective maintenance items or problem identification reports which would indicate

electrical problems with the motor.

As an immediate corrective action, the licensee replaced the Division II fuel oil transfer

pump motor with a new motor and restored the DG to operability within the allowed

outage time required by the Technical Specification (TS). The licensee performed an

extent of condition inspection on the Division I fuel oil transfer pump motor on May 19,

2002 (Notification 1014224), and found a slight phase imbalance. The licensee found

that Phase B was approximately 2.2 amps, while Phases A and C were 2.5 to 2.6 amps.

After running several minutes, all phases of the motor equalized at approximately 2.3 to

2.4 amps. This was lower than the thermal overload setting of 2.95 amps. As a

preventive maintenance item, the licensee scheduled replacement of the Division I

motor in mid-June. The inspectors concluded that these corrective actions were

reasonable.

Potential for Common Mode Failure

The Divisions I & II diesel fuel oil transfer subsystems are cross-connected through a

normally opened valve (DGDO-19) that allows for the filling of either day tank from either

fuel oil transfer pump. This valve remained open with no administrative controls

following the failure of the Division II fuel oil transfer pump. Therefore, if a low level in

the Division I tank occurred, the Division I pump would have started and supplied both

day tanks.

Prior to replacement of the Division II pump motor, the inspectors questioned control

room operators as to whether one transfer pump was sufficient to supply two fully

loaded DGs. The operators were unsure. Upon further questioning by the inspectors,

the licensee acknowledged that one transfer pump would not be sufficient to supply two

fully loaded emergency DGs. As a result, Valve DGDO-19 was caution tagged closed to

assure that the operable diesel would receive enough fuel.

The inspectors assessed the consequences of a failure of the Division II diesel fuel oil

transfer pump if both DGs were fully loaded. Due to differences in the piping

configuration between the Division I and Division II fuel oil transfer systems, the

inspectors concluded that with only one pump running the Division II day tank would fill

preferentially before the Division I day tank, and the Division I day tank low level alarm

would be received prior to the alarm on Division II. In this situation, Alarm Response

Procedure 2.3 DG-1, Panel DG-1-Annunciator DG-1, directed operators to secure the

-9-

Division I fuel oil pump and isolate the day tank. This would have exacerbated the

situation since both DGs would have been operating with no fuel supply from the

storage tanks. The alarm response instructions were similar for the Division II pump as

well.

TS 5.4.1(a) requires that the licensee establish, implement, and maintain written

procedures recommended in Regulatory Guide 1.33, Revision 2, Appendix A, February

1978. Appendix A recommends procedures for abnormal, off-normal, or alarm

conditions. The failure to establish an adequate alarm response procedure for a DG

fuel oil day tank low level alarm is a violation of TS 5.4.1(a). This violation is being

treated as a noncited violation, consistent with Section VI.A of the NRC Enforcement

Policy (50-298/0208-02). The licensee issued a procedure change request for both

procedures and entered this into their corrective action system as Notification

10163642.

Significance Determination Process

This finding had a credible impact on safety since it could have led operators to perform

inappropriate actions which could have rendered both emergency DGs inoperable. The

emergency DGs are considered to be mitigation systems; therefore, the finding was

more than minor and the safety significance was evaluated using MC 0609. The

following assumptions were used during this evaluation:

The condition affecting the fuel oil transfer pump motor was assumed to have

existed for half of the time since the last successful surveillance test, or 15 days,

which exceeded the allowed outage time for the DG in TSs.

Credit was given for recovery of a failed train since calculations showed that both

DGs could operate fully loaded for approximately 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with only one diesel fuel

oil transfer pump in operation. Furthermore, Emergency Procedure 5.3EMPWR,

Emergency Power, required operators to monitor diesel fuel consumption to assure

that enough fuel is available during the 7-day period that a DG is required to

operate. Therefore, credit was given for recovery of a failed train, since it was

reasonable to assume that operators would have recognized the need to secure the

Division II diesel and would have had sufficient time to do so during an event prior to

challenging the operability of both DGs.

The emergency power system was treated as a single train system versus a multi-

train system, since it was assumed that operators would have recognized the failed

pump and secured the Division II DG.

The Phase 1 evaluation determined the need for Phase 2 since the finding represented

an actual loss of safety function of a single train for greater than its TS allowed outage

time. The Phase 2 evaluation resulted in very low safety significance (Green).

-10-

03

Meetings

03.01 Exit Meeting Summary

On June 20, 2002, the results of the inspection were discussed with Mr. M. Coyle and

other members of the licensees staff. The licensee acknowledged the inspection

results and informed the inspectors that no proprietary information was discussed during

the inspection.

ATTACHMENT

PARTIAL LIST OF PERSONS CONTACTED

Licensee

M. Bergman, Plant Engineering

J. Charterina, Plant Engineering Supervisor

M. Coyle, Site Vice President

K. Dia, Plant Engineer

F. Diya, Plant Engineering Manager

P. Fleming, Risk & Regulatory Affairs Manager/Licensing Manager

R. Gardner, Operations Manager

J. Gren, Plant engineering

M. Lingenfelter, DG System Engineer

M. Manning, Plant Engineering Supervisor

M. McKormack, Design Engineering Supervisor

M. Metzger, Plant Engineering

J. Ranalli, Senior Manager of Engineering

G. Seeman, Risk Management Engineer

D. Shrader, SRO operations specialist, OER group

K. Sutton, Risk Management Engineer

M. Tackett, Operations Supervisor

R. Wachowiak, Risk Management Supervisor

D. Wilson, Vice President - Nuclear

R. Yantz, Design Engineering

NRC

D. Loveless, Senior Reactor Analyst, Region IV

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-298/0208-01

AP

Failure to take corrective actions for instrument line snubber

clogging (Section 2.03)

Opened and Closed During this Inspection

50-298/0208-02

NCV

Inadequate procedure for response to a DG fuel oil day tank low

level alarm (Section 2.04)

Discussed

None.

-2-

DOCUMENTS REVIEWED

The following documents were selected and reviewed by the inspectors to accomplish the

objectives and scope of the inspection and to support any findings:

Procedures

Procedure

Number

Title

Revision

2.3 DG1

Panel DB-1 Annunciator DG-1, pages 16&17

1

5.3EMPWR

Emergency Procedure, Emergency Power

3C1

6.1DG.401

Diesel Generator Fuel Oil Transfer Pump IST Flow Test (DIV I)

8C1

6.1DG.401

Diesel Generator Fuel Oil Transfer Pump IST Flow Test (DIV I)

9

6.2DG.401

Diesel Generator Fuel Oil Transfer Pump IST Flow Test

(DIV II)

9

6.2DG.401

Diesel Generator Fuel Oil Transfer Pump IST Flow Test

(DIV II)

10

Drawings

Drawing

Number

Title

Revision

or Date

2011, sheet 1

Flow Diagrams, Turbine Oil Purification & Transfer Systems &

Diesel Oil System

N24

2077

Flow Diagram - Diesel Generator Buildings Service Water,

Starting Air, Fuel Oil, Sump System and Roof Drains

N48

X2825-202

Isometric - DO-1 Piping Inside DO-1 Tank Access Housing

N01

X2825-201

Isometric - DO-1 Piping Inside DO-1 Tank Access Housing

N01

-3-

X-2300-200

Isometric - DO-1 Diesel Oil

N02

28239

2"-DO-1 Discharge Yard Piping

4

3006 SH 5

Auxiliary One Line Diagram Starter Racks LZ and TZ; MCCs

K, L, LX, RA, RX, S, T, TX, X

N67

Work Orders

MWR 4242711

MWR 93-1993

Calculations

Number

Title

Revision

NEDC 97-012

Emergency Diesel Generator Fuel Oil On-Site Storage

Technical Specification Requirements

2

NEDC 02-046

Seismic Analysis of Gould Model 3171 Pump for the

Diesel Generator Fuel Oil Transfer Pumps

0

NEDC91-184

Motor Overload HeaterSizing

3

NEDC 86-105B

CNS Critical AC Bus Coordination Survey

7C2

NEDC 00-111

CNS Auxiliary Power System AC Loads

2C1

NEDC 00-004

Minimum MCC Voltage for Essential Loads

1C1

NEDC 87-047K

MCC K Load Summary

3C2

NEDC 87-047S

MCC S Load Summary

2C2

NRDC 91-146

Core Uncovery Analysis

0

Condition Reports

-4-

Number

Title

Date

10163486

Inadvertent DG Trip In Simulator I.C.20

5/15/02

10163513

DGDO XFER P B Overloads Tripped

5/16/02

10164123

1-CTP-DG-1B Inboard Seal Leaks

5/17/02

10163642

DG Fuel Oil Transfer Pump Capacity

5/16/02

10164235

On modification lessons learned for DG Fuel Oil Motor

Replacement

5/19/02

10164180

Nonconforming material conditionally released for work

on DG fuel oil motor.

5/17/02

SCR 2002-

0815

TGF Discharge DP High Alarm

5/14/02

10163182

RCIC Steam Line High Flow Isolation

5/14/02

10165870

No Long Term Action Implemented as Required by NRC

Information Notice 92-33

5/23/02

10163548

Evaluation for RCIC Half group 5 Isolation

5/15/02

10163182

RCIC-MO-16 Auto-Isolated on High Steam Line Flow

Channel A

5/14/02

Other Documents

Doc Number

Title

Revision

or Date

CED 6008866

DGDO-P-DOTA/B Motor Replacement

5/19/01

Maintenance history listing for DGDO-MOT-DFOTA

-5-

PRA02016

Risk Management input into 2.0.6 Evaluation for Forced

Outage 02-01

5/20/01

Work Number

90-2017

While rebuilding pump under MWR 90-1684, noticed motor

bearings were rough (canceled)

4/23/90

S2002037

SORC Meeting S2002-037

5/17/02

PSA-ES059

Risk Significance of Conditions Identified During the May 14,

2002 Forced Outage 02-01

1

Turbine High Pressure Fluid System Anomalies Result in

Manual Scram

5/17/02