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Category:Letter type:L
MONTHYEARL-MT-23-054, Subsequent License Renewal Application Supplement 82024-01-11011 January 2024 Subsequent License Renewal Application Supplement 8 L-MT-23-047, License Amendment Request: Revision to the MNGP Pressure Temperature Limits Report to Change the Neutron Fluence Methodology and Incorporate New Surveillance Capsule Data2023-12-29029 December 2023 License Amendment Request: Revision to the MNGP Pressure Temperature Limits Report to Change the Neutron Fluence Methodology and Incorporate New Surveillance Capsule Data L-MT-23-056, Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 1 Part 22023-12-18018 December 2023 Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 1 Part 2 L-MT-23-042, 2023 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.462023-12-11011 December 2023 2023 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.46 L-MT-23-052, Subsequent License Renewal Application Supplement 72023-11-30030 November 2023 Subsequent License Renewal Application Supplement 7 L-MT-23-051, Update to the Technical Specification Bases2023-11-28028 November 2023 Update to the Technical Specification Bases L-MT-23-049, Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 12023-11-21021 November 2023 Subsequent License Renewal Application Response to Request for Additional Information and Request for Confirmation of Information - Set 1 L-MT-23-043, 10 CFR 50.55a(z)(1) Request Regarding OMN-17, Revision 1. VR-092023-11-13013 November 2023 10 CFR 50.55a(z)(1) Request Regarding OMN-17, Revision 1. VR-09 L-MT-23-038, License Amendment Request to Revise Monticello Technical Specification Surveillance Requirement 3.8.6.62023-11-10010 November 2023 License Amendment Request to Revise Monticello Technical Specification Surveillance Requirement 3.8.6.6 L-MT-23-046, Subsequent License Renewal Application Response to Request for Additional Information Round 2 - Set 12023-11-0909 November 2023 Subsequent License Renewal Application Response to Request for Additional Information Round 2 - Set 1 L-MT-23-041, Subsequent License Renewal Application Response to Request for Confirmation of Information Set 22023-10-0303 October 2023 Subsequent License Renewal Application Response to Request for Confirmation of Information Set 2 L-MT-23-037, Subsequent License Renewal Application Response to Request for Additional Information Set 32023-09-22022 September 2023 Subsequent License Renewal Application Response to Request for Additional Information Set 3 L-MT-23-036, Subsequent License Renewal Application Response to Request for Additional Information Set 2 and Supplement 62023-09-0505 September 2023 Subsequent License Renewal Application Response to Request for Additional Information Set 2 and Supplement 6 L-MT-23-035, Subsequent License Renewal Application Supplement 52023-08-28028 August 2023 Subsequent License Renewal Application Supplement 5 L-MT-23-034, Subsequent License Renewal Application Response to Request for Additional Information Set 12023-08-15015 August 2023 Subsequent License Renewal Application Response to Request for Additional Information Set 1 L-MT-23-028, 2023 Refueling Outage 90-Day Inservice Inspection (ISI) Summary Report2023-07-31031 July 2023 2023 Refueling Outage 90-Day Inservice Inspection (ISI) Summary Report L-MT-23-032, 10 CFR 50.55a(z)(2) Request Regarding MO-2397, VR-112023-07-31031 July 2023 10 CFR 50.55a(z)(2) Request Regarding MO-2397, VR-11 L-MT-23-031, Subsequent License Renewal Application Supplement 4 and Responses to Request for Confirmation of Information - Set 12023-07-18018 July 2023 Subsequent License Renewal Application Supplement 4 and Responses to Request for Confirmation of Information - Set 1 L-MT-23-030, Subsequent License Renewal Application Supplement 32023-07-0404 July 2023 Subsequent License Renewal Application Supplement 3 L-MT-23-025, Subsequent License Renewal Application Supplement 22023-06-26026 June 2023 Subsequent License Renewal Application Supplement 2 L-MT-23-019, Submittal of 2022 Annual Radiological Environmental Operating Report2023-05-10010 May 2023 Submittal of 2022 Annual Radiological Environmental Operating Report L-MT-23-020, Submittal of 2022 Annual Radioactive Effluent Release Report2023-05-10010 May 2023 Submittal of 2022 Annual Radioactive Effluent Release Report L-MT-23-021, Core Operating Limits Report (COLR) for the Monticello Nuclear Generating Plant for Cycle 322023-05-0202 May 2023 Core Operating Limits Report (COLR) for the Monticello Nuclear Generating Plant for Cycle 32 L-MT-23-017, 2022 Annual Report of Individual Monitoring for the Monticello Nuclear Generating Plant (MNGP)2023-04-18018 April 2023 2022 Annual Report of Individual Monitoring for the Monticello Nuclear Generating Plant (MNGP) L-MT-23-010, Subsequent License Renewal Application Supplement 12023-04-0303 April 2023 Subsequent License Renewal Application Supplement 1 L-MT-23-013, Core Operating Limits Report (COLR) for Cycle 31, Revision 32023-03-28028 March 2023 Core Operating Limits Report (COLR) for Cycle 31, Revision 3 L-MT-23-012, Core Operating Limits Report (COLR) for Monticello Nuclear Generating Plant Cycle 31, Revision 22023-03-17017 March 2023 Core Operating Limits Report (COLR) for Monticello Nuclear Generating Plant Cycle 31, Revision 2 L-MT-23-008, 10CFR50.55a Request to Use Later Edition of ASME Section XI for ISI Code of Record (RR-003)2023-02-0707 February 2023 10CFR50.55a Request to Use Later Edition of ASME Section XI for ISI Code of Record (RR-003) L-MT-23-004, CFR 50.55a Request RR-001, Request to Use a Provision of a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI for the Monticello Third Interval Containment Inservice Inspection Program2023-01-23023 January 2023 CFR 50.55a Request RR-001, Request to Use a Provision of a Later Edition of the ASME Boiler and Pressure Vessel Code, Section XI for the Monticello Third Interval Containment Inservice Inspection Program L-MT-23-005, Response to the NRC Request for Additional Information Regarding the 50.55a Request Pr 08, HPCI Pump Quarterly Testing (EPID Number L-2022-LLR-0088)2023-01-0606 January 2023 Response to the NRC Request for Additional Information Regarding the 50.55a Request Pr 08, HPCI Pump Quarterly Testing (EPID Number L-2022-LLR-0088) L-MT-22-049, Industry Groundwater Protection Initiative Special Report2022-12-15015 December 2022 Industry Groundwater Protection Initiative Special Report L-MT-22-052, L-MT-22-052 Monticello Nuclear Generating Plant 10 CFR 50.55a Request No. Pr 08, Request for HPCI Pump Quarterly Alternative2022-12-15015 December 2022 L-MT-22-052 Monticello Nuclear Generating Plant 10 CFR 50.55a Request No. Pr 08, Request for HPCI Pump Quarterly Alternative L-MT-22-046, 2022 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.462022-12-13013 December 2022 2022 Annual Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.46 L-MT-22-048, Update to the Monticello Technical Specification Bases2022-11-28028 November 2022 Update to the Monticello Technical Specification Bases L-MT-22-047, Withdrawal of Request for Relief from ASME OM Code for the Sixth Inservice Testing Interval2022-11-10010 November 2022 Withdrawal of Request for Relief from ASME OM Code for the Sixth Inservice Testing Interval L-MT-22-045, Letter Submitting Post-Exam Package2022-11-0404 November 2022 Letter Submitting Post-Exam Package L-MT-22-030, Sixth Interval Inservice Testing (1ST) Plan2022-09-0606 September 2022 Sixth Interval Inservice Testing (1ST) Plan L-MT-22-037, Supplement to 10 CFR 50.55a Request Associated with the Monticello Sixth Inservice Testing Ten-Year Interval, Alternative VR-10, Excess Flow Check Valve Testing Frequency2022-08-29029 August 2022 Supplement to 10 CFR 50.55a Request Associated with the Monticello Sixth Inservice Testing Ten-Year Interval, Alternative VR-10, Excess Flow Check Valve Testing Frequency L-MT-22-007, Response to Request for Additional Information for the Monticello Nuclear Generating Plant Alternative Request VR-08 (EPID: L-MT-22-007)2022-07-22022 July 2022 Response to Request for Additional Information for the Monticello Nuclear Generating Plant Alternative Request VR-08 (EPID: L-MT-22-007) L-MT-22-026, Changes to the Emergency Plan2022-07-19019 July 2022 Changes to the Emergency Plan L-MT-22-024, Response to a Request for Additional Information for the Monticello Nuclear Generating Plant Related to the Amendment to Adopt Advanced Framatome Methodologies2022-06-0606 June 2022 Response to a Request for Additional Information for the Monticello Nuclear Generating Plant Related to the Amendment to Adopt Advanced Framatome Methodologies L-MT-22-022, Response to a Request for Additional Information: Monticello Alternative VR-10, Excess Flow Check Valve Testing Frequency2022-05-25025 May 2022 Response to a Request for Additional Information: Monticello Alternative VR-10, Excess Flow Check Valve Testing Frequency L-MT-22-017, 2021 Annual Radiological Environmental Operating Report2022-05-11011 May 2022 2021 Annual Radiological Environmental Operating Report L-MT-22-018, 2021 Annual Radioactive Effluent Release Report2022-05-11011 May 2022 2021 Annual Radioactive Effluent Release Report L-MT-22-016, 2021 Annual Report of Individual Monitoring2022-04-28028 April 2022 2021 Annual Report of Individual Monitoring L-MT-22-019, Withdrawal of Requests for Relief from ASME OM Code for the Sixth Inservice Testing Interval2022-04-18018 April 2022 Withdrawal of Requests for Relief from ASME OM Code for the Sixth Inservice Testing Interval L-MT-22-010, License Amendment Request to Revise Technical Specification 3.6.1.8 Residual Heat Removal (RHR) Drywell Spray Header and Nozzle Surveillance Frequency2022-03-18018 March 2022 License Amendment Request to Revise Technical Specification 3.6.1.8 Residual Heat Removal (RHR) Drywell Spray Header and Nozzle Surveillance Frequency L-MT-22-012, Special Report for the Bypass of the Offgas Treatment Storage System2022-03-15015 March 2022 Special Report for the Bypass of the Offgas Treatment Storage System L-MT-22-008, 10 CFR 50.55a Request Associated with the Monticello Sixth Inservice Testing Ten-Year Interval Alternative Related to Excess Flow Check Valve Testing Frequency (L-MT-22-008)2022-03-0707 March 2022 10 CFR 50.55a Request Associated with the Monticello Sixth Inservice Testing Ten-Year Interval Alternative Related to Excess Flow Check Valve Testing Frequency (L-MT-22-008) L-MT-22-006, 10 CFR 50.55a Request Associated with the Monticello Sixth Inservice Testing Ten-Year Interval OMN-26 (L-MT-22-006)2022-02-18018 February 2022 10 CFR 50.55a Request Associated with the Monticello Sixth Inservice Testing Ten-Year Interval OMN-26 (L-MT-22-006) 2024-01-11
[Table view] Category:Licensee 30-Day Written Event Report
MONTHYEARL-MT-16-050, Thirty-Day Notification for Dry Shielded Canister MNP-61 BTH-1-B-2-016 Pursuant to 10 CFR 72.212, Conditions of General License Issued Under 10 CFR 72.210, for the Storage of Spent Fuel2016-10-20020 October 2016 Thirty-Day Notification for Dry Shielded Canister MNP-61 BTH-1-B-2-016 Pursuant to 10 CFR 72.212, Conditions of General License Issued Under 10 CFR 72.210, for the Storage of Spent Fuel L-MT-14-054, Thirty-Day Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.462014-06-17017 June 2014 Thirty-Day Report of Changes in Emergency Core Cooling System Evaluation Models Pursuant to 10 CFR 50.46 L-MT-13-090, August 2013, 10 CFR 50.46 Thirty-Day Report2013-08-27027 August 2013 August 2013, 10 CFR 50.46 Thirty-Day Report L-MT-11-039, Submittal of 10 CFR 50.46 Thirty Day Report2011-07-0707 July 2011 Submittal of 10 CFR 50.46 Thirty Day Report ML0923803802009-09-0303 September 2009 LER 263/2008-005, Monticello, Partial Loss of Offsite Power Event with HPCI High Level Instrument Trip Failures L-MT-05-116, Day Special Report: Failure of Wide Range Radiation Monitor Electronic Process Flow Probe2005-11-30030 November 2005 Day Special Report: Failure of Wide Range Radiation Monitor Electronic Process Flow Probe ML0232904112002-11-0404 November 2002 30-Day Special Report, Inoperable Offgas Stack Wide Range Monitors 2016-10-20
[Table view] Category:Written Event Report (30 or 60 day)
[Table view] |
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Monticello Nuclear Generating Plant Committed to Nuclear Operated by Nuclear Management Company, LLC November 30, 2005 L-MT-05-116 Technical Specification 3.14.1 U.S. Nuclear Regulatory Commission ATTN: Document Control Desk Washington, DC 20555 Monticello Nuclear Generating Plant Docket No. 50-263 License No. DPR-22 30-Day Special Report: Failure of Wide Ranae Radiation Monitor Electronic Process Flow Probe Nuclear Management Company, LLC is submitting this report based on the potential that the Channel "A" Reactor Building Vent Wide Range Radiation Monitor (WRGM) may have been inoperable for greater than the seven days in accordance with the Monticello Nuclear Generating Plant Technical Specification Table 3.14.1. This report is being submitted for an inoperable Reactor Building Vent WRGM flow probe. provides the results of our review of the event. Appropriate entries were made into the Corrective Action Program in response to this event.
This letter contains no new commitments and no revisions to existing commitments.
ohn . a f Site Vice President, Monticel uclear Generating Plant Nuclear Management Company, LLC Enclosure cc: Administrator, Region Ill, USNRC Project Manager, Monticello, USNRC Resident Inspector, Monticello, USNRC 2807 West County Road 75
- Monticello, Minnesota 55362-9637 Telephone: 763-295-5151 a Fax: 763-295-1454
ENCLOSURE I BACKGROUND AND ACTION TAKEN Monticello Nuclear Generating Plant (MNGP) Technical Specification (TS) Table 3.14.1, "Instrumentation for Accident Monitoring," includes the Reactor Building Vent Wide Range Radiation Monitors (also known as Wide Range Gas Monitors or WRGMs). This TS Table requires two instrument channels to be operable, or one channel may be inoperable for no longer than seven days. Since the "A"channel of the Reactor Building Vent WRGM may have been inoperable for longer than seven days, a 30-day special report is being voluntarily submitted.
On September 19, 2005, in response to recommendations from the original equipment manufacturer, the process flow board and flow probe for the "A"channel of the Reactor Building Vent WRGM were replaced. On September 22, 2005, a control room operator observed indications indicative of a change in total process flow between the two Reactor Building Vent WRGM channels. Trending plots confirmed the differences and a work order was written to investigate the condition. During performance of the work order between November 1 - 4, 2005, it was determined that electrolytic capacitors on the "A" Channel Reactor Building Vent WRGM process flow board had failed. The "A" Channel Reactor Building Vent process flow probe board was refurbished with new capacitors, reinstalled, and tested under the seven day allowed outage time permitted by TS Table 3.14.1.
CAUSE OF INOPERABILTY After replacement of the "A"Channel Reactor Building Vent WRGM flow probe and process board, the WRGM channels exhibited indications of a change in system conditions. The total process flow trend increased over the course of several days and then decreased back to within its expected range. Some variation between units is not unusual due to the location of the probes in the vent ducts and flow patterns. A work order was written to investigate the condition. The work order subsequently determined that electrolytic capacitors on the "A" Channel Reactor Building Vent WRGM process flow board had failed.
Based on the channel's performance between the first sign of variation, it is not possible to determine the exact time of failure. However, since there were indications that the problem began as early as September 22, 2005, it is being conservatively reported as an inoperable condition which lasted longer than the TS permitted allowed outage time.
PLANS AND SCHEDULE FOR RESTORING THE SYSTEM TO OPERABLE STATUS The "A"Channel Reactor Building Vent WRGM flow probe board was refurbished with new capacitors, reinstalled, tested and returned to service on November 4, 2005. The Page 1 of 2
ENCLOSURE I WRGM is currently operating as designed. Work orders have been created to refurbish the Reactor Building Vent WRGM "B"channel.
SAFETY SIGNIFICANCE The Reactor Building Vent WRGMs are not safety related nor are they included in the Maintenance Rule. They are Category 2, Regulatory Guide 1.97 accident monitoring systems. The Channel "B"Reactor Building Vent WRGM was fully capable of performing its design function during the entire period in which the Channel "A' Reactor Building Vent WRGM process flow probe was acting abnormally.
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