Information Notice 2004-04, Fuel Damage During Cleaning at a Foreign Pressurized Water Reactor

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Fuel Damage During Cleaning at a Foreign Pressurized Water Reactor
ML040540778
Person / Time
Issue date: 02/24/2004
From: Beckner W
NRC/NRR/DIPM/IROB
To:
Dozier J, NRR/IROB 415-1014
References
IN-04-004
Download: ML040540778 (8)


UNITED STATES

NUCLEAR REGULATORY COMMISSION

OFFICE OF NUCLEAR REACTOR REGULATION

WASHINGTON, DC 20555-0001 February 24, 2004 NRC INFORMATION NOTICE 2004-04: FUEL DAMAGE DURING CLEANING AT A

FOREIGN PRESSURIZED WATER REACTOR

Addressees

All holders of operating licenses for light-water reactors, except those who have permanently

ceased operations and have certified that fuel has been permanently removed from the reactor.

Purpose

The U.S. Nuclear Regulatory Commission (NRC) is issuing this information notice to inform

addressees about a recent fuel damage event that occurred during chemical cleaning of the fuel

at a foreign pressurized-water reactor (PWR). The fuel cleaning system involved in the event

was not of domestic (U.S.) design or manufacture; however, the fuel and processes used

at the affected PWR are similar to those that may be used in domestic light-water reactors.

This event involved a release of radioactive material to the environment and was publicly

reported in the news media. The occupational dose to workers was well within regulatory limits, and the estimated dose to members of the public was a small fraction of regulatory limits

and less than 1 days exposure to natural background radiation. The event was classified as

Level 3 on the International Nuclear Event Scale, based on substantial damage to irradiated fuel.

The NRC expects recipients to review the information in this notice for applicability to their facilities

and consider actions, as appropriate, to avoid similar problems. However, suggestions contained

in this information notice do not constitute NRC requirements and, therefore, do not require

any specific action or written response.

Description of Circumstances

The event in question occurred at a foreign PWR that was undergoing chemical cleaning

of the fuel because the reactor had experienced corrosion product deposition that affected

core thermal performance. This corrosion product deposition was attributable to a variety of factors, including earlier steam generator chemical decontamination. The plants management elected

to conduct the chemical cleaning, which was originally scheduled to take place during an

upcoming refueling outage to improve core thermal performance during the subsequent

operating cycle.

The facility had received licensing approval for the fuel cleaning system, based in part on

previous successful cleaning of seven-assembly batches of fuel that had decayed for more than

a year. The operator installed the fuel cleaning system in the cask transfer area adjacent to the

spent fuel pool. The fuel cleaning system consisted of a large tank designed to hold 30 fuel

assemblies, other tanks to hold and collect the cleaning solution, pumps to circulate the cooling

water and cleaning solutions, filters to trap removed corrosion products, and valves and hoses

to control and direct the flow of the cleaning solution. The tank containing the fuel assemblies was

insulated to facilitate the maintenance of temperatures to support the cleaning process. Openings in

the top of the tank consisted only of a small line to vent noncondensible gases and a covered

access opening to permit movement of the fuel assemblies. (The latter opening was closed

during the cleaning process.) The cooling flow entered the bottom of the tank, flowed up

through the fuel assemblies, flowed down around the shroud surrounding each assembly, and

exited the tank through a plenum at the bottom. However, bypass flow paths reduced the

effectiveness of the available cooling flow. The flow during the cleaning process was high, but

the standby cooling pump used after completion of the cleaning cycle produced much lower

flow.

Following reactor shutdown on March 29, 2003, the reactor operator began fuel cleaning operations

with fuel removed from the reactor vessel. The operators successfully cleaned three batches

of recently irradiated fuel without incident. However, unlike the earlier batches, the operators

did not remove the tank access cover shortly after the completion of the cleaning process

for the fourth batch on April 10, 2003, because the crane was being used for another task.

The 30 fuel assemblies in the tank represented about 10 percent of the core and had an estimated

decay heat rate of 240 to 270 kW. Analyses later demonstrated that the single cooling pump

in operation after the completion of the cleaning process provided insufficient flow to effectively

cool the fuel assemblies with the access cover in place because bypass flow paths and the

development of a negative thermal head precluded upward flow through the fuel assemblies.

The decay heat began producing steam within the cleaning tank. Because the vent line

was inadequate for the rate of steam generation, the steam displaced the water surrounding

the fuel assemblies within several hours. In a steam environment, the fuel temperature increased

rapidly to an estimated 1,200 Kelvin. This temperature increase caused a minor release

of noble gases from the fuel assemblies, which was detected by plant instruments. In response

to this release, plant operators decided to remove the cleaning tank access cover. The absence

of instrumentation within the cleaning tank precluded the assessment of conditions within

the cleaning tank prior to removal of its access cover. When the access cover seal was broken

early in the morning of April 11, 2003, water entered the tank and contacted the hot fuel assemblies.

Subsequent video examination of the cleaning tank revealed severe fuel damage that resulted

from the water quenching of the hot fuel assemblies and their surrounding shroud. The operator

estimated that this fuel damage event resulted in the release of a few hundred Tera Becquerels

(about 10,000 Curies) of nobel gases, a few tenths of a Tera Becquerel (about 10 Curies)

of radioiodine, and less than one-hundredth of a Tera Becquerel (about a quarter of a Curie)

of other particulate radionuclides (principally Cesium isotopes). Offsite environmental measurements

were consistent with these release estimates.

The failure of the fuel cladding and surrounding shroud resulted in a redistribution of fuel material, with much of it settling to the bottom of the cleaning tank. This distribution of fuel material was outside the configurations analyzed to verify a substantial margin to criticality. To ensure

an adequate margin to criticality, the operators substantially increased the dissolved boron

concentration in the spent fuel pool and adjacent cask transfer pit.

Discussion:

Provision of adequate cooling, maintenance of a margin to criticality, and maintenance of fuel

integrity for fission product retention are essential functions for the safe storage of irradiated

fuel. These functions are normally accomplished through passive design features incorporated

in the design of the fuel and the storage racks.

This event demonstrates the importance of maintaining adequate cooling of fuel after discharge

from the reactor vessel. In this event, the design features that provide adequate natural circulation

cooling were not maintained in the design of the cleaning system. Instead, the cleaning system

design relied on forced circulation cooling without adequate consideration of the reliability

and capability provided for this function. The damage to the integrity of the fuel, which resulted

from the inadequate cooling, threatened the maintenance of an adequate margin to criticality

and released a substantial quantity of radioactive material to the environment.

Related Generic Communications:

The following NRC generic communications describe related reactor operating experience:

(1) Information Notice 97-85, Effects of Crud Buildup and Boron Deposition on Power Distribution

and Shutdown Margin, December 11, 1997.

(2) Information Notice 97-14, Assessment of Spent Fuel Cooling, March 28, 1997.

(3) Generic Letter 88-17, Loss of Decay Heat Removal 10 CFR 50.54(f), October 17, 1988.

(4) Generic Letter 87-12, Loss of Residual Heat Removal (RHR) while the Reactor Coolant System

(RCS) is Partially Filled, July 9, 1987.

This information notice does not require any specific action or written response. If you have

any questions about the information in this notice, please contact one of the technical contacts

listed below or the appropriate project manager in the NRCs Office of Nuclear Reactor Regulation.

/RA/

William D. Beckner, Chief

Reactors Operations Branch

Division of Inspection Program Management

Office of Nuclear Reactor Regulation

Technical contacts: S.R. Jones, NRR Jerry Dozier, NRR

(301) 415-2712 (301) 415-1014 Email: srj@nrc.gov Email: jxd@nrc.gov

Attachment: List of Recently Issued NRC Information Notices

ML040540778 OFFICE RSE:RORP:DRIP Tech Editor RSE:SPLB:DSSA

NAME IJDozier PAGarrity* SRJones

DATE 02/09/2004 02/09/2004 02/09/2004 OFFICE BC:SPLB:DSSA SC:OES:IRIB:DIPM C:IROB:IROB:DIPM

NAME JNHannon TReis WDBeckner

DATE 02/10/2004 02/20/2004 02/24 /2004

Attachment 1 LIST OF RECENTLY ISSUED

NRC INFORMATION NOTICES

_____________________________________________________________________________________

Information Date of

Notice No. Subject Issuance Issued to

_____________________________________________________________________________________

2004-03 Radiation Exposures to Pending All well-logging licensees.

Members of the Public in

Excess of Regulatory Limits

Caused by Failures to Perform

Appropriate Radiation Surveys

During Well-logging

Operations

2004-02 Strontium-90 Eye Applicators 02/05/2004 All U.S. Nuclear Regulatory

New Calibration Values and Commission (NRC) medical-use

Use licensees and NRC master

materials license medical-use

Permittees.

2004-01 Auxiliary Feedwater Pump 01/21/2004 All holders of operating licenses

Recirculation Line Orifice or construction permits for

Fouling - Potential Common nuclear power reactors, except

Cause Failure those that have permanently

ceased operations and have

certified that fuel has been

permanently removed from the

reactor.

2002-26, Sup 2 Additional Failure of Steam 01/09/2004 All holders of an operating license

Dryer After A Recent Power or a construction permit for

Uprate nuclear power reactors, except

those that have permanently

ceased operations and have

certified that fuel has been

permanently removed from the

reactor.

Note: NRC generic communications may be received in electronic format shortly after they are

issued by subscribing to the NRC listserver as follows:

To subscribe send an e-mail to <listproc@nrc.gov >, no subject, and the following

command in the message portion:

subscribe gc-nrr firstname lastname

______________________________________________________________________________________

OL = Operating License

CP = Construction Permit