IR 05000456/2025004

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Integrated Inspection Report 05000456/2025004 and 05000457/2025004
ML26030A045
Person / Time
Site: Braidwood  
(NPF-072, NPF-077)
Issue date: 01/30/2026
From: Dariusz Szwarc
NRC/RGN-III/DORS/RPB3
To: Mudrick C
Constellation Energy Generation, Constellation Nuclear
References
IR 2025004
Download: ML26030A045 (0)


Text

SUBJECT:

BRAIDWOOD STATION - INTEGRATED INSPECTION REPORT 05000456/2025004 AND 05000457/2025004

Dear Christopher H. Mudrick:

On December 31, 2025, the U.S. Nuclear Regulatory Commission (NRC) completed an inspection at Braidwood Station. On January 12, 2026, the NRC inspectors discussed the results of this inspection with A. Schuerman, Site Vice President, and other members of your staff. The results of this inspection are documented in the enclosed report.

No findings or violations of more than minor significance were identified during this inspection.

This letter, its enclosure, and your response (if any) will be made available for public inspection and copying at http://www.nrc.gov/reading-rm/adams.html and at the NRC Public Document Room in accordance with Title 10 of the Code of Federal Regulations 2.390, Public Inspections, Exemptions, Requests for Withholding.

Sincerely, Dariusz Szwarc, Chief Reactor Projects Branch 3 Division of Operating Reactor Safety Docket Nos. 05000456 and 05000457 License Nos. NPF-72 and NPF-77 Enclosure:

As stated cc w/ encl: Distribution via GovDelivery January 30, 2026 Signed by Szwarc, Dariusz on 01/30/26

Letter to Christopher

SUMMARY

The U.S. Nuclear Regulatory Commission (NRC) continued monitoring the licensees performance by conducting an integrated inspection at Braidwood Station, in accordance with the Reactor Oversight Process. The Reactor Oversight Process is the NRCs program for overseeing the safe operation of commercial nuclear power reactors. Refer to https://www.nrc.gov/reactors/operating/oversight.html for more information.

List of Findings and Violations

No findings or violations of more than minor significance were identified.

Additional Tracking Items

Type Issue Number Title Report Section Status LER 05000456/2025-001-00 LER 2025-001-00 for Braidwood Station, Unit 1,

Over Temperature Delta Temperature due to Lightning Strike 71153 Closed

PLANT STATUS

Unit 1 began the inspection period operating at 89 percent power due to coasting down for a scheduled refueling outage. On October 5, 2025, the unit was taken offline to begin scheduled refueling outage A1R25. On October 22, 2025, the unit achieved criticality. Several hours later, on October 23, 2025, the unit entered Mode 1. The unit reached full power on October 29, 2025.

With the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the rest of the inspection period.

Unit 2 began the inspection period operating at full power. With the exception of minor reductions in power to support scheduled testing activities and load changes requested by the transmission system dispatcher, the unit remained operating at or near full power for the entire inspection period.

INSPECTION SCOPES

Inspections were conducted using the appropriate portions of the inspection procedures (IPs)in effect at the beginning of the inspection unless otherwise noted. Currently approved IPs with their attached revision histories are located on the public website at http://www.nrc.gov/reading-rm/doc-collections/insp-manual/inspection-procedure/index.html. Samples were declared complete when the IP requirements most appropriate to the inspection activity were met consistent with Inspection Manual Chapter (IMC) 2515, Light-Water Reactor Inspection Program - Operations Phase. The inspectors performed activities described in IMC 2515, Appendix D, Plant Status, observed risk significant activities, and completed on-site portions of IPs. The inspectors reviewed selected procedures and records, observed activities, and interviewed personnel to assess licensee performance and compliance with Commission rules and regulations, license conditions, site procedures, and standards.

REACTOR SAFETY

71111.04 - Equipment Alignment

Partial Walkdown Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated system configurations during partial walkdowns of the following systems/trains:

(1) Unit 1 residual heat removal system train A while protected for shutdown cooling during A1R25 the week ending October 11, 2025
(2) Both trains of the fuel pool cooling system while the core was fully offloaded during A1R25 during the week ending October 11, 2025

71111.05 - Fire Protection

Fire Area Walkdown and Inspection Sample (IP Section 03.01) (2 Samples)

The inspectors evaluated the implementation of the fire protection program by conducting a walkdown and performing a review to verify program compliance, equipment functionality, material condition, and operational readiness of the following fire areas:

(1) Fire Zone 8.3-1, turbine building, 401' elevation, Unit 1 grade level (NW)during hot work for valve replacement during the week ending October 11, 2025
(2) Fire Zone 8.5-1, turbine building, 426' elevation, Unit 1 mezzanine floor (SE)during hot work for piping replacement during the week ending October 11, 2025

71111.11Q - Licensed Operator Requalification Program and Licensed Operator Performance

Licensed Operator Performance in the Actual Plant/Main Control Room (IP Section 03.01) (1 Sample)

(1) The inspectors observed and evaluated various activities involving on-watch operations crews in the main control room on October 5, 2025, during shutdown of Unit 1 for refueling outage A1R25.

Licensed Operator Requalification Training/Examinations (IP Section 03.02) (1 Sample)

(1) Observation of the performance of a crew of licensed plant operators in the facilitys simulator performing just in time training on October 1, 2025

71111.12 - Maintenance Effectiveness

Maintenance Effectiveness (IP Section 03.01) (4 Samples)

The inspectors evaluated the effectiveness of maintenance to ensure the following structures, systems, and components (SSCs) remain capable of performing their intended function:

(1) Maintenance effectiveness review of 1RC014A-D, reactor head vent valves following discovery of leakage during refueling outage A1R25
(2) Maintenance effectiveness review of 0VC43Y, Unit Common, Train A (0A)recirc charcoal absorber bypass damper during the week ending October 25, 2025
(3) Maintenance effectiveness review of the Unit 2 steam generator PORVs during the weeks ending November 8 and 15, 2025
(4) Maintenance effectiveness review of 0SX147, Unit Common component cooling heat exchanger outlet valve during the weeks ending December 5 and December 19, 2025

71111.13 - Maintenance Risk Assessments and Emergent Work Control

Risk Assessment and Management Sample (IP Section 03.01) (1 Sample)

The inspectors evaluated the accuracy and completeness of risk assessments for the following planned and emergent work activities to ensure configuration changes and appropriate work controls were addressed:

(1) Unit 2 elevated risk while emergency DC bus 212 was cross-tied to Unit 1 for refueling outage A1R25 during the week ending October 11, 2025

71111.15 - Operability Determinations and Functionality Assessments

Operability Determination or Functionality Assessment (IP Section 03.01) (2 Samples)

The inspectors evaluated the licensees justifications and actions associated with the following operability determinations and functionality assessments:

(1) Evaluation of the operability of ESF (Engineered Safety Feature) Transformer 132X, as documented in action request (AR) 4906585 during the weeks ending October 25 and November 1, 2025
(2) Evaluation of the operability of the 2B emergency diesel generator (EDG),as documented in AR 4907289 during the weeks ending October 25 and November 1, 2025

71111.20 - Refueling and Other Outage Activities

Refueling/Other Outage Sample (IP Section 03.01) (1 Sample)

(1) The inspectors evaluated refueling outage A1R25 activities from October 6, 2025, to October 23, 2025

71111.24 - Testing and Maintenance of Equipment Important to Risk

The inspectors evaluated the following testing and maintenance activities to verify system operability and/or functionality:

Post-Maintenance Testing (PMT) (IP Section 03.01) (8 Samples)

(1) Functional and operational testing of the Unit 1 DC-112 125V ESF bus following battery cell replacement during refueling outage A1R25, as documented in Work Order (WO) 5528760
(2) Functional and operational testing of 1CC9518 after valve replacement during refueling outage A1R25, as documented in WO 5735934.
(3) Functional and operational testing of the Unit 1 Train B auxiliary feedwater system following maintenance during refueling outage A1R25, as documented in WO 5723897
(4) Core reload verification following refueling outage A1R25, as documented in WO 5533252
(5) Low power physics testing following refueling outage A1R25, as documented in WO 5536091
(6) Functional and operational testing of the Unit 1 Solid State Protection System (SSPS)following maintenance during refueling outage A1R25, as documented in WOs 5566824 and 5588144
(7) Functional and operational testing of control rod drive system following refueling outage A1R25, as documented in WO 5536100
(8) Hydraulic pressure testing of the reactor coolant system following refueling outage A1R25 on October 22, 2025

Surveillance Testing (IP Section 03.01) (2 Samples)

(1) Unit 1 auxiliary feedwater full flow and response time testing, as documented in WO 5549001
(2) Unit 1 main steam safety valve testing, as documented in WO 5540154

Containment Isolation Valve (CIV) Testing (IP Section 03.01) (1 Sample)

(1) Local leak rate testing of Unit 1 primary containment isolation valves CC 9518/9438/685 for the reactor coolant pump thermal barrier return, as documented in WO 5232324.

71114.04 - Emergency Action Level and Emergency Plan Changes

Inspection Review (IP Section 02.01-02.03) (1 Sample)

(1) The inspectors evaluated the following submitted Emergency Action Level and Emergency Plan changes.

71114.06 - Drill Evaluation

Additional Drill and/or Training Evolution (1 Sample)

The inspectors evaluated sites emergency plan by observing the following emergency response organization (ERO) activities:

(1) A limited emergency preparedness drill that resulted in a simulated Site Area Emergency event classification on November 10, 2025

OTHER ACTIVITIES - BASELINE

71151 - Performance Indicator Verification The inspectors verified licensee performance indicators submittals listed below:

BI02: RCS Leak Rate Sample (IP Section 02.11) (2 Samples)

(1) Unit 1 (October 1, 2024, through September 30, 2025)
(2) Unit 2 (October 1, 2024, through September 30, 2025)71152A - Annual Follow-up Problem Identification and Resolution

Annual Follow-up of Selected Issues (Section 03.03) (3 Samples)

The inspectors reviewed the licensees implementation of its corrective action program related to the following issues:

(1) The inspectors reviewed the corrective actions associated with AR 4901565, high head FLEX pumps high hydraulic fluid temperature
(2) The inspectors reviewed the corrective actions associated with AR 4424225, 2A CV Pump Significantly Weaker than 2B CV Pump
(3) The inspectors reviewed the corrective actions associated with AR 4890667, Switchyard Ground Repair

71152S - Semiannual Trend Problem Identification and Resolution Semiannual Trend Review (Section 03.02) (1 Sample)

(1) The inspectors reviewed the licensees corrective action program to identify potential trends with ground water intrusion in Unit 2 curved wall area that might be indicative of a more significant safety issue.

71153 - Follow-up of Events and Notices of Enforcement Discretion Event Report (IP Section 03.02) (1 Sample)

The inspectors evaluated the following licensee event reports (LERs):

(1) LER 05000456/2025-001-00, Over Temperature Delta Temperature Reactor Trip Due to Lightning Strike (ADAMS Accession No. ML25269A165)

The inspectors determined that the cause of the condition described in the LER was not reasonably within the licensees ability to foresee and correct, and therefore was not reasonably preventable. No performance deficiency nor violation of NRC requirements was identified. This LER is Closed.

INSPECTION RESULTS

Observation: Ground Water Intrusion Trend

The inspectors reviewed AR 4899202 for a licensee identified trend in ground water intrusion into the Unit 2 curved wall area, 364' elevation by safety injection (SI) valves. The inspectors reviewed past action requests (ARs), work orders, and procedures and interviewed licensee engineers to ascertain the causes and potential safety impact of the ground water intrusion.

The inspectors determined that the current rate of ground water intrusion does not have an impact on the function of safety-related systems or is the result of degradation of the auxiliary building structure. The licensee has developed long term plans and initiated actions to monitor and address the issue. No findings or violations were identified.

EXIT MEETINGS AND DEBRIEFS

The inspectors verified no proprietary information was retained or documented in this report.

  • On January 12, 2026, the inspectors presented the integrated inspection results to A. Schuerman, Site Vice President, and other members of the licensee staff.

DOCUMENTS REVIEWED

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Miscellaneous

1A RH Protected

for S/D Cooling

A1R25 Equipment List

10/02/2025

1BwGP 100-5

Plant Shutdown and Cooldown

BwOP FC-M1

Operating Mechanical Lineup Unit 1

71111.04

Procedures

BwOP RH-6

Placing the RH System in Shutdown Cooling

1074183

NRC Questions Regarding 1(2)RC014A-D Head Vent Valves

05/27/2010

266402

External Leakage (1RC014 Sol. Va. Assemblies)

10/23/2004

4414119

01-OSP-A Reactor Head Vent BA

04/05/2021

4516310

MOV 0SX147 - Valve Shaft / Bearing Replacement

08/11/2022

20574

0A VC Charcoal Adsorber Bypass Leakage Results

OOT [Out of Tolerance]

11/30/2023

4896712

0A-VC Charcoal Absorber Leakage Test OOT

09/11/2025

4903195

SOP-A Boric Acid Overflow from Leakby on

1RC014 Valves

10/06/2025

Corrective Action

Documents

4916143

Follow-Up to AR 4516310 for Upcoming 0SX147 Diagnostic

11/20/2025

Engineering

Changes

646516

Evaluate Acceptance of Weak Link Analysis for

Jamesbury 30 Butterfly Valve, 0SX147

Engineering

Evaluations

EQ Binder, EQ-

GEN040

V526 Series Solenoid Valves

Miscellaneous

IST-BRW-PLAN

Inservice Testing Program Fourth Ten Year Interval

03/24/2021

1397268

Task 1, 0FZ-VC023 Hydramotor Replacement PM

05/29/2013

71111.12

Work Orders

29335

0SX147 Motor Operated Valve Diagnostic Test

2/19/2025

Miscellaneous

25VDC DC-111

and DC-212

Protected

Equipment List

10/07/2025

71111.13

Procedures

BwOP DC-7-112

25V DC ESF Bus 112 Cross-tie/Restoration

4906585

OSP-R XFMR 132X Cooling Fans Incorrect Safety Level

10/17/2025

Corrective Action

Documents

4907289

2B DG Jacket Water Sightglass Lower than Ops Rounds

Specs

10/20/2025

71111.15

Engineering

Changes

645974

TCCP to Allow the Use of 132X Transformer Without Forced

Air Cooling Fans Available - 1AP13E

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Engineering

Evaluations

BRW-E-2025-012

Remove Power from Cooling Fans to Transformer 132X

Procedures

BwOP DG-3

Filling the Diesel Generator Jacket Water System

4905391

A1R25 Source Range Response Not Verified

10/14/2025

Corrective Action

Documents

4905733

A1R25 Core Reload - FM Discovered in Cavity

10/14/2025

1BwGP 100-5

Plant Shutdown and Cooldown

71111.20

Procedures

BwOP RH-6

Placing the RH System in Shutdown Cooling

4902164

DPM AF Leak 1D SG Flow Instrument Flange During

VT-2

10/01/2025

4906995

OSP-R LLRT for 1CC9438 and 1CC9518 in WARNING

Range

10/18/2025

4907143

OSP-X 1PA09J Permissive Test Switch Dirty Contacts

10/19/2025

Corrective Action

Documents

4907149

TD-1 in 1PA09J Degraded

10/19/2025

1BwHSR 3.8.4.2-

2

Unit One 125 Volt ESF Batter Charger 112 Capacity Test

1BwOS TRM

2.7.a.1

Unit One Auxiliary Feedwater Diesel Prime Mover

Performance Surveillance

1BwOSR 3.1.7.1

Digital Rod Position Indication (DRPI) Operability Checkout

1BwOSR 3.3.1.4-

Unit One SSPS, Reactor Trip Breaker, and Reactor Trip

Bypass Breaker Surveillance (Train B)

1BwOSR 3.7.5.4-

Unit One Diesel Driven Auxiliary Feedwater Pump

Surveillance

1BwOSR 3.8.9.1

Unit One 125V DC Bus Division 111/112 Operability

Surveillance

1BwOSR

5.5.8.AF-3B

Group A IST Requirements for Unit 1 Diesel Driven

Auxiliary Feedwater Pump

1BwOSR

5.5.8.AF-4A

Unit One Comprehensive Testing (IST) Requirements

for 1A Auxiliary Feedwater Pump

1BwOSR

5.5.8.AF-4B

Unit One Comprehensive Testing (IST) Requirements

for 1B Auxiliary Feedwater Pump

BwMP 3305-003

Main Steam Safety Valve Testing Using Setpoint Verification

Device

Procedures

BwVS 500-6

Low Power Physics Test Program

71111.24

Work Orders

28760

Unit One 125V ESF Battery Charger 112 Capacity Test

10/11/2025

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

28761

PMT 1DC04E Functional Check per 1BwOSR 3.8.9.1

10/11/2025

5536091

Low Power Physics Test Program with Dynamic Rod Worth

Measurement

10/22/2025

5536100

DRPI Operability Checkout

10/22/2025

5539209

U1 AF Diesel Prime Mover Performance Surveillance

10/20/2025

5539633

Unit 1 SSPS, Rx BRKR, RX Trip BRKR Train A

10/20/2025

5540154

MSSV Operability Test

10/02/2025

5549001

Unit 1 AF Pumps Comprehensive Full Flow Test and

Equipment Response Time

10/01/2025

5553418

Perform A Full PM On Reactor Trip Breaker

10/19/2025

5588144

Unit 1 SSPS, Reactor Breaker, Reactor Trip Bypass Breaker

Train B

10/20/2025

23897

1B AF Pump Monthly Surveillance Run

10/20/2025

5735934

1CC9518 LLRT Failure

10/19/2025

Calculations

EP-AA-120-1001

Evaluation No.:

24-49

§50.54(q) Program Evaluation Assessment Review for

Standardized Radiological Emergency Plan Revision 34

2/28/2025

EPA-400/R-

17/001

PAG Manual: Protective Action Guides and Planning

Guidance for Radiological Incidents

01/2017

Miscellaneous

EPID L-2018-

LLA-0045

Issuance of Amendments to Revise the Emergency

Response Organization Staffing Requirements

03/21/2019

EP-AA-1000

Exelon Nuclear Standardized Radiological Emergency Plan

71114.04

Procedures

EP-AA-1000

Standardized Radiological Emergency Plan

71114.06

Miscellaneous

None

Braidwood SED [Site Emergency Director] Qualifying Drill

25

11/10/2025

4813791

U2 Leak Rate Deviation Action Level III Exceeded

10/31/2024

4814330

U2 Leak Rate Deviation Action Level II, Improved Leakage

11/01/2024

4815076

2BwOSR 3.4.13.1 Exceeds Deviation Action Levels II & III

11/04/2024

4817516

U2 RCS Leak Rate Action Level I Exceeded

11/14/2024

4818974

U2 Leak Rate Deviation Action Level II

11/21/2025

20205

U2 RCS Leak Rate Action Level II Exceeded

11/27/2024

25260

U2 RCS Leak Rate Exceeds Deviation Action Level III

2/20/2024

71151

Corrective Action

Documents

4836504

U1 RCS Leak Rate Reached Deviation Action Level I

2/11/2025

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

4863515

U1 Hand Calculation Leak Rate Values Action Level III

05/06/2025

4864195

U1 Hand Calculation Leak Rate Values Action Level II

05/08/2025

4888910

U1 RCS Leak Rate Action Level II Exceeded

08/06/2025

4890073

U1 RCS Leak Rate Exceeded Deviation Action Level I

08/13/2025

4890306

U1 RCS Leak Rate Deviation Action Level I Exceeded

08/13/2025

2713661

Review of IST Surveillance Test Results

09/08/2016

4394374

2A CV Pump D/P Less Than 2390 PSID

01/07/2021

24225

2A CV Pump Significantly Weaker than 2B CV Pump

05/18/2021

4682881

0BwOS FX-12 PCRA

06/06/2023

22420

Long Term FLEX Pump Storage Strategy

2/08/2023

4872335

0C High Head FLEX Pump Trip

06/11/2025

4890477

0FX02PC C High Head FLEX Pump Still Overheating

08/14/2025

Corrective Action

Documents

4901565

0FX02PC High Head FLEX Pump High Hydraulic Fluid Temp

09/29/2025

BRW-16-0001-E

Evaluation of the Effects of Emergency Diesel Generator

(EDG) Voltage and Frequency Variations on

Safety-Related Equipment Powered by EDGs

Report PP-CV-1

IST Eval PP-CV-1 2CV01PA

Report PP-CV-15

IST Eval PP-CV-15 CV01ASME Qtrly

11/19/2019

Report PP-CV-3

IST Eval PP-CV-3

Engineering

Evaluations

Report PP-CV-5

IST Evaluation PP-CV-05 2CV01PA

10/24/2009

Miscellaneous

None

CV Pump Performance Trending Data from 4th Qtr. 2022

thru 4th Qtr. 2025

10/27/2025

0BwOS FX-12

FLEX Pump Full Flow Test Surveillance

0BwOS FX-9

FLEX Pump Flow Surveillance

2BwOSR

5.5.8.CV-4A

Group A IST Requirements for 2A Centrifugal Charging

Pump (2CV01PA) and Check Valve 2CV8480A Stroke Test

2BwOSR

5.5.8.CV-4B

Group A IST Requirements for 2B Centrifugal Charging

Pump (2CV01PB) and Check Valve 2CV8480B Stroke Test

2BwOSR

5.5.8.CV-8

Comprehensive Inservice Testing (IST) Requirements for

Unit 2 Charging Pumps and Safety Injection System

Charging Check Valve Stroke Test

71152A

Procedures

CC-AA-118

Diverse and Flexible Coping Strategies (FLEX), Spent Fuel

Pool Instrumentation (SFPI), and Hardened Containment

Inspection

Procedure

Type

Designation

Description or Title

Revision or

Date

Vent System (HCVS) Program Document

CC-BR-118-1001

Site Implementation of Diverse and Flexible Coping

Strategies (FLEX) And Spent Fuel Pool Instrumentation

Program

4447069

Groundwater Intrusion Near 2SI8811A Needs Attention

09/17/2021

4701562

Groundwater Below 2SI8811A

09/10/2023

4742830

Ground Water Seeping in Around 2SI8811A Crosses CA

2/04/2024

4895612

Water Beneath U2 SI Can Valves Due to Clogged Catch

Basin

09/05/2025

Corrective Action

Documents

4899202

Trend in 2SI Penetration In-Leakage

09/19/2025

5195853

Groundwater In-Leakage Walkdown / Inspection - U2

Auxiliary Building 364' Penetration Area

07/08/2023

292795

Unit 2 - Area 7 Maintenance Rule Inspection_Aux Bldg 364

2/17/2025

71152S

Work Orders

5403593

Groundwater Below 2SI8811A

10/13/2024

4887138

OTDT Channel Investigation - U1 Reactor Trip

07/30/2025

4887148

1MS147B MCR Monitor Light is Dual Instead of Red

07/30/2025

71153

Corrective Action

Documents

4887512

W/O 5642969 Switchyard Ground Grid Testing to be

Pulled Up

07/30/2025