IR 05000445/2005301

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Er 05000445-05-301, 05000446-05-301; 3/28-30/2005; Comanche Peak Steam Electric Station, Initial Operator Licensing Examination Report, Abnormal Procedure Quality and Equipment Availability for Emergency Fill of the Condensate Storage Tank
ML051300070
Person / Time
Site: Comanche Peak  Luminant icon.png
Issue date: 05/09/2005
From: Gody A
Division of Reactor Safety IV
To: Blevins M
TXU Electric
References
50-445/05-301, 50-446/05-301 50-445/05-301, 50-446/05-301
Download: ML051300070 (12)


Text

May 9, 2005

SUBJECT:

COMANCHE PEAK STEAM ELECTRIC STATION - NRC EXAMINATION REPORT - 05000445/2005301, 05000446/2005301

Dear Mr. Blevins:

On March 29, 2005, the NRC completed an initial examination at your Comanche Peak Steam Electric Station. The enclosed report documents the examination findings, which were discussed on March 30, 2005, with Mr. Rafael Flores and other members of your staff.

The examination included an evaluation of three applicants for reactor and senior operator licenses. The written and operating examinations were developed using NUREG-1021,

"Operator Licensing Examination Standards for Power Reactors," Revision 9. We determined that two applicants satisfied the requirements of 10 CFR Part 55, and the appropriate licenses have been issued.

During the examination, the NRC identified one finding that was evaluated under the Significance Determination Process as having very low safety significance (Green). The NRC has also determined that a violation is associated with the finding. Consistent with Section VI.A of the Enforcement Policy, the violation is being treated as a noncited violation because it has been entered into your corrective action program. The violation is described in the subject examination report. If you contest the violation or its significance, you should provide a response within 30 days of the date of this examination report, with the basis for your denial, to the U.S. Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional Administrator, U.S. Nuclear Regulatory Commission, Region IV, 611 Ryan Plaza Drive, Suite 400, Arlington, Texas 76011; the Director, Office of Enforcement, U.S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Comanche Peak Steam Electric Station facility.

TXU Power-2-In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its enclosure will be available electronically for public inspection in the NRC Public Document Room or from the Publicly Available Records (PARS) component of NRCs document system (ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Anthony T. Gody Operations Branch Division of Reactor Safety Dockets: 50-445; 50-446 Licenses: NPF-87; NPF-89 cc w/enclosure:

Fred W. Madden, Director Regulatory Affairs TXU Power P.O. Box 1002 Glen Rose, TX 76043 George L. Edgar, Esq.

Morgan Lewis 1111 Pennsylvania Avenue, NW Washington, DC 20004 Terry Parks, Chief Inspector Texas Department of Licensing and Regulation Boiler Program P.O. Box 12157 Austin, TX 78711 The Honorable Walter Maynard Somervell County Judge P.O. Box 851 Glen Rose, TX 76043 Richard A. Ratliff, Chief Bureau of Radiation Control Texas Department of Health 1100 West 49th Street Austin, TX 78756-3189

TXU Power-3-Environmental and Natural Resources Policy Director Office of the Governor P.O. Box 12428 Austin, TX 78711-3189 Brian Almon Public Utility Commission William B. Travis Building P.O. Box 13326 Austin, TX 78711-3326 Susan M. Jablonski Office of Permitting, Remediation and Registration Texas Commission on Environmental Quality MC-122 P.O. Box 13087 Austin, TX 78711-3087

TXU Power-4-Electronic distribution by RIV:

Regional Administrator (BSM1)

DRP Director (ATH)

DRS Director (DDC)

DRS Deputy Director (KSW)

Senior Resident Inspector (DBA)

Branch Chief, DRP/A (WDJ)

Senior Project Engineer, DRP/A (TRF)

Team Leader, DRP/TSS (RLN1)

RITS Coordinator (KEG)

DRS STA (DAP)

J. Dixon-Herrity, OEDO RIV Coordinator (JLD)

RidsNrrDipmIipb CP Site Secretary (ESS)

SISP Review Completed: Y______ ADAMS: : Yes G No Initials: ______

Publicly Available G Non-Publicly Available G Sensitive
Non-Sensitive SOE:OB OE:OB C:OB C:PBA C:OB M. E. Murphy K. Clayton A.. T. Gody W. Johnson A. T. Gody

/RA/

/RA/

/RA/

/RA/

/RA/ MXH for 5/9/05 5/4/05 5/5/05 5/4/05 5/9/05 OFFICIAL RECORD COPY T=Telephone E=E-mail F=Fax

Enclosure-1-ENCLOSURE U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Dockets:

50-445; 50-446 Licenses:

NPF-87; NPF-89 Report No.:

05000445/2005301; 05000446/2005301 Licensee:

TXU Power Facility:

Comanche Peak Steam Electric Station Location:

Glen Rose, Texas Dates:

March 28-30, 2005 Examiner:

Michael E. Murphy, Senior Operations Engineer, Operations Branch Kelly Clayton, Operations Engineer, Operations Branch Approved By:

Anthony T. Gody, Chief Operations Branch Division of Reactor Safety

Enclosure-2-SUMMARY OF FINDINGS ER 05000445/2005301, 05000446/2005301; 3/28-30/2005; Comanche Peak Steam Electric Station, Initial Operator Licensing Examination Report, Abnormal Procedure Quality and Equipment Availability for Emergency Fill of the Condensate Storage Tank from the Fire Protection Water Stations.

NRC examiners evaluated the competency of three applicants; one for reactor operator license, and two for instant senior operator licenses at Comanche Peak Steam Electric Station, Units 1 and 2. The written examination was developed by the NRC staff and the operating test was developed by the licensee staff using NUREG-1021, "Operator Licensing Examination Standards for Power Reactors," Revision 9. The licensee administered the written examination to the applicants on March 24, 2005. The NRC examiners administered the operating test on March 28-29, 2005. The license examiners determined that two of the three applicants satisfied the requirements of 10 CFR Part 55, and the appropriate licenses have been issued. One Green noncited violation was identified. The significance of this finding is indicated by its color (Green, White, Yellow, Red) using Inspection Manual Chapter 0609, Significance Determination Process. The NRCs program for overseeing the safe operation of commercial nuclear power reactors is described in NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

NRC-Identified and Self-Revealing Findings Cornerstone: Mitigating Systems

Green. The examiners identified a noncited violation of Technical Specification 5.4.1 associated with an inadequate abnormal operating procedure. Specifically, the examiners determined that Procedure ABN-305, Auxiliary Feedwater System Malfunction, Revision 5, was not adequate, in that, Attachment 4 of the procedure did not have an accurate list of all the adapters required to complete the connections to the valves listed in the attachment. Additionally, adapters required in Attachment 4 to complete connections to perform an emergency fill of the condensate storage tank with fire protection water were not readily available. This deficiency was discovered while walking down a job performance measure task during examination validation week. The licensed senior operator that was used for the task validation could not locate the required fitting in the nearby cabinets for the valve required to be used to fill the condensate storage tank in the procedures attachment. Also, the attachment did not mention the specific types of adapters required for each of the different connection sources. The licensee is correcting the procedure to include information on the types of adapters required and the order of preference of these supply points for filling the condensate storage tank and has staged the proper adapters for each of the valve types in the area required by this procedure and has documented this issue in Condition Report/Smart Form SMF-2005-001022-00.

Enclosure-3-The finding is a performance deficiency in that the licensee failed to identify that the proper equipment was not readily available and the procedure did not correctly identify the required fittings for each of the possible supply valve choices. The finding is more than minor because it affects the Mitigating Systems Cornerstone of procedural quality and equipment performance, in that, it could result in a failure to locate and use the proper equipment to fulfill the abnormal procedure, Attachment 4, when the condensate storage tank is at a low level. Using the Phase 1 worksheet in Manual Chapter 0609, Significance Determination Process, this finding is determined to be of very low safety significance because there was no actual loss of a safety function (Section 1R04).

Enclosure-1-Report Details 1.

REACTOR SAFETY Cornerstone: Mitigating Systems 1R04 Equipment Alignment b.

Examination Scope The examiners were walking down a systems examination task - an in-plant Job Performance Measure P3 - to ensure that all tasks were relevant and accurately reflected in the standard prior to administering the exam. The Job Performance Measure P3 task required alternate filling of the condensate storage tank with fire protection water, using a fire hose station and adapters as required in the procedure.

b.

Findings Introduction. A Green noncited violation of Technical Specification 5.4.1 was identified for an inadequate procedure associated with alternate filling of the condensate storage tank with fire protection water during abnormal conditions.

Description. On March 1, 2005, while validating the operating test portion of an initial license examination, the examiners were walking down an in-plant Job Performance Measure P3 that utilized Abnormal Procedure ABN-305, Auxiliary Feedwater Malfunction. This job performance measure required the operator to simulate filling the condensate storage tank from fire protection water using a local fire station hose and a quick-disconnect, pneumatic-style adapter for the valve specified in Job Performance Measure P3. The licensed senior operator utilized as the examination candidate could not find the required adapter for the valve near the location of the fire station nor in several cabinets located inside the radiologically controlled area where these adapters are stored. Also, the procedure did not list the pneumatic-style of adapter required for the valve specified in the task to be validated. The other adapters listed could not be used for the specified valve to fill the condensate storage tank. Because of the potential impact on actual plant safety the task was removed from the examination and the issue was released to the licensee in order for corrective actions to be implemented. The licensee created an entry into their respective corrective action program for the missing adapters and a procedure change for the valve that required the pneumatic-style adapter, Condition Report/Smart Form SMF-2005-001022-00.

Analysis. The finding is a performance deficiency in that the licensee failed to identify that the proper equipment was not readily available and the procedure did not correctly identify the required adapters for each of the possible supply valve choices. The finding is more than minor because it affects the Mitigating Systems Cornerstone for procedure quality and equipment performance in that it could result in a failure to locate and use the proper equipment to fulfill the abnormal procedure, Attachment 4, when the condensate storage tank is at a low level. The finding is of very low safety significance

Enclosure-2-(Green) because the finding did not result in a loss of safety function and other sources of water to the auxiliary feedwater pumps were available. This finding was evaluated using the At-Power Situations Significance Determination Process.

Enforcement. Technical Specification 5.4.1 requires, in part, that written procedures be established, implemented, and maintained as recommended in Appendix A of Regulatory Guide 1.33, "Quality Assurance Program Requirements (Operation),"

Revision 2, February 1978. Regulatory Guide 1.33, Revision 2, Appendix A, provides the typical activities that should be covered by written procedures. Section 5 requires procedures for combating abnormal, off-normal, or alarm conditions.

Contrary to the above, Procedure ABN-305, Attachment 4, Revision 5, failed to implement proper equipment requirements for certain valves available to fill the condensate storage tank. Also, the licensee failed to have some of the equipment available that would be necessary to fill the tank using this procedure. Because this example of an inadequate procedure is of very low safety significance and has been entered into the licensees corrective action program (SMF-2005-001022-00), this violation is being treated as a noncited violation, consistent with Section VI.A of the NRC Enforcement Policy: Noncited Violation 05000445;05000446/2005301-01, Inadequate Procedure ABN-305, Revision 5.

4.

OTHER ACTIVITIES (OA)

4OA4 Initial Operator License Examination 1.

Operator Knowledge and Performance c.

Scope On March 24, 2005 the Licensee administered the written examination to the applicants.

The licensee graded the examination, analyzed the results, and submitted the final package on March 31, 2005.

The NRC examiners administered the operating test portion of the examination on March 28-29, 2005. The three applicants participated in three dynamic simulator scenarios. The two applicants for senior operator licenses participated in a control room and facilities walkthrough test consisting of 10 system tasks, and an administrative test consisting of 5 administrative tasks. The applicant for a reactor operator license participated in a control room and facilities walkthrough test consisting of 11 system tasks, and an administrative test consisting of four administrative tasks.

d.

Findings The two applicants for senior operator license passed the written examination. The overall written examination grade average was 81 percent.

Enclosure-3-The licensee conducted a performance analysis for the written examination to determine if there were any knowledge weakness commonalities or training issues associated with the questions missed by the applicants and submitted this analysis to the chief examiner for review on March 31, 2005. The licensee did not identify weaknesses or training issues. The chief examiner reviewed the facilitys submittal and concurred with the results.

The final written examinations and answer keys, as well as the licensees post examination analysis can be viewed in the NRCs document management system (ADAMS) under the accession numbers referenced in the attachment to this report.

All three applicants passed the operating test portion of the examination.

2.

Initial Licensing Examination Development a.

Scope The NRC developed the written examination in accordance with NUREG-1021, Revision 9, using facility training and operations staff on the security agreement to validate the written examination. The facilitys training staff developed the operating examination. The training staff also assisted the NRC examiners in validating the operating examination during the week of February 28, 2005.

b.

Findings One noncited violation involving an inadequate procedure was identified during the examination validation, which is documented in Section 1R04.

There were a number of minor violations found during examination development, such as an inadequate abnormal operating procedure entry condition, that were not documented in the report. These minor violations were placed in the licensee's corrective action program.

The reference materials provided to the NRC were also inadequate, in that, they were several years old and did not include training objective links to the knowledge and abilities prescribed in NUREG-1122, Knowledge and Abilities Catalog for Nuclear Power Plant Operators: Pressurized Water Reactors," Revision 1. The licensee acknowledged the finding after the examination was administered and determined that there was no impact on examination validity.

3.

Simulation Facility Performance a.

Scope The examiners observed simulator performance with regard to plant fidelity during the examination validation and administration.

Enclosure-4-b.

Findings No findings of significance were identified.

4.

Examination Security a.

Scope The examiners reviewed examination security both during the onsite preparation week and examination administration week for compliance with NUREG-1021 requirements.

Plans for simulator security and applicant control were reviewed and discussed with licensee personnel.

b.

Findings No findings of significance were identified.

4OA6 Management Meeting Exit Meeting Summary On March 30, 2005, the examiners presented the examination results to Mr. Rafael Flores and other members of the licensees staff who acknowledged the findings. The inspectors confirmed that proprietary information was not provided or reviewed during the examination process.

ATTACHMENT: SUPPLEMENTAL INFORMATION

Attachment A-1 SUPPLEMENTAL INFORMATION KEY POINTS OF CONTACT Licensee personnel T. Clooszr, Shift Operations Manager C. Dillard, Training Instructor G. Ellis, Training Supervisor S. Ellis, Director, Nuclear Overview R. Flores, VP of Nuclear Operations M. Lucas, VP of Nuclear Engineering F. Madden, Director, Regulatory Affairs S. Sewell, Nuclear Training Manager R. Slough, Nuclear Technologist, Regulatory Affairs R. Smith, Operations Director G. Struble, Training Supervisor T. Werk, Training Instructor NRC personnel Don Allen, Senior Resident Inspector Fred Sanchez, Resident Inspector ITEMS OPENED AND CLOSED Opened and Closed 05000445; 05000446/2005-301-01 NCV Inadequate Procedure ABN-305, Filling the Condensate Storage Tank with Fire Protection Water (1R04)

ADAMS DOCUMENTS REFERENCED Accession No. ML051230431 Final Written Examination and Answer Key Accession No. ML051230435 Final Operating Examination and Answer Key Accession No. ML051230437 Post Examination Analysis