IR 05000315/1988016

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Insp Repts 50-315/88-16 & 50-316/88-18 on 880711-0808. Violations Noted.Major Areas Inspected:Maint Activities Using Selected Portions of Insp Procedures 62700,62702, 62704,62705 & 62720
ML17325A914
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 08/23/1988
From: Ted Carter, Choules N, Eick S, Jablonski F, Tella T
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17325A912 List:
References
50-315-88-16, 50-316-88-18, NUDOCS 8808300212
Download: ML17325A914 (14)


Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

Reports No. 50-315/88016(DRS);

50-316/88018(DRS)

Docket Nos.

50-315; 50-316 Licenses No. DPR-58; DPR-74 Licensee:

American Electric Power Service Corporation Indiana'

Michigan Power Company 1 Riverside Plaza Columbus, OH 43216 Facility Name:

D.C.

Cook Nuclear Plant, Units 1 and

Inspection At:

D.C.

Cook Site, Bridgman, Michigan Inspection Conducted:

July 11-15, 18-22, 27, and August 8, 1988 Inspectors:

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C. Choules Date

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H. Car er Dat Da e

T. Tella 8 zg8s Date Approved By:

a k J. Jablonski, Chief Maintenance and Outages Section Date Ins ection Sumar Ins ection on Jul 11-15, 18-22 27, and Au ust 8, 1988 Re orts No. 50-315/88016 DRS 50-316/88018 DRS Areas Ins ected:

Routine, announced inspection of maintenance activities using se ecte portions of Inspection Procedures 62700, 62702, 62704, 62705, and 62720.

Results:

Control in some of the areas inspected appeared to be weak.

Based on this inspection, the inspectors reached the following conclusions:

Maintenance was accomplished, effective, and self assessed; however, continued aggressive and significant involvement by management is needed to reduce the backlog of job orders.

8808300212 880823 PDR ADOCK 05000315 PNU

Continued management involvement is needed to implement the recommendations of the licensee's self assessment including upgrade of the preventive maintenance (PM) program.

Housekeeping and material condition of the plant was adequate and the threshold for placing equipment problems on maintenance job orders appeared sufficient to maintain the material condition.

Coordination of contractor and site maintenance personnel was well planned and effective for the accomplishment of maintenance, and the program for improving motor operated valve performance appeared to be adequate.

equality verification was not always effective in producing performance oriented audits.

At times, action to correct audit findings was poor, however, the persistence of the quality organization at getting matters corrected was perceived as a strength.

Management's approach to resolution of technical issues from a safety standpoint was not adequate as shown in the violation described in Section 2. DETAILS 1.

Persons Contacted Indiana and Michi an Electric Com an 18REC

""W. Smith, Jr., Plant Manager

~"K. Baker, Operations Superintendent

  • T. Bei lman, Instrumentation and Calibration Superintendent

"A. Blind, Assistant Plant Manager, Organization and Administration

"J. Droste, Maintenance Superintendent

"D. Gallagher, Maintenance Administrative Comp'liance Coordinator

~L. Gibson, Assistant Plant Manager, Technical T. Postlewait, Technical Superintendent, Engineering

  • J. Rutkowski, Assistant Plant Manager, Production

~D. Wizner, Maintenance Production Controller U.S. Nuclear Re viator Commission USNRC)

~B. Jorgengen, Senior Resident Inspector

~*J. Heller, Resident Inspector

"Indicates those attending the exit meeting at D.C.

Cook Plant on July 27, 1988.

""Indicates those attending the exit meeting at D.C.

Cook Plant on August 8, 1988.

Other licensee personnel were contacted as a matter of routine during the inspection.

2.

Evaluation and Assessment of Maintenance The purpose of this inspection was to evaluate and assess the accomplishment and effectiveness of maintenance activities at D.C.

Cook.

The evaluation and assessment were accomplished by:

Review of Preventive Maintenance Program Review of Motor Operated Valve Improvement Plan Evaluation of maintenance backlog Review of completed job orders Observation of maintenance activities Evaluation of maintenance rework Walkdown of plant systems

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Review of training records This inspection also assessed the quality verification process related to maintenance, which was accomplished by:

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Review of audit and surveillance reports Review of the licensee's self assessment reports 2. 1 Preventive Maintenance Pro ram PM The equipment included in the PM program did not appear complete.

For instance, balance of plant (BOP) motor operated valves (MOV) and motors were not included in the program.

However, a program was developed for diagnostic testing of all safety-related (SR)

MOVs and some BOP MOVS important to safety or with recurring problems.

The program included PM diagnostic testing, parts and procedures.

The PMs were based on vendor recommendations and operating history.

Approximately 33Ã of the safety-related (SR) valves receive a general inspection and lubrication change-out during every 18 month refueling outage.

The current MOV program appeared adequate and the final program was scheduled to be implemented in July 1989.

Administration of the PM program was not computerized and continued reviews of the program to expand or decrease PM items had not been established.

This same weakness was identified during the licensee's self assessment of PM.

The licensee plans to upgrade both the administrative and equipment aspects of the PM program, but will not be completed until late 1989.

Review of equipment failures and interviews with licensee personnel indicated that there had been few failures due to the lack of PMs, especially with MOVs.

2.2 Accom lishment of Maintenance Maintenance Backlo The inspectors reviewed the licensee's system for monitoring the backlog of PM and corrective maintenance (CM) job orders (JO).

On July 19, 1988, the total JO backlog was approximately 5100.

There had been an increase of about 1200 JOs due to the Unit 2 outage that began in April 1988.

The non-outage CM JO backlog was about 1300.

There had been little change in this backlog due to the outage.

The total PM backlog was 363 with a moderate 132 non-outage PM backlog.

Most of the non-outage backlog was less than 90 days old or written before the PM was required to be performed.

Review of data submitted to INPO for the first quarter of 1988 indicates that 95K of the PMs were performed within the specified interval The total number of JOs initiated during 1988, up to July 27, 1988, was 8676.

A total of 7096 JOs were completed.

The backlog was difficult to judge at the time of the inspection because there were so many outage related JOs.

The licensee does not estimate the man-hours to do JOs, which hampered the determination of additional manpower.

This weakness was identified in the licensee's self assessment performed in late 1987.

The inspectors reviewed computer printouts of all uncompleted CM JOs.

The review indicated adequate technical reasons for not being completed and the operability of equipment required by the Technical Specification was not jeopardized.

2.2.2 Com leted Job Orders Forty completed job orders (JO) were selected and reviewed for identification of equipment, description of problem, adequacy of work instructions, description of work performed, replacement parts used, required approvals, required post-maintenance testing, and Technical Specifications (TS) operability tests, if applicable.

Work instructions usually referenced an existing PM or CM maintenance procedure.

These procedures were detailed and adequately addressed equipment repairs needed.

Post maintenance and TS operability tests were referenced and results documented on a Technical Specification and Testing (TST) form.

A weakness was identified in the documentation on JOs of

"as-found" conditions of equipment needing repair.

Although the lack of documentation does not appear to be a safety issue, the licensee will consider adding a section to the JO form that specifically addresses root cause evaluations.

2.2.3 Summar of Maintenance Accom lishment The backlog of maintenance indicated that CM and PM was being accomplished.

Nothing in the backlog indicated a negative effect on system operabi 1 ity.

Documentation of "as found" conditions was such that root causes of problems could not be analyzed.

No violations were identified.

2.3 Effectiveness of Maintenance Rework The licensee did not have a formal program to keep track of rework.

The licensee's Safety Assessment Group tracks equipment failures by use of a Consolidated Trend Program (KTP) based on condition reports.

However, only a limited number of equipment failures were identified by condition reports.

For example, a review of a Nuclear Reliability Data System (NPRDS) printout indicated that containment isolation valve CCR-441 had a diaphragm failure three times in two month These failures were not identified in a Condition Report; therefore, the failures were not tracked through KTP.

After investigating this event, the licensee determined that improper maintenance on the second failure appeared to be the root cause of the third failure identified during post-maintenance testing.

By review of air actuator and valve diaphragm replacements the inspector determined that approximately 6X were replaced per year.

Although no immediate safety concerns existed, management should be more sensitive to identifying repetitive failures through JO.tracking/trending.

This same tracking weakness was identified during the maintenance self-assessment.

Com onent Coolin Water CCW)

S stem The inspectors reviewed the CCW system LERs, NPRDS reports, system diagrams, procedures, maintenance records, and performed a

CCW system walkdown to determine if the system was being properly maintained.

The inspectors verified that Technical Specification surveillance requirements of verifying CCW valve positions and pump discharge pressure were being performed by review of completed surveillance records.

The inspectors reviewed the PM program for the CCW system and verified from review of PM records that PMs were being performed as specified.

PMs on the CCW system included pumps, valves electrical breakers, and MOVs.

During the walkdown of the kCW system, using drawings, the inspector verified that as-built status of the plant, matched the drawings.

No items of concern were identified during the review of the CCW system.

Containment Pur e and Containment Isolation Valves Containment Purge and Containment Isolation Valves records were reviewed to ensure PMs were completed and the work history was evaluated to identify any possible adverse trends.

No problems or concerns were noted in the review.

Appropriate PMs, surveillances, and post-maintenance testing were performed after maintenance work.

A Request For Change (RFC) 12-2877 was also reviewed during this inspection.

The RFC required an installation of a drive lock pin in all Containment Purge valves installed in the non-horizontal position.

This change helped prevent a downward shift of the valve

'isc on its seat which could cause seat leakage.

This problem was identified during leak testing of the purge valves and subsequent discussions with the vendor.

All 10 CFR 50.59 reviews were complete and all valves were appropriately tested after the design change.

DC Ground Detection S stem The inspectors reviewed the operation of the 250 Vdc ground detection system and associated operating procedures.

Interviews with operations personnel indicated an attempt to find and correct a ground was performed at the time a ground was annunciated in the control room.

Procedure 1-OHP 4021.012,

"Location 250 VDC Grounds,"

Revision 2, provided guidance for locating a ground.

Personnel were aware that one ground could mask another groun The inspectors noted that there was a negative ground on the Unit 1 CD battery system.

The ground had existed since January 5, 1988.

Several attempts were made by the licensee to isolate equipment and locate the ground, but were unsuccessful.

The licensee stated that a plant outage would be required to locate the ground because some equipment could not be isolated during normal operations.

The inspectors inquired if the licensee had performed and documented a safety evaluation regarding continued operations with the ground.

The licensee indicated an evaluation had not been performed.

In a telephone conversation between the licensee and Region III on July 28, 1988, the licensee committed to perform a'afety evaluation.

On August 8, 1988, the inspectors reviewed a safety evaluation that was prepared on August 5, 1988.

The safety evaluation was incomplete in that it did not address whether the operability status of a system would be indicated to the operators if fuses were blown should the ungrounded polarity also become grounded.

The licensee agreed to review the system for potential indication and equipment operability due to blown fuses.

The inspectors noted that FSAR Section 8.3.4 stated

"The battery distribution switch board consists of several metal-clad structures and each with a 250 Vdc, 2-wire ungrounded main bus;" indicating the battery systems normally operated ungrounded.

Although the licensee had attempted to locate the ground, corrective action was incomplete in that no technical evaluation was performed to ensure that operability of safety-related equipment was not effected by the ground.

Failure to complete proper corrective action regarding long term operation of the plant with the ground is a violation of 10 CFR 50 Appendix B, Criterion XVI (315/88016-01).

During the review of the operations of the ground detection system, the inspectors noted that there was no continuous recording of the magnitude (voltage) of a ground, nor were personnel required to record the voltage when the ground annunciator alarmed.

During the telephone conversation on July 28, 1988, the licensee committed to record the ground voltage once a shift whenever a ground alarm is noted in order to identify any new grounds that may be masked.

Plant Observations and S stems Walkdowns The overall material condition of the plant appeared to be adequate based on the inspector's walkdown of several portions of the Component Cooling Water (CCW) and Containment Purge Systems.

MOV stems appeared to be lubricated and various pump oil levels were noted as acceptable.

JO tags were noted during the walkdowns and were identified on the open JO list with one exception.

A JO tag (727902)

was noted in the control room and during followup was identified as completed and closed in September 1987.

The JO tag was removed by the licensee during the inspection and was an isolated finding.

The inspectors observed the conditions for which JOs were written for diesel generator (DG) fuel oil transfer pump leaks, DG related oil leaks, a battery leak, a fan bearing high temperature, and an

auxiliary feedwater steam turbine isolation valve (1 MCM-221)

packing leak.

The leaks and temperature anomaly were minor.

The threshold for writing work requests appeared to be low, which is considered a strength.

The inspectors noted that the 1 MCM-221 valve, which was leaking a small amount of steam was not isolable and required a plant shutdown and cooldown to repair.

Interviews with engineering personnel indicated the leakage was being closely monitored and there had been no change since April 1988.

2.3.6 2. 3. 6. 1 Val ve Maintenance During the performance of MOVATS testing of valve 2-ICM-251 according to JO 24366, the inspector noted a well-coordinated work environment with contractor, licensee, and MOVATS personnel.

This coordination appeared to be effective in the accomplishment of the maintenance activity.

During observation of the replacement of valve 2-CMO-413 according to JO 28351, the inspector noted that the replacement valve appeared to be different than the original valve.

Craft personnel indicated that the adjacent valve 2-CM0-411, would also be replaced.

Further investigation of the replacement indicated that valve 2-CMO 413 was a Pratt butterfly valve replaced with a like-for-like valve.

However, valve 2-CMO-411 was a Centerline butterfly valve, that would be replaced with a Pratt butterfly valve.

Since like-for-like valves were not being used for the 2-CMO-411 replacement, a minor modification was issued.

All engineering and design reviews, including a 10 CFR 50.59 review, were completed and approved according to Procedure PMP 5040 MOD.002, "Minor Modifications," Revision 0.

2.3.6.2 Electrical Circuit Breaker Maintenance The inspectors observed maintenance (cleaning and adjustment)

of two Pressurizer Heater Circuit breakers (600/480 volt).

The work was conducted in accordance with procedures.

The equipment used was in calibration per the attached stickers.

The replacement arc chute used on one of the breakers was traced for conformance to procurement requirements.

The part was procured as safety-related and certificates of Compliance and Conformance were verified by AEP engineers.

2.3.6.3 Calibration of Pressure Indicatin Transmitter The inspectors observed a portion of the calibration of a Pressurizer Indicating Transmitter by I8C personnel.

The pressure gauges used for the calibration had current calibration stickers and personnel performed the calibration in accordance with the calibration procedure for the transmitte.3.6.4 Essential Service Water Pum Re lacement The inspectors observed the removal of the Unit 2 West Essential Service Water Pump.

Performance of this pump and the causes for its replacement were discussed with the responsible performance engineers.

The original pump was replaced because performance had degraded over the years.

The replacement pump was removed after one month because it failed to meet the manufacturer's performance curves.

The pump's developed head was about ten feet less than the manufacturer's data over its entire operating range.

On July 22, 1988, a new pump was installed, but the test data also did not correlate with the manufacturer's data.

The ESW pump developed 9800 gpm at a total developed head of-142 feet, which is about 93X of the head as shown on the manufacturer's pump curve.

Table 9.8.5 of the FSAR requires the ESW pump to develop 10,000 gpm flow at a total developed head of 145 feet.

The low developed head is an unresolved item, pending further testing and evaluation by the licensee'316/88018-01).

2.3.6.5

~Tnainin Training and qualification records were reviewed for maintenance personnel that participated in maintenance activities witnessed by the inspectors.

Training files were readily available.

The inspectors determined from review of the training records that personnel were qualified to perform the assigned maintenance activities.

2.3.7 Summar of Maintenance Effectiveness Containment purge and isolation valves received appropriate PM, surveillance, and post maintenance testing after maintenance work.

Coordination of contractor and licensee maintenance personnel was well planned and effective.

Engineering support was evident in the minor modification effort of valve replacements.

Corrective action was not effective for a chronic dc ground condition.

No formal method was used to keep track of maintenance rework.

Craft personnel appeared knowledgeable and exhibited skills appropriate to the task.

Housekeeping and material condition of the plant was adequate.

One violation was identifie. 4 Licensee

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Assessment of Maintenance ual it Verification)

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The inspectors reviewed audit reports, corrective action documents, NPRDS equipment fa>lure pr>ntouts, and a self-assessment report to evaluate the licensee's quality verification process.

The documents were reviewed for root cause analysis, timely corrective action, technical assessments, and justifications for closeout of corrective action documents.

2.4.1 Review of Audits and Survei-llances The inspector reviewed maintenance audits conducted in 1986, 1987 and 1988.

Audits performed in 1986 and early 1987 were very program oriented with little observation of work activities.

In late 1987 and 1988 audits were more performance oriented and included some observation of work activities to verify that procedures were followed, and maintenance personnel were qualified to perform the maintenance observed, however, audits could still be more performance oriented if more maintenance activities were observed and evaluated for technical adequacy.

The inspectors noted that gA and gC had performed numerous surveillances of maintenance activities and had identified some problems.

The inspectors reviewed several surveillance and audit indexes.

Tracking of audits and surveillance findings appeared to be good.

The inspectors noted that gA does not accept just any corrective action.

A few items were sent back to the groups responsible for corrective action three or four times.

This was considered a

strength for gA but a weakness for the respondents.

Response to audit items were timely and usually adequate.

The inspector reviewed auditor qualifications and noted there was a good mixture of backgrounds including experience with mechanical, electrical, radiation protection, chemistry, ASME/NDE, and security.

2.4. 2 Review of Licensee's Self-Assessment The licensee performed a

INPO self-assessment of maintenance in late 1987.

The self-assessment report was published February 10, 1988.

The report identified several findings and included recommendations to make improvement.

As indicated throughout this report, weaknesses identified by the inspectors were also identified during the self-assessment.

The inspectors discussed with the maintenance superintendent the licensee's plans to implement the recommendations of the self-assessment report.

The licensee delayed action on most of the recommendations until an INPO corporate evaluation, which included maintenance, was completed.

The evaluation was recently completed and the licensee had the results in rough draft.

During August 1988, the licensee will put together a Maintenance Policy that will include the self-assessment recommendations.

Implementation of the maintenance policy will follow with complete implementation expected by late 1989.

2.4.3 Summar of Licensee's Assessment ( ualit Verification of Maintenance Audits of performance should be improved.

Tracking of audit and surveillance findings was good.

gA's threshold for accepting corrective action on findings was high and is considered a strength.

The fact that a few groups had to respond three or four times to a gA finding is considered a weakness.

2.5 Conclusions Based on inspection activities described in this report, the inspectors concluded that:

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Continued management involvement is needed to implement the recommendations of the licensee's self assessment including upgrade of the preventive maintenance (PM) program.

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Housekeeping and material condition of the plant was adequate and the threshold for placing equipment problems on maintenance job orders appeared sufficient to maintain the.material condition.

Coordination of contractor and site maintenance personnel was well planned and effective for the accomplishment of maintenance, and the program for improving motor operated valve performance appeared to be adequate.

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equality verification was not always effective in producing performance oriented audits.

At times, action to correct audit findings was poor, however, the quality organization persistence at getting matters corrected was perceived as a strength.

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Management's approach to resolution of technical issues from a safety standpoint was not adequate as shown in the violation described in Section 2.3.4.

4.0 Unresolved Items Unresolved items are matters about which more information is required in order to ascertain whether they are acceptable items, violations, or deviations.

An unresolved item disclosed during this inspection is included in Paragraph 2.3.6.4.

5.0 Exit Interview The inspectors met with licensee representatives (denoted in Paragraph 1)

on July 27 and August 8, 1988, and summarized the purpose and findings of the inspection.

The inspectors discussed the likely content of the inspection report with regard to documents or processes reviewed by inspectors during the inspection.

The licensee identified the maintenance self-assessment report as proprietary.