IR 05000277/1987029
| ML20148T912 | |
| Person / Time | |
|---|---|
| Site: | Peach Bottom |
| Issue date: | 01/14/1988 |
| From: | Linville J, Williams J NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML20148T839 | List: |
| References | |
| 50-277-87-29, 50-278-87-29, IEB-87-002, IEB-87-2, NUDOCS 8802030420 | |
| Download: ML20148T912 (31) | |
Text
. __ _ _ _ _ _ ____ ____
_. _ _ _ _ _
.
..
.
I
'
~
- ,
.
U. S. NUCLEAR REGULATORY COMMISSION
!
- -
REGION I
Docket / Report No. 50-277/87-29 License No. DPR-44 i
50-278/87-29 DPR-56 Licensee: Philadelphia Electric Company
,
2301 Market Street
!
Philadelphia, Pennsylvania 19101 Facility Name:
Peach Bottom Atomic Power Station Units 2 and 3
-
Inspection At:
Delta, Pennsylvania Dates: November 28 - December 31, 1987 Inspectors:
T. P. Johnson, Senior Resident Inspector
!
R. J. Urban, Resident Inspector
,
L. 7. Myers, esident Inspector
,
Reviewed By-b N
. f>Tfiams, Fr,
Engineer
' d te
Approved By:
' h-
/
/ //
Jg. ; LWT111e, Chief, '
/ dat'e Jteactor Projects.Section 2A, t
sfvision of React 6r Projects i
,
Summary t
Areas Inspected:
Routine, on site regular and backshift resident inspection f
(107 hours0.00124 days <br />0.0297 hours <br />1.76918e-4 weeks <br />4.07135e-5 months <br /> Unit 2; 109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br /> Unit 3) of accessible portions of Unit 2 and 3,
operational safety, radiation protection, physical security, control room
activities, licensee events, surveillance testing, refueling and outage
activities, maintenance, and outstanding items.
.
Results:
Four unresolved items were identified:
(1) the seismic adequacy of the control room panels (section 4.1.15); (2) failures with GE-AM-4.16-250 General Electric breakers (section 4.2.5); (3) diesel
generator lube oil fires in the exhaust manifold (section 4,4); and, (4)
copper contamination of the Exide 125 VDC batteries (section 8.2).
The l
,
implementation of the QC shift monitors was reviewed (section 4.1.1).
.
Operator and shift manager response and followup critique of a partial loss i
of off site power was good (section 4.2.7).
Numerous security events
occurred including security force member post abandonment and inattentiveness (section 10.0).
r
!
.
I
$
$77 POR
-
.
_
.
_.
.-
-_ _
-
-.
,
.
!
.
.
.=
.,
.. -
.
.
SUMMARY (NON-SAFETY RELATED)
SAMPLE ITEM MATL.
COMMENT
1/2" Capscrew J429 Gr5 Manuf. KS
5/8" Bolt A325 Manuf. KS
5/8" Nut A325
5/8" Capscrew J429 Gr5 Manuf. A
3/4" Nut A194 Gr4 Manuf. J
1-1/2" Stud A193 B7
3/8" Capscrew J429 Gr5 Manuf. A
7/8" Stud Stock A193 B16 Unmarked
5/8" Stud Stock A193 B16 Unmarked
3/4" Stud Stock A193 B7 Unmarked
Nut A194 Gr2
7/8" Nut A194 Gr2H Manuf. H
7/8" Nut A194 Gr2H
3/4" Bolt A325
3/4" Nut A325 Manuf. H i
9/16" Capscrew A193 B8
' Unmarked
'
9/16" Capscrew A193 B8 Unmarked
Nut A194 Gr2 Unmarked
Nut A194 Gr2 Unmarked
3/4" Nut A194 Gr4 Manuf. J
5/8" Nut A194 Gr2H
. -
t
i T
a-
.-
--
. _ - _.,.
_._
-, _ - -. _
__,,,
_._.,-y..
,.
-4 y my,-
y