IR 05000277/1987029

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Insp Repts 50-277/87-29 & 50-278/87-29 on 871128-1231.No Violations Noted.Major Areas Inspected:Operational Safety, Radiation Protection,Physical Security,Control Room Activities,Licensee Events,Surveillance Testing & Maint
ML20148T912
Person / Time
Site: Peach Bottom  Constellation icon.png
Issue date: 01/14/1988
From: Linville J, Williams J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20148T839 List:
References
50-277-87-29, 50-278-87-29, IEB-87-002, IEB-87-2, NUDOCS 8802030420
Download: ML20148T912 (31)


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U. S. NUCLEAR REGULATORY COMMISSION

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REGION I

Docket / Report No. 50-277/87-29 License No. DPR-44 i

50-278/87-29 DPR-56 Licensee: Philadelphia Electric Company

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2301 Market Street

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Philadelphia, Pennsylvania 19101 Facility Name:

Peach Bottom Atomic Power Station Units 2 and 3

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Inspection At:

Delta, Pennsylvania Dates: November 28 - December 31, 1987 Inspectors:

T. P. Johnson, Senior Resident Inspector

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R. J. Urban, Resident Inspector

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L. 7. Myers, esident Inspector

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Reviewed By-b N

. f>Tfiams, Fr,

Engineer

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Approved By:

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Jg. ; LWT111e, Chief, '

/ dat'e Jteactor Projects.Section 2A, t

sfvision of React 6r Projects i

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Summary t

Areas Inspected:

Routine, on site regular and backshift resident inspection f

(107 hours0.00124 days <br />0.0297 hours <br />1.76918e-4 weeks <br />4.07135e-5 months <br /> Unit 2; 109 hours0.00126 days <br />0.0303 hours <br />1.802249e-4 weeks <br />4.14745e-5 months <br /> Unit 3) of accessible portions of Unit 2 and 3,

operational safety, radiation protection, physical security, control room

activities, licensee events, surveillance testing, refueling and outage

activities, maintenance, and outstanding items.

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Results:

Four unresolved items were identified:

(1) the seismic adequacy of the control room panels (section 4.1.15); (2) failures with GE-AM-4.16-250 General Electric breakers (section 4.2.5); (3) diesel

generator lube oil fires in the exhaust manifold (section 4,4); and, (4)

copper contamination of the Exide 125 VDC batteries (section 8.2).

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implementation of the QC shift monitors was reviewed (section 4.1.1).

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Operator and shift manager response and followup critique of a partial loss i

of off site power was good (section 4.2.7).

Numerous security events

occurred including security force member post abandonment and inattentiveness (section 10.0).

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$77 POR

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SUMMARY (NON-SAFETY RELATED)

SAMPLE ITEM MATL.

COMMENT

1/2" Capscrew J429 Gr5 Manuf. KS

5/8" Bolt A325 Manuf. KS

5/8" Nut A325

5/8" Capscrew J429 Gr5 Manuf. A

3/4" Nut A194 Gr4 Manuf. J

1-1/2" Stud A193 B7

3/8" Capscrew J429 Gr5 Manuf. A

7/8" Stud Stock A193 B16 Unmarked

5/8" Stud Stock A193 B16 Unmarked

3/4" Stud Stock A193 B7 Unmarked

Nut A194 Gr2

7/8" Nut A194 Gr2H Manuf. H

7/8" Nut A194 Gr2H

3/4" Bolt A325

3/4" Nut A325 Manuf. H i

9/16" Capscrew A193 B8

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9/16" Capscrew A193 B8 Unmarked

Nut A194 Gr2 Unmarked

Nut A194 Gr2 Unmarked

3/4" Nut A194 Gr4 Manuf. J

5/8" Nut A194 Gr2H

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