IR 05000219/1999009

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Inspection 05000219/1999009 003676745
ML003676745
Person / Time
Site: Oyster Creek, 07201004
Issue date: 01/21/2000
From: Eselgroth P
Division of Nuclear Materials Safety I
To: Levin S
GPU Nuclear
References
05000219 IR 1999009
Download: ML003676745 (24)


Text

January 21, 2000

SUBJECT:

NRC INTEGRATED INSPECTION REPORT NO. 05000219/1999009

Dear Mr. Levin:

On January 2, 2000, the NRC completed an integrated inspection at your Oyster Creek reactor facility. The enclosed report presents the results of that inspection.

During the eight-week period covered by this inspection report, your conduct of activities at the Oyster Creek facility was characterized by safe operations, sound engineering and maintenance practices, and careful radiological work controls.

Selected aspects of the radiological controls program were also reviewed, including contamination control practices, calibration of area radiation monitors and 1999 quality assurance audits and surveillances of the radiation protection program. Overall, these areas were deemed satisfactory.

Based on the results of this inspection, the NRC has determined that one Severity Level IV violation of NRC requirements occurred. This violation is being treated as a Non-Cited Violation (NCV), consistent with Section VII.B.1.a of the Enforcement Policy. This NCV regarding inadequate corrective actions associated with control rod drive pump cooling system post maintenance configuration control is described in this inspection report. If you contest the violation or severity level of this NCV, you should provide a response within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear Regulatory Commission, ATTN: Document Control Desk, Washington DC 20555-0001; with copies to the Regional Administrator, Region 1; the Director, Office of Enforcement, United States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident Inspector at the Oyster Creek facility.

Mr. Sander Levin

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its enclosures will be placed in the NRC Public Document Room (PDR).

We appreciate your cooperation.

Sincerely, ORIGINAL SIGNED BY:

Peter W. Eselgroth, Chief Projects Branch No. 7 Division of Reactor Projects Docket No.: 05000219 07201004 License No.: DPR-16

Enclosure:

NRC Inspection Report No. 05000219/1999009

REGION I==

Report No.

05000219/1999009 Docket No.

05000219 72-1004 License No.

DPR-16 Licensee:

GPU Nuclear Incorporated 1 Upper Pond Road Parsippany, New Jersey 07054 Facility Name:

Oyster Creek Nuclear Generating Station Location:

Forked River, New Jersey Inspection Period:

November 8, 1999 - January 2, 2000 Inspectors:

Laura A. Dudes, Senior Resident Inspector Thomas R. Hipschman, Resident Inspector Joseph T. Furia, Senior Radiation Specialist, December 6-10, 1999 Jason C. Jang, Senior Radiation Specialist, November 15-19, 1999 Approved By:

Peter W. Eselgroth, Chief Projects Branch No. 7 Division of Reactor Projects

EXECUTIVE SUMMARY Oyster Creek Nuclear Generating Station Report No. 05000219/1999009 This integrated inspection included aspects of licensee operations, engineering, maintenance, and plant support. The report covers an eight-week period of inspection.

Plant Operations

Operator performance during this inspection period was adequate. Overall operator response during the year 2000 (Y2K) transition was appropriate and focus on plant activities was at a high level. (Section O1.1)

Operations management demonstrated safety-focus to determine appropriate actions in the event the Q121 offsite power line is lost. (Section E2.1)

Maintenance

Maintenance personnel obtained approval for work and conducted activities in accordance with approved job orders and applicable technical manuals and instructions.

Personnel were knowledgeable of the activities and observed appropriate safety precautions and radiological practices. The licensee was appropriately monitoring performance for equipment within the scope of the maintenance rule. (Section M1.1)

Overall, personnel used the appropriate procedure, obtained prior approval, and completed applicable surveillance testing prerequisites. Personnel used properly calibrated test instrumentation, observed good radiological practices, and properly documented test results to ensure that equipment met TS requirements. However the inspector did note one instance where two surveillances which had the potential to impact safety related control room torus level indicators, were inappropriately authorized to be performed simultaneously. (Section M1.2)

Ineffective corrective actions and a less than thorough work package led to a condition which could have degraded a pump that is important to safety. Specifically, after a maintenance activity to replace a valve in the control rod drive pump oil cooling system, operators identified that the valve was left in the wrong position and the pump was put in service for fifteen hours with no oil cooling available. A similar issue associated with post maintenance configuration control was identified in November 1998 and the licensee did not take adequate corrective actions as evidenced by the second occurrence in 1999. The inadequate corrective actions associated with this activity were determined to be a Severity Level IV violation of 10 CFR, Appendix B, Criterion 16, Corrective Action. This severity level IV violation is being treated as a Non-Cited Violation, consistent with Section VII.B.1.a of the NRC Enforcement Policy. This matter is in the licensees corrective action program as CAP No. 1999-1557. (NCV 50-219/99009-01) (Section M.2.1)

Engineering ii

Executive Summary

Following the identification that the core spray room recirculation cooling fans were not working properly, engineering performed a thorough evaluation of the operability requirements and initiated appropriate corrective actions to assure the fans would be maintained within the preventive maintenance program. (Section E1.1)

Engineering performed a thorough evaluation and determined that one of the technical specification credited offsite power sources (Z52 line) should not be considered an active source of offsite power. (Section E1.2)

The licensees 10 CFR 50.59 safety evaluation for the sale of the Forked River land appropriately addressed any potential changes to the technical specifications and the final safety analysis report. (Section E8.1)

Plant Support

Poor radiation work practices, specifically less than thorough planning and communications, led to increased radiation exposures during an emergent work activity.

During a leak repair, the radiological conditions at the work location were significantly different than those specified on the radiation work permit survey used to plan the job.

As a result of this mis-communication unnecessary radiation surveys were performed in the condenser bay leading to an additional radiation dose of approximately 100 millirem to radiation technicians. No individual personnel exposure limits were exceeded.

(Section R1.1)

While contaminated area controls in the turbine building, reactor building, and yard area were generally acceptable, controls in the old radwaste building were generally lacking.

In addition, there appeared to be a lack of upkeep in the old radwaste building.

(Section R1.2)

As of December 10, 1999, the licensee was within its annual exposure goal and, based on remaining work in 1999, was expected to meet its goal. (Section R1.2)

Calibration records for area monitors were appropriately maintained and retrievable, and demonstrated acceptable calibration practices. Three monitors, listed in the Updated Final Safety Analysis Report (UFSAR), were no longer in service, and an action to modify the UFSAR is being prepared. (Section R1.2)

Although the scope of Quality Assurance Services reviews of the health physics program evaluated all major functional areas, a lack of review depth was apparent. (Section R7.1)

iii

TABLE OF CONTENTS Page EXECUTIVE SUMMARY....................................................... ii TABLE OF CONTENTS....................................................... iv I. OPERATIONS........................................................... 1 O1 Conduct of Operations............................................... 1 O1.1 General Observations....................................... 1 II. MAINTENANCE.......................................................... 2 M1 Conduct of Maintenance............................................. 2 M1.1 Maintenance Activities....................................... 2 M1.2 Surveillance Activities....................................... 3 M2 Maintenance and Material Condition of Facilities and Equipment.............. 4 M2.1 Control Rod Drive Pump Post Maintenance Configuration Restoration.. 4 III. ENGINEERING.......................................................... 6 E1 Conduct of Engineering.............................................. 6 E1.1 Core Spray Cooling Fans..................................... 6 E8 Miscellaneous Engineering Issues...................................... 8 E8.1 10 CFR 50.59 Evaluation for the Sale of Part of the Oyster Creek Site Bundary................................................... 8 IV. PLANT SUPPORT....................................................... 10 R1 Radiological Protection and Chemistry (RP&C) Controls.................... 10 R1.1 Radiation Protection Performance During an Emergent Condenser Bay Leak Repair.............................................. 10 R1.2 Performance Review of Radiation Protection Practices and Procedures 11 R7 Quality Assurance in RP&C Activities.................................. 13 R7.1 Review of Oyster Creek Quality Assurance in Radiation Protection... 13 S1 Conduct of Security and Safeguards Activities........................... 14 S1.1 General Observations...................................... 14 V. MANAGEMENT MEETINGS............................................... 14 X1 Exit Meeting Summary.............................................. 14 INSPECTION PROCEDURES USED.................................. 15 ITEMS OPENED AND CLOSED...................................... 16 LIST OF ACRONYMS USED......................................... 17 iv

Report Details Summary of Plant Status The plant began this inspection period at full power and remained there until December 31, 1999, when power was reduced to 70 percent to accommodate potential grid challenges due to the year 2000 (Y2K) rollover. The unit was restored to full power on January 1, 2000; however, an erratic temperature indicator on the A feedwater pump motor bearing caused operators to reduce power a second time to 80 percent to troubleshoot the problem. The indicator troubles were not related to any Y2K rollover problems. The indicator was repaired and full power was achieved on January 2, 2000.

I. OPERATIONS O1 Conduct of Operations O1.1 General Observations (71707)

a.

Inspection Scope (71707)

The inspectors observed operations shift turnover meetings, control room activities, equipment operator tours and operators response during the year 2000 (Y2K) rollover.

Also, the inspectors conducted routine plant tours to assess equipment conditions, indications of operator work-arounds, procedural adherence, and compliance with regulatory requirements.

b.

Observations and Findings Overall, the operators used three part communications, conducted detailed status briefings during shift turnovers and demonstrated good command and control in the control room during normal operations.

Operators conducted control room activities in a professional manner with staffing levels above those required by technical specifications (TS). The inspectors verified operator knowledge of ongoing plant activities, the reason for any lit annunciators, and the adequacy of existing fire watches. The inspectors also routinely performed independent verification of safety system status, from the control room indications and in the plant observation of equipment operation/position, for the plant operational mode.

The inspector observed the Y2K rollover transition briefing and observed a high level of management attention and focus on human performance. In the control room during the transition the inspector noted good command and control by the group operating supervisor. After the rollover period the operators remained focused on the reactivity management of the plant during post transition testing.

c.

Conclusions Operator performance during this inspection period was adequate. Overall operator response during the Y2K transition was appropriate and focus on plant activities was at a high level.

II. MAINTENANCE M1 Conduct of Maintenance M1.1 Maintenance Activities a.

Inspection Scope (62707)

The inspectors observed selected maintenance activities on risk significant safety-related and non safety-related equipment to ascertain that the licensee conducted these activities in accordance with approved procedures, TS, and appropriate industrial codes and standards. Activities were selected based on systems, structures, or components being contained within the scope of the maintenance rule.

b.

Observations and Findings The inspectors observed all or portions of the following job orders (JO):

JO 535206 Temperature Indicator From Stand-By Gas Treatment System (SBGTS)

JO 536560 Collect Y2K Data from Emergency Diesel Generator No. 1.

JO 537093 Main Feedwater Regulating Valve

JO 537163 480V Motor Control Center (MCC) Breaker for Reactor Building Supply Fan

JO 531995 Control Rod Drive (CRD) Pump Planned Outage for Seal/Oil Cooler Valve Replacements

JO 537712 CRD Pump Gear Box Inspection and Oil Change c.

Conclusions Maintenance personnel obtained approval for work and conducted activities in accordance with approved job orders and applicable technical manuals and instructions.

Personnel were knowledgeable of the activities and observed appropriate safety precautions and radiological practices. The licensee was appropriately monitoring performance for equipment within the scope of the maintenance rule.

M1.2 Surveillance Activities a.

Inspection Scope (62707)

The inspectors performed technical procedure reviews, witnessed in-progress surveillance testing, and reviewed completed surveillance packages. They verified that the surveillance tests were performed in accordance with TS, approved procedures, and NRC regulations. Activities were selected based on the systems, structures, or components being contained within the scope of the maintenance rule.

b.

Observations and Findings The inspectors reviewed all or portions of the following surveillance tests:

619.3.001 Turbine Load Rejection above 45 percent power

617.4.001 A CRD Pump Operability test

607.4.055, Rev 37, Containment Spray and Emergency Service Water Pump System 2 Operability and Inservice Test.

Overall, surveillances were conducted with an appropriate focus on safety; however, while observing the performance of the,Containment Spray and Emergency Service Water Pump System 2 Operability and Inservice Test (607.4.055, Rev 37,), the inspector noted that operations allowed two surveillances that when performed together, had the potential to impact safety related torus level indicators.

Specifically, procedure 607.4.055, includes a precautionary statement which indicates that operators may need to rely on the torus wide range level instrumentation while performing this test due to the fact that the narrow range indication may not be acceptable during portions of the test. While performing this test, a second surveillance was authorized by the control room supervisor. This second surveillance calibrated the torus wide range instrumentation and would render both indicators inoperable for a brief period of time. Although, the pump test was completed prior to the time when the torus wide range instrumentation was inoperable, the inspector concluded that the authorization of both tests simultaneously was not in accordance with management expectations and did not demonstrate conservative decision making.

Further inspection revealed that these tests were not originally scheduled to be performed on the same day; however, due to changes earlier in the work week, the tests were moved to the same day without an additional operations review.

c.

Conclusions Overall, personnel used the appropriate procedure, obtained prior approval, and completed applicable surveillance testing prerequisites. Personnel used properly calibrated test instrumentation, observed good radiological practices, and properly documented test results to ensure that equipment met TS requirements. However the inspector did note one instance where two surveillances which had the potential to impact safety related control room torus level indicators, were inappropriately authorized to be performed simultaneously.

M2 Maintenance and Material Condition of Facilities and Equipment M2.1 Control Rod Drive Pump Post Maintenance Configuration Restoration a.

Inspection Scope (71707, 62707)

The inspector reviewed the work package and observed portions of the maintenance activities associated with the A control rod drive pump.

b.

Observations and Findings On December 2, the licensee removed the A control rod drive (CRD) pump from service to perform minor maintenance and to replace three valves associated with the pump oil cooling system.

On December 5, after the pump had been returned to service for 15 hours1.736111e-4 days <br />0.00417 hours <br />2.480159e-5 weeks <br />5.7075e-6 months <br />, an equipment operator noted that the valve which isolates cooling water to the CRD pump oil cooler was in the closed position. The licensee immediately removed the pump from service and performed diagnostic testing of the pump to determine if the isolated oil cooling caused any degradation to the pump. Further investigation revealed that this valve had been replaced during the pump maintenance; however, its appropriate inservice position had not been established by maintenance prior to turning over the pump to operations. In addition, operations did not perform a system valve line-up to verify that the pump and its supporting systems were in the appropriate configuration.

The inspector observed portions of the diagnostic testing including the oil change, portions of the gear box inspection and the final operability run of the pump. The oil analysis and gear box inspection indicated no damage to the pump as a result of the isolated oil cooling water.

In reviewing this event, the inspector noted that on November 11, 1998, a similar event occurred during maintenance on the same pump. The licensee initiated a corrective action program document (CAP 1998-1178) to review the root cause and develop corrective actions. The 1998 corrective actions did not fully address the configuration control issues associated with restoring equipment from a maintenance activity.

Specifically, the actions did not preclude the recurrence of a configuration control issue within the boundaries of a similar CRD pump maintenance work activity. Although, maintenance workers were counseled on the sensitivity of valve manipulation during work activities the work process was not enhanced to include additional information

involving as left positions for valves that are replaced during maintenance activities.

The inspector reviewed the work package associated with the December 2 maintenance activity and noted that there were no instructions as to what position maintenance personnel should leave the valves that they had replaced. In addition, there were no additional instructions for operations personnel to verify that the new valves were in the proper position after the maintenance activity. Configuration control after the maintenance activity was limited to the restoration of those valves which had been used to provide personnel and system protection during the maintenance activity. Any valves that were replaced during the activity that were within the protective tagout boundary were left in an unknown position with no further configuration control. The inspector concluded that the work package did not provide adequate information to control the position of the new valves, nor did the work management process provide direction to the operators for restoring the system to an appropriate system configuration.

The inspector concluded that the licensees corrective actions associated with the 1998 configuration control issue were ineffective and did not address the issue of maintaining system configuration after maintenance activities. The inadequate corrective actions associated with this activity were determined to be a Severity Level IV violation of 10 CFR, Appendix B, Criterion 16, Corrective Action. This severity level IV violation is being treated as a Non-Cited Violation, consistent with Section VII.B.1.a of the NRC Enforcement Policy. This matter is in the licensees corrective action program as CAP No. 1999-1557. (NCV 50-219/99009-01)

c.

Conclusions Ineffective corrective actions and a less than thorough work package led to a condition which could have degraded a pump that is important to safety. Specifically, after a maintenance activity to replace a valve in the control rod drive pump oil cooling system, the valve was left in the wrong position and the pump was put in service for fifteen hours with no oil cooling available. A similar issue associated with post maintenance configuration control was identified in November 1998 and the licensee did not take adequate corrective actions as evidenced by the second occurrence in 1999. The inadequate corrective actions associated with this activity were determined to be a Severity Level IV violation of 10 CFR, Appendix B, Criterion 16, Corrective Action. This severity level IV violation is being treated as a Non-Cited Violation, consistent with Section VII.B.1.a of the NRC Enforcement Policy. This matter is in the licensees corrective action program as CAP No. 1999-1557. (NCV 50-219/99009-01)

III. ENGINEERING E1 Conduct of Engineering E1.1 Core Spray Cooling Fans a.

Inspection Scope (37551, 71707)

The inspector reviewed the licensees response to an unknown condition regarding the adequacy and availability of a core spray room recirculation cooling fan.

b.

Observations and Findings On November 9, 1999, the quality assurance organization initiated a corrective action program document (CAP1999-1464) to capture an unknown condition of the core spray room recirculation cooling fans. These fans were originally intended to keep the core spray system, control rod drive pumps and associated equipment cool as described in the Updated Final Safety Analysis Report (UFSAR) section 9.4.2.2.3. However, the quality assurance inspector observed that although the motor was running, there did not appear to be any air flow into the room. Discussions with maintenance and operations personnel indicated that this fan was not needed and had been abandoned in place because the coolers were plugged with dirt and debris from the room.

The system engineers assessed the validity and safety impact of this issue. No immediate safety concerns were identified as routine monitoring indicated that the temperatures within that room were well within the design limits for the pumps. In addition, the fans are not seismically qualified and therefore are not credited under accident conditions. Section 6.3.2.5.6 of the UFSAR indicated that the loss of corner room cooling has been evaluated and the pumps can be operated for more than 48 days without mechanical cooling from the coolers.

However, system engineering did note that there were certain accident conditions which could necessitate personnel having to enter the room to perform emergency maintenance. Because of the room habitability associated with some emergency operating procedural steps, engineering concluded that the fans should be available and initiated action items to develop more extensive preventive maintenance programs for the fans and their support equipment.

c.

Conclusions Engineering performed a thorough evaluation of the core spray motor pump cooling fan operability requirements and initiated appropriate corrective actions to assure the fans would be maintained within the preventive maintenance program.

E1.2 Closed URI 50-219/99007-01: Offsite Power Source Availability a.

Inspection Scope (71707, 37551)

The inspector reviewed engineerings operability evaluation of the Z52 line offsite power source. The inspector performed this review due to an unresolved issue identified in NRC Integrated Inspection Report No. 50-219/99-07 (URI 50-219/99-07-01) when engineering identified a potential operability concern involving one of two redundant TS-required 34.5KV offsite power sources.

b.

Observations and Findings Technical Specification (TS) 3.7.A.3 requires one 230KV line and one 34.5KV line to be fully operational. There are two 34.5KV offsite power sources connected to Oyster Creek Nuclear Generating Station (OCNGS). The Manitou line (Z52) provides an interconnection with the 34.5KV General Public Utilities - Electric (GPUE) transmission system at the Manitou substation and delivers power to OCNGS. The second offsite source is the Whiting line (Q121) which also provides an interconnection with the 34.5KV GPUE transmission system at the Whiting substation and delivers power to OCNGS.

In October 1999, engineering noted that the Z52 line is normally configured with an open load break switch at the Pinewald substation. Under normal conditions, the 34.5KV Z52 line can not provide power to OCNGS without GPUE actions to close the Pinewald load break switch. The Q121 line does not have a normally open load break switch. When in service, the Q121 line satisfies the TS requirement. Another line, the Sands Point tie (69 kV), is also available for system restoration; however, the Sands Point tie is not included in TS.

Engineering performed a thorough evaluation and determined that the Z52 line should not be considered an active source of offsite power. Engineering questioned the operability of the Z52 line and reportability (operation outside the design basis),

especially during periods when GPUE removed the Q121 line for maintenance. As a result of this concern, a preliminary engineering evaluation determined that the Z52 line should not be considered an active transmission source even if the disconnect were closed. They determined that if the Q121 line is lost, Z52 would not be capable of providing sufficient voltage to the plants safety related busses because they are too heavily loaded. As a result of this review, engineering also determined that the startup transformer voltage regulators must be in the automatic mode of operation in order to provide sufficient voltage to the plants safety related busses.

The engineering analysis of offsite power sources determined changes were made in the offsite transmission system since the initial licensing of the facility. The initial system design was for the Z52 line to be continuous to the Oyster Creek substation, but a load break switch in another substation was opened around 1989. The Z52 line is no longer used to transmit power to the Oyster Creek substation, and is not referenced in any GPUE restoration procedures. GPUE procedures reference the Q121 line and the Sands Point tie for system restoration, however, the Sands Point tie is not included in TS. The Z52 line could be used for emergency restoration, but GPUE procedures would prefer the Q121 and Sands Point lines. Because of the current transmission system

configuration, loss or maintenance on the Q121 line makes the OCNGS vulnerable to be outside of TS requirements. The inspector reviewed operations logs for the previous 18 months and did not identify any occurrences that would have placed the plant in a TS LCO condition other than that already identified by licensee staff. The licensee is continuing to review the reportability to determine if a situation existed when the facility did not meet the offsite power sources TS requirement. The inspector determined that the licensee is adequately addressing the availability of offsite power sources and that this previously unresolved item is closed. The licensee plans to make changes to the FSAR and submit a TS amendment to accurately reflect offsite power sources.

Operations management demonstrated safety-focus to determine appropriate actions in the event the Q121 offsite power line is lost. On October 22, 1999, the Operations Director appropriately provided guidance to operations personnel to enter a 30 hour3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br /> shutdown LCO in the event the Q121 was lost. Subsequently, the Operations Director made a change to procedure 106, Conduct of Operations, attachment 106-4, to provide further guidance concerning startup transformer daily checks and operability. The inspector reviewed the procedure changes and determined that they were adequate.

The inspector interviewed several operations personnel, concerning the availability of the Z52 line and the requirement that the startup transformer voltage regulators be in automatic, to evaluate their knowledge of offsite power sources. Generally, operations personnel were familiar with the changes, however, a few licensed personnel were not aware of the requirement to declare a startup transformer inoperable whenever its associated voltage regulator is not in the automatic mode of operation.

c.

Conclusions

Following the identification that the core spray room recirculation cooling fans were not working properly, engineering performed a thorough evaluation of the operability requirements and initiated appropriate corrective actions to assure the fans would be maintained within the preventive maintenance program.

E8 Miscellaneous Engineering Issues E8.1 10 CFR 50.59 Evaluation for the Sale of Part of the Oyster Creek Site Boundary a.

Inspection Scope (37551)

In August 1999, the licensee documented a safety evaluation, performed in accordance with 10 CFR 50.59, to support that the proposed sale of the Forked River Site, which would effectively reduce the current site boundary, and included combustion turbines currently relied on as an alternate AC power source for station blackout recovery, did not constitute an unresolved safety question. This inspection activity included in-office review by the NRC staff to determine the adequacy of the licensees evaluation with respect to addressing: 1) control and availability of the combustion turbines if transferred

to a non-licensee owner; 2) the continued maintenance of the limits established by 40 CFR Part 190; and 3) assessment of the licensees evaluation affecting maintenance of 10 CFR Part 100 design basis accident radiation dose limits with respect to the exclusion area boundary (EAB).

b.

Observations and Findings The staff determined that the sale of the combustion turbines did not constitute a change to the current licensing basis of Oyster Creek, provided that the licensee maintained commitments as specified in Schedule 6.13, Additional Forked River Covenants, of the licensees 10 CFR 50.59.

The staff determined that the licensees qualitative analysis for the impact of a reduced site boundary on the dose to the members of the public from routine radioactive gaseous and liquid effluents provided reasonable assurance that public exposure would be maintained in accordance with the requirements of 40 CFR 190. The staff determined that the analysis was adequate and the licensees continued maintenance of the radiological effluent control program in accordance with regulatory requirements provide adequate assurance that the change in site boundary would not affect environmental dose assessment specifications or result in exposure in excess of the environmental standard specified in 40 CFR 190.

To confirm this aspect, the inspector reviewed data collected from the licensees direct radiation measurement program, i.e. the environmental thermoluminescent dosimeter (TLD) program for 1997 and 1998. The review included TLD monitoring results for 10 TLDs located on the Forked River Site property, in closest proximity to the Oyster Creek facility, i.e. adjacent to the switch yard at the Forked River site. The highest site boundary TLD readings (Station No. 55) were 66.4 mrem and 66.0 mrem, respectively.

The control TLD readings (background) for 1997 and 1998 were 50.2 mrem and 45.6 mrem, respectively. Accordingly, the net dose rates at Station No. 55 during 1997 and 1998 were 16.2 mrem/year and 20.4 mrem/year, respectively. These dose rates were less than the 40 CFR Part 190 environmental standard of 25 mrem/year, whole body.

The NRC also determined that the design basis dose assessment calculations would not be affected as long as the EAB remained unchanged. Although the site boundary would be affected if the property is transferred, the inspectors confirmed that the licensee would continue to maintain effective control of the exclusion area boundary as defined in the current design basis for the Oyster Creek facility.

c.

Conclusions The licensees 10 CFR 50.59 safety evaluation for the proposed sale of the Forked River Site property was sufficient to demonstrate that the transfer of the property would not result in an unresolved safety question.

IV. PLANT SUPPORT R1 Radiological Protection and Chemistry (RP&C) Controls R1.1 Radiation Protection Performance During an Emergent Condenser Bay Leak Repair a.

Inspection Scope (71750, 71707)

The inspector reviewed the licensees performance with respect to radiation protection during an emergent repair to a leaking sea water condenser bay pipe. In addition, the inspector reviewed the adequacy of the communications and how information was translated into the final planning and preparation of the work package.

b.

Observations and Findings On November 5, 1999, the licensee noted high conductivity in the 1-3 sump due to a leak on the 72 inch sea water piping down stream of the C condenser bay backwash outlet valve. The licensee made preparations to perform a leak repair on the piping.

The initial pre-job walkdown was performed by representatives from operations and maintenance. The workers entered the condenser bay area, a high radiation area, and proceeded to the location of the condenser bay backwash outlet valve. They noted that the leak was further downstream of the valve than originally thought which would change the location of the repair work. This information was not clearly communicated to radiation personnel and therefore no one questioned the radiation survey used to identify and minimize radiation exposure during the work activity.

A radiation technician did accompany the maintenance mechanics into the area when the work package was ready to work. At that time, the work group proceeded to the location of the leak rather than the location where the leak was originally thought to have been. The electronic dosimeters worn by the mechanics began to alarm indicating that they were in an area where the dose rates exceed the expected level. The maintenance workers and the radiation technician immediately left the area. Two radiation technician then re-entered the area and performed a thorough survey of the condenser bay. This survey which examined locations directly in contact with the condenser bay yielded contact dose rates on the order of 400 to 800 mR/hr. Initially, the licensee responded as if the dose rate in the area had increased significantly without a reason. Several engineers were called in to try to identify possible sources of radiation with systems that interact with the condenser bay. Upon further investigation, the licensee concluded that the original radiation work permit (RWP) had been assigned to the exact location of the valve instead of approximately ten feet away where the leak had occurred. At that location the dose rate were, and had always been, significantly higher than the dose rates recorded at the valve location.

The inspector noted that the second survey performed by the radiation technicians in response to the alarming dosimeters was unnecessary and exposed the two technicians to an additional 100 millirem radiation dose. Less than thorough planning and communications contributed to this additional radiation dose. The licensee initiated a corrective action program (CAP 1999-1456) report on this matter.

c.

Conclusions Poor radiation work practices, specifically less than thorough planning and communications, led to increased radiation exposures during an emergent work activity.

During a leak repair, the radiological conditions at the work location were significantly different than those specified on the radiation work permit survey used to plan the job.

As a result of this mis-communication unnecessary radiation surveys were performed in the condenser bay leading to an additional radiation dose of approximately 100 millirem to radiation technicians. No individual personnel exposure limits were exceeded.

R1.2 Performance Review of Radiation Protection Practices and Procedures During radiologically controlled area (RCA) tours the inspectors observed that technicians: posted proper warning signs, conducted adequate radiological monitoring of personnel and materials leaving the RCA, maintained monitoring instrumentation functional and in calibration, and maintained radiation work permits (RWPs) and survey status boards up-to-date and accurate. Technicians observed activities in the RCA and verified that personnel complied with the requirements of applicable RWPs, and that workers remained aware of the radiological conditions in the area.

a.

Inspection Scope (83726)

Areas of inspection focus were based on the following regulatory requirements from 10 CFR Part 20:

20.1101 Radiation protection program 20.1601 Control of access to high radiation areas 20.1602 Control of access to very high radiation areas 20.1902 Posting requirements 20.1904 Labeling containers 20.2103 Records of surveys The inspection was conducted via direct observation of in-process work in the radiologically controlled areas (RCA), review of pertinent documents including surveys, radiation work permits (RWPs) and as low as is reasonably achievable (ALARA)

reviews, and discussions with cognizant personnel.

Specific inspection focus was placed on the program for controlling the generation and spread of contaminated materials. Review of procedures and practices related to the identification, posting and control of contaminated areas within the plant, and the surveillance of materials exiting the RCA, was conducted.

b.

Observations and Findings

Radiological housekeeping and contamination control practices were generally acceptable in the reactor and turbine buildings and RCA yard area. However, conditions within the old radwaste building were generally below that exhibited in other portions of the station. Numerous examples of poor contamination control practices, abandoned contamination control boundaries and piles of uncontrolled and abandoned loose materials were observed throughout the facility. Areas such as the centrifuge and hopper rooms, which were cleaned as part of a campaign in the early 1990's have been permitted to deteriorate, and now again require control as contaminated or highly contaminated areas. Also, extensive portions of the facility contain abandoned in place radwaste processing equipment, but a number of piping runs are still in service, such as the fuel pool clean-up system components. The inspector tours also identified some areas (e.g., the small and large pump rooms, large tank room and stairway to the mezzanine and centrifuge rooms) that exhibited difficult walking conditions due to a lack of sufficient lighting. The conditions appeared, based on discussions, to have existed for an extended period and appeared attributable to a lack of basic maintenance activities within the old radwaste building.

For 1999, the licensee had established an exposure goal of not more than 45 person-rem. Through December 8, 1999, total site exposure was approximately 41.1 person-rem, and it appeared, based on remaining work, that the licensee would meet its annual exposure goal. While the goal included no planned outages at the facility, it was established with the planned use of quarterly power reductions to allow for scheduled maintenance and observations in the condenser area, and included a budget for clean-up work in the spent fuel pool, involving the volume reduction and packaging of irradiated hardware. The most dose significant emergent work which has occurred was work in condenser water box A to locate and plug leaking condenser tubes, resulting in 4.755 person-rem of dose, which was not planned in the budget.

For 2000, the licensee has begun planning for the 18R outage, which is scheduled to commence in the fall. Due to a number of deferred work items from the 17R outage, especially in-service inspections, the scope of the 18R outage is significantly larger.

Although final dose goals for this outage have not yet been established, preliminary estimates by the radiological engineering staff are for an estimated dose of 375 person-rem.

From a listing of monitors found in Section 12.3 of the Updated Final Safety Analysis Report (UFSAR) 13 monitors were randomly selected for review. Three of the selected monitors, listed in the UFSAR and located in the new radwaste building, are no longer in service. An action to modify the UFSAR is being prepared. All of the remaining monitors selected had records of their calibration available for review. No discrepancies were identified in reviewing the calibration documentation.

c.

Conclusions While contaminated area controls in the turbine building, reactor building, and yard area were generally acceptable, controls in the old radwaste building were generally lacking.

In addition, there appeared to be a lack of upkeep in the old radwaste building.

As of December 10, 1999, the licensee was within its annual exposure goal and, based on remaining work in 1999, was expected to meet its goal.

Calibration records for area monitors were appropriately maintained and retrievable, and demonstrated acceptable calibration practices. Three monitors, listed in the UFSAR, were no longer in service, and an action to modify the UFSAR is being prepared.

R7 Quality Assurance in RP&C Activities R7.1 Review of Oyster Creek Quality Assurance in Radiation Protection a.

Inspection Scope (83726)

Audits and surveillances performed by Quality Assurance Services (QAS) during 1999 were reviewed. An evaluation of the scope and depth of these reviews, together with the tracking to resolution of identified deficiencies was conducted.

b.

Observations and Findings Monthly plant support surveillances were performed in 1999, and included some topics in health physics. A review of the surveillances performed demonstrated that while the scope was sufficiently broad to include most of the major functional areas of the health physics program, they lacked depth of review and tended to be compliance-based reviews only. No corrective action process (CAP) forms were generated as a result of these surveillances. No QAS audits of the health physics program were performed in 1999.

Additionally, QAS has a radiological assessor who performs monthly assessments of the radiation protection programs at all GPUN facilities on a monthly basis. Due to personnel changes, however, only five monthly assessments were performed in 1999.

Again, the focus of these assessments was primarily compliance-based, and they were lacking in depth of review. The only additional periodic reviews of the health physics program were contained in departmental self-assessments.

c.

Conclusions Although the scope of QAS reviews of the health physics program evaluated all major functional areas, a lack of review depth was apparent.

S1 Conduct of Security and Safeguards Activities S1.1 General Observations (71750)

During routine tours, the inspectors noted that security controlled vital and protected area access in accordance with the security plan, properly manned security posts, locked or guarded protected area gates, and maintained isolation zones free of obstructions.

V. MANAGEMENT MEETINGS X1 Exit Meeting Summary The inspectors provided a verbal summary of preliminary findings to senior licensee management at an exit meeting on January 6, 2000. During the inspection period, inspectors periodically discussed preliminary findings with licensee management.

Inspectors did not provide any written inspection material to the licensee. The licensee did not indicate that any of the information presented at the exit meeting was proprietary.

INSPECTION PROCEDURES USED Procedure No.

Title 37551 Onsite Engineering 61726 Surveillance Observation 62707 Maintenance Observation 71707 Plant Operations 71750 Plant Support 83726 Control of Radioactive Materials and Contamination, Surveys, and Monitoring

ITEMS OPENED AND CLOSED Opened\\Closed Number Type Description 50-219/99-09-01 NCV Control rod drive pump post maintenance configuration inadequate corrective actions.

(Section M2.1)

Closed Number Type Description 50-219/99-07-01 URI Operability and reportability aspects concerning 34.5KV offsite power availability.

(Section E1.2)

LIST OF ACRONYMS USED AC Alternating Current ALARA As Low As Is Reasonably Achievable CAP Corrective Action Process CFM Containment Failure CRD Control Rod Drive CFR Code of Federal Regulations DRP Division of Reactor Projects EAB Exclusion Area Boundary FSAR Final Safety Analysis Report DRS Division of Reactor Safety GPUE General Public Utilities (GPU) - Electric GPUN General Public Utilities (GPU) - Nuclear IST In-Service Test JO Job Order LCO Limiting Condition for Operation NCV Non-Cited Violation NRC Nuclear Regulatory Commission NRR Office of Nuclear Reactor Regulation OCNGS Oyster Creek Nuclear Generating Station PDR Public Document Room QAS Quality Assurance Services RCA Radiologically Controlled Area REMP Radiological Environmental Monitoring Program RWP Radiation Work Permit RP&C Radiological Protection and Chemistry SBGTS Stand-By Gas Treatment System TIA Task Interface Agreement TLD Thermoluminescent Dosimeter TS Technical Specifications UFSAR Updated Final Safety Analysis Report Y2K Year 2000