IR 05000219/1983014

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IE Insp Rept 50-219/83-14 on 830503-0608.No Noncompliance Noted.Major Areas Inspected:Followup of Previous Insp Findings,Review of Plant Operations,Log & Record Review, Plant Tours,Physical Security & Radiation Protection
ML20024A834
Person / Time
Site: Oyster Creek, 05002198
Issue date: 06/16/1983
From: Conner E, Connor E, Cowgill C, John Thomas
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML20024A826 List:
References
50-219-83-14, NUDOCS 8307010025
Download: ML20024A834 (11)


Text

Docket Nrs: 05000219-830327

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05000219-830406 U. S. NUCLEAR REGULATORY COMMISSION 05000219-830418 05000219-830516 05000219-830606

REGION I

05000219-830607 Report No.

83-14 Docket No.

50-219 License No.

DPR-16 Priority Category C

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License:

GPU Nuclear Corporation 100 Interpace Parkway Parsippany, New Jersey 07054 Facility Name: Oyster Creek Nuclear Generating Station Inspection at: Forked River, New Jersey Inspection Conducted:

May 3 - June 8,1983 Inspectors:

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[r/3[f3 C. Co ill, nior Resident Inspector date signed DiL t clale

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homas, Resident Inspector date signed Approved by:

[7 M!///T3 E. L. Conner, Chief, Reactor date signed Projects Section 2D Inspection Summary: Inspection on May 3 - June 8,1983 (Report No. 50-219/83-14)

Routine inspection by the resident inspectors (144 hours0.00167 days <br />0.04 hours <br />2.380952e-4 weeks <br />5.4792e-5 months <br />) which included followup of previous inspection findings, review of plant operations, log and record review, plant tours, physical security, radiation protection, surveillance observation, maintenance and refueling maintenance observation, followup of onsite events, licensee event report review, attendance at licensee meetings, review of IE Bulletins, and review of periodic and special reports.

Results: No Violations

8307010025 830617 PDR ADOCK 05000219 Q

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DETAILS

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Persons Contacted

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J. Brownridge, Maintenance and Construction Jobs Manager M. Budaj, Manager, Plans and Programs P. Fiedler, Vice President, Director, Oyster Creek V. Foglia, Manager, Operational Corrective Maintenance / Preventive Maintenance E. Growney, Safety Review Manager M. Laggart, Manager, Oyster Creek Licensing B. Leavitt, Deputy Manager, Radiological Controls J. Maloney, Manager, Plant Materiel J. Maughn, Supervisor Security R. Mc Keon, Manager, Plant Operations

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W. Smith, Plant Engineering Director W. Stewart, Operations Control Manager J. Sullivan, Plant Operations Director D. Turner, Manager, Radiological Controls 2.

Review of Previous Inspection Findinas (Closed) Violation (83-04-01)

Failure to conduct adequate search.

During normal access to and egress from both the north anc main entrances to the site protected area, the inspectors have' routinely observed search procedures.

All packages except those containing liquids, are now required to be processed through X-ray machines.

During these observations, no search violations have been identified.

(Closed) Violation (83-04-02) Violation of Security Procedures for Personnel Escort. The licensee took immediate corrective action to place the subject visitor under escort and to correct the deficient performance of the individual who had been assigned to escort duty.

The licensee's current procedures for visitor control are adequate. The requirements have been reemphasized and the violation discussed with all departments.

The inspector had no further questions on this item.

(Closed) Violation (83-08-01) Failure to properly control access to vital areas.

The inspector has observed control at selected vital area access points during routine plant tours and has noted that site protection force personnel are posted as required, and appropriate log entries are made when required. The vital area locking devices discussed in the licensees letter dated June 6,1983 have been installed.

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No unacceptable conditions were identified.

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Plant Operations Review 3.1 Shift Logs and Operating Records Shift Logs and Operating Records were reviewed to verify that they were properly completed and signed and had received proper supervisory reviews. The inspectors verified that entries involving abnornal conditions provided sufficient details to communicate equipment status and followup actions. Logs were compared to equipment control records to verify that equipment removed from or returned to service was properly noted in operating logs when required. Operating memos and orders were reviewed to insure that they did not conflict with Technical Specification requirements.

The logs and records were compared to the requirements of Procedure 106,

" Conduct of Operations", and Procedure 108, " Equipment Control". The following were reviewed:

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Control Room and Group Shift Supervisor's Logs;

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Control Room, and Shift Supervisor's Turnover Check List;

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Control Room Shutdown Log;

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Reactor Building and Turbine Building Tour Sheets;

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Standing Orders;

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Operational Memos and Directives.

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No unacceptable conditions were noted.

3.2 Facility Tours The inspectors frequently toured the following areas:

Control Room (daily)

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Reactor Building l

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Turbine Building

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Augmented Off-Gas Building New Rad-Waste Building

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Cooling Water Intake and Dilution Plant Structure

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Monitor and Change Area

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4160 Volt Switchgear, 460 Volt Switchgear, and Cable Spreading Room

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Diesel Generator Building Battery Rooms

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Maintenance Work Areas

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Yard Areas (including Protected Area Perimeter)

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The following were observed:

3.2.1 During daily control _ room tours, the inspectors verified that the control room manning requirements of 10 CFR 50.54(k),

Technical Specifications and the licensee's conduct of operations procedure were met. Shift turnovers were observed for adequacy.

Selected control room instrumentation needed to support the cold shutdown conditions was verified to be operable and indicated parameters within normal expected limits.

Recorders ware examined for evidence of abnormal or unexplained transients. Plant stack radiation recorder traces were examined for evidence of abnormal or unplanned releases of radioactive gases. The inspectors verified compliance with Technical Specification Limiting Conditions for Operation (LCO's) applicable to the cold shutdown condition and refueling activities, including those relating to primary and secondary containment integrity, and fire protection systems. The inspectors closely monitored outage activities and verified that operators and supervisors were aware of work in progress and complied with applicable Technical Specification requirements.

No unacceptable conditions were identified.

3.2.2 Selected alamed annunciators were discussed with control room operators and supervisors. A large number of annunciators were in an alarmed condition because of systems being shutdown or drained and layed up to support outage related maintenance activities. The inspectors verified that operators were knowledgeable of system status and were aware of which alarms were indicative of abnormal conditions requiring followup and corrective action.

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The inspectors noted that the annunciator and alarm panels will be removed from service for system modification during this outage.

A temporary alarm panel is being installed to provide those alarm indications needed to support the plant's cold shutdown, defueled condition. The inspectors will monitor the installation and examine the temporary system for adequacy.

No unacceptable conditions were identified.

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3.2.3 The inspectors verified the operability of selected systems considered important to safety by direct observation of valve, breaker,and switch position.

Components were examined for leakage, proper lubrication, operating air supply, and general conditions.

Selected pipe hangers and seismic restraints were examined for indications of mechanical interference and fluid leaks. Systems inspected included Control Rod Drive Hydraulic, Standby Gas Treatment, and portions of the 4160 and 460 volt electrical distribution systems.

On May 17,1983, the inspector noted an oil leak on the

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outboard bearing of the 'D' Augmented Spent Fuel Pool Pump.

The inspector infomed the operations department and detemined that the leak had been identified by the operators, maintenance actions initiated, and steps taken to closely monitor the pump while it was operating pending repairs.

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No unacceptable conditions were identified.

3.2.4 Equipment Control procedures were examined for proper implementation by verifying that tags were properly filled out, posted, and removed as required, that jumpers were properly installed and removed, and that equipment control logs and records were complete. Selected active tagouts were independently verified by the inspectors. Selected cleared tagouts were reviewed to detemine that system alignments had been properly restored and safety systems returned to service had been properly

tested. Selected locked valves were examined for proper position and installation of locking devices. The inspectors monitored outage related activities including erection of scaffold and work platforms, installation of temporary hoses and cables, and the set up of radiological control barriers, to ensure that these activities did not block or otherwise impair the operability of components important to safety, and were controlled in accordance with the equipment control procedures when required.

No unacceptable conditions were identified.

3.2.5 The inspectors examined plant housekeeping conditions including general cleanliness, control of material to prevent fire hazards, maintenance of fire barriers, storage and maintenance of fire fighting equipment, and radiological housekeeping.

At about 10:30 P.M. on May 31, 1983, there was a minor fire in the torus. A fault on an energized welding lead caused an electrical arc which burned the insulation on the welding lead cable. The arcing was seen by the fire watch who extinguished the fire by deenergizing the cable. There was only minor smoke, no personnel injuries, and no damage. No fire brigade response was needed.

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i The faulted welding lead was replaced and other leads were inspected for possible insulation degradation.

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No unacceptable conditions were identified.

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4.

Radiation Protection

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During entry to and exit from radiation controlled areas (RCA), the

inspectors verified that proper warning signs were posted, personnel i-entering were wearing proper dosimetry, that personnel and materials leaving were properly monitored for radioactive contamination and that monitoring instruments were functional and in calibration.

Posted Radiation Work

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Permits (RWP's) and survey status boards were reviewed to verify that they were current and accurate. The inspector observed activities in the RCA to verify that personnel complied with the requirements.of applicable RWP's and that workers were aware of the radiological conditions in the area. Particular attention was given to activities around the control points on the refueling floor, the drywell entry, the torus access point, and the turbine operating floor.

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health physics technicians manning the control points and monitoring activities within the RWP areas were very knowledgeable of the radiological working conditions and were well abreast of outage activities in progress and planned for their

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assigned areas. They assured that people entering the areas were apprised of the radiological conditions and that proper protective measures were taken.

No unacceptable conditions were identified.

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Physical Security During daily entry and egress from the protected area, the inspectors verified

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that access controls were in accordance with the security plan and that security posts were properly manned. During facility tours, the inspectors

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verified that protected area gates were locked or guarded and that isolation zones were free of obstructions. The inspectors examined vital area access points to verify that they were properly locked or guarded and that access control was in accordance with the security plan. Vehicles onsite were periodically observed to verify proper controls. Visitors onsite were observed to verify that security plan escort requirements were met.

No unacceptable conditions were identified.

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Maintenance and Surveillance Testing The inspectors observed maintenance and surveillance activities to verify that activities were properly approved, operations personnel were cognizant of activities in progress, pmper procedural controls were in effect, redundant systems and components were available when required, test instrLanentation was

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calibrated, activities were perfonned in an acceptable manner by appropriately qualified personnel, and material and replacement parts were properly controlled.

The following procedures were reviewed:

Procedure 756.1.003, revision 4, November 30, 1982, Shield Plugs Removal and

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Replacement.

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Procedure SP 83-045, Installation and Removal of Recirculation Outlet

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Nozzle Shield Curtains.

Procedure 205.98, revision 0, April 26,1983, Reactor Vessel Draining

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Procedure.

No unacceptable conditions were identified.

Review of maintenance activities included direct observation of the performance of portions of the evolution, observation of work crew briefings, reviews of the planning of the evolution, and reviews of the radiological precautions.

Portions of the following activities were observed:

Construction activities in the new cable spreading room.

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Torquing of anchor bolts on new cable tray supports.

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Feedwater system flow control valve rebuild.

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Reactor feed pump maintenance.

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Control Rod Drive Hydraulic pump rebuild.

Turbine Building Closed Cooling Water system modification.

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Turbine disassembly,' inspection, and reassembly.

No unacceptable conditions were identified.

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Emercency Preparedness Drill and Exercise Observations On May 4 and 10 the licensee conducted emergency plan exercises in preparation for the NRC/FEVA observed exercise on May 24, 1983.

Each exercise implemented all phases of the site emergency plan. On both occasions, the State of New Jersey participated. The inspector observed selected portions of each exercise including control room, Technical Support Center and Near Site Emergency operating facility activities. The inspector noted that exercise objectives were met in each case. He also provided comments to utility management.

On May 24, 1983, the inspectors participated as nembers of the NRC observation team for the full scale observed exercise. The exercise activated all levels of the site emergency plan and included participation by State and local officials.

Inspector observations of this exercise will be included in NRC inspection report 50-219/83-1 _ _ _ _ _

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Inspector Attendance at Significant Licensee Meetings.

8.1 Systematic Assessment of Licensee Performance (SALP)

On May 12, 1983, NRC met with licensee representatives to discuss the results of the Regional SALP assessment of GPU Nuclear Oyster Creek for the period February 1,1982 through January 31, 1983. The meeting provided open discussion of the assessment as well as licensee plans for improvements in the next period. The results will be forwarded in NRC inspection report 50-219/83-16.

8.2 Post-Accident Sampling System (PASS)

On May 12th, NRC representatives from NRC Region I and the Office of Nuclear Reactor Regulation met with the licensee regarding completion of NUREG 0737, Item II.B.3 Post-Accident Sampling.

During the meeting, the following agreements were reached and confirmed by the licensee in a letter to NRC:NRR dated May 20, 1983.

Complete installation work requiring reactor shutdown during the current

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refueling outage.

The PASS will be fully operational 6 months following completion of

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the current refueling cutage.

Alternate methodology developed that estimates extent of post-

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accident core degradation.

The inspectors will follow licensee progress on completion of the PASS.

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Review of Licensee Event Reports (LER's)

9.1 The inspector reviewed LER's submitted to NRC:R1 to verify that the details were clearly reported, including the accuracy of the description and corrective action adequacy. The inspector determined whether further information was required, whether generic implications were indicated, and whether the event warranted onsite followup. The following LER's were reviewed:

LER SUBJECT 83-07 Standby Gas Treatment System II was declared inoperable and removed from service for HEPA filter replacement.

83-13 Both doors of one reactor building personnel access airlock were open simultaneously due to personnel error.

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filter heater control circuit.

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9.2 For those LER's selected for on-site followup, the inspector verified that reporting requirements of Technical Specifications and Regulatory Guide 1.16 had been met, that appropriate corrective action had been taken, that the event was reviewed by-the licensee as required by facility procedures, and that continued operation of the facility was conducted in accordance with Technical Specification limits. The LER's selected for on-site followup are denoted by an asterisk (*)

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in detail 9.1 above.

9.2.1 Licensee Event Report 83-14 reported a design deficiency in the Standby Gas Treatment System (SGTS) heater control circuit which could have impaired the operation of SGTS II filters if during an accident situation Diesel Generator 1 failed while SGTS II was in operation.

Electric heaters are installed in the redundant filter trains to reduce the relative humidity of the incoming air stream. The SGTS I is powered from the number 1 Diesel Generator Bus and system II is powered from the number 2 Diesel Generator Bus. However, both systems' heater control circuits are powered from the number 1 Diesel Generator Bus. Thus, the high humidity that may result from heater failure caused by a loss of number 1 Diesel Generator could reduce the systems' filter efficiencies.

The licensee took immediate corrective action to install a temporary power supply from number 2 Diesel Generator Bus to the heater control circuit for SGTS II.

A cermanent modification will be installed during the curr' nt outage.

e This event is under review by NRC headquarters for potential generic implications.

The inspectors had no further questions on this item.

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Followup of Events That Occurred During the Inspection 10.1 On May 16,1983, a rotor assembly from a contaminated pump was being transported in a licensee owned vehicle to Three Mile Island Nuclear Station for dynamic balancing. The vehicle was involved in an accident about 3.5 miles south of the plant when it was struck broadside by another vehicle that failed to stop at a traffic light. The pump rotor, which had fixed radioactive contamination of 200 to 400 counts per minute and a total activity of 0.08 microcuries, was packaged in a heavy wooden crate and was undamaged in the accident. The inspector went to the scene of the accident with a licensee health physics technician and a licensee health physics supervisor. Contact radiation measurements and smear surveys of the package showed no levels above background and no release of radioactive material. The package was returned to the site, inspected, repackaged, and shipped on to its original destination. There

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were no personnel injuries and no radiological hazards resulting from the accident. The licensee's actions were prompt and proper.

The inspectors had no further questions on this item.

10.2 Late on June 6,1983, chlorine gas was released into the atmosphere when a one-half inch plastic pipe (poly vinyl chloride) in the outlet of the chlorinator evaporator ruptured. The leak was identified and isolated about 11:07 P.M.. Licensee declared an unusual event at 11:17 P.M. and made all appropriate notifications.

Due to the nature of the event, station accountability was ordered and all persons onsite at the time (approximately 500) were mustered at remote assembly areas and accounted for shortly after midnite.

One person was transported to a local hospital via ambulance and remained overnite for observation. Several others were examined and released.

Licensee representatives conducted a thorough site tour and the event terminated about 2 A.M. on June 7th.

The inspector reviewed licensee actions and identified no unacceptable conditions.

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Licensee investigatiori of this event determined that the failed PVC piping is incompatible with the chlorine at the temperatures and pressures (1500F and 150 psig) to which it was exposed. Alternative materials are being evaluated and the inspectors will follow the licensee's corrective action on this item.

10.3 About 2 P.M. on June 7,1983, an individual was injured during a tour of the drywell when a heavy bag (approximately 25 pounds) of used insulation fell on him. He was removed from the drywell and transferred to a local area hospital for treatment. He was transferred as potentially contaminated due to the nature of his injury. Later licensee surveys determined that no contamination was present.

Licensee declared an unusual event and made appropriate notifications. The inspector reviewed licensee actions and identified no unacceptable conditions.

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Review of IE Bulletin 79-09 Bulletin 79-09, Failures of GE Type AK-2 Circuit Breakers, was issued in April 1979 to warn of failures of the subject breakers to trip due to binding of the linkage of the undervoltage trip device and trip shaft assembly. The licensee responded to the bulletin on May 17, 1979, stating that the requirements of the bulletin and the referenced GE Service Advise Letter (SAL) 175 (CPDD) 9.3 had been implemented. The actions were reviewed and documented in NRC Inspection 50-219/79-14. Type AK-2 breakers are used at Oyster Creek in the 480 volt power supplies to Core Spray Booster pumps, Containment Spray pumps, Service Water pumps, and Control Rod Drive pumps.

During preparations for preventive maintenance on these breakers during the current refueling outage,

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The bulletin referred to the GE SAL which required that the torque required on the trip shaft to trip a closed breaker be checked and should not exceed 1.5 pounds - inches. This requirement had not been incorporated into procedure 761.2.003, "480 Volt Breaker Preventive Maintenance". Following the licensee's identification of this deficiency, he notified the resident inspector, added the requirement to the preventive maintenance check lists, and initiated action to change the maintenance procedure. The torque checks were perfomed on the trip shafts of the breakers in question and no abnormal operation was noted.

The inspectors had no further questions on this item.

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Review of Periodic Reports Upon receipt, periodic and special reports submitted by the licensee pursuant to Technical Specification 6.9.1 were reviewed by the inspector.

This review included the following considerations: the report includes the infomation required to be reported to the NRC; planned corrective actions are adequate for resolution of identified problems; and that the reported infomation is valid. Within the scope of the above, the following periodic reports were reviewed by the inspector.

April 1983 Monthly Operating Report

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No unacceptable conditions were identified.

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Exit Interview

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At periodic intervals during the course of this inspection, meetings were held with senior facility management to discuss inspection scope and findings.

A sumary of findings was presented at the conclusion of the inspection.

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