ENS 51696
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ENS Event | |
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18:22 Jan 29, 2016 | |
Title | Automatic Reactor Trip Due to Reactor Protection System Actuation |
Event Description | At 1322 EST, with the unit operating at approximately 100% full power, an automatic reactor trip occurred due to actuation of Reactor Protection System (RPS) Channel 4. The cause of the RPS actuation is being investigated at this time. Nuclear Instrumentation calibration for RPS Channel 2 was in progress at the time of the trip, with Channel 2 in bypass and Channel 1 in trip. All control rods fully inserted. Immediately post trip, the Steam Feedwater Rupture Control System actuated due to high Steam Generator 1 level due to unknown causes. The Main Steam Isolation Valves closed and Auxiliary Feedwater started as expected. Secondary side relief valves lifted in response to the trip, with two of the relief valves (one on each header) not properly reseating until operators manually lowered Main Steam Header pressure. The Bayshore 345 kV Offsite Electrical Distribution Circuit automatically isolated at the time of the unit trip. This was unexpected. The remaining offsite circuits remain in service.
The unit is currently in Mode 3 (Hot Standby) and stable, at approximately 550 degrees F and 2155 psig. Steam is being discharged through the Atmospheric Vent Valves for decay heat removal. There is no known primary to secondary leakage, and all safety systems functioned as expected. Both primary Source Range nuclear instruments automatically energized, however, they were previously declared inoperable due to an administrative issue. Both Source Range instruments are functional and indicating properly. Both alternate Source Range instruments are operable, and all required Technical Specification actions have been completed. The NRC Resident Inspector has been notified of the event. |
Where | |
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Davis Besse Ohio (NRC Region 3) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
LER: | 05000346/LER-2016-001 |
Time - Person (Reporting Time:+-1.65 h-0.0688 days <br />-0.00982 weeks <br />-0.00226 months <br />) | |
Opened: | Thomas Philips 16:43 Jan 29, 2016 |
NRC Officer: | Dong Park |
Last Updated: | Jan 29, 2016 |
51696 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | A/R |
Before | Power Operation (100 %) |
After | Hot Standby (0 %) |
Davis Besse with 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation | |
WEEKMONTHYEARENS 553462021-07-09T01:54:0009 July 2021 01:54:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Main Turbine Trip ENS 546112020-03-25T16:40:00025 March 2020 16:40:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Loss of Reactor Coolant Pumps ENS 542632019-09-07T17:09:0007 September 2019 17:09:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 522322016-09-10T07:43:00010 September 2016 07:43:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Unit Trip Due to Main Generator Lock-Out ENS 517022016-01-30T06:23:00030 January 2016 06:23:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unanticipated Sfrcs Actuation While Restoring Main Feedwater to Steam Generators ENS 516962016-01-29T18:22:00029 January 2016 18:22:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Reactor Protection System Actuation ENS 510612015-05-09T22:55:0009 May 2015 22:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Steam Leak in the Turbine Building ENS 500862014-05-05T18:56:0005 May 2014 18:56:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Scram with Rod Motion While Shutdown ENS 500972014-05-04T12:32:0004 May 2014 12:32:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Initiation of the Reactor Protection System While Shutdown ENS 491592013-06-30T01:20:00030 June 2013 01:20:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Reactor Coolant Pump Trip ENS 428282006-09-06T06:31:0006 September 2006 06:31:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip on Loss of Condenser Vacuum ENS 413302005-01-13T14:49:00013 January 2005 14:49:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Entry Into Technical Specification Required Shut Down Due to Loss of Essential Bus ENS 409212004-08-04T14:24:0004 August 2004 14:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unexpected Reactor Trip During Maintenance Activities ENS 402082003-10-01T01:34:0001 October 2003 01:34:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Valid Specified System Actuation ENS 401612003-09-16T04:30:00016 September 2003 04:30:00 10 CFR 50.72(b)(3)(iv)(A), System Actuation Reactor Coolant System Pressure Increase Caused a Valid Signal 2021-07-09T01:54:00 | |
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