ENS 47585
ENS Event | |
|---|---|
03:15 Jan 12, 2012 | |
| Title | High Pressure Coolant Injection System Declared Inoperable |
| Event Description | On January 11, 2012 at 22:15 [EST], the High Pressure Coolant Injection System (HPCI) was declared inoperable due to a failure of the turbine governor valve to respond to demanded position. When demanded to travel to the full closed position, the governor valve remained full open rendering the speed and flow control system for the turbine inoperable. The failure was discovered as part of a planned maintenance evolution.
All other Emergency Core Cooling Systems and the Reactor Core Isolation Cooling (RCIC) system remain operable. The unit remains at 100% power. The station has initiated an Event Response Team to identify and correct the cause of the failure. No personnel injuries resulted from the event. The NRC Resident Inspector [has been notified] and Lower Alloway Creek Township will be notified. The unit is in a 14-day LCO for HPCI inoperability.
The following is a retraction of ENS Notification #47585: On January 11, 2012, Hope Creek Generating Station reported to the NRC that High Pressure Coolant Injection System (HPCI) was declared inoperable due to a failure of the turbine governor valve to respond to demanded position. This condition was discovered when obtaining an oil sample from the HPCI system. According to the procedure, the HPCI flow controller automatic setpoint was lowered to zero. The procedure set the manual controller setpoint by having the operator lower the demand for a time period rather than verifying the setpoint at zero. The HPCI Auxiliary Oil Pump is then started. The governor valve was expected to start to open (intermediate position) and then close. Instead the valve went to the full open position and did not respond to attempts to close the valve from the flow controller. Accordingly, Control Room personnel conservatively initiated ENS reporting under 10CFR50.72(b)(3)(v) in response to the apparent loss of safety function for Unit 1. Subsequent technical evaluation concluded that the performance and response of the HPCI turbine governor control valve was as expected based on the manual controller demand being at 35% when the HPCI Auxiliary Oil Pump was started to collect a HPCI oil sample. The Engineering review concluded that there are no problems with the HPCI turbine governor control valve response to controller demand. Operating procedures have been revised to provide guidance on verifying manual controller demand at 0% before placing the HPCI Auxiliary Oil Pump in service under standby conditions for oil sampling or similar evolutions. Since January 11th, 2012, HPCI has remained available to perform its required safety functions and only became inoperable during planned evolutions to either obtain oil samples or to investigate HPCI turbine governor control valve performance. On this basis, the HPCI system was capable of performing its function to mitigate the consequences of an accident and the issue described in Event #47585 is not reportable under 10 CFR 50.72(b)(3)(v). The NRC Resident Inspector and Lower Alloway Creek Township will be notified of this retraction. Notified R1DO (Trapp). |
| Where | |
|---|---|
| Hope Creek New Jersey (NRC Region 1) | |
| Reporting | |
| 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
| Time - Person (Reporting Time:+1.2 h0.05 days <br />0.00714 weeks <br />0.00164 months <br />) | |
| Opened: | Kenneth Breslin 04:27 Jan 12, 2012 |
| NRC Officer: | Mark Abramovitz |
| Last Updated: | Jan 13, 2012 |
| 47585 - NRC Website
Loading map... | |
Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | No |
| Before | Power Operation (100 %) |
| After | Power Operation (100 %) |
Hope Creek | |
WEEKMONTHYEARENS 564942023-04-30T05:00:00030 April 2023 05:00:00
[Table view]10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Primary Containment Integrity Degraded ENS 536252018-09-26T04:00:00026 September 2018 04:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Core Injection (Hpci) System Inoperable ENS 521592016-08-07T05:01:0007 August 2016 05:01:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 499092014-03-13T10:31:00013 March 2014 10:31:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Standby Liquid Control System Sample Concentration Outside Technical Specification Limits ENS 496712013-12-20T18:03:00020 December 2013 18:03:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Both Control Room Air Conditioning Subsystems Inoperable ENS 488972013-04-08T15:15:0008 April 2013 15:15:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Hpci Declared Inoperable During Surveillance Testing ENS 482742012-09-04T04:00:0004 September 2012 04:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection Declared Inoperable ENS 477452012-03-15T00:34:00015 March 2012 00:34:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Hpci Inoperable Due to Failure of Turbine Governor Valve ENS 475852012-01-12T03:15:00012 January 2012 03:15:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 445412008-10-05T08:31:0005 October 2008 08:31:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection (Hpci) System Inoperable ENS 442632008-06-04T06:57:0004 June 2008 06:57:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 441542008-04-22T12:41:00022 April 2008 12:41:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Loss of Safety Function Due to Blown Fuse ENS 439202008-01-19T16:52:00019 January 2008 16:52:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 'A' and 'B' Recirculation Pump Motor Generator Overspeed Stops Found Set High (Non-Conservative) During Surveillance Testing ENS 437792007-11-11T21:39:00011 November 2007 21:39:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Hpci Inoperable Due to Valve Failure During Quarterly Surveillance ENS 435372007-07-31T04:51:00031 July 2007 04:51:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 424222006-03-14T21:59:00014 March 2006 21:59:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Loss of Control Room Emergency Filtration ENS 419952005-09-15T01:38:00015 September 2005 01:38:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Failed Surveillance Testing ENS 418522005-07-19T07:45:00019 July 2005 07:45:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Inoperable ENS 408762004-07-16T14:00:00016 July 2004 14:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown/Loss of Single Safety Function ENS 406482004-04-06T00:30:0006 April 2004 00:30:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Offsite Electrical Power Sources and 1E 4Kv Distribution Buses Inoperable ENS 405392004-02-23T06:52:00023 February 2004 06:52:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Started Due to Grass Intrusion ENS 402252003-10-05T07:00:0005 October 2003 07:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Inoperable Trains of Control Room Emergency Filtration at Hope Creek ENS 401072003-08-27T13:24:00027 August 2003 13:24:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Control Room Access Door Latch Was Determiend to Be Not Fully Engaging. 2023-04-30T05:00:00 | |