ENS 40876
ENS Event | |
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14:00 Jul 16, 2004 | |
Title | Technical Specification Shutdown/Loss of Single Safety Function |
Event Description | A Unit shutdown was initiated at 1100 [ET 07/16/04] to comply with Technical Specifications. The High Pressure Coolant Injection (HPCI) System was declared inoperable at 1000 on 7/16/04 due to an inability to demonstrate that it is capable of meeting its design flow and pressure requirements identified during an extent of condition review being conducted in conjunction with an ongoing Safety System Design Inspection. Concurrently, the `D' Emergency Diesel Generator (EDG) was inoperable due to an in-progress surveillance. This rendered the `D' Low Pressure Coolant Injection (LPCI) subsystem and `B' Core Spray subsystem inoperable resulting in entry into Technical Specification 3.0.3 requiring within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> initiating action to place the unit in at least startup within the next 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />, hot shutdown within the following 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br /> and cold shutdown within the subsequent 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
Power ascension was in progress with reactor power at 95%. Power ascension was suspended. Preparations for power reduction were initiated. Actions were taken to restore the `D' EDG to an operable, standby alignment, which was complete at 1145 rendering `D' LPCI subsystem and `B' Core Spray subsystem operable. Technical Specification 3.0.3 was exited. No power reduction was conducted. The HPCI system remains inoperable constituting a condition that could have prevented the fulfillment of a safety function. The investigation is ongoing including a determination of the need for any physical modifications that may be required. Prior to the event, the `C' Station Service Water pump, `D' Filtration Recirculation, Ventilation System recirculation fan, and `B' Primary Containment Instrument gas compressor were out of service for scheduled maintenance. There were no personnel injuries as a result of this event. The NRC Resident inspector was notified of this event. |
Where | |
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Hope Creek New Jersey (NRC Region 1) | |
Reporting | |
10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident | |
Time - Person (Reporting Time:+0.17 h0.00708 days <br />0.00101 weeks <br />2.32866e-4 months <br />) | |
Opened: | Rita Braddick 14:10 Jul 16, 2004 |
NRC Officer: | Mike Ripley |
Last Updated: | Jul 16, 2004 |
40876 - NRC Website
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Unit 1 | |
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Reactor critical | Critical |
Scram | No |
Before | Power Operation (95 %) |
After | Power Operation (95 %) |
Hope Creek with 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown | |
WEEKMONTHYEARENS 564952023-04-30T06:00:00030 April 2023 06:00:00
[Table view]10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown ENS 564942023-04-30T05:00:00030 April 2023 05:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(3)(ii)(A), Seriously Degraded Primary Containment Integrity Degraded ENS 536252018-09-26T04:00:00026 September 2018 04:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Core Injection (Hpci) System Inoperable ENS 521592016-08-07T05:01:0007 August 2016 05:01:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 499092014-03-13T10:31:00013 March 2014 10:31:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Standby Liquid Control System Sample Concentration Outside Technical Specification Limits ENS 496712013-12-20T18:03:00020 December 2013 18:03:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Both Control Room Air Conditioning Subsystems Inoperable ENS 488972013-04-08T15:15:0008 April 2013 15:15:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Hpci Declared Inoperable During Surveillance Testing ENS 482742012-09-04T04:00:0004 September 2012 04:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection Declared Inoperable ENS 477452012-03-15T00:34:00015 March 2012 00:34:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Hpci Inoperable Due to Failure of Turbine Governor Valve ENS 475852012-01-12T03:15:00012 January 2012 03:15:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 445412008-10-05T08:31:0005 October 2008 08:31:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection (Hpci) System Inoperable ENS 442632008-06-04T06:57:0004 June 2008 06:57:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 442402008-05-25T13:30:00025 May 2008 13:30:00 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Inverter Fuse Failure ENS 441542008-04-22T12:41:00022 April 2008 12:41:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Loss of Safety Function Due to Blown Fuse ENS 439202008-01-19T16:52:00019 January 2008 16:52:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident 'A' and 'B' Recirculation Pump Motor Generator Overspeed Stops Found Set High (Non-Conservative) During Surveillance Testing ENS 437792007-11-11T21:39:00011 November 2007 21:39:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Hpci Inoperable Due to Valve Failure During Quarterly Surveillance ENS 435372007-07-31T04:51:00031 July 2007 04:51:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Declared Inoperable ENS 424222006-03-14T21:59:00014 March 2006 21:59:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Loss of Control Room Emergency Filtration ENS 419952005-09-15T01:38:00015 September 2005 01:38:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Failed Surveillance Testing ENS 419562005-08-28T15:00:00028 August 2005 15:00:00 10 CFR 50.72(b)(3)(v)(A), Loss of Safety Function - Shutdown the Reactor, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Due to Inoperable Suppression Chamber Vacuum Breaker ENS 418522005-07-19T07:45:00019 July 2005 07:45:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident High Pressure Coolant Injection System Inoperable ENS 408762004-07-16T14:00:00016 July 2004 14:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Shutdown/Loss of Single Safety Function ENS 406482004-04-06T00:30:0006 April 2004 00:30:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Offsite Electrical Power Sources and 1E 4Kv Distribution Buses Inoperable ENS 405392004-02-23T06:52:00023 February 2004 06:52:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Technical Specification Required Shutdown Started Due to Grass Intrusion ENS 402252003-10-05T07:00:0005 October 2003 07:00:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Inoperable Trains of Control Room Emergency Filtration at Hope Creek ENS 401072003-08-27T13:24:00027 August 2003 13:24:00 10 CFR 50.72(b)(3)(v)(D), Loss of Safety Function - Mitigate the Consequences of an Accident Control Room Access Door Latch Was Determiend to Be Not Fully Engaging. 2023-04-30T06:00:00 | |