ENS 44837
ENS Event | |
|---|---|
16:59 Feb 7, 2009 | |
| Title | Unusual Event Declared Due to a Fire Onsite |
| Event Description | Arkansas Nuclear One Unit 1 declared an Unusual Event per EAL 7.5 at 1059 CST based on a fire onsite. The fire occurred on the 354 foot elevation iso-phase bus deck of the turbine building. The fire was attributed to a failed bonnet on a manual valve which had unthreaded during operation releasing hydrogen in the vicinity of the hydrogen add station. The licensee extinguished the fire using water and posted a reflash watch. There were no reported personnel injuries. Offsite assistance was requested from the London Fire Department which arrived onsite after the fire had been extinguished.
The reactor was manually tripped with all control rods fully inserting. The plant is currently stable with decay heat removal via the steam dumps to the main condenser. The licensee informed state/local agencies and the NRC Resident Inspector.
The Unusual Event was terminated at 1338 CST after confirmation that the fire was extinguished and a review of the exit criteria as defined in plant procedures. The licensee is performing a damage assessment at this time. The licensee was in the process of informing state/local agencies and will inform the NRC Resident Inspector. Notified R4DO (Clark), NRR(Hiland), IRD (Grant), DHS (Banner) and FEMA (Canupp).
The subject event notification erroneously reported that all control rods fully inserted following the manual reactor trip initiated in response to a fire on site. In actuality, the rod bottom light for Rod 6 in Rod Group 7 on the CRD Position Indication Panel did not illuminate following the reactor trip and it was verified by plant computer to have inserted to 2.3 percent withdrawn. The control board operator identified this condition quickly and reported it to the Control Room Supervisor in his immediate action response. This condition did not necessitate any additional operator actions and shutdown margin requirements were maintained. The licensee has informed the NRC Resident Inspector. R4DO (Miller) notified. |
| Where | |
|---|---|
| Arkansas Nuclear Arkansas (NRC Region 4) | |
| Reporting | |
| Emergency class: | Unusual Event |
| 10 CFR 50.72(a) (1) (i), Emergency Class Declaration 10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
| Time - Person (Reporting Time:+-4.68 h-0.195 days <br />-0.0279 weeks <br />-0.00641 months <br />) | |
| Opened: | Peter Jackson 12:18 Feb 7, 2009 |
| NRC Officer: | Vince Klco |
| Last Updated: | Feb 10, 2009 |
| 44837 - NRC Website
Loading map... {"minzoom":false,"maxzoom":false,"mappingservice":"leaflet","width":"350px","height":"250px","centre":false,"title":"","label":"","icon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"copycoords":false,"static":false,"zoom":6,"defzoom":14,"layers":["OpenStreetMap"],"image layers":[],"overlays":[],"resizable":false,"fullscreen":false,"scrollwheelzoom":true,"cluster":false,"clustermaxzoom":20,"clusterzoomonclick":true,"clustermaxradius":80,"clusterspiderfy":true,"geojson":"","clicktarget":"","imageLayers":[],"locations":[{"text":"\u003Cb\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003E\u003Ca class=\"mw-selflink selflink\"\u003EENS 44837\u003C/a\u003E - \u003Ca href=\"/Arkansas_Nuclear\" title=\"Arkansas Nuclear\"\u003EArkansas Nuclear\u003C/a\u003E\n\u003C/p\u003E\u003C/div\u003E\u003C/b\u003E\u003Cdiv class=\"mw-parser-output\"\u003E\u003Cp\u003EUnusual Event Declared Due to a Fire Onsite\n\u003C/p\u003E\u003C/div\u003E","title":"ENS 44837 - Arkansas Nuclear\n","link":"","lat":35.31055555555555,"lon":-93.23084444444444,"icon":"/w/images/7/79/Entergy_icon.png"}],"imageoverlays":null} | |
Unit 1 | |
|---|---|
| Reactor critical | Critical |
| Scram | Yes, Manual Scram |
| Before | Power Operation (90 %) |
| After | Hot Standby (0 %) |
Arkansas Nuclear | |
WEEKMONTHYEARENS 579492025-09-24T18:47:00024 September 2025 18:47:00
[Table view]10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip ENS 563512023-02-14T17:03:00014 February 2023 17:03:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Trip Due to Two Reactor Coolant Pumps Tripping ENS 556142021-11-29T20:58:00029 November 2021 20:58:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 551382021-03-14T19:15:00014 March 2021 19:15:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Trip Due to Loss Bus Voltage ENS 550282020-12-10T22:08:00010 December 2020 22:08:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Automatic Reactor Scram Due to Low Steam Generator Water Level ENS 540912019-05-26T10:12:00026 May 2019 10:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to a Reactor Coolant Pump Trip on Ground Fault ENS 537932018-12-18T06:00:00018 December 2018 06:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip - Loss of Non-Vital Bus ENS 534592018-06-16T05:00:00016 June 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Startup ENS 534042018-05-16T22:50:00016 May 2018 22:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Main Feedwater Pump ENS 527102017-04-26T15:04:00026 April 2017 15:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Automatic Reactor Scram Due to Partial Loss of Offsite Power ENS 516072015-12-15T11:44:00015 December 2015 11:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Feed to One Steam Generator ENS 500632014-04-28T01:12:00028 April 2014 01:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to an Auxiliary Trip on Core Protection Calculator ENS 499952014-04-03T18:01:0003 April 2014 18:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 496182013-12-09T14:00:0009 December 2013 14:00:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Unit 2 Auxiliary Transformer Explosion ENS 488692013-03-31T15:33:00031 March 2013 15:33:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Notification of Unusual Event Declared Due to a Breaker Explosion in the Protected Area ENS 481692012-08-08T13:23:0008 August 2012 13:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to High Reactor Coolant System Pressurizer Pressure ENS 465552011-01-20T02:58:00020 January 2011 02:58:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Notice of Unusual Event Due to a Security Event ENS 458722010-04-26T05:00:00026 April 2010 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Experienced an Automatic Reactor Trip During an Ni Calibration ENS 458542010-04-18T18:57:00018 April 2010 18:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip During Reactor Startup ENS 455492009-12-08T14:42:0008 December 2009 14:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Low Steam Generator Level Caused by Loss of Main Feed Water Pump ENS 449062009-03-14T02:51:00014 March 2009 02:51:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Feedwater Regulating Valve Failure Leads to Manual Reactor Trip ENS 448372009-02-07T16:59:0007 February 2009 16:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to a Fire Onsite ENS 448312009-02-05T21:24:0005 February 2009 21:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Manually Tripped Due to Control Rod Drive Motor High Temperatures ENS 447362008-12-20T18:12:00020 December 2008 18:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip When Control Rod Bank Inserted Without Operator Action ENS 447162008-12-12T14:55:00012 December 2008 14:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Was Manually Tripped from 32% Power Due to an Abnormal Rod Pattern ENS 437422007-10-24T04:05:00024 October 2007 04:05:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Alert Declared Due to Electrical Fire in the Auxiliary Building ENS 429492006-10-30T19:04:00030 October 2006 19:04:00 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(2)(i), Tech Spec Required Shutdown Alert Declaration Due to Electrical Fire Affecting One Esf Train ENS 422292005-12-26T16:47:00026 December 2005 16:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Turbine Trip ENS 401192003-08-29T19:28:00029 August 2003 19:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on High Rcs Pressure 2025-09-24T18:47:00 | |