ENS 44831
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ENS Event | |
---|---|
21:24 Feb 5, 2009 | |
Title | Unit 1 Manually Tripped Due to Control Rod Drive Motor High Temperatures |
Event Description | Arkansas Nuclear One Unit 1 was manually tripped from 61% power due to Control Rod Drive motor (CRD) high temperatures due to a loss of cooling water flow from Non-Nuclear Intermediate Cooling Water (ICW). No significant equipment issues were observed. No primary safeties lifted. Secondary safeties lifted for ~18 seconds. Emergency feedwater did not actuate and was not needed. Post trip response was normal and the plant is stable in mode 3. Post transient review is in progress.
All control rods fully inserted into the core. There is no known primary-secondary steam generator tube leakage. The offsite electrical grid is stable. The loss of ICW flow is attributed to the mechanical failure of service air compressor C-3A. Decay heat removal is via main feedwater to the steam generator and steam to the main condenser. The licensee informed state, other government agencies and the NRC Resident Inspector and will inform local government agencies. No press release is planned. |
Where | |
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Arkansas Nuclear Arkansas (NRC Region 4) | |
Reporting | |
10 CFR 50.72(b)(2)(iv)(B), RPS Actuation | |
Time - Person (Reporting Time:+-2.07 h-0.0863 days <br />-0.0123 weeks <br />-0.00284 months <br />) | |
Opened: | Bob Fowler 19:20 Feb 5, 2009 |
NRC Officer: | Steve Sandin |
Last Updated: | Feb 5, 2009 |
44831 - NRC Website
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Unit 1 | |
---|---|
Reactor critical | Critical |
Scram | Yes, Manual Scram |
Before | Power Operation (61 %) |
After | Hot Standby (0 %) |
WEEKMONTHYEARENS 563512023-02-14T17:03:00014 February 2023 17:03:00
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Non-Vital Bus ENS 534592018-06-16T05:00:00016 June 2018 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip During Startup ENS 534042018-05-16T22:50:00016 May 2018 22:50:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to Loss of Main Feedwater Pump ENS 527102017-04-26T15:04:00026 April 2017 15:04:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unit 1 Automatic Reactor Scram Due to Partial Loss of Offsite Power ENS 516072015-12-15T11:44:00015 December 2015 11:44:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Loss of Feed to One Steam Generator ENS 500632014-04-28T01:12:00028 April 2014 01:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to an Auxiliary Trip on Core Protection Calculator ENS 499952014-04-03T18:01:0003 April 2014 18:01:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip ENS 496182013-12-09T14:00:0009 December 2013 14:00:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Unusual Event Declared Due to Unit 2 Auxiliary Transformer Explosion ENS 488692013-03-31T15:33:00031 March 2013 15:33:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Notification of Unusual Event Declared Due to a Breaker Explosion in the Protected Area ENS 481692012-08-08T13:23:0008 August 2012 13:23:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Due to High Reactor Coolant System Pressurizer Pressure ENS 458722010-04-26T05:00:00026 April 2010 05:00:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Experienced an Automatic Reactor Trip During an Ni Calibration ENS 458542010-04-18T18:57:00018 April 2010 18:57:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip During Reactor Startup ENS 455492009-12-08T14:42:0008 December 2009 14:42:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Manual Reactor Trip Due to Low Steam Generator Level Caused by Loss of Main Feed Water Pump ENS 449062009-03-14T02:51:00014 March 2009 02:51:00 10 CFR 50.72(b)(2)(xi), Notification to Government Agency or News Release, 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Feedwater Regulating Valve Failure Leads to Manual Reactor Trip ENS 448372009-02-07T16:59:0007 February 2009 16:59:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(a)(1)(i), Emergency Class Declaration Unusual Event Declared Due to a Fire Onsite ENS 448312009-02-05T21:24:0005 February 2009 21:24:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Manually Tripped Due to Control Rod Drive Motor High Temperatures ENS 447362008-12-20T18:12:00020 December 2008 18:12:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Manual Reactor Trip When Control Rod Bank Inserted Without Operator Action ENS 447162008-12-12T14:55:00012 December 2008 14:55:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation Unit 1 Was Manually Tripped from 32% Power Due to an Abnormal Rod Pattern ENS 422292005-12-26T16:47:00026 December 2005 16:47:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip Following Turbine Trip ENS 401192003-08-29T19:28:00029 August 2003 19:28:00 10 CFR 50.72(b)(2)(iv)(B), RPS System Actuation, 10 CFR 50.72(b)(3)(iv)(A), System Actuation Automatic Reactor Trip on High Rcs Pressure 2023-02-14T17:03:00 | |
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